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Issue date | Title | Topic | |
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ML20151U467 | 18 April 1977 | PNO-77-058:on 770418,following Logic Testing Small Fire of Less than 1 Minute Was Extinguished in Relay Cabinet in Cable Room Using Hand Held CO2 Extinguisher.Shutdown in Progress to Permit Replacement of Relays | |
ML20151U630 | 19 May 1977 | PNO-77-086:on 770518,eight Horizontal Cracks Five to Seven Inches in Length Identified in Area Just Below CRD Nozzle on Reactor Vessel Wall.Licensee & GE Evaluating Cracks.Media Interest Not Expected & Press Release Not Planned | |
ML20151V001 | 12 May 1977 | PNO-77-082:insp of CRD Return Nozzle Identified Cracks Which Appear to Be of Same Magnitude as Those Identified at Unit 3 During Earlier Outage.Licensee in Process of Grinding Out Cracks | |
ML20151X744 | 5 October 1977 | PNO-77-175:licensee Reported That Reactor Cleanup Sys Leaks in Equipment Room Resulted in Release of 80,870 Mci, Predominantly Iodine,Based on 24-hour Sample Taken from 771003-04.Commonwealth of PA Notified | |
ML20151X778 | 29 July 1977 | PNO-77-136:on 770729,during Daily Surveillance Testing of Insert & Retract Circuits for Neutron Detectors in SRM & IRM Channel of Nuclear Instrumentation,Evidence of Fire That Had Self Extinguished Was Discovered in Relay Cabinet | |
ML20155H132 | 8 May 1986 | PNS-I-86-005:on 860506 & 07,bomb Threats Received. Nonessential Personnel Evacuated.No Device Found. Investigation Continuing | |
ML20198B372 | 9 March 1983 | PNS-I-83-002:on 830308,reactor Operator Observed Small Smoldering Fire in Area Containing Sorted Radwaste Matl in Radwaste Bldg.Investigators Found Two Burned Out Cardboard Matches Stuck to One of Unburned Bags in Pile | |
ML20205T188 | 1 April 1987 | PNO-I-87-26A:on 870331,order Issued Suspending Power Operation Immediately.Unit 3 Began Controlled Shutdown from 100% Reactor Power.Unit 2 Currently in Scheduled Refueling Outage W/In Progress Core Offload 2/3 Complete | |
ML20211E357 | 20 October 1986 | PNS-I-86-020:on 861017,licensee Determined That Terminal Strip in Motor Control Ctr Disengaged.Preliminary Investigation by Licensee Found No Evidence of Authorized Work Performed on Sys.Investigation Continuing | |
ML20213D166 | 12 March 1980 | PNO-I-80-40:on 800312,control Operator Injured While Attempting to Free Air Injector Gas Valve When Valve Opened & Caught Right Hand Between Valve Body & Position Indicator. Sustained Gash Between Thumb & Index Finger | Mission time |
ML20236F300 | 10 June 1976 | PNS-76-026:on 760610,State Police Advised Peach Bottom Station That Friends of Animals Organization from Lancaster,Pa Plans to Demonstrate Outside Plant Gate on 760703 or 04.Media Interest Expected | |
ML20236L505 | 8 February 1977 | PNO-77-025:during Refueling Outage Inservice Insp Have Identified Following Pipe Cracks in Primary Coolant Boundary.Cracks Caused Delay in Scheduled Date for Plant Restart from 770223 to 770305 | |
ML20236M087 | 24 January 1977 | PNO-77-013:on 770124,licensee Reported That During Performance of Inservice Inspections During Current Refueling Outage,Ultrasonic Testing Revealed Crack in 12 Diameter Core Spray Pipe Line | |
