IR 05000456/2021004

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Integrated Inspection Report 05000456/2021004 and 05000457/2021004
ML22028A195
Person / Time
Site: Braidwood  
Issue date: 01/28/2022
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Exelon Generation Co
References
IR 2021004
Download: ML22028A195 (36)


Text

SUBJECT:

BRAIDWOOD STATION - INTEGRATED INSPECTION REPORT 05000456/2021004 AND 05000457/2021004

Dear Mr. Rhoades:

On December 31, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station. On January 18, 2022, the NRC inspectors discussed the results of this inspection with Mr. J. Keenan, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Braidwood Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Braidwood Station.

January 28, 2022 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2021004 and 05000457/2021004

Enterprise Identifier:

I-2021-004-0065

Licensee:

Constellation Energy Generation, LLC

Facility:

Braidwood Station

Location:

Braceville, IL

Inspection Dates:

October 01, 2021 to December 31, 2021

Inspectors:

R. Bowen, Illinois Emergency Management Agency

J. Bozga, Senior Reactor Inspector

A. Demeter, Reactor Engineer

G. Edwards, Health Physicist

D. Kimble, Senior Resident Inspector

J. Park, Reactor Inspector

P. Smagacz, Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Inadequate Tracking of Equipment Status Required by Plant Technical Specifications Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000456/2021004-02 Open/Closed

[H.4] -

Teamwork 71153 A self-revealed finding of very low safety significance and an associated non-cited violation (NCV) of Technical Specification (TS) 3.3.1, Reactor Trip System (RTS) Instrumentation, were identified when the licensee operated Braidwood Unit 1 with the reactor trip functions for both of the units source range neutron flux channels, N31 and N32, manually bypassed.

Specifically, the units source range neutron flux channels, N31 and N32, are required to be operable:

In Modes 3, 4, and 5 with the rod control system capable of rod withdrawal or with one or more rods not fully inserted; or

In Mode 2 when power is below the source range block permissive interlock.

A review of this event determined that there were several periods between April 21, 2021, and April 23, 2021, when Unit 1 was operated with source range neutron flux channels, N31 and N32, inoperable due to their reactor trip functions being manually bypassed, and in a condition prohibited by TS 3.3.1. Additionally, there were two instances of mode changes during this timeframe, into Mode 4 and again into Mode 2, that were not in accordance with TS LCO

[Limiting Condition for Operation] 3.0.4 requirements.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000456,05000457/

2021004-01 2SI8822B Cold Leg Injection Throttle Valve Cage Failure 71152 Open LER 05000456/2021-001-00 LER 2021-001-00 for Braidwood Station, Unit 1,

Train A and B Source Range Neutron Flux Trip Functions Bypassed During Plant Startup 71153 Closed LER 05000456/2021-002-00 LER 2021-002-00 for Braidwood Station, Unit 1,

Unit Trip on Generator Load Rejection Due to Lightning Strike Within the Unit Switchyard Exceeding the Capabilities of the Switchyard Grounding System 71153 Closed

PLANT STATUS

Unit 1 began the inspection period operating at full power. With the exception of planned reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the entire inspection period.

Unit 2 began the inspection period operating at approximately 91 percent power and in power coast down for the planned end of the fuel cycle. On October 18, 2021, the unit was shut down for its planned 22nd refueling outage (A2R22). Following completion of refueling and other maintenance activities, the reactor was restarted and taken critical on November 5, 2021, and the main electrical generator was synchronized to the power grid later that same day. The unit reached full power operation on November 8, 2021, and continued operating at or near full power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors reviewed and evaluated the station's readiness for seasonal extreme weather conditions prior to the onset of seasonal cold temperatures during the week ending December 25, 2021.

External Flooding Sample (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated selected flood protection barriers, mitigation plans, procedures, and equipment to verify that they were consistent with the licensees design requirements and risk analysis assumptions for coping with external flooding during the week ending December 4, 2021.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors reviewed and evaluated selected system configurations during partial physical alignment verifications of the following systems/trains:

(1) The Unit 2 Residual Heat Removal (RH) system while the system was required for the decay heat removal function as a part of Refuel Outage A2R22 during the week ending October 23, 2021.
(2) The Unit 2 Spent Fuel Pool Cooling (SFP) system while the Unit 2 reactor core was removed and residing in the SFP as a part of Refuel Outage A2R22 during the week ending October 30, 2021.

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors reviewed and evaluated system configurations during a complete physical alignment verification of the Unit 2 Containment Spray system during the weeks ending October 16 through November 6, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting physical inspections and performing reviews to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) The Unit 2 Containment, Elevations 377' and 401', Missile Shield Area as part of the A2R22 Refuel Outage during the week ending October 23, 2021.
(2) The Unit 2 Containment, Elevation 426', Upper Area as part of the A2R22 Refuel Outage during the week ending October 23, 2021.
(3) The Auxiliary Building, Elevation 383', General Area South during the week ending December 4, 2021.
(4) The Auxiliary Building, Elevation 383', Unit 1 and Unit 2 Auxiliary Feedwater (AF)

Pump Diesel Rooms during the week ending December 4, 2021.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)

The inspectors reviewed and evaluated internal flooding mitigation protections for the following areas of the station:

(1) The Unit 2 Lower Cable Spreading Room Auxiliary Building, 439' Elevation, during the week ending December 11, 2021.

71111.08P - Inservice Inspection Activities (PWR) PWR Inservice Inspection Activities Sample (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk significant piping system boundaries, and containment boundary were appropriately monitored for degradation and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from October 18, 2021 to November 2, 2021:

03.01.a - Nondestructive Examination and Welding Activities.

Ultrasonic (UT) examination between pressurizer safety nozzle to safe end weld 2PZR-01-SE-02

UT examination between nozzle to safe end (22 degrees) weld 2RV-01-022

UT examination between safe end to nozzle (113 degrees) weld 2RV-01-024

UT examination between pressurizer to relief nozzle weld 2PZR-01-N3

UT examination between elbow to pipe weld 2MS-04-56

UT examination of reactor coolant pump main flange bolts 2RCP-01-RCP-PA-01 to 24

Liquid penetrant examination of bottom head to support skirt weld of 2RHX-01-2RHES-01

Magnetic particle examination of pressurizer support skirt attachment weld 2PZR-01-07

Pressure boundary welds 1, 1A, 2, 3, 4, and 5 fabricated during repair &

replacement of Valve 2RC8042A 03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination Activities

Bare Metal Visual (BMV) examination of the RPV upper head penetrations 03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities.

Boric Acid Leakage Evaluation of Component ID 2SI02PB, Issue Report (IR) 04344206

Boric Acid Leakage Evaluation and Corrective Action of Component ID 2CV239, IR 04376331

Boric Acid Leakage Evaluation and Corrective Action of Component ID 2CV8425, IR 04398552 03.01.d - Pressurized-Water Reactor Steam Generator Tube Examination Activities.

Unit 2 A, B, C, D, steam generators were examined by eddy current

There were no tubes subjected to in-situ pressure testing

Unit 2 A, B, C, D steam generators were examined visually on secondary side

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated the following licensed operator activities in the control room:

(1) Various activities involving on-watch operations crews. These activities included, but were not limited to:

Selected portions of the shutdown of Unit 2 for the A2R22 Refuel Outage, during the week ending October 23, 2021.

Selected portions of the cooldown of Unit 2 for the A2R22 Refuel Outage, during the week ending October 23, 2021.

Selected portions of the Unit 2 reactor coolant system drain to reduced inventory in support of A2R22 Refuel Outage reactor vessel head lift, during the week ending October 23, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated the following licensed operator training activity:

(1) A complex casualty graded scenario involving a crew of licensed operators was observed in facility's simulator on December 3, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure that selected structures, systems, and components (SSCs) remain capable of performing their intended functions. The following SSCs and/or maintenance activities were reviewed:

(1) Engineering Change (EC) 632665, which is in the process of being installed on all four
(4) of the station's EDGs to replace existing Kilovac relays with a Struthers-Dunn model for improved reliability, during the week ending December 4, 2021.
(2) A review of the effectiveness of maintenance activities planned and performed on the Unit 2 Control Rod Drive (RD) power supplies, during the week ending December 31, 2021.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluation of the work activities and risk associated with emergent troubleshooting and repairs to Unit 2 RD Power Cabinet 2BD, as documented in Work Order (WO)

===5195634 and IR 4452605 during the week ending October 16, 2021.

