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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000311/LER-1990-0301990-07-24024 July 1990 LER 90-030-00:on 900703,ESF Actuation Containment Purge/ Pressure Vacuum Relief Sys Isolation Occurred After Channel Function Not Placed in Block.Caused by Personnel Error. Individuals Involved Held accountable.W/900724 Ltr 05000311/LER-1990-0271990-07-17017 July 1990 LER 90-027-00:on 900628,determined That ESF Signal Actuation 2R41C Channel Failed Low Due to 2R45 Interlock.Caused by Design/Equipment Concerns.Engineering Investigated Concerns & Uninterruptable Power Sys installed.W/900717 Ltr 05000311/LER-1990-0261990-07-0909 July 1990 LER 90-026-00:on 900609,radiation Monitoring Sys Channel 2R12B Failed Low.Caused by Design/Equipment Concerns.Failed Components Replaced & Pins Connecting Backplane Replaced W/Longer pins.W/900709 Ltr 05000311/LER-1984-010, Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed1984-05-23023 May 1984 Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed 05000272/LER-1981-059, Supplemental LER 81-059/01X-01:on 810616,during Initial Testing,Auxiliary Feedwater Pump 23 Turbine Steam Supply Check Valves 21MS46 & 23MS46 Found Damaged Internally.Caused by Steam Flow Sys Oscillations1984-02-24024 February 1984 Supplemental LER 81-059/01X-01:on 810616,during Initial Testing,Auxiliary Feedwater Pump 23 Turbine Steam Supply Check Valves 21MS46 & 23MS46 Found Damaged Internally.Caused by Steam Flow Sys Oscillations 05000272/LER-1983-062, Supplemental LER 83-062/99X-1:on 831122,during Testing on Seismic Instrumentation,Triaxial Time History Accelograph Did Not Respond as Required.Caused by Detector Failure. Accelerometer Replaced1984-02-24024 February 1984 Supplemental LER 83-062/99X-1:on 831122,during Testing on Seismic Instrumentation,Triaxial Time History Accelograph Did Not Respond as Required.Caused by Detector Failure. Accelerometer Replaced 05000272/LER-1979-068, Supplemental LER 79-068/03X-1:on 791018,safety Injection Pump Motor 12 Tripped on Overcurrent.Caused by Impeller Locknuts Improperly Secured at Mfg Facility.Pumps Reassembled Using Locktite Compound1984-02-24024 February 1984 Supplemental LER 79-068/03X-1:on 791018,safety Injection Pump Motor 12 Tripped on Overcurrent.Caused by Impeller Locknuts Improperly Secured at Mfg Facility.Pumps Reassembled Using Locktite Compound 05000311/LER-1982-141, Updated LER 82-141/03X-1:on 821121 & 1204,P-250 Computer Inoperable Due to Parity Error.Caused by Periodic Increases in Ambient Temp Due to Insufficient Ventilation.Computer Reprogrammed & Action Statement Terminated1983-12-16016 December 1983 Updated LER 82-141/03X-1:on 821121 & 1204,P-250 Computer Inoperable Due to Parity Error.Caused by Periodic Increases in Ambient Temp Due to Insufficient Ventilation.Computer Reprogrammed & Action Statement Terminated 05000272/LER-1983-023, Supplemental LER 83-023/01X-1:on 830602,notification Received from Westinghouse of Potential Unreviewed Safety Question Re Operation at Full Power Following Extended Reduced Power Operation.Procedures Implemented1983-12-13013 December 1983 Supplemental LER 83-023/01X-1:on 830602,notification Received from Westinghouse of Potential Unreviewed Safety Question Re Operation at Full Power Following Extended Reduced Power Operation.Procedures Implemented 05000272/LER-1982-024, Supplemental LER 82-024/03X-1:on 820410,svc Water Flow to Containment Fan Coil Unit 12 Discovered to Be Less than Required 700 Gpm.Caused by Valve 12SW223 Being Stuck in Closed Position.Valve Exercised1983-11-17017 November 1983 Supplemental LER 82-024/03X-1:on 820410,svc Water Flow to Containment Fan Coil Unit 12 Discovered to Be Less than Required 700 Gpm.Caused by Valve 12SW223 Being Stuck in Closed Position.Valve Exercised 05000311/LER-1982-017, Supplemental LER 82-017/03X-1:on 820228,svc Water Flow Indicated Zero Upon Starting Containment Fan Coil Unit 22 (Cfcu).On 820301,svc Water Flow to Cfcu 23 Less than Required 2,500 Gpm.Caused by Stuck Valve1983-11-17017 November 1983 Supplemental