ML082270712

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IR 05000454-08-003; 05000454-08-003, on April 01 2008 - June 30, 2008, Byron Station, Units 1 and 2; Fire Protection, Inservice Inspection Activities, Maintenance Effectiveness and Maintenance Risk Assessments and Emergent Work Control
ML082270712
Person / Time
Site: Byron  Constellation icon.png
Issue date: 08/14/2008
From: Pederson C
Division Reactor Projects III
To: Pardee C
Exelon Generation Co, Exelon Nuclear
References
EA-08-197 IR-08-003
Download: ML082270712 (76)


See also: IR 05000454/2008003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

August 14, 2008

EA-08-197

Mr. Charles G. Pardee

Chief Nuclear Officer and

Senior Vice President

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: BYRON STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION

REPORT 05000454/2008-003 05000455/2008-003 PRELIMINARY

WHITE FINDING

Dear Mr. Pardee:

On June 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Byron Station, Units 1 and 2. The enclosed report documents the inspection

findings, which were discussed on July 10, 2008, with Mr. D. Hoots and other members of your

staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The enclosed inspection report discusses a finding that appears to have low to moderate safety

significance. As documented in Section 1R13 of this report, the licensee inadvertently entered

an elevated risk condition for Unit 2 in April 2008. At that time, the two Unit 1 essential service

water train cross-tie isolation valves were out of service for maintenance. These two valves

were opened locally to support the Unit 1 Train A emergency diesel generator testing and could

not to be closed from the main control room. The licensee later determined that this

configuration represented an elevated risk condition for Unit 2 due to degraded internal flood

mitigation capability.

This finding was assessed based on the best available information, including influential

assumptions, using the applicable significance determination process (SDP) and was

preliminarily determined to be of low to moderate safety significance (White) for Unit 2 and of

very low safety significance (Green) for Unit 1. The safety significance of the finding was

determined assuming a Unit 1 essential service water pipe break in the auxiliary building that is

not isolated due to unavailability of the two Unit 1 train cross-tie isolation valves and an

exposure time of 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br />. The final resolution of this finding will convey the increment in the

importance to safety by assigning the corresponding color i.e. (White), a finding with some

increased importance to safety, which may require additional NRC inspection.

C. Pardee -2-

This finding was not an immediate safety concern because upon identification Byron Station

took immediate actions to assign a dedicated operator to locally close the valves when

necessary and to restore the remote actuation capability from the main control room. You have

also entered the issue into your corrective action program (CAP).

Based on the results of this inspection, one apparent violation was identified for Unit 2

and is being considered for escalated enforcement action in accordance with the NRC

Enforcement Policy. The current Enforcement Policy is included on the NRCs Web site at

http://www.nrc.gov/reading-rm/adams.html.

In accordance with Inspection Manual Chapter (IMC) 0609, we intend to complete our

evaluation using the best available information and issue our final determination of safety

significance within 90 days of this letter.

The significant determination process encourages an open dialog between the staff and

the licensee, however the dialogue should not impact the timeliness of the staffs final

determination. Before the NRC makes its enforcement decision, we are providing you an

opportunity to either: (1) present to the NRC your perspectives on the facts and assumptions,

used by the NRC to arrive at the finding and its significance at a Regulatory Conference or

(2) submit your position on the finding to the NRC in writing. If you request a Regulatory

Conference, it should be held within 30 days of the receipt of this letter and we encourage you

to submit supporting documentation at least one week prior to the conference in an effort to

make the conference more efficient and effective. If a conference is held, it will be open for

public observation. The NRC will also issue a press release to announce the conference. If

you decide to submit only a written response, such submittal should be sent to the NRC within

30 days of the receipt of this letter. If you decline to request a Regulatory Conference or to

submit a written response, your ability to appeal the final SDP determination can be affected, in

that by not doing either you fail to meet the appeal requirements stated in the Prerequisite and

Limitation sections of Attachment 2 of IMC 0609.

Please contact Richard Skokowski at 630-829-9620 within 10 days of the date of this letter to

notify the NRC of your intended response. If an adequate response is not received within the

time specified or an extension of time has not been granted by the NRC, the NRC will proceed

with its enforcement decision and you will be advised by separate correspondence of the results

of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for these inspection findings at this time. Please be advised that the number and

characterization of apparent violations described in the enclosed inspection report may change

as a result of further NRC review. You will be advised by separate correspondence of the

results of our deliberations on this matter. Since the finding for Unit 1 is of very low safety

significance, it is being treated as a Licensee Identified Non-Cited Violation in this report.

In addition, three NRC-identified and one self-revealed findings of very low safety significance

(Green) were also documented in the enclosed inspection report. All four findings were

determined to involve violations of NRC requirements. However, because of their very low

safety significance, and because the issues were entered into your CAP, the NRC is treating the

issues as Non-Cited Violations in accordance with Section VI.A.1 of the NRC Enforcement

Policy. Furthermore, three licensee identified violations are listed in Section 4OA7 of this report.

C. Pardee -3-

If you contest the subject or severity of the Non-Cited Violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial,

to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director,

Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and

the Resident Inspector Office at the Byron Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room). To the extent possible, you response should not include any

personal privacy, proprietary, or safeguards information so that it can be made available to the

Public without redaction.

Sincerely,

/RA/

Cynthia D. Pederson, Director

Division of Reactor Projects

Docket Nos. 50-454; 50-455

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report 05000454/2008-003; 05000455/2008-003

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Byron Station

Plant Manager - Byron Station

Regulatory Assurance Manager - Byron Station

Chief Operating Officer and Senior Vice President

Senior Vice President - Midwest Operations

Senior Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director - Licensing and Regulatory Affairs

Manager Licensing - Braidwood, Byron, and LaSalle

Associate General Counsel

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

J. Klinger, State Liaison Officer,

Illinois Emergency Management Agency

P. Schmidt, State Liaison Officer, State of Wisconsin

Chairman, Illinois Commerce Commission

B. Quigley, Byron Station

C. Pardee -3-

If you contest the subject or severity of the Non-Cited Violations, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial,

to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,

DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory

Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director,

Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and

the Resident Inspector Office at the Byron Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the

Public Electronic Reading Room). To the extent possible, you response should not include any

personal privacy, proprietary, or safeguards information so that it can be made available to the

Public without redaction.

Sincerely,

Cynthia D. Pederson, Director

Division of Reactor Projects

Docket Nos. 50-454; 50-455

License Nos. NPF-37; NPF-66

Enclosure: Inspection Report 05000454/2008-003; 05000455/2008-003

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Byron Station

Plant Manager - Byron Station

Regulatory Assurance Manager - Byron Station

Chief Operating Officer and Senior Vice President

Senior Vice President - Midwest Operations

Senior Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director - Licensing and Regulatory Affairs

Manager Licensing - Braidwood, Byron, and LaSalle

Associate General Counsel

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

J. Klinger, State Liaison Officer,

Illinois Emergency Management Agency

P. Schmidt, State Liaison Officer, State of Wisconsin

Chairman, Illinois Commerce Commission

B. Quigley, Byron Station

Document: G:\Byro\Byron 2008 003.doc

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII RIII RIII

NAME JDalzell:dtp RSkokowski KOBrien 1R13 CPederson

DATE 08/14/08 08/14/08 08/13/08 08/14/08

OFFICIAL RECORD COPY

Letter to C. Pardee from Cynthia Pederson dated August 14, 2008

SUBJECT: BYRON STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT

05000454/2008-003 05000455/2008-003 PRELIMINARY WHITE FINDING

DISTRIBUTION:

Russell Gibbs

Tamara Bloomer

Meghan Thorpe-Kavanaugh

RidsNrrDirsIrib Resource

Mark Satorius

Kenneth OBrien

Jared Heck

Roland Lickus

Carole Ariano

Linda Linn

Cynthia Pederson (hard copy - IRs only)

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

ADAMS (PARS)

SECY

OCA

M. Virgilio, DEDMRS

C. Carpenter, OE

D. Starkey, OE

J. Wray, OE

A. Sapountzis, OE

E. Leeds, NRR

M. Ashley, NRR

F. Brown, NRR

J. Caldwell, RIII

L. Chandler, OGC

C. Marco, OGC

R. Romine, OGC

E. Brenner, OPA

H. Bell, OIG

G. Caputo, OI

D. Holody, RI

C. Evans, RII

W. Jones, RIV

V. Mitlyng, RIII

P. Chandrathil, RIII

A. Barker, RIII

J. Lynch, RIII

P. Lougheed, RIII

P. R. Pelke, RIII

M. Gryglak, RIII

OEMAIL

OEWEB

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-454; 50-455

License Nos: NPF-37; NPF-66

Report Nos: 05000454/2008003 and 05000455/2008003

Licensee: Exelon Generation Company, LLC

Facility: Byron Station, Units 1 and 2

Location: Byron, Illinois

Dates: April 01, 2008, through June 30, 2008

Inspectors: B. Bartlett, Senior Resident Inspector

R. Ng, Resident Inspector

C. Acosta, Reactor Inspector

T. Bilik, Reactor Inspector

J. Cassidy, Senior Health Physicist

N. Féliz Adorno, Reactor Engineer

J. Jacobson, Senior Reactor Inspector

R. Jickling, Senior Emergency Preparedness Analyst

D. Jones, Reactor Inspector

V. Meghani, Reactor Inspector

R. Russell, Emergency Preparedness Analyst

C. Zoia, Project Engineer

C. Thompson, Resident Inspector, Illinois Department of

Emergency Management

Approved by: R. Skokowski, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

REPORT DETAILS .......................................................................................................................4

Summary of Plant Status...........................................................................................................4

1. REACTOR SAFETY ..........................................................................................................4

1R01 Adverse Weather Protection (71111.01) .....................................................4

1R04 Equipment Alignment (71111.04) ................................................................6

1R05 Fire Protection (71111.05)...........................................................................7

1R06 Flooding (71111.06) ....................................................................................9

1R08 Inservice Inspection (ISI) Activities (71111.08P) .......................................10

1R12 Maintenance Effectiveness (71111.12) .....................................................17

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

...................................................................................................................20

1R15 Operability Evaluations (71111.15) ...........................................................24

1R19 Post Maintenance Testing (71111.19).......................................................25

1R20 Outage Activities (71111.20) .....................................................................26

1R22 Surveillance Testing (71111.22)................................................................27

1EP2 Alert and Notification System (ANS) Evaluation (71114.02) .....................30

1EP3 Emergency Response Organization (ERO) Augmentation Testing

(71114.03) .................................................................................................31

1EP5 Correction of EP Weaknesses and Deficiencies (71114.05).....................31

2. RADIATION SAFETY ......................................................................................................32

2OS1 Access Control to Radiologically Significant Areas (71121.01) .................32

2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning And Controls

(71121.02) .................................................................................................33

4. Other Activities.................................................................................................................35

4OA1 PI Verification (71151) ...............................................................................35

4OA2 Identification and Resolution of Problems (71152)....................................37

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153) .......41

4OA5 Other Activities ..........................................................................................42

4OA6 Management Meetings ..............................................................................51

4OA7 Licensee-Identified Violations....................................................................52

KEY POINTS OF CONTACT ........................................................................................................1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED ............................................................1

LIST OF DOCUMENTS REVIEWED ............................................................................................3

LIST OF ACRONYMS USED......................................................................................................15

Enclosure

SUMMARY OF FINDINGS

IR 05000454/2008-003; 05000454/2008-003; April 01 2008 - June 30, 2008; Byron Station,

Units 1 and 2; Fire Protection, Inservice Inspection Activities, Maintenance Effectiveness and

Maintenance Risk Assessments and Emergent Work Control.

This report covers a three-month period of inspection by resident inspectors and an announced

baseline inspections by six regional inspectors. Four Green findings were identified by the

inspectors. These findings were considered Non-Cited Violations (NCVs) of Nuclear Regulatory

Commission (NRC) regulations. In addition, one apparent violation with potential safety

significance greater than green was identified. The significance of most findings is indicated by

their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding of very low safety significance and associated

NCV of the Byron Unit 1 Operating License (OL), Condition 2.C.(6) for failure to comply

with the spacing standard for sprinkler systems of the Fire Protection Program (FPP).

Specifically, a permanent scaffold obstructed a fire protection suppression sprinkler in

the Unit 1, train A (1A) diesel oil storage rank room and no replacement sprinkler was

installed. The licensee entered the issue into the corrective action program (CAP) and

subsequently removed the scaffold decking.

This finding is more than minor because it was associated with the external factor

attribute of the Initiating Events (IE) cornerstone and affected the cornerstone objective

to limit the likelihood of those events that upset plant stability and challenge critical

safety functions during shutdown as well as power operations. The finding is of very low

safety significance because it has a low degradation rating as only one out of eleven

sprinklers in the room was obstructed and there was another functional head within

10 feet of the combustible concern. This finding has a cross-cutting aspect in the area of

Human Performance for Work Practices (H.4.(b)) because the licensee failed to define

and effectively communicate expectations regarding procedural compliance and

personnel following procedures. (Section 1R05.1.b)

  • Green. The inspectors identified a finding of very low safety significance and associated

NCV of Title 10 of the Code of Federal Regulations (10 CFR), Part 50, Section 50.55a,

for the failure to correctly disposition an ultrasonic (UT) examination indication found in

feedwater weld 1FW87CA-6O/C08A as required by American Society of Mechanical

Engineers (ASME) Code,Section XI. This issue was entered into the licensees CAP;

the indication was re-examined and correctly dispositioned.

The inspectors concluded that the finding was more than minor because a failure to

perform the required corrective action could have allowed an unacceptable flaw to

remain in service and so could become a more significant safety concern. The

1 Enclosure

inspectors applied the IMC 0609, Attachment 0609.04, Phase 1 - Initial Screening and

Characterization of Findings to this finding. The inspectors concluded that the finding

was of very low safety significance, because the licensee re-performed the UT

examination, and correctly dispositioned the indication in accordance with ASME Code.

Furthermore, the finding did not contribute to both the likelihood of a reactor trip, and the

likelihood that mitigation equipment will not be available. The inspectors determined that

this finding was related to the Decision Making Component (H.1(b)) for the cross-cutting

area of Human Performance. (Section 1R08.1.b)

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance and associated

NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

regarding the licensees failure to perform adequate evaluations of the boric acid

leakage from bolted connections in accordance with Procedure ER-AP-331-1002, Boric

Acid Corrosion Control Program Identification, Screening, and Evaluations. This issue

was entered into the licensees CAP. Licensee corrective actions included revising the

procedure and re-performing the evaluation.

As implied by Example 4a of IMC 0612, Power Reactor Inspection Reports,

Appendix E, Examples of Minor Issues, the finding was not minor under the

category of Insignificant Procedural Errors, because the licensee routinely failed to

perform/document engineering evaluations for bolted connections with boric acid leaks.

A failure to adequately perform the required evaluation could result in equipment

susceptible to the corrosive effects of boric acid being returned to service in a degraded

condition and so could become a more significant safety concern.

The inspectors applied the IMC 0609, Attachment 0609.04, to this finding. The

inspectors checked the Reactivity Control Degraded box in the Mitigation System

Cornerstone column of Table 2, and answered no to all of the questions in the

Mitigation System Cornerstone column of Table 4a, to conclude that the finding was of

very low safety significance (Green). Specifically, the finding did not represent a loss of

any safety function. The inspectors determined that this finding was related to the cross-

cutting component of Human Performance for Work Practices (H.4.(b)).

(Section 1R08.3.b)

  • Green. A finding of very low safety significance and associated NCV of Technical

Specification (TS) 5.4, Procedures, was self-revealed on May 27, 2008, when the

0B essential service water (SX) system makeup pump failed to start during a planned

monthly surveillance test. The pump failed to start due to a lack of fuel prime. The

licensee determined that on April 29, 2008, the check valve on the fuel oil supply line

between the day tank and the engine had been replaced as part of a routine preventive

maintenance program. The check valve was found in the installed condition with a loose

fitting. The loose fitting had leaked slowly allowing fuel oil to drain from the primed fuel

oil supply line. The issue has been entered into the licensees CAP (IR 779699). The

licensees corrective actions included repairing the check valve and associated

deficiencies, as well as revising the maintenance procedure.

The finding was considered more than minor because there was an actual loss of safety

function of a single train for greater than its TS allowed outage time. The finding was

determined to be of very low safety significance during a Phase 3 SDP. The primary

2 Enclosure

cause of this finding was related to the cross-cutting area of Human Performance for

Work Practices (H.4(c)) because licensee supervisory oversight of work activity failed to

ensure procedural compliance. (Section 1R12.1.b)

  • AV. The licensee identified an apparent violation of 10 CFR 50.65, Requirements for

Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, (a)(4) for failure

to perform an updated risk evaluation prior to surveillance testing of the Unit 1 Train A

emergency diesel generator (EDG) based on existing plant conditions. This failure

resulted in an inadvertent entry into an elevated online risk condition for Unit 2. This

issue has potential safety significance greater than very low safety significance for

Unit 2, which may change pending completion of the SDP. This issue was entered into

their corrective action program as IR 759945. The licensee immediately implemented

the compensatory measure of an operator stationed at the valve. They also took

corrective actions to reassemble the valves and place them back in service.

The finding is more than minor in accordance with IMC 0612, Appendix E, Section 7,

Example f, because the elevated overall plant risk when correctly accessed, is greater

than 1.0E-6 Incremental Core Damage Probability (ICDP) and also put the plant into a

higher risk category with additional risk management actions. The cause of this finding

was related to the cross-cutting element of human performance for work control

(H.3.(b)). (Section 1R13.1.b)

B. Licensee-Identified Violations

Three violations of very low safety significance that were identified by the licensee have

been reviewed by inspectors. Corrective actions planned or taken by the licensee have

been entered into the licensees CAP. These violations and corrective action tracking

numbers are listed in Section 4OA7 of this report.

3 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 was in a refueling outage at the start of this inspection period. Initial criticality following

the refueling outage was on April 14, 2008, and the unit returned to full power on April 22, 2008,

after fuel pre-conditioning. The unit remained at or near full power throughout the rest of the

inspection period with minor exceptions for testing.

Unit 2 operated at or near full power throughout the inspection period with minor exceptions.

On May 8, 2008, power was reduced to 87 percent for turbine valve testing.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1 Readiness of Offsite and Alternate Alternating Current (AC) Power Systems

a. Inspection Scope

The inspectors verified that plant features and procedures for operation and continued

availability of offsite and alternate AC power systems during adverse weather were

appropriate. The inspectors reviewed the licensees procedures affecting these areas

and the communications protocols between the transmission system operator (TSO) and

the plant to verify that the appropriate information was being exchanged when issues

arose that could impact the offsite power system. Examples of aspects considered in

the inspectors review included:

  • The coordination between the TSO and the plant during off-normal or emergency

events;

  • The explanations for the events;
  • The estimates of when the offsite power system would be returned to a normal

state; and

  • The notifications from the TSO to the plant when the offsite power system was

returned to normal.

The inspectors also verified that plant procedures addressed measures to monitor and

maintain availability and reliability of both the offsite AC power system and the onsite

alternate AC power system prior to or during adverse weather conditions. Specifically,

the inspectors verified that the procedures addressed the following:

  • The actions to be taken when notified by the TSO that the post-trip voltage of the

offsite power system at the plant would not be acceptable to assure the

continued operation of the safety-related loads without transferring to the onsite

power supply;

  • The compensatory actions identified to be performed if it would not be possible to

predict the post-trip voltage at the plant for the current grid conditions;

4 Enclosure

  • A re-assessment of plant risk based on maintenance activities that could affect

grid reliability, or the ability of the transmission system to provide offsite power;

and

  • The communications between the plant and the TSO when changes at the plant

could impact the transmission system, or when the capability of the transmission

system to provide adequate offsite power was challenged.

Specific documents reviewed during this inspection are listed in the Attachment. The

inspectors also reviewed Corrective Action Program (CAP) items to verify that the

licensee was identifying adverse weather issues at an appropriate threshold and

entering them into their CAP in accordance with station corrective action procedures.