(2) Evaluation of the work activities and risk associated with emergent troubleshooting and repairs to the Unit 2 Safety Injection (SI) system following full flow testing performance issues, as documented in IR 4454447 during the weeks ending October 23 through October 30, 2021.
(3) Evaluation of the work activities and risk associated with Unit 2 Essential Service Water (SX) work (2A SX Strainer, as documented in WO 1752367, and 2SX002A Check Valve replacement, as documented in WO 5023104) during the week ending October 30, 2021.
(4) Evaluation of the work activities and risk associated with emergent repairs to the Penetration 55 RD funnel on the Unit 2 reactor vessel head during Refuel Outage A2R22, as documented in WO 5199832 during the week ending October 30, 2021.
(5) Evaluation of the work activities and risk associated with unplanned maintenance on the 2A Emergency Diesel Generator (EDG) during Refuel Outage A2R22, as documented in WO 5200200 during the week ending November 6, 2021.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01)===

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Evaluation of the operability of Unit 2 Source Range Nuclear Instrument (SRNI) N32 following a decision to postpone a planned detector replacement activity during the A2R22 Refuel Outage, as documented in IRs 4452229 and 4448954 during the weeks ending October 23 through October 30, 2021.
(2) Evaluation of the operability of the Unit 1 SRNIs with their high flux trips bypassed during reactor startup, as documented in IR 4418688 during the weeks ending July 1 through November 20, 2021.
(3) Evaluation of the operability of the 1C Overpower Delta Temperature (OPDT)instrumentation channel following a spurious trip of the channel, as documented in IR 4465938 during the week ending December 18, 2021.
(4) Evaluation of the functionality and operability of the Unit 2 Flex to AF connection isolation valves, as documented in IR 4466073 during the week ending December 18, 2021.
(5) Evaluation of the operability of the Unit 2 RD system after receiving a non-urgent rod control failure alarm, as documented in IR 4467108 during the week ending December 25, 2021.
(6) Evaluation of the operability of the Unit 2 SI system following issues identified as a part of full flow testing during the A2R22 Refuel Outage, as documented in IRs

===4454443 and 4454447 during the weeks ending October 23 through December 31, 2021.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

=

The inspectors reviewed and evaluated the following permanent changes to the facility:

(1) EC 633170: Units 1 and 2 rod speed demand scaling correction during the weeks ending October 30 through November 6, 2021.
(2) EC 634332: A weld overlay on the 2B Feedwater Pump discharge nozzle as a part of the A2R22 Refuel Outage during the weeks ending October 30 through November 6, 2021.
(3) ECs 378130, 388910, 393104, and 412478: Replacement of the 2SX002A Check Valve as a part of the A2R22 Refuel Outage during the week ending November 6, 2021.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (8 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1) Functional testing of the Unit 2 RD system after emergent maintenance involving Unit 2 RD Cabinet 1BD, as documented in WO 5195634 and IR 4452605 during the week ending October 16, 2021.
(2) Functional and operational testing of the Unit 2 AF system after maintenance during Refuel Outage A2R22, as documented in WO 1767441 during the week ending November 6, 2021.
(3) Functional and operational testing of Unit 2 control rods after maintenance during Refuel Outage A2R22, as documented in WOs 5106805 and 5201996 during the week ending November 6, 2021.
(4) Functional testing of the 2A EDG following work during Refuel Outage A2R22, as documented in WO 4868293 during the week ending October 30, 2021.
(5) Low power core physics testing following reactor refueling, as documented in WOs

===5058689 and 5039073 during the week ending November 6, 2021.

(6) Functional and operational testing of the 2A EDG following work to replace the EDG's emergency regulating circuit, as documented in WO 5200200 during the week ending November 6, 2021.
(7) Functional and operational testing of the main steam isolation valves after maintenance activities during Refuel Outage A2R22, as documented in WO 5044103 during the week ending November 6, 2021.
(8) Functional and operational testing of the AF system after maintenance during Refuel Outage A2R22, as documented in WOs 5044103, 5085932, 4868517, and 1737030 during the week ending November 6, 2021.

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01)===

(1) The inspectors reviewed licensee activities and evaluated licensee performance associated with Unit 2 Refuel Outage A2R22, during the weeks ending October 17 through November 13, 2021.

71111.22 - Surveillance Testing

The inspectors reviewed and evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1)2BwOSR 5.5.8.AF-4A(B): Unit 2 Comprehensive Inservice Testing Requirements for 2A(B) AF Pump during the weeks ending October 16 through October 23, 2021.

(2)1/2BwOSR 3.3.2.3: Undervoltage Simulated Start of AF Pump surveillances for the 1A and 2A AF Pumps during the weeks ending December 18 through December 25, 2021.

(3)2BwOSR 3.8.1.2-2: 2B EDG Operability surveillance during the week ending December 25, 2021.

Containment Isolation Valve Testing (IP Section 03.01) (1 Sample)

(1)2BwOSR 3.6.3.7-2: Primary Containment Type C Local Leakage Rate Tests of Containment Purge Exhaust Isolation Valves during the weeks ending October 23 through October 30, 2021.

FLEX Testing (IP Section 03.02) (1 Sample)

(1)0BwOS FX-9: Flex Pump Flow surveillance during the week ending December 11,

RADIATION SAFETY

71124.01 - Radiological Hazard Assessment and Exposure Controls

Radiological Hazard Assessment (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated how the licensee identifies the magnitude and extent of radiation levels and the concentrations and quantities of radioactive materials and how the licensee assesses radiological hazards.

Instructions to Workers (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated instructions to workers including radiation work permits used to access high radiation areas and labeling of radioactive material in containers.

Contamination and Radioactive Material Control (IP Section 03.03) (3 Samples)

The inspectors observed/evaluated the following licensee processes for monitoring and controlling contamination and radioactive material:

(1) The inspectors observed workers exiting the radiological controlled area at Unit 2 during a refueling outage.
(2) The inspectors observed licensee surveys of potentially contaminated material leaving the radiological controlled area.
(3) The inspectors observed work area staging for inspections of steam generators in Unit 2.

Radiological Hazards Control and Work Coverage (IP Section 03.04) (3 Samples)

The inspectors evaluated the licensee's control of radiological hazards for the following radiological work:

(1) The inspectors observed steam generator bowl installation and removal during the fall 2021 outage (Radiation Work Permit BW-02-21-00701 and associated ALARA documentation).
(2) The inspectors observed seal table maintenance activities during the fall 2021 outage (Radiation Work Permit BW-02-21-00649 and associated ALARA documentation).
(3) The inspectors observed reactor vessel head removal activities during the fall 2021 outage (Radiation Work Permit BW-02-21-00614 and associated ALARA documentation).

High Radiation Area and Very High Radiation Area Controls (IP Section 03.05) (2 Samples)

The inspectors evaluated licensee controls of the following High Radiation Areas and Very High Radiation Areas:

(1) Unit 2 steam generator platforms.
(2) Unit 2 reactor vessel head removal activities.

Radiation Worker Performance and Radiation Protection Technician Proficiency (IP Section 03.06) (1 Sample)

(1) The inspectors evaluated radiation worker and radiation protection technician performance as it pertains to radiation protection requirements.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors reviewed and verified selected portions of the licensee's performance indicator submittals listed below:

BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10)===

(1) Unit 1 (August 1, 2020 through September 30, 2021)
(2) Unit 2 (August 1, 2020 through September 30, 2021)

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (August 1, 2020 through September 30, 2021)
(2) Unit 2 (August 1, 2020 through September 30, 2021)

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1)

(August 1, 2020 through September 30, 2021)

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1)

(August 1, 2020 through September 30, 2021)

71152 - Problem Identification and Resolution (PI&R)

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors conducted a semiannual review of the licensees corrective action program (CAP) for potential adverse trends that might be indicative of a more significant safety concern during the weeks ending December 18 through December 31, 2021. A specific trend related to Delta T instrumentation and protection channels on Unit 1 is documented in the Results Section of this report.