LER 82-017/03X-1:on 820228,svc Water Flow Indicated Zero Upon Starting Containment Fan Coil Unit 22 (Cfcu).On 820301,svc Water Flow to Cfcu 23 Less than Required 2,500 Gpm.Caused by Stuck Valve 05000272/LER-1982-029, Supplemental LER 82-029/03X-1:on 820501,during Surveillance Testing,Svc Water Flow to Containment Fan Coil Unit 12 Discovered Less than Required 2,500 Gallons Per Minute for Low Speed.Caused by Stuck Flow Control Valve1983-11-17017 November 1983 Supplemental LER 82-029/03X-1:on 820501,during Surveillance Testing,Svc Water Flow to Containment Fan Coil Unit 12 Discovered Less than Required 2,500 Gallons Per Minute for Low Speed.Caused by Stuck Flow Control Valve 05000311/LER-1982-001, Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed1983-11-11011 November 1983 Supplemental LER 82-001/03X-1:on 820110,steam Generator 24 Pressure Channel 4 Failed High.Caused by Ventilation Damper Stuck Open,Freezing Pressure Sensing Line.Damper Freed, Exercised & Closed 05000311/LER-1983-017, Supplemental LER 83-017/03X-1:on 810515,during Startup & Cycle 1 Operations,Leakage Past Pressurizer PORVs & Pressurizer Overpressure Protection Sys Values Observed. Cause Not Stated.Porvs Modified1983-09-16016 September 1983 Supplemental LER 83-017/03X-1:on 810515,during Startup & Cycle 1 Operations,Leakage Past Pressurizer PORVs & Pressurizer Overpressure Protection Sys Values Observed. Cause Not Stated.Porvs Modified 05000272/LER-1983-008, Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions1983-07-13013 July 1983 Supplemental LER 83-008/03X-1:on 830311,pressurizer Code Safety Valves 1PR3,1PR4 & 1PR5 Exceeded Lift Set Pressure Range & Had Heavy Seat Leakage.Partly Caused by Difference in Test Vs Actual Operating Conditions 05000311/LER-1982-077, Supplemental LER 82-077/01X-1:on 820818,leakage Discovered from Containment Fan Coil 21.Caused by Erosion of Copper Nickel Piping.Cooling Coils Replaced w/erosion-resistant Matl1983-06-29029 June 1983 Supplemental LER 82-077/01X-1:on 820818,leakage Discovered from Containment Fan Coil 21.Caused by Erosion of Copper Nickel Piping.Cooling Coils Replaced w/erosion-resistant Matl 05000311/LER-1982-024, Supplemental LER 82-024/03X-1:on 820328,sample Results from Boric Acid Storage Tank 21 & Boron Injection Tank 22 Indicated Concentrations Below Tech Spec Limit.Cause Unknown.Boric Acid Added1983-06-29029 June 1983 Supplemental LER 82-024/03X-1:on 820328,sample Results from Boric Acid Storage Tank 21 & Boron Injection Tank 22 Indicated Concentrations Below Tech Spec Limit.Cause Unknown.Boric Acid Added 05000311/LER-1982-070, Supplemental LER 82-070/01X-1:on 830809,0.5 Gpm Svc Water Leak Observed on Containment Fan Coil 24.Caused by Failed Cooling Coil Resulting from Silt Erosion by Particles in Svc Water1983-06-29029 June 1983 Supplemental LER 82-070/01X-1:on 830809,0.5 Gpm Svc Water Leak Observed on Containment Fan Coil 24.Caused by Failed Cooling Coil Resulting from Silt Erosion by Particles in Svc Water 05000311/LER-1982-092, Supplemental LER 82-092/01X-1:on 820908,svc Water Leak Discovered on Containment Fan Coil Unit 21,rendering Unit Inoperable.Caused by Motor Cooler Erosion Due to Silt in Svc Water.Cooler Replaced1983-06-29029 June 1983 Supplemental LER 82-092/01X-1:on 820908,svc Water Leak Discovered on Containment Fan Coil Unit 21,rendering Unit Inoperable.Caused by Motor Cooler Erosion Due to Silt in Svc Water.Cooler Replaced 05000272/LER-1982-090, Supplemental LER 82-090/01X-1:on 821121,video Insp of Removed Fuel Assemblies Revealed Cladding Ruptures on Element 13 in Fuel Assembly D-20.Caused by Isolated Instance of Secondary Hydriding1983-06-29029 June 1983 Supplemental LER 82-090/01X-1:on 821121,video Insp of Removed Fuel Assemblies Revealed Cladding Ruptures on Element 13 in Fuel Assembly D-20.Caused by Isolated Instance of Secondary Hydriding 05000311/LER-1983-023, Corrected LER 83-023/03L-0:on 830117-0418,seven Containment Isolation Valves Experienced Leakage Rates Greater than Max Range of Test Equipment.Total Containment Type B & C Leakage Could Not Be