IR 05000456/2020003

From kanterella
Jump to navigation Jump to search
Integrated Inspection Report 05000456/2020003 and 05000457/2020003
ML20315A490
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 11/10/2020
From: Hironori Peterson
NRC/RGN-III
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2020003
Download: ML20315A490 (21)


Text

November 10, 2020

SUBJECT:

BRAIDWOOD GENERATING STATION - INTEGRATED INSPECTION REPORT 05000456/2020003 AND 05000457/2020003

Dear Mr. Hanson:

On September 30, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Generating Station. On October 6, 2020, the NRC inspectors discussed the results of this inspection with Mr. J. Keenan, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No NRC-identified or self-revealing findings were identified during this inspection.

A licensee-identified violation which was determined to be of very low safety significance is documented in this report. We are treating this violation as a non-cited violation (NCV)

consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Braidwood Generating Station. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Hironori Peterson, Chief Branch 3 Division of Reactor Projects

Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2020003 and 05000457/2020003

Enterprise Identifier: I-2020-003-0021

Licensee:

Exelon Generation Company, LLC

Facility:

Braidwood Generating Station

Location:

Braceville, IL

Inspection Dates:

July 01, 2020 to September 30, 2020

Inspectors:

R. Bowen, Illinois Emergency Management Agency

G. Edwards, Health Physicist

R. Edwards, Senior Health Physicist

D. Kimble, Senior Resident Inspector

P. Smagacz, Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Generating Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71111.1

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 and Unit 2 both began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, both units remained operating at or near full power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time the resident inspectors performed periodic site visits each week and during that time conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities, and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from an impending extreme/extended heat wave during the week ending July 11, 2020.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations and material condition during partial physical alignment verifications of the following systems/trains:

(1) The spent fuel pool cooling (SF) system during the station's summer readiness period, concurrent with a spent fuel dry cask storage (DCS) loading campaign during the week ending July 18, 2020.
(2) The 2B Safety Injection (SI) Train during maintenance on the 2A SI Train during the week ending August 29, 2020.
(3) The 2B Auxiliary Feedwater (AF) Train during Unit 2 System Auxiliary Transformer (SAT) 242 maintenance during the week ending September 19, 2020.

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

The inspectors evaluated system configurations and material condition during a full system physical alignment verification of the following system/train:

(1) The Unit 2 emergency diesel generators (EDGs) during the weeks ending September 5 through September 12, 2020.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting physical inspections/equipment verifications and performing reviews to verify program compliance, equipment functionality, material condition, and operational readiness for the following fire areas/zones:

(1) Fire Zone 5.6-2; The Unit 2 Division 21 Miscellaneous Electric Equipment Room (MEER) and battery room during the week ending September 19, 2020.
(2) Fire Zone 5.4-2; The Unit 2 Division 22 MEER and battery room during the week ending September 19, 2020.
(3) Fire Zone 18.2-2; The 2A EDG Room and ventilation shaft during the week ending September 19, 2020.
(4) Fire Zone 18.1-1; The 2B EDG Room and ventilation shaft during the week ending September 19, 2020.
(5) Fire Zone 18.10E-1; The Unit 1 SATs 141-1 and 142-2 during the week ending September 19, 2020.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors evaluated internal flooding mitigation protections and features for the following area:

(1) The Unit 2 turbine building basement, Elevation 369', for a postulated/hypothetical main circulating water system failure during the weeks ending September 19 through September 26, 2020.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the main control room (MCR) during various activities involving on-watch operations crews during the weeks ending August 15 through September 30, 2020. These activities included, but were not limited to:
  • Response of the MCR Unit 2 crew to a trip of the 2B Containment Ventilation (VP) Chiller and subsequent failure of the standby 2A VP Chiller to start during the week ending August 22, 2020.
  • Response of the MCR crew to the failure of the 0A MCR Ventilation (VC)

Makeup Fan during the week ending September 5, 2020.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors conducted an observation of the performance of a complex casualty graded scenario by a crew of licensed plant operators in the facility's simulator on July 28, 2020.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remained capable of performing their intended function:

(1) Maintenance effectiveness and performance history review of 0A and 0B VC Chiller units during the weeks ending August 1 through September 30, 2020.
(2) Maintenance effectiveness and performance history review of the circulating water blowdown line and permitted radiological liquid effluent discharge path during the weeks ending August 1 through September 5, 2020.

