IR 05000456/2022002

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Integrated Inspection Report 05000456/2022002; 05000457/2022002; and 07200073/2022001
ML22206A235
Person / Time
Site: Braidwood  
Issue date: 07/26/2022
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Constellation Energy Generation, Constellation Nuclear
References
IR 2022002
Download: ML22206A235 (24)


Text

SUBJECT:

BRAIDWOOD STATION - INTEGRATED INSPECTION REPORT 05000456/2022002; 05000457/2022002; AND 07200073/2022001

Dear Mr. Rhoades:

On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station. On July 15, 2022, the NRC inspectors discussed the results of this inspection with Mr. G. Gugle, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000456; 05000457; and 07200073 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456; 05000457; and 07200073

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2022002; 05000457/2022002; and 07200073/2022001

Enterprise Identifier:

I-2022-002-0044 and I-2022-001-0100

Licensee:

Constellation Energy Generation, LLC

Facility:

Braidwood Station

Location:

Braceville, IL

Inspection Dates:

April 01, 2022 to June 30, 2022

Inspectors:

R. Bowen, Illinois Emergency Management Agency

A. Demeter, Acting Resident Inspector

G. Edwards, Health Physicist

D. Kimble, Senior Resident Inspector

J. Masse, Reactor Engineer

P. Smagacz, Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 and Unit 2 began the inspection period operating at full power. With the exception of short duration reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, both units remained operating at or near full power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated the station's offsite and alternate alternating current (AC)power systems for summer readiness and the onset of hot weather during the weeks ending May 21 through June 4, 2022.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated system configurations during partial physical alignment verifications of the following systems/trains:

(1) The 1B Emergency Diesel Generator (EDG) during 1A EDG maintenance during the week ending April 16, 2022
(2) The 2B Residual Heat Removal (RH) Train during 2A RH Train maintenance during the week ending May 5, 2022
(3) Unit 1 and Unit 2, Division 1, direct current (DC) power while protected during an extended Unit 1 Station Auxiliary Transformer (SAT) maintenance window during the week ending May 14, 2022
(4) Unit 1 EDGs while protected during an extended Unit 1 SAT maintenance window during the week ending May 14,2022
(5) The 2B Auxiliary Feedwater (AF) Train while protected during an extended Unit 1 SAT maintenance window during the week ending May 14, 2022

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated the following licensed operator activities in the control room:

(1) Various activities involving on-watch operations crews. These activities included, but were not limited to:

Unit 1 power maneuvering in response to the system transmission dispatcher, during the week ending April 30, 2022.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated the following licensed operator training activity:

(1) A complex casualty graded scenario involving a crew of licensed operators was observed in facility's simulator on June 11, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Maintenance effectiveness review associated with leakage from the Unit 1 Charging and Letdown Regenerative Heat Exchanger Return to the Reactor Coolant System (RCS) Manual Isolation Valve (1CV-8321A) during the weeks ending April 23 through June 25, 2022.
(2) Maintenance effectiveness review associated with EDG local annunciator panel power supplies during the week ending April 23, 2022.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluation of the emergent work associated with the 2B EDG annunciator panel, as documented in Issue Report (IR) 4490289 during the week ending April 9, 2022.
(2) Evaluation of the planned work associated with 1A EDG, as documented in Work Order (WO) 4901183 during the week ending April 16, 2022.
(3) Evaluation of the emergency activities associated with a leak from a welded joint on the Unit 0 Component Cooling (CC) Heat Exchanger Essential Service Water (SX)

Outlet, as documented in IR 4494801 and WO 5252064 during the weeks ending April 23 through April 30, 2022.

(4) Evaluation of the emergent activities associated with the loss of local alarm annunciators for the 2A EDG, as documented in IR 4493589 and 5249849 during the week ending April 23, 2022.
(5) Evaluation of the work associated with the Unit 1 SAT maintenance window utilizing a planned Technical Specification Risk-Informed Completion Time (TS RICT), as documented in multiple WOs during the week ending May 14, 2022.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Evaluation of the operability of the 1B EDG following identification of a crack in the jacket water cooling manifold, as documented in IR 4492197 during the week ending April 16, 2022.
(2) Evaluation of the functionality of the Unit 2 Rod Drive System following identification of a degraded power supply, as documented in IR 4471553 during the week ending May 28, 2022.
(3) Evaluation of the operability of the Unit 0 CC Heat Exchanger following identification of a leak through a welded joint on the SX outlet of the heat exchanger, as documented in IR 4494801 during the week ending June 4, 2022.
(4) Evaluation of the operability of the 0B Control Room Chiller (VC) following identification of a degraded chiller oil level, as documented in IR 4505042 during the weeks ending June 25 through June 30, 2022.