Demonstrated.Valves Repaired1983-06-0808 June 1983 Corrected LER 83-023/03L-0:on 830117-0418,seven Containment Isolation Valves Experienced Leakage Rates Greater than Max Range of Test Equipment.Total Containment Type B & C Leakage Could Not Be Demonstrated.Valves Repaired 05000272/LER-1982-091, Supplemental LER 82-091/01X-1:on 821130,operator Discovered Leakage from Weld of Svc Water Piping to Component Cooling HX 12.Caused by Extensive Biofouling & Corrosion of Circumferential Welds1983-06-0808 June 1983 Supplemental LER 82-091/01X-1:on 821130,operator Discovered Leakage from Weld of Svc Water Piping to Component Cooling HX 12.Caused by Extensive Biofouling & Corrosion of Circumferential Welds 05000272/LER-1982-083, Supplemental LER 82-083/03X-1:on 821102,control Room Operator Observed Temp Recorder for Air temp-delta T Channels Not Printing.Caused by Failure of Pinion Gear on Chart Drive Motor.Motor Replaced1983-06-0101 June 1983 Supplemental LER 82-083/03X-1:on 821102,control Room Operator Observed Temp Recorder for Air temp-delta T Channels Not Printing.Caused by Failure of Pinion Gear on Chart Drive Motor.Motor Replaced 05000272/LER-1982-035, Supplemental LER 82-035/99X-1:on 820526,fire Pump 2 Failed to Start.Caused by Damaged Fire Pump Electrical Sys Voltage Regulator/Alternator,Due to Faulty Wiring Harness.Damaged Components Replaced1983-06-0101 June 1983 Supplemental LER 82-035/99X-1:on 820526,fire Pump 2 Failed to Start.Caused by Damaged Fire Pump Electrical Sys Voltage Regulator/Alternator,Due to Faulty Wiring Harness.Damaged Components Replaced 05000311/LER-1982-083, Supplemental LER 82-083/03X-1:on 820812,during Routine Surveillance,Control Room Operator Received Low Svc Water Flow Indication on Containment Fan Coil Unit (Cfcu) 25. Caused by Oysters or Silt Restricting Cfcu Flow1983-04-20020 April 1983 Supplemental LER 82-083/03X-1:on 820812,during Routine Surveillance,Control Room Operator Received Low Svc Water Flow Indication on Containment Fan Coil Unit (Cfcu) 25. Caused by Oysters or Silt Restricting Cfcu Flow 05000272/LER-1981-121, Supplemental LER 81-121/03X-1:on 811228,svc Water Leak in Spool Piece Discovered Between Valves 12SW57 & 58.Design Change Package 1EC-0504 Implemented to Replace Piece W/Stainless Steel for Improved Corrosion Resistance1983-03-30030 March 1983 Supplemental LER 81-121/03X-1:on 811228,svc Water Leak in Spool Piece Discovered Between Valves 12SW57 & 58.Design Change Package 1EC-0504 Implemented to Replace Piece W/Stainless Steel for Improved Corrosion Resistance 05000272/LER-1982-081, Supplemental LER 82-081/01X-1:on 821104,16 1,000-kip Steam Generator Snubbers Found Out of Spec on Bleed Test & Six Snubbers Failed Acceleration Test.Caused by Flattened Piston Seal Rubber Matl Due to Aging.Seals Rebuilt1983-03-0303 March 1983 Supplemental LER 82-081/01X-1:on 821104,16 1,000-kip Steam Generator Snubbers Found Out of Spec on Bleed Test & Six Snubbers Failed Acceleration Test.Caused by Flattened Piston Seal Rubber Matl Due to Aging.Seals Rebuilt 05000272/LER-1983-012, Telecopy Message of LER 83-012/01P-0:on 830222,both Reactor Trip Breakers Failed to Open.Cause Not Yet Determined. Investigation Underway1983-02-28028 February 1983 Telecopy Message of LER 83-012/01P-0:on 830222,both Reactor Trip Breakers Failed to Open.Cause Not Yet Determined. Investigation Underway 05000311/LER-1983-007, Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days1983-02-18018 February 1983 Telecopy Message of LER 83-007/01P:on 830218,two 1,000-kip Steam Generator Snubbers Failed to Meet Lockup & Bleed Rate Velocity Requirements.Cause Not Stated.Investigation Continuing.Detailed Rept to Be Submitted in 14 Days 05000272/LER-1982-002, Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing1982-12-29029 December 1982 Supplemental LER 82-002/01X-2:on 820119,during Surveillance, Indications of Tube Thinning Detected by Eddy Current Exam. Tubes Above 30% Degradation Plugged.Tube R44C62 Sent to Westinghouse for Chemical & Metallurgical Testing 