ML20236R575 | 19 November 1987 | PNS-I-87-019:on 871118,nonspecific Bomb Threats Received Over Plant Internal Telephone Sys.Steps to Heighten Security Awareness Among Plant & Security Supervisors Taken. Investigation Initiated by Licensee | |
ML20246H591 | 25 August 1989 | PNS-I-89-012:on 890825,3 Bomb Threats Received.Vital Areas & Administration Bldg Searched.Threat Considered Hoax.Nrc & Commonwealth of PA Informed | |
ML20246P582 | 30 August 1989 | PNS-I-89-014:on 890829,unusual Event Declared Due to Mischievous Vandalism of Electrical Circuit Breakers.Total of 10 Breakers Found W/Cut Leads.Region I Physical Security Inspector Dispatched to Site & Press Release Issued | |
ML20247D442 | 19 July 1989 | PNS-I-89-013:on 890711,trespasser Arrested by Commonwealth of PA at Plant & While Arrested Made Ref to Large Amounts of Weapons & Explosives Stored at Residence in Edgewood,Md.Explosives & Detonators Removed from Residence | |
ML20247H855 | 25 May 1989 | PNS-I-89-007:on 890525,telephone Call Received at Util Headquarters in Philadelphia,Pa Indicating That Van Loaded W/Explosives Would Arrive at Plant.Threat Evaluated as Noncredible.Heightened Security Awareness Initiated | |
ML20247H867 | 26 May 1989 | PNS-I-89-007A:on 890525,two Vehicle Bomb Threats Received at Facility.Licensee Maintaining in-force Heightened Security Measures.Law Enforcement Agencies in Plant Vicinity & Commonwealth of PA Notified | |
ML20247N007 | 11 September 1989 | PNS-I-89-015:revised Notification of Telephone Threat, Correcting Event Date from 890909 to 890911.Call, Originating from Limerick or Peach Bottom,Received at Corporate Ofc.On 890525,threat Received at Peach Bottom | |
ML20249B132 | 19 February 1976 | PNO-76-028:on 760218,gaseous Radioactive Release Occurred for 1 H Period While Processing Spent Resin.No Personnel Overexposures & No Particulate or Halogens Released.State of PA Informed | |
ML20249B179 | 30 March 1976 | PNO-76-057:on 760329,gaseous Radioactive Release Occurred for One Hour Period,While Unit Being Cooled Down for Refueling Outage.Release Occurred When Main Steam Isolation Valves Reopened to Control Pressure | |
ML20249B229 | 7 November 1977 | PNS-77-044:on 771106,message Received by Telephone at Garage of Henkel & Mccoy,Contractor Working at Peach Bottom,Stated That Caller Knew of Person Planning to Place Bomb in Peach Bottom Nuclear Site | |
ML20249B234 | 15 March 1976 | PNO-76-042:on 760313,while Operating at 99% Power,Increased Reactor Coolant Sys Leakage Was Noted.Reactor Was Shutdown & Drywell Entry Was Made to Investigate Leak Source.Leak Was Repaired & Reactor Returning to Power | |
ML20249B259 | 8 April 1976 | PNO-76-069:on 760407,dye Penetrant Testing on 6 Feedwater Nozzles Revealed 120 Crack Indications While Shutdown for Routine Refueling Outage.Contractor,Swri,Scheduled to Perform Addl Nondestructive UT Exam of Nozzles | |
ML20249B272 | 14 April 1976 | PNO-76-072:on 760413,review of Lpci/Rhr Pump Start Circuitry Conducted by Licensee,Revealed Circuit Design Error.Second Pump in Each Loop Will Not in Some Cases Automatically Start Following Loss of AC Power | |
ML20249B321 | 5 May 1976 | PNO-76-082:on 760505,contractor Employee Fell 50 Feet While Riding Crane Hook in Radwaste Bldg.Employee Taken to Delta, PA by Ambulance & from There by State Police Helicopter to Hospital in Baltimore.Licensee Conducting Investigating | |