Annual Follow-Up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors conducted in-depth reviews of the licensees implementation of the CAP related to the following issues:

(1) Review and assessment of the corrective actions from Unit 2 SI full flow testing issues during Refuel Outage A2R22, as documented in IRs 445443 and 445447 during the weeks ending October 30 through December 31, 2021.
(2) Review and assessment of the results of the Unit 2 Refuel Outage A2R22 reactor vessel head thermal sleeve measurements and ongoing licensee actions to monitor and address the condition, as documented in IR 4455790 during the weeks ending October 30 through November 6, 2021.

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)

The inspectors reviewed, evaluated, and closed the following licensee event reports (LERs):

(1) Unit 1 LER 05000456/2021-002-00, Unit Trip on Generator Load Rejection Due to Lightning Strike Within the Unit Switchyard Grounding System. (ADAMS Accession No. ML21230A030) The inspectors determined that it was not reasonable to foresee or correct the cause discussed in the LER therefore no performance deficiency was identified. The inspectors reviewed the LER during the weeks ending November 20 through December 4, 2021, and determined there were no associated findings or violations.
(2) Unit 1 LER 05000456/2021-001-00, Train A and B Source Range Neutron Flux Trip Functions Bypassed During Plant Startup. (ADAMS Accession No.

ML21172A153) The inspectors reviewed the LER during the week ending December 25, 2021. A finding of very low safety significance (Green) and an associated NCV are documented in the Results Section of this report.

INSPECTION RESULTS

Unresolved Item (Open)2SI8822B Cold Leg Injection Throttle Valve Cage Failure URI 05000456,05000457/2021004-01 71152

Description:

The inspectors performed a detailed review and assessment of the licensees corrective actions for several issues that were identified during full flow surveillance testing of the Unit 2 safety injection (SI) system during the A2R22 Refuel Outage in the fall of 2021. The inspectors reviews included, but were not limited to, the following IRs:

4454447: Failed Acceptance Criteria for 2BwOSR 5.5.8.SI-11 F.1

4454443: 03-OSP-A Evaluate Flow Balance for Unit 2 SI Cold Leg Injection

4455415: Foreign Material Recovered from 2SI8822B/C/D Throttle Valves

4183402: 2SI8810D Inspection Results FME

4455569: 2SI8822B As-Found Inspection Unsatisfactory

4455416: Foreign Material Recovered from 2CV8369A/D Throttle Valves The inspectors chose this issue for an in-depth review of the licensees actions within their CAP because of the inherent safety significance of issues involving the operability, availability, and capability of the units SI system. Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensees corrective actions taken to restore the system to its full capabilities.

On October 21, 2021, as part of scheduled testing activities for the Unit 2 A2R22 Refuel Outage, the licensee performed 2BwOSR 5.5.8.SI-11, Comprehensive Inservice Testing (IST) Requirements for Unit 2 Safety Injection Pumps and Safety Injection System Check Valve Stroke Test. As discussed in IR 4454447, The total flow acceptance criteria for the test of 140 gpm was not met, with the measured value being 139.6 gpm. Additionally, criterion within 2BwOSR 5.5.8.SI-11 requires the licensee to evaluate the need for SI system flow balancing if the three lowest line flows are less than 439 gpm, and/or the difference between the highest and lowest line flows is greater than 10 gpm. In this instance, the value obtained for the three lowest line flows was 437.6 gpm, and the value obtained for the difference between the highest and lowest line flows was 13 gpm.

Due to past issues with foreign material having been introduced into the Unit 2 SI system, the licensee developed a comprehensive plan to disassemble and inspect several throttle valves within the system where tight clearances might trap foreign material in the flow stream. As discussed in IR 4455415, small amounts of foreign material were identified within the 2SI8822B, 2SI8822C, and 2SI8822D Cold Leg Injection SI Throttle Valves. As part of their corrective actions, the licensee removed the materials that were found and sent them out for laboratory analysis off site. The licensee also flushed the system thoroughly and conducted flow balancing to restore each cold leg injection flow path to its optimum value. The licensee was able to show by calculation that the small amount by which the SI system flow was found out-of-tolerance was within the existing margin for the system and did not impact the system function. The inspectors did not identify any issues with the licensees CAP actions taken for these aspects of the issue.

During disassembly and inspection of the 2SI8822B Cold Leg Injection Throttle Valve, the licensee identified that the throttle valve cage had cracked and failed. The licensee replaced the valve internals and successfully rebalanced the SI cold leg injection flows as noted above. However, the licensees follow-on analysis was not able to identify a cause or adequately explain the reasons behind the failure. Laboratory analysis of the failed internal components suggested that the valve seat ring was most probably the first component to fail, and the fracture surfaces were consistent with intergranular stress corrosion cracking and inconsistent with an overload failure.

Near the end of the inspection period, the licensee decided to commission a formal CAP causal evaluation to further look into the 2SI8822B Cold Leg Injection SI Throttle Valve cage failure.

Planned Closure Actions: The failure of the 2SI8822B Cold Leg Injection SI Throttle Valve cage is considered unresolved pending the inspectors receipt and review of the licensees formal causal evaluation. At the end of the inspection period, the licensee planned to complete this evaluation during the 1st Quarter of 2022.

Licensee Actions: No additional licensee actions are necessary at this time.

Corrective Action References:

IR 4455415: Foreign Material Recovered from 2SI8822B/C/D Throttle Valves

IR 4455569: 2SI8822B As-Found Inspection Unsatisfactory Observation: Trend in Unit 1 Overpower Delta T Issues 71152 The inspectors performed a review of plant issues, particularly those entered into the licensees CAP over the past several months. During their review, the inspectors noted an adverse trend on Unit 1 involving the performance of the units Overpower Delta T (OPDT)protection channels. Specific CAP entries reviewed by the inspectors included, but were not limited to:

- IR 4421778; Unexpected Alarms 1-10-A5 and 1-14-A1 for OPDT.

- IR 4441987; Unexpected Alarms 1-10-A5 and 1-14-A1 for 1C OPDT.

- IR 4465938; 1C OPDT Setpoint Spiked Low. Unexpected Alarms and Half-Trip.

In the first instance, documented under IR 4421778 on May 5, 2021, the 1B OPDT Channel was involved. The subsequent cases, documented under IR 4441987 on August 22, 2021, and IR 4465938 on December 10, 2021, involved the 1C OPDT Channel. In each case, a momentary downward spike in the OPDT setpoint resulted in a spurious half-trip condition within the Unit 1 solid state protection system (SSPS). Following each instance, the licensee replaced one or more cards within the Unit 1 SSPS and successfully retested and restored the affected channel to service.

The inspectors noted that while these spurious half-trip signals had not resulted in an actual plant transient to date, their continuing presence was problematic with respect to event free unit operations. The inspectors further noted that the licensee was placing an appropriate level of emphasis on this issue; shortly after the conclusion of the inspection period the licensee generated IR 4470640, Proactive Replacement of Unit 1 7300 NSA Cards, within the stations CAP to drive the replacement of certain Unit 1 SSPS cards that been identified as suspect during the extent-of-condition reviews for this issue.

The inspectors did not identify any findings or violations of NRC requirements in the course of their review.

Observation: Control Rod Drive Mechanism Thermal Sleeves 71152 The inspectors performed a detailed review of IR 4455790, A2R22 CRDM Thermal Sleeve Metrology VT-1 Exam Results.

The sample selected was associated with a 10 CFR Part 21 notification to the NRC (Westinghouse LTR-NRC-19-79, dated December 12, 2019; ADAMS Accession No.