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary configuration change on Unit 2:

(1) A temporary plant modification per Engineering Change (EC) 635793: Install Temporary Power Supply in 2RD033, during the weeks ending May 21 through May 28, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and functionality:

(1) Non-destructive testing on the SX side of the Unit 0 CC Heat Exchanger following analysis and evaluation of a leak through a welded joint, as documented in WO 5253243 during the week ending May 21, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities:

Surveillance Tests (other) (IP Section 03.01)

(1) BwISR 3.3.1.6-004: Quarterly Excore Power Range N44 Axial Flux/7300 Delta Flux Penalty Calibration, as documented in WO 5242877 during the weeks ending June 11 through June 18, 2022

FLEX Testing (IP Section 03.02) (1 Sample)

(1)0BwOS FX-12: FLEX Pump Full Flow Test Surveillance, as documented in WOs 5011598 and 5013180 during the weeks ending June 18 through June 25, 2022

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (2 Samples)

The inspectors evaluated site's emergency plan by observing the following emergency response organization (ERO) activities:

(1) A site-wide emergency preparedness drill that resulted in a simulated General Emergency event classification on May 18, 2022
(2) A site-wide emergency preparedness drill that resulted in a simulated General Emergency event classification on June 1,

RADIATION SAFETY

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation systems:

(1) Fuel Handling Building ventilation systems

Use of Respiratory Protection Devices (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the licensees use of respiratory protection devices

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1) The inspectors evaluated the licensees use and maintenance of self-contained breathing apparatuses

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated licensee performance as it pertains to radioactive source term characterization

External Dosimetry (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated how the licensee processes, stores, and uses external dosimetry

Internal Dosimetry (IP Section 03.03) (2 Samples)

The inspectors evaluated the following internal dose assessments:

(1) Internal dose assessment conducted for an individual reporting onsite that had previously reported having an intake at another facility conducted on October 20, 2021
(2) Internal dose assessment conducted for an individual who was hanging shielding during a valve repair on February 9, 2021

Special Dosimetric Situations (IP Section 03.04) (2 Samples)

The inspectors evaluated the following special dosimetric situations:

(1) Dose assessment for a declared pregnant worker in 2021
(2) Dose assessment for a declared pregnant worker in 2022

71124.05 - Radiation Monitoring Instrumentation

Walkdowns and Observations (IP Section 03.01) (5 Samples)

The inspectors evaluated the following radiation detection instrumentation during plant walkdowns:

(1) Area Radiation Monitors in auxiliary building
(2) Area Radiation Monitors in the fuel handling building
(3) Friskers used at the exit to the auxiliary building
(4) Portable ion chambers stored ready for use and/or during use at the Radiation Protection checkpoint at the auxiliary building entrance
(5) Portable ion chambers stored ready for use and/or during use in the Radiation Protection instrument room in the auxiliary building

Calibration and Testing Program (IP Section 03.02) (10 Samples)

The inspectors evaluated the calibration and testing of the following radiation detection instruments:

(1) Thermo Scientific PM12; SN #12084
(2) Bicron RSO-50E; SN #C613F
(3) Thermo Scientific SAM12; SN #235A
(4) Mirion Telepole II; SN #0019520
(5) Mirion Argos 5; SN #1011-279
(6) Ludlum Model 30; SN #26144
(7) Ludlum Model 12-4; SN #336338
(8) Thermo Scientific PM12; SN #12060
(9) Thermo Scientific PM12; SN #12082
(10) Mirion RDS-31; SN #2B.106 Effluent Monitoring Calibration and Testing Program Sample (IP Sample 03.03) (2 Samples)

The inspectors evaluated the calibration and maintenance of the following radioactive effluent monitoring and measurement instrumentation:

(1) Auxiliary building ventilation stack effluent stack monitor, 1PRJ28
(2) Station blowdown line liquid effluent radiation monitor, 0R-PR010

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors reviewed and verified selected portions of the licensee's performance indicator submittals listed below:

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===

(1) Unit 1 (April 1, 2021 - March 31, 2022)
(2) Unit 2 (April 1, 2021 - March 31, 2022)

MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)

(1) Unit 1 (April 1, 2021 - March 31, 2022)
(2) Unit 2 (April 1, 2021 - March 31, 2022)

MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)

(1) Unit 1 (April 1, 2021 - March 31, 2022)
(2) Unit 2 (April 1, 2021 - March 31, 2022)

71152A - Annual Follow-Up Problem Identification and Resolution Annual Follow-Up of Selected Issues (Section 03.03)

The inspectors conducted an in-depth review of the licensees implementation of the corrective action program (CAP) related to the following issue:

(1) Review and assessment of the station's corrective actions from a Unit 2 configuration control event where a pressure test signal was applied to the incorrect instrument loop, as documented in IR 4474052 during the weeks ending April 2 through June 30, 2022.