Quality Control (IP Section 03.02) (1 Sample)

The inspectors evaluated the effectiveness of maintenance and quality control activities undertaken by the licensee to ensure the following SSC remained capable of performing its intended function:

(1) Maintenance effectiveness and performance history review for the 2A EDG, specifically the EDG's Direct Current (DC) Control Circuit No.1, during the weeks ending August 22 through September 30, 2020.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Assessment of risk associated with summer 2020 DCS spent fuel loading campaign, specifically cask 3 of 6 (HI-STORM 912; MPC 32-409) in accordance with Work Order (WO) 4719945 during the weeks ending August 22 through August 29, 2020.
(2) Assessment of risk associated with changes to the Unit 1 & 2 Westinghouse OvationTM digital control systems in accordance with WO 5054243 during the weeks ending August 15 through September 5, 2020.
(3) Emergent work on the Unit 0 Station Air Compressor (SAC) to replace motor bearings in accordance with WO 5067011 during the weeks ending August 8 through September 5, 2020.
(4) Assessment of risk associated with a planned SAT 242 maintenance window utilizing a Technical Specification (TS) Risk Informed Completion Time (RICT) in accordance with WO 4724683 during the week ending September 19, 2020.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (3 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Assessment of the operability of the 0B VC Chiller after a step change in condenser pressure and identification of air in-leakage as documented in Issue Report (IR)

===4353544 during the weeks ending July 4 through July 11, 2020.

(2) Assessment of the impact on the Unit 1 containment isolation function following identification of debris found in 1VQ025 as documented in IR 4365308 during the week ending August 29, 2020.
(3) Assessment of the operability of the 2B EDG following the unexpected receipt of annunciator alarm 2-22-C8 for 2B EDG control power failure as documented in IR 4370636 during the weeks ending September 26 through September 30, 2020.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01)===

The inspectors evaluated the following post maintenance testing activities to verify SSC operability and/or functionality, as applicable:

(1) Return to service testing of the 0B Diesel Fire Pump after a jacket water leak repair in accordance with WO 5014782 during the week ending July 25, 2020.
(2) Return to service testing of the 2A Containment Spray (CS) Pump following preventative maintenance in accordance with WO 4895576 during the weeks ending August 8 through August 15, 2020.
(3) Testing of the Unit 2 Rod Drive Westinghouse OvationTM Logic after maintenance in accordance with WO 5054243 during the week ending August 15, 2020.
(4) Testing of the Unit 1 Rod Drive Westinghouse Ovation' Logic after maintenance in accordance with WO 5054182 during the week ending August 22, 2020.
(5) Functional and operational testing of the Unit 0 (Common) SAC following an extensive maintenance work window in accordance with WO 4737430 during the weeks ending August 8 through September 5, 2020.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities:

Surveillance Tests (other) (IP Section 03.01)

(1) Observation of 2BwOSR 3.8.1.2-2: The 2B EDG operability surveillance during the week ending July 25, 2020.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated the following emergency preparedness drill/training evolution:

(1) Review of the implementation of the site's emergency plan by a crew of licensed operators during an evaluated emergency scenario in the facility's simulator on July 28,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walkdowns and Observations (IP Section 03.01) (3 Samples)

The inspectors evaluated the following radioactive effluent systems during walkdowns:

(1) Unit 1, 1PR28J, Auxiliary Building ventilation system discharge to main plant vent stack.
(2) Unit 2, 2PR28J, Auxiliary Building ventilation system discharge to main plant vent stack.
(3) Unit 1, 1PR029, Auxiliary Building ventilation system radiation monitor.

Sampling and Analysis (IP Section 03.02) (3 Samples)

(1) Inspectors evaluated compensatory samples.
(2) Inspectors evaluated the sampling and sample analysis of the Unit 1 Auxiliary Building ventilation system discharge.
(3) Inspectors evaluated the sampling and sample analysis of the Circulating Water Blowdown discharge.

