IR 05000456/2021003

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Integrated Inspection Report 05000456/2021003 and 05000457/2021003
ML21299A077
Person / Time
Site: Braidwood  
Issue date: 10/26/2021
From: Hironori Peterson
Region 3 Branch 3
To: Rhoades D
Exelon Generation Co, Exelon Nuclear
References
IR 2021003
Download: ML21299A077 (24)


Text

SUBJECT:

BRAIDWOOD STATION - INTEGRATED INSPECTION REPORT 05000456/2021003 AND 05000457/2021003

Dear Mr. Rhoades:

On September 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station. On October 13, 2021, the NRC inspectors discussed the results of this inspection with Mr. J. Keenan, the Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77

Enclosure:

As stated

Inspection Report

Docket Numbers:

05000456 and 05000457

License Numbers:

NPF-72 and NPF-77

Report Numbers:

05000456/2021003 and 05000457/2021003

Enterprise Identifier:

I-2021-003-0059

Licensee:

Exelon Generation Company, LLC

Facility:

Braidwood Station

Location:

Braceville, IL

Inspection Dates:

July 01, 2021 to September 30, 2021

Inspectors:

B. Bartlett, Senior Operations Engineer

G. Edwards, Health Physicist

D. Kimble, Senior Resident Inspector

J. Nance, Operations Engineer

N. Shah, Project Engineer

P. Smagacz, Resident Inspector

Approved By:

Hironori Peterson, Chief

Branch 3

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 1 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the entire inspection period.

Unit 2 began the inspection period operating at full power. On September 16, 2021, the unit reached the end of the fuel cycle and power coast down operations commenced in preparation for a planned refuel outage. The unit continued to reduce power in accordance with the licensees approved reactivity management plan, and was operating at approximately 91 percent power at the end of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on-site as local COVID-19 conditions permitted.

As part of their on-site activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution, observed risk significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial physical alignment verifications of the following systems/trains:

(1)1A Residual Heat Removal (RH) Train during 1B RH Train maintenance during the week ending July 24, 2021.

(2)1B Safety Injection (SI) Train during 1A SI Train maintenance during the week ending August 28, 2021.

(3)2A Station Air Compressor during replacement of the Unit 0 Station Air Compressor replacement during the week ending September 4, 2021.

(4)2A Auxiliary Feedwater (AF) Train during 2B AF Train maintenance during the week ending September 11, 2021.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting physical inspections and reviews to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Units 1 and 2 Auxiliary Building, 346' Elevation, General Area, during the week ending August 7, 2021.
(2) Units 1 and 2 Auxiliary Building, 330' Elevation, 1A and 2A Essential Service Water (SX) Pump Room, during the week ending August 7, 2021.
(3) Units 1 and 2 Auxiliary Building, 330' Elevation, 1B and 2B SX Pump Room, during the week ending August 7, 2021.

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)

The inspectors evaluated internal flooding mitigation protection features in the following plant areas:

(1) Unit 1 Auxiliary Building, 330', 346', and 364' Elevations, during the week ending August 7, 2021.
(2) Unit 2 Auxiliary Building, 330', 346', and 364' Elevations, during the week ending August 7, 2021.

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification annual operating exam and biennial written examination administered from August 9, 2021 through September 17, 2021.

71111.11B - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Program (IP Section 03.04) (1 Sample)

(1) Biennial Requalification Written Examinations The inspectors evaluated the quality of the licensed operator biennial requalification written examination administered between August 9, 2021 and September 17, 2021.

Annual Requalification Operating Tests The inspectors evaluated the adequacy of the facility licensees annual requalification operating test.

Administration of an Annual Requalification Operating Test The inspectors evaluated the effectiveness of the facility licensee in administering requalification operating tests required by 10 CFR 55.59(a)(2) and that the facility licensee is effectively evaluating their licensed operators for mastery of training objectives.

Requalification Examination Security The inspectors evaluated the ability of the facility licensee to safeguard examination material, such that the examination is not compromised.

Remedial Training and Re-examinations The inspectors evaluated the effectiveness of remedial training conducted by the licensee, and reviewed the adequacy of re-examinations for licensed operators who did not pass a required requalification examination.

Operator License Conditions The inspectors evaluated the licensees program for ensuring that licensed operators meet the conditions of their licenses.

Control Room Simulator The inspectors evaluated the adequacy of the facility licensees control room simulator in modeling the actual plant, and for meeting the requirements contained in 10 CFR 55.46.