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02)

(1) The inspectors conducted a semiannual review of the licensees CAP for potential adverse trends that might be indicative of a more significant safety concern during the weeks ending June 4 through June 30, 2022. A specific trend related to Reactor Vessel Level Indication System (RVLIS) issues is documented in the Results Section of this report.

OTHER ACTIVITIES

- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL

60855 - Operation of an ISFSI Operation of an ISFSI

(1) The inspectors assessed the licensees Independent Spent Fuel Storage Installation (ISFSI) cask loading activities from May 16 through May 20, 2022. Specifically, the inspectors observed the following activities during the loading of multi-purpose canister (MPC) No. 676:
  • heavy lift of the loaded transfer cask (HI-TRAC) from the spent fuel pool to the cask processing area
  • closure welding and non-destructive evaluations
  • canister processing including blowdown and forced helium dehydration
  • stack-up and download of the MPC from the HI-TRAC into the storage cask (HI-STORM)
  • radiological field surveys

The inspectors performed walkdowns of the ISFSI pad, including walkdowns of the ISFSI haul path.

The inspectors evaluated the following:

  • spent fuel selected for loading into dry cask storage during this loading campaign
  • selected corrective action program documents
  • selected 72.48 screenings and evaluations

INSPECTION RESULTS

Observation: Test Signal Inadvertently Applied to the Incorrect Instrument Loop 71152A The inspectors performed a detailed review of IR 4474052, Level 3 Configuration Control:

Incorrect Connection of Test Equipment. The issue involved Instrument Maintenance Department (IMD) calibration procedure BwIP 2P-0120, Calibration of Charging Header Pressure Loop 2P-0120 (CV), which was performed under Work Order (WO) 5063738, 2P-0120 Charging Header Pressure Loop. On January 26, 2022, IMD technicians performing this calibration activity were prompted to change out their test signal equipment partway through the procedure due to a low battery indication. Despite the use of robust barriers within the applicable 2PA06J instrumentation cabinet intended to prevent such an error, the IMD technicians connected the replacement test signal equipment to test connection points associated with the Unit 2 Volume Control Tank (VCT) pressure instrument loop, vice the intended 2P-0120 Charging Header Pressure instrument loop. When the test signal was subsequently applied, Unit 2 operators in the main control room were forced to respond to invalid VCT pressure indications and took steps to stabilize VCT pressure.

The inspectors chose this issue for an in-depth review of the licensees actions within their corrective action program (CAP) because of the inherent risk associated with wrong unit /

wrong component manipulations. While in this particular case the wrong component error did not result in any significant adverse impact to the applicable unit, such an error could have resulted in a significant plant transient or unintended automatic equipment actuation.

Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensees corrective actions taken both for this specific error, as well as those targeted at the more generic issue of addressing potential wrong unit / wrong component errors.

The inspectors determined that the erroneous connection of the IMD test signal equipment to test connection points associated with the Unit 2 VCT pressure instrument loop, vice the intended 2P-0120 Charging Header Pressure instrument loop on January 26, 2022, had constituted a violation of the requirements of TS 5.4.1(a), which requires that written procedures be established, implemented, and maintained for the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. In this case, Section 8.a of Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, contains the requirement for procedures associated with instrument calibrations, and licensee procedure BwIP 2P-0120, Calibration of Charging Header Pressure Loop 2P-0120 (CV),

Revision 1, is an applicable procedure. Section 4.1, Test Setup, of this procedure directs that the IMD test equipment is to be connected to Terminals TBF-7 and TBF-8 in Cabinet 2PA06J to facilitate calibration of the Charging Header Pressure Loop 2P-0120. Contrary to these instructions, the IMD test signal equipment was connected to Terminals TBF-1 and TBF-2 in Cabinet 2PA06J. However, because there were no safety consequences associated with this event, the inspectors concluded that the error had not adversely affected the Initiating Events Cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. As a result, the issue was determined to be a violation of minor significance that was not subject to formal actions per Section 2.3.1 of the NRC Enforcement Policy.

The inspectors did not identify any issues with the licensees CAP actions taken. The licensees formal CAP evaluation revealed that human performance failures had occurred at multiple times during the calibration. Subsequent interviews performed with station supervisors and technicians revealed that multiple interpretations of standards and expectations existed with respect to the use of several human performance tools. Multiple corrective actions targeting this aspect of the event were implemented by the licensee; these included the reinforcement of standards and expectations by plant management with shop superintendents regarding the use of human performance tools, peer-to-peer coaching, and supervisory oversight in the field.

No findings or violations of NRC requirements of more than minor safety significance were identified by the inspectors in the course of this review.