Dose Calculations (IP Section 03.03) (2 Samples)

The inspectors evaluated the following dose calculations:

(1) March 2019 liquid and gaseous effluent offsite dose calculations.
(2) April 2019 liquid and gaseous effluent offsite dose calculations.

Abnormal Discharges (IP Section 03.04) (1 Sample)

The inspectors evaluated the following abnormal discharges:

(1) No abnormal discharges occurred during this period.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07)===

(1) Unit 1 (July 1, 2019 through June 30, 2020)
(2) Unit 2 (July 1, 2019 through June 30, 2020)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (July 1, 2019 through June 30, 2020)
(2) Unit 2 (July 1, 2019 through June 30, 2020)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (July 1, 2019 through June 30, 2020)
(2) Unit 2 (July 1, 2019 through June 30, 2020)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Partial)

The inspectors reviewed the licensees implementation of the station corrective action program (CAP) related to the following issues:

(1)

(Partial)

In-depth review of various human performance issues, as well as the licensee's corrective actions, associated with the summer 2020 DCS loading campaign as documented in IR 4364058 during the weeks ending September 12 through September 30, 2020.

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Follow-up (IP Section 03.01)

The inspectors assessed licensee performance related to the following events:

(1) Review and tracking of licensee actions during the COVID-19 National Emergency declaration, as set forth by the President of the United States during the weeks ending July 4 through September 30,

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71111.12 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation: Appendix B to 10 CFR Part 50, Criterion V, Instructions, Procedures, and Drawings, requires that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accomplished.

Contrary to this requirement, the licensees maintenance work instructions for the 0B Main Control Room Ventilation System (VC) Chiller, Work Order (WO) 5004208-24, 0WO01BC Dehydrator Inspection, which was designated by the licensee as a work order affecting quality, failed to contain instructions that were appropriate to the circumstances from the start of work on February 13, 2020, until work was stopped on February 21, 2020, upon completion of the task. Specifically, WO 5004208-24 failed to include details for the orientation dehydrator float valve assembly for the 0B VC Chiller condenser to ensure that the component was installed correctly.

Significance/Severity: Green. The inspectors assessed the significance of the finding using Inspection Manual Chapter (IMC) 0609, Attachment 4, Initial Characterization of Findings, dated December 20, 2019, and IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, dated December 20, 2019. Using Exhibit 2, Mitigating Systems Screening Questions, the inspectors determined that the finding was of very low safety significance (i.e., Green). Although the finding represented a deficiency affecting the design or qualification of a mitigating system, structure, or component (SSC), the 0B VC Chiller, neither the operability nor the probabilistic risk assessment (PRA) functionality of the SSC were lost due to the licensees ability to maintain condenser pressure within specifications via periodic manual venting.

Corrective Action References: Issue Report (IR) 4321449, 0B VC Chiller - 0WO1CB - Dehydrator Float Valve Assembly; IR 4351281, 0B VC Chiller Condenser Refrigerant Pressure High; and IR 4353544, 0B VC Chiller Condenser Pressure Step Change Noted

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On October 6, 2020, the inspectors presented the integrated inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.
  • On August 3, 2020, the inspectors presented the radiation protection baseline inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

4354661

Received Expected SX Discharge Temperature High Alarm

on Unit 2

07/04/2020

4354754

Received Expected SX Discharge Temperature High Alarm

on Unit 1

07/05/2020

4354805

0A VS Chiller Tripped on Low Refrigerant Evaporator

Temperature

07/06/2020

4354825

2C Condensate Booster Pump Lube Oil Temp Greater than

20 deg F

07/06/2020

4354978

1A Reactor Coolant Pump Lower Thrust Bearing Step

Change from 128 deg F to 139 deg F

07/06/2020

4355052

Unexpected Alarm; 1-7-D3 Reactor Coolant Pump Seal

Outlet Temp High (1B)

