IR 05000454/2021002
| ML21215A078 | |
| Person / Time | |
|---|---|
| Site: | Byron |
| Issue date: | 08/04/2021 |
| From: | Hironori Peterson Region 3 Branch 3 |
| To: | Rhoades D Exelon Generation Co |
| References | |
| IR 2021001 | |
| Download: ML21215A078 (18) | |
Text
SUBJECT:
BYRON STATION - INTEGRATED INSPECTION REPORT 05000454/2021002; 05000455/2021002; AND 07200068/2021001
Dear Mr. Rhoades:
On June 30, 2021, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Byron Station. On July 12, 2021, the NRC inspectors discussed the results of this inspection with Mr. J. Kowalski, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely, Hironori Peterson, Chief Branch 3 Division of Reactor Projects Docket Nos. 05000454; 05000455; 07200068 License Nos. NPF-37 and NPF-66
Enclosure:
As stated
Inspection Report
Docket Numbers:
05000454; 05000455; 007200068
License Numbers:
Report Numbers:
05000454/2021002; 05000455/2021002; 07200068/2021001
Enterprise Identifier:
I-2021-002-0068; 1-2021-001-0160
Licensee:
Exelon Generation Company, LLC
Facility:
Byron Station
Location:
Byron, IL
Inspection Dates:
April 01, 2021 to June 30, 2021
Inspectors:
D. Betancourt-Roldan, Senior Resident Inspector
J. Dalzell, Project Engineer
C. Thompson, Illinois Emergency Management Agency
J. Weigandt, Resident Inspector
Approved By:
Hironori Peterson, Chief
Branch 3
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Byron Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 1 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities or small load changes requested by the transmission dispatcher, the unit remained at or near full power for the entire inspection period.
Unit 2 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities or small load changes requested by the transmission dispatcher, the unit remained at or near full power for the entire inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the coronavirus (COVID-19), resident and regional inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week, increasing the amount of time on site as local COVID-19 conditions permitted.
As part of their onsite activities, resident inspectors conducted plant status activities as described in IMC 2515, Appendix D; observed risk significant activities; and completed on site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or a portion of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection
Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated summer readiness of offsite and alternate alternating current (AC) power systems April 19 through June 1, 2021.
71111.04 - Equipment Alignment
Partial Walkdown Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 1 'A' Auxiliary Feedwater (AF) during 'B' battery issue on April 24, 2021 (2)2A Emergency Diesel Generator (EDG) during Station Auxiliary Transformer (SAT)window on May 5, 2021
- (3) Fire Protection System Train A while the 'B' Fire Pump was out of service on May 15, 2021
- (4) Unit 1 Instrument Power and 125 Volt Direct Current (DC) during 1B Diesel Generator (DG) outage on June 16, 2021
- (5) Diesel fuel oil during 2B EDG monthly test and after fuel oil transfer tests on June 27, 2021
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the Unit 2 AF begun during the first quarter 2021 inspection period and completed on May 14, 2021.