05000272/LER-1982-008, Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added1982-12-29029 December 1982 Supplemental LER 82-008/03X-1:on 820126,boric Acid Concentrations in Boric Acid Storage Tanks 11 & 12 Found Below Tech Spec Limit.Caused by Dilution of Concentration by Flushing Water in Tank Following Maint.Boric Acid Added 05000311/LER-1982-015, Supplemental LER 82-015/03X-1:on 820221,discovered That Reactor Coolant Leak Rate Surveillance 4.4.7.2.d Due 820220 Not Performed Because Plant Had Not Been in steady-state Condition Due to 820219 Reactor Trip1982-12-0808 December 1982 Supplemental LER 82-015/03X-1:on 820221,discovered That Reactor Coolant Leak Rate Surveillance 4.4.7.2.d Due 820220 Not Performed Because Plant Had Not Been in steady-state Condition Due to 820219 Reactor Trip 05000311/LER-1981-089, Supplemental LER 81-089/03X-1:on 810817,during Routine Wear & Alignment Check,Auxiliary Feedwater Pump 23 Linkage Between Trip Mechanism & Valve Found Loose.Caused by Loose Bolts.Bolts Tightened1982-11-0303 November 1982 Supplemental LER 81-089/03X-1:on 810817,during Routine Wear & Alignment Check,Auxiliary Feedwater Pump 23 Linkage Between Trip Mechanism & Valve Found Loose.Caused by Loose Bolts.Bolts Tightened 05000311/LER-1982-027, Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State1982-10-20020 October 1982 Supplemental LER 82-027/03X-1:on 820418,RCS Water Inventory SP(o)4.4.7.2.d Not Performed within Required Time Interval. License Change Request 82-14 Submitted to Eliminate RCS Water Inventory Requirement During Nonsteady State 05000272/LER-1982-042, Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised1982-10-20020 October 1982 Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised 05000272/LER-1982-009, Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage1982-10-20020 October 1982 Supplemental LER 82-009/03X-1:on 820118 & 25,Cardox Fire Suppression Sys for 1A,1B & 1C Diesel Generator Areas & Fuel Oil Storage Area 12 Inoperable for More than 14 Days.Caused by Sys in Manual Mode Due to Maint Outage 05000311/LER-1982-002, Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Vo1982-10-20020 October 1982 Supplemental LER 82-002/03X-1:on 820111,battery Charger 2A1 Tripped.Charger Tripped Again Upon Resetting Breaker.Caused by Difference Between Battery & Battery Charger Voltages. Operating Instructions Revised to Adjust Float Voltage 05000311/LER-1982-072, Supplemental LER 82-072/03X-1:on 820820,during Surveillance Testing,Discovered That Reactor Trip Breaker B Would Not Trip.Caused by Binding of Undervoltage Coil Solenoid.Coil Replaced & Breaker Reinstalled1982-10-20020 October 1982 Supplemental LER 82-072/03X-1:on 820820,during Surveillance Testing,Discovered That Reactor Trip Breaker B Would Not Trip.Caused by Binding of Undervoltage Coil Solenoid.Coil Replaced & Breaker Reinstalled 05000272/LER-1982-004, Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration1982-10-20020 October 1982 Supplemental LER 82-004/03X-1:on 820108,charging Pump 13 Declared Inoperable Due to Component Cooling Water Sys Being Tagged Out for Planned Maint.On 820109,positive Reactivity Change Found in RCS Boron Concentration 05000311/LER-1982-111, Telecopy Message of LER 82-111/01P:on 821002,during Routine Power Operation,Svc Water Leak Discovered Inside Containment Bldg on Containment Fan Coil Unit 23.Cause Undetermined.Rept Will Be Submitted Per IE Bulletin 80-241982-10-0404 October 1982 Telecopy Message of LER 82-111/01P:on 821002,during Routine Power Operation,Svc Water Leak Discovered Inside Containment Bldg on Containment Fan Coil Unit 23.Cause Undetermined.Rept Will Be Submitted Per IE Bulletin 80-24 05000311/LER-1982-084, Telecopy Message of LER 82-084/01P:on 820829,svc Water Leak on Containment Fan Coil Unit 23 Discovered.Leak Isolated.No Cause Stated.Investigation in Progress1982-08-30030 August 1982 Telecopy Message of LER 82-084/01P:on 820829,svc Water Leak on Containment Fan Coil Unit 23 Discovered.Leak Isolated.No Cause Stated.Investigation in Progress 05000311/LER-1982-074, Corrected LER 82-074/01T-0:on 820813,control Operator