IR 05000456/2022011

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Biennial Problem Identification and Resolution Inspection Report 05000456/2022011 and 05000457/2022011
ML22201A227
Person / Time
Site: Braidwood  
Issue date: 07/20/2022
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022011
Download: ML22201A227 (15)


Text

SUBJECT:

BRAIDWOOD STATION - BIENNIAL PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000456/2022011 AND 05000457/2022011

Dear Mr. Rhoades:

On June 29, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your Braidwood Station and discussed the results of this inspection with Mr. James Petty, Plant Manager, and other members of your staff. The results of this inspection are documented in the enclosed report.

The NRC inspection team reviewed the stations problem identification and resolution program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for problem identification and resolution programs.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information, and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews the team found no evidence of challenges to your organizations safety-conscious work environment. Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

July 20, 2022 No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2022011 and 05000457/2022011

Enterprise Identifier:

I-2022-011-0038

Licensee:

Constellation Energy Generation, LLC

Facility:

Braidwood Station

Location:

Braceville, IL

Inspection Dates:

June 06, 2022 to June 29, 2022

Inspectors:

A. Demeter, Resident Inspector

D. Kimble, Senior Resident Inspector

A. Muneeruddin, Resident Inspector

N. Shah, Project Engineer

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a biennial problem identification and resolution inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

OTHER ACTIVITIES - BASELINE

71152B - Problem Identification and Resolution Biennial Team Inspection (IP Section 03.04)

(1) The inspectors performed a biennial assessment of the effectiveness of the licensees Problem Identification and Resolution program, use of operating experience, self-assessments and audits, and safety-conscious work environment.

Problem Identification and Resolution Effectiveness: The inspectors assessed the effectiveness of the licensees Problem Identification and Resolution program in identifying, prioritizing, evaluating, and correcting problems. The inspectors also conducted a five-year review of the Unit 1 and 2 heating, ventilation, and air conditioning (HVAC) Chillers.

Operating Experience: The inspectors assessed the effectiveness of the licensees processes for use of operating experience.

Self-Assessments and Audits: The inspectors assessed the effectiveness of the licensees identification and correction of problems identified through audits and self-assessments.

Safety-Conscious Work Environment: The inspectors assessed the effectiveness of the stations programs to establish and maintain a safety-conscious work environment.

INSPECTION RESULTS

Assessment 71152B Assessment of the Corrective Action Program Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

No violations or findings were identified.

Effectiveness of Problem Identification Overall, the station was effective at identifying issues at a low threshold and was properly entering them into the corrective action program (CAP) as required by station procedures.

During interviews, workers were familiar with how to enter issues into the CAP and stated that they were encouraged to use it to document issues. During plant walkdowns, the team observed numerous action tags, indicating that workers were identifying issues in the field. A selective review of several of these action tags verified that these issues were being properly documented in the CAP. The team determined that the station was generally effective at identifying negative trends that could potentially impact nuclear safety. For the areas reviewed, the team did not identify any issues in problem identification.

Effectiveness of Prioritization and Evaluation of Issues In-depth reviews of a risk-informed sampling of issue reports (IRs), work orders (WOs), and root and apparent cause and condition evaluations were completed. The team determined that the licensee had established a low threshold for entering deficiencies into the CAP, that the issues were generally being appropriately prioritized and evaluated for resolution, and that corrective actions (CAs) were implemented to mitigate the future risk of issues occurring that could affect overall system operability and/or reliability.

The inspectors noted that issues were properly screened with most either classified as Conditions Adverse to Quality (CAQ) or Non-Corrective Action Program (NCAP) items.

Through a selective review of CAP and NCAP items, the inspectors found no issues either with the assigned level of evaluation or the proposed corrective actions. Issues having potential operability concerns were properly addressed through the screening process and during control room observations and accompaniment of non-licensed operators during daily rounds, the inspectors did not identify any significant operator workarounds or similar deficiencies.

The inspectors also did a selective review of issues identified by the NRC either documented as observations or for which findings or other enforcement was issued. These issues were properly documented and screened in the CAP.

Issue evaluations were generally sound and of good quality. Most issues were screened as low significance and were assigned a work group evaluation (the lowest level of review);more significant issues were assigned a Corrective Action Program Evaluation or if highly significant, a root cause evaluation. The inspectors verified that the assigned evaluations were consistent with the significance of the issue as defined in the licensees process.