Problem Identification and Resolution The inspectors evaluated the licensees ability to identify and resolve problems associated with licensed operator performance.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

The inspectors observed and evaluated the following licensed operator activities in the control room:

(1) Various activities involving on-watch operations crews. These activities included, but were not limited to:

End-of-cycle reactivity maneuvers leading into Unit 2 coast down operations for the A2R22 refuel outage during the week ending September 18, 2021.

4,160 Vac electric plant maneuvers in support of emergency diesel generator testing during the week ending September 18, 2021.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

The inspectors observed and evaluated the following licensed operator training activity:

(1) A complex casualty graded scenario involving a crew of licensed operators was observed in facility's simulator on September 7, 2021.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Maintenance effectiveness and performance history review of the Direct Current (DC)

Batteries and Distribution System during the weeks ending August 21 through August 28, 2021.

(2) Maintenance effectiveness and performance history review of nuclear instrumentation during the week ending August 28, 2021.
(3) Maintenance effectiveness and performance history review of Overpower Delta Temperature (OPDT) components during the weeks ending September 4 through September 30, 2021.

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Evaluation of the activities and risk associated with emergent troubleshooting and repairs to the 1A Emergency Diesel Generator (EDG), as documented in Issue Report (IR) 4437474 during the week ending July 31, 2021.
(2) Evaluation of the work activities and risk associated with planned maintenance on the 1B SI Recirculation Isolation Valve, 1SI8920, in conjunction with emergent work on 1HD026A, the 12A Feedwater Heater Normal Level Control Valve, during the week ending September 18, 2021.
(3) Evaluation of the work activities and risk associated with several concurrent planned work activities, including acceptance testing for the 1A Station Air Compressor, 1A EDG monthly operability testing, 1A RH Train operability testing, and 2A Containment Spray Train operability testing during the week ending September 30, 2021.

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples 1 Partial)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Evaluation of the availability of the 2B Start Up Feedwater Pump due to low oil pressure, as documented in IR 4428965 during the weeks ending July 10 through August 14, 2021.
(2) Evaluation of the operability of the 2B RH system due to boric acid leakage on the 2FIS-0611 Recirculation Valve Controller, as documented in IR 4436953 during the weeks ending July 31 through August 14, 2021.
(3) Evaluation of the operability of the 1A EDG after a failure to start during a monthly surveillance, as documented in IR 4437474 during the weeks ending August 7 through September 18, 2021.
(4) Evaluation of the operability of the 2A EDG following identification of a sheared bolt associated with the 4L cylinder air manifold, as documented in IR 4443522 during the weeks ending September 4 through September 25, 2021.

(5)

(Partial)

Continued evaluation of the operability of the source range nuclear instruments with their high flux trips bypassed during reactor startup, as documented in IR 4418688 during the weeks ending July 1 through September 25, 2021.

(6) Review of Unit 1 Core Exit Thermocouple (CETC) operability following several issues, as documented in IRs 4419609, 4420610, and 4423740 during the weeks ending September 25 through September 30, 2021.
(7) Review of the 0B Auxiliary Building Nonaccessible Area (NAC) Exhaust Filter Plenum Ventilation Train operability following identification of testing equipment being left installed since May 2021, as documented in IR 4447805 during the weeks ending July 10 through September 30, 2021.

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1) Testing of the 1SI8920 Mini-Flow Recirculation Valve after maintenance, as set forth in Work Order (WO) 4904903 during the week ending September 18, 2021.
(2) Comprehensive functional and operational acceptance testing of the 1A Station Air Compressor following replacement and installation, as documented in station procedure SPP-21-002 during the weeks ending September 25 through September 30, 2021.

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1)2BwOSR 3.8.1.2-1, Technical Specification operability surveillance for the 2A EDG, during the weeks ending August 7 through August 14, 2021.

(2) BwIP 2500-070, calibration of the 2B Steam Generator main steam atmospheric relief valve control loop, during the week ending August 14, 2021.

Inservice Testing (IP Section 03.01) (1 Sample)

(1)2BwOSR 5.5.8.RH, inservice testing for the 2B RH Train, during the weeks ending August 14 through August 21, 2021.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes.

Eval No. 20-71 Emergency Action Levels for Braidwood Station, EP-AA-1001, Addendum 3 This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Select Emergency Preparedness Drills and/or Training for Observation (IP Section 03.01) (1 Sample)

The inspectors evaluated the following select emergency preparedness (EP) drill:

(1) Observation and evaluation of the station's Emergency Response Organization during the performance of a full-scale site-wide EP drill on August 2, 2021.