This inspection constitutes one readiness of offsite and alternate AC power systems

sample as defined in Inspection Procedure (IP) 71111.01-05.

b. Findings

No findings of significance were identified.

.2 Summer Seasonal Readiness Preparations

a. Inspection Scope

The inspectors performed a review of the licensees preparations for summer weather

for selected systems, including conditions that could lead to an extended drought as a

result of high temperatures.

During the inspection, the inspectors focused on plant specific design features and the

licensees procedures used to mitigate or respond to adverse weather conditions.

Additionally, the inspectors reviewed the Updated Final Safety Analysis Report (UFSAR)

and performance requirements for systems selected for inspection, and verified that

operator actions were appropriate as specified by plant specific procedures. Specific

documents reviewed during this inspection are listed in the Attachment. The inspectors

also reviewed CAP items to verify that the licensee was identifying adverse weather

issues at an appropriate threshold and entering them into their CAP in accordance with

station corrective action procedures. The inspectors reviews focused specifically on the

following plant systems:

  • Auxiliary Building Ventilation System; and
  • Auxiliary Transformers

This inspection constitutes one seasonal adverse weather sample as defined in

IP 71111.01-05.

b. Findings

No findings of significance were identified.

5 Enclosure

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

  • Spent Fuel Pool Cooling following Unit 1 Core Off-Load;
  • Unit 1 Train A Diesel Generator while Unit 1 Train B Diesel Generator was Out of

Service (OOS);

  • Unit 1 Train B Safety Injection while Unit 1 Train A Safety Injection was OOS;

System was OOS; and

  • Unit 2 Train B RHR while Unit 2 Train A RHR was OOS.

The inspectors selected these systems based on their risk significance relative to the

reactor safety cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders, condition reports, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the CAP

with the appropriate significance characterization. Documents reviewed are listed in the

Attachment.

These activities constituted five partial system walkdown samples as defined by

IP 71111.04-05.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

On April 9, 2008, through April 10, 2008, the inspectors performed a complete system

alignment inspection of Control Room Ventilation to verify the functional capability of the

system. This system was selected because it was considered safety-significant. The

inspectors walked down the system to review mechanical and electrical equipment line

ups, electrical power availability, system pressure and temperature indications as

appropriate, component labeling, component lubrication, component and equipment

6 Enclosure

cooling, hangers and supports, operability of support systems, and to ensure that

ancillary equipment or debris did not interfere with equipment operation. A review of a

sample of past and outstanding work requests was performed to determine whether any

deficiencies significantly affected the system function. In addition, the inspectors

reviewed the CAP database to ensure that system equipment alignment problems were

being identified and appropriately resolved. The documents used for the walkdown and

issue review are listed in the Attachment.

These activities constituted one complete system walkdown sample as defined by

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns that were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

  • Unit 1 Diesel Oil Storage Tank Rooms (Zone 10.1-1 & 10.2-1);
  • Unit 2 Diesel Oil Storage Tank Rooms (Zone 10.1-2 & 10.2-2);
  • Fuel Handling Building (Zone 12.1-0); and
  • River Screen House Including SX Makeup Pumps (Zones 18.11-0, 1 and 2).

The inspectors reviewed areas to assess if the licensee had implemented a Fire

Protection Program (FPP) that adequately controlled combustibles and ignition sources

within the plant, effectively maintained fire detection and suppression capability,

maintained passive fire protection features in good material condition, and had

implemented adequate compensatory measures for out of service, degraded or

inoperable fire protection equipment, systems, or features in accordance with the

licensees fire plan. The inspectors selected fire areas based on their overall

contribution to internal fire risk as documented in the plants Individual Plant Examination

of External Events with later additional insights, their potential to impact equipment

which could initiate or mitigate a plant transient, or their impact on the plants ability to

respond to a security event. Using the documents listed in the Attachment, the

inspectors verified that fire hoses and extinguishers were in their designated locations

and available for immediate use; that fire detectors and sprinklers were unobstructed,

that transient material loading was within the analyzed limits; and fire doors, dampers,

and penetration seals appeared to be in satisfactory condition. The inspectors also

verified that minor issues identified during the inspection were entered into the licensees

CAP.

These activities constituted four quarterly fire protection inspection samples as defined

by IP 71111.05-05.

7 Enclosure

b. Findings

(1) Fire Suppression Sprinkler Obstruction in the Diesel Oil Storage Tank Room

Introduction: A finding of very low safety significance and associated non-cited violation

(NCV) of the Byron Unit 1 Operating License (OL) Condition 2.C(6) for the licensees

failure to comply with the spacing standard for sprinkler systems of the Fire Protection

Program (FPP) was identified by the inspectors. Specifically, a permanent scaffold

obstructed a fire protection suppression sprinkler in the 1A diesel oil storage rank room

and no replacement sprinkler was installed.

Description: On April 30, 2008, the inspectors performed a fire protection walkdown of

the 1A diesel oil storage tank room. The inspectors identified that a permanent scaffold

with solid decking material was erected underneath a fire suppression sprinkler and next

to a working platform. This permanent scaffold, in conjunction with the working platform,

created a deck area below the sprinkler that was 8 feet 9 inches in the north-south

direction and 6 feet 5 inches in the east-west direction. Since this area was irregular

shaped, the shortest dimension was 4 feet 4 inches in the southwest diagonal direction.

The combination of the permanent scaffold and the working platform obstructed a major

portion of the spray pattern of one of the foam based fire suppression sprinklers to a

portion of the floor area in the diesel oil storage tank room. No sprinkler was installed to

supplement the one that had been obstructed. The 1A diesel oil storage tank room

houses two diesel oil storage tanks that contain the diesel fuel oil used by the 1A

emergency diesel generator (EDG) and 1A diesel driven auxiliary feedwater (AFW)

pump.

The licensee declared the fire suppression system for the 1A diesel oil storage tank

room inoperable and verified that the automatic fire detection instrumentation was

operable in accordance with the Technical Requirement Manual (TRM). The licensee

subsequently removed the decking of the permanent scaffold.

The inspectors reviewed that the Permanent Scaffold Request B-4855 and determined

that the permanent scaffold had been inspected, evaluated and approved by engineering

personnel in March 2004. However, the procedure in effect at the time of the scaffold

erection, MA-AA-716-025, Scaffold Installation, Modification, and Removal Request

Process, Revision 0, required that engineering review and evaluate the technical impact

of the proposed permanent scaffold and approve post erection inspections as needed.

One of the evaluation criteria specified by the procedure was to determine if the scaffold

would affect the coverage zone of any in-place fire protection sprinkler heads in the

immediate proximity. No specific concern or instruction was noted when the scaffold

request was approved by engineering.

The inspectors determined that the licensee was committed to National Fire Protection

Association (NFPA) Code 13, Standard for the Installation of Sprinkler Systems,

1983 Edition, and NFPA Code 16, Deluge Foam Water Sprinkler and Sprays Systems,

1980 Edition, according to the licensees Fire Protection Report. Per these standards,

sprinklers shall be installed under decks which are over four feet wide to prevent

obstruction for the spray pattern of the sprinkler. Specifically, Section 4-2.1 of NFPA-16

stated that foam-water sprinkler system designs shall conform to all of the applicable

requirements of NFPA-13 except where otherwise specified in NFPA-16. Section 4-4.11

of NFPA-13 specified that sprinklers be installed under decks and galleries which are

8 Enclosure

over four feet wide. As NFPA-16 did not specifically address sprinkler obstructions, the

requirements of NFPA-13 pertaining to obstructions applied.

Analysis: The inspectors determined that the licensees failure to comply with the

spacing standard for sprinkler systems in accordance with the FPP was a performance

deficiency that warranted a IMC 0609, Significance Determination Process (SDP)

evaluation. The inspector concluded that the finding was greater than minor in

accordance with IMC 0612, Appendix B, Issue Disposition Screening. Specifically, it

was associated with the external factor attribute of the Initiating Events cornerstone and

affected the cornerstone objective to limit the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations.

The inspectors determined that the finding could be evaluated using the SDP in

accordance with IMC 0609, Appendix F, Fire Protection Significance Determination

Process, because it was associated with fire protection defense-in-depth strategies

involving suppression system. The inspectors determined that the finding has a low

degradation rating since only one out of eleven sprinklers in the room was obstructed

and there was another functional head within ten feet of the combustible concern. In

addition, other aspects of the system complied with NFPA code. Therefore the finding

was determined to be of very low safety significance (Green).

This finding has a cross-cutting aspect in the area of Human Performance for Work

Practices (H.4.(b)) because the licensee failed to define and effectively communicate

expectations regarding procedural compliance and personnel following procedures.

Enforcement: Byron Unit 1 OL, Condition 2.C.(6) states, in part, that the licensee shall

implement and maintain in effect all provisions of the approved FPP as described in the

licensees Fire Protection Report. The Fire Protection Report stated that the licensees

sprinkler system conformed to NFPA Code 13, 1983, edition, and no deviation applied to

this fire area. Per the NFPA standard, sprinklers shall be installed under decks that are

over four feet wide. Contrary to the above, a permanent scaffold was erected in

conjunction with an existing platform structure, creating a deck area that was 4 feet 4

inches in the diagonal direction. This permanent scaffold, in conjunction with the

working platform, obstructed a fire suppression sprinkler and no sprinkler was installed

to supplement the obstructed one. Because this violation was of very low safety

significance and because it was entered into the licensees CAP as Issue Report (IR)

770364, this violation is being treated as a NCV, consistent with Section VI.A.1 of the

NRC enforcement policy. (NCV 05000454/2008003-01)

1R06 Flooding (71111.06)

.1 Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures, for

licensee commitments. The specific documents reviewed are listed in the Attachment.

9 Enclosure

In addition, the inspectors reviewed licensee drawings to identify areas and equipment

that may be affected by internal flooding caused by the failure or misalignment of nearby

sources of water, such as the fire suppression or the circulating water systems. The

inspectors also reviewed the licensees CAP documents with respect to past

flood-related items identified in the CAP to verify the adequacy of the corrective actions.

The inspectors performed a walkdown of the following plant area to assess the

adequacy of watertight doors and to verify drains and sumps were clear of debris and

operable and that the licensee complied with its commitments:

  • Turbine Building Basement.

These inspection activities constitute one internal flooding sample as defined in

IP 71111.06-05.

a. Findings

No findings of significance were identified.

1R08 Inservice Inspection (ISI) Activities (71111.08P)

From March 24, 2008, through April 3, 2008, the inspectors conducted a review of the

implementation of the licensees ISI Program for monitoring degradation of the reactor

coolant system, steam generator tubes, emergency feedwater systems, risk significant

piping, and components and containment systems.

The inspections described in Sections 1R08.1, 1R08.2, 1R08.3, 1R08.4, and 1R08.5

below count as one inspection sample as defined by IP 71111.08-05.

.1 Piping Systems ISI

a. Inspection Scope

The inspectors reviewed records of the following nondestructive (NDE) examinations

mandated by the American Society of Mechanical Engineers (ASME) Code,Section XI

to evaluate compliance with the ASME Code,Section XI and Section V, requirements

and if any indications and defects were detected, to determine if these were

dispositioned in accordance with the ASME Code or an NRC approved alternative

requirement.

NIR inner radius; and

The inspectors reviewed the following examinations completed during the previous

outage with relevant/recordable conditions/indications accepted for continued service to

determine if acceptance was in accordance with the ASME Code Section XI or an NRC

approved alternative.

RHEC-013; and

10 Enclosure

Review of pressure boundary welding was completed during performance of Temporary

Instruction (TI)-172 as documented in Section 4OA5, and this review is credited for

meeting this inspection procedure attribute.

b. Findings

(1) Failure to Correctly Evaluate and Disposition a Weld Indication

Introduction: The inspectors identified a Green NCV of 10 CFR Part 50.55a,

for failure of the licensee to correctly disposition a flaw found in feedwater weld

1FW87CA-6O/C08A as required by ASME Code Section XI discovered while

performing a Performance Demonstration Initiative (PDI) UT examination.

Description: During a records review of the UT examination performed on

September 15, 2006, of feedwater weld 1FW87CA-6O/C08A as directed by IP 71111.08

Section 02.01(e), the inspectors observed that the licensee had failed to correctly

evaluate and disposition a weld indication in accordance with ASME Code after it was

identified during a PDI UT examination.

While performing a PDI UT examination of a weld of a 6O, 0.432O nominal thickness,

ferritic feedwater pipe, using 45 degree and 60 degree shear waves, the examiners

identified a mid-wall indication, with an L max dimension of 2.0O. The indication

occurred outside of the minimum required exam volume and reportedly did not have an

inside diameter connection. A sketch included with the licensees report shows the

indication to be near the fusion zone of the weld, and the indication was detected with

the 60 degree search unit. While the examiners reported the indication as a recordable

indication, the reviewer indicated that no further evaluation of the flaw was required. The

decision to forgo further evaluation was supported by both the licensees UT Level III

and the Authorized Nuclear Inservice Inspector. In response to the inspectors question

as to why there was no further evaluation performed, the licensee stated that it was

because the indication was not located in the minimum required weld volume they had

interrogated, nor was there any guidance in the procedure for addressing indications

outside of the volume they intended to examine. However, the inspectors determined

that ASME evaluation requirements are not limited to just indications that are found in

the minimum weld volume.

Analysis: The inspectors determined that the failure of the licensee to perform

ASME Code required corrective actions for an indication found during PDI UT

examination of a feedwater weld, was a performance deficiency that warranted a SDP

evaluation. The inspectors compared this issue to the issues identified in Appendix E of

IMC 0612 to determine whether the issue was minor, and concluded that none of the

examples listed in Appendix E, accurately represented this example. As a result, the

inspector compared this issue to the minor questions contained in Section 3, Minor

Questions, to IMC 0612, Appendix B, Issue Screening. The inspectors concluded that

the finding was more than minor because a failure to perform the required corrective

action could have allowed an unacceptable flaw to remain in service and so could

become a more significant safety concern.

The inspectors applied the IMC 0609, Attachment IMC 0609.04, to this finding. The

inspectors checked the Primary System LOCA Initiator Contributor box in the Initiating

Events Cornerstone column of Table 2, and answered no to the question in the LOCA

11 Enclosure

Initiator Cornerstone column of Table 4a, to conclude that the finding was of very low

safety significance (Green).

Specifically, the licensee re-performed the UT examination and correctly dispositioned

the indication in accordance with ASME Code. Furthermore, the finding did not

contribute to both the likelihood of a reactor trip, and the likelihood that mitigation

equipment will not be available.

The inspectors determined that this finding was related to the Decision Making

Component (H.1(b)) aspect for the cross-cutting area of Human Performance, because

the licensee failed to make conservative assumptions in decisions affecting the integrity

of the feedwater piping. Specifically, the licensees presumption of weld integrity was

not based on sufficient information to be able to demonstrate that the action/decision to

leave the feedwater piping with an unevaluated piping weld indication in service was

safe.

Enforcement: Between March 24, 2008, and April 3, 2008, while performing baseline

IP 71111.08, the inspectors identified a NCV of 10 CFR 50.55(a)(g)(4), in that the

licensee failed to correctly disposition an indication found in feedwater weld

1FW87CA-6O/C08A, as required by ASME Code Section XI, discovered while

performing a PDI UT examination.

Title 10 CFR 50.55(a)(g)(4), required, in part, that pressurized water-cooled nuclear

power facility components classified as ASME Class 1, Class 2, and Class 3 meet the

requirements set forth in ASME Code Section XI. ASME Code,Section XI,

IWB-3131(c), required in part, that acceptance of components for continued service shall

be in accordance with Tables IWB-3132, IWB-3133, and IWB - 3134. IWB-3132.1,

stated in part, that a component that does not meet the acceptance standards of

Table IWB-3410-1 shall be corrected in accordance with the provisions of IWB-3132.2

(Acceptance by Repair/Replacement) or IWB-3132.3 (Acceptance by Analytical

Evaluation).

Contrary to the above, on September 15, 2006, during B1R14, after identifying a UT

indication in feedwater weld 1FW87CA-6O/C08A, which did not meet the acceptance

standards of Table IWB-3410-1 (identified in report number B1R14-UT-027), the

licensee failed to disposition by repair, replacement, or acceptance by evaluation as

required by the ASME Code prior to returning Unit 1 to service.

Because of the very low safety significance of this finding and because the issue was

entered into the licensees CAP (IR 756048), it is being treated as a NCV, consistent

with Section VI.A.1, of the NRC Enforcement Policy (NCV 05000454/2008003-02).

.2 Reactor Pressure Vessel Upper Head Penetration Inspection Activities

a. Inspection Scope

The inspectors reviewed a video recording of the visual examinations conducted on the

Unit 1 reactor vessel head to determine if the activities were performed in accordance

with the requirements of NRC Order EA-03-009, and if any indications and defects were

detected, to determine if these were dispositioned in accordance with the ASME Code or

an NRC approved alternative requirement. The inspectors also reviewed the vessel

12 Enclosure

head visual examination procedure to determine if criteria existed for visual examination

quality and if instructions existed for resolving interference or masking issues.

The licensee did not perform any weld repairs to vessel head penetrations since the

beginning of the preceding outage for Unit 1. Therefore, no NRC review was completed

for this IP attribute.

b. Findings

No findings of significance were identified.

.3 Boric Acid Corrosion Control (BACC)

a. Inspection Scope

The inspectors observed the licensee BACC visual examinations for portions of the

Reactor Coolant System (RCS) to determine if these visual examinations emphasized

locations where boric acid leaks can cause degradation of safety significant

components.

The inspectors reviewed the following engineering evaluations of reactor coolant system

components with boric acid deposits to determine if degraded components were properly

documented in the CAP. The inspectors also evaluated corrective actions for any

degraded RCS components to determine if they met the ASME Code,Section XI, or

NRC approved alternative.

  • IR 650150; 1CV066A Pipe Cap Leak (Boric Acid)-Valve Leak By Issue;
  • IR 563581; 1CV8524B Body to Bonnet Leakage; and
  • IR 641851; 1SI8812B Inactive Body-to Bonnet Leak.

The inspectors reviewed the following corrective actions related to evidence of boric

acid leakage to determine if the corrective actions completed were consistent with the

requirements of the ASME Code,Section XI, and 10 CFR Part 50, Appendix B,

Criterion XVI.

  • IR 640441; Damp Boric Acid Present on 1AB03T Tank FLGD Tap; and
  • IR 616011; 2RH8702A Active Body to Bonnet Leak.

b. Findings

(1) Failure to Perform Evaluation of a Leaking Bolted Connection

Introduction: The inspectors identified a Green NCV of 10 CFR Part 50, Appendix B,

Criterion V, regarding the licensees failure to perform adequate evaluations of the boric

acid leakage from bolted connections in accordance with the procedure

ER-AP-331-1002, Boric Acid Corrosion Control Program Identification, Screening, and

Evaluations. Specifically, in the evaluations of the boric acid leaks documented in

IR 641851 and IR 563581, the licensee did not adequately address all applicable

considerations per ER-AP-331-1002, Attachment 3, Evaluation of Leakage from Bolted

Connection, Section 7.

13 Enclosure

Description: ASME Code,Section XI (2001, through 2003 Addenda), IWA-5250(a)(2),

requires removal and VT-3 examination of the bolts as corrective action, when a leak

occurs at a bolted connection in a borated system. Code Case N-566-2, Corrective

Action for Leakage Identified at Bolted Connections, provides for evaluation as an

alternative to removal of the bolts. The Code Case was approved by the NRC on

March 28, 2001, and is included in the Licensees ISI Program Plan. The Code Case

specifies the parameters to be included in the evaluation. The licensee has incorporated

these parameters in Attachment 3, of the Procedure ERAP331-1002.