ML19346H873) and additional information on the 10 CFR Part 21 in Nuclear Safety Advisory Letter (NSAL) NSAL-20-1, Reactor Vessel Head Control Rod Drive Mechanism Penetration Thermal Sleeve Cross-Sectional Failure, dated February 14, 2020 (ADAMS Accession No.

ML20063J583). The specific issue was associated with mechanical fatigue and fracture that leads to flange separation of thermal sleeves in the control rod drive mechanism (CRDM)penetration tubes which could have a safety consequence that was not previously considered. In addition, the sample was associated with NSAL-18-1, Thermal Sleeve Flange Wear Leads to Stuck Control Rod, dated July 9, 2018 (ADAMS Accession No.

ML18198A275). The specific issue was associated with thermal sleeve flange wear that leads to complete flange separation of the thermal sleeves which may prevent control rod insertion. PWROG-16003-P, Evaluation of Potential Thermal Sleeve Flange Wear, Revision 2, provides acceptance criteria for evaluation of thermal sleeve flange wear associated with NSAL 18-1.

The licensee performed an evaluation of the actual thermal sleeve wear measurements taken at thermal sleeve penetrations during the fall Unit 2 2021 refuel outage (A2R22). Penetration No. 55 appeared to contain a measurement discrepancy. The licensee performed a follow-up inspection on thermal sleeve Penetration No. 55 using a telescoping camera, and that inspection revealed that the funnel on the thermal sleeve had partially unscrewed by approximately 5 full revolutions. This accounted for the unusual drop measurement found during the thermal sleeve measurement inspections. Following reattachment of the funnel and reperformance of the thermal sleeve measurements on Penetration No. 55, thermal sleeve measurements taken for all penetrations were less than the NSAL-20-1 lowering criteria and the PWROG-16003-P, Revision 2, acceptance criteria. VT-1 visual examinations were performed on Penetration Nos. 8, 36, 60, 40, and 67. No recordable or relevant indications (i.e., cracking) were identified. The inspectors reviewed the evaluations and consulted with technical staff from the NRC Office of Nuclear Reactor Regulation (NRR). Based on this review, the inspectors concluded that the licensee was taking appropriate actions to monitor and address this issue. No findings or violations were identified.

Inadequate Tracking of Equipment Status Required by Plant Technical Specifications Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000456/2021004-02 Open/Closed

[H.4] -

Teamwork 71153 A self-revealed finding of very low safety significance and an associated non-cited violation (NCV) of Technical Specification (TS) 3.3.1, Reactor Trip System (RTS) Instrumentation, were identified when the licensee operated Braidwood Unit 1 with the reactor trip functions for both of the units source range neutron flux channels, N31 and N32, manually bypassed. Specifically, the units source range neutron flux channels, N31 and N32, are required to be operable:

In Modes 3, 4, and 5 with the rod control system capable of rod withdrawal or with one or more rods not fully inserted; or

In Mode 2 when power is below the source range block permissive interlock.

A review of this event determined that there were several periods between April 21, 2021, and April 23, 2021, when Unit 1 was operated with source range neutron flux channels, N31 and N32, inoperable due to their reactor trip functions being manually bypassed, and in a condition prohibited by TS 3.3.1. Additionally, there were two instances of mode changes during this timeframe, into Mode 4 and again into Mode 2, that were not in accordance with TS LCO [Limiting Condition for Operation] 3.0.4 requirements.

Description:

Unit 1 entered Refuel Outage A1R22 on April 5, 2021. Part of the scheduled outage work activities included transmission system work within the stations 345 KV switchyard, some of which had been known to cause electrical interference with a units nuclear instruments and other sensitive instrumentation. Station procedure BwOP RP-9, Disabling and Restoring Source Range Nuclear Instruments, provides procedural guidance to disable and restore source range nuclear instrument (SRNI) reactor trips and high flux at shutdown alarms, and was created, in part, to specifically address this known vulnerability.

The licensee had affixed a placard on main control room (MCR) panel 0PM03J for the 345 KV switchyard controls that read, Refer to BwOP RP-9 Prior to Switchyard Operations.

At approximately 7:24 a.m. on April 21, 2021, with Unit 1 in cold shutdown (Mode 5) and control rods not capable of being withdrawn, plant operators in the MCR received communications from the transmission system operator directing them to perform switching operations in the 345 KV switchyard. Without performing an adequate pre-job briefing or establishing clear roles and responsibilities for the activity, including responsibilities for tracking and subsequent restoration, plant operators performed the initial steps of BwOP RP-9 to defeat SRNI automatic actuations for both N31 and N32. The in-progress procedure was then returned to the Unit 1 Supervisors desk in the MCR. No formal tracking mechanism was used for the in-progress procedure, and no entries were made in the Unit 1 narrative log or degraded equipment log regarding the status of the units SRNIs.

Switching operations in the stations 345 KV switchyard were performed as directed by the transmission system operator, but BwOP RP-9 steps to restore the N31 and N32 SRNI trips and alarms were subsequently not performed due to the lack of proper formal tracking of the instruments status and the fact that no formal ownership for the completion of the BwOP RP-9 procedure had been established by the MCR crew. Later during the same shift in the MCR, the crew reached the point in their preparations for unit startup from the refueling outage where the Unit 1 rod drive system was required for scheduled surveillances to verify operability of the digital rod position indication and to perform control rod drive mechanism timing testing. At approximately 3:09 p.m. on April 21, 2021, lift disconnects for control and shutdown bank rod groups and reactor trip breakers were closed enabling control rod withdrawal. These actions met the entry conditions for TS LCO 3.3.1, Table 3.3.1-1, Function 5, which is applicable in Modes 3, 4, and 5 with control rods capable of withdrawal. With both N31 and N32 SRNI high flux reactor trip functions bypassed, TS 3.3.1, Required Action I.1, directs operators to immediately open the reactor trip breakers. This action was not completed because the MCR operations crew had lost track of the actual status of N31 and N32 and because they incorrectly assumed that the SRNIs were operable based on expected visual and audible indications.

In the evening on April 21, 2021, MCR operator turnover from dayshift to nightshift occurred with the rod control surveillance tests still in-progress. Operators conducting turnover activities failed to recognize main control board alarm annunciators on Unit 1 that indicated that the SRNI reactor trips were bypassed, as well as the SRNI level trip bypass switch positions and status lights located on the N31 and N32 instrument drawers. The rod control surveillances were completed at approximately 7:30 p.m., but the Unit 1 reactor trip breakers remained closed and control rods capable of withdrawal as the second control rod drive motor-generator set was being returned to service following emergent maintenance.

At approximately 10:21 p.m. on April 21, 2021, Unit 1 entered hot shutdown (Mode 4). With both of the units source range neutron flux channels, N31 and N32, manually bypassed and, therefore, inoperable and control rods capable of being withdrawn, this change in reactor operating mode failed to meet the requirements of TS LCO 3.0.4. Later in the same shift at approximately 1:24 a.m. on April 22, 2021, the units reactor trip breakers were opened, and control rods were no longer capable of being withdrawn. At this point, SRNI reactor trip functions were no longer required for compliance with TS 3.3.1. At approximately 3:24 a.m.

on April 22, 2021, Unit 1 entered hot standby (Mode 3). Fortuitously, since the units reactor trip breakers were open and control rods were not capable of being withdrawn, this change in reactor operating modes did meet the requirements of TS LCO 3.0.4.

In the morning on April 22, 2021, MCR operator turnover from nightshift to dayshift took place without operators noting the main control board alarm annunciators on Unit 1 that indicated that the SRNI reactor trips were bypassed, or the SRNI level trip bypass switch positions and status lights located on the N31 and N32 instrument drawers. Control rods were made capable of withdrawal at approximately 1:54 p.m. on April 22, 2021, for control rod drive system relay trip checks. This resulted in a second example of the same noncompliance with the requirements of TS 3.3.1. Unit 1 reactor trip breakers were opened at approximately 4:21 p.m. on April 22, 2021.