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated the following EP drill/training evolution:

(1) Review of the implementation of the site's emergency plan by a crew of licensed operators during an evaluated emergency scenario in the facility's simulator on September 7,

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Calibration and Testing Program (IP Section 03.02) (6 Samples)

The inspectors evaluated the calibration and testing of the following radiation detection instruments:

(1) Thermo Fisher RO20 SN#0013941
(2) Eberline Model 3 SN#0017854
(3) Ludlum 177 SN#0025821
(4) Thermo Fisher RO20 SN#0018388
(5) Eberline Model 3 SN#0014351
(6) Ludlum 3030P SN#0015022

71124.07 - Radiological Environmental Monitoring Program

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples.

Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program.

GPI Implementation (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative program to identify incomplete or discontinued program elements.

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage,

& Transportation

Radioactive Material Storage (IP Section 03.01)

(1) Inspectors evaluated the licensees performance in controlling, labeling, and securing radioactive materials. This included the radioactive waste storage portion of the facility.

Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)

(1) Inspectors walked down accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality.

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

(1) The inspectors evaluated the licensees characterization and classification of radioactive waste. This included the resin waste streams at the facility.
(2) The inspectors evaluated the licensees characterization and classification of radioactive waste. This included the dry activated waste (DAW) stream at the facility.

Shipment Preparation (IP Section 03.04) (1 Sample)

(1) The inspectors observed that a shipment containing radioactive material is prepared according to requirements. The shipment identification number was RWS21-015 for seven B-25 Boxes of Condensate Polish Resin shipped on August 17, 2021.

Shipping Records (IP Section 03.05) (3 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through a record review:

(1) Shipment RWS21-001 UN3321 LSA-II; Resin Liner P0695283-14 in Cask 14-215.
(2) Shipment RWS20-015 UN3321 LSA-II; 14 DAW Legacy Waste in Cask 14-210.
(3) Shipment RWS20-018 UN2916 Type (B) Package; Resin Liner PO 692200-4.

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors reviewed and verified selected portions of the licensee's performance indicator submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07)===

(1) Unit 1 (July 1, 2020 through June 30, 2021)
(2) Unit 2 (July 1, 2020 through June 30, 2021)

MS09: Residual Heat Removal Systems (IP Section 02.08) (2 Samples)

(1) Unit 1 (July 1, 2020 through June 30, 2021)
(2) Unit 2 (July 1, 2020 through June 30, 2021)

MS10: Cooling Water Support Systems (IP Section 02.09) (2 Samples)

(1) Unit 1 (July 1, 2020 through June 30, 2021)
(2) Unit 2 (July 1, 2020 through June 30, 2021)

71152 - Problem Identification and Resolution

Annual Follow-up of Selected Issues (IP Section 02.03) (2 Samples)

The inspectors conducted in-depth reviews of the licensees implementation of the CAP related to the following issues:

(1) Review and assessment of the corrective actions for the spent fuel dry cask storage (DCS) system forced helium drying errors, as documented in IR 4364058 during the weeks ending August 7 through August 14, 2021.
(2) Review and assessment of the corrective actions for the 1/2CC202B wrong unit valve operation, as documented in IR 4434922 during the weeks ending July 17 through September 30,

INSPECTION RESULTS

Observation: Forced Helium Drying Skid Issue During Dry Cask Processing 71152 The inspectors performed a detailed review of IR 4364058, Forced Helium Drying Skid Issue. Specifically, on August 19, 2020, a reactor services crew connected hoses incorrectly in preparation for Multi-Purpose Cannister (MPC) blowdown, resulting in an increased risk of the cask being over-pressurized due to bulk water boiling inside the cask. The inspectors chose this issue for an in-depth review of the licensee's actions within their corrective action program (CAP) due to the potential of cask failure and damage to the integrity of the fuel stored within the cask. Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensee's corrective actions taken to address this condition.

The licensees evaluation concluded that the direct cause was the failure by the fuel handlers to verify that the correct hoses were properly attached to the MPC prior to starting work.

Contributing to this were inappropriate actions taken by supervision overseeing the work activities, in part, due to a culture of not reinforcing expectations for using human performance tools during previous work activities and workers not effectively challenging supervision when faced with potential issues.