During inspections performed between March 24, 2008, and April 3, 2008, the

inspectors identified that the licensee had failed to adequately document evaluations

of bolted connections with evidence of boric acid leakage. Specifically, in the

evaluations for body-to-bonnet leaks for Valve 1SI8812B documented in IR 563581

on November 30, 2006, and Valve 1CV8524B documented in IR 563581 on

February 1, 2007, the licensee concluded that it was not necessary to remove the bolts

for further examination without adequately addressing in the evaluation all the

parameters specified in Code Case N-566-2. The licensee used Attachment 3, of

Procedure ER-AP-331-1002, to document the evaluation. Section 7 of the Attachment

lists all the parameters included in the Code Case and required their consideration in the

evaluation. The inspectors however, were not able to verify through review of licensees

documentation that all the parameters were considered in the evaluation, which based

its conclusion of acceptability on the material being stainless steel, not susceptible to

boric acid corrosion. The inspectors found similar instances in other boric acid

evaluations including some where the affected bolt material was carbon steel and

therefore concluded that adequate evaluations were not being performed prior to

documenting the conclusions. After identification by the inspector, the licensee

documented the issue in their CAP as IR 755998, Inadequate Boric Acid Evaluations of

Mechanical Joints, dated March 3, 2008. The licensees corrective actions involved

revising the procedure and then re-performing the evaluations.

Analysis: The inspectors determined that the failure of the licensee to perform adequate

evaluation of bolted connections with evidence of leakage as required by the Code

Case N-566-2 and their procedure was a performance deficiency that warranted a

significance evaluation. The inspectors believed that for the evaluations reviewed,

based on the amount of leakage and degradation documented, the conclusion of the

evaluation would not have changed had an adequate evaluation been performed.

However, as implied by Example 4a of IMC 0612, Appendix E, the finding was not minor

under the category of Insignificant Procedural Errors, because the licensee routinely

failed to perform/document engineering evaluations for bolted connections with boric

acid leaks. The finding was also more than minor because a failure to adequately

perform the required evaluation could result in equipment susceptible to the corrosive

effects of boric acid being returned to service in a degraded condition and thus become

a more significant safety concern.

The inspectors applied the IMC 0609, Attachment 0609.04, to this finding. The

inspectors checked the Reactivity Control Degraded box in the Mitigation System

Cornerstone column of Table 2, and answered no to all of the questions in the

Mitigation System Cornerstone column of Table 4a, to conclude that the finding was of

very low safety significance (Green). Specifically, the finding did not represent a loss of

any safety function.

14 Enclosure

This finding was related to the cross-cutting component of Human Performance for Work

Practices (H.4.(b)) in that, the licensee failed to define and effectively communicate

expectations regarding procedural compliance. Specifically, the licensee repeatedly

failed to adequately perform/document the evaluations required per Attachment 3,

Section 7 of the ER-AP-331-1002, Revision 3.

Enforcement: During inspections performed between March 24, 2008, and April 3, 2008,

the inspectors identified a NCV of 10 CFR Part 50, Appendix B, Criterion V, in that the

licensee failed to perform engineering evaluations on bolted connections with evidence

of leakage in accordance with their procedure.

Title 10 CFR Part 50, Appendix B, Criterion V, requires in part, that activities affecting

quality shall be prescribed by documented instructions, procedures, or drawings of a

type appropriate to the circumstances, and shall be accomplished in accordance with

these instructions, procedures, or drawings.

License Procedure ER-AP-331-1002, Revision 3, Attachment 3, Section 7 lists the

parameters/attributes that must be considered in the evaluation.

Contrary to the above, on August 20, 2007, for Valve 1SI8812B, and on

January 31, 2007, for Valve 1CV8524B, the licensee failed to perform adequate

evaluations in accordance with Procedure ER-AP-331-1002, Revision 3. Specifically, in

the evaluations for leakage from bolted connections discovered per IR 641851 and

IR 563581, the licensee staff failed to perform/document evaluations considering all the

parameters/attributes specified in the Attachment 3, Section 7 of ER-AP-331-1002.

Because of the very low safety significance of this finding and because the issue was

entered into the licensees CAP (IR 755998), it is being treated as a NCV, consistent

with Section VI.A.1 of the Enforcement Policy (NCV 05000454/2008003-03).

.4 SG Tube Inspection Activities

a. Inspection Scope

The inspectors observed acquisition of eddy current (ET) data, interviewed ET resolution

analysts, and reviewed documentation related to the SG ISI program to determine if:

  • in-situ SG tube pressure testing screening criteria used were consistent with

those identified in the Electric Power Research Institute (EPRI) TR-107620,

Steam Generator In-Situ Pressure Test Guidelines and that these criteria were

properly applied to screen degraded SG tubes for in-situ pressure testing;

  • the numbers and sizes of SG tube flaws/degradation identified was bound by the

licensees previous outage Operational Assessment predictions;

  • the numbers and sizes of SG tube flaws/degradation identified was bound by the

licensees previous outage Operational Assessment predictions;

  • the SG tube ET examination scope and expansion criteria were sufficient to meet

the Technical Specifications, and the EPRI 1003138, Pressurized Water Reactor

Steam Generator Examination Guidelines: Revision 6;

  • the SG tube ET examination scope included potential areas of tube degradation

identified in prior outage SG tube inspections and/or as identified in NRC generic

industry operating experience applicable to these SG tubes;

15 Enclosure

  • the licensee identified new tube degradation mechanisms and implemented

adequate extent of condition inspection scope and repairs for the new tube

degradation mechanism;

  • the licensee implemented repair methods which were consistent with the repair

processes allowed in the plant TS requirements and to determine if qualified

depth sizing methods were applied to degraded tubes accepted for continued

service;

  • the licensee implemented an inappropriate plug on detection tube repair

threshold (e.g., no attempt at sizing of flaws to confirm tube integrity);

  • the licensee primary-to-secondary leakage (e.g., SG tube leakage) was below

3 gallons-per-day or the detection threshold during the previous operating cycle;

the ET probes and equipment configurations used to acquire data from the SG

tubes were qualified to detect the known/expected types of SG tube degradation

in accordance with Appendix H, Performance Demonstration for Eddy Current

Examination, of EPRI 1003138, Pressurized Water Reactor Steam Generator

Examination Guidelines, Revision 6;

  • the licensee performed secondary side SG inspections for location and removal

of foreign materials; and

  • inaccessible foreign objects were left within the secondary side of the SGs, and if

so, that the licensee implemented evaluations which included the effects of

foreign object migration and/or tube fretting damage.

The licensee did not perform in-situ pressure testing of SG tubes. Therefore, no NRC

review was completed for this inspection attribute.

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI/SG related problems entered into the

licensees CAP and conducted interviews with licensee staff to determine if;

  • the licensee had established an appropriate threshold for identifying ISI/SG

related problems;

  • the licensee had performed a root cause (if applicable) and taken appropriate

corrective actions; and

  • the licensee had evaluated operating experience and industry generic issues

related to ISI and pressure boundary integrity.

The inspectors performed these reviews to evaluate compliance with 10 CFR Part 50,

Appendix B, Criterion XVI, Corrective Action, requirements. The CAP documents

reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

16 Enclosure

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On June 3, 2008, the inspectors observed a crew of licensed operators in the plant

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements.

This inspection constitutes one quarterly licensed operator requalification program

sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk

significant systems:

  • Station Auxiliary Transformer 242-2 Differential Overcurrent Trip; and
  • Essential Service Water Makeup Pump 0B Failure to Start on Demand.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;

17 Enclosure

  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2) or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the corrective action program with the appropriate

significance characterization. Documents reviewed are listed in the Attachment.

This inspection constitutes two quarterly maintenance effectiveness samples as defined

in IP 71111.12-05.

b. Findings

(1) Essential Service Water Makeup Pump 0B Failure to Start on Demand

Introduction: A finding of very low safety significance and an NCV of TS 5.4 was

self-revealed on May 27, 2008, when the 0B SX Makeup pump failed to start during a

planned monthly surveillance test. The pump failed to start due to a lack of fuel prime.

Description: On May 27, 2008, a routine monthly surveillance was initiated on the 0B SX

Makeup pump. The pump failed to start and troubleshooting was initiated. The diesel

portion of the pump was determined to have lost fuel oil prime in the fuel line from the

day tank to the engine. In addition, a loose fitting allowed air to be drawn into the line

resulting in an inability to prime the line.

The licensee determined that on April 29, 2008, the check valve on the fuel oil supply

line between the day tank and the engine had been replaced as part of a routine

preventive maintenance program. The check valve was found in the installed condition

with a loose fitting. The loose fitting had leaked slowly allowing fuel oil to drain from the

primed fuel oil supply line. This leak had also allowed air to enter the line when the

engine driven fuel pump operated during the start attempt. The fuel oil line has a sight

glass that allows operators, during their daily rounds, to check to ensure the line has

remained full of fuel. The licensee determined that following the maintenance in April

that the sight glass had been left with a slight down slope. This allowed fuel to remain in

the sight glass even though the fuel oil line it was attached to had drained. This slope

was not significant enough to be noticed by the operators.

Work Order (WO) 912183, Replace Parker check valve at SX Makeup pump fuel oil

line, was utilized by the workers when replacing the check valve. Document 1 of the

work package instructions required, Install new check valve using approved thread

sealant and tighten fittings in accordance with Parker Tightening Instructions. The

licensee determined that the fitting was loose when installed and did not become fully

tightened during assembly.

18 Enclosure

Technical Specification 3.7.9, Ultimate Heat Sink, Condition C, required that with both

units in Mode 1, 2, 3, or 4, that one inoperable SX makeup pump be restored to operable

within seven days and if not to perform a unit shutdown. The pump maintenance was

performed April 29, 2008, and while a precise leak rate could not be calculated as the

check valve as found condition was disturbed when it was replaced it was estimated to

be a small fraction of the 26 days between the maintenance activity and the discovery of

the failed pump. The estimation was performed by the inspectors after discussions with

licensee personnel, inspection of the check valve, inspection of the total volume of the

engine fuel oil system, and estimation of the relative size of the fuel oil leak given that an

in-leakage of air sufficient to prevent priming of the line was occurring.

Analysis: The inspectors determined that the licensees failure to adequately follow the

work instructions was a performance deficiency warranting a significance evaluation.

The inspectors concluded that the finding was greater than minor in accordance with

Appendix B of IMC 0612, because there was an actual loss of safety function of a single

train for greater than its TS allowed outage time.

The inspectors performed a SDP of this issue using IMC 0609, Attachment

IMC 0609.04. The inspectors determined the finding fell under the Mitigating Systems

Cornerstone and that the finding did not represent a design or qualification deficiency,

did not represent a loss of a safety system function, but did represent an actual loss of

safety function of a single train for greater than its TS allowed outage time. The

inspectors then performed a Phase 2 SDP using the risk informed inspection notebook.

The Phase 2 SDP result was greater than green assuming that the unavailability of the

0B SX make-up pump increases the likelihood of a loss of essential service water event

for an exposure period of between 3 and 30 days.

However, the Senior Reactor Analyst (SRA) determined that this result was overly

conservative because the unavailability of the 0B SX make-up pump would not increase

the likelihood of a loss of essential service water pump by an order of magnitude. A

Phase 3 SDP evaluation was completed using the Simplified Plant Analysis Risk Model

(SPAR) for Byron, Revision 3.31. The 0B SX make-up pump was assumed to be

unavailable and not recoverable for a bounding period of 30 days. The change in core

damage frequency was calculated to be 1E-7/yr, which represented a finding of very low

safety significance (Green). The dominant core damage sequence was a dual unit loss

of offsite power, failure of all SX makeup which in turn fails the DGs and results in a

station blackout. Recovery of offsite or onsite AC power fails resulting in core damage.

Therefore, the inspectors determined that the finding was of very low safety significance.

The primary cause of this finding was related to the cross-cutting area of Human

Performance for Work Practices (H.4.(c)) because licensee supervisory oversight of

work activity failed to ensure procedural compliance.

Enforcement: Technical Specification 5.4 required the implementation of the applicable

procedures recommended in Regulatory Guide 1.33, Quality Assurance Program

Requirements, Revision 2, dated February 1978. Regulatory Guide 1.33, Appendix A,

recommended procedures for the system. Maintenance Procedure MA-AA-716-011,

Work Execution and Close Out, Revision 11 was written in accordance with Section 9,

Performing Maintenance. Step 4.8.1.1.B required Perform work activities and

equipment checks in accordance with approved procedures or work instructions.

Contrary to this requirement, a work instruction contained within WO 912183 was not

followed in that fittings were not tightened resulting in an inoperable SX makeup pump.

19 Enclosure

However, because of the very low safety significance of the issue and because the issue

has been entered into the licensees CAP (IR 779699); the issue is being treated as an

NCV, consistent with Section VI.A.1, of the NRC Enforcement Policy. The licensees

corrective actions included repairing the check valve and associated deficiencies, as well

as revising the maintenance procedure. (NCV 05000454/2008003-04;

05000455/2008003-04)

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • Emergent Shutdown Safety Change due to Extended Work on Unit 1 Train A

Charging Pump;

  • Unit 1 Train A RHR Suction Drain while Unit 1 Division 11 DC Bus was OOS;
  • Inadvertent Orange Risk Entry due to Both Unit 1 SX Unit Cross-tie Isolation

Valves Unavailable for Remote Operation; and

  • Bus 22 Battery Charger while Unit 2 System Auxiliary Transformer (SAT) and

Unit 2 Train C Power Operated Relief Valves (PORVs) were OOS.

These activities were selected based on their potential risk significance relative to the

reactor safety cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

These activities constituted four samples as defined by IP 71111.13-05.

b. Findings

(1) Failure to Perform an Updated Risk Evaluation Prior to Surveillance Testing of the Unit 1

Train A Diesel Generator Based on Existing Plant Conditions.

Introduction: The licensee identified an apparent violation of 10 CFR 50.65(a)(4) for the

licensees failure to perform an updated risk evaluation prior to surveillance testing of the

Unit 1 Train A EDG based on existing plant conditions.

Description: On March 31, 2008, Unit 1 was in a refueling outage with the head

removed, cavity flooded up and defueled. The spent fuel pool was at normal level and

decay heat was being removed via the component cooling exchanger to the SX system.

20 Enclosure

Unit 2 was at 100 percent power and normal operation. Online risk for Unit 2 was

evaluated as Yellow assuming all planned maintenance for the week occurred at the

same time. Shutdown risk for Unit 1 was Green.

The Unit 1 SX train cross-tie isolation valve (1SX034) was scheduled for replacement

during the week of March 31, 2008. As part of the maintenance isolation and

replacement activities, both Unit 1 SX train cross-tie isolation valves (1SX033 and

1SX034) were closed and electrically isolated. The licensees risk assessment

considered both Unit 1 train cross-tie valves closed. The valves are normally open but

need to be able to close to mitigate flooding in auxiliary building due to an SX system

pipe break.

The licensee began disassembling the electrical connection of the valve actuator for

1SX034 on March 31, 2008. Due to isolation issues, the scheduled replacement of

1SX034 was aborted but the electrical connection was not restored immediately. In

addition, 1SX033 was observed to have an actuator problem so maintenance activities

for 1SX033 commenced on April 2, 2008. Valve 1SX034 was utilized as an isolation

point for the maintenance on 1SX033. A new risk assessment was performed and

considered both valves unable to open. Online risk for Unit 2 was evaluated as Yellow

and shutdown risk for Unit 1 was evaluated as Green. Appropriate risk management

actions were carried out for this condition.

At 12:31 on April 3, 2008, Unit 1 entered Mode 6 when the first fuel assembly was

moved back into the reactor vessel. Time to boil was calculated to be 14.7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> at the

time and shutdown risk for Unit 1 was Yellow for reactivity due to fuel moves.

At 03:04 on April 5, 2008, both the 1SX033 and 1SX034 valves were fully opened to

support Unit 1 Train A diesel generator testing. Remote manipulation capability of the

two valves remained unavailable in the main control room since the electrical isolations

remained in place. The open position is the normal operating position of both the

1SX033 and 1SX034 valves. This alignment cross-ties the SX pump supply to the A and

B headers for Unit 1 and is needed for diesel generator testing. This open valve

configuration was not evaluated for Unit 1 shutdown risk, nor was it evaluated for Unit 2

online risk. At the time, time to boil for Unit 1 was calculated to be 16.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />.

At 08:05 on April 6, 2008, core reload was completed and shutdown risk for Unit 1

returned to Green. At 13:00 on April 6, 2008, the upper internals were installed which

reduced time to boil to 7.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />.

At about mid-morning on April 6, 2008, while developing the risk evaluation for the week

of April 7, 2008, the work control cycle manager was informed by the cycle manager

from the previous week that the work for the two SX cross-tie valves was carrying over

to the week of April 7, 2008. The cycle manager identified the bounding cases for these

valves as 1SX033/34 unable to open if closed and 1SX033/34 unable to close if open.

These bounding cases were discussed with the site risk engineer and the engineer

performed a risk evaluation under those assumptions. The risk engineer determined

that with both valves opened and unable to be closed from the main control room, the

online risk profile for Unit 2 would be Orange. The shift manager was then contacted to

confirm the configuration of the valves and the cycle manager discovered that both

1SX033 and 1SX034 were electrically de-energized and in the open position.

21 Enclosure

At 16:52 on April 6, 2008, the licensee declared the Unit 2 online risk to be Orange due

to the inability to close 1SX033 and 1SX034 from the main control room to prevent

flooding. Unit 1 shutdown risk remained unchanged. At 17:12 on April 6, 2008, an

operator was stationed locally at 1SX033 to close the valve if necessary. The Unit 2

online risk was then returned to green. The total time the plant was in Orange risk

condition was 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br /> and 8 minutes. Time to boil for Unit 1 remained at 7.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> at

that time. The licensee immediately implemented the compensatory measure of an

operator stationed at the valve. They also took corrective actions to reassemble the

valves and place them back in service.

Analysis: The inspectors determined that the licensee failed to update a prior risk

assessment due to changing plant conditions. Specifically, the licensee did not perform

an updated risk evaluation prior to surveillance testing of the Unit 1 Train A EDG based

on existing plant conditions with the 1SX033 and 1SX034 valves opened and unable to

close from the main control room. This plant configuration degraded auxiliary building

flooding mitigation capability during diesel generator testing. The inspectors determined

this to be a performance deficiency warranting a significance evaluation.

The inspectors determined that the licensee failed to consider risk significant SSCs that

were unavailable during maintenance and the issue was within the licensees ability to

foresee and correct and the condition could have been prevented.

The inspectors determined the performance deficiency was more than minor in

accordance with IMC 0612, Appendix E, Section 7, Example f, because the elevated

overall plant risk when correctly assessed was greater than 1.0E-6 Incremental Core

Damage Probability (ICDP) and also put the plant into a higher risk category with

additional risk management actions. This finding had the potential to become a more

significant event if the two isolation valves were required to mitigate flooding in the

auxiliary building.

IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management

Significance Determination Process, was used to determine the significance of the

finding for Unit 2, which was at power during the exposure period. The inspectors

requested that the licensee re-perform the 10 CFR 50.65(a)(4) assessment for the

exposure period of the finding assuming that both 1SX033 and 1SX034 valves were

unable to close. For Unit 2, which was operating at full power at the time, the

Incremental Core Damage Frequency (ICDF) was calculated to be 7.56E-4/yr. Given

that the condition existed for 38 hours4.398148e-4 days <br />0.0106 hours <br />6.283069e-5 weeks <br />1.4459e-5 months <br />, the ICDP was 3.3E-6.

Since the licensee failed to conduct an adequate risk evaluation for the maintenance

activities, the ICDP is equal to the Incremental Core Damage Probability Deficit

(ICDPD). No risk management actions (RMAs) were specified or taken because no risk

evaluation of the actual configuration was performed. Using flowchart 1 of IMC 0609

Appendix K, a finding with an ICDPD of 3.3E-6 with no RMAs is assessed as a White

finding (low to moderate safety significance).

The dominant sequence for this configuration is an Unit 1 pipe break in the auxiliary

building that is not isolated due to the unavailability of the 1SX033 and 1SX034 valves.

The failure of the 1SX033 and 1SX034 valves to close is assumed to result in the failure

to isolate the flood. As auxiliary building flooding continues, the SX pumps for both units

22 Enclosure

will be rendered inoperable resulting in a loss of all SX. Eventually an reactor coolant

pump (RCP) seal LOCA will occur with no inventory makeup capability.