Discovered Increased Leakage to Containment Sump.Caused by Coil Failures Due to Silt Particles in Svc Water.Leak Repaired by Blanking Flanges1982-08-18018 August 1982 Corrected LER 82-074/01T-0:on 820813,control Operator Discovered Increased Leakage to Containment Sump.Caused by Coil Failures Due to Silt Particles in Svc Water.Leak Repaired by Blanking Flanges 05000272/LER-1982-0031982-05-26026 May 1982 LER 82-03L/031-0:on 820502,while Testing Valve 11SW122, Safeguards Equipment Control Cabinet Actuation Occurred. Caused by Locked Out Supply Breaker to Safety Injection Pump 11,due to Spurious Nature of Actuation 05000272/LER-1982-028, Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated1982-05-21021 May 1982 Corrected LER 82-028/03L-0:on 820425,both Channels of Refueling Water Storage Tank (RWST) Level Indication Showed Less than Min Vol.Caused by Refilling Spent Fuel Pool. Makeup to RWST Initiated 05000311/LER-1982-0191982-03-31031 March 1982 LER 82-019/03L-0:on 820307,undervoltage Condition in Safeguards Equipment Control Cabinet Caused Mod 1 2A Sec Actuation.Caused by Failure of Card File Assembly.Card File Assembly Replaced & Loads Secured.Sys Returned to Svc 05000272/LER-1982-0141982-03-31031 March 1982 LER 82-014/03L-0:on 820306,wind Speed Indications for 150 & 300-ft Elevations Failed.Local Indications Also Failed. Caused by iced-up Anemometers.Anemometers Thawed & Declared Operable 05000311/LER-1982-0181982-03-31031 March 1982 LER 82-018/03L-0:on 820304,steam Generator 24 Feedwater Channel 2 Flow Indicator Failed.Caused by Failure of Force Motor in Flow Transmitter.Transmitter Properly Repaired, Calibr & Returned to Svc 05000272/LER-1981-0921981-11-0202 November 1981 LER 81-092/01T-0:on 811020,during Routine Containment Insp, Operator Discovered Svc Water Leaking from Third from Top Secondary Coil on Containment Fan Coil Unit 15.Caused by Secondary Coil Failure.Leaking Coil Blank Flanged Off 05000311/LER-1981-0361981-07-0606 July 1981 LER 81-036/03L-0:on 810606,pressurizer Pressure Channel 1 Indicated Greater than Max Allowable Tolerance.Caused by Pressure Transmitter 2PT455 Out of Spec.Unit Calibr & Returned to Svc 05000272/LER-1976-030, Updated LER 76-030/03L:on 761228,during Sample Analysis of Boric Acid Storage Tanks 11 & 12,boron Concentration Noted Low.Cause Unknown.Chemical Analysis After Batching Confirmed Findings1978-04-0404 April 1978 Updated LER 76-030/03L:on 761228,during Sample Analysis of Boric Acid Storage Tanks 11 & 12,boron Concentration Noted Low.Cause Unknown.Chemical Analysis After Batching Confirmed Findings 1990-07-09
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
LER-2084-010, Corrected LER 84-010-00:on 840423,during Startup Operations, Turbine Trip & Reactor Trip Occurred.Caused by hi-hi Level in Steam Generator 23.Feedwater Flow Nozzle Replaced & All Sys Performed as Designed |
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3112084010R00 - NRC Website |
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UCENSEE EVENT REPORT (LER)
OOCE ST " *-" A m meu m PACILITY IsAan pp Salem Generating Station - Unit 2 o ,5 ,o ,o ,o,3 gli l i jo,l0 ,7 TiTLS 646 Reactor Trips From 22% & 30% - High-High Level #23 Steam Generator Lan ~ R le REPOft? OATS 171 OTMER FACILITIES tefv0Lvec WI SVeNT OATS m DOCKET muassene escasTM OAv vfAA VEAR .*.M h*' EM esONTN DAV v5AR ' ace 6sTv asansse oimiviogo; i l 0l4 2l3 84 TMis 8l4 0l 1l 0 0 l0 0 l5 2l3 8l4 oisio s o s oi ; i nepoaf W suennTYsO puasuA=7 TO Two asauimense=To os se Cra O rCa e ., er sae sw= ist nu se.,,,,,mo,e moos m 1 m _
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AssTnACT ro . ..se .--I. , A. _ _ ~ ase. --e m , nei On April 23, 1984, a turbine trip and reactor trip occurred during unit startup operations, due to high-high level in No. 23 Steam l
Generator. The event was attributed to sluggish response of the Feeduater Level Control System during low power operation, with minor binding of the Feedwater Control Valve Bypass Valve suspected of contributing to the magnitude of steam generator level swing.