Corrective actions included, but were not limited to, revising procedures to use color coded hoses to ensure correct connections and requiring that supervisors sign off on specific, key steps to ensure proper system setup. Additionally, coaching/training was provided to ensure fuel handling supervision understood the expectations for performing work observations and in how to identify and correct key behaviors. Further, fuel handling management verified the efficacy of these actions by holding monthly meetings to evaluate the observations performed and proffer feedback on their effectiveness.

The inspectors review did not identify any issues of note with the corrective actions taken; however, their effectiveness could not be confirmed as the licensee had not performed any cask handling activities since implementation.

No findings or violations of NRC requirements were identified by the inspectors in the course of this review.

Observation: 1/2CC202B Wrong Unit Error 71152 The inspectors performed a detailed review of IR 4434922, Level 4 Configuration Control - Received Unexpected Alarm 1-2-E3. The issue involved the mistaken operation of 1CC202B, Motor-Operated Valve (MOV) 1B SX to CC Makeup Downstream Isolation, during what was planned to have been a post-maintenance stroke test of 2CC202B, MOV 2B SX to CC Makeup Downstream Isolation, on July 14, 2021. The inspectors determined that the mistaken operation of 1CC202B instead of the planned and briefed 2CC202B had constituted a violation of the requirements of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings. However, because the SX to Component Cooling (CC)emergency makeup line on each unit is protected from the effects of inadvertent valve operation by the use of two MOVs in series, the mistaken operation of the 1CC202B valve instead of the intended 2CC202B valve did not result in any adverse consequences.

Subsequently, the inspectors concluded that the violation had not adversely impacted the Reactor Safety Mitigating Systems Cornerstone objective and, therefore, constituted a violation of minor significance that was not subject to formal actions per Section 2.3.1 of the NRC Enforcement Policy.

The inspectors chose this issue for an in-depth review of the licensees actions within their CAP because of the inherent risk associated with wrong unit/wrong component operational errors. Consequently, for this detailed Problem Identification and Resolution inspection sample, the inspectors focused on assessment of the licensees corrective actions taken both for this specific error, as well as those targeted at the more generic issue of preventing wrong unit/wrong component operational errors.

The inspectors did not identify any issues with the licensees CAP actions taken. Actions targeting the more generic issue of wrong unit/wrong component operational errors were focused on reinforcing existing human performance tool use and appreciation by the workforce. Actions targeting this specific event included painting the control panels for the MOV hand switches involved in this event with the appropriate unit-specific color scheme - yellow for Unit 1 and green for Unit 2. At the time of the event, all of the control panels involved, all of which are located in the same physical area of the station, were painted with a non-distinct color.

No findings or violations of NRC requirements of more than minor safety significance were identified by the inspectors in the course of this review.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 13, 2021, the inspectors presented the integrated inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On July 15, 2021, the inspectors presented the radiation protection inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On August 20, 2021, the inspectors presented the radiation protection inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On August 20, 2021, the inspectors presented the biennial requalification inspection results inspection results to Mr. J. Keenan, Site Vice President, and other members of the licensee staff.

On October 1, 2021, the inspectors presented the EPlan and EAL Change Inspection Exit inspection results to Mr. D. Moore, Senior Manager, Emergency Preparedness, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

29000

SA SAC (2SA02C) Oil Temperature High

06/12/2021

4436087

1RH8729A Lock Issues

07/20/2021

4436735

2SA02C Oil Temperature High

07/23/2021

4437788

2SA02C Margin Improvement Initiative

07/29/2021

4443172

2SA01C FNL I/S Temperature is High

08/28/2021

Corrective Action

Documents

BwOP RH-M1

Operating Mechanical Lineup Unit 1 1A RH Train

BwOP AF-E2

Electrical Lineup Unit 2 Operating

BwOP AF-M2

Operating Mechanical Lineup, Auxiliary Feedwater, Unit 2

BwOP RH-E1

Electrical Lineup Unit 1 Operating

BwOP SA-E2

Electrical Lineup Unit 2 Station Air System Operating

BwOP SA-M2

Operating Mechanical Lineup Unit 2

BwOP SI-E1

Electrical Lineup Unit 1 Operating

71111.04

Procedures

BwOP SI-M1

Operating Mechanical Lineup Unit 1

Pre-Fire Plan No.

101

Fire Zone 11.2-0; Auxiliary Building 346' Elevation,

Auxiliary Building General Area South

Pre-Fire Plan No.