The finding also affected the risk for Unit 1. Since the unit was in a refueling outage, all

maintenance risk assessments are qualitative; therefore the IMC 0609 Appendix K

approach cannot be applied. The risk impact to Unit 1 was considered to be lower than

for Unit 2 because the unit had been shutdown since March 23, 2008, decay heat load

was low, and the time to boil was long. Using these qualitative risk insights, the finding

is assessed to be of very low safety significance (Green) for Unit 1.

The licensee subsequently performed a risk evaluation of the condition that considered

1SX034 available through recovery efforts. In this evaluation, the licensee assumed that

once flooding isolation was needed the valve would be returned to service, the breaker

closed, and the valve operated as necessary from the control room with a slightly

increased human error probability. The inspectors determined that the assumption that

1SX034 was recoverable was incorrect because the valve was electrically isolated and

could not be operated from the control room. More specifically, workers would have to

re-connect wiring and perform other maintenance actions to return the valve to service,

which would not have been feasible in a potentially flooded environment.

The licensee performed another risk evaluation that credited an alternate strategy for

isolating leakage from an SX pipe break in the auxiliary building. The conclusion of this

evaluation was that the risk of the unavailability of the 1SX033 and 1SX034 valves was

of very low safety significance (Green). The inspectors and the SRA reviewed the

alternate strategy and determined that it was not appropriate to credit this strategy for

the reasons described in the following paragraphs.

The alternate strategy for isolating flooding is significantly different from the success

strategy credited in the licensees Probability Risk Analysis (PRA). The PRA credits

detection and isolation of the affected train by closing several motor-operated valves and

shutting down the pump in the train. The strategy is directed by the use of an Abnormal

Operating Procedure, 0BOA PRI-8, Auxiliary Building Flooding. Most of the actions are

performed from the control room. The alternate strategy relies on local visual

identification of the pipe break and local manual actions to close valves to isolate the

flood. Operators would be required to identify the specific section of pipe that failed, use

drawings and other reference information to determine which valves to close, and would

have to locally close valves in the auxiliary building. In some cases, the valves are

normally locked open and operators would be required to obtain a key and unlock the

valve before manually closing it. Since flooding would be in progress in the auxiliary

building, access to equipment is not assured and local actions cannot be considered to

be appropriately reliable to credit for mitigation.

The procedure guidance to implement the alternate strategy was weak. The alternate

strategy requires the use of reference Procedure BOP SX-22, Essential Service Water

Leak Isolation to specify which valves need to be closed based on the line segment of

piping that is determined to be failed. It is not clear how operators would transition from

abnormal operating Procedure 0BOA PRI-8 to reference Procedure BOP SX-22 based

on the inability to close the train Cross-tie Isolation Valves 1SX033 and 1SX034.

Abnormal Operating Procedure 0BOA PRI-8 does not have any actions in the Response

Not Obtained column for the failure of 1SX033 and 1SX034. Although Abnormal

Operating Procedure 0BOA PRI-8 references BOP SX-22, it is only in the system

23 Enclosure

restoration section of the procedure, not in the leak isolation procedure section. It

appears that reference Procedure BOP SX-22 was intended to provide guidance on

specific valves to close to isolate a section of SX piping for repair and not intended to be

required to stop internal flooding.

These procedures were recently implemented, and based on interviews there was

limited operator familiarity. A short training session, focusing on a single flood scenario

as an example, had been given to only three of five crews at the time this condition

existed.

In summary, due to the complex nature of the actions required to isolate flooding if

1SX033 and 1SX034 could not be closed, the lack of adequate procedure guidance, and

limited training and familiarity with leak isolation strategies, the NRC determined that the

likelihood of success was low and the alternate strategy should not be credited to

mitigate the risk from internal flooding if 1SX033 and 1SX034 are unavailable.

The primary cause of this issue is related to the cross-cutting area of Human

Performance for Work Control (H.3.(b)), because the licensee did not appropriately

coordinate work activities by incorporating actions to address the impact of 1SX033 and

1SX034 not able to be closed from control room during diesel generator testing and the

need for work groups to communicate coordinate and cooperate with each others.

Enforcement: 10 CFR 50.65(a)(4) requires in part, that the licensee shall assess and

manage the increase in risk that may result from the proposed maintenance activities

before performing maintenance. Contrary to the above, from April 5, 2008, to

April 6, 2008, the licensee failed to consider risk significant components that were

unavailable in their risk evaluation before performing maintenance. Specifically,

between 03:04 on April 5, 2008, and 17:12 on April 6, 2008, the licensee was at an

unrecognized Orange risk condition for Byron Unit 2 when the licensee conducted the

1A EDG testing with both Unit 1 essential service water train Cross-tie Isolation Valves,

1SX033 and 1SX034, left opened and unable to be closed in the main control room. For

Unit 2, this is an apparent violation of 10 CFR 50.65(a)(4) pending the completion of the

final significance determination. (AV 05000455/2008003-05)

Since the licensee restored the remote operation capability of one of the two isolation

valves after its discovery, the finding does not represent an immediate or current safety

concern. This issue was entered into their corrective action program as IR 759945.

For Unit 1, because of the very low safety significance of the issue and because the

issue has been entered into the licensees CAP, the issue is being treated as a NCV

consistent with Section VI.A.1 of the NRC Enforcement Policy. Since this violation was

licensee identified, the enforcement aspect is described in Section 4OA7 of this report.

1R15 Operability Evaluations (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

24 Enclosure

  • Unit 2 Train A Diesel Generator Air Leak;
  • Foreign Materials Left in Unit 1 Containment;
  • RHR Air Operated Valve Positioner Arm Failure; and
  • Unventable Gas Voids in Containment Recirculation Sump Piping.

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and UFSAR to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment.

This inspection constitutes five samples as defined in IP 71111.15-05.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

.1 Post Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • Unit 1 Train B AFW Pump Fire Related Repair;
  • Auxiliary Building Ventilation 0E Charcoal Booster Fan Damper Work Window;
  • Unit 0 Component Cooling Pump Work Window; and
  • Unit 1 Train B Centrifugal Charging Pump Emergent Shaft Collar Repair.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion), and test

documentation was properly evaluated. The inspectors evaluated the activities against

25 Enclosure

TS, the UFSAR, 10 CFR 50 requirements, licensee procedures, and various NRC

generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the

corrective action program and that the problems were being corrected commensurate

with their importance to safety. Documents reviewed are listed in the Attachment.

This inspection constitutes four samples as defined in IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R20 Outage Activities (71111.20)

.1 Refueling Outage Activities

a. Inspection Scope

The inspectors reviewed the outage schedule and contingency plans for the Unit 1

refueling outage, conducted March 24, 2008, through April 14, 2008, to confirm that the

licensee had appropriately considered risk, industry experience, and previous site-

specific problems in developing and implementing a plan that assured maintenance of

defense-in-depth. During the refueling outage, the inspectors observed portions of the

shutdown and cooldown processes and monitored licensee controls over the outage

activities listed below.

  • Licensee configuration management, including maintenance of defense-in-depth

commensurate with the outage schedule for key safety functions and compliance

with the applicable TS when taking equipment out of service.

  • Implementation of clearance activities and confirmation that tags were properly

hung and equipment appropriately configured to safely support the work or

testing.

  • Controls over the status and configuration of electrical systems to ensure that TS

and outage schedule requirements were met, and controls over switchyard

activities.

  • Controls to ensure that outage work was not impacting the ability of the operators

to operate the spent fuel pool cooling system.

alternative means for inventory addition, and controls to prevent inventory loss.

  • Controls over activities that could affect reactivity.
  • Refueling activities, including fuel handling.
  • Startup and ascension to full power operation, tracking of startup prerequisites,

walkdown of the containment to verify that debris had not been left which could

block emergency core cooling system (ECCS) suction strainers, and reactor

physics testing.

  • Licensee identification and resolution of problems related to refueling outage

activities.

26 Enclosure

In addition to documentation reviews, the inspectors observed the initial Unit 1 head

removal lift as well as the final head reinstallation. The inspectors verified that the height

limitations were maintained during the lifts. Documents reviewed are listed in the

Attachment to this report.

This inspection constitutes one refueling outage sample as defined in IP 71111.20-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

.1 Routine Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Unit 2 Diesel Driven AFW Pump Monthly Surveillance;
  • Unit 1 Bus 112 125V Battery Charger Operability Test;
  • Fire Hazard Panel 18-month Surveillance;
  • Unit 2 Reactor Containment Fan Cooler Monthly Surveillance; and
  • Unit 1 Reheat and Intercept Valve Quarterly Surveillance.

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine whether:

  • any preconditioning occurred;
  • effects of the testing were adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented; as

left setpoints were within required ranges;

  • the calibration frequency was in accordance with TS, the UFSAR, procedures,

and applicable commitments;

  • measuring and test equipment calibration was current; test equipment was used

within the required range and accuracy;

  • applicable prerequisites described in the test procedures were satisfied; test

frequencies met TS requirements to demonstrate operability and reliability;

  • tests were performed in accordance with the test procedures and other

applicable procedures;

  • jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;

27 Enclosure

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of the safety functions;

  • and all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment.

This inspection constitutes five routine surveillance testing sample as defined in

IP 71111.22 Sections -02 and -05.

b. Findings

No findings of significance were identified.

.2 Inservice Testing Surveillance

a. Inspection Scope

The inspectors reviewed the test results for the following activity to determine whether

risk-significant system and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Unit 1 Train B AFW System Full Flow Test (IST).

The inspectors observed activities and reviewed procedures and associated records to

determine whether:

  • any preconditioning occurred;
  • effects of the testing were adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented; as

left setpoints were within required ranges;

  • and the calibration frequency were in accordance with TSs, the USAR,

procedures, and applicable commitments;

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

28 Enclosure

  • tests were performed in accordance with the test procedures and other

applicable procedures;

  • jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of ASME Code,Section XI, and reference

values were consistent with the system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions;

  • and all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment.

This inspection constitutes one inservice inspection sample as defined in Inspection

Procedure 71111.22-05.

b. Findings

No findings of significance were identified.

.3 RCS Leak Detection Inspection Surveillance

The inspectors reviewed the test results for the following activity to determine whether

the equipment was capable of performing its intended function of monitoring RCS

leakage and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Unit 2 RCS Water Inventory Balance February 7, 2008

The inspectors observed in plant activities and reviewed procedures and associated

records to determine whether:

  • preconditioning occurred;
  • effects of the testing were adequately addressed by control room personnel or

engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;

29 Enclosure

  • as left setpoints were within required ranges, and the calibration frequency were

in accordance with TSs, the USAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

  • test equipment was used within the required range and accuracy;
  • applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability;
  • tests were performed in accordance with the test procedures and other

applicable procedures;

  • jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid; test

equipment was removed after testing;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • and all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment.

This inspection constitutes one RCS leak detection inspection sample as defined in

IP 71111.22-05.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System (ANS) Evaluation (71114.02)

.1 ANS Evaluation

a. Inspection Scope

The inspectors reviewed documents and conducted interviews with Emergency

Preparedness (EP) staff regarding the operation, maintenance, and periodic testing of

the ANS in the Byron Stations plume pathway Emergency Planning Zone. The

inspectors reviewed monthly trend reports and siren test failure records from April 2006

through March 2008. Information gathered during document reviews and interviews was

used to determine whether the ANS equipment was maintained and tested in

accordance with Emergency Plan commitments and procedures.

This inspection constitutes one sample as defined in IP 71114.02-05.

b. Findings

No findings of significance were identified.

30 Enclosure

1EP3 Emergency Response Organization (ERO) Augmentation Testing (71114.03)

.1 ERO Augmentation Testing

a. Inspection Scope

The inspectors reviewed and discussed with plant EP staff the emergency plan

commitments and procedures that addressed the primary and alternate methods of

initiating an ERO activation to augment the on-shift ERO as well as the provisions for

maintaining the plants ERO roster. The inspectors also reviewed reports and a sample

of corrective action program records of unannounced off hour augmentation tests, which

were conducted from February 2006 through January 2008 to determine the adequacy

of problem identification and associated corrective actions. The inspectors also

reviewed a sample of the EP training records, approximately 26 records for ERO

personnel, who were assigned to key and support positions, to determine the status of

their training related to their assigned ERO positions.

This inspection constitutes one sample as defined in IP 71114.03-05.

b. Findings

No findings of significance were identified.

1EP5 Correction of EP Weaknesses and Deficiencies (71114.05)

.1 Correction of EP Weaknesses and Deficiencies

a. Inspection Scope

The inspectors reviewed a sample of the Nuclear Oversight staffs 2006 and 2007 audits

of the Byron Station EP program to determine whether these independent assessments

met the requirements of 10 CFR 50.54(t). The inspectors also reviewed critique reports

and samples of corrective action program records associated with the 2007 biennial

exercise, as well as various EP drills conducted in 2007, in order to determine whether

the licensee fulfilled its drill commitments and to evaluate the licensees efforts to

identify, track, and resolve concerns identified during these activities. Additionally, the

inspectors reviewed one actual emergency plan activation that involved an Alert

declaration on November 27, 2007, due to toxic or asphyxiate gases in the plant. The

inspectors independently evaluated the event and the licensee self-assessment to

determine if the licensee effectively implemented the requirements of the emergency

plan. The inspectors reviewed a sample of EP items and corrective actions related to

the facilitys EP program and activities to determine whether corrective actions were

completed in accordance with the sites CAP.

This inspection constitutes one sample as defined in IP 71114.05-05.

b. Findings

No findings of significance were identified.

31 Enclosure

2. RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Review of Licensee Performance Indicators for the Occupational Exposure Cornerstone

a. Inspection Scope

The inspectors reviewed the licensees occupational exposure control cornerstone

performance indicators (PIs) to determine whether the conditions resulting in any PI

occurrences had been evaluated, and identified problems had been entered into the

CAP for resolution.

This inspection does not constitute an inspection sample as defined in IP 71121.01-5,

but it does supplements the sample reported in inspection report 05000454/2008002;

05000455/2008002.

b. Findings

No findings of significance were identified.

.2 Plant Walkdowns and Radiation Work Permit (RWP) Reviews

a. Inspection Scope

The adequacy of the licensees internal dose assessment process for internal exposures

>50 millirem committed effective dose equivalent was assessed. There were no internal

exposures >50 millirem committed effective dose equivalent.

This inspection constitutes one required sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.3 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed a sample of the licensees self-assessments, audits, Licensee

Event Reports (LERs), and Special Reports related to the access control program to

verify that identified problems were entered into the CAP for resolution.

Also, the inspectors reviewed licensee documentation packages for all PI events

occurring since the last inspection to determine if any of these PI events involved dose

rates >25 R/hr at 30 centimeters or >500 R/hr at 1 meter. Barriers were evaluated for

failure and to determine if there were any barriers left to prevent personnel access.

There were no events of unintended exposures >100 millirem total effective dose

equivalent (or >5 rem shallow dose equivalent or >1.5 rem lens dose equivalent),

therefore a substantial potential for an overexposure did not occur.

32 Enclosure

This inspection constitutes two required samples as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning And Controls (71121.02)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed plant collective exposure history, current exposure trends,

ongoing and planned activities in order to assess current performance and exposure

challenges. This included determining the plants current three-year rolling average for

collective exposure in order to help establish resource allocations and to provide a

perspective of significance for any resulting inspection finding assessment.

Also, the inspectors reviewed documents to determine if there were site-specific trends

in collective exposures and source-term measurements.

Additionally, the inspectors reviewed procedures associated with maintaining

occupational exposures ALARA and processes used to estimate and track work activity

specific exposures.

This inspection constitutes three required samples as defined in IP 71121.02-5.

b. Findings

No findings of significance were identified.

.2 Radiological Work Planning

a. Inspection Scope

The inspectors compared the results achieved including dose rate reductions and

person-rem used with the intended dose established in the licensees ALARA planning

for these work activities. Reasons for inconsistencies between intended and actual work

activity doses were reviewed.

This inspection constitutes one required sample as defined in IP 71121.02-5.

b. Findings

No findings of significance were identified.

.3 Verification of Dose Estimates and Exposure Tracking Systems

a. Inspection Scope

The inspectors reviewed the assumptions and bases for the current annual collective

exposure estimate including procedures, in order to evaluate the licensees methodology

33 Enclosure

for estimating work activity-specific exposures and the intended dose outcome. Dose

rate and man-hour estimates were evaluated for reasonable accuracy.

Additionally, the licensees exposure tracking system was evaluated to determine

whether the level of exposure tracking detail, exposure report timeliness, and exposure

report distribution was sufficient to support control of collective exposures. RWPs were

reviewed to determine if they covered too many work activities to allow work activity

specific exposure trends to be detected and controlled. During the conduct of exposure

significant work, the inspectors evaluated if licensee management was aware of the

exposure status of the work and would intervene if exposure trends increased beyond

exposure estimates.

This inspection constitutes one required and one optional sample as defined in

IP 71121.02-5.

b. Findings

No findings of significance were identified.

.4 Source-Term Reduction and Control

a. Inspection Scope

The inspectors reviewed licensee records to determine the historical trends and current

status of tracked plant source terms and determined that the licensee was making

allowances and had developing contingency plans for expected changes in the source

term due to changes in plant fuel performance issues or changes in plant primary

chemistry.

Also, the inspectors verified that the licensee had developed an understanding of the

plant source-term, that this included knowledge of input mechanisms to reduce the

source term and that the licensee had a source-term control strategy in place that

included a cobalt reduction strategy and shutdown ramping and operating chemistry plan

which was designed to minimize the source-term external to the core. Other methods

used by the licensee to control the source term including component and system

decontamination, and use of shielding were evaluated.

This inspection constitutes one required and one optional sample as defined in

IP 71121.02-5.

b. Findings

No findings of significance were identified.

.5 Declared Pregnant Workers

a. Inspection Scope

The inspectors reviewed dose records of declared pregnant workers for the current

assessment period to verify that the exposure results and monitoring controls employed

by the licensee complied with the requirements of 10 CFR Part 20.

34 Enclosure

This inspection constitutes one required sample as defined in IP71121.02-5.

b. Findings

No findings of significance were identified.

.6 Problem Identification and Resolutions

a. Inspection Scope

The inspectors reviewed the licensees self-assessments, audits, and Special Reports

related to the ALARA program since the last inspection to determine if the licensees

overall audit programs scope and frequency for all applicable areas under the

Occupational Cornerstone met the requirements of 10 CFR 20.1101(c).

Additionally, the licensees CAP program was also reviewed to determine if repetitive

deficiencies and/or significant individual deficiencies in problem identification and

resolution had been addressed.

This inspection constitutes two required samples as defined in IP 71121.02-5.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 PI Verification (71151)

.1 Drill/Exercise Performance

a. Inspection Scope

The inspectors sampled licensee submittals for the Drill/Exercise Performance PI for the

period from the second quarter 2007 through fourth quarter 2007. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors

reviewed the licensees records associated with the performance indicator to verify that

the licensee accurately reported the indicators in accordance with relevant procedures

and the NEI guidance. Specifically, the inspectors reviewed licensee records and

processes including procedural guidance on assessing opportunities for the PI;

assessments of PI opportunities during pre-designated control room simulator training

sessions, performance during the 2007 biennial exercise, and performance during other

drills. Specific documents reviewed are described in the Attachment to this report.

This inspection constitutes one drill/exercise performance sample as defined by

IP 71151-05.

b. Findings

No findings of significance were identified.

35 Enclosure

.2 ERO Drill Participation

a. Inspection Scope

The inspectors sampled licensee submittals for the ERO Drill Participation PI for the

period from the second quarter 2007 through fourth quarter 2007. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI Document 99-02, Revision 5, were used. The inspectors reviewed

the licensees records associated with the performance indicator to verify that the

licensee accurately reported the indicator in accordance with relevant procedures and

the NEI guidance. Specifically, the inspectors reviewed licensee records and processes

including procedural guidance on assessing opportunities for the PI; performance during

the 2007 biennial exercise and other drills; and revisions of the roster of personnel

assigned to key emergency response organization positions. Specific documents

reviewed are described in the Attachment to this report.