71111.05 - Fire Protection
Fire Area Walkdown and Inspection Sample (IP Section 03.01) (5 Samples)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Fire Zone (FZ) 8.31 Northeast: Turbine Building 401' Elevation on April 7, 2021
- (2) FZs 3.2A/B/C/D/E-1 PFPs: Unit 1 Lower Cable Spreading Rooms on April 30, 2021
- (3) FZs 3.2A/B/C/D/E-2 PFPs: Unit 2 Lower Cable Spreading Rooms on April 30, 2021
- (4) FZ 11.2-0 North/11.3-0 South: Auxiliary Building General Area 364' Elevation on May 3, 2021
- (5) FZs 18.12-0 & 18.13-0: Circulating Water Pumphouse on May 15, 2021
71111.06 - Flood Protection Measures
Inspection Activities - Internal Flooding (IP Section 03.01) (1 Sample)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Turbine Building basement on April 16, 2021
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)
The inspectors observed and evaluated the following licensed operator activities in the control room:
- (1) Various activities involving on-watch operations crews. These activities included, but were not limited to:
Unit 1 downpower 100MWe for Advanced Nuclear Dispatch on April 9, 2021
Dilution on Unit 1 on June 1, 2021
71111.12 - Maintenance Effectiveness
Maintenance Effectiveness (IP Section 03.01) (2 Samples)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) Maintenance effectiveness and performance review of the pressurizer heaters on April 21, 2021
- (2) Maintenance effectiveness and performance review of the Technical Support Center (TSC) ventilation on June 14, 2021
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Unit 2 'B' Component Cooling Pump as set forth in Work Order (WO) 5006411 on April 17, 2021
- (2) Evaluation of the scheduled Risk Informed Completion Time (RICT) window SAT outage on May 3, 2021 (3)2A EDG work window as set forth in WO 5063615 and Engineering Change (EC)
===632199 on June 2, 2021
- (4) 1B EDG work window on June 14, 2021
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01)===
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) NRC Information Notice 2017-06 evaluation as documented in Action Request (AR) 04415085 on April 9, 2021
- (2) Evaluation of the operability of a lube oil leak on the 1A AF pump as documented in AR 04417861 on April 20, 2021
- (3) Evaluation of the operability of 1HK-AF031A flow control POT needs adjustment as documented in AR 4418342 on April 22, 2021
- (4) Evaluation of the operability of the 1A EDG manually secured due to exhaust leak as documented in AR 04419745 on April 28, 2021
- (5) Evaluation of the operability of 1SX68AB-1.5 pinhole leak (OP 2021-001) on May 3, 2021
71111.19 - Post-Maintenance Testing
Post-Maintenance Test Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
(1)2BOSR 8.6.1-2, 2BHSSR 8.4.2-2, and MA-BY-223.053: DC 211 Charger and Battery return to service after inspection as set forth in WOs 5136320, 4966367, and
===4945435 respectively, on April 10, 2021
- (2) Unit 2 'B' CC Pump as set forth in WOs 5006411 and 5110415 on April 17, 2021 (3)1BOSR 5.5.8.SI.5-2A 1B Safety Injection (SI) Inservice Test (IST) Group A Pump Test as set forth in WO 5126604 on May 13, 2021
71111.22 - Surveillance Testing
The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01)
(1)2B DG Semiannual Run as set forth in WO 05086672 on April 20, 2021
- (2) Unit 2 Engineered Safety Feature (ESF) K602 Relay Test as set forth in WO 4918193 on April 24, 2021 (3)1A DG Testing on April 30, 2021 Inservice Testing (IP Section 03.01)===
(1)2BOSR 5.5.8.SI.5-2a, Group A IST Requirements for SI Pump 2SI01PB as set forth in WO 5118448 on April 17,
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04)===
- (1) Unit 1 (April 1, 2020 - March 31, 2021)
- (2) Unit 2 (April 1, 2020 - March 31, 2021)
MS06: Emergency AC Power Systems (IP Section 02.05) (2 Samples)
- (1) Unit 1 (April 1, 2020 - March 31, 2021)
- (2) Unit 2 (April 1, 2020 - March 31, 2021)
MS07: High Pressure Injection Systems (IP Section 02.06) (2 Samples)
- (1) Unit 1 (April 1, 2020 - March 31, 2021)
- (2) Unit 2 (April 1, 2020 - March 31, 2021)
71152 - Problem Identification and Resolution
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its Corrective Action Program (CAP) related to the following issues:
4418342, and 4430576 71153 - Follow-up of Events and Notices of Enforcement Discretion Reporting (IP Section 03.05)
- (1) Evaluated reportability of loss of TSC Heating, Ventilation and Air Conditioning compressors as documented in ARs 4421161 & 4427773 for the week ending June 19, 2021
- (2) Evaluated the reportability of Unit 1 Containment Ventilation Isolation as documented in AR 4430194 on June 18, 2021
- (3) Evaluated reportability of loss of Unit 2 annunciators as documented in AR 4429603 on June 16,
OTHER ACTIVITIES
- TEMPORARY INSTRUCTIONS, INFREQUENT AND ABNORMAL 60855 - Operation of an Independent Spent Fuel Storage Installation The inspectors evaluated the licensees independent spent fuel storage installation (ISFSI) cask loading activities on March 29 through April 2, 2021. Specifically, the inspectors observed the following activities:
Heavy lifts of the loaded transfer cask from the wet pit to the cask processing area
Lid-to-shell root pass welding
Canister processing including forced helium dehydration
Closure ring welding and non-destructive weld evaluations
Stack-up and download of the Multi-Purpose Canister (MPC) from the HI-TRAC into the storage cask (HI-STORM) and
Radiological field surveys The inspectors performed walkdowns of the ISFSI pad, including independent radiation surveys, and walkdowns of the ISFSI haul path and vertical cask transporter.