Fire Zone 11.1A-0; Auxiliary Building 330' Elevation, Unit 1

Auxiliary Building Basement (1A/2A SX)

Pre-Fire Plan No.

Fire Zone 11.1B-0; Auxiliary Building 330' Elevation, Unit 2

Auxiliary Building Basement (1B/2B SX)

Pre-Fire Plan No.

Fire Zone 11.2-0; Auxiliary Building 346' Elevation,

Auxiliary Building General Area Center

Fire Plans

Pre-Fire Plan No.

Fire Zone 11.2-0; Auxiliary Building 346' Elevation,

Auxiliary Building General Area North

BwAP 1110-1

Fire Protection Program System Requirements

BwAP 1110-3

Plant Barrier Impairment Program

BwOP PBI-1

Plant Barrier Impairment Program Pre-Evaluated Barrier

Matrix

CC-AA-201

Plant Barrier Control Program

ER-AA-600-1069

High-Risk Fire Area Identification

71111.05

Procedures

ER-BR-600-1069

Site List of High-Risk Fire Areas Braidwood Unit 1 and

Unit 2

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-201-008

Pre-Fire Plan Manual

OP-AA-201-009

Control of Transient Combustible Material

OP-AA-201-1001

Operations On-Line Fire Risk Management

3C8-0685-002

Auxiliary Building Flood Level Calculation

3C8-0787-001

Confirmation of Safe Shutdown Capability After Auxiliary

Building Flooding

Calculations

3C8-1281-001

Auxiliary Building Flood Level Calculations

4355236

The Plug for the 0TR19P (Lime Sludge West Lagoon Sump

Pump) is Damaged and Needs to be Replaced

08/07/2020

4366140

Unexpected Alarm 1-1-A2 Containment Drain Leak

Detection Flow High

08/29/2020

4391353

0TR19P WWT West Lime Sludge Lagoon #2 Sump Pump is

Degraded

2/20/2020

4405498

SD-191 Discrepancy During Watertight Door Surveillance

03/01/2021

4418893

WO 01785089-09 Stud Missing for Re-Installation of Flood

Seal

04/25/2021

22795

Procedural Guidance for Setting Cable Vault Sump Pumps

05/11/2021

27580

IAM for Sump Pump 0CP05P WO 5157026-01

06/04/2021

28760

Received the Unit 1 SX Sump Level High High Alarm

06/11/2021

Corrective Action

Documents

4438648

Door Operator Loose on Unit 2 SX Pump Room

08/03/2021

BB-PRA-012

Byron and Braidwood Probabilistic Risk Assessment,

Internal Flood Evaluation Summary Notebook

Miscellaneous

NEI 12-07

Guidelines for Performing Verification Walkdowns of Plant

Flood Protection Features

0BwOA PRI-8

Auxiliary Building Flooding Unit 0

Procedures

ER-AA-450

Structures Monitoring

1860257

1DSFO06/08 Outage Flood Seals Surveillance

03/03/2017

1915060

2DSFSO06/08 Outage Flood Seals Surveillance

10/18/2017

4838070

Remove/Replace Flood Seal Covers

1DSFSO07 & 09 Auxiliary Feedwater Tunnel Outage

03/25/2020

71111.06

Work Orders

5079981

Watertight Door Inspection

03/18/2021

4340246

4.0 Critique for Recent and Ramps

05/012020

71111.11B

Corrective Action

Documents

4398670

4.0 Critique U0 CC Heat Exchanger Side Drain Down

01/28/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4418688

Level 3 Configuration Control SRNI's Required Function

Bypassed

04/24/2021

4430586

4.0 Critique U1 Reactor Trip Due to Generator Load Reject

06/21/2021

Corrective Action

Documents

Resulting from

Inspection

4441641

NRC Identified Unattended Exam Material

08/19/2021

Fire Plans

Simulator Post

Event Testing

1A MFP Start (PMT)