This inspection constitutes one ERO drill participation sample as defined by

IP 71151-05.

b. Findings

No findings of significance were identified.

.3 ANS

a. Inspection Scope

The inspectors sampled licensee submittals for the ANS PI for the period from the

second quarter 2007 through fourth quarter 2007. To determine the accuracy of the PI

data reported during those periods, PI definitions and guidance contained in the NEI

Document 99-02, Revision 5, were used. The inspectors reviewed the licensees

records associated with the PI to verify that the licensee accurately reported the indicator

in accordance with relevant procedures and the NEI guidance. Specifically, the

inspectors reviewed licensee records and processes including procedural guidance on

assessing opportunities for the PI and results of periodic ANS operability tests. Specific

documents reviewed are described in the Attachment to this report.

This inspection constitutes one alert and notification system sample as defined by

IP 71151-05.

b. Findings

No findings of significance were identified.

.4 Unplanned Power Changes per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Power Changes per 7000

Critical Hours PI for Units 1 and 2 for the second quarter 2007 through fourth quarter

2007. To determine the accuracy of the PI data reported during those periods, the

36 Enclosure

inspectors used PI definitions and guidance contained in Revision 5 of NEI 99-02. The

inspectors reviewed the licensees operator narrative logs, issue reports, maintenance

rule records, event reports, and NRC integrated inspection reports for this period to

validate the accuracy of the submittals. The inspectors also reviewed the licensees

issue report database to determine if any problems had been identified with the PI data

collected or transmitted for this indicator and none were identified. Specific documents

reviewed are described in the Attachment to this report.

This inspection constitutes two samples of the Unplanned Power Changes per

7000 Critical Hours PI as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.5 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences PI for the period of July 2007 through March 2008. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI 99-02, Revision 5, were used. The inspectors reviewed the

licensees assessment of the PI for occupational radiation safety to determine if indicator

related data was adequately assessed and reported. To assess the adequacy of the

licensees PI data collection and analyses, the inspectors discussed with radiation

protection staff, the scope and breadth of its data review, and the results of those

reviews. The inspectors independently reviewed electronic dosimetry dose rate and

accumulated dose alarm and dose reports and the dose assignments for any intakes

that occurred during the time period reviewed to determine if there were potentially

unrecognized occurrences. The inspectors also conducted walkdowns of numerous

locked high and very high radiation area entrances to determine the adequacy of the

controls in place for these areas. Specific documents reviewed are described in the

Attachment to this report.

This inspection constitutes one required occupational radiological occurrences sample

as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of items Entered Into the CAP

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify that they were being entered into the licensees CAP at

37 Enclosure

an appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent of condition reviews, and previous occurrences reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached list of documents reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Sections 1 and 2 of this report.

b. Findings

No findings of significance were identified.

a. (Open) Unresolved Item (URI) 05000454/455/2008003-06: Unit 1 and Unit 2 AFW

Tunnel Hatch Margin to Safety

Late in the inspection period the licensee identified that the design analysis for

evaluation of the AFW tunnel flood seal covers did not include the effects of a high

energy line break in the main steam isolation valve tunnels at another facility. The NRC

inspectors at that facility questioned why a dynamic load factor as a result of the impulse

pressure following a high energy line break had not been considered in an analytic

calculation perform to support the operability evaluation.

Following a review of the licensees evaluation, the inspectors questioned the licensees

conclusion that the operability of the AFW hatches continued to be supported despite

analytical results showing a factor of safety for the concrete expansion anchors

supporting the hatches of less than 2.0, which is contrary to the guidance provided in

NRC Bulletin 79-02, Pipe Support Base Plate Designs Using Concrete Expansion

Anchors. Additionally, the inspectors noted that the licensees evaluation did not

address Section C.13 of NRC Technical Guidance 9900, Operability Determinations &

Functionality Assessment for Resolution of Degraded or Nonconforming Conditions

Adverse to Quality or Safety. Specifically, Section C.13 stated that if a structure was

degraded, the licensee should assess the structures capability of performing its

specified function. As long as the identified degradation did not result in exceeding

acceptance limits specified in applicable design codes and standards referenced in the

design basis documents, the affected structure was either operable or functional. The

licensee also identified additional errors that reduced the margin of safety for the

structural integrity of a high energy line break barrier.

At the close of the inspection period temporary modifications had been implemented at

both facilities that restored the margin of safety to greater than 2.0. Pending additional

follow-up by the inspectors for the past operability and timeliness of corrective actions,

extent of condition, and corrective actions, this item will remain open.

(URI 005000454/2008003-06;05000455/2008003-06)

38 Enclosure

.2 Daily CAP Reviews

a. Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the six month period of December 1, 2007 through

May 31, 2008, although some examples expanded beyond those dates where the scope

of the trend warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees CAP

trending reports. Corrective actions associated with a sample of the issues identified in

the licensees trending reports were reviewed for adequacy.

This review constituted a single semi-annual trend inspection sample.

b. Findings

The inspectors identified two apparent trends during this review. The first trend is the

identification by the NRC of six findings or violations with a cross cutting aspect of

decision making within the last four calendar quarters. Three of these findings were

documented in NRC inspection report 05000454/2007009, two of the findings were

documented in NRC inspection report 05000454/2007004 and the remaining item was

documented in this inspection report. Four of these items were in the Mitigating

Systems cornerstone and two were in the Initiating Events cornerstone.

39 Enclosure

The licensee had previously implemented a Human Performance Improvement Plan

(HPIP) as part of a previous negative trend. This trend was initially documented in the

NRC Mid-Cycle Review dated August 30, 2005 as a substantive cross cutting issue.

The licensees corrective actions were assessed and based upon that assessment and a

declining trend of cross cutting issues the substantive cross cutting issue was closed in

the Mid-Cycle Review dated August 31, 2006.

The inspectors assessment determined that the licensee had recognized the new trend

and taken actions to address the declining performance. However, these actions had

not yet proven effective in substantially mitigating the adverse trend.

The second trend identified during this semi-annual trend review was a negative trend in

plant aging issues. Examples included:

Station Auxiliary Transformer 242-2 failure documented in this inspection report

was identified by the licensee as caused by age related failure of an electrical

insulator;

The fire on the Unit 1 Train B diesel driven auxiliary feedwater pump was

identified by the licensee as age related relaxation of the exhaust manifold bolts

along with an inadequate preventative maintenance program. This item was

documented in this inspection report;

The licensees unplanned entry into an Orange risk condition, documented in this

inspection report, was to correct long standing age-related issues with poor

material condition of certain SX valves. These valves had not been removed for

maintenance since initial startup;

The degradation of the SX return header piping risers to the Ultimate Heat Sink

cooling tower was an age related degradation combined with inadequate

corrective actions. This item was documented in NRC inspection report

05000454/2007009;

In the Spring of 2006 the licensee identified degraded vacuum breakers on the

blowdown line to the river. The vacuum breakers had degraded over time and

were not receiving maintenance. The issue related to leaking vacuum breakers

was documented in NRC inspection report 05000454/2006-002 and

05000454/2006004; and

The degradation of non-safety related circulating water piping was identified in

the basement of the Unit 1 and Unit 2 turbine building. This degradation was

found as part of the extent of condition assessment by the licensee to the SX

riser issue. This piping was degraded due to the licensees practice of draining

water to the area around the piping during refueling outages which over many

years caused pipe corrosion.

Each of the first five examples listed above received appropriate regulatory follow-up in

the inspection reports listed. The last example was not of direct regulatory significance

and was not documented in an NRC inspection report. In response to the above issues,

most notably the SX riser degradation the licensee has greatly increased their

assessment of the current condition of plant equipment and has significantly increased

40 Enclosure

the efforts spent to address these issues. Nevertheless as the plant continues to

operate age related degradation will cause challenges.

No findings of significance were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 Plant Response to Seismic Activity

a. Inspection Scope

The inspectors reviewed the plants response to a seismic event. On April 18, 2008, an

earthquake occurred in Southern Illinois. No individual at the licensees facility felt the

earthquake and no instrumentation on site detected the earthquake but personnel offsite

did feel the earthquake and reported it to the control room personnel. Shift personnel

entered the appropriate abnormal operating procedure and attempted to contact the

National Earthquake Information Center but were only able to leave a message.

Subsequently licensee personnel performed an inspection of selected plant facilities and

systems and did not identify any damage. The inspectors also performed a walkdown of

licensee facilities and systems and did not identify any damage. The licensee issued a

corporate wide Press Release and made a voluntary Event Notification to the NRC

Headquarters Operations Officer. Documents reviewed in this inspection are listed in

the Attachment.

This inspection constitutes one sample as defined in IP 71153.

b. Findings

No findings of significance were identified.

.2 (Closed) LER 05000454/2008-001-00: Technical Specification Non-Compliance of

Containment Sump Monitor Due to Improper Installation During Original Construction.

This LER, addresses a past operability issue with the Unit 1 containment floor

drain sump flow monitor that was discovered on March 28, 2008. Technical

Specification3.4.15, RCS Leakage Detection Instrumentation, required one

containment sump monitor to be operable in order to detect reactor coolant system

leaks. The sump was required to be able to detect a one gpm leak within one hour.

During a refueling outage a member of the licensees staff questioned the operability of

the sump with penetrations through the cover allowing water to flow into the sump while

bypassing the leakage measuring device. Subsequently the licensee determined the

sump was improperly installed and had been so since initial construction in 1976.

A corrective action document was written and the sump was modified to restore

operability prior to the restart of the unit. This same error had previously existed on

Unit 2 but had been inadvertently corrected in 2004 during a modification to install a

different type of sump level instrument. Alternative equipment existed to assist the

operators in identifying RCS unidentified leakage. These instruments included a

containment radiation monitor, volume control tank level indicators, post accident

containment sump level instruments, containment pressure indicators, containment

41 Enclosure

temperature indicators, and pressurizer level instruments. The enforcement aspects of

this finding are discussed in Section 4OA7 of this report. Documents reviewed as part of

this inspection are listed in the Attachment. This LER is closed.

This inspection constitutes one sample as defined in IP 71153.

.3 (Closed) LER 05000455/2008-001-00: Unit 2 Emergency Diesel Generators and

Auxiliary Feedwater Pump Automatic Start Resulting from a Loss of Offsite Power Due

to a Failed Insulator Causing a Differential Phase Overcurrent.

This event was previously discussed in Inspection Report 05000454/2008002;

05000455/2008002, Section 4OA3, and in Section 1R12 of this Report. The NRC

reviewed the event risk in accordance with Management Directive 8.3, NRC Incident

Investigation Program, and determined that the conditional core damage probability did

not warrant additional inspection. Documents reviewed as part of this inspection are

listed in the Attachment. This LER is closed.

This inspection constitutes one sample as defined in IP 71153.

4OA5 Other Activities

.1 Follow-up of Backfit Activities

a. Inspection Scope

As documented in Inspection Report 05000454/2008008; 05000455/2008008, the

inspectors identified the licensee did not consider spurious failure/opening of

the 4160 volt or 480 Volts AC as a valid single failure in Amendment No. 95. The

inspectors further noted that the NRC did not evaluate the potential for a passive failure

of the electrical breakers even though passive failures were required to be evaluated

under 10 CFR Part 50, Appendix A. After further review, the inspectors determined that

the provisions of 10 CFR 50.109(a)(4), were applicable and that a modification is

necessary to bring a facility into compliance with the rules or orders of the NRC. The

licensee was requested to respond with a description of the intended actions to address

the noncompliance including a proposed schedule to complete those actions.

In a letter dated June 4, 2008, from D. Hoots (ADAMS Accession No. ML081560649),

the licensee stated that a design basis re-analysis of the ultimate heat sink would be

completed by December 5, 2008. This issue is considered open pending completion of

the licensees re-analysis. (OTHR 05000454/2008003-07; 05000455/2008003-07)

.2 RCS Dissimilar Metal Butt Welds (DMBW) (TI 2515/172, Revision 0)

a. Inspection Scope

The inspectors conducted a review of the licensees activities regarding DMBW

mitigation and inspection implemented in accordance with the industry self-imposed

mandatory requirements of Materials Reliability Program, (MRP) -139, Primary System

Piping Butt Weld Inspection and Evaluation Guidelines. TI 2515/172, Reactor Coolant

System Dissimilar Metal Butt Welds, was issued February 21, 2008, to support the

42 Enclosure

evaluation of the licensees implementation of MRP-139. This review was conducted for

both Units 1 and 2 unless otherwise noted.

The documents reviewed by the inspector for this inspection are listed in the Attachment

to this report.

From March 24, 2008 through April 3, 2008, the inspectors performed a review in

accordance with TI-172 which included the following:

(1) Licensees Implementation of the MRP-139 Baseline Inspections

The inspectors verified that the licensees inspection program included inspections of the

pressurizer, hot let and cold leg temperature DMBWs and that the schedules for these

baseline inspections are consistent with the requirements stated in MRP-139. If any

baseline inspection schedules deviated from MRP-139 guidelines, the inspectors also

determined what deviations were planned and what the general basis for the deviation

was.

The inspectors verified that the licensee had completed MRP-139 baseline inspections

of all pressurizer DMBWs by December 31, 2007.

(2) Volumetric Examinations

The inspectors reviewed the volumetric examinations of the Unit 1 reactor vessel outlet

safe end to nozzle weld baseline inspection completed in 2005 and the Unit 2 reactor

vessel inlet safe end to nozzle weld baseline inspection completed in 2007 and verified

the examinations were performed in accordance with the guidelines in MRP-139,

Section 5.1. The inspectors also verified that these examinations were performed by

qualified personnel and that any deficiencies identified were appropriately dispositioned

and resolved.

The inspectors reviewed the volumetric examinations of the Unit 1 pressurizer surge

nozzle overlay completed in 2006 and the Unit 2 pressurizer relief valve nozzle overlay

completed in 2007 and verified the examination was performed consistent with the NRC

staff relief request authorization for the weld overlay. If the inspection coverage

warranted further evaluation, the inspector also reviewed the licensees documentation

of the basis for achieving the required inspection coverage.

The inspectors verified that the above examinations were performed by qualified

personnel and that any deficiencies identified were appropriately dispositioned and

resolved.

(3) Weld Overlays

During the current outage no weld overlays pertinent to MRP-139 were performed on

Unit 1. The inspectors reviewed weld overlay documentation for the Unit 1 pressurizer

surge nozzle overlay and the Unit 2 pressurizer relief valve nozzle overlay to verify that

the welds were performed in accordance with NRC staff relief request authorizations and

the ASME Code. The inspectors also verified that the welds were performed by qualified

personnel and that any deficiencies were appropriately dispositioned and resolved.

43 Enclosure

(4) Mechanical Stress Improvement

There were no mechanical stress improvement activities performed or planned by the

licensee to comply with their MRP-139 commitments. Hence, NRC inspection of such

mechanical stress improvements was not applicable.

(5) ISI Program

The inspectors verified that the licensees MRP-139 ISI program includes the applicable

welds and that the welds are included in categories consistent with MRP-139 guidelines.

The inspectors verified that the licensees inspection program and procedures specified

inspection frequencies consistent with Tables 6-1 and 6-2 of MRP-139. The inspectors

also determined if any welds were categorized as H or I, and for those welds reviewed

the licensees basis for the categorization and the licensees plans for addressing

potential primary water stress corrosion cracking. The inspector also determined if any

deviations were planned from the inspection guidelines of MRP-139.

b. Observations

Summary: Byron Units 1 and 2 are Westinghouse four loop design plants and were

determined by the licensee to contain susceptible DMBWs per MRP-139. To date,

the pressurizer DMBWs on both units have been mitigated by full structural overlays

and have received baseline volumetric examination. The remaining susceptible welds

(MRP-139 category "D" and "E") for Units 1 and 2 are planned for possible mitigation in

2011 and 2013 respectively. In accordance with requirements of TI 2515/172,

Revision 0, the inspectors evaluated and answered the following questions:

(1) Licensees Implementation of the MRP-139 Baseline Inspections:

1. a. Have the baseline inspections been performed or are they scheduled to be

performed in accordance with MRP-139 guidance?

Yes. Baseline inspections for pressurizer DMBWs were performed post

mitigation in the Fall of 2006 for Unit 1 and in the Spring of 2007 for

Unit 2. The Category "D" and "E" welds were inspected in the Spring of

2005 for Unit 1 and in the Fall of 2005 for Unit 2.

b. Were the baseline inspections of the pressurizer temperature DMBWs of the

nine plants listed in 03.01.b completed during the spring outages?

No. Byron is not one of the nine plants listed in 03.01.b.

2. Is the licensee planning to take any deviations from the MRP-139 baseline

inspection requirements? If so, what deviations are planned, what is the general

basis for the deviation, and was the NEI- 03-08 process for filing a deviation

followed?

No. No deviations from the MRP-139 baseline inspection requirements are

planned for either unit.

44 Enclosure

(2) Volumetric Examinations

1. Performed in accordance with the examination guidelines in MRP-139,

Section 5.1, for unmitigated welds or mechanical stress improvement welds and

consistent with NRC staff relief request authorization for weld overlaid welds?

Yes. The inspectors reviewed the volumetric examinations of the Unit 1

pressurizer surge nozzle overlay completed in 2006 and the Unit 2 PORV

nozzle overlay completed in 2007 and verified the examination was

performed consistent with the NRC staff relief request authorization for

the weld overlay. The inspectors also reviewed the volumetric

examinations of the Unit 1 reactor vessel outlet safe end to nozzle weld

baseline inspection completed in 2005 and the Unit 2 reactor vessel inlet

safe end to nozzle weld baseline inspection completed in 2007 and

verified the examinations were performed in accordance with the

guidelines in MRP-139, Section 5.1.

2. Performed by qualified personnel? (Briefly describe the personnel

training/qualification process used by the licensee for this activity.)

Yes. The UT examiners were qualified to the applicable ASME Code,

Section XI, Appendix VIII, PDI requirements.

Performed such that deficiencies were identified, dispositioned, and resolved?

Yes. Indications were identified in the weld overlay for several DMBWs on both

the Unit 1 and Unit 2 pressurizers. The inspectors reviewed the

evaluations performed for the Unit 1 surge nozzle overlay and the Unit 2

PORV nozzle overlay and determined that the evaluations were

acceptable.

(3) Weld Overlays

1. Performed in accordance with ASME Code welding requirements and consistent

with NRC staff relief request authorizations? Has the licensee submitted a relief

request and obtained NRR staff authorization to install the weld overlays?

Yes. Weld overlay documentation for the Unit 1 surge nozzle overlay and the

Unit 2 PORV nozzle overlay were reviewed. The welds were performed

in accordance with NRC staff relief request authorizations and the ASME

Code.

2. Performed by qualified personnel? (Briefly describe the personnel

training/qualification process used by the licensee for this activity.)

Yes. Welders were qualified in accordance with ASME Code,Section IX and

were verified to be current.

3. Performed such that deficiencies were identified, dispositioned, and resolved?

45 Enclosure

Yes. Welds were performed in accordance with the ASME Code and

10 CFR 50, Appendix B requirements.

(4) Mechanical Stress Improvement

There were no stress improvement activities performed or planned by this licensee to

comply with their MRP-139 commitments.

(5) ISI Program

1. Has the licensee prepared an MRP-139 ISI program? If not, briefly summarize

the licensees basis for not having a documented program and when the licensee

plans to complete preparation of the program.

Yes. Susceptible welds were appropriately included in the program and

categorization and inspection schedules are in accordance with MRP-139

guidance.

2. In the MRP-139 ISI program, are the welds appropriately categorized in

accordance with MRP-139? If any welds are not appropriately categorized,

briefly explain the discrepancies.

Yes. Welds included in the MRP-139 program were properly categorized.

3. In the MRP-139 ISI program, are the ISI frequencies, which may differ between

the first and second intervals after the MRP-139 baseline inspection, consistent

with the inservice inspections frequencies called for by MRP-139?