Effectiveness of Corrective Actions The team concluded that the licensee was generally effective in developing CAs that were appropriately focused to correct the identified problem and to address the root and contributing causes for significant conditions adverse to quality to preclude repetition. The licensee generally completed CAs in a timely manner and in accordance with procedural requirements commensurate with the safety significance of the issue. For NRC-identified issues, the team determined that the licensee generally assigned CAs that were effective and timely. The inspectors also did a selective review of CAs that were still open at least two years after the issue was identified to verify that it was appropriate for these items to remain open and that the licensee was managing them correctly; no issues were identified.

The inspectors noted that while issue evaluations were generally sound, there were several examples where additional research was needed to verify that the appropriate corrective actions were taken, primarily due to a lack of clear documentation. This theme had previously been identified in earlier licensee self-assessments and CAP audits, and several recent CAP items had been written to address this issue. These CAPs were still open; however, the inspector determined the proposed corrective actions were adequate.

Assessment 71152B Five-Year Review of Units 1 and 2 Heating, Ventilation, and Air Conditioning System Chillers The inspectors performed an expanded 5-year review of the Units 1 and 2 heating, ventilation and air conditioning (HVAC) chillers; specifically, by performing system walkdowns, evaluating condition reports and work orders. The inspectors also interviewed personnel responsible for working on the system. Overall, the inspectors determined that the licensee was effectively managing issues associated with this system.

Since 2017, the licensee has observed challenges in the operation of Unit 1 and 2 HVAC chillers. Frequently observed issues by the licensee dealt with the guide vanes, divider plate gaskets, out of band oil level, and various trips throughout this time period. These issues were documented in the CAP and the NRC resident inspectors have been reviewing them through the baseline inspection program. The inspectors identified no operability or other immediate safety concerns with these issues and concluded that the licensee had taken proactive actions to find and correct the cause of these issues.

No violations or findings were identified.

Assessment 71152B Assessment of Operating Experience and Self-Assessment and Audits Based on the samples reviewed, the team determined that licensee performance in the use of Operating Experience (OE) and Self-Assessments and Audits adequately supported nuclear safety.

No violations or findings were identified.

Use of Operating Experience The licensee routinely screened industry and NRC OE information for station applicability.

Based on these initial screenings, the licensee-initiated actions in the CAP to fully evaluate the impact, if any, to the station. When applicable, actions were developed and implemented in a timely manner to prevent similar issues from occurring. During interviews, licensee staff stated that operating experience lessons-learned were communicated during work briefings and department meetings and incorporated into plant operations.

Self-Assessments and Audits The inspectors reviewed several audits and self-assessments and deemed those sampled as thorough and intrusive with regards to following up with the issues that were identified through previous NRC inspections, and in the self-assessments and fleet oversight audits.

Reviewed corrective actions for the identified issues were deemed reasonable and completed commensurate with their safety significance. The inspectors regarded licensee performance as adequately self-critical of their own performance and that performance-related issues were being identified through their self-assessment process.

Assessment 71152B Assessment of Safety-Conscious Work Environment The team reviewed the stations programs to establish and maintain a safety-conscious work environment and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, workers at the station expressed freedom to raise and enter safety concerns through any one of the various avenues available to them, and the team encountered no indications of chilling or retaliation.

During interviews, some staff expressed concerns about workload and staffing primarily due to effects from the ongoing COVID epidemic. This same issue was also identified by the licensee during recent safety culture assessments, and actions were being taken to increase staffing and manage the workload. The interviewees acknowledged these efforts and generally stated that management was taking steps to address the issue. Additionally, none of the interviewees expressed any safety culture concerns from this issue. Employees consistently communicated the belief that sufficient competency, engagement, resources, and commitment exist at the station to maintain high performance standards at the site.

Workers expressed favorable opinions of the Employee Concerns Program (ECP) during interviews, but not all workers were familiar with how to raise issues through the ECP, specifically, who to contact on-site. The site ECP representative had recently resigned and in the interim, the function was being fulfilled by the corporate ECP manager, who was only on-site periodically. Although there were several signs posted with the name and contact info of the corporate ECP representative, this information was apparently not well known by the interviewees. The inspectors noted that issues were still being identified by the ECP and that most workers felt no need to approach the ECP. The inspectors reviewed those issues documented in the ECP over the previous two years and identified no adverse trends.

Overall, inspectors found no evidence of challenges to the licensee's safety-conscious work environment, as licensee employees were willing to raise nuclear safety concerns through at least one of several means available.