07/07/2020

4355375

Spent Fuel Pool Temperature Above Rounds Limit - Trend

Only

07/08/2020

4355498

1B VP Chiller Evaporator Pressure Reads Low 1PI-WO081

07/08/2020

Engineering

Changes

2041

Engineering Support Material for NOED - Ultimate Heat Sink

Temperature Increase to 103 deg F

07/07/2020

Procedures

0BwOA ENV-1

Adverse Weather Conditions Unit 0

23

0BwOS XHT-A1

Unit Common High Temperature Equipment Protection

Surveillance

EN-BR-402-005

Extreme Heat Implementation Plan

OP-AA-102-102

General Area Checks and Operator Field Rounds

OP-AA-108-107-

1001

Station Response to Grid Capacity Conditions

OP-AA-108-111-

1991

Severe Weather and Natural Disaster Guidelines

OP-BR-102-102-

1001

Augmented Operator Field Rounds

WC-AA-107

Seasonal Readiness

71111.04

Drawings

M-50, Sheet 2

Diagram of Diesel Fuel Oil Unit 1 & 2

AD

M-50, Sheet 3

Diagram of Diesel Fuel Oil Unit 1 & 2

AX

M-50, Sheet 5

Diagram of Diesel Fuel Oil Supply Units 1 & 2

I

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

BwOP AF-E2

Electrical Lineup - Unit 2 Operating

BwOP AF-M2

Operating Mechanical Lineup, Auxiliary Feedwater, Unit 2

BwOP DG-E3

Electrical Lineup - Unit 2 2A Diesel Generator

BwOP DG-E4

Electrical Lineup - Unit 2 2B Diesel Generator

BwOP DG-M3

Operating Mechanical Lineup Unit 2 2A D/G

BwOP DG-M4

Operating Mechanical Lineup Unit 2 2B D/G

BwOP DO-E2

Electrical Lineup - Unit 2 Diesel Lube Oil

BwOP DO-M10

Operating Mechanical Lineup Unit 2 D/G Fuel Oil Storage

BwOP DO-M12

Operating Mechanical Lineup Unit 2 D/G 2A Fuel Oil

BwOP DO-M14

Operating Mechanical Lineup Unit 2 D/G 2B Fuel Oil

BwOP FC-E1

Electrical Lineup - Unit 1

BwOP FC-E2

Electrical Lineup - Unit 2

1E1

BwOP FC-M1

Operating Mechanical Lineup Unit 1

BwOP FC-M2

Operating Mechanical Lineup Unit 2

BwOP SI-E2

Electrical Lineup - Unit 2 Operating

BwOP SI-M2

Operating Mechanical Lineup Unit 2

71111.05

Fire Plans

Pre-Fire Plan No.

194

Fire Zone 18.1-2; Auxiliary Building 401' Elevation, Diesel

Generator 2B & Switchgear Room Air Shaft

Pre-Fire Plan No.

195

Fire Zone 18.1-2; Auxiliary Building 426' Elevation, Diesel

Generator 2B & Switchgear Room Air Shaft

Pre-Fire Plan No.

196

Fire Zone 18.1-2; Auxiliary Building 451' Elevation, Diesel

Generator 2B & Switchgear Room Air Shaft

Pre-Fire Plan No.

200

Fire Zone 18.2-2, Auxiliary Building 401' Elevation, Diesel

Generator 2A & Switchgear Room Air Shaft

Pre-Fire Plan No.

201

Fire Zone 18.2-2, Auxiliary Building 426' Elevation, Diesel

Generator 2A & Switchgear Room Air Shaft

Pre-Fire Plan No.

201

Fire Zone 18.2-2, Auxiliary Building 426' Elevation, Diesel

Generator 2A & Switchgear Room Air Shaft

Pre-Fire Plan No.

2

Fire Zone 18.2-2, Auxiliary Building 451' Elevation, Diesel

Generator 2A & Switchgear Room Air Shaft

Pre-Fire Plan No.

21

Fire Zone 18.10E; Outside 401' Elevation, Unit 1 System

Auxiliary Transformers 141-1 and 142-2

Pre-Fire Plan No.

Fire Zone 5.4-2; Auxiliary Building 451' Elevation, Unit 2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Division 22 Miscellaneous Electric Equipment Room and

Battery Room

Pre-Fire Plan No.

