ML17326A042

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NPDES Noncompliance Notification:On 990707,sample Taken Showed Residual Clam-Trol CT-2 Value of 0.17 Ppm.Caused by Interruption of Clay Feed to Unit 1 Discharge Vault.Valve Was Cleared & Clay Feed Was re-established
ML17326A042
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 07/09/1999
From: Carlson J
INDIANA MICHIGAN POWER CO.
To: Morley F
MICHIGAN, STATE OF
References
NUDOCS 9907160102
Download: ML17326A042 (5)


Text

~ . REGULA RY INFORMATION DZSTRIBUTI SYSTEM (RIDS)

E ACCESSION .NBR:9907160102 DOC.DATE: 99/07/09 NOTARIZED: NO DOCKET ¹ FACIL,.50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 RUTHiCTAME AUTHOR AFFILIATION CARLSON,J.P. Indiana Michigan Power Co.

RECZP.NAME RECIPIENT AFFILIATION MORLEY,F. Michigan, State of

SUBJECT:

NPDES noncompliance notification:on 990707,sample taken C showed residual Clam-Trol CT-2 value of 0.17 ppm.Caused by interruption of clay feed, to Unit 1 discharge vault. Valve A was cleared & clay feed was re-established.

T D1STR1BUT1'ON CODE: C001D CORTES RECEXVED:LTR I ENCL ( STRE:

TITLE: Licensing Submittal: Environmental Rept Amdt & Related Correspondence E NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL STANG, J 1 1 INTERNAL: 1 1 LA 1 1 NUDOCS-ABSTRACT 1 1 OGC/RP 1 0 RGN3, DRS/RSB 1 1 EXTERNAL: NOAC 1 1 NRC PDR 1 1 D

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NOTE TO ALL "RIDSU RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 8 ENCL 7

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6I6 465 5901 IHOIANA NICHIGAN POWER Mr. Fred Morley, District Supervisor Surface Water Quality Division Michigan Department of Environmental Quality 1342 SR M89 West Suite B Plainwell MI 49080 July 9, 1999

Dear Mr. Morley:

Re: Cook Nuclear Plant NPDES Permit MI0005827 This notification is provided as required by Part I Section A.1**

Effluent limit, and Part II Section A.5, Noncompliance Notification of NPDES Permit MI0005827.

During the biocide treatment performed at the Donald C. Cook Nuclear Plant on Wednesday, July 7'", two short interruptions in detoxification agent bentonite clay occurred. These interruptions led to NPDES permit exceedences in Outfall 001.

On 7/7/99, Outfall 001 (Circulating Water Discharge) sample taken at 2100 hrs. showed a residual Clam-Trol CT-2 value of 0.17 ppm.

The discharge exceedence was the result in an interruption of the clay feed to the Unit 1 Discharge Vault. A valve placed at the end of the line going down the Unit 1 Discharge Vault became blocked with clay and restricted the flow of clay slurry to the vault. The valve was cleared and clay feed was re-established.

Another sample was pulled at 2207 hrs. and showed less than the detectable concentration of 0.05 ppm Clam-Trol CT-2.

Clam-Trol CT-2 feed had been completed at 2252 hrs. on 7/7/99.

Clay feed was continued for purposes of detoxifying the Clam-Trol CT-2 residual that was left in the system until it passed through plant equipment between 0145-0200 hrs. on 7/8/99. On 7/8/99, Outfall 001(Circulating Water Discharge) samples taken at 0130 and 0200 hrs. showed 0.08 ppm and 0.06 ppm Clam-Trol CT-2 respectively. The cause of the 0130 hrs. exceedence was due to the air operated clay pump freezing just before the sample was taken at 0130 hrs. The cause of the 0200 hrs. exceedence was due to the clay truck running out of clay slurry at 0145-0200 hrs. Outfall 001 was again sampled at 0300 hrs. and showed less than the detectable concentration of 0.05 ppm Clam-Trol CT-2.

The impact of the CT-2 discharge on Lake Michigan fish at Unit 1 discharge should be zero because of the following:

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Mr. Fred Morley July 9, 1999 NPDES Notification of CT-2 exceedence at 001.

1. Bio-assay data for the CT-2 product for NOEL (No Observable Effect Limit) is 2.0 ppm as CT-2 for Trout as tested in a 96 hour0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> flow through bio-assay test. The maximum exposure to the fish would have been 0.17 ppm for a maximum of 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> at 2100 hours0.0243 days <br />0.583 hours <br />0.00347 weeks <br />7.9905e-4 months <br /> on 7/7/99 and 0.08 ppm for a maximum of 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> on 7/8/99.
2. The Unit 1 discharge stream was 1/10 of the total treatment flow of 150, 000 gallons per minute for the combined Unit 1 and 2 discharge. The majority of discharge was directed to Unit 2's Outfall 002 where the circulating water pump discharge was directed. This does not take into account the further dilution available at the discharge mixing zone at the end of the pipe, which would further reduce CT-2 concentration.

P To prevent future exceedences, we will implement the following actions for all subsequent CT-2 applications that require detoxification by clay addition.

1. The inventory of clay will be maintained to allow for an added two hours of detoxification after a calculated zero CT-2 level is reached. Actual feed of clay will be done for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after actual test sample of zero for service water is recorded
2. Visual/instrument verification of the clay feed point discharge will be continuous to ensure clay feed to the Unit discharge vault. Also, clay feed slurry back-up pumps will be installed as spares for immediate availability should the main pump fail.

Should you have any questions please contact me at (616)465-5901 ext. 1153.

Sincerely John P. Carlson Environmental Superintendent C: Nuclear Regulatory Commission Sihenvlro lhcorreepondenceahonr!ace vateHCT-2 001.doc

Mr. Fred Morley July 9, 1999 NPDES Notification of CT-2 exceedence at 001.

.I certify under penalty of law that I have personally examined and am familiar with the information submitted on this and all attached documents, and based on my inquiry of those individuals immediately responsible for obtaining the information, I believe the submitted information is true, accurate and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fine and imprisonment.

T. P. Noonan Plant Manager