No violations or findings were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On June 29, 2022, the inspectors presented the biennial problem identification and resolution inspection results to Mr. James Petty, Plant Manager, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

1451512

Unit 2 Core Exit Thermocouple, Nozzle 77 Connections

Swapped Affecting Indications

2/12/2012

2448240-03

Westinghouse NSAL 15-1 FQ(z) Tech Spec Surveillance

2/05/2015

4033543

Fuel Pool Temperature Exceeding Rounds Setpoint

07/20/2017

4194578

Unit 0 Instrument Air Dryer Trouble, 0BWOA SEC-4 Entry

11/13/2018

4195675

Instrument Air Dryer Vulnerability

11/16/2018

217180

Part 21 Deviation of Switches (SOR)-EN 53856

2/04/2019

27719

04-OSP-A 2C Hot Leg Flow Out-of-Tolerance Low During

2BwOSR 5.5.8.SI-11

04/22/2020

235265

Potential Deficiency in Emergency Preparedness Scenario

03/05/2019

280416

Entry into 0/1/2BwOA SEC-04

09/18/2019

4307603

NRC Special Inspection-Cooper Essential Service Water

Inoperable due to Silt Buildup

01/02/2020

4307925

Follow-up Inspection of Power Take Off Coupling-Auxiliary

Feedwater Diesel 1AF01PM

01/03/2020

4309449

SIF-Foreign Material Exclusion Practices

01/10/2020

4309728

1FW035B Stroke Time Exceeded Operability Limits

01/13/2020

4314287

Level 3 OPEX Review Request for Clinton ABB 27N Relays

OOT

01/31/2020

4315003

2A VP Chiller Evap Missing 1 ft of Divider Plate Gasket

01/28/2020

4315005

2A VP Chiller Condenser Missing 10 in of Divider Plate Gasket

01/28/2020

4316542

Roll up of NOS Maintenance Audit Deficiencies

2/10/2020

4316631

INPO Significant Event Unintentional Draining Reactor Cavity

2/10/2020

4319985

Self-Assessment-2020 Nuclear Oversight Audit of the

Employee Concerns Program

3/12/2020

23077

2A Station Air Compressor Implementation Delays

03/02/2020

25067

Corrective Action Program Evaluation Following Inaccurate

Identification of Release Path During the March 3, 2020,

Braidwood NRC Graded Exercise

04/06/2020

26961

Leakage (Dry LCS-60) at Packing on 2CC9489A

03/16/2020

71152B

Corrective Action

Documents

28788

CFR Part 21 Notice on the Rosemont 1150 and 3150

Transmitters

03/23/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4335846

2MS016A - Pre-A2R21 Testing As-Found Outside of

Acceptance Range

04/15/2020

4338581

2A VP Chiller Drain Back Solenoid Stuck Open

04/17/2020

4348893

OIO Benchmark-Effluent Calculations

06/08/2020

4353381-02

Midcycle GTE: MA. 1-17/LE.1-e/TE.5-d

06/26/2020

4355375

Spent Fuel Pool Temperature Above Rounds Limit - Trend

Only

07/08//2020

4355832

Unexpected Alarm 1-1-A2, Cnmt Drain Leak Detect Flow High

07/09/2020

4361295

Unit 0 Station Air Compressor Outboard Motor Bearing Oil Is

Discolored

08/05/2020

4362232

Unexpected Annunciator 1-15-D4 SG 1D Flow Mismatch

08/10/2020

4366140

Unexpected Alarm 1-1-A2 Cnmt Drain Leak Detect Flow High

08/29/2020

4368131

Industry Scram: Catawba Human Error Over Power Delta T

09/08/2020

4369686

NRC IN 2020-02 - Flex Diesel Operational Challenges

09/15/2020

4370636

Unexpected Alarm 2-22-C8: 2B Diesel Generator Control

Power Failure

09/19/2020

4374128

P2301 Indication Suspect

01/22/2021

4375974

2MP01E TMS Warning Light is Lit

10/12/2020

4376375

Trend in TMS Alarms

10/13/2020

4382448

Unexpected Alarms - 0-28-C4 and D4, RSH Air System

Alarms

11/05/2020

4387762

0A VC Chiller Trip

2/02/2020

4389024

U1 RCS Leak Rate Trend

01/08/2021

4389421

3Q20 NRC LIV - 0B VC Chiller Issues (Ref. IR 4321449)