Observation: Trend in Reactor Vessel Level Indication System (RVLIS) Issues 71152S The inspectors performed a review of plant issues, particularly those entered into the licensees CAP over the past several months. During their review, the inspectors noted an adverse trend involving the performance of the Reactor Vessel Level Indication System (RVLIS). The majority of issues were on Unit 1, but the inspectors noted that the trend was not exclusive to only that unit. Specific CAP entries reviewed by the inspectors included, but were not limited to:

- IR 4442055; 1-9-D6 - Unexpected Main Control Room Alarm - RVLIS Sensor Uncovered.

- IR 4442887; 1-9-D6 - Unexpected Main Control Room Alarm - RVLIS Sensor Uncovered.

- IR 4450389; Unexpected Main Control Room Alarm - RVLIS Sensor/Core Exit Thermocouple (CETC) Failure.

- IR 4472056; Alarm 2-9-D6 - RVLIS Level Sensor 7B Erratic.

- IR 4482013; 1-9-D6, RVLIS Sensor Uncovered, Sensor 6A (Plenum 27%).

- IR 4488602; Unexpected Alarm on Unit One A-Train RVLIS.

- IR 4508584; Unexpected Alarm 1-9-D6, RVLIS Sensor Uncovered, Sensor 3A.

The Reactor Vessel Level Indication System is described in Appendix E, Requirements Resulting from the Three Mile Island 2 Accident, of the stations Updated Final Safety Analysis Report (UFSAR) as part of a system of instrumentation used to detect inadequate core cooling (ICC) during significant accident scenarios. Operability requirements for RVLIS in operational Modes 1, 2, and 3 are set forth in Section 3.3.3 of the stations Technical Specifications (TS). The Bases for TS 3.3.3 states, in part:

The Reactor Vessel Water Level Monitoring System provides a direct measurement of the liquid level above the fuel. Two channels are required OPERABLE (Train A and Train B). Each channel consists of eight sensors on a probe. For a channel to be considered OPERABLE one of the two sensors in the "head" region and three of the six sensors in the "plenum" region shall be OPERABLE. The level indicated by the OPERABLE sensors represents the amount of liquid mass that is in the reactor vessel above the core. Operability of each sensor may be determined by reviewing the error codes displayed on the control room indicator.

In the cases reviewed, the inspectors noted that the issues typically involved brief or spurious abnormal readings from a single RVLIS sensor, which was insufficient by itself to render the applicable RVLIS channel inoperable. The inspectors also noted, however, that the continuing presence and frequency of these abnormal readings was, at best, becoming a nuisance for control room operators and, at worst, a chronic issue that could eventually challenge RVLIS TS operability.

The inspectors further noted that the licensee was placing an appropriate level of emphasis on this issue; at the conclusion of the inspection period the licensee generated IR 4508208; Potential Trend in Unit 1/Unit 2 RVLIS Issues, within the stations CAP to drive additional engineering reviews into this issue.

The inspectors did not identify any findings or violations of NRC requirements in the course of their review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 15, 2022, the inspectors presented the integrated inspection results to Mr. G. Gugle, Site Vice President, and other members of the licensee staff.

On April 1, 2022, the inspectors presented the radiation protection inspection results to Mr. J. Petty, Plant Manager, and other members of the licensee staff.

On May 20, 2022, the inspectors presented the ISFSI Cask Loading inspection results to Mr. G. Gugle, Site Vice President, and other members of the licensee staff.

On June 10, 2022, the inspectors presented the radiation protection inspection results to Mr. G. Gugle, Site Vice President, and other members of the licensee staff.

THIRD PARTY REVIEWS As discussed in IMC 0611, Section 13.01, the inspectors completed a review of the final report issued by the Institute of Nuclear Power Operations (INPO) for the most recent periodic plant performance evaluation of Braidwood Station, which was performed during July 2021 and had a formal exit on September 13, 2021.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

ALARA Plans

BW-00-22-00325

Dry Cask Storage and Support Activities

BRW-14-0070-N

Braidwood Cask Model Update for 2014 ISFSI Campaign

Calculations

BRW-21-0027-N

Braidwood Cask Model Update for 2022 ISFSI Campaign

00157367

Entry Into 1BwOA PRI-4 Due to High RCS Activity on

1PR06J

05/05/2003

244340

Abnormal Noise Emanating from the FHB Crane

04/29/2019

265230

DCS - Indication Found During MPC Delivery Inspection

07/18/2019

270528

MPC 531 Lid Has Minor Indications (Acceptable)

08/08/2019

274522

2019 Braidwood DCS Campaign Lessons Learned

08/26/2019

04323080

DCS PM Partial Performance

03/02/2020

04329064

PCRA to Update BwFP FH-20 FHB Crane Temp

Requirement

03/24/2020

04375525

NOS Finding: M&TE Not Entered for ISFSI Campaign WOs

10/09/2020

Corrective Action

Documents

04486579

OI Benchmark: Industry Use of Admin Controls for Cask

Ops

03/22/2022

SFP Boron Sample Results

05/16/2022

2.48-203

Procedure OU-MW-671-300

7B

2.48-204

Holtec RRTI-2788-002

2.48-205

EC 628051/Analysis No. BRW-09-0028 and Analysis No.