Yes. Those DMBWs which have been overlaid and those yet to be mitigated

are scheduled for reexamination in accordance with MRP-139.

4. If any welds are categorized as H or I, briefly explain the licensees basis of the

categorization and the licensees plans for addressing potential primary water

stress corrosion cracking (PWSCC).

Pressurizer DMBWs (safety valve, relief valve, spray, and surge line nozzles) for

both units were categorized as "H" due to a lack of qualified technique which

prevented an Appendix VIII examination. These welds, on both units have been

mitigated by full structural weld overlays.

5. If the licensee is planning to take deviations from the inservice inspection

requirements of MRP-139, what are the deviations and what are the general

bases for the deviations? Was the NEI 03-08 process for filing deviations

followed?

No. No deviations are currently planned for either unit.

c. Findings

No findings of significance were identified.

46 Enclosure

.3 (Closed) Unresolved Item (URI) 05000455/2008002-03: Unit 2 Notice of Unusual Event

due to Loss of Both SATs

On March 25, 2008, Unit 2 SAT 242-2 de-energized upon receipt of a C phase to ground

relay actuation. As designed the upstream switchyard breakers opened de-energizing

both SAT 242-1 and 242-2. Also, as designed, the downstream breakers opened

resulting in a fast transfer of the 6.9KiloVolt buses to the Unit Auxiliary Transformers and

the transfer of the 4KiloVolt buses to the EDGs which had automatically started. The

licensee entered a Notification of Unusual Event and the NRC entered the Monitoring

Mode. The licensee subsequently transferred the 4KiloVolt loads to the Unit 1 SATs and

began troubleshooting efforts. Following verification that a fault did not exist on the SAT

242-1 circuit all Unit 2 house loads were transferred to SAT 242-1. Subsequently the

licensee exited the Unusual Event and the NRC exited the Monitoring Mode.

The inspectors reviewed the plants and the operators responses to the loss of both unit

SATs to determine if the responses were appropriate and in accordance with design,

procedures and training.

At the close of the previous inspection period additional information was required to

determine if the loss of the SAT was a finding, or if it constituted a deviation or violation.

The additional information needed was the results of the licensees root cause

evaluation and proposed corrective actions. The inspectors reviewed the licensees root

cause analysis report, additional documentation, and interviewed licensee personnel.

The root cause analysis determined that the SAT tripped due to the failure of a ceramic

insulator on the B-Phase of the 4KiloVolt non-segregated bus duct. Routine preventive

testing of the bus duct did not identify the degraded insulator. The testing performed

was in accordance with licensee procedures and industry recommended practices.

Based upon these reviews, the inspectors determined that the loss of the SAT was not a

finding, deviation, or violation. Documents reviewed are listed in the Attachment. This

URI is closed.

.4 (Closed) URI 05000455/2008002-04: Unit 1 Train B Auxiliary Feedwater Pump Diesel

Fire and Shutdown During Surveillance

On March 21, 2008, during a routine 18-month surveillance test of the Unit 1 AFW pump,

the operator in the room reported that the diesel was on fire. The diesel driven AFW

pump was shutdown and declared inoperable resulting in the licensee entering a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

shutdown Limiting Condition for Operation. Subsequently, the licensee shutdown for a

planned refueling outage, exiting the applicable operating modes, and negating the need

to repair the diesel within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Prior to the end of the refueling outage the licensee

repaired the diesel, performed appropriate surveillance tests, and declared the diesel

driven pump operable. Review was performed as part of IP 71111.15, Operability

Evaluations and after reviewing engineering documents, interviewing operators, and

performing a specific assessment of the effects of a carbon dioxide release on the

operation of the diesel the inspectors agreed with the licensees conclusion that the

diesel remained operable during the fire. Even if the operators secure the AFW pump in

the event of a fire, they would be able to restart the pump as necessary as the pump is

fully operable. Documents reviewed are listed in that section. This URI is closed.

47 Enclosure

.5 (Closed) NRC Temporary Instruction (TI) 2515/166, Pressurized Water Reactor

Containment Sump Blockage (NRC Generic Letter 2004-02) - Units 1 and 2

a. Inspection Scope

The inspectors reviewed the station implementation of the licensees commitments

documented in their December 31, 2007, response to Generic Letter (GL) 2004-02,

Potential Impact of Debris Blockage on Emergency Recirculation during Design Basis

Accidents at Pressurized Water Reactors. The inspectors performed walkdowns and

reviewed the Engineering Change Packages (ECs) associated with the ECCS throttle

valves modifications and the 10 CFR 50.59 evaluations for these ECs. In addition, the

inspectors reviewed: two samples of the completed and approved for use changes for

the UFSAR, Revision 12, that have not been incorporated yet; one sample of an in-route

change for the UFSAR, Revision 12; and one sample already incorporated in

Revision 11. The documents reviewed are listed at the end of the report. The

inspection was conducted in accordance with TI 2515/166.

b. Inspection Documentation

The inspectors determined the following answers to the Reporting Requirements

detailed in the TI 2515/166:

(1) Did the licensee implement the plant modifications and procedure changes committed to

in their GL 2004-02 responses?

The licensee has implemented the plant modifications and procedure changes

committed to in their GL 2004-02. In addition, the licensee cancelled the cyclone

separator modification for Unit 1 because test results showed that they are not

susceptible to blockage as documented in EC 364979, Evaluate SI Throttle Valve Test

Results from Wyle Labs to Document Acceptability of New Trim Design. The

commitments included:

  • Installation of permanent modification of the sump strainer assemblies.

This commitment was previously reviewed and documented in NRC Inspection

Reports 05000454/2007003 and 05000455/2007003. Structural analyses of

the new strainer assemblies were performed through BYR06-025, Design

Loads and Sizing Limitations for the ECCS Containment Sump Trash Rack,

and 3 SA-096-016, CCI Structural Analysis of Strainer and Support Structure.

  • Installation of permanent modification of the ECCS throttle valves at Unit 2 and

replacement of the fibrous insulation with reflective metal insulation within the zone

of influence at Unit 1.

This commitment was previously reviewed and documented in NRC Inspection

Reports 05000454/2008006 and 05000455/2008006.

  • Installation of permanent modification of the ECCS throttle valves at Unit 1 for which

licensee received approval for an extension until Spring 2008.

48 Enclosure

This modification was completed at the time of this inspection and was

documented in EC 359455, Downstream Activities Effects Related to [Generic

Safety Issue] (GSI) -191 - U1. In addition, the inspectors performed a

walkdown of this modification.

  • Perform latent debris walkdowns, and debris generation and transport analyses.

The commitment to perform containment walkdowns was previously reviewed

and documented in NRC Inspection Report 05000454/2008006 and

05000455/2008006. The debris generation was estimated by S040-BY-5010,

GSI-191 Latent Debris Collection-Unit 1, and S040-BY-5030, GSI-191 Latent

Debris Collection-Unit 2. Debris generation was analyzed by BYR05-041,

GSI-191 post-LOCA Debris Generation. Debris transportation was analyzed

through BYR05-042, Post-LOCA Debris Transport Evaluation for Resolution of

GSI-191.

  • Perform evaluation of strainer performance including chemical effects.

Head loss testing and analysis, including chemical effects, were previously

reviewed and documented in NRC Inspection Report 05000454/2008006

and 05000455/2008006. In addition, the following tests were reviewed:

(1) DIT-BYR-06-007, Debris Concentration Measurements Results, and

(2) BYR-05-061, GSI-191 Evaluation of Long Term Downstream Effects.

  • Perform evaluation of downstream and upstream effects.

Downstream effects analysis for fuel, vessel, and component wear and

blockage were previously reviewed and documented in NRC Inspection Report 05000454/2008006 and 05000455/2008006. Testing of wear and blockage to

the ECCS throttle valves and Containment Spray System Cyclone Separator

was documented in EC 364979, Evaluate SI Throttle Valve Test Results from

Wyle Labs to Document Acceptability of New Trim Design. Upstream effects

were evaluated by S040-BYR-5032, GSI-191 Debris Generation Walkdown-

U2, and S040-BYR-5011, GSI-191 Debris Generation Walkdown-U1.

  • Determine minimum available net positive suction head margin for the RHR pumps

at switchover to sump recirculation.

Minimum available net positive suction head margin was previously reviewed

and documented in NRC Inspection Report 05000454/2008006 and

05000455/2008006. The hydraulic model of the ECCS was performed

by BYR06-029, SI/RHR/CS/CV System Hydraulic Analysis in Support of

GSI-191.

  • Establish programmatic controls to ensure that potential sources of debris introduced

into containment are assessed for adverse affects.

The licensee performed an enhancement to CC-AA-102, Design Input and

Configuration Change Impact Screening, to introduce a requirement to

review the impact of a proposed change on the documentation that forms

the design basis for their response to GL 2004-02. In addition, the licensee

49 Enclosure

upgraded OP-AA-116-101, Equipment Labeling, and committed to use

1/2 BOSR Z.5.1.1-1, Containment Loose Debris Inspection, CC-AA-205,

Control of Undocumented/Unqualified Coatings Inside Containment, and

1/2 BVSR XII-11, Containment Building Interior Surface Coating Inspection as

administrative controls for limiting debris sources inside containment. Also,

latent debris measurements inside containment every four refueling outages

are currently being tracked by Predefines 174052 and 174053. IR 777152 is

tracking the addition of a note explaining the basis for the activity and a caution

to factor in the impact of changes to it when the procedure is generated.

(2) Has the licensee updated its licensing bases to reflect the corrective actions taken in

response to GL 2004-02?

The licensee has updated its licensing bases to reflect the corrective actions taken in

response to GL 2004-02 with the exception of one change to the UFSAR relevant to the

recently completed modification of the ECCS throttle valves for Unit 1. This UFSAR

change is pending licensee approval.

(3) If the licensee or plant has obtained an extension past the completion date of this TI,

document what actions have been completed and what actions are outstanding.

The licensee requested and received approval for an extension until spring 2008 to

complete the installation of ECCS throttle valves for Unit 1. During the refueling outage

of spring 2008, the licensee completed this action.

Completed actions are:

  • Installation of new strainer assemblies for both units;
  • Installation of modified ECCS throttle valves at both units;
  • Replacement of fibrous insulation with reflective metal insulation within the zone

of influence at Unit 1;

  • Programmatic controls had been put in place;
  • Associated analyses and testing; and
  • Licensing bases update of the pertinent completed actions.

Outstanding actions are:

  • Licensing bases update relevant to the ECCS throttle valve modification at Unit 1

This TI is closed for both units. This documentation of TI-2515/166 completion as well

as any results of sampling audits of licensee actions will be reviewed by the NRC staff

(Office of Nuclear Reactor Regulation - NRR) as input along with the GL 2004-02

responses to support closure of GL 2004-02 and GSI-191, Assessment of Debris

Accumulation on Pressurized-Water Reactor (PWR) Sump Performance." The NRC will

notify each licensee by letter of the results of the overall assessment as to whether

GSI-191 and GL 2004-02 have been satisfactorily addressed at that licensees plant(s).

Completion of TI-2515/166 does not necessarily indicate that a licensee has finished all

testing and analyses needed to demonstrate the adequacy of their modifications and

procedure changes. Licensees may also have obtained approval of plant-specific

extensions that allow for later implementation of plant modifications. Licensees will

confirm completion of all corrective actions to the NRC. The NRC will track all such yet-

50 Enclosure

to-be-performed items identified in the TI-2515/166 inspection reports to completion and

may choose to inspect implementation of some or all of them.

.6 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

Exit Meeting Summary

On July 10, 2008, the inspectors presented the inspection results to Mr. Dave Hoots,

and other members of the licensee staff. The licensee acknowledged the issues

presented. The inspectors confirmed that none of the potential report input discussed

was considered proprietary.

Interim Exit Meetings

Interim exits were conducted for:

on April 3, 2008. The inspectors returned proprietary information reviewed

during the inspection prior to leaving the site and the licensee confirmed that

none of the potential report input discussed was considered proprietary.

acknowledged the issues presented. The inspectors confirmed that none of the

potential report input discussed was considered proprietary.

Significant Areas and ALARA Planning and Controls Inspections with

Mr. D. Hoots and other members of the licensees staff on June 20, 2008.

51 Enclosure

4OA7 Licensee-Identified Violations

The following violations of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

Cornerstone: Mitigating System

containment sump monitor be returned to operable status within 30 days.

Technical Specification 3.4.15, Condition C, requires that if Condition A was not

met, the unit must be in Mode 3 in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in Mode 5 in 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. Contrary

to these, Unit 1 was operated since 1976 with the containment sump monitor

inoperable. Alternative equipment existed to assist the operators in identifying

RCS unidentified leakage. These instruments included a containment radiation

monitor, volume control tank level indicators, post accident containment sump

level instruments, containment pressure indicators, containment temperature

indicators, and pressurizer level instruments. Based upon this, the violation was

of very low safety significance. The licensee entered this issue into the

corrective action program as IR 755837.

high radiation area to have an alarming radiation monitoring device that

continuously integrates the radiation dose rate (electronic dosimeter). Contrary

to the above, on March 29, 2008, an individual entered containment, a posted

high radiation area, without an electronic dosimeter. The inspector verified that

dose rates >1000 mR/hour were present and that there were no additional

physical controls to prevent unauthorized access to these areas. This was

identified in the licensees corrective action program as IR 756342 and corrective

actions included removing the individual from the area, reading the individuals

thermoluminescent dosimeter, and established single point accountability for

individuals controlling access to the locked high radiation area. The finding was

determined to be of very low safety significance because it was not an ALARA

planning issue, there was no overexposure nor potential for overexposure, and

the licensees ability to assess dose was not compromised. The inspectors

discussed with the licensee that this event should have been reported as a PI

occurrence for the first quarter of 2008.

the increase in risk that may result from the proposed maintenance activities

before performing maintenance. Contrary to the above, between April 5, 2008 to

April 6, 2008, the licensee failed to consider that both Unit 1 Essential Service

Water Train Cross-tie Isolation Valves, 1SX033 and 1SX034, were left opened

and unable to be closed in the main control room in their risk evaluation before

conducting the 1A EDG testing. This finding affected the mitigating capability

during an internal flooding event in the auxiliary building. The finding was

determined to be of very low safety significance for Unit 1 because the unit had

been shutdown since March 23, 2008, decay heat load was low, and the time to

boil was long. The licensee entered this issue into their corrective action

program as IR 759945.

52 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Hoots, Site Vice President

B. Adams, Plant Manager

A. Daniels, NOS Manager

A. Giancatarino, Performance Improvement Director

C. Gayheart, WC Manager

S. Greenlee, Engineering Director

B. Kouba, Operations Support Manager

D. Thompson, Radiation Protection Manager

W. Grundmann, Regulatory Assurance Manager

B. Spahr, Maintenance Director

R. Zuffa, IEMA

Nuclear Regulatory Commission

R. Skokowski, Chief, Branch 3, Division of Reactor Projects

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000454/2008-003-01 NCV Fire Suppression Sprinkler Obstruction in the Diesel Oil

Storage Tank Room

05000454/2008-003-02 NCV Failure to Correctly Evaluate and Disposition of a Weld

Indication

05000454/2008-003-03 NCV Failure to Perform Evaluation of a Leaking Bolted

Connection

05000454, 455/2008-003-04 NCV Failure to Correctly Tighten Fittings Leads to Failure to

Start During a Surveillance of the 0B SX Makeup Pump

05000455/2008-003-05 AV Failure to Perform an Updated Risk Evaluation Prior to

Surveillance Testing of the Unit 1 Train A Diesel

Generator Based on Existing Plant Conditions.

05000454, 455/2008-003-06 URI Unit 1 and Unit 2 Auxiliary Feedwater Tunnel Hatch

Margin to Safety

05000454, 455/2008-003-07 OTHR Design Basis Re-Analysis of the Ultimate Heat Sink

1 Attachment

Closed

05000454/2008-003-01 NCV Fire Suppression Sprinkler Obstruction in the Diesel Oil

Storage Tank Room

05000454/2008-003-02 NCV Failure to Correctly Evaluate and Disposition of a Weld

Indication

05000454/2008-003-03 NCV Failure to Perform Evaluation of a Leaking Bolted

Connection

05000454, 455/2008-003-04 NCV Failure to Correctly Tighten Fittings Leads to Failure to

Start During a Surveillance of the 0B SX Makeup Pump

05000454/2008-001-00 LER Technical Specification Non-Compliance of

Containment Sump Monitor Due to Improper

Installation During Original Construction

05000455/2008-001-00 LER Unit 2 Emergency Diesel Generators and Auxiliary

Feedwater Pump Automatic Start Resulting from a Loss

of Offsite Power Due to a Failed Insulator Causing a

Differential Phase Overcurrent

05000455/2008002-03 URI Unit 2 Notice of Unusual Event due to Loss of Both

System Auxiliary Transformers05000455/2008002-04 URI Unit 1 Train B Auxiliary Feedwater Pump Diesel Fire

and Shutdown During Surveillance

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety, but rather, that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

Section 1R01: Adverse Weather Protection

Byron Condition Reports; Open, Auxiliary Building Ventilation System

Byron Condition Reports; Open, Auxiliary Power System

Byron Condition Reports; Open, Essential Service Water System

Oil Sample Results for UAT 241-2, September 1998 - May 2008

Oil Sample Results for SAT 242-1, September 1990 - March 2008

Oil Sample Results for SAT 242-2, June 1992 - May 2008

Oil Sample Results for 1W MPT, April 1989 - June 2008

IEEE Std C57.104-1991; IEEE Guide for the Interpretation of Gases Generated in Oil-Immersed

Transformers, November 20, 1991

IR 786022; Switchyard Thermography Needed Following Adverse Weather, June 13, 2008

IR 786025; Emergency Load Reduction Requested and Started, June 13, 2008

OP-AA-108-107-1001; Station Response to Grid Capacity Conditions, Revision 2

OP-AA108-107-1002; Interface Agreement Between Exelon Energy Delivery and Exelon

Generation for Switchyard Operations, Revision 4

OP-AA-108-107; Switchyard Control, Revision 2

WC-AA-8000; Interface Procedure Between Exelon Energy Delivery (Comed/Peco) and Exelon

Generation (Nuclear/Power) for Construction and Maintenance Activities, Revision 2

WC-AA-8003; Interface Procedure Between Exelon Generation (Nuclear/Power) for Design

Engineering and Transmission Planning Activities, Revision 1

Section 1R04: Equipment Alignment

IR 741835; Start/Stop OB VC from 1PL05JA not performed as scheduled; February 27, 2008

IR 666981; 1A DG Common Mode Failure Evaluation; March 21, 2008

IR 591516; 1A DG Tripped on High JW Temperature During Cooldown; February 14, 2007

IR 759737; 1A DG Failed 1BOSR 8.1.17-1 Due to Low Voltage; April 05, 2008

IR 747616; 1A DG Walkdown Results for NER NC-08-010; March 10, 2008

IR 733706; Auxiliary Electric Room Return Damper Failed Closed; February 08, 2008

IR 585935; OB VC M/U Fan Tripped During a Start for PMT; March 02, 2007

IR 461596; OA VC Train Inoperability - 0VC032Y Failure; March 02, 2006

IR 461319; 0VC032Y Fails, Retested w/o Determining Cause; March 02, 2006

IR 461245; 0VC032Y Will Not Close on M/U Signal; March 02, 2006

BOP VC-M1; Control Room Heating and Ventilation (HVAC) System Valve Lineup; Revision 5

BOP VC-E1; Control Room Ventilation Electrical Lineup; Revision 4

BOP VC-1; Startup of Control Room HVAC; Revision 5

BOP VC-17; Swapping Control Room Chiller and HVAC Trains; Revision 6

BOP DG M1A; Train A Diesel Generator System Valve Lineup; Revision 11

BOP DG-E1A; Diesel Generator Train A; Revision 2

BOP FC-E1; Fuel Pool Cooling System Electrical Lineup; Revision 2

BOP FC-T3; Spent Fuel Pool Skimmer One-Line Diagram; Revision 0

BOP FC-M1; Fuel Pool Cooling and Cleanup System Valve Lineup; Revision 17

3 Attachment

BOP RH-M2B; Train B Residual Heat Removal System Valve Lineup, Revision 7

BOP RH-E2B; Unit 2 Residual Heat Removal System, Train B Electrical Lineup, Revision 2