Fire Zone 5.6-2; Auxiliary Building 451' Elevation, Unit 2

Division 21 Miscellaneous Electric Equipment Room and

Battery Room

Procedures

BwAP 1110-1

Fire Protection Program System Requirements

BwAP 1110-3

Plant Barrier Impairment Program

BwOP PBI-1

Plant Barrier Impairment Program Pre-Evaluated Barrier

Matrix

CC-AA-201

Plant Barrier Control Program

ER-AA-600-1069

High Risk Fire Area Identification

ER-BR-600-1069

Braidwood Units 1 and 2 - Site List of High-Risk Fire Areas

OP-AA-201-007

Fire Protection System Impairment Control

OP-AA-201-008

Pre-Fire Plan Manual

OP-AA-201-009

Control of Transient Combustible Material

OP-AA-201-010-

1001

Operations On-Line Fire Risk Management

71111.06

Corrective Action

Documents

4368854

Defects Found on the Circulating Water Expansion Joint

09/11/2020

Drawings

M-81, Sheet 1

Diagram of Turbine Building Equipment Drains

AC

M-81, Sheet 12

Diagram of Turbine Building Equipment Drains Unit 2

H

71111.11Q Corrective Action

Documents

4347746

Crew 4 Failure During OBE [Out of the Box Evaluation]

06/03/2020

4347746

Crew 4 Failure During OBE [Out of the Box Evaluation]

06/03/2020

4356726

Crew 3 Failures During OBE

07/14/2020

Procedures

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-AA-101-113

Operator Fundamentals

OP-AA-101-113-

1006

4.0 Crew Critique Guidelines

OP-AA-103-102

Watch-Standing Practices

OP-AA-103-102-

1001

Strategies for Successful Transient Mitigation

OP-AA-103-103

Operation of Plant Equipment

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-104-101

Communications

OP-AA-108-107-

1002

Interface Procedure Between BGE/COMED/PECO and

Exelon Generation (Nuclear/Power) for Transmission

Operations

OP-AA-111-101

Operating Narrative Logs and Records

OP-AA-300

Reactivity Management

TQ-AA-10

Systematic Approach to Training Process Description

TQ-AA-150

Operator Training Programs

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-201

Examination Security and Administration

TQ-AA-306

Simulator Management

TQ-BR-201-0113

Braidwood Training Department Simulator Examination

Security Actions

71111.12

Corrective Action

Documents

252176

Unexpected Annunciator 2-21-C8, EDG 2A Trouble/Fail to

Start

05/28/2019

297811

Discovery on 0WO01CB

11/16/2019

297945

Intentionally Abbreviated Maintenance on 0WO01CB Purge

Unit Filter

11/17/2019

298002

Foreign Material Found in Refrigerant Filter Housing

11/17/2019

298245

Found Broken Pipe During Pressure Test

11/18/2019

21449

0B VC Chiller - 0WO01CB - Dehydrator Float Valve

Assembly

2/25/2020

4353544

0B VC Chiller Condenser Pressure Step Change Noted

06/29/2020

4353654

Air In-Leakage at Suction Elbow of 0B VC Compressor

06/30/2020

4353656

Air In-Leakage at Guide Vane Shaft Seal of 0B VC

Compressor

06/30/2020

4353657

Air In-Leakage at Oil Recovery Line of 0B VC Chiller

06/30/2020

4361255

SAC Work Window Lessons Learned

08/05/2020

4363448

Unexpected Annunciator 2-21-C8, EDG 2A Trouble/Fail to

Start

08/16/2020

436439

2A EDG 2PL07J-4X3A Terminal Screw is Broken

08/20/2020

708989

0A VC Chiller Purge Unity Refrigerant Level Not in Sight-

glass

2/07/2007

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

717908

Late Planning of WO 1089110-01 0A VC Chiller Purge Unit

01/03/2008

Drawings

20E-2-4030DG31

Schematic Diagram, Diesel Generator 2A Starting Sequence

Control, 2DG01KA Part 1

AM

Engineering

Changes

630844

Evaluation Supporting Inspection for EC 629319 (Circulating

Blowdown Piping Inspection Scope Support)

Miscellaneous

Adverse Condition Monitoring and Contingency Plan;