BRW-09-0029

0, 2, 1A

2.48-206

Holtec Notice HN-01

2.48-208

ECR 443383, ISFSI Grillage Polyethylene Bars

2.48-212

Holtec FCR 27881002

2.48-223

EC 629492/Analysis No. BRW-09-0028 and Analysis No.

BRW-09-0029

0, 2A, 1B

2.48-224

BWNPS 10 CFR 72.212 Evaluation Report

06-01

2.48-226

EC 635339

2.48-227

EC 635339

2.48-228

EC 635339

2.48-229

BWNPS 10 CFR 72.212 Evaluation Report

06-02

60855

Miscellaneous

2.48-31

Review of PCI/CES and LTS Procedures

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

BRW-21-0026-N

Braidwood Fuel Selection Package and Alternative List for

22 ISFSI Campaign

DIT-BRW-2010-

0104

Braidwood Fuel Characterization

2/14/2010

DOC-1023-677

MPC 32 to Braidwood Generating Station

21-175

MPC Lift Spider Assembly

2/07/2021

Report No.

914743-676-01

Lid to Shell

05/17/2022

Report No.

914743-676-02

Lid to Shell / SN 676

05/17/2022

Report No.

914743-676-03

Lid to Shell / SN 676

05/18/2022

NDE Reports

Report No.

914743-676-04

Lid to Shell / SN 676

05/18/2022

BwFP FH-69

HI-TRAC Movement Within the Fuel Building

BwFP FH-83

Spent Fuel Cask Contingency Procedures

OU-MW-671-300

Forced Helium Dehydration (FHD) for PWRs (ISFSI)

Procedures

PC-CNSTR-OP-

EXE-H-01

Closure Welding of Holtec Multi-Purpose Canisters at Exelon

Facilities

Revision 22

Self-Assessments NOSA-BRW-20-

(AR 4370017)