The valve was repaired and a f alse load was established with the Main Steam atmospheric vents during the subsequent startup. On April 27, a similar event occurred. Because the previous corrective actions had failed to remedy No. 23 Steam Generator level instability problem, the entire Feedwater Level Control System was extensively tested. The system was instrumented in order to continue During this the testing at low power with the turbine not latched.
testing, on April 28, No. 23 Steam Generator Feedwater Flow indi-cation failed to respond. The Feedwater Flow Channels were declared inoperable, and a unit shutdown was performed.
Radiography revealed that the feedwater flow nozzle had moved from its designed location.
This apparently occurred as a result of a feedwater water hammer incident which occurred on April 6, 1984. The feedwater flow nozzle was replaced, and all systems performed as designed during the subsequent startup on May 5, 1984.
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LICENSEE EVENT REPORT (LER) TEXT CONTINUATION empires 8/3146 8 ActLsTV esassa gig OOCKET seuasetR 12) LER NuesBER ISI PAQs (3p Salem Generating Station n.. nog;p,*6 gg Unit 2 olsjojojol3ll]l 8l 4 --
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0] O 0l 2 OF 0l7 Tufn, . e ss ance ,astwim PLANT AND SYSTEM IDENTIFICATION:
Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as (XX).
l IDENTIFICATION OF OCCURRENCES:
i l
Reactor Protection System (JC) - Reactor Trips From 22% & 30% -
i High High Level #23 Steam Generator - (Reactor Trips #84-07 and l #84-09) l Event Dates: 04/23/84 04/27/84 Report Date: 05/23/84 .
This report was initiated by Incident Reports84-058 & 84-060 CONDITIONS PRIOR TO OCCURRENCES:
I 04/23/84 - Mode 1 - Rx Power 022% - Unit Load 0075 MWe 04/27/84 - Mode 1 - Rx Power 030% - Unit Load 0120 MWe DESCRIPTION OF OCCURRENCES:
On April 23, 1984, unit startup operations were in progress. The generator was synchronized with the grid at 1554 hours0.018 days <br />0.432 hours <br />0.00257 weeks <br />5.91297e-4 months <br />. All Steam Generator Feedwater Level Control Systems (JB) were in automatic; and, No. 23 Steam Generator was experiencing fif teen to twenty percent (15% to 20%) level oscillations. At 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, a turbine trip and reactor trip occurred due to high-high level in No. 23 Steam Generator.
The Steam Generator Feedwater Level Control System is normally a three (3) element control system, during automatic operation. It receives signals from steam flow, feed flow and steam generator level error. At very low power levels the control system senses only the steam generator level error signal, because of the minimum steam flow and feed flow conditions. A steam generatorThis level change has to occur before the level controller can respond. results in sluggish response and overcompensation by the controller; and consequently, relatively large deviations from the level setpoint.
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( DESCRIPTION OF OCCURRENCES: (continued)
Following this particular occurrence, 23BF19 and 23BF40 (No. 23 Steam Generator Feedwater Control Valve and Bypass Valve, respectively) were stroked. Investigation indicated that the packing was slightly
" cocked" on 23BF40, causing the valve to " pop" open. It was felt that this could possibly be contributing to the magnitude of level swing associated with No. 23 Steam Generator. ,
Permission to perform a unit startup was given pending completion of l repairs to 23BF40 packing. Instructions were also issued to the i operators to establish a dummy load on the reactor using the MS10 )
valves (Main Steam Atmospheric Vents), and to place Steam Generator Feedwater Level Control in manual if the level was observed to spike higher than fifty percent (50%) by Narrow Range Level Indication.
In addition, because of previous problems with level control during low power levels, an engineering investigation into possible future ,
system changes was requested. l A reactor startup was performed on April 24, 1984; but a reactor trip occurred before the corrective actions taken (following the trip on April 23, 1984) could be verified to have remedied the level 1 instability of No. 23 Steam Generator. The trip on April 24, 1984 )
was caused by a late opening turbine stop valve, with a subsequent i momentary steam flow spike, resulting in a steam flow / feed flow
- mismatch with a concurrent twenty-five percent (25%) level in No. 21 l Steam Generator. Since this trip was unrelated to the trip on April .
l
' 23, 1984, the circumstances surrounding that occurrence are docu- 1 mented in LER 84-012-00.
On April 27, 1984, unit startup operations were again in progress, with all Steam Generator Feedwater Level Control Systems being ]
monitored very closely. The generator was synchronized with the l
l grid at 1920 hours0.0222 days <br />0.533 hours <br />0.00317 weeks <br />7.3056e-4 months <br />. No. 21, 22 and 24 Steam Generator Feedwater Level Control Systems had been placed in automatic prior to l
synchronization. In accordance with the previous recommendations, reactor power was increased utilizing the MS10 valves. At 19 23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />, when reactor power level reached thirty percent (30 %) , No.
