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Issue date | Title | Topic | |
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ML17326A119 | 10 September 1999 | NPDES Noncompliance Notification:On 990909,unnatural Turbidity Was Observed at Cook Plant Outfall 001 & 002. Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Terminated Clay Feed | Zebra Mussel |
ML17326A043 | 9 July 1999 | NPDES Noncompliance Notification:On 990707,unnatural Turbidity Was Observed at Outfall 002.Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Clay Feed Was Terminated on 990708 | Zebra Mussel |
ML17326A042 | 9 July 1999 | NPDES Noncompliance Notification:On 990707,sample Taken Showed Residual Clam-Trol CT-2 Value of 0.17 Ppm.Caused by Interruption of Clay Feed to Unit 1 Discharge Vault.Valve Was Cleared & Clay Feed Was re-established | |
ML17335A144 | 31 July 1998 | NPDES Noncompliance Notification:On 980623,ice-making Sys Discharge Line Developed Leak & Oversprayed Containment Spillings Approx 50 Gallons.Caused by Vibration & Wear Against Line.Discharge Line Supports Have Been Redesigned | |
ML17334B816 | 8 July 1998 | NPDES Noncompliance Notification:On 980617,discovered Lube Oil Discharge.Caused by Leaking Tubes Due to Corrosion of Tubes.Leaking Tubes Repaired & Established Insp/Preventive Maint Program for Lube Oil Coolers | |
ML17334B757 | 27 April 1998 | NPDES Noncompliance notification:980327,boiler Condensate Spill Occurred.Caused by Small Amount of Condensate on Metal Skirting Surrounding Containment Berm.Failed Condensate Valve Was Replaced | |
ML17334A686 | 13 March 1998 | NPDES Noncompliance Notification:On 980209,boiler Condensate Spill Occurred.Caused by Failed Sight Glass on Rental Plant Heating Boiler.Replaced Site Glass & Installed Plexiglass Shield Around Site Glass to Protect Operators | |
ML17334A588 | 9 December 1997 | NPDES Noncompliance Notification:On 971108 Plant Personnel Chlorination Sys Was Shut Down,Due to Valve Lineup Error Made During Startup of Continuous Chlorination After Shutdown.Corrected Lineup & Repositioned Valve | |
ML17333A388 | 13 March 1996 | NPDES Noncompliance Notification:On 960310,continuous Ph Monitoring of Outfall 00D(turbine Room Sump)Interrupted. Caused by Electronic Failure of Monitoring Instrumentation. Grab Samples Performed & Monitor Recalibrated on 960311 | Grab sample |
ML17333A387 | 28 February 1996 | NPDES Noncompliance Notification:On 960226,continuous Ph Monitoring of Outfall 00D(Turbine Room Sump) Interrupted. Caused by Fouling of Ph Instrumentation Glass Electrode. Electrode Cleaned & Ph Monitor Returned to Svc | |
ML17332A979 | 21 September 1995 | NPDES Noncompliance Notification:On 950916,unnatural Turbidity Observed at Plant Outfalls 001 & 002 During Molluscicide Treatment at Plant.Preventive Actions Not Possible Due to Detoxificaion Requirements in NPDES Permit | Zebra Mussel |
ML17332A955 | 8 September 1995 | NPDES Noncompliance Notification:On 950829,hydraulic Oil Spill Occurred While Divers Using Hydraulic Brushes to Remove Zebra Mussels from Plant Screenhouse Intake Forebay Walls.Oil Absorbent Booms Deployed Into Forebay | Zebra Mussel |
ML17332A954 | 7 September 1995 | NPDES Noncompliance Notification:On 950831,determined That Discharge from Outfall 00C (Heating Boiler Blowdown) Exceeded Concentration of Monethanolamine Submitted in NPDES Application Due to Valve Being Aligned in Open Position | |
ML17332A830 | 8 June 1995 | NPDES Noncompliance Notification:On 950530,spill of Ethylene Glycol Occurred When Contracted Svc Technician Troubleshooting Portable Welding Machine.Ethylene Glycol Coolant Replaced W/Propylene Glycol Coolant | |
ML17332A699 | 23 March 1995 | NPDES Noncompliance Notification:On 950205 to 16,33 Wild Ducks Entrained in Intake Cribs & Subsequently Collected on Intake Screens within Screenhouse.Suspect Ducks Entrained While Feeding on Zebra Mussels | Zebra Mussel |
ML17332A696 | 20 March 1995 | NPDES Noncompliance Notification:On 950301,bypass Discharge from Turbine Room Sump Through Emergency Over Flow Piping Into Intake Forebay to Lake Michigan | |