Independent Spent Fuel Storage Installation Audit Report

10/14/2020

00676183 01

WH-Perform In-Mast Sipping of All Fuel Assemblies

10/18/2004

04673912 01

Fuel BLDG Overhead Crane Lubrication

04/29/2019

05063024

0HC03G INSP of FHB Overhead Crane

06/03/2021

05063029

LR-Yearly Inspection

06/18/2021

05121105 05

ISFSI RX ENG Inventory MPC After Fuel Load

05/17/2022

05123909

MPC Lift Cleat Inspection

2/07/2021

05123918

HI STORM Lift Bracket Inspection

2/07/2021

05123919

Inspect MPC Spider Lift

2/07/2021

05138020

HI-TRAC Trunnion Inspect

2/11/2022

Work Orders

05138021

Lift Yoke Inspection

2/11/2022

71111.01

Miscellaneous

Letter from Mr. Greg Gugle to Ms. Marri Marchionda-Palmer,

Certification of 2022 Summer Readiness

05/13/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

0BwOA ENV-1

Adverse Weather Conditions Unit 0

24

CC-BR-118-1001

Site Implementation of Diverse and Flexible Coping

Strategies (FLEX) and Spent Fuel Pool Instrumentation

Program

OP-AA-102-102

General Area Checks and Operator Field Rounds

OP-AA-108-107-

1001

Station Response to Grid Capacity Conditions

OP-AA-108-111-

1001

Severe Weather and Natural Disaster Guidelines

OP-BR-102-102-

1001

Augmented Operator Field Rounds

Procedures

WC-AA-107

Seasonal Readiness

4407811

Date Wrong for 1ER-DC05E/Evaluate for Y2K Compliancy

03/10/2021

Corrective Action

Documents

4452755

1ER-DC05E Positive Ground Pushed is High Out of Band

10/13/2021

BwOP AF-E2

Electrical Lineup Unit 2 Operating

BwOP AF-M2

Operating Mechanical Lineup, Auxiliary Feedwater, Unit 2

BwOP DC-E2

Electrical Lineup Unit 1 Operating-125V DC Division

BwOP DG-E1

Electrical Lineup Unit 1 1A Diesel Generator

BwOP DG-M1

Operating Mechanical Lineup Unit 1 1A D/G

BwOP DG-M2

Operating Mechanical Lineup Unit 1 1B D/G

BwOP RH-E2

Electrical Lineup Unit 2 Operating

BwOP RH-E2

Electrical Lineup Unit 2 Operating

71111.04

Procedures

BwOP RH-M4

Operating Mechanical Lineup Unit 2 2B Train

Miscellaneous

Braidwood Station Licensed Operator Requalification

Simulator Scenario Guide, Cycle 22-3 OBE

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-AA-101-113

Operator Fundamentals

OP-AA-101-113-

1006

4.0 Crew Critique Guidelines

OP-AA-103-1-2-

1001

Strategies for Successful Transient Mitigation

71111.11Q

Procedures

OP-AA-103-102

Watch-Standing Practices

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-103-103

Operation of Equipment

OP-AA-104-101

Communications

OP-AA-108-107-

1002

Interface Procedure Between BGE/COMED/PECO and

Exelon Generation (Nuclear/Power) for Transmission

Operations

OP-AA-111-101

Operating Narrative Logs and Records

OP-AA-300

Reactivity Management

TQ-AA-10

Systematic Approach to Training Process Description

TQ-AA-150

Operator Training Programs

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-306

Simulator Management

TQ-BR-201-0113

Braidwood Training Department Simulator Examination

Security Actions

4482320

Boron Accumulation at 1CV8321A

03/03/2022

4490289

2PL08J Annunciator Panel Has No Power

04/05/2022

4492850

1CV8321A Steam Leak

04/13/2022

4493891

Work Request for 1B EDG Annunciator Power Supply

04/18/2022

Corrective Action

Documents

4493892

Work Request for 1A EDG Annunciator Power Supply

04/18/2022

Drawings

M-64, Sheet 5

Diagram of Chemical and Volume Control and Boron

Thermal Regeneration Unit 1

BI

ER-AA-310-1002

Maintenance Rule Functions Safety Significant

Classification

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1001

Maintenance Rule 18-10 Scoping

ER-AA-320-1003

Maintenance Rule 18-10 Failure Definitions

Procedures

ER-AA-320-1004

Maintenance Rule 18-10 Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

71111.12

Work Orders

4901183

Year Inspection

06/03/2022

4493589

Unexpected Annunciators: 2-21-C8 & 2-21-D8

04/16/2022

4494966

Scope Expansion of 0SX02D-30"

04/22/2022

4494967

Scope Expansion Inspection of 1SX02B-30"

04/22/2022

4494969

Scope Expansion Inspection of 1SX03A-30"

04/22/2022

71111.13

Corrective Action

Documents

4494970

Scope Expansion Inspection of 2SX02B-30"

04/22/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Adverse Condition Monitoring and Contingency Plan

(ACMP): SX Leak on Unit 0 CC Heat Exchanger (0SX03A)

Miscellaneous

Final RICT Record for Unit 1 Station Auxiliary Transformer

(SAT) 142-1 and 142-2 Work Window

05/15/2022

ER-AA-600

Risk Management

ER-AA-600-1023

PARAGON Model Capability

ER-AA-600-1042

On-Line Risk Management

ER-AA-600-1052

Risk Management Support of RICT

ER-AA-600-1053

Calculation of RMAT and RICT for Risk Informed Completion

Time Program

ER-BW-600-2001

Braidwood RICT System Guidelines

MA-AA-716-004

Conduct of Troubleshooting

OP-AA-107

Integrated Risk Management

OP-AA-108-117

Protected Equipment Program

OP-AA-108-118

Risk Informed Completion Time

Procedures

WC-AA-101-1006

On-Line Risk Management and Assessment

4901183

Year Inspection

06/03/2022

249849-01

Troubleshoot Annunciator Panel

04/18/2022

253243-01

Ultrasonic Thickness Exam on Line 0SX02D-30" - 0CC01A

Heat Exchanger Inlet Nozzle

05/17/2022

253244-01

Ultrasonic Thickness Exam on Line 1SX02B-30" - 0CC1A

Heat Exchanger Inlet Nozzle

05/04/2022

Work Orders

253245-02

Ultrasonic Thickness Exam on 1SX03A-30" - 1CC01A Heat

Exchanger Outlet Nozzle

05/04/2022

4471553

Reflash of U2 Rod Control Non-Urgent Failure Alarm

01/13/2022

4492197

1B DG Repair Crack in Manifold

04/11/2022

4494801

SX Piping Leakage at Outlet of U-O CC Hx

04/22/2022

Corrective Action

Documents

4505042

0B VC Chiller Oil Additions

06/11/2022

635793

Install Temporary Power Supply in 2RD03J

636541

Engineering to Evaluate Seal Weld for Cracked 1B DG

Manifold

71111.15

Engineering

Changes

636627

Configuration Control Processing of Design Analysis

051853, Revision 005M, for Evaluation of the Structural

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Integrity of Line 0SX03A-30" per Code Case N-513-4,

Considering the Through Wall Leakage Identified

636646

Operability Evaluation 22-001: Pinhole Leak on a Weld on

Line 0SX03A-30"