23 Steam Generator Feedwater Level Control System was placed in automatic. Level in No. 23 Steam Generator rapidly increased, resulting in a turbine and reactor trip due to high-high level in No. 23 Steam Generator. The trip occurred before the level control system could be returned to manual.
Following this occurrence, it was recognized Ehat the corrective l
actions taken (following the trip on April 23, 1984) were not successful in solving the level instability of No. 23 Steam Generator. As a result, additional measures related to the entire l
Steam Generator Veedwater Level Control System were ordered.
These actiona are as follows:
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UCENSEE EVENT REPORT (LER) TEXT CONTINUATION ExPings gr3t g6 paClurv senase 113 Cocker 8eveEBER (21 (ER =UnaSGA tEl Pact (36 Salem Generating Station i.a "M,2 i -"l'Jf;p Unit 2 o l5 l0 l0 10 l 31 11 1 44 -
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A complete channel calibration procedure was performed for No. 23 Steam Generator Process Control System. The output of the valve l
demand controller (2FC500C) was found to be failed low. The controller would not integrate up, regardless of feed flow / steam
( flow mismatch and/or level error input signals. The controller i was replaced, and the calibration procedure was satisfactorily completed.
Feedwater flow, steam flow and level recorders for all steam generators were calibrated. 23BF40 was stroked; the stroke was satisfactory, and its operation was smooth. No. 23 Steam Generator Process Control Loop was instrumented for subsequent startup; this included feedwater flow and steam flow process input, feedwater flow / steam flow signal summator output, level error output, controller 2FC500C output, and 23BF40 valve position. Sensor calibrations were completed on No. 23 feedwater flow (Cnannel I and Channel II) transmitters. A blowdown of all steam generator feed-water flow transmitter sensing lines was performed. All lines were clear with the exception of No. 23 Steam Generator Channel II.
The high side transmitter line was plugged.
Af ter reviewing the results of these investigations and corrective actions, it was concluded that the cause of the occurrence was the plugged high side sensing line of No. 23 Steam Generator Feedwater Flow Transmitter. The Station Operations Review Committee felt that the failed valve demand controller may have been a contributing factor, even though it was failed low (when discovered) ; which, would not have caused a high level situation. Unit startup was authorized, providing the level control systems were monitored closely for proper operation, with additional test instrumentation installed, prior to turbine latching and generator synchronization.
On April 28, 1984, a unit startup was performed. Reactor power was l
held at six percent (6%) while testing continued. While performing comparison checks of No. 23 Steam Generator Feedwater Control Valve (23BF19) demand signals and observing the operation of 23BF19, and also monitoring No. 23 Steam Generator level, it was discovered that feedwater flow indication failed to respond. No. 23 Steam Generator Feedwater Flow (Channels I and II) were declared inoperable. At 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br /> Technical Specification Limiting Condition For Operation 3.0.3 was entered. At 0023 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />, April 29, 1984, the unit was placed in hot standby in accordance with the Technical Specification requirements. This occurrence is documented in LER 84-011-00.
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Expents S/3115 8actLITV 8eamet (16 00CK87 8evadBER tal LER NutaBER (66 Paes tas Salem Generating Station via= aog ar g Unit 2 o s 10 l 0 lo l 3l 11 1814 -
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0 l0 0 l5 or 0 [7 rext n . ames anewnn APPARENT CAUSE OF OCCURRENCES: l As a result of the testing, which was performed during low power l operation following the unit startup on April 28, 1984, it was I suspected that No. 23 Feedwater Flow Nozzle (which provides the pressure drop for flow measurements used for indication, level )
control and protection signals) was not functioning properly; <
resulting in the inoperability of the feedwater flow channels.
Radiography results, following the controlled shutdown, revealed that the nozzle was located approximately twenty-four inches (24")
from its design location. The pins which hold the nozzle in place I were apparently broken during a feedwater water hammer which .
occurred on April 6, 1984. l 1
That occurrence was due to the failure of 23BF22 (No. 23 Steam l Generator Feedwater Stop Check Valve) to " check" closed against steam generator pressure, while performing surveillance testing on 23BF19 (No. 23 Steam Generator Feedwater Regulating Valve). -
l That occurrence is fully' documented in Engineering Evaluation l S-2-F300-MEE-021. This was determined to be the cause of the l reactor trips which occurred on April 23, and April 27, 1984. )
I ANALYSIS OF OCCURRENCES:
The turbine trip, on high-high level in the steam generator, is an anticipatory trip. The primary function of this turbine trip is to prevent moisture carry-over, and subsequent damage to the turbine blades. The primary function of the reactor trip, on turbine trip, is to prevent steam generator safety valve actuation, due to the l steam generator pressure increase, in the event that a turbine trip ,
occurs during power operation. A turbine trip is sensed by two (2) (
out of three (3) signals from low autostop oil pressure or all turbine steam stop valves closed signals. A turbine trip causes a j direct reactor trip above approximately ten percent (10%) reactor i power (P-7 interlock circuitry) , and results in a controlled short l l
term release of steam to the turbine condenser. This steam release removes sensible heat from the RCS, and thereby avoids steam generator safety valve actuation. This reactor trip is anticipatory, and included as part of good engineering practice and prudent design. ;
No credit is taken in any of the safety analyses for this trip.