In the evening on April 22, 2021, MCR operator turnover from dayshift to nightshift occurred again without operators noting the main control board alarm annunciators on Unit 1 that indicated that the SRNI reactor trips were bypassed, or the SRNI level trip bypass switch positions and status lights located on the N31 and N32 instrument drawers. At approximately, 6:29 p.m. on April 22, 2021, Unit 1 reactor trip breakers were closed in order to perform rod drop time testing, leading to a third example of the same noncompliance with the requirements of TS 3.3.1. The testing concluded at approximately 10:07 p.m. on April 22, 2021, and the Unit 1 reactor trip breakers were once again opened.

In preparation for the Unit 1 reactor startup from Refuel Outage A1R22, reactor trip breakers were closed at approximately 1:22 a.m. on April 23, 2021, leading to a fourth example of the same noncompliance with the requirements of TS 3.3.1. At approximately 11:54 a.m. on April 23, 2021, Unit 1 entered startup (Mode 2). With both of the units source range neutron flux channels, N31 and N32, manually bypassed and, therefore, inoperable and control rods capable of being withdrawn, this change in reactor operating mode failed to meet the requirements of TS LCO 3.0.4. At approximately 12:16 p.m. on April 23,2021, the condition was identified by MCR personnel. Upon identification, the SRNI high neutron flux trips were immediately restored and N31 and N32 made operable.

The licensee reported this event in accordance with 10 CFR 50.73(a)(2)(v)(A), as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to shut down the reactor and maintain it in a safe shutdown condition, and in accordance with 10 CFR 50.73(a)(2)(i)(B), as an operation or condition prohibited by the plant's TS. The licensee reported this event to the NRC as LER 2021-001-00, Train A and B Source Range Neutron Flux Trip Functions Bypassed During Plant Startup, on June 21, 2021, (ADAMS Accession Number ML21172A153).

Corrective Actions: Immediately following the identification of the condition, the licensee completed station procedure BwOP RP-9 to restore SRNIs N31 and N32 to an operable status. Detailed extent-of-condition physical walkdowns in the MCR and reviews for in-progress plant procedures were performed to identify any other similar issues. The licensee commissioned a full root cause investigation for the event, which prompted changes to in-progress procedure tracking, MCR shiftly and daily operator rounds, and mode change checklists. Additionally, the licensee developed and implemented a comprehensive plan to improve MCR operator standards.

Corrective Action References: 4418688; Source Range High Flux Reactor Trip Bypassed When Required; 04/24/2021.

Performance Assessment:

Performance Deficiency: Station procedure BwOP RP-9, Disabling and Restoring Source Range Nuclear Instruments, provides procedural guidance to disable and restore SRNI reactor trips and high flux at shutdown alarms. Section F.1 of this procedure provides the actions necessary to disable the disable the SRNI reactor trips and high flux at shutdown alarms, while Section F.2 provides the actions necessary to restore the SRNI reactor trips and high flux at shutdown alarms. On April 21, 2021, the MCR crew performed Section F.1, but lost track of the status of the in-progress procedure and never performed Section F.2 prior to the SRNIs being required per TS 3.3.1. The inspectors concluded that the licensees failure to have completed station procedure BwOP RP-9 as written and in a timely manner constituted a performance deficiency that was within the licensees ability to have foreseen and that should have been prevented.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Configuration Control and Human Performance attributes of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inspectors determined that the licensees failure to have restored the reactor trips and high flux at shutdown alarms for SRNIs N31 and N32 in a timely manner led to multiple examples where the TS 3.3.1 Required Actions were not met or an LCO was not met prior to a mode change in accordance with TS LCO 3.0.4. The inspectors also compared the finding with the examples listed in IMC 0612, Power Reactor Inspection Reports, Appendix E, Example of Minor Issues. Example 4.k was found to be similar in that the performance deficiency adversely affected Mitigating Systems Cornerstone of Reactor Safety objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and IMC 0609, Appendix G, Shutdown Operations Significance Determination Process. This event began on April 21, 2021, with Unit 1 in cold shutdown (Mode 5). It concluded on April 23, 2021, when Unit 1 was in startup (Mode 2). As a result, the inspectors determined that both IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, and IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, were applicable for parts of the event, and that assistance from the NRC Region III Senior Reactor Analyst (SRA) was required in order to properly characterize the findings significance.

Starting with the portion of the event that occurred with Unit 1 in startup (Mode 2), the inspectors using IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, Exhibit 2, Mitigating Systems Screening Questions, were able to answer no to all questions and determined that the significance of the finding was indicative of being of very low safety significance (Green). More specifically, the inspectors, in consultation with the NRC Region III SRA, concluded that probabilistic risk assessment (PRA) functionality of the Unit 1 reactor protection system had not been lost with Unit 1 in Mode 2 because the power range high neutron flux reactor trip (low setting) was available and provided redundant protection to that afforded by the N31 and N32 SRNI high flux reactor trip function.

For the portions of the event that occurred with Unit 1 in Modes 3 through 5, however, the inspectors found that there was a loss of PRA functionality of the Unit 1 reactor protection system, as the power range nuclear instruments (PRNIs) are incapable of detecting neutron power levels in this range. Using IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, the inspectors and the NRC Region III SRA subsequently concluded that the event was of very low safety significance (Green) based on the following:

For the uncontrolled rod withdrawal casualty, despite the fact that the SRNI high flux reactor trip functions from N31 and N32 are credited in the stations updated final safety analysis report (UFSAR) for providing protection for the event, the probability of such an event remained highly unlikely. A review by the inspectors of the required and actual reactor coolant system (RCS) boron concentration for the time in question (from 2:00 a.m. on April 21, 2021, to noon on April 23, 2021) confirmed that RCS boron concentration remain above the minimum required to prevent criticality, even with a full bank of control rods being fully withdrawn.

For the inadvertent boron dilution event, which is a slower reactivity addition event than the uncontrolled rod withdrawal event, operator action is credited for responding to and mitigating the event. A review by the inspectors concluded that there were multiple redundant indications that remained available to alert plant operators to such a potential dilution, and thus, initiate the required operator response.

Cross-Cutting Aspect: H.4 - Teamwork: Individuals and work groups communicate and coordinate their activities within and across organizational boundaries to ensure nuclear safety is maintained. Specifically, this event illustrated multiple missed opportunities (e.g.,

crew turnovers, MCR board walkdowns, log reviews, etc.) for operators in the MCR to have more rapidly identified the error responsible for the event.

Enforcement:

Violation: Technical Specification (TS) 3.3.1, Reactor Trip System (RTS) Instrumentation, requires that a units source range neutron flux channels, N31 and N32, are operable:

In Modes 3, 4, and 5 with the rod control system capable of rod withdrawal or with one or more rods not fully inserted; or

In Mode 2 when power is below the source range block permissive interlock.

Further, TS LCO 3.0.4 states, in part, that:

When an LCO is not met, entry into a Mode or other specified condition in the Applicability shall only be made:

1. When the associated ACTIONS to be entered permit continued operation in the

MODE or other specified condition in the Applicability for an unlimited period of time;

2. After performance of a risk assessment addressing inoperable systems and

components, consideration of the results, determination of the acceptability of entering the MODE or other specified condition in the Applicability, and establishment of risk management actions, if appropriate (exceptions to this Specification are stated in the individual Specifications); or

3. When an allowance is stated in the individual value, parameter, or other Specification.

Contrary to these requirements, from April 21, 2021, through April 23, 2021, there were multiple instances where the licensee operated Unit 1 in Mode 2 with power below the source range block permissive interlock, and in Modes 3, 4, and 5 with the rod control system capable of rod withdrawal, while the units source range neutron flux channels, N31 and N32, were inoperable; and there were two instances where Mode changes were performed by the licensee under these conditions.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: LER 05000456/2021-002-00: Unit Trip on Generator Load Rejection Due to Lightning Strike Within the Unit Switchyard Exceeding the Capabilities of the Switchyard Grounding System 71153 The inspectors performed a detailed review of the licensees root cause evaluation associated with IR 4430441, Braidwood Unit 1 Reactor Trip on Generator Load Rejection.

