ML18107A530

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Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr
ML18107A530
Person / Time
Site: Salem PSEG icon.png
Issue date: 08/31/1999
From: Bezilla M, Knieriem R
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
LR-N99-0416, NUDOCS 9909170015
Download: ML18107A530 (4)


Text

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/Public ~ervice Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit LR-N99-0416 SEP131999 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn: Document Control Desk MONTHLY OPERATING REPORT SALEM UNIT NO. 2 DOCKET NO. 50-311 Gentlemen:

In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original Monthly Operating report for August 1999 is attached. As I

indicated in the Salem Unit 2 July Monthly Operating Report, the summary of safety evaluations for design changes implemented during July and August 1999 are included in this report.

Sincerely,

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9909170015 990831 M. 8. Bezilla , T""'

PDR ADOCK 05000311 Vice President - Operations R PDR

/rbk Enclosures C Mr. H.J. Miller Regional Administrator USNRC, Region 1 475 Allendale Road King of Prussia, PA 19046

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DOCKET NO.:

UNIT:

DATE:

50-311 Salem 2 9/15/99 COMPLETED BY: R. Knieriem TELEPHONE: (856) 339-1782 Reporting Period: August 1999 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) 1115 Maximum Dependable Capacity (MWe-Net) 1106 Month Year-to-date Cumulative No. of hours reactor was critical 744 4558 93176 No. of hours generator was on line (service hours) 744 4502 i--~~--ii--~~~~~~+-~~~~~--t 89853 Unit reserve shutdown hours 0.0 0.0 0.0 Net Electrical Energy (MWH) 787038 4742738 89715569 UNIT SHUTDOWNS NO. DATE TYPE DURATION REASON METHOD OF CORRECTIVE F=FORCED (HOURS) (1) SHUTIING ACTION/COMMENT S=SCHEDULED DOWN THE REACTOR (2)

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip/Scram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4 - Continuation E - Operator Training/License Examination 5 - Other (Explain)

F -Administrative G - Operational Error (Explain)

H - Other Summary:

Salem Unit 2 began the month of August 1999 operating at full power. Full power operation continued until August 21, when power was reduced to 37% to perform Turbine Valve Testing and to effect repairs to the 23RS6, Turbine Intercept Valve.

Salem Unit 2 returned to full power on August 22, and continued full power operation through the end of the month.

  • DOCKET NO.:
  • 50-311 UNIT: Salem 2 DATE: 9/15/99 COMPLETED BY: R. B. Knieriem TELEPHONE: (856) 339-1782

SUMMARY

OF CHANGES, TESTS, AND EXPERIMENTS FOR THE SALEM UNIT 2 GENERATING STATION MONTH: August 1999 The following items completed during August 1999 have been evaluated to determine:

1. If the probability of occurrence or the consequences of an accident or malfunction of equipment important to safety previously evaluated in the safety analysis report may be increased; or
2. If a possibility for an accident or malfunction of a different type than any evaluated previously in the safety analysis report may be created; or
3. If the margin of safety as defined in the basis for any technical specification is reduced.

The 10CFR50.59 Safety Evaluations showed that these items did not create a new safety hazard to the plant; nor did they affect the safe shutdown of the reactor. These items did not change the plant effluent releases and did not alter the existing environmental impact. The 10CFR50.59 Safety Evaluations determined that no unreviewed safety or environmental questions are involved.

Design Changes - Summary of Safety Evaluations Modification 2EC-3654, Pkg. 1, Auxiliary Annunciator (AAS) Replacement Project This modification implemented design changes to the AAS to address Year 2000 concerns. The modification included replacement of Rochester Instrument Systems (RIS) 3800 series equipment and replacement of an existing typewriter/printer unit.

Review of this modification under 10CFR50.59 was required because the replacement of the AAS equipment constituted a change to the facility as described in the UFSAR. This evaluation concluded that this change would not increase the probability or consequences of an accident previously analyzed.

Additionally, this change did not increase the probability or consequences of a malfunction of equipment important to safety. This change would not create any new accidents or malfunctions since no new failure modes were introduced. In addition the Technical Specification Bases were not affected and no changes to the Technical Specifications were required.

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Temporary Modifications - Summary of Safety Evaluations There were no changes in this category implemented during August 1999.

Procedures - Summary of Safety Evaluations There were no changes in this category implemented during August 1999.

UFSAR Change Notices - Summary of Safety Evaluations UFSAR Change Notice SCN99-048, Reactor Coolant System Chemical Degassing Operation During Shutdown This UFSAR change involved the addition of hydrogen peroxide to the Reactor Coolant System (RCS) following plant shutdown and cooldown for the purpose of chemically depleting RCS dissolved hydrogen inventory. Chemical degassing will occur only in operational Mode 5 and below.

Review of this temporary modification under 10CFRS0.59 was required because chemical degassing of the RCS constituted a change to the facility as described in the UFSAR and constituted a change to procedures as described in the UFSAR. The evaluation concluded that this change would not increase the probability or consequences of an accident previously analyzed. Additionally, this change did not increase the probability or consequences of a malfunction of equipment important to safety. This change would not create any new accidents or malfunctions since no new failure modes were introduced. In addition the Technical Specification Bases were not affected and no changes to the Technical Specifications were required.

Deficiency Reports - Summary of Safety Evaluations There were no changes in this category implemented during August 19~9.

Other - Summary of Safety Evaluations There were no changes in this category implemented during August 1999.