Reactor protection during startup operations is provided by the l
J Source Range, Intermediate Range and low setting of the Power Range neutron flux trips. In both occurrences, the Reactor Protection System (JC) functioned as designed. These occurrences involved no undue risk to the health or safety of the public. Because of the automatic act ation of the Reactor Protection System, the events are reportable in accordance with the Code of Federal Regulations, j 10CFR 50.73 (a) (2) (iv) .
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EXPIRES 8/3i/06
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Following the reactor trip on April 23, 1984, a review of the strip ;
charts indicated zero feed flow to No. 23 Steam Generator; although, I it was extremely hard to tell at that power level. This indication I was questioned at that time, but was explained as inaccuracy of the l strip chart recorders during low power operation.
was authorized pending repairs to 23BF40 packing. Areactorstartupl In addition, special instructions were issued to the operators, and close monitoring of the level control systems was ordered.
Following the trip on April 27, 1984, a review of the strip charts revealed the same indication. Since reactor power level was at thirty percent (30%) prior to the trip, it was realized that the inaccuracy of the strip chart recorders during low power operation was no longer a plausible explanation. Although a plugged high side sensing line of No. 23 Feed Flow Transmitter was the suspected cause, further testing was scheduled to confirm these suspicions. ,
No. 23 Steam Generator Process Control Loop was instrumented, and a unit startup was authorized, providing testing verified proper level control system operation prior to turbine latching and synchroni-zation. When subsequent testing revealed the malfunctioning feed-water flow channels, the unit was placed in hot standby, in accordance with Technical Specification requirements.
No. 23 Feedwater Flow Nozzle was replaced with No. 13 Feedwater Flow Nozzle (from Unit 1, which is presently in a refueling outage). The feed flow transmitters associated with No. 23 Steam Generator were calibrated, utilizing the new data associated with the replacement 1984.
nozzle. A unit startup was commenced at 0541 hours0.00626 days <br />0.15 hours <br />8.945106e-4 weeks <br />2.058505e-4 months <br />, May 5, Criticality wac achieved at 1245 hours0.0144 days <br />0.346 hours <br />0.00206 weeks <br />4.737225e-4 months <br />, and the generator was synchronized at 1731 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.586455e-4 months <br />. All Steam Generator Water Level Control Systems functioned as designed.
The Station Operations Review Committee (SORC) questioned After subsequent the effectiveness of the post-trip review procedures.
investigations, it was determined that the post-trip review procedures were adequate and had identified a questionable feed flow indication (following the trip on April 23, 1984); however, the explanation offered was incorrect. A memorandum will be issued (with a copy of this LER attached) to all SORC members and alternates, and to those personnel involved in the post trip review. The memorandum will address the lessons learned from these events, with the intent of improving the overall quality of the post trip review process.
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LICENIEE EVENT REPORT (LER) TEXT CONTINUATION EMPIRES e/3146 00CEST "?"' A Gi LER Nuante tel FAGE(3 FACILaTV esAant its Salem Generating Station vE*a aogp, ' :
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Salem Operations JLR:kil SORC Mtg.84-058 i
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O PSEG Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station May 25, 1984 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 84-010-00 This letter is to correct an error in previously submitted LER 84-010-00 dated May 23, 1984. On page 6 of 7, line 6 23BF40 was erroneously reported as 23BF23. The corrected report is attached.
Sincerely yours, J.M. Zupko, Jr. ~
General Manager -
Salem Operations JR:kil W.
CC: Distribution f
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O PSEG Public Service Elec'5ic and Gas Company P b. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station May 23, 1984 i
U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-75 DCCKET NO. 50-311 4 UNIT NO. 2 -
LICENSEE EVENT REPORT 84-010-00 This Licensee Event Repor't is being submitted, pursuant to the requirements of 10CFR 50.73 (a) (2) (iv) . This report is required within thirty (30) days of discovery.
Sincerely yours, l
J. M. Zupko, Jr.
General Manager -
Salem Operations JR:kil CC: T>is tributian tb
- , f T$k The Energy People
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