636646

Operability Evaluation 22-001: Pinhole Leak on a Weld on

Line 0SX03A-30"

Miscellaneous

BRW-2-2021-

0304

ODM: Unit 2 Rod Drive Non-Urgent Failure

CC-AA-309-101

Engineering Technical Evaluations

ER-AA-600-1012

Risk Management Documentation

OP-AA-106-101-

1006

Operational Decision-Making Process

OP-AA-108-111

Adverse Condition Monitoring and Contingency Planning

Procedures

OP-AA-108-115

Operability Determinations (CM-1)

Work Orders

214697

IM 2RD03J Fab & Install Temp PS in Parallel with PS1, PS2

05/25/2022

4467108

Unexpected Annunciator 2-10-D6: Rod Control Non-Urgent

Failure

2/16/2021

4468189

Reflash of Unit 2 Rod Control Non-Urgent Failure Alarm

2-10-D6

2/24/2021

Corrective Action

Documents

4471553

Reflash of Unit 2 Rod Control Non-Urgent Failure Alarm

01/13/2022

Engineering

Changes

635793

Install Temporary Power Supply in 2RD03J

CC-AA-112

Temporary Configuration Changes

29-30

Procedures

IP-ENG-001

Standard Design Process (EB-17-06)

71111.18

Work Orders

253243-01

Ultrasonic Thickness Exam on Line 0SX02D-30" - 0CC01A

Heat Exchanger Inlet Nozzle

05/17/2022

71111.19

Procedures

ER-AA-335-004

Ultrasonic (UT) Measurement of Material Thickness and

Interfering Conditions

4502482

0FX03PA Battery Voltage Low - Failed Acceptance Criteria

05/28/2022

4502483

0FX03PB Battery Voltage Low - Failed Acceptance Criteria

05/282022

4502484

0FX01PA Battery Voltage Low - Failed Acceptance Criteria

05/28/2022

71111.22

Corrective Action

Documents

4502485

0FX01PB and 0FX01PC Battery Voltages Low but Still in

Band

05/28/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4504183

OOT and Blown Control Power Fuse on 2N-NR8041

06/07/2022

4504563

Cleared Controller Fuse for 2N-NR8042

06/09/2022

4505840

0FX03PA Voltage Low

06/16/2022

4505992

0A Medium Head Flex Pump Won't Stay Running

06/16/2022

4505994

0A High Head Flex Test Connection Bad Fitting

06/16/2022

4506515

0FX03PB Developed Leak from Diesel Oil Filter When

Started

06/20/2022

4507359

0FX03PB Low Head Flex Pump Flow

06/24/2022

4507621

0FX03PB Fuel Oil Leak

06/26/2022

4507623

B High Head Flex Pump Did Not Meet Test Parameters

06/26/2022

4508035

0B High Head Flex Pump High Oil Temp

06/28/2022

0BwOS FX-12

FLEX Pump Full Flow Test Surveillance

BwISR 3.3.1.6-

004

Quarterly Excore Power Range N44 Axial Flux

Difference/7300 Delta Flux Penalty Calibration

OP-BR-FX-1003

High Head FLEX Pump Operating Guideline

OP-BR-FX-1004

Medium Head FLEX Pump Operating Guideline

Procedures

OP-BR-FX-1005

Low Head FLEX Pump Operating Guideline

5011598

0FX01PA (A Train Medium Head FLEX Pump) Performance

Test

06/20/2022

Work Orders

5013180

0FX03PA (A Train Low Head FLEX Pump) Performance

Test

06/16/2022

4504645

Braidwood 2022 Performance Indicator Drill Critique and

Learnings Operations Support Center

06/09/2022

4504679

Braidwood 2022 Performance Indicator Drill Learnings

Technical Support Center 1 of 2

06/09/2022

4504684

Braidwood 2022 Performance Indicator Drill Learnings

Technical Support Center 2 of 2

06/09/2022

Corrective Action

Documents

4504733

Braidwood 2022 Performance Indicator Drill Learnings

Main Control Room / Simulator

06/09/2022

EP-AA-1000

Standardized Radiological Emergency Plan

EP-AA-1001

Radiological Emergency Plan Annex for Braidwood Station

71114.06

Procedures

EP-AA-1001,

Addendum 1

Braidwood Station On-Shift Staffing Technical Basis

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

EP-AA-1001,

Addendum 3

Emergency Action Levels for Braidwood Station

AR 04435959

0EA01C SCBA Air Compressor PM's Needed Air

Replacement

07/21/2021

Corrective Action

Documents

AR 04490491

SCBA Compressor Out of Service

04/05/2022

Trace Analytics SCBA Grade D Quality Air Report

05/05/2022

Miscellaneous

Air One Equipment SCBA Hydrostatic Testing Results

01/25/2022

RP-AA-444

Controlled Negative Pressure (CNP) Fit Testing

RP-AA-700-1246

Operation of Air Samplers

71124.03

Procedures

RP-AA-825

Maintenance, Care, and Inspection of Respiratory Protective

Equipment

Calibration

Records

Calibration of the Accuscan II WBC System at the Exelon

Generating Station

2/23/2022

Dose Assessment for a Declared Pregnant Worker.