ML20249B379 | 5 April 1976 | PNO-76-063:while Reactor Was in Refueling Outage on 760403,RHR Heat Exchanger Leak Occurred Which Released Reactor Water to Plant Effluent Via Heat Exchanger Cooling Water Sys.Region I Investigating Cause of Failure | |
PNO-I-79-040, on 791218,contractor Painter Fell from Ladder in Reactor Bldg & Sprained Ankle.Painter Was Treated & Released from Hosp.No Radiation or Contamination Involved | 18 December 1979 | PNO-I-79-040:on 791218,contractor Painter Fell from Ladder in Reactor Bldg & Sprained Ankle.Painter Was Treated & Released from Hosp.No Radiation or Contamination Involved | Mission time |
PNO-I-82-044, on 820619,w/Unit 3 at Full Power,Hpci & Reactor Core Isolation Cooling Sys Injected Water to Core for 30 Before Safety Injection Verified Unnecessary.Caused by Degradation of Power Supply Unit | 21 June 1982 | PNO-I-82-044:on 820619,w/Unit 3 at Full Power,Hpci & Reactor Core Isolation Cooling Sys Injected Water to Core for 30 Before Safety Injection Verified Unnecessary.Caused by Degradation of Power Supply Unit | |
PNO-I-83-038A, on 830427,recirculation Loop a Riser Exam Completed.One Weld in Each of Two Risers Had Crack Indications.Data Forwarded to GE for More Detailed Analysis. Licensee Addressing Repair Method & Impact on Outage | 27 April 1983 | PNO-I-83-038A:on 830427,recirculation Loop a Riser Exam Completed.One Weld in Each of Two Risers Had Crack Indications.Data Forwarded to GE for More Detailed Analysis. Licensee Addressing Repair Method & Impact on Outage | |
PNO-I-85-048, on 850709,maint Worker Suffered First Degree Burns to Hands & Second Degree Burns to Arms & Face While Cleaning 13 Kv Transformer Disconnect Panel.Short Circuit Caused Voltage Transient.Sys Lineup Being Restored | 9 July 1985 | PNO-I-85-048:on 850709,maint Worker Suffered First Degree Burns to Hands & Second Degree Burns to Arms & Face While Cleaning 13 Kv Transformer Disconnect Panel.Short Circuit Caused Voltage Transient.Sys Lineup Being Restored | |
PNO-I-85-057, on 850812,facility Began Shutdown Due to Unusual Event.Caused by Inoperable LPCI Loop a Due to Diesel Generator E3 Out of Svc for Annual Insp & RHR-LPCI Outer Isolation Valve (MO-154A) Not Opening During Surveillance | 13 August 1985 | PNO-I-85-057:on 850812,facility Began Shutdown Due to Unusual Event.Caused by Inoperable LPCI Loop a Due to Diesel Generator E3 Out of Svc for Annual Insp & RHR-LPCI Outer Isolation Valve (MO-154A) Not Opening During Surveillance | |
PNO-I-85-060, on 850819,unit Shut Down.Caused by Diesel Generator E2 Out of Svc for Annual Insp & RHR-LPCI Outer Isolation Valve MO-154A Not Opening During Surveillance. Valve Will Be Repaired & Diesel Generator Returned to Svc | 20 August 1985 | PNO-I-85-060:on 850819,unit Shut Down.Caused by Diesel Generator E2 Out of Svc for Annual Insp & RHR-LPCI Outer Isolation Valve MO-154A Not Opening During Surveillance. Valve Will Be Repaired & Diesel Generator Returned to Svc | |
PNO-I-85-068, on 850923,chemistry Technician Determined to Be Missing & Possibly Drowned After Being Sent to Obtain Environ Water Grab Sample from Discharge Canal.Search by Util & State Police Unsuccessful | 24 September 1985 | PNO-I-85-068:on 850923,chemistry Technician Determined to Be Missing & Possibly Drowned After Being Sent to Obtain Environ Water Grab Sample from Discharge Canal.Search by Util & State Police Unsuccessful | Grab sample |