03/05/2020

Simulator Post

Event Testing

1A MFP Start

11/06/2019

Simulator Post

Event Testing

2CC130 Issues / Drop 7 failure

07/23/2021

Simulator Post

Event Testing

2CV131 - Securing Letdown Evolution

07/14/2021

Simulator Post

Event Testing

Unit 2A MFP Start 12/7/2020

2/10/2021

TQ-AA-306

ATT 10 PWR Moderator Temperature Coefficient of

Reactivity, Cycle 23 Compare to Plant Startup Data

04/29/2021

TQ-AA-306

ATT 10 PWR Moderator Temperature Coefficient of

Reactivity Cycle 23 New Core Test

04/27/2021

TQ-AA-306

ATT 11 PWR Rod Worth Coefficient of Reactivity Cycle 23

New Core Test

04/27/2021

TQ-AA-306

ATT 12 PWR Boron Coefficient of Reactivity Cycle 23,

New Core Test

04/27/2021

TQ-AA-306

ATT 13 PWR Xenon Worths Cycle 23, New Core Test

04/27/2021

TQ-AA-306

ATT 16 PWR Approach to Criticality Using Boric Acid

Cycle 23, Comparison to Plant Data

04/29/2021

TQ-AA-306

ATT 16 PWR Approach to Criticality Using Boric Acid

Cycle 23, New Core Test

04/27/2021

TQ-AA-306

ATT 17 PWR Approach to Criticality Using Rods Cycle 23,

New Core Test

04/27/2021

Miscellaneous

TQ-BR-0115

Transient 10, Slow Primary Depressurization Due to Open

PORV w/o Charging Pumps

03/22/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

TQ-BR-302-0103

Braidwood Steady State Testing 100% and 75%

03/05/2020

TQ-BR-302-0103

FW/CV Letdown System Tuning 49%

03/05/2020

TQ-BR-302-0106

Transient Test - 1, Manual Reactor Trip

03/22/2021

TQ-BR-302-0107

Transient Test 2, Simultaneous Trip of All Main Feedwater

Pumps

03/22/2021

TQ-BR-302-0108

Transient Test 3, Simultaneous Closure of All Main Steam

Isolation Valves

03/22/2021

TQ-BR-302-0109

Transient Test 4, Simultaneous Trip of All Reactor Coolant

Pumps

03/22/2021

TQ-BR-302-0110

Transient Test 5, Trip of Any Single Reactor Coolant Pump

03/22/2021

TQ-BR-302-0111

Transient Test 6, Turbine Trip
<P-8

03/22/2021

TQ-BR-302-0112

Transient 7, Maximum Ramp Rate (100% to 75% to 100%)

03/22/2021

TQ-BR-302-0113

Transient 8, LBLOCA with LOOP

03/22/2021

TQ-BR-302-0114

Transient 9, Maximum Size Main Steam Line Rupture

03/22/2021

TQ-BR-302-0116

Maximum Design Load Reject

03/22/2021

TQ-AA-10

Systematic Approach to Training Process Description

TQ-AA-150

Operator Training Programs

TQ-AA-155

Conduct of Simulator Training and Evaluation

TQ-AA-201

Examination Security and Administration

TQ-AA-306

Simulator Management

Procedures

TQ-BR-201-0113

Braidwood Training Department Simulator Examination

Security Actions

Self-Assessments

Differences Between Braidwood Simulator and Braidwood

Unit 1

SRB 21-2

Work Orders

Open Service Work Requests

08/16/2021

OP-AA-101-111-

1001

Operations Standards and Expectations

OP-AA-101-113

Operator Fundamentals

OP-AA-101-113-

1006

4.0 Crew Critique Guidelines

OP-AA-103-102

Watch-Standing Practices

71111.11Q

Procedures

OP-AA-103-102-

1001

Strategies for Successful Transient Mitigation

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

OP-AA-103-103

Operation of Plant Equipment

OP-AA-104-101

Communications

OP-AA-111-101

Operating Narrative Logs and Records

OP-AA-300

Reactivity Management

1451512

Unit 2 Core Exit Thermocouple Nozzle 77 Connections

Swapped Affecting Indications

2/12/2012

4370362

Recurring Equipment Reliability Issue Unit 1 D

Incore Detector

09/18/2020

4393580

Hairline Cracks in Tops of Battery Cells (1DC02E)