On June 21, 2021, at 12:51 a.m., Braidwood Unit 1 experienced turbine and reactor trips preceded by a main electrical generator load reject. The cause of the main generator load reject was not initially known by plant operators, who successfully completed the Unit 1 shut down in accordance with plant procedures. Following the event, plant personnel began an investigation into the cause of the event. Through a review of various data recorded on both station recorders and the equipment of the transmission system owner (ComEd), plant technical personnel were able to determine the cause of the event.

A thunderstorm in the area produced a lightning strike within the stations switchyard at the exact time of the main electrical generator load reject. The root cause of the load rejection was determined to have been this lightning strike within the stations switchyard, which exceeded the capabilities of the switchyard grounding system. The lightning strike resulted in and induced voltage on the 125 Volts - direct current (Vdc) load rejection circuit for the Unit 1 generator output breakers, which resulted in both breakers opening.

The licensee determined that station equipment operated as designed to prevent a nuclear safety impact and/or equipment damage from the lightning strike. Licensee inspections of the switchyard grounding system confirmed that it was not degraded. However, the system was not designed to be able to fully handle a direct lightning strike of the magnitude that was seen. The national average magnitude for a lightning strike is approximately 30 kiloamps (kA); the lightning strike during this event was approximately 98 kA, or over three times the national average, as measured by the switchyard data recording systems.

The inspectors did not identify any issues with the licensees actions taken in response to this event. No findings or violations of NRC requirements were identified by the inspectors in the course of this review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On January 18, 2022, the inspectors presented the integrated inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On October 22, 2021, the inspectors presented the radiation protection inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On November 2, 2021, the inspectors presented the Braidwood Unit 2 ISI inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

4467447

FLEX Building Unavailable >72 Hours Due to Offsite Power

2/18/2021

Miscellaneous

Letter from Mr. John Keenan to Mr. Shane Marik; 2022

Winter Readiness Certification

11/15/2021

0BwOS XFT-A1

Unit Common Freezing Temperature Equipment Protection

Surveillance

0BwOS XFT-A2a

Unit Common Station Heat Area Heaters Freezing

Temperature Equipment Protection Surveillance

0BwOS XFT-A2b

Unit Common Station Heat Area Heaters Freezing

Temperature Equipment Protection Surveillance

0BwOS XFT-A3

Unit Common Cold Weather Surveillance

0BwOS XFT-A4

Unit Common Freezing Temperature Equipment Protection

Inside Surveillance

BwOP SI-10

RWST Heating Pump and Heater Operations

71111.01

Procedures

CC-BR-118-1001

Site Implementation of Diverse and Flexible Coping

Strategies (FLEX) and Spent Fuel Pool Instrumentation

Program

212516

0FC8754 is Broken and Will not Operate

01/20/2019

284038

0FC8754 Handwheel Degraded Due to Vibration

10/01/2019

4353919

2CS01PA ASME Lost Surveillance Paperwork

06/30/2020

4361554

2A CS Pump DP Tracking EDG Uncertainties

08/06/2020

4364030

2A CS Pump Seal and Shaft Coupling has Boric Acid

Buildup

08/19/2020

4418729

0FC8754 High Vibrations in Area

04/24/2021

Corrective Action

Documents

4436483

0FC8754 Valve Handwheel Operator Detached

07/22/2021

M-129 Sheet 1A

Diagram of Containment Spray

AP

M-129 Sheet 1B

Diagram of Containment Spray

AX

M-129 Sheet 1C

Diagram of Containment Spray

AO

M-2129 Sheet 1

P&ID/D&I Diagrams Containment Spray System

L

M-2129 Sheet 2

P&ID/C&I Diagrams Containment Spray System

L

M-2129 Sheet 4

P&ID/C&I Diagrams Containment Spray System

D

71111.04

Drawings

M-2129 Sheet 5

P&ID/C&I Diagrams Containment Spray System

C

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Bw-OP FC-M2

Operating Mechanical Lineup Unit 2

BwOP CS-E2

Electrical Lineup Unit 2

BwOP CS-M2

Operating Mechanical Lineup Unit 2

BwOP FC-E1

Electrical Lineup Unit 1

BwOP FC-E2

Electrical Lineup Unit 2

BwOP FC-M1

Operating Mechanical Lineup Unit 1

BwOP RH-6

Placing the RH System in Shutdown Cooling

Procedures

BwOP RH-M3

Operating Mechanical Lineup Unit 2 2A RH Train

BwAP 1110-1

Fire Protection Program System Requirements

BwAP 1110-3

Plant Barrier Impairment Program

BwOP PBI-1

Plant Barrier Impairment Program Pre-Evaluated Barrier

Matrix

CC-AA-201

Plant Barrier Control Program

ER-AA-600-1069

High Risk Fire Area Identification

ER-BR-600-1069

Site List of High-Risk Fire Areas Braidwood Unit 1 and

Unit 2

OP-AA-201-009

Control of Transient Combustible Material

71111.05

Procedures

OP-AA-201-012-

1001

Operations On-Line Fire Risk Management

3C8-0685-002

Auxiliary Building Flood Level Calculation

Calculations

3C8-0887-001

Confirmation of Safe Shutdown Capability After Auxiliary

Building Flooding

Corrective Action

Documents

4447598

Floor Drain Overflowing in Unit 2 Cable Spreading Room

09/20/2021

Miscellaneous

BB-PRA-012

Byron and Braidwood Probabilistic Risk Assessment,

Internal Flood Evaluation Summary Notebook

0BwOA PRI-8

Auxiliary Building Flooding Unit 0

71111.06

Procedures

ER-AA-450

Structures Monitoring

4344206

2SI01PB Active Leakage from Gasket

05/18/2020

4376331

2CV239, Pen 41 377'+14' Unit 2 CNMT

10/13/2020

4397547

Previous IWL Sample Sizes not IAW ASME IWL Code

Requirements

01/22/2021

71111.08P

Corrective Action

Documents

4398552

2CV8425 Diaphragm Leak

01/28/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4454677

Action Plan to Address Unit 2 Rx Head Residues

10/21/2021

4455474

Change in 2B SG Steam Drum Degradation (A2R22)

10/25/2021

4455917

Eddy Current Indication in SG B During A2R22

10/26/2021

4456449

Foreign Object Found In 2D SG Secondary Side - A2R22

10/28/2021

4456561

FME: Foreign Object Found In 2B SG Secondary Side -

A2R22

10/28/2021

618744

A2R19 Condition Monitoring and Operational Assessment

(CMOA) (Including the Foreign Object Evaluation) Unit 2

Steam Generator

634787

A2R22 Steam Generator Degradation Assessment

Engineering

Changes

635377

2RC01R Upper Head Primer Coating Delamination

Resulting in Spotting on Surface

1-51A

Procedure Qualification Record

2/28/1983

4-51A

Procedure Qualification Record

09/12/1986

Procedure Qualification Record

2/08/2000

Procedure Qualification Record

2/08/2000

AIM 200310778-

2-2

Braidwood Unit 2 Operational Assessment Addressing

Deferment of A2R21 Steam Generator Tube Examination to

A2R22, October 2021

04/15/2020

LTR-CDMP-21-

Evaluation of Condition Monitoring and in Situ Screening of

PWSCC Located in SG-B at R1C25 U-Bend at Braidwood

Unit 2

MRS-TRC-2374

Site Validation of EPRI Appendix H / Appendix I Techniques

10/21/2021

QR-20-164-04

Certified Material Test Report for Tube Plugs

10/06/2021

Miscellaneous

SGP-PLG-RIB-

FP-GEN

Mechanical Ribbed Plugging of Steam Generator Tubes

4.1

A2R22-MT-002

Pressurizer Support Skirt Attachment Weld 2PZR-01-07

10/25/2021

A2R22-UT-002

Pressurizer to Relief Nozzle Weld 2PZR-01-N3

10/24/2021

A2R22-VEN-002

2PZR-01-SE-02 (Pressurizer Safety Nozzle - Safe End

Weld)