0WO01CB (0B VC Chiller) Monitoring

07/15/2020

Procedures

ER-AA-310-1002

Maintenance Rule Functions - Safety Significant

Classification

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1001

Maintenance Rule 18-10 - Scoping

ER-AA-320-1003

Maintenance Rule 18-10 - Failure Definitions

ER-AA-320-1004

Maintenance Rule 18-10 - Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

Work Orders

5004208-24

0WO01CB Dehydrator Inspection

2/13/2020

5069949

Unexpected Annunciator 2-21-C8, EDG 2A Trouble/Rail to

Start

08/20/2020

71111.13

Corrective Action

Documents

4361010

0SA01C-M Oil Analysis

08/04/2020

4361255

SAC Work Window Lessons Learned

08/05/2020

4361295

Unit 0 SAC Outboard Motor Bearing Oil is Discolored

08/05/2020

4362665

0SA01C Oil Mist Eliminator

08/12/2020

4376411

Lessons Learned for Unit 2 SAT Use of RICT

10/13/2020

Engineering

Changes

631843

Ovation Software Update to Correct Rod Control (RD) Logic

Sheet Errors Causing Intermittent Urgent Failure Alarms

(Units 1 & 2)

Miscellaneous

Approved RICT Record for SAT 242 Maintenance Window

Completed RICT Record for SAT 242 Maintenance Window

09/25/2020

Procedures

1BwGP 100-8

Generic Reactor Control Guidance

ER-AA-600

Risk Management

ER-AA-600-1042

On-Line Risk Management

ER-AA-600-1052

Risk Management Support of RICT

ER-AA-600-1053

Calculation of RMAT and RICT for Risk Informed Completion

Time Program

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ER-BW-600-2001

Braidwood RICT System Guidelines

MA-AA0716-004

Conduct of Troubleshooting

OP-AA-108-117

Protected Equipment Program

OP-AA-108-118

Risk Informed Completion Time

WC-AA-101-1006

On-Line Risk Management and Assessment

Work Orders

4719945-02

ISFSI Load and Process HI-STORM 912 / MPC 32-409

08/17/2020

5054182

Unit 1 RD Ovation Logic Error Causing UA Alarms

(EC 631843)

08/12/2020

5054243

Unit 2 RD Ovation Logic Error Causing UA Alarms

(EC 631843)

08/12/2020

71111.15

Corrective Action

Documents

4353544

0B VC Chiller Condenser Press Step Change Noted

06/29/2020

4353654

Air In-Leakage at Suction Elbow of 0B BC Chiller

06/30/2020

4353654

Air In-Leakage at Suction Elbow of 0B BC Chiller

06/30/2020

4353656

Air In-Leakage at Guide Vane Shaft Seal of 0B VC Chiller

06/30/2020

4353657

Air In-Leakage at Oil Recovery Line of 0B VC Chiller

06/30/2020

4365308

Valve Plate and Debris Found in 1VQ02S

08/25/2020

4370636

Unexpected Alarm 2-22-C8, 2B Emergency Diesel

Generator Control Power Failure

09/19/2020

Procedures

ER-AA-600-1012

Risk Management Documentation

OP-AA-108-111

Adverse Condition Monitoring and Contingency Planning

OP-AA-108-115

Operability Determinations (CM-1)

Radiation

Surveys

OP-AA-106-101-

1006

Operational Decision-Making Process

71111.19

Corrective Action

Documents

4360835

Loose Fitting Caused Delay of Unit 0 Station Air Compressor

Surge Test

08/04/2020

Procedures

0BwOS SA-1

Unit 0 Station Air Compressor Surge Point Testing

WC-AA-101

On-Line Work Control Process

Work Orders

4737430-10

PMT 0SA01C - Surge Test and Functional

08/03/2020

4895576

Change Oil in Motor Bearings & Take Sample

08/06/2020

5014782

OFP03PB Diesel Driven Fire Pump Jacket Water Heater

Leak at fitting

07/22/2020

5052469

Diesel Driven Fire Pump Monthly Surveillance

07/23/2020

5054182

Unit 1 Rod Drive Ovation Logic Error Causing UA Alarms

08/17/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

(EC 631843)

5054243

Unit 2 Rod Drive Ovation Logic Error Causing UA Alarms

(EC 631843)