ML17331B331 | 30 March 1994 | NPDES Noncompliance Notification:On 940303,determined HVAC Sys Leaking Water Containing Approx 1,000 Mg/Liter Sodium Nitrite at Calculated Rate of 0.5 Gpm | |
ML17331A884 | 8 June 1993 | NPDES Noncompliance Notification:On 930526 Chlorine Exceedance Incorrectly Stated Event Occurred on May 21 Instead of Actual Date of May 19.Licensee Apologizes for Inconvenience Error May Have Caused | |
ML17331A125 | 24 March 1993 | NPDES Noncompliance Notification:On 930322,plant Personnel Discovered Small Oil Sheen at North Storm Water Outfall 001S.Oil Residue from Parking Lot Gradually Entered Lake Michigan.Oil Absorbent Booms in Place at Outfall | |
ML17329A682 | 12 November 1992 | NPDES Noncompliance Notification:On 921109,review of Records Determined That First Quarter 1992 Samples for Stormwater Outfall 001S Not Collected.Quarterly Sampling Requirement Added to Computerized Tracking Sys | |
ML17329A552 | 2 July 1992 | NPDES Noncompliance Notification:On 920630,minor Inadvertent Discharge of Treatment Chemical Clam-trol CT-1 May Have Occurred.Fire Protection Clam-trol Treatment Was Suspended Immediately & Will Not Be Resumed Until Alterations Made | Zebra Mussel |
ML17329A548 | 29 June 1992 | NPDES Noncompliance Notification:On 920624,grab Sample of Outfall 002 Circulating Water Discharge Indicated TRC Concentration of 0.33 mg/1.Caused by Flow Balance Between Plant Sys.Unit 1 in Shutdown Condition | Grab sample |
ML17329A540 | 10 June 1992 | NPDES Noncompliance Notification:On 920606,grab Sample of Outfall 002 Circulating Water Discharge Indicated Total Residual Chlorine Above Timits.Caused by Manfunctioning Svc Water Flow Meter.Flow Meter Will Be Replaced | Grab sample |
ML20086T991 | 3 January 1992 | Noncompliance Notification:On 911219,approx 400 Diving Ducks Collected in Circulating Water Sys Screenwash Baskets.Caused by Abundant Food Supply Provided by Circulating Water Discharge.Flow Rates Reduced | Zebra Mussel |
ML17329A323 | 10 December 1991 | NPDES Noncompliance Notification:On 911129,discovered That HX Associated W/Component Cooling Water Sys Leaking & Drop in Sys Surge Tank Level Occurred.Approx 5,300 Gallons of Water Leaked from Sys.Hx Isolated for Repairs | |
ML17329A096 | 11 July 1991 | Final NPDES Notification Re Exceeding Heat Addition Effluent Limitation on 910701-05 on Outfall 001 & 002. Cause Under Investigation.Power Reduction Initiated on 910705 to Meet Limitations | |
ML17328B009 | 9 April 1991 | NPDES Noncompliance Notification:On 910327,automatic Temp Recorder for Outfall 001 Failed & No Temp Measurements Recorded from 910328-31.Plant Procedures Will Be Revised to Describe Compensatory Sampling Measures in Event of Failure | |
ML17334B396 | 26 February 1991 | NPDES Noncompliance Notification:On 910220 & 21,unmonitored Discharges Occurred from Turbine Room Sump.Caused by Inoperable Ph Meter.Turbine Sump Room Isolated & Job Order Written to Repair Meter | |
ML17328A764 | 30 October 1990 | NPDES Noncompliance Notification:On 901025,five Unmonitored Discharges from Turbine Room Sump Occurred Releasing 250,000 Gallons of Water.Caused by Downstream Blockage of Flow to TRS Sample Line.In Interim,Ph Sampling Performed | |
ML17325B331 | 7 November 1989 | Notifies That Total Recoverable Petroleum Hydrocarbons Sample Collected on 891006 Contained 0.9 mg/1 Trph.Util Believes Amount to Be Anomalous Value | |
ML17326B570 | 9 March 1989 | NPDES Noncompliance Notification:Prefilter Backwash Limitations Exceeded for Feb 1989.Plan to Ensure Future Compliance W/Npdes Permit Requirements Will Be Submitted to Plainwell District Ofc | |
ML17326B554 | 6 March 1989 | NPDES Noncompliance Notification:On 890224,leak Found in Main Turbine Lubricating Oil Coolers.Cause Not Stated. Leaking Cooler Isolated & Tube Plugged & Eddy Current Testing Performed to Determine Integrity of Remaining Tubes | |
ML17326B498 | 18 November 1988 | NPDES Noncompliance Notification:On 881114,sample of Prefilter Backwash Effluent (Outfall 00F) Analyzed for Suspended Solids & Indicated 171 mg/1.Rough Lake Conditions Stirred Bottom Sediments Coming Into Plant Intake Water | |