10/23/2021

A2R22-VEN-005

Bare Metal Visual Examination of Reactor Pressure Vessel

Head

10/28/2021

NDE Reports

WN22-01

2RV-01-022 Nozzle to Safe End (22 Degrees) Weld

10/25/2021

Procedures

ER-AA-335-003

Magnetic Particle (MT) Examination

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ER-AA-335-036

Ultrasonic Examination of Weld Overlaid Similar and

Dissimilar Metal Welds

ER-AP-335-001

Bare Metal Visual Examination for Nickel Alloy Materials

ER-AP-420-002

Byron/Braidwood Unit 2: Steam Generator Eddy Current

Activities

ER-AP-420-0051

Conduct of Steam Generator Management Program

Activities

PDI-UT-8

Generic Procedure for the Ultrasonic Examination of Weld

Overlaid Similar and Dissimilar Metal Welds

I

SGP-PLG-RIB-

PS-GEN

Steam Generator Tube Plugging Procedure Specification for

Expanded Ribbed Mechanical Plugs

WDI-STD-1165

Automated Ultrasonic Examination of the Remote Inservice

Inspection of Reactor Vessel Nozzle to Safe End, Nozzle to

Pipe, and Safe End to Pipe Welds Using the Athena Phased

Array System

WPS 8-8-GTSM

ASME Welding Procedure Specification Record

05032066-01

CM - 2RC8042A Replace Valve

04/28/2020

Work Orders

05120762-01

FNM Repair 2CV8425 Diaphragm Leak

01/29/2021

71111.11A

Procedures

TQ-BR-201-0113

Braidwood Training Department Simulator Examination

Security Actions

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-AA-101-113

Operator Fundamentals

OP-AA-101-113-

1006

4.0 Crew Critique Guidelines

OP-AA-103-102

Watch-Standing Practices

OP-AA-103-102-

1001

Strategies for Successful Transient Mitigation

OP-AA-103-103

Operation of Plant Equipment

OP-AA-104-101

Communications

OP-AA-111-101

Operating Narrative Logs and Records

OP-AA-300

Reactivity Management

TQ-AA-10

Systematic Approach to Training Process Description

71111.11Q

Procedures

TQ-AA-150

Operator Training Programs

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-201

Examination Security and Administration

TQ-AA-306

Simulator Management

4467108

Unexpected Annunciator 2-10-D6 Rod Control Non-Urgent

Failure

2/16/2021

Corrective Action

Documents

4468189

Reflash of Unit 2 Rod Control Non-Urgent Failure Alarm

2-10-D6

2/23/2021

Engineering

Changes

2665

Diesel Generator (DG) Kilovac Relay Replacement with

Struthers-Dunn Model (Units 1 and 2)

ER-AA-310-1002

Maintenance Rule Functions Safety Significant

Classification

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1001

Maintenance Rule 18-10 Scoping

ER-AA-320-1003

Maintenance Rule 18-10 Failure Definitions

71111.12

Procedures

ER-AA-320-1004

Maintenance Rule 18-10 Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

4452605

Received Unexpected Alarm 2-10-C6 Rod Control Urgent

Failure

10/13/2021

4454443

03-OSP-A Evaluate Flow Balance for U2 Cold Leg Injection

11/20/2021

4454447

Failed Acceptance Criteria for 2BwOSR 5.5.8.SI-11 F.1

10/21/2021

4455090

A2R22 Expanded Scope on 2SX216A

10/23/2021

4455696

2SX174 Dis/Insp PM Requires Additional Isolation

10/26/2021

4456393

10-OSP-A: 2A Diesel Generator Suspected Relay Failure

4EX3

10/28/2021

4456459

11-OSP-R: 2A EDG No PI Parameters

10/28/2021

4456705

11-OSP-A: 2A Diesel Generator Relay 4EX1 Not Making Full

Contact

10/28/2021

Corrective Action

Documents

4456769

11-OSP-A: 2A Diesel Generator Manually Tripped During

Testing

10/29/2021

Engineering

Changes

619607

Alternative Weld Detail for CRDM Guide Funnel

BwAR 2-10-C6

Rod Control Urgent Failure

71111.13

Procedures

CC-AA-206

Fuse Control

Revision 11

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CC-BR-206-1000

Fuse Replacement

ER-AA-600

Risk Management

ER-AA-600-1042

On-Line Risk Management

MA-AA-716-004

Conduct of Troubleshooting

OP-AA-107

Integrated Risk Management

OP-AA-108-117

Protected Equipment Program

OU-AA-101-1011

Outage Risk Management

WC-AA-101-1006

On-Line Risk Management and Assessment

1752367

Overhaul SX Strainer

10/22/2021

23104

Replace 36" Check Valve 2SX002A With a Replacement

Valve

10/22/2021

5195634

FNE Replace Fuse 1BD in Panel 2RD05J

10/13/2021

Work Orders

5199832

Control Rod Drive System Funnel at Penetration No. 55

Almost Disengaged from Head

10/28/2021

4448954

Work Request Needed for Source Range Unit 2 N32

09/27/2021

4452229

As-Found Condition of 2N-NR08032 Replacement Detector

10/11/2021

44544443

03-OSP-A Evaluate Flow Balance for U2 SI Cold Leg

Injection

11/20/2021

4454447

Failed Acceptance Criteria for 2BwOSR 5.5.8SI-11 F.1

10/21/2021

Corrective Action

Documents

4467108

Unexpected Annunciator 2-10-D6 Rod Control Non-Urgent

Failure

2/16/2021

25953

Evaluation of A2R20 SI and CV Flow Balance Results in

Support of TRM TSR 2.5.C.2 and TSR 2.5.C.3

Engineering

Changes

631476

ECCS Performance Analysis of SI Hot Leg Flow Deviation in

A2R21 Documentation of Review of Potentially Affected

Analyses

2BwOSR

5.5.8.SI-11

Comprehensive Testing (IST) Requirements for Unit 2

Safety Injection Pumps and Safety Injection System Check

Valve Stroke Test

CC-AA-309-101

Engineering Technical Evaluations

ER-AA-600-1012

Risk Management Documentation

71111.15

Procedures

OP-AA-106-101-

1006

Operational Decision-Making Process

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-108-111

Adverse Condition Monitoring and Contingency Planning

OP-AA-108-115

Operability Determinations (CM-1)