2/10/2020

4391803

NRC Information Notice 2020-04 Fire Protection Maintenance

Yard Buried Cast Iron Pipe Failures

2/23/2020

4399254

4Q20 NRC Level IV NCV on MPC Blowdown Event

(Ref IR 4364058)

01/31/2021

4399255

4Q20 NRC NCV on Main Steam Safety Valve Lift Setpoint

Issue (Ref IR 4335846)

01/31/2021

4402949

Self-Assessment: Operator Fundamentals

2/17/2021

4416082

1Sl8842 Failed Relief Valve Testing

04/13/2021

4417141

2-OSP-A 1RD02E Coupling Damaged & Will Need to be

04/16/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Replaced

4417966

18-OSP-R CETC #19 (C-12) Reading High

04/21/2021

4418449

U1 CETC Information Update Following Outage Repairs

04/22/2021

4418688

Level 3 Configuration Control: Source Range Nuclear

Instruments (SRNIs) Required Trip Function Bypassed

04/24/2021

4418835

1BWOS TRM 3.3.H.1 Failed Symmetric CETC Temperature

Limits

04/25/2021

4419609

U1 CETC, Nozzle 74 Connections Swapped Affecting

Indications

04/28/2021

21660

2-10-C6 Rod Control Urgent Failure, SER#2165

05/05/2021

23455

Support Activities for EC 634192 CETC Train Swap at Pen 74

05/13/2021

24250

U1 CETC, Nozzle 74 Connections Swapped Affecting

Indications

05/18/2021

27164

2W MPT WO Needed to Support SCFR Action

06/02/2021

4430441

U1 Automatic Reactor Trip due to Generator Load Reject

06/21/2021

4430441

Root Cause Investigation Report for Braidwood Unit 1 Reactor

Trip on Generator Load Rejection

08/02/2021

4432865

Braidwood Site Ground Testing Following Unit 1 Trip due to

Lightning Strike in Switchyard

07/01/2021

4433415

Corrective Action Program Evaluation for Foreign Material

Recovered from Unit Two SI8822B/C/D Throttle Valves

2/11/2022

4435859

NOSA-BRW-21-05 Corrective Action Program Audit Report

08/27/2021

4437157

2Q21 NRC Obs. Trend U1 MSIV Bypass Valve Ops

Ref IR 4428897

07/27/2021

4440617

Unexpected BwAR 1-10-C3 Power Range Flux Rate Trip Alert

for N41

01/14/2022

4440852

NRC Information Notice 2020-04 Fire Protection Maintenance

Yard Buried Cast Iron Piping Failures

2/23/2020

4440852

NRC Information Notice 2021-03 Operating Experience on

Duane Arnold Derecho

08/16/2021

4440914

NERC: PRC-019 R2 Coordination Verification

05/14/2021

4443522

2A Diesel Generator Bolt on 4L Cylinder Sheared During

Scheduled Run

08/30/2021

4445827

1MS101C Failed to Open During Position Indication Test (PIT)

09/11/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4455045

Need Work Request for 2A Emergency Diesel Generator

Manifold

10/23/2021

4455415

FM Recovered from 2SI8822B/C/D Throttle Valves

10/25/2021

4456561

Foreign Material Exclusion: Foreign Material Found in 2B

Steam Generator Secondary Side-A2R22

10/28/2021

4458973

U2 CETC, Nozzle 74 Connections Swapped Affecting

Indication

11/05/2021

4459657

Support Activities for EC 635519 CETC Train Swap at Pen 74

11/09/2021

4465956

22 Pre-PI&R Inspection Self-Assessment

06/24/2022

4473438

Unexpected Annunciator 0-38-A2 SAC 1A Trip

01/23/2022

4473444

U2 SAC Trip After Start. Continuation of IR# 4473438.

01/23/2022

4474052

Level 3 Config Control: Incorrect Connection of Test

Equipment

01/26/2022

4477450

4Q21 NRC Observation - CRDM Thermal Sleeves

(Ref IR 4455790)