ML17326B494 | 7 November 1988 | NPDES Noncompliance Notification:On 881031,prefilter Backwash Discharge (Outfall 00F) Indicated Suspended Solids Concentration of 138 Mg/L | |
ML17325A981 | 5 October 1988 | NPDES Noncompliance Notification:On 880919,water Makeup Prefilter Backwash Sample Exceeded Limitations.Caused by High Solids in Intake from Lake Michigan.Plant Personnel Reminded About Need to Evaluate & Rept Analyses Promptly | |
ML17325A929 | 13 September 1988 | NPDES Noncompliance Notification:On 880910,Unit 1 Discharged Taken During Circulating Water Chlorination Showed Chlorine Concentration of 0.135 Mg/L.Caused by Temporary Reduced Water Flow Through Sys.Pump Chlorine Feed Reduced | Grab sample |
ML17325A844 | 15 June 1988 | NPDES Noncompliance Notification:On 880602,oil Spill of Approx 300 Gallons from Underground Storage Tank Occurred. Cleanup & Recovery Measures Underway.Repairs Will Be Made to Leak Area.Cleanup Will Be Completed by 880617 | |
ML17325A491 | 23 November 1987 | NPDES Noncompliance Notification:On 871117,analysis of Grab Sample of Unit Discharge Taken During Circulating Water Chlorination Showed Total Residual Chlorine Concentration Above Limits.Caused by Vibration Causing Valve to Close | Grab sample |
ML17325A296 | 14 September 1987 | NPDES Noncompliance Notification:On 870901,spill from Turbine Room Sump,Outfall 00D Occurred.Approx 9,000 Gallons of Water Overflowed to Lake Michigan.Grab Sample Indicated Ph of 6.57 & No Trace of Oil & Grease.Caused by Repairs | Grab sample |
ML17325A268 | 11 August 1987 | NPDES Noncompliance Notification:On 870805,chlorination of Circulating Water Commenced Due to Biological Fouling.Total Residual Chlorine Levels Recorded on 870805,08 & 09 Listed | |
ML17334B116 | 6 July 1987 | NPDES Noncompliance Notification:On 870630,monitoring Turbine Room Sump Process Ph Meter Found to Be Inoperative. Turbine Room Sump May Have Discharged to Absorption Pond During Previous 5 H W/O Continuous Monitoring | Grab sample |
ML17325A083 | 27 April 1987 | NPDES Noncompliance Notification:On 870410,oil Entered Yard Drain When Pressurized Tank Sprayed Out 10 Gallons Number 2 Fuel Oil During Attempt to Measure Level in east-middle Heating Boiler Fuel Oil Tank.Cleanup Began Immediately | |
ML20213G989 | 14 November 1986 | NPDES Noncompliance Notification:On 861107,recording Instrument from Which Circulating Water Intake & Discharge Temps Obtained Failed.Caused by Faulty servo-motor.Recording Instrument Repaired & Returned to Svc | |
ML20214P996 | 9 September 1986 | Corrected NPDES Noncompliance Notification:On 860903,turbine Room Sump Overflowed Into Circulating Water Sys Intake Forebay.Caused by Airlocked Suction Lines.Grab Sample Taken. Condition Rept Will Determine Corrective Action | Grab sample |
ML17324A998 | 14 July 1986 | NPDES Noncompliance Notification:On 860709,discovered That Grab Sample for Suspended Solids Not Obtained for Steam Generator Blowdown During 860629 Startup.Blowdown Sys Used for Weekly Sampling Frequency | Grab sample |
ML20211K513 | 19 June 1986 | NPDES Noncompliance Notification:On 860616,during Draining & Cleaning Steam Generators,Suspended Solids Sample from Startup Blowdown Flash Tank Revealed Concentration of 172 Ppm.Probably Caused by Boric Acid | Boric Acid |
ML20205S849 | 2 June 1986 | NPDES Noncompliance Notification:On 860528,w/both Nuclear Units Out of Svc,Heating Boiler Started.Blowdown Sample Had Suspended Solids Concentration of 129.Caused by Chemical Shock | |
ML17321A941 | 24 October 1985 | NPDES Noncompliance Notification:On 851023,sample Taken of Suspended Solids Concentration Elevated.Caused by Chemical Shock Due to Batch Addition of Chemical Treatment | |
ML20198A863 | 24 October 1985 | NPDES Noncompliance Notification:On 851019,steam Generator Found to Have Suspended Solids Concentration of 2,442 Ppm. Caused by Recent Steam Generator Cleaning | |
ML20138N627 | 24 October 1985 | NPDES Noncompliance Notification:On 850716,plant Heating Boiler Started While Both NSSS Out of Svc.Blowdown Sample Taken on 851022,contained Suspended Solids Concentration of 169 Ppm.On 851023,sample Contained 195 Ppm |