BOP SI-E1B; Unit 1 Safety Injection System Train B Electrical Lineup, Revision 3

BOP SI-E1; Unit 1 Safety Injection System Electrical Lineup, Revision 7

BOP SI-M1B; Train B Safety Injection System Valve Lineup, Revision 3

BOP SI-E1C; Unit 1 Safety Injection System Electrical Lineup, Revision 4

BOP RH-E2A; Unit 2 Residual Heat Removal System Electrical Lineup, Revision 3

BOP RH-M2A; Train A Residual Heat Removal System Valve Lineup, Revision 6

BOP RH-E2; Unit 2 Residual Heat Removal System Electrical Lineup, Revision 0

WR 231867; 1A DG Tripped on High JW Temperature During Cooldown; February 14, 2007

WR 268493; 1A DG Failed 1BOSR 8.1.17-1 Due to Low Voltage; April 06, 2008

WR 265663; DG Walkdown Results for NER NC-08-010; March 11, 2008

WR 262636; Auxiliary Electric Room Return Damper Failed Closed; February 08, 2008

WR 202809; 0VC032Y Will Not Close on M/U Signal; March 03, 2006

Diagram of Safety Injection M-61 Sheet Number 1B, Revision AW

Diagram of Residual Heat Removal M-137, Revision BD

Corrective Action Documents as a Result of NRC Inspection

IR 761127; NRC Identified Tagging Issues - Not B1R15 Related, April 9, 2008

IR 766819; NRC Identified - 1SI8804B Frayed Sealtite, April 23, 2008

IR 766814; NRC Identified - 1SI8806 Old Grease Leaking from Actuator, April 23, 2008

IR 769637; NRC Identified Procedure Discrepancy, April 30, 2008

Section 1R05: Fire Protection

Permanent Scaffold Request B4855, April 3, 2004

Unit 1 Diesel Fuel Oil Storage Room 1A, Zone 10.2-1, January 31, 2007

Unit 1 Diesel Fuel Oil Storage Room 1B, Zone 10.1-1

Unit 2 Diesel Fuel Oil Storage Room 2A, Zone 10.2-2, January 31, 2007

Unit 2 Diesel Fuel Oil Storage Room 2B, Zone 10.1-2, January 31, 2007

Pre-Fire Plan; Fuel Handling Building, Elevation 401-0, Zone 12.1-0, January 31, 2007

Pre-Fire Plan; Fuel Handling Building, Elevation 426-0, Zone 12.1-0, January 31, 2007

Fire Protection Report; Section 18.11-0, December 1998

Fire Protection Report; Section 18.11-1, December 1998

Fire Protection Report; Section 18.11-2, December 1998

Fire Protection Report; Figure 2.3-29

Fire Protection Report; Figure 2.3-30

PMID 106774; Disassemble, Clean and Inspect, Assemble Deluge System, August 21, 2007

IR 779116; Scaffold Planks Removed, May 23, 2008

MA-AA-716-025; Scaffold Installation, Modification, and Removal Request Process, Revision 0

Drawing M-1280; Auxiliary Building Ventilation Floor Plan Elevation 373-6, Revision U

Drawing M-245; Auxiliary Building Piping Plan Elevation 383-0, Revision P

M-603 - Sheet Number 64; Viking Sprinkler System Auxiliary Building Area 1-T1 & Area 1-T2,

Basement Elevation 373-0, Revision F

2BOSR 7.5.4-2; Unit 2 Diesel Driven Auxiliary Feedwater Pump Monthly Surveillance,

Revision 15

4 Attachment

Corrective Action Documents as a Result of NRC Inspection

IR 770364; NRC Questioning FP Sprinkler Potential Spray Obstructions, April 30, 2008

IR 775188; NRC Walkdown Items, May 13, 2008

IR 776571; NRC Raised FP Questions During FHB Tour, May 16, 2008

IR 787352; River Screenhouse 0A Diesel Exhaust Piping Penetration Insulation, June 17, 2008

IR 787353; River Screenhouse 0B Diesel Exhaust Piping Penetration Insulation, June 17, 2008

IR 788076; Bird Nest in Horizontal Exhaust, June 19, 2008

Section 1R06: Flood Protection

IR 761585; Door Handwheel is Binding When Door Closes, April 10, 2008

IR 767486; Inappropriate Engineering Involvement in Flooding Risk Issue, April 25, 2008

BAR 0-38-A14; Turbine Building Fire/Oil Sump Flood Level, Revision 5

DCR # 990198; Turbine Building Water Level After Circ. Water Line Break, October, 14, 1999

0BMSRDD-1; Water-Tight Barrier Inspection (CM-6.1.1), Revision 5

WO 836114-12; Remove & Repair Water-Tight Barrier 2DSFS002

Section 1R08: ISI Activities

IR 717257; NRC IN 2007-37; Buildup of Deposits in Steam Generators, January 2, 2008

IR 668998; NRC RIS 2007-20 Primary to Secondary Leakage, September 7, 2007

AT: 00717275-02; Buildup of Deposits in Steam Generators, NRC IN 2007-37

ER-AP-335-1012; Bare Metal Visual Examination of PWR Vessel Penetration and Nozzle

Safe-Ends, Revision 3

ER-AP-335-040; Evaluation of Eddy Current Data for Steam Generator Tubing Revision 3

ER-AP-335-039; Multi-frequency Eddy Current Data Acquisition of Steam Generator Tubing,

Revision 4

ER-MW-335-1009; Site Specific Performance Demonstration Program, Revision 3

LS-AA-115; Operating Experience Procedure, Revision 11

Byron Unit 1, B1R15 Degradation Assessment and Condition Monitoring Checklist, Revision 0

EXE-UT-68; Ultrasonic Examination of Unit 1 Replacement Steam Generator Main Feedwater

Nozzle Inside Radius Section at Braidwood, Revision 2

Westinghouse Data Pkg B1R15-UT-001; Ultrasound Examination of Feedwater Nozzle Inner

Radius 1RC-01-BB, N-3-NIR, March 30, 2008

Westinghouse Data Pkg B1R15-PT-001; Penetrant Examination of 1SI03DA-2/W-09,

March 29, 2008

08-11; Evaluation of B1R14 Imbedded Ultrasonic Indication Outside Required Examination

Volume, April 1, 2008

Section 1R12: Maintenance Effectiveness (Quarterly)

LER 455-2008-001-00; Unit 2 Emergency Diesel Generators and Auxiliary Feedwater Pump

Automatic Start Resulting from a Loss of Offsite Power Due to a Failed Insulator Causing a

Differential Phase Overcurrent.

Root Cause Report; Byron Station Unit 2 Loss of Off-Site Power Event, March 25, 2008

NRC Information Notice 98-36; Inadequate or Poorly Controlled, Non-Safety-Related

Maintenance Activities Unnecessarily Challenged Safety Systems, September 18, 1998

Drawing No. 6E-2-4419; Three Line Diagram System Auxiliary Transformers 242-1 & 242-2,

Revision C

5 Attachment

Drawing No. 6E-2-4016D; Relaying & Metering Diagram Differential Relay Transfer Scheme

System Auxiliary Transformers 242-1 & 242-2, Revision D

6E-2-4016C; Relaying & Metering Diagram System Auxiliary Transformers 242-1 & 242-2,

Revision J

Calibration Data; Attachment 3 HU, HU-1, HU-4 Type Differential relay, March 26, 2008

Nuclear Accident Reporting System (NARS) Form, March 25, 2008

B1R15 Shutdown Risk, March 25, 2008

BOP AP-86; Isolating SAT 242-2 At Power, Revision 9

EC 370080 00; Engineering Evaluation of the SAT 242-1 Testing Requirements Following the

Actuation of the Differential Protection for SAT 242-2, March 27, 2008

EPRI TR-112784; Isolated Phase Bus Maintenance Guide, May 1999

Drawing No. 6E-2-4003A; Phasing Diagram Part 1, Revision B

Drawing No. 6E-2-4003B; Phasing Diagram Part 2, Revision C

NES-EIC-17.03; Nuclear Engineering Standards, High Potential Tests, Revision 0

Log No.08-031; Unit 2 Standing Order, June 13, 2008

IR 772956; Maintenance Rule (A)(1) Determination Required for MP2, May 7, 2008

IR 773419; Work Request to Install Filter Drain in Rubber Boot Seals, May 8, 2008

IR 783134; 0B SX Makeup Pump Needs Reportability Review, June 5, 2008`

Project No. BYR-92592; Failure Analysis of the Byron Auxiliary 242-2, Non-Segregated Bus

Duct, Section 15, B Phase Insulator, April 25, 2008

IR 754582; Unit 2 Loss of Off-Site Power, March 25, 2008

IR 754585; Two of Four Fans Not Running on 2B SX Pump Cubicle Cooler, March 25, 2008

IR 754602; SAT 242-2 Phase C Overcurrent, March 25, 2008

IR 755875; Maintenance Rule (A)(2) at Risk Due to Unplanned SAT Outage, March 28, 2008

IR 760354; Bolted Connection on 6.9KV Non Seg Found Loose, April 7, 2008

IR 761246; Non-Seg Bus Duct Inspection, April 9, 2008

IR 762409; Replace Rubber Expansion Boot Around Non-Seg Bus Duct, April 11, 2008

IR 762638; Megger Test UAT 141-1 4KV & 6.9KV, April 12, 2008

IR 768314; Unexpected Alarms - Unit 2 SATs, April 27, 2008

IR 768317; SAT 242-2 Phase -A Differential Overcurrent Lockout When SAT Energized,

April 27, 2008

IR 774259; SAT Isolation Procedure Differences - Plant and OLR Impacts, May 11, 2008

IR 779699; 0B SX M/U Pump Failed to Run During Low Level Start, May 27, 2008

WO 912183 01; Replace Parker Check Valve at SX M/U Pump Fuel Oil Line, April 29, 2008

MA-AA-716-011; Work Execution & Close Out, Revision 11

Corrective Action Documents as a Result of NRC Inspection

IR 770417; NRC Concern on SAT 242-2 Trip When Energized, April 28, 2008

IR 780732; NRC Requested Past Operability Evaluation - 0B SX M/U Pump, May 29, 2008

Section 1R13: Maintenance Risk Assessments and Emergent Work Evaluation

Unit 2 Risk Configurations, Week of March 31, 2008

Unit 2 Risk Configurations, Week of March 31, 2008, Revision 1

Unit 2 Risk Configurations, Week of March 31, 2008, Revision 2

Unit 2 Risk Configurations, Week of March 31, 2008, Revision 3

Unit 2 Risk Configurations, Week of April 7, 2008

Unit 2 Risk Configurations, Week of April 7, 2008, Revision 1

Unit 2 Risk Configurations, Week of May 5, 2008, Revision 1

Unit 2 Risk Configurations, Week of May 26, 2008, Revision 3

6 Attachment

Protected Equipment Log, May 7, 2008

Protected Equipment Log, May 28, 2008

IR 562336-13; License Amendment Implementation Consider License Amendment for

RPS/ESFAS Test times and Completion Times Relaxations for Operator Training,

September 1, 2007

IR 759929; Clearance Order Returned with Dead Man Switch Still Installed, April 6, 2008

IR 759945; Unplanned Unit 2 Online Risk Orange Condition, April 6, 2008

Unit 1/2 Standing Order 08-011; Technical Specification Amendment 153, February 14, 2008

WO 836114; Replace 1SX034 in B1R15, April 7, 2008

WO 836114 06; Remove/Reinstall Flood Seal 2DSFS003 to Support 1SX034 Valve

Replacement

WO 1120558 01; 1SX033 - Remove and Inspect/Rebuild Limitorque Operator and Gear,

April 9, 2008

Clearance 63416; EPN 1SX033

Clearance 57893; 1SX034 - De-Term/Re-Term Valve for Replacement

Clearance 57894; 1SX034 - Replace Valve, April 1, 2008

B1R15 OCC Turnover, April 5, 2008 - June 7, 2008

Quick Human Performance Investigation Report; Unplanned Unit 2 On-Line Risk (OLR) Orange

Condition, April 7, 2008

EST 08-0242; Abnormal Component Position 1SX033, April 5, 2008

Byrons Archival Operations Narrative Logs, March 31, 2008 to April 7, 2008

B1R15 Shutdown Risk; April 5, 2008 and April 6, 2008

BYR-1SX034; Diagnostic Test Instructions - Control Circuit Changes to Support Testing,

April 7, 2008

Draft Unplanned Unit 2 On-Line Risk (OLR) Orange Condition Root Cause Investigation Report

PBI 07-513; Plant Barrier Impairment Permit

WC-AA-101; Attachment 6 Unavailability Guidelines, Revision 14

0B0A PRI-8; Auxiliary Building Flooding Unit 0, Revision 0

1BOA PRI-7; Essential Service Water Malfunction Unit 1, Revision 104

2BOA PRI-7; Essential Service Water Malfunction Unit 2, Revision 105

BB PRA-017.91B; Byron SDP Evaluation of Failure to Conduct a Risk Evaluation Prior to

Disabling 1SX033 and 1SX034 Remote Isolation Capability, Revision 0

BOP SX-22; Essential Service Water Leak Isolation, Revision 0

BAR 0PLO1J-9B1; Essential Service Water Pump 2A Leak Detected - Pump Level High,

Revision 1

Diagram of Essential Service Water; M-42 Sheet Number 3, Revision AZ

Diagram of Essential Service Water; M-42 Sheet Number 5A &5B Revision AE

Diagram of Essential Service Water; M-42 Sheet Number 1A & 1B, Revision AN

Diagram of Essential Service Water; M-42 Sheet Number 2A & 2B Revision AW

Corrective Action Documents as a Result of NRC Inspection

IR 773344; DC Emergency Light 0LL076E is Malfunctioning, May 8, 2008

Section 1R15: Operability Evaluations

Analysis No. ATD-0111; Containment Flood Level, Revision 013D

Analysis No. BYR2000-180; Available Margin for Miscellaneous Hydrogen Producing Materials

in the Byron Unit 1 and 2 Containment Buildings, Revision 8

Calculation No. CN-LIS-00-55; LBL0CA/SBL0CA Evaluation of Revised Containment Data for

Byron/Braidwood Units 1 and 2 (CAE/CBE/CCE/ CAE), Revision 0

7 Attachment

EC 370179; Machining of Flange Surface of 1B AF Diesel Exhaust Manifold, Revision 0

EC 370163; Operations Evaluation 08-005, 1B/2B AF Diesel Insulation, Revisions 1 & 2

EC 370270; Foreign Material (Scaffold) Potentially Left in Unit 1 Containment for a Cycle,

Revision 000

EC 370369; Past Operability of the 1B AF Pump with Respect to Exhaust Manifold Fire,

Revision 0

EC 333036; Install Scaffold Saddles on 401 IMB Between SG AD and BC. This EC

Incorporates All Permanent Scaffold Storage Requirements for Containment, Revision 000

EC No. 362730; Foreign Material Not Recovered From Unit 1 ECCS Sump Trash Rack Area,

Revision 000

EC 363000; Evaluation for Foreign Material Left in Unit 1 Containment, Revision 000

EC 366163 01; OP Evaluation 07-005 Unventable Gas Voids in Containment Recirculation

Pump Piping, February 12, 2008

EC Request 147981; DG: Sealant for Exterior of Intake to Head Flange Interface, June 24, 1999

EC Request 072499; DG Intake Manifolds Leaking Air Around Flange, January 12, 1996

EC Request 358726; Evaluate Permanent/Temporary Repair for Oil Leakage Coming from what

Appears to be the CAM Housing Gasket Area, February 26, 2003

IR 493593; 2A DG Minor Air Leak on L8 Cylinder Head Intake Flange, May 25, 2006

IR 727020; Unexpected 2C SI Accumulator Level Drop, January 25, 2008

IR 729265; Gas Void UT Exam Results for Unit 2 SI, January 30, 2008

IR 753008; Cause of 1B AF Pump Fire Conditions May Exist on 2B AF Pump, March 21, 2008

IR 753012; During 1B AFW Pump Test an Oil Leak Developed with Flames, March 21, 2008

IR 753383; Starter Motor Shorted during Pump Start, March 23, 2008

Quick Human Performance Investigation Report on IR 753383

IR 755140; 1RH619 Failed Open, March 26, 2008

IR 759028; As Found Results of 1B AF Exhaust Manifolds Out of Spec, April 3, 2008

IR 760408; Insulation in Poor Condition, April 8, 2008

IR 761633; VTIP Information Conflicts with As Built, April 10, 2008

IR 763216; AF System to Remain Yellow in Ship, April 14, 2008

IR 771208; ECs for Equipment Stored in Containment Due to GSI-191, May 2, 2008

IR 775293; Need a WR to Resolve Potential Failure of RH Valves, May 14, 2008

IR 776353; Void Found at 2SI8811A After 2A RH Pump Window, May 16, 2008

IR 756739; Scaffold Left IMB Since B1R14, March 30, 2008

IR 765637; Fires Involving Diesel Engine Exhaust Manifolds, April 21, 2008

IR 779122; Gas Void Discovered After Fill & Vent of 1A RH Suction, May 23, 2008

IR 783173; Delamination Issue with Valve Cover Gasket for AF Diesel, June 5, 2008

WO Task; 934752 01; MM-2DG01KA-24 Month Mechanical Inspection, April 24, 2008

WC-BY-106; Condition Based Monitoring Program, Appendix A, Revision 1

BYR-92045; Evaluation of Exhaust Manifold Gaskets from the Byron 1B AF Pump Diesel

Engine, April 7, 2008

BYR-92276; Laboratory Examination of Insulation from the Byron Unit 1 1B AF Pump Diesel

SW Exhaust Manifold, April 4, 2008

IR 776484; Additional Voiding at 2SI8811A After 2A RH Pump Window, May 16, 2008

IR 783051; Check Rocker Covers for Flatness at Next Work Window, April 9, 2008

IR 783052; Check Rocker Covers for Flatness at Next Work Window, April 9, 2008

Report Number 2008-418; Ultrasonic Examination for 2SI06BB-24, May 16, 2008

Report Number 2008-419; Ultrasonic Examination for 2SI06BB-24, May 16, 2008

Report Number 2008-432; Ultrasonic Examination for 1A RH Suction Line, May 23, 2008

Report Number 2008-434; Ultrasonic Examination for 1A RH Suction Line, May 24, 2008

Report Number 2008-436; Ultrasonic Examination for 1A RH Suction Line, May 27, 2008

8 Attachment

NRC Generic Letter 2008-01; Managing Gas Accumulation in Emergency Core Cooling, Decay

Heat Removal, and Containment Spray Systems, January 11, 2008

Corrective Action Documents as a Result of NRC Inspection

IR 786168; Limited Operations Involvement in Past Operability Calls, June 13, 2008

IR 778656; NRC Questions on Positioners for RH Valves, May 22, 2008

Section 1R19: Post Maintenance Testing

WO 0112/189; PMT ESF Relay K602B Start for OE Charcoal Booster Fan, May 7, 2008

WO 920901 02; OPS PMT Functional 0VA052Y, May 7, 2008

WO 792520 01; Replace Aux FW Pump 1B Eng Fuel Shutoff Solenoid

WO 868574 02; OPS PMT Stroke Damper Run 0VA03CE, May 7, 2008

WO 884583-01; Calibration of Component Cooling Pump OC Suction Pressure Indicator,

0PI-069, November 16, 2006

WO 884584-01; Calibration of Component Cooling Pump Discharge Pressure Indicator,

1PI-0673, December 6, 2006

WO 961008 01; Auxiliary Feedwater Diesel Prime Mover Inspection, April 10, 2008

WO 961101 02; Start/Stop 1B AF PP Locally From MCR

WO 961715 03; Verify 1B AF Diesel Starts and Does Not Trip

WO 962127 01; 1B AF Pump Emergency Actuation Signal Verification Test, April 12, 2008