2/11/2022

4479173

Nuclear Oversight Finding: The Measurement and Test

Equipment Program was not Adequately Implemented

2/18/2022

4481238

A Level 3 Operating Experience Review is Warranted for

IRIS 514499

2/28/2022

4483946

0B VC Chiller Lowering Oil Trend and Refrig Recommendation

03/10/2022

4484304

VA/VC Filters Information Obtained

03/11/2022

4504131

2MP02E Warning Light Lit

06/07/2022

4504501

Steam Leak Under U2 Dawghouse

06/08/2022

4504849

22 PI&R: MA Excellence Standards Improvement

Opportunity

06/10/2022

4506106

22 PI&R: Preliminary OPEX Review Improvement

Opportunity

06/17/2022

Corrective Action

Documents

Resulting from

Inspection

4506856

22 PI&R: SA Completed Without Creation of Actions

06/22/2022

Engineering

Changes

636627

Configuration Control Processing of Design Analysis 051853,

Rev. 005M, for Evaluation of the Structural Integrity of Line

0SX03A-30" per Code Case N-513-4, Considering the Through

Wall Leakage Identified

000

Engineering

Evaluations

631400

Unit 2 Main Steam Safety Valves As-Found Lift Setpoint

Evaluation for Pre-A2R21 Testing

Revision 0

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

631485

Lost Parts Evaluation for Foreign Materials in Safety Injection

Hot Leg 2SI8816C - A2R21

Revision 0

631492

Evaluation of Running Unit 2 One Cycle with the 2MS014B and

2MS016C Valves Not Rebuilt

Revision 0

CPA - Compressed Air Engage Health Report

06/08/2022

Braidwood Nuclear Safety Culture Committee Meeting Minutes

05/20/2022

Braidwood Nuclear Safety Culture Committee Meeting Minutes

01/31/2022

Emergent Braidwood Nuclear Safety Culture Committee

Meeting Minutes

08/25/2021

BRWD SA-11 (A)(1) Determination

11/20/2019

051853

Design Analysis and Piping Stress Report for the Essential

Service Water System (Subsystem 1SX02)

005M

IN 2020-02

FLEX Diesel Generator Operational Challenges

09/15/2020

IN 2021-03

Operating Experience Related to the Duane Arnold Energy

Center Derecho Event on August 10, 2020

08/11/2021

IRIS Experience

Report 460761

Unplanned Decrease in Reactor Cavity Level During

Decontamination Activities

05/17/2019

IRIS Experience

Report 485806

Overpower Delta Temperature Human Performance-Related

Reactor Trip

09/08/2020

LER 2020-001-00

Licensee Event Report 2020-001-00: The Unit 1 Train A

Auxiliary Feedwater Pump was Inoperable Due to a Failed

Suction Pressure Lead/Lag Card

11/25/2020

LER 2021-001-00

Train A and B Source Range Neutron Flux Trip Functions

Bypassed During Plant Startup

06/21/2021

Miscellaneous

LER 2021-002-00

Licensee Event Report 2021-002-00 - Unit Trip on Generator

Load Rejection Due to Lightning Strick Within the Unit

Switchyard Exceeding the Capabilities of the Switchyard

Grounding System

08/18/2021

NDE Reports

BRW-41029

Exelon PowerLabs On-Site Material Identification of Debris

from SI System

04/28/2020

BwOP RC-4

Reactor Coolant System Drain

OP-AA-108-111

Adverse Condition Monitoring and Contingency Plan for SX

leak on Unit 0 CC HX (0SX03A)

Procedures

PI-AA-115

Operating Experience Program

Revision 5

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

PI-AA-115-1003

Level 3 OpEx Evaluation for NRC IN 2021-03: Duane Arnold

Derecho Event

11/05/2021

PI-AA-115-1003

Operating Experience Related to Unplanned Decrease in

Reactor Level During Decontamination Activities

09/23/2021

PI-AA-115-1003

Level 3 OpEx Evaluation for Catawba Scram

10/09/2020

PI-AA-115-1003

Operating Experience Related to FLEX Diesel Generator

Operational Challenges

03/03/2020

PI-AA-120

Issue Identification and Screening Process

Revision 11

04327092-02

Braidwood Operations Training Objective 1 and Simulator

Compliance Self-Assessment

08/03/2020

4333108-03

21 FME Program Health

01/25/2021

4363689-03

Freon Management, Ozone Depleting Substances, Refrigerant

Program

09/29/2021

4375038-03

Station Leak Reduction

01/28/2021

4402105

21 ISM Self-Assessment Discrepancies

2/12/2021

Self-Assessments

4402949-04

Braidwood Operator Fundamentals

05/31/2021

256109-01

Day Periodic Non-Destructive Testing of 0SX03A to Monitor

the Growth of the Through Wall Flax Identified on 0SX03A per

IR 04494801

05/19/2022

Work Orders

264068-01

Day Periodic Non-Destructive Testing of 0SX03A to Monitor

the Growth of the Through Wall Flax Identified on 0SX03A per

IR 04494801

06/17/2022