01/03/2021

4402276

Battery 211 Terminal Voltage High Out of Admin Limit

2/14/2021

4402279

Battery 112 Quarterly Temp Deviation High Out of Admin

Limit

2/14/2021

4403966

1D Incore Detector Issues

2/22/2021

4411770

Failed Post-Maintenance Test 1D Incore

03/26/2021

4413950

Battery 211 Has Cap Broken on Cell 56

04/04/2021

4418835

1BwOS TRM 3.3.H.1 Failed Symmetric Core Exit

Thermocouple Temperature Limits

04/25/2021

4419609

Unit 1 Core Exit Thermocouple Nozzle 74 Connections

Swapped Affecting Indications

04/28/2021

21778

Unexpected Alarms 1-10-A5 and 1-114-A1 for OPDT

05/05/2021

23740

Unit 1 Core Exit Thermocouples Exceed Allowed Maximum

Deviation

05/15/2021

25470

DC111 Cracked Battery Cells

05/25/2021

4436872

Pilot Cell for Battery 112 Specific Gravity Found Low

07/25/2021

4439676

Summary of Findings from Braidwood Unit 1 Source Range

Nuclear Instrument Cable Testing

08/09/2021

4440617

Unexpected BwAR 1-10-C3 Poer Range Flux Rate Trip Alert

for N41

08/13/2021

4440747

Battery 111 Average Cell Temp High

08/15/2021

Corrective Action

Documents

4441987

Unexpected Alarms 1-10-A5 and 1-14-A1 for 1C OPDT

08/22/2021

Operability

Evaluations

ER-AA-320-1001

Maintenance Rule 18-10 Scoping

71111.12

Procedures

ER-AA-312-1002

Maintenance Rule Functions Safety Significant

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Classification

ER-AA-320

Maintenance Rule Implementation per NEI 18-10

ER-AA-320-1001

Maintenance Rule 18-10 Failure Definitions

ER-AA-320-1004

Maintenance Rule 18-10 Performance Monitoring and

Dispositioning Between (a)(1) and (a)(2)

4446169

Unexpected MRC Alarm; 12A HTR LO

09/14/2021

Corrective Action

Documents

4446232

1HD054A Continuous Operation Evaluation Required

09/14/2021

Miscellaneous

1SI8920 Work Window Protected Equipment List

09/13/2021

ER-AA-600

Risk Management

ER-AA-600-1042

On-Line Risk Management

MA-AA-716-004

Conduct of Troubleshooting

OP-AA-108-117

Protected Equipment Program

71111.13

Procedures

WC-AA-101-1006

On-Line Risk Management and Assessment

213984

A2R15LL: S/U FW PP Press Switch Isolation Leak-By

05/10/2011

20432

2PS-FW282A Isolation Valve Leaks-By

04/02/2005

4419609

Unit 1 Core Exit Thermocouple Nozzle 74 - Connections

Swapped Affecting Indications

04/28/2021

20610

B Train Core Exit Thermocouples Not Communicating with

Plant Process Computer

05/01/2021

23740

Unit 1 Core Exit Thermocouples Exceed Allowed Maximum

Deviation

05/15/2021

28965

U-2 Startup Feedwater Pump Oil Pressure Low

06/12/2021

4436953

2FIS-0611 is Weeping Boric Acid

07/26/2021

4437474

1SX169A Failed to Open on Slow Local Start of 1A DG

07/28/2021

4443522

2A DG Bolt on 4L Cylinder Sheared During Scheduled Run

08/30/2021

Corrective Action

Documents

4447805

0B Non-Accessible Plenum Delay

09/21/2021

BwOP FW-24

Filling and Venting an Isolated Feedwater Pump

ER-AA-600-1012

Risk Management Documentation

OP-AA-106-101-

1006

Operational Decision-Making Process

OP-AA-108-111

Adverse Condition Monitoring and Contingency Planning

71111.15

Procedures

OP-AA-108-115

Operability Determinations (CM-1)

71111.19

Procedures

1BwOSR

Group A IST Requirements for 1B Safety Injection Pump

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

5.5.8.SI-10B

(1SI01PB)