08/13/2020

5061397

ISR for 2CS003A/11A-ASME Surveillance Requirements for

2CS01PA & Check Valves

08/06/2020

71111.22

Procedures

2BwOSR 3.8.1.2-

Unit Two 2B Diesel Generator Operability surveillance

BwOP DG-1

Diesel Generator Alignment to Standby Condition

BwOP DG-11

Diesel Generator Startup and Operation

BwOP DG-12

Diesel Generator Shutdown

Work Orders

5052933

Inservice Testing: 2B EDG Monthly Operability Testing

07/22/2020

71114.06

Procedures

EP-AA-1000

Standardized Radiological Emergency Plan

EP-AA-1001

Radiological Emergency Plan Annex for Braidwood Station

71124.06

Corrective Action

Documents

AR 04233094

Open EMS Software Non-Conservative for Waste Gas

Release

03/25/2019

AR 04233618

Open EMS Software Issue for Liquid Releases

03/27/2019

AR 04272206

0CW058 Vacuum Breaker #1 Gas Leak from Air Release

Valve

08/14/2019

AR 04353041

Issues Identified with Open EMS

06/26/2020

Miscellaneous

BW200036

2019 Braidwood Nuclear Power Station Annual Radioactive

Effluent Release Report

2019

Interlab 2020

Radiochemistry Cross Check Program, 1st and 2nd Quarter

20

06/18/2020

Permit L-

20190105-314-B

Liquid Effluent Discharge

01/05/2019

Permit L-

20190213-016-B

Liquid Effluent Discharge

2/13/2019

Procedures

CY-BR-170-3001

Plant Effluent Dose Projections

CY-BR-170-301

Offsite Dose Calculation Manual

CY-BR-170-304

ODCM Quarterly Effluent Composite

CY-BR-170-3100

Alternate Sampling for Inoperable Automatic Samplers

Permit L-

20191101-103-C

Liquid Effluent Discharge

11/01/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Self-Assessments AR 04315192

Pre-NRC Inspection: Radioactive Gaseous and Liquid

Effluent Treatment (RETS) (IP 71124.06) and Radiological

Environmental Monitoring Program (REMP) (IP 71124.07)

05/28/2020

71151

Miscellaneous

NRC Performance Indicator Data; Mitigating Systems -

Mitigating Systems Performance Index for Heat Removal

Systems

07/2019-

06/2020

NRC Performance Indicator Data; Mitigating Systems -

Mitigating System Performance Index for Residual Heat

Removal Systems

07/2019 -

06/2020

NRC Performance Indicator Data; Mitigating Systems -

Mitigating System Performance Index for Cooling Water

Systems

07/2019 -

06/2020

Procedures

LS-AA-2001

Collecting and Reporting of NRC Performance Indicator

Data

15-16

LS-AA-2200

Mitigating System Performance Index Data Acquisition and

Reporting

6-7

71152

Corrective Action

Documents

4364058

Forced Helium Drying Skid Issue

08/19/2020

4364205

Decontamination May Be Needed Under 426' Fuel Handling

Building Aluminum Decking

08/19/2020

Procedures

BwFP FH-34

Water Transfers of the Spent Fuel Pool, Wet Cask Pit or

Transfer Canal

BwFP FH-64

Transporter Operations

BwFP FH-65

Spent Fuel Cask Site Transportation

BwFP FH-67

Trackmobile Operations

BwFP FH-68

HI-TRAC Preparation

BwFP FH-69

HI-TRAC Movement Within the Fuel Building

BwFP FH-70

HI-TRAC Loading Operations

BwFP FH-72

HI-STORM Processing

BwFP FH-74

MPC Reflood

BwFP FH-83

Spent Fuel Cask Contingency Actions

NO-AA-10

Quality Assurance Topical Report (AQTR)

OU-MW-671-300

MPC Processing Forced Helium Dehydration (FHD) for

PWRs (ISFSI)

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OU-MW-671-300

MPC Processing Forced Helium Dehydration (FHD) for

PWRs (ISFSI)

OU-MW-679-300

MPC Alternate Cooling for PWRs

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP Procedure)

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

6