WO 997550 03; OPS PMT - Startup Unit 1 AF Diesel, Verify No Unexpected Alarms

WO 1037480-04; Unit 0 Back Flow Test for Component Cooling Discharge Check Valve

0CC9464, May 19, 2008

WO 1139777 01; 1B PP Shaft Collar Shifted BY - 3/4 inch, June 04, 2008

WO Task 01139777 02; OPS PMT Verify Inboard/Outboard Shaft Bushings in Proper

Orientation, June 4, 2008

WO 525537-08; Unit 0 Comprehensive In-service Testing (IST) Surveillance Requirements for

Component Cooling Pump 0CC01P, May 19, 2008

WO Task 961104 02; Verify the AF Diesel Starts from Both Battery Banks, April 12, 2008

Schematic Diagram; Auxiliary Building Non-Accessible Area Exhaust Filter Plenum C Charcoal

Booster Fans 0B & 0E Isolation & Control Dampers - 0VA086yA, 0VA067YA&B, 0VA023YA&B,

Revision L

IR 781947; Request Calibration Check on CC Pump Discharge Gauge for ASME Test,

June 2, 2008

IR 781948; Request Calibration Check on CC Pump Suction Press Gauge for ASME Test,

June 2, 2008

IR 782306; 1B CV PP Shaft Collar Shifted BY - 3/4 inch, June 03, 2008

EC 357768; Replace Pressure Gauges to Improve Accuracy for IST Testing, Revision 001,

January 26, 2007

Service Request 13127; Various CC Instrument Loops Calibration Frequency Change,

September 15, 2002

Corrective Action Documents as a Result of NRC Inspection

IR 782298; NRC Question Concerning Instrument Calibrations, June 3, 2008

9 Attachment

Section 1R20: Refueling and Outage Activities

WO 885776 01; IM Calibrate and Install New Press Indicator 1PI-AF058, Per EC 357770

WO 885779 01; IM Calibrate and Install New Press Indicator 1PI-AF151, Per EC 357770

WO 01001347 01; 1AF01PB Comprehensive IST Requirements for the Diesel Driven AF PMP,

April 29, 2008

WO 972033; Unit 1 PRT Slow Fill Rate - Inspect 1PW005 During B1R15, March 14, 2008

IR 753603; RY Surge Line Insulation Damaged, March 24, 2008

IR 768943; Adverse Atmosphere for 1B AF PP Rounds, April 29, 2008

IR 768955; Room Uninhabitable During 1B AF PP Full Flow Test, April 29, 2008

IR 762543l 1B AF PP Exhaust Leaks and Cancer, April 12, 2008

IR 768979; 1B AF Diesel Gear Box and Right Angle Gear Drive VIBS High, April 29, 2008

Selected B1R15 Shutdown Risk, April 1 - April 14, 2008

Selected B1R15 OCC Turnover, April 1 - April 14, 2008

Selected B1R15 Outage News, April 1 - April 14, 2008

Corrective Action Documents as a Result of NRC Inspection

IR 00758286; NRC Identified Concern Over Timeliness of repair of UFSAR Function,

April 2, 2008

Section 1R22: Surveillance Testing

WO 979055 01; Unit 2 Fire Hazards Panel Instrumentation 18 Month Surveillance,

May 17, 2008

WO 1120857 01; 2BOSR 7.5.4-2, 2B AF PP Run

1BOSR 3.g.3-1; Unit 1 Reheat and Intercept Valve Quarterly Surveillance, Revision 13

2BOSR 6.6.2-1; Unit 2 Reactor Containment Fan Cooler Monthly Surveillance, Revision 19

1BVSR 8.4.2-2; Unit 1 BUS 112 125V Battery Charger Operability, Revision 3

IR 742714; Implement RCS Leak Rate Recommendations in OG-07-387, February 29, 2008

IR 647077; RCS Leak-rate Program (Applies to Both Units), July 3, 2007

IR 707153; Unit 2 RCS Leak-rate Procedures, December 4, 2007

IR 709143; 1/2 BOSR 4.13.1-2 Utilize Same RCS Volume Number, December 8, 2007

NFS Memo PSA: 97-005; Braidwood Unit 1/2 RCS Leakage Rate, February 26, 1997

Reactor Coolant System Leak-rate Package Software Design Description; PCS Product

Number GN05038, Revision 0.1 October 5, 1988, date signed January 18, 1989

2BOSR 4.13.1-2; Reactor Coolant System Water Inventory Balance Daily Surveillance Manual

Calculation

2BOSR 4.13.1-1; Unit 2 Reactor Coolant System Water Inventory Balance Daily Surveillance

Computer Calculation, Revision 16

Document Identification Number SSS-89-002, Revision 1.1; Functional Requirement

Specification for the Reactor Coolant System Leakage Rate Program, March 1, 1989

Document Identification Number PSA-B-97-02; Braidwood Unit 1/2 RCS Leakage Rate Statistical

Analysis, February 26, 1997

Document Identification Number SSS-88-001; Functional Requirement Specification for the

Reactor Coolant System Leakage Rate Program, Revision 1

10 Attachment

Corrective Action Documents as a Result of NRC Inspection

IR 619429; Questions on RCS Leak-rate Methods, April 19, 2007

IR 753983; NRC Identified Potential Discrepancies with RCS Leak-rate Calculations,

March 24, 2008

IR 777782; NRC Identified Error in Completed 2BOSR XFP-R1 Surveillance, May 20, 2008

Corrective Action Documents as a Result of NRC Inspection

IR 767699; NRC Resident Reported Significant Oil Buildup on 2B CV Pump, April 25, 2008

IR 770647; Air Intake Leak on 1B DG, April 30, 2008

IR 770651; Diesel Fuel Leak on 1B DG, April 30, 2008

IR 779045; NRC Identified Corrosion on Alternate Train SX Blow-down Vent Piping,

May 23 2008

Corrective Action Documents as a Result of NRC Inspection

IR 757172; Lessons Learned on Report Outs on NRC IRC Status Calls, March 31, 2008

Section 1E92: EP

Byron Off-Site Siren Test Plan; April 2008

IR 00491028; ANS Servicing Byron EPZ Reached 25% Unavailability; May 17, 2006

IR 00510166; One Off-Site Alert and Notification System Siren Lost Power; July 17, 2006

IR 00510239; Warning Siren Failure During Thunderstorm; July 17, 2006

IR 00510575; 25% Inoperability of the Byron Station ANS Due to Loss of AC; July 18, 2006

IR 00707169; Winter Storm Causing Siren Power Outage; December 4, 2007

IR 00490356; Loss of 28 EPZ Sirens Due to Offsite Power Issue; May 16, 2006

Byron Plant Warning System Maintenance and Operational Report; March 13 - June 7, 2007

Byron Plant Warning System Maintenance and Operational Report; February 16 - May 19, 2006

Annual Siren Daily Operability Reports; 2006 - 2008

Siren Monthly Operability Report - Byron Monthly Siren Availability Report (Telemetry);

2006 - 2008

An Off-Site Emergency Plan Prompt Alert and Notification System Addendum for the Byron

Nuclear Power Station, submitted by: Illinois Emergency Management Agency and

Commonwealth Edison Company; October 1992

Exelon Semi-Annual Siren Report; January 1 - June 30, 2007

Exelon Semi-Annual Siren Report; July 1 - Dec. 31, 2007

Section 1EP3: ERO Augmentation Testing

EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan, Section B;

Emergency Response Training; Revision 19

EP-AA-1000; Exelon Nuclear Standardized Radiological Emergency Plan, Part II, Section B,

Table B-1; Revision 19

EP-AA-122-1001; Drill & Exercise Scheduling, Development and Conduct; Revision 9

EP-AA-112-100-F-01; Shift Emergency Director Checklist; Revision H

EP-AA-112-100-F-06; Midwest ERO Notification or Augmentation; Revision G

IR 00474834; On-Call Emergency Response Organization Failed to Respond to Call In Drill,

April 3, 2006

IR 00476632; EP-AA-1221001 T& RM Non-Compliance (Drive in Drills), April 9, 2006

11 Attachment

IR 00681706; OSC RP Group Lead/Asst. OSC Director Not Available for Duty, October 8, 2007

IR 00682166; Degraded Performance in Alpha Pager Response, October 9, 2007

Unannounced, Off-Hour Call-in Drill Results and Records, February 2006 - January 2008

Memorandum; Exelon Nuclear Byron Station EP-ERO Expectations, January 25, 2008

Memorandum; Emergency Response Organization Roster, April 2008

Section 1EP5: Correction of EP Weaknesses and Deficiencies

EP-AA-1002; Emergency Action level HA7, Revision 21 and 22

EP-AA-120F-05; Event Review Checklist, Revision A

RP-AA-440; Respiratory Protection Program, Revision 8

LS-AA-126-1005; 2008 NRC EP Baseline Program Inspection Readiness Assessment,

Revision 3

IR 00559030; NSRB Comments of Emergency Preparedness, November 16, 2006

IR 00624526; NOS ID: RP Issue with EP Equipment, May 2, 2007

IR 00625086; Meteorology Instrument Accuracy Does Not Meet Requirements, May 3, 2007

IR 00621691; NOS ID Inconsistent Requirements Between EOF Director Checklist and E-Plan,

April 25, 2007

IR 00698053; EP Baseline Inspection Check-In, November 12, 2007

IR 00639899; Byron EP Pre-Exercise Low Level OSC Items, June 13, 2007

IR 00640485; NOS ID Review EP Pre-Exercise Conclusion for Potential DEP Failure,

June 14, 2007

IR 00636115; DEP Hit and Failed Objective EP Pre-Exercise, June 1, 2007

IR 00651666; Byron 07 EP Exercise TSC Failed Demonstration Criteria, July 19, 2007

IR 00638881; Byron Pre-Exercise TSC Failed Demonstration Criteria, June 10, 2007

IR 00638883; Byron Pre-Exercise OSC Failed Demonstration Criteria, June 10, 2007

IR 00708316; ERO Response to ALERT on 11/27/2007, December 6, 2007

IR 00709554; Training - LORT Cycle 07-06 EP Roll Up, December 10, 2007

IR 00709563; Training - Week 4 Annual and Comprehensive Written, December 10, 2007

IR 00708906; NRC Follow-up Question on November 27, 2007, Alert, December 7, 2007

IR 00708316; Emergency Response Organization Response to Alert, November 27, 2007

IR 00704697; Emergency Operations Center Communicator Failed to Meet EP Expectations,

November 28, 2007

IR 00703919; Apparent Cause Report, Alert (HA7) Declared Due to Low Oxygen Levels in 1B

Containment Spray Pump Room, November 27, 2007

Byron 2007 NARS/PARS/EALs Performance Indicator Drills, November 13 - December 4, 2007

Byron 2007 EP/Security Integrated Drill Findings and Observation Report, November 15, 2007

Byron Nuclear Power Station In-Plant Health Physics Drill Report First Half 2007, June 25, 2007

Byron 2007 NRC Graded Exercise Evaluation Report, June 20, 2007

Byron Station Alert Event Report for 11/27/2007, December 26, 2007

NOSA-BYR-06-03, IR 437588; Byron Station Emergency Preparedness Audit for 4/10 through

4/14/2006, April 18, 2006

NOSA-BYR-07-04, IR 571163; Emergency Preparedness Audit for 4/30 through 5/4/2007,

May 9, 2007

NOSA-NCS-06-03, IR 469749; Emergency Preparedness Audit Report

NOSA-NCS-07-04, IR 574311; Emergency Preparedness Audit Report, Cantera and Kennett

Square

NO-AA-1024, Attachment 1; NOS Objective Evidence Report, April 28, 2006 & May 18, 2007

Byron EP Information Newsletter #08-01, January 2008

Byron EP Information Newsletter #08-03, March 2008

12 Attachment

Memo to M. Snow from D. Drawbaugh; Byron Station November 27, 2007, Alert Event Report,

December 26, 2007

Letter to D. Smith from W. King; FEMA Conditional Approval of IEMA 11/14/2007 ANS

Proposal, March 19, 2008

Nuclear Accident Report System Form, November 27, 2007

Section 40A1: Performance Indicator Verification

EP-AA-125-1001; EP Performance Indicator Guidance, Revision 5

EP-AA-125-1002; ERO Performance - Performance Indicator Guidance, Revision 4

EP-AA-125-1003; ERO Readiness - Performance Indicator Guidance, Revision 6

EP-AA-125-1004; Emergency Response Facilities and Equipment Performance Indicator

Guidance, Revision 4

IR 00648201; Training - LORT WD.3E OBE Failure Rate PI in Variance, July 9, 2007

NRC Emergency Response Organization Drill Participation Records, April - December, 2007

LS-AA-2110; Monthly Data Elements for NRC Drill/Exercise Participation, April -

December, 2007

LS-AA-2120; Monthly Data Elements for NRC Drill/Exercise Performance,

April-December, 2007

Section 40A2: Identification and Resolution of Problems

OP-AA-101-113-1001; Station event Free Clock Program, Revision 4

Section 40A3: Event Followup

0B0A ENV-4; Earthquake Unit 0, Revision 102

1B0A-ENV-4; Earthquake Unit 1, Revision 100

2B0A-ENV-4; Earthquake Unit 2, Revision 100

EC 370132 00; Provide Patches for Holes around the Tube Track in RF Sump (1RF02T) Cover

Condition Report 755837; RF Sump Not Constructed in Accordance with Design

LER 454-2008-001-00; Technical Specification Non-Compliance of Containment Sump Monitor

Due to Improper Installation During Original Construction, June 13, 2008

Section 4OA5: Other Activities

EPRI 1010087; Materials Reliability Program: Primary System Piping Butt Weld Inspection and

Evaluation Guideline (MRP-139), July 14, 2005

Byron Letter 2006-0050; Third 10-Year Inservice Inspection Interval, Relief Request 13R-08,

Structural Weld Overlays on Pressurizer Spray, Relief, Safety and Surge Nozzle Safe-Ends and

Associated Alternative Repair Techniques, April 28, 2006

EXE-PDI-108; Ultrasonic Examination of Weld Overlaid Similar and Dissimilar Welds in

Accordance with PDI-UT-8, Revision 0

EXE ISI-11; Liquid Penetrant Examination, Revision 2

PDI-UT-8; Generic Procedure for the Ultrasonic Examination of Weld Overlaid Similar and

Dissimilar Metal Welds, Revision F

PCI WPS 3-8/52-TB MC-GTAW-N638; Ambient Temperature Temper Bead Structural Overlay

Without Elevated Preheat, Revision 5 & 7

PCI WPS 8 MC-GTAW; Grove, Fillet, no PWHT, with Supplement dated 2/21/2007, Revision 10

Westdyne Data Pkg, B1R14-PN-01-SWI; Surge Line Nozzle, September 23, 2006

Westdyne Evaluation B1R14-PN-01-SW1-EVAL-01; Surge Line Nozzle, September 23, 2006

13 Attachment

Westdyne Data Pkg B2R13-PN-03-SW3; PORV Nozzle, April 16, 2007

Westdyne Evaluation B2R13-PN-03-SW3; PORV Nozzle, April 17, 2007

Westdyne Data Pkg B1R14-PN-01-SW1; Surge Line Nozzle, September 23, 2006

Westdyne Evaluation B1R14-PN-01-SW1-Eval-01; Surge Line Nozzle, September 23, 2006

PN-03-F3; Weld Overlay Process Traveler with Sacrificial Layer - Pressurizer Unit 2 PORV

Nozzle, March 27, 2007

PN-01-F1; Weld Overlay Process Traveler - Pressurizer 1RY01 Surge Nozzle,

September 8, 2006

CN-PAFM-06-139; Byron Units 1 and 2 Pressurizer Surge, Spray and Safety and Relief Nozzles

Maximum Allowable Flaw Sizes in Weld Overlay, Revision 5

3SA-096-016; CCI Structural Analysis of Strainer and Support Structure, Revision 3

Service Request 174053; Latent Debris Walkdown - Unit 2, September 27, 2008

Service Request 174052; Latent Debris Walkdown - Unit 1, September 27, 2008

EC 364979; Evaluate SI Throttle Valve Test Results from Wyle Labs to Document Acceptability

of New Trim Design, April 23, 2007

EC 360120; Replace SI Throttle Valve Trim, Bonnet, Stem and Operators, and Remove

Downstream Orifices Plates to Support GSI-191 - Unit 2, Revision 0

EC 359455; Downstream Activities Effects Related to GSI-191 - Unit 1, Revision 0

S040-BY-5010; GSI-191 Latent Debris Collection Unit 1, April 4, 2005

S040-BY-5030; GSI-191 Latent Debris Collection Unit 1, November 15, 2005

S040-BYR-5032; GSI-191 Debris Generation Walkdown - Unit 2, May 8, 2006

S040-BYR-5011; GSI-191 Debris Generation Walkdown - Unit 1, April 8, 2005

BYR05-041; GSI-191 Post-LOCA Debris Generation, Revision 1

BYR05-042; Post-LOCA Debris Transport Evaluation for Resolution of GSI-191, Revision 1

BYR05-061; GSI-191 Evaluation of Long Term Downstream Effects, Revision 2

BYR06-025; Design Loads and Sizing Limitations for the ECCS Containment Sump Trash Rack,

Revision 0

OP-AA-116-101; Equipment Labeling, Revision 1

CC-AA-102; Design Input and Configuration Change Impact Screening, Revision 14

1/2 BOSR Z.5.1.1-1; Containment Loose Debris Inspection, Revision 8

CC-AA-205; Control of Undocumented/Unqualified Coatings Inside the Containment, Revision 4

1/2 BVSR XII-11; Containment Building Interior Surface Coating Inspection, Revision 4

DIT-BYR-06-007; Debris Concentration Measurements Results, January 27, 2006

IR 777152; Actions Related to Latent Debris Surveillance (G2004-02), May 19, 2008

14 Attachment

LIST OF ACRONYMS USED

AC Alternating Current

AFW Auxiliary Feed Water

ALARA As-Low-As-Is-Reasonably-Achievable

ANS Alert and Notification System

ASME American Society of Mechanical Engineers

BACC Boric Acid Corrosion Control

CAP Corrective Action Program

CFR Code of Federal Regulations

CS Containment Spray

CSS Containment Spray System

CV Charging Pump

DMBW Dissimilar Metal Butt Weld

EC Engineering Change

ECCS Emergency Core Cooling System

EDG Emergency Diesel Generator

EP Emergency Preparedness

ERO Emergency Response Organization

EPRI Electric Power Research Institute

ET Eddy Current

FPP Fire Protection Program

GL Generic Letter

GSI Generic Safety Issue

ICDF Incremental Core Damage Frequency

ICDP Incremental Core Damage Probability

ICDPD Incremental Core Damage Probability Deficit

IMC Inspection Manual Chapter

IP Inspection Procedure

IR Issue Report

ISI Inservice Inspection

LER Licensee Event Report

LOCA Loss of Coolant Accident

MRP Material Reliability Program

NCV Non-Cited Violation

NDE Non-destructive Examination

NEI Nuclear Energy Institute

NFPA National Fire Protection Association

NRC U.S. Nuclear Regulatory Commission

OL Operating License

OOS Out of Service

PDI Performance Demonstration Initiative

PI Performance Indicator

PORV Power Operated Relief Valve

PRA Probabilistic Risk Assessment

RCS Reactor Coolant System

RH Residual Heat Removal

RMA Risk Management Action

RP Radiation Protection

SAT System Auxiliary Transformer

SDP Significance Determination Process

15 Attachment

SG Steam Generator

SI Safety Injection

SPAR Simplified Plant Analysis Risk Model

SX Essential Service Water System

TI Temporary Instruction

TLD Thermoluminescent Dosimeters

TRM Technical Requirements Manual

TS Technical Specification

TSO Transmission System Operator

UFSAR Updated Final Safety Analysis Report

UHS Ultimate Heat Sink

URI Unresolved Item

UT Ultrasonic Testing

WO Work Order 16 Attachment