PNO-I-85-080, on 851017,plant Tripped on Low Level Due to Loss of All Three turbine-driven Main Feed Pumps.Cause Unstated.Reactor Vessel Level Recovered by HPCI & RCIC Injection | 17 October 1985 | PNO-I-85-080:on 851017,plant Tripped on Low Level Due to Loss of All Three turbine-driven Main Feed Pumps.Cause Unstated.Reactor Vessel Level Recovered by HPCI & RCIC Injection | |
PNO-I-85-094, on 851226,reactor Scrammed on Low Reactor Water Level.Caused by Loss of Feed Pump & Fluctuations in Feedwater Level Control Sys.Condensate & Feedwater Sys Isolated.Rcic Sys Manually Started to Control Water Level | 27 December 1985 | PNO-I-85-094:on 851226,reactor Scrammed on Low Reactor Water Level.Caused by Loss of Feed Pump & Fluctuations in Feedwater Level Control Sys.Condensate & Feedwater Sys Isolated.Rcic Sys Manually Started to Control Water Level | |
PNO-I-86-008, on 860124,unit Scrammed from 95% Power After Diesel Generator E-2 Tripped When Loaded W/Certain Emergency Buses.Caused by Mechanical Failure of Scavenging Air Blower. Addl Damage Caused by Debris | 27 January 1986 | PNO-I-86-008:on 860124,unit Scrammed from 95% Power After Diesel Generator E-2 Tripped When Loaded W/Certain Emergency Buses.Caused by Mechanical Failure of Scavenging Air Blower. Addl Damage Caused by Debris | |
PNO-I-86-015, on 860216,water in Condenser Pumped to Condensate Storage Tank,Resulting in Overflow.Caused by Blown Fuse in Main Condenser Hotwell Level Control Sys.Water Drained by Yard Drain Sys & Released to River | 18 February 1986 | PNO-I-86-015:on 860216,water in Condenser Pumped to Condensate Storage Tank,Resulting in Overflow.Caused by Blown Fuse in Main Condenser Hotwell Level Control Sys.Water Drained by Yard Drain Sys & Released to River | |
PNO-I-86-019, on 860124,diesel Generator E-2 Scavenging Air Blower Failed After 21 H Continuous Operation at Low Load. Caused by Excessive Low Load Operation,As Reported by Vendor.Blower Replaced W/Higher Tolerance Blower | 20 February 1986 | PNO-I-86-019:on 860124,diesel Generator E-2 Scavenging Air Blower Failed After 21 H Continuous Operation at Low Load. Caused by Excessive Low Load Operation,As Reported by Vendor.Blower Replaced W/Higher Tolerance Blower | |
PNO-I-86-029, on 860413,explosion & Resultant Fire Occurred in Offsite Transformer.Caused by Internal Phase a Electrical Fault,Resulting in Fire & Damage to Adjacent Phase B.Plant Fire Brigade Extinguished Fire | 14 April 1986 | PNO-I-86-029:on 860413,explosion & Resultant Fire Occurred in Offsite Transformer.Caused by Internal Phase a Electrical Fault,Resulting in Fire & Damage to Adjacent Phase B.Plant Fire Brigade Extinguished Fire | |
PNO-I-86-043, on 860618,unplanned Shutdown Commenced Due to Leak in Emergency Svc Water Sys.Leak Stopped by Installing Pipe Clamp.Permanent Repairs Will Be Made Prior to Startup | 18 June 1986 | PNO-I-86-043:on 860618,unplanned Shutdown Commenced Due to Leak in Emergency Svc Water Sys.Leak Stopped by Installing Pipe Clamp.Permanent Repairs Will Be Made Prior to Startup | |