The inspectors evaluated the following:
Spent fuel selection for the cask for this loading campaign
Selected CAPs action requests
Selected 72.48 screenings and evaluations
INSPECTION RESULTS
Observation: Unit 1 Auxiliary Feedwater Discharge Valve Hand Controller Settings 71152 On April 19, 2021, while performing a control room panel walkdown the inspectors noted that the AF discharge flow control valve hand controller (HK) meter indications and the potentiometer settings did not match each other. The inspectors noted that the HKs meters indicated 70 percent +/- 2 percent while the potentiometer settings appeared to vary between 6.8 and 7.1. Upon identification, the inspectors questioned the operators on shift of the condition. The operators then entered the condition into the Corrective Action Program as CAPs 4418342 and 4418343 for 1HK-AF0031A and 38A, 1A & 1D AF to Steam Generator Setpoint Stations being set above 6.8.
To further evaluate the condition the inspectors proceeded to review the related reference documents and noted that the HKs setpoint should be 6.8 for 1AF005A/B/C/D/E/F/G/H, AF Discharge Flow Control Air Operated Valves to yield 170 gpm. Additionally, 1BOL 7.g, AF Flow Control Valves, included direction in part to apply Technical Requirement Manual (TRM) 3.7.g condition C, which states in part that:
Condition C: One or more AF Flow Control Valve(s) not capable of throttling flow as assumed in the safety analysis for Steam Generator Tube Rupture Margin to Overfill event.
(Note 2) C.1 Restore AF Flow Control Valve(s) to OPERABLE status. 30 days.
Note 2: Condition C is applicable for any AF flow control valve thats flow control pot (1HK-AF031-38A) is adjusted to a setpoint above that specified within 1BGP 100-1A or is incapable of being throttled to control flow at or below the value specified within Design Analysis for Steam Generator Tube Rupture Margin to Overfill, CN-CRA-07-47 Revision 4.
(Pot Setpoint of 6.8 - 170 gpm).
The inspectors reviewed the observations related response in the CAP products. According to the CAP notes, output voltage checks were performed and verified that the current setting would result in the desired voltage and flow. Additionally, it was reported that the meters may vary due to not being calibrated at a specific frequency. From their review the inspectors questioned why the TRM condition was not entered upon discovery as the condition appeared to be met. The inspectors identified that this failure to follow the 1BOL 7.g requirements was a performance deficiency. The deficiency was determined to be of minor significance since the output voltage was verified to result in the desired flow of 170 gpm.
Corrective actions planned by the licensee included revising operating procedures to provide guidance on when to enter the TRM action.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
On July 12, 2021, the inspectors presented the integrated inspection results to Mr. J. Kowalski, Site Vice President, and other members of the licensee staff.