1BwOSR

5.5.8.SI-1B

Train B Safety Injection System Valve Stroke Surveillance

1BwOSR

5.5.8.SI-2B

Train B Safety Injection System Isolation Valve Indication

Surveillance

SPP-21-002

Modification Test of 1SA01CA Station Air Compressor

4762173

1SI8920 Motor Operated Valve Diagnostic Test

09/14/2021

5092650

Electrical Replacement of U0 SAC EC 630879

10/06/2021

Work Orders

5175731

IST for 1SI8919A/B/8922B/8926 ASME Surveillance

Requirements for 1SI01PM

09/14/2021

Corrective Action

Documents

4438884

2A DG Lower Lube Oil Cooler Oil Leak When Running

08/04/2021

Miscellaneous

Calibration of Steam Generator 2B Main Steam Atmospheric

Relief Valve Control Loop Test Report Package

2P-MS042 BwIP 2500-070

2BwOSR 3.8.1.2-

Unit Two 2A Diesel Generator Operability Surveillance

2BwOSR

5.5.8.RH-5B

Group A IST Requirements for Residual Heat Removal

Pump 2RH01PB

Procedures

BwIP 2500-070

Calibration of Steam Generator Main Steam Atmospheric

Relief Valve Control Loop

71111.22

Work Orders

4718820

2P-MS042 S/G 2B Steam Outlet Pressure Loop

08/23/2021

71114.04

Miscellaneous

Eval No. 20-71

Emergency Action Levels for Braidwood Station,

EP-AA-1001, Addendum 3

09/08/2020

EP-AA-1000

Standardized Radiological Emergency Plan

71114.06

Procedures

EP-AA-1001

Radiological Emergency Plan Annex for Braidwood Station

71124.05

Procedures

RP-AA-700

Controls for Radiation Protection Instrumentation

AR 04359867

1st and 2nd Quarter REMP Samples to Document in

20 AREOR

07/30/2020

AR 04398177

BD-22

01/26/2021

Corrective Action

Documents

AR 04398679

3rd and 4th Quarter REMP Samples to Document in

20 AREOR

01/28/2021

71124.07

Miscellaneous

Braidwood Station Unit 1 and 2 Annual Radiological

Environmental Operating Report 2019

05/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Meteorological Tower Inspection Report

06/2019

Meteorological Tower Inspection Report

06/2020

Braidwood Nuclear Power Station Annual Radioactive

Effluent Release Report (ARERR) 2020

05/2021

Braidwood Station Unit 1 and 2 Annual Radiological

Environmental Operating Report 2020

05/2021

AR 04364522

0B RW Demin Inlet Pressure High Out of Band

08/21/2020

AR 04375152

0PL01J, Liquid RW Control Panel, Alarm Check

Unsatisfactory

10/07/2020

Corrective Action

Documents

AR 04403327

Lesson Learned: Dose Received During RW Resin Liner

Survey

2/18/2021

Miscellaneous

CFR 61 Analysis for Primary Resin Filters

04/16/2021

Procedures

RP-AA-600

Radioactive Material/Waste Shipments

RWS20-015

UN3321 LSA-II; 14 DAW Legacy Waste in Cask 14-210

08/27/2020

RWS20-018

UN2916 Type (B) Package; Resin Liner PO 692200-4

11/12/2020

RWS21-001

UN3321 LSA-II; Resin Liner P0695283-14 in Cask 14-215

01/12/2021

71124.08

Shipping Records

RWS21-015

UN2910 Limited Quantity of Material; Seven B-25 Boxes of

CP Resin

08/17/2021

NRC Performance Indicator Data; Mitigating

Systems Mitigating System Performance Index for Heat

Removal Systems

07/01/2020 -

06/30/2021

NRC Performance Indicator Data; Mitigating

Systems Mitigating System Performance Index for

Residual Heat Removal Systems

07/01/2020 -

06/30/2021

Miscellaneous

NRC Performance Indicator Data; Mitigating

Systems Mitigating System Performance Index for

Cooling Water Systems

07/01/2020 -

06/30/2021

LS-AA-2001

Collecting and Reporting of NRC Performance Indicator Data

71151

Procedures

LS-AA-2200

Mitigating System Performance Index Data Acquisition and

Reporting

4364058

Forced Helium Drying Skid Issue

08/19/2021

71152

Corrective Action

Documents

4433954

It Was Identified That Corrective Action 04364058-22 Had

Been Extended Twice, In Reviewing the CA Template, the

Extensions and Their Approvals Were Not Documented

07/08/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4434922

Level 4 Configuration Control - Received Unexpected Alarm

1-2-Ec

07/14/2021

Drawings

M-66, Sheet 3A

Diagram of Component Cooling Water, Units 1 and 2

AW

Miscellaneous

Gap Analysis for Braidwood DCS Human Performance Error

08/18/2020

2BwOSR

5.5.8.CC-3

Common Train Component Cooling Isolation Valve Stroke

Surveillance

NO-AA-10

Quality Assurance Topical Report (QATR)

OU-MW-671-300

MPC Processing Forced Helium Dehydration (FHD) for

PWRS (ISFSI)

PI-AA-120

Issue Identification and Screening Process

PI-AA-125

Corrective Action Program (CAP) Procedure

PI-AA-125-1001

Root Cause Analysis Manual

PI-AA-125-1003

Corrective Action Program Evaluation Manual

Procedures

PI-AA-125-1004

Effectiveness Review Manual

2