PNO-I-86-053, on 860719,scram Occurred When Reactor Pressure Spike Caused High Neutron Flux Signal.Caused by MSIV Closure During Offsite Power Trip Resulting in Loss of Emergency Power.Util Will Repair Failed Dc Coil on MSIV | 21 July 1986 | PNO-I-86-053:on 860719,scram Occurred When Reactor Pressure Spike Caused High Neutron Flux Signal.Caused by MSIV Closure During Offsite Power Trip Resulting in Loss of Emergency Power.Util Will Repair Failed Dc Coil on MSIV | |
PNO-I-86-080, on 860929,licensee Commenced Shutdown Upon Discovering Water Leakage Into Main Turbine Electrohydraulic Control Oil Sys.Return to Svc Not Expected for Approx 5 Days Following Determination of Source of Leakage | 30 September 1986 | PNO-I-86-080:on 860929,licensee Commenced Shutdown Upon Discovering Water Leakage Into Main Turbine Electrohydraulic Control Oil Sys.Return to Svc Not Expected for Approx 5 Days Following Determination of Source of Leakage | |
PNO-I-86-083, on 861015,licensee Manually Scrammed Unit & Placed in Cold Shutdown for Condensate Pump Repairs.Damaged Thrust Bearing Will Be Repaired & Pump Will Be Returned to Svc on 861019.Startup Planned on 861019 | 17 October 1986 | PNO-I-86-083:on 861015,licensee Manually Scrammed Unit & Placed in Cold Shutdown for Condensate Pump Repairs.Damaged Thrust Bearing Will Be Repaired & Pump Will Be Returned to Svc on 861019.Startup Planned on 861019 | |
PNO-I-87-001, on 870102,licensee Notified Region I Ofc of Unplanned Shut Down to Repair Steam Leak on High Pressure Turbine Inlet Flange.Facility Expected to Be Shut Down for Approx 4 Days | 2 January 1987 | PNO-I-87-001:on 870102,licensee Notified Region I Ofc of Unplanned Shut Down to Repair Steam Leak on High Pressure Turbine Inlet Flange.Facility Expected to Be Shut Down for Approx 4 Days | |
PNO-I-87-015, on 870304,smoke Reported in Turbine Bldg.Fire Found in Maint Cage in Turbine Bldg Fan Room.Fire Extinguished.Caused by Small Electrical Fan Suspended from Cage | 5 March 1987 | PNO-I-87-015:on 870304,smoke Reported in Turbine Bldg.Fire Found in Maint Cage in Turbine Bldg Fan Room.Fire Extinguished.Caused by Small Electrical Fan Suspended from Cage | |
PNO-I-87-018, on 870305,unit Shut Down Due to Hydrogen Leak from Main Generator.Leak Testing of Generator Identified Several Small & One Large Leak from Hydrogen Control & Analyzer Cabinet.Repairs to Generator & RHR HX in Progress | 9 March 1987 | PNO-I-87-018:on 870305,unit Shut Down Due to Hydrogen Leak from Main Generator.Leak Testing of Generator Identified Several Small & One Large Leak from Hydrogen Control & Analyzer Cabinet.Repairs to Generator & RHR HX in Progress | |
PNO-I-87-022, on 870317,hi-hi APRM Flux Scram & Group II & III Primary Containment Isolations Occurred.Caused by Electrohydraulic Control Sys Fluctuations.Unit in Cold Shutdown.Isolations Reset | 18 March 1987 | PNO-I-87-022:on 870317,hi-hi APRM Flux Scram & Group II & III Primary Containment Isolations Occurred.Caused by Electrohydraulic Control Sys Fluctuations.Unit in Cold Shutdown.Isolations Reset | |
PNO-I-87-024, on 870325,unit Auto Scrammed on Low Reactor Water Level When Engineer Lifted Electrohydraulic Control Lead Causing Bypass Valves to Open.Reactor Feed Pump Restarted.Water Level Recovered | 25 March 1987 | PNO-I-87-024:on 870325,unit Auto Scrammed on Low Reactor Water Level When Engineer Lifted Electrohydraulic Control Lead Causing Bypass Valves to Open.Reactor Feed Pump Restarted.Water Level Recovered |