On April 7, 2021, the inspectors presented the Independent Spent Fuel Storage Installation inspection results to Mr. H. Welt, Plant Manager, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Calculations
HI-2146074
Thermal Evaluation of the Hi-TRAC in the Decon Pit at
Byron/Braidwood
Corrective Action
Documents
Corrective Action Reports from March 2018 through
April 2021
03/01/2018 -
04/30/2021
Corrective Action
Documents
Resulting from
Inspection
NRC ID - Improper Work Order Closure
03/31/2021
2.48 Screening
No. 72.48-102
Corrected 72.48 for Dry Cask License Upgrade 72.48-102
2.48 Screening
No. 72.48-168
HI-TRAC Movement Within the Fuel Building
2.48 Screening
No. 72.48-170
DCR to Incorporate Revision to Analysis No. BYR13-063 for
Replacement Nylatron
2.48 Screening
No. 72.48-174
EC 621659/BFP FH-69/BFP FH-70/BFP FH-82/BFP
FH-83/OU-MW-671-300/OU-MW-671-F-01/BYNPS 72.212
Evaluation Report Change Request 06-06
2.48 Screening
No. 72.48-177
Holtec Supplier Manufacturing Deviation Report (SMDR)
No. 1024-2687 Review
2.48 Screening
No. 72.48-179
Replace 3" HI-STORM Lift Bracket Strongback Spacers (for
Ancillary #107)
2.48 Screening
No. 72.48-182
ISFSI Pad/CTOZ Joint Surface Alternate Detail Repair
Method
2.48 Screening
No. 72.48-191
HI-TRAC Movement Within the Fuel Building
2.48 Screening
No. 72.48-192
Analysis No. HI-2146074, Revision 4 - Site-Specific Thermal
Analysis
2.48 Screening
No. 72.48-197
Holtec Supplier Manufacturing Deviation Report (SMDR)
Affecting HI-STORM Serial No. 1118
2.48 Screening
No. 72.48-200
HI-TRAC Loading Operations
60855
Engineering
Changes
2.48 Screening
Approve Use of Nylon-Insert Locknut on HI-TRAC Lift Yoke
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
No. 72.48-202
Spacer Pins
2.48 Screening
No. 72.48-207
Gouge on MPC Lid of MPC Serial No.32-502
2.48 Screening
No. 72.48-209
Spent Fuel Cask Site Transportation
2.48 Screening
No. 72.48-217
Supplier Manufacturing Deviation Report No. 1024-1831
Revision 1
Replace Existing FH Building Overhead Crane SD-41 Weigh
System Controller with a Model SD-50 Controller
LMS Qual Matrix Report
01/05/2021
Physical Inventory of Byron ISFSI MPC-32-0644
03/29/2021
2.212 Change
Request No.
07-02
2.212 Evaluation Change Request
03/04/2019
2.212 Change
Request No.
08-01
2.212 Evaluation Change Request
06/14/2020
2.212 Change
Request No.
08-02
2.212 Evaluation Change Request
06/12/2020
BYR11-182
Byron Cask Loader Database Cask Model and Limits Update
for 2012 ISFSI Campaign
BYR19-006
Byron Cask Model Update for 2019 ISFSI Campaign - ISFSI
BYR20-018
Fuel Selection Package and Alternate List for the Byron 2021
ISFSI Campaign
Contractor Welding Review
01/28/2021
NCR 0832-51
Non-Conformance Report for Pool Lid
Miscellaneous
RRTI-2730-002
Response to Request for Technical Information for Gouge in
MPC-32 S/N 502
Report No.
914667-644-01
through 914667-
644-04
Report of Non-Destructive Examination Lid-to-Shell Weld
03/30/2021
NDE Reports
Report No.
Report of Non-Destructive Examination Closure Welding
03/31/2021
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
914667-644-05
through
914667-644-07
Helium Leak Test Report
03/31/2021
2018 Annual Radiological Environmental Operating Report
04/18/2019
2018 Annual Radioactive Effluent Release Report
04/18/2019
Braidwood and Byron ISFSI Radiation Survey
04/01/2021
Radiation
Surveys
Survey Map # 292
ISFSI Pad Radiation Surveys 2018-2021
03/05/2021
Radiation Work
Permits (RWPs)
Dry Cask Storage ALARA Plan
01/25/2021
NOSA-BYR-20-10
