05000272/LER-1982-028, Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated

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Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated
ML20054E302
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/21/1982
From: Frahm R
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20054E296 List:
References
LER-82-028-03L-01, LER-82-28-3L-1, NUDOCS 8206110047
Download: ML20054E302 (1)


LER-2082-028, Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated
Event date:
Report date:
2722082028R00 - NRC Website

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o : lOn April 25, 1982, during routine operation, the Control Room Operator noticed thatl level indication showed that g l both channels of Refueling Water Storage Tank (RWST) g g lthe tank contained less than the minimum volume required by the Technical Specifi- l

[o,,,l cation. At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, the RWST was declared inoperable, and Action Statement l ITTin 13.5.5 was entered. This occurrence constituted operation in a degraded mode in l ,.

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l i l o l l The R IST contained volume was inadvertently decreased below the specification limit l W l while refilling the Spent Fuel Pool. Makeup to the RWST was initiated, and at 17291 m l hours, the contained volume was within specification. The RWST was declared I W l enerable, and Action Statenent 3.5.5 was terminated. The enerator involved was I m I counseled by the Senior Shift Supervisor concerning Technical Specification 3.5.5. I 7 ee so sTAIU %Powtm OTutmsTATus ois V otscovEnv otscaiPTioN h R d@ l 0l 6l 21hl" N/A l [Aj@l Operator Ovservation l ACTiviTV Co TENT acLEAsto oPm LEAst LoCArioN oP att Ast h 1

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