4649122

OP Safety Injection Cold Leg Check Valve Test

2BwOSR 5.5.8.SI-11

10/10/2021

Work Orders

4840548

Flow Change During 2BwOSR 5.5.8.SI-11

10/13/2018

633170

Unit 1 & 2 Rod Speed Demand Scaling Correction

Engineering

Changes

634332

Perform Weld Overlay for 2B FW Pump Discharge Nozzle

Pup

5106805

Install EC 633170 Unit 2 Rod Speed Demand Scaling

Correction

11/03/2021

71111.18

Work Orders

5111397

2FW78AB-20" A2R22 Capital FAC Piping Replacement

10/23/2021

4458162

2B AF Pump Air Box did not Trip When Expected

11/02/2021

4458258

2AF01PB Diesel Engine

11/03/2021

Corrective Action

Documents

4458282

AF Diesel Air Box Solenoid Replacement PM Testing

UNSAT

10/22/2021

2BwOSR 3.1.6.1

Unit Two ECC Above Control Rod Insertion Limit Startup

Surveillance

2BwOSR

3.6.3.5.AF-1A

Unit Two Train A Auxiliary Feedwater Valve Stroke

Surveillance

2BwOSR 3.7.2.1

Main Steam Isolation Valve Full Stroke Surveillance

2BwOSR

5.5.8.AF-3B

Group A IST Requirements for Unit Two Diesel Driven

Auxiliary Feedwater Pump

BwHS 900-35

Diesel Generator Governor Set-Up Following Governor

Replacement

BwMP 3305-003

Main Steam Safety Valve Testing Using Setpoint Verification

Device

BwOP DG-11

Diesel Generator Startup and Operation

BwOS DG-2

2A Diesel Generator Overspeed Trip Test

BwVS 500-6

Low Power Physics Test Program

Procedures

ER-AA-335-025-

2013

VT-2 Visual Examination in Accordance with ASME 2013

Edition

1737030

Replace Manual Setpoint Control Station

11/03/2021

71111.19

Work Orders

176441

Very Low Flow Identified in 2A AB Tell-Tale Drain Sightglass

11/01/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4635735

2AF006A Replace Actuator with Rebuilt Spare

10/24/2021

4868517

OP PMT - 2AF-14E - 2BwOSR 3.7.5.7-2 (Flow) and Leak

Check

11/02/2021

5039073

Low Power Physics Test Program with Dynamic Rod Worth

Measurement

11/04/2021

5044103

OP Train B AF Flowpath Operability Following Cold

Shutdown

11/02/2021

5044113

IST-2MS001A-D-MSIV Full Stroke

10/18/2021

5058689

Reload Startup Physics Testing Following Refueling

10/20/2021

5085932

LR - OP PMT - 2B AF Pump - Functional Run (ASME)

11/02/2021

5106805

Install EC 633170 Unit 2 Rod Speed Demand Scaling

Correction

11/03/2021

2BwGP 100-1

Plant Heat up

2BwGP 100-2

Plant Startup

2BwGP 100-3

Power Ascension 5% to 100%

2BwGP 100-4

Power Descension

2BwGP 100-5

Plant Shutdown and Cooldown

2BwGP 100-6

Refueling Outage

2BwOS TRM

2.5.b.1

Unit Two - Containment Loose Debris Inspection

BwAP 1450-1

Access to Containment

BwVS TRM

3.1.h.1

Core Reload Sequence and Verification

ER-AA-600-1043

Shutdown Risk Management

HU-AA-1211

Pre-Job Briefings

LS-AA-119

Fatigue Management and Work Hour Rules

MA-AA-716-008-

1008

Reactor Services: Refuel Floor FME Plan

OP-AA-108-108

Unit Restart Review

OP-AA-108-108-

1001

Drywell/Containment Closeout

OP-AA-108-110

Evaluation of Special Tests or Evolutions

71111.20

Procedures

OP-AA-300-1520

Reactivity Management - Fuel Handling, Storage, and

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Refueling

OU-AA-103

Shutdown Safety Management Program

OU-AA-103-1001

Shutdown Safety Plan Independent Review

2BwOSR 3.6.3.7-

Primary Containment Type C Local Leakage Rate Tests of

Containment Purge Exhaust Isolation Valves (VQ)

2BwOSR

5.5.8.AG-4A

Unit Two Comprehensive Inservice Testing (IST)

Requirements for 2A Auxiliary Feedwater Pump

Procedures

BwOP PC-1

Local Leak Rate Flowmeter Monitor Operation

5034477

IST-US Full Flow Test and Equipment Response Time of

Aux FW Pumps

10/15/2021

71111.22

Work Orders

5036717

IST-LT 2VQ002A/B-PRI Containment Type C LLRT of

Containment Purge

10/07/2021

04439827

Radwaste ARGOS Needs Repair

08/10/2021

Corrective Action

Documents

AR 04447933

Plant Shadow Shield Extensions Late

09/22/2021

Procedures

Access Control

for High Radiation

Areas

NISP-RP-005

BW-02-21-00614

Remove/Reinstall Reactor Head/Upper Internals/Flange

Inspection

BW-02-21-00649

Seal Table Room Work

Radiation Work

Permits (RWPs)

BW-02-21-00701

S/G Bowl Drain Installation Removal

AR 04291875-01

Control of Radioactive Material

11/30/2020

71124.01

Self-Assessments

AR 4291877-01

Contamination Control Self-Assessment

11/30/2020

Monthly Data Elements for NRC Radiological Effluent

Technical Specifications/Offsite Dose Calculation Manual

Radiological Effluent Occurrences (RETS/ODCM)

Radiological Effluent Occurrences Sample (08/01/2020 -

09/31/2021)

08/01/2020 -

09/31/2021

Monthly Data Elements for NRC Reactor Coolant System

(RCS) Specific Activity (08/01/2020 - 09/31/2021)

08/01/2020 -

09/31/2021

Miscellaneous

Monthly Data Elements for NRC Occupational Exposure

Control Effectiveness Sample (08/01/2020 - 09/31/2021)

08/01/2020 -

09/31/2021

71151

Procedures

2BwOSR

5.5.8.AF-4B

Unit Two Comprehensive Inservice Testing (IST)

Requirements for 2B Auxiliary Feedwater Pump

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

LS-AA-2001

Collecting and Reporting of NRC Performance Indicator

Data

LS-AA-2100

Monthly Data Elements for NRC Reactor Coolant System

(RCS) Leakage

4183402

2SI8810D Inspection Results FME

10/14/2018

21778

Unexpected Alarms 1-10-A5 and 1-14-A1 for OPDT

05/05/2021

4441987

Unexpected Alarms 1-10-A5 and 1-14-A1 for 1C OPDT

08/22/2021

4455415

Foreign Material Recovered from 2SI8822B/C/D Throttle

Valves

10/25/2021

4455569

2SI8822B As-Found Inspection Unsatisfactory

10/25/2021

4455790

10-OSP-A A2R22 CRDM Thermal Sleeve Metrology VT-1

Exam Results

10/26/2021

4455790

A2R22 CRDM Thermal Sleeve Metrology and VT-1 Exam

Results

10/23/2021

4465938

1C OPDT Setpoint Spiked Low; Unexpected Alarms and

Half-Trip

2/10/2021

Corrective Action

Documents

4470640

Proactive Replacement of Unit 1 7300 NSA Cards

01/07/2022

Corrective Action

Documents

Resulting from

Inspection

4455416

Foreign Material Recovered from 2CV8369A/D Throttle

Valves

10/25/2021

Miscellaneous

Document No.

2-9338475-000

Braidwood Unit 2 CRDM Thermal Sleeve As-Found

Dimensional Report

NDE Reports

180-9338670-000

Braidwood Unit 2 2R22 Thermal Sleeve ID Examination

NO-AA-10

Quality Assurance Topical Report (QATR)

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

71152

Procedures

PI-AA-125-1004

Effectiveness Review Manual

4418688

Source Range Nuclear Instruments Bypassed

04/24/2021

21307

4.0 Critique for A1R22 Start-Up

05/04/2021

71153

Corrective Action

Documents

4430406

Multiple MCR Alarms Received Due to Adverse Weather

06/20/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4430440

Indication Lost for 1MS-147A Following Unit 1 Reactor Trip

06/21/2021

4430441

Unit 1 Reactor Trip - Load Reject

06/21/2021

4430442

Unexpected Annunciator: 1-4-D5

06/21/2021

4430444

1A/D MSIV Room Fire Alarm Following Reactor Trip

06/21/2021

4430446

N35 and N36 Appear to be Undercompensated

06/21/2021

4430586

4.0 Critique Unit 1 Reactor Trip Due to Generator Load

Reject

06/21/2021

4430895

Need WO Generated for Testing Station Site Grounding

System

06/22/2021

4432865

Braidwood Site Ground Testing

07/01/2021

Engineering

Changes

DIT-BRW-2021-

0009

A1R22 Reactor Coolant System Boron Samples

06/07/2021

Operations

Standing Order

No.21-002

Actions to Ensure Operational Excellence Following A1R22

04/23/2021

Miscellaneous

Operations

Standing Order

No.21-003

Actions to Refocus on Operating Fundamentals

04/24/2021

BwAR 1-10-D1

Source Range Trip Bypassed

51E1

BwOP RP-9

Disabling and Restoring Source Range Nuclear Instruments

Procedures

HU-AA-1211

Pre-Job Briefings

14