Independent Spent Fuel Storage Installation Audit Report
10/07/2020
Self-Assessments
PI-AA-126-1001-
F-01
BYRON Spent Fuel Loading Campaign (SFLC)
Readiness Assessment
01/22/2021
PMID/RQ
00191464-01
ISFSI Pad Structural Inspection (5 Years)
10/13/2020
LR-FHB-Overhead Bridge Crane Mech Inspection
01/06/2020
EWP EM Crane Inspection (Fuel Handling Bldg) - 0HC03G
01/06/2020
RXS Perform Special Lifting Device INSP/TEST per BHP
FH-85
2/09/2020
Work Orders
EWP MM:0FH05G INSP Spent Fuel Pit/HNDLNG Machine
(LR)
11/23/2020
Extreme Heat Implementation
Procedures
EN-BY-402-0005
Extreme Heat Implementation
4418342
1HK-AF036A AF Flow Control POT Needs Adjustment
04/22/2021
Corrective Action
Documents
Resulting from
Inspection
4418343
1HK-AF031A AF Flow Control POT Needs Adjustment
04/22/2021
Drawings
M-52 sh. 5
Diagram of Fire Protection at Circulating Water Pumphouse
1BGP 100-1A1
Controller Setpoints 1PM06J
BOP AF-E1A
Auxiliary Feedwater Train "A" Electrical Lineup
BOP AF-M1A
Auxiliary Feedwater Train "A" Valve Lineup
BOP DC-E1
DC Battery & Distribution Center Electrical Lineup
Procedures
Fire Protection System Valve Lineup
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
BOP IP-1
Instrument Bus Inverter Startup
BOP IP-1E
Instrument Power Electrical Lineup
20437
NRC Identified: LCSR Housekeeping
04/30/2021
20499
NRC Identified: 0DSD401 Door Closer Not Attached
04/30/2021
20500
NRC Identified: LCSR Housekeeping Items
04/30/2021
23478
NRC Identified: Condition Noted in U1 LCSR Area
05/13/2021
Corrective Action
Documents
Resulting from
Inspection
27381
NRC Identified: Gasket on 0DSD408 Degraded
06/03/2021
PFB TB FZ 8.3-1
Turbine Building 401'-0" ELEV, Unit 1 Turbine Building NE
PFP FZ 11.3-0
North
Auxiliary Building 364' 0" Elev General Area - North
PFP FZ 11.3-0
South
Auxiliary Building 364' 0" Elev General Area South
PFP FZ 18.12-0
AND FZ 18.13-0
Circulating Water Pump House / 0B Fire Pump Room
PFP FZ 3.2-0
U2 Auxiliary BLDG 439'-0" Elevation, Cable Spreading Room
PFP FZ 3.2A-1
U1 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2B-1
U1 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2B-2
U2 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2C-1
U1 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2C-2
U2 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2D-1
U1 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2D-2
U2 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
PFP FZ 3.2E-1
Auxiliary BLDG 439'-0" Elev. Unit 1 Division 11 Cable Riser,
LCSR
PFP FZ 3.2E-2
Auxiliary BLDG 439'-0" Elev. Unit 2 Cable Riser
Fire Plans
PFP FZ3.2A-2
U2 Auxiliary Building 439'-0" Elevation, Lower Cable
Spreading Room
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Engineering
Evaluations
BB-AA-PRA-012
Braidwood/Byron Flood Scenarios
04308126
TSC Compressor 1 Tripped High Refrigerant Pressure
01/05/2020
04327769
IST Stroke Time Failure
04/17/2020
04327798
Pzr Heater Ground Alarm Group A Backup Heater
03/19/2020
04347948
TSC Condensing Unit Trouble
06/04/2020
Corrective Action
Documents
04366934
U-1 Pressurizer Pressure Control Not Responding Normally
09/02/2020
4416548
NRC Identified: Discovered an Employees Badge was Worn
Off
04/14/2021
Corrective Action
Documents
Resulting from
Inspection
23122
PM 4KV Cubicle Inspection and Tagout Procedure
Enhancement
05/12/2021
Miscellaneous
RICT Package
2BOA ELEC-5
Local Emergency Control of Safe Shutdown Equipment
Unit 2
108
Protected Equipment Program
Procedures
OP-BY-108-117-
1000
Byron Protected Equipment Program