2/01/2022

Dose Assessment for a Declared Pregnant Worker.

2/20/2021

Miscellaneous

Braidwood Dry Activated Waste Part 61 Analysis

20

RP-AA-12

Internal Dose Control Program Description

RP-AA-441

TEDE ALARA Evaluation

71124.04

Procedures

RP-AA-700-1235

Operation and Calibration of the PM-12 Gamma Portal

Monitor

Serial Number

0019520

Mirion Telepole II

07/27/2021

Serial Number

1011-279

Argos 5 Monitor

03/17/2022

Serial Number

2060

Thermo Scientific PM12

03/22/2022

Serial Number

2082

Thermo Scientific PM12

2/03/2021

Serial Number

2084

Thermo Scientific PM12 Unit 1 Containment Access Facility

03/23/2022

Serial Number

235A

Thermo Scientific SAM12

03/17/2022

71124.05

Calibration

Records

Serial Number

Ludlum Model 30

2/25/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

26144

Serial Number

2B.106

Mirion RDS-31

09/21/2021

Serial Number

336338

Ludlum Model 12-4

2/25/2021

Serial Number

C613F

Bicron RSO-50E

03/14/2022

AR 04431313

Low Flow and Pump (2PR30PB) Turning Off on 2PR3DJ

07/24/2021

AR 04444789

Unexpected Alarm: 0AR68J High Alarm

09/05/2021

Corrective Action

Documents

AR 04486858

U1 CAF PM12 12010 Needs Battery Replaced

03/23/2022

04956514

1PR28J Calibration of Effluent Gaseous Rad Monitor Plant

Ventilation Monitor

01/27/2021

Work Orders

04999329-01

Calibration Liquid Effluent Radiation Monitor Station

Blowdown Line

09/01/2021

NRC Performance Indicator Data; Mitigating Systems

Safety System Functional Failures

04/01/2021 -

03/31/2022

NRC Performance Indicator Data; Mitigating Systems

Mitigating System Performance Index for Emergency AC

Power

04/01/2021 -

03/31/2022

Miscellaneous

NRC Performance Indicator Data; Mitigating Systems

Mitigating Systems Performance Index for High Pressure

Injection

04/01/2021 -

03/31/2022

LS-AA-2001

Collecting and Reporting of NRC Performance Indicator

Data

LS-AA-2080

Monthly Data Elements for NRC Safety System Functional

Failures

71151

Procedures

LS-AA-2200

Mitigating System Performance Index Data Acquisition and

Reporting

4474052

Level 3 Configuration Control: Incorrect Connection of Test

Equipment

01/26/2022

4475596

4.0 Critique - Volume Control Tank Pressure Abnormal

Indication

2/02/2022

71152A

Corrective Action

Documents

4475837

Maintenance Department For-Cause Management Review

Meeting Results

2/03/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

BwAR 2-9-B2

Volume Control Tak (VCT) Pressure High/Low

BwIP 2P-0120

Calibration of Charging Header Pressure Loop 2P-0120 (CV)

BwOP RP-11A18

2PA06J Panel Appendix

NO-AA-10

Quality Assurance Topical Report (QATR)

PI-AA-120

Issue Identification and Screening Process

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

Procedures

PI-AA-125-1004

Effectiveness Review Manual

Work Orders

5063738

2P-0120 Charging Header Pressure Loop

01/26/2022

4442055

1-9-D6 - Unexpected Main Control Room Alarm -RVLIS

Sensor Uncovered

08/23/2021

4442887

1-9-D6 - Unexpected Main Control Room Alarm - RVLIS

Sensor Uncovered

08/26/2021

4450389

Unexpected Main Control Room Alarm - Reactor Vessel

Level Indication System (RVLIS) Sensor/Core Exit

Thermocouple (CETC) Failure

10/03/2021

4472056

Alarm 2-9-D6 - RVLIS Level Sensor 7B Erratic

01/15/2022

4482013

1-9-D6, RVLIS Sensor Uncovered Sensor 6A (Plenum 27%)

03/02/2022

4488602

Unexpected Alarm on Unit One-A RVLIS

03/30/2022

4508208

Potential Trend in Unit 1/Unit 2 RVLIS Issues

06/29/2022

71152S

Corrective Action

Documents

4508584

Unexpected Alarm 1-9-D6, RVLIS Sensor Uncovered

Sensor 3A

06/30/2022