Work Orders
5006411
(Sample/Change) Component Cooling Pump 2B
04/15/2021
04417861
Review UT Inspection of 1A01PA Pump Lube Oil Piping
04/20/2021
4415085
NRC DBAI: NRC information Notice 2017-06 Evaluation
04/08/2021
Corrective Action
Documents
4419745
1A DG Manually Secured Due to Exhaust Leak
04/28/2021
04418342
1HK-AF036A, AF Flow Control POT Needs Adjustment
04/22/2021
Corrective Action
Documents
Resulting from
Inspection
4418343
1HK-AF031A, AF Flow Control POT Needs Adjustment
04/22/2021
Corrective Action
Documents
Resulting from
Inspection
25509
NRC Identified: Erroneous ASME Vibration Data
05/25/2021
2BHSR 8.4.2-2
Unit 2 Bus 212 125V Battery Charger Operability
2BOSR 8.6.1-2
25V DC ESF Battery Bank and Charger 212 Operability
Monthly Surveillance (CM-3)
Procedure Use and Adherence
Procedures
MA-BY-723-053
Station Battery Charger 18 Month Surveillance
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
4945435
Clean Battery Charger and Check Connections
04/12/2021
4966367
2 "B" Train 125V Battery Charger Operability Test
04/12/2021
5006411
(Sample/Change) Component Cooling Pump 2B
04/15/2021
5110415
(NEIL)- 2CC01PB Comp IST RQMTS for Residual CC Pump
04/15/2021
26604
1BOSR 5.5.8.SI.5-2A 1B SI IST Group A Pump Test
05/13/2021
Work Orders
5136320
2BOSR 8.6.1-2, 125V Battery & Charger 212 Operability
04/12/2021
Corrective Action
Documents
Resulting from
Inspection
4416813
NRC IDENTIFIED: Residual Boric Acid Leak in Area 7
04/15/2021
Procedures
1BOSR 3.2.8-
2B
Unit One ESFAS Instrumentation Slave Relay Surveillance
(Train B Automatic Safety Injection and RWST LO-2 Level -
K602, K647, K648)
05086672
2B Diesel Generator Operability Run and Semiannual
Surveillance
04/19/2021
4918193
Slave Relay Trn B SI-K602, 647/VA, VC, CV, SI (WK D)
04/21/2021
Work Orders
5118448
(NEIL) - 2SI01PB Group A IST Requirements for Safety
Injection
04/15/2021
Miscellaneous
Operations Logs for Selected MSPI
04/01/2020 -
03/31/2021
71151
Procedures
BY-MSPI-001
Reactor Oversight Program MSPI Basis Document
01/30/2020
4416842
NRC Question on DC 211 Ground Status
04/15/2021
4417638
0FP176A Packing Leak
04/19/2021
23476
NRC Identified: 1B SI Pump Window Tags-Plus
05/13/2021
4430576
NRC Identified: 1HK-AF038A has 3% and 5% Indicator
Offset
06/21/2021
Corrective Action
Documents
Resulting from
Inspection
4430638
NRC Identified: Sign Offs Missing in 1AF-018 Loop Cal
Package
06/21/2021
Drawings
M-2037 sh. 1
P&ID/C&I Diagrams Auxiliary Feedwater System-AF
P
Miscellaneous
Auxiliary Feedwater to Steam Generator 1D Flow Control
Loop (AF) (Train B) - Test Report Package (TRP)
1BOL 7.g
LCOAR Auxiliary Feedwater (AF) Flow Control Valves
Procedures
BISR 3.4.2-200
Surveillance Calibration of Aux Feedwater to Steam
Generators A, B, C, and D Flow Control Loops
Inspection
Procedure
Type
Designation
Description or Title
Revision or
Date
Work Orders
4965532
Calibrate Electronic Portion of AF Loop
05/21/2021
21161
TSC Condensing Unit 0VV30C - Compressor 2 Trouble
05/03/2021
27773
0VV30C Comp 1 Trouble
06/06/2021
29603
Annunciator System Trouble
06/16/2021
4430194
1AR12J Spiked into High Alarm
06/18/2021
Corrective Action
Documents
4430661
TSC Condensing Unit 0VV30C - Compressors Tripped
06/21/2021
2BOA ELEC-7
Loss of Annunciators
2BOSR AN-SA1
Annunciator System Input Isolator Circuit Operability
Semiannual Surveillance
BAR 2-4-E7
AN SYS Field Contactor Pwr Trouble
EP Reportability - Loss of Emergency Preparedness
Capabilities
Procedures
Safety (SAF) Reportability Manual
31