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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20217D8361999-10-11011 October 1999 Provides NRC with Summary of Activities at TMI-2 During 3rd Quarter of 1999 ML20217F8271999-10-0707 October 1999 Forwards Pmpr 99-13, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990828- 0924.Diskette Containing Pmpr in Wordperfect 8 Is Encl. All Variances Are Expressed with Regard to Current Plans ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20216J6581999-09-28028 September 1999 Provides Info as Requested of Licensees by NRC in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A2101999-09-13013 September 1999 Forwards Rev 3 of Gpu Nuclear Post-Defueling Monitored Storage QAP for Three Mile Island Unit 2, Including Changes Made During 1998.Description of Changes Provided on Page 2 ML20216G4151999-09-0909 September 1999 Forwards Pmpr 99-12, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting Period 990731- 0827.All Variances Expressed with Regard to Current Operations Plans ML20211M5861999-09-0202 September 1999 Forwards non-proprietary & Proprietary Response to NRC 990708 RAI Re TS Change Request 272,reactor Coolant Sys Coolant Activity.Proprietary Encl Withheld ML20211M6591999-09-0101 September 1999 Forwards Errata Page to 990729 Suppl to TS Change Request 274,to Reflect Proposed Changes Requested by . Page Transmitted by Submitted in Error ML20211L2401999-09-0101 September 1999 Submits Response to NRC AL 99-02, Operator Reactor Licensing Action Estimates ML20211H3731999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI LAR 285 & TMI-2 LAR 77 Re Changes Reflecting Storage of TMI-1 Radioactive Matls in TMI-2 Facility.Revised License Page mark-up,incorporating Response,Encl ML20211H4001999-08-27027 August 1999 Responds to NRC 990810 RAI Re TMI-1 LAR 285 & TMI-2 LAR 77 Re Changes to Clarify Authority to Possess Radioactive Matls Without Unit Distinction.Revised License Page mark-up, Incorporating Response Encl ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211H5041999-08-20020 August 1999 Forwards Proprietary & non-proprietary Rept MPR-1820,rev 1, TMI Nuclear Generating Station OTSG Kinetic Expansion Insp Criteria Analysis. Affidavit Encl.Proprietary Rept Wihheld 05000289/LER-1999-007, Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface1999-08-20020 August 1999 Forwards LER 99-007-01 Re Increasing Failure Rate of ESAS Relays.Rept Supplements Preliminary Info Re Determination of Root Cause & Long Term Corrective Actions.Changes Made for Supplement Are Indicated in Bold Typeface ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20211H3571999-08-19019 August 1999 Forwards Itemized Response to NRC 990712 RAI Re TS Change Request 248 Re Remote Shutdown Sys,Submitted on 981019 ML20211A3931999-08-12012 August 1999 Requests NRC Concurrence with Ongoing Analytical Approach as Described in Attachment,Which Is Being Utilized by Gpu Nuclear to Support Detailed License Amend Request to Revise Design Basis for TMI-1 Pressurizer Supports ML20210R4691999-08-11011 August 1999 Forwards Update 3 to Post-Defueling Monitored Storage SAR, for TMI-2.Update 3 Revises SAR to Reflect Current Plant Configuration & Includes Minor Editorial Changes & Corrections.Revised Pages on List of Effective Pages ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210L3831999-07-30030 July 1999 Responds to NRC 990617 RAI Re OTSG Kinetic Expansion Region Insp Acceptance Criteria That Was Used for Dispositioning Indications During Cycle 12 Refueling (12R) Outage ML20210K7371999-07-30030 July 1999 Forwards Rev 2 to 86-5002073-02, Summary Rept for Bwog 20% Tp LOCA, Which Corrects Evaluation Model for Mk-B9 non- Mixing Vane Grid Previously Reported in Util to Nrc,Per 10CFR50.46 ML20210L1151999-07-28028 July 1999 Confirms Two Senior Management Changes Made within Amergen Energy Co,Per Proposed License Transfer & Conforming Administrative License Amends for TMI-1 05000289/LER-1999-009, Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section1999-07-22022 July 1999 Forwards LER 99-009-00 Re 990626 Event Involving Partial Loss of Offsite Power & Subsequent Automatic Start of EDG 1A.Commitments Made by Util Are Contained in long-term Corrective Actions Section ML20216D4001999-07-22022 July 1999 Provides Summary of Activities at TMI-2 During 2nd Quarter of 1999 ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20210G9471999-07-15015 July 1999 Forwards Pmpr 99-10, CNWRA Program Manager Periodic Rept on Activities of CNWRA, for Fiscal Reporting period,990605- 0702.Diskette Containing Pmpr in Wordperfect 8 Format Is Also Encl ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20212K1701999-07-13013 July 1999 Submits Concerns Re Millstone & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Should Provide Adequate Emergency Planning in Case of Radiological Accident ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days 05000289/LER-1999-008, Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public1999-07-0202 July 1999 Forwards LER 99-008-00 Re Discovery of Degraded But Operable Condition of RB Emergency Cooling Sys.Condition Did Not Adversely Affect Health & Safety of Public ML20196J3981999-07-0101 July 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Npps. Y2K Readiness Disclosure for TMI-1 Encl ML20209C1131999-07-0101 July 1999 Forwards Signed Agreement as Proposed in NRC Requesting Gpu Nuclear Consent in Incorporate TMI-1 Thermo Lag Fire Barrier Final Corrective Action Completion Schedule Commitment of 000630 Into Co Modifying License 1999-09-09
[Table view] Category:NRC TO PUBLIC ENTITY/CITIZEN/ORGANIZATION/MEDIA
MONTHYEARML20056A3691990-07-30030 July 1990 Discusses Office of Investigations Rept 1-87-008 Re Observation of Sleeping or Appearance of Sleeping on Duty & Forwards Notice of Violation ML20055F4161990-07-0909 July 1990 Final Response to FOIA Request.App a Record Encl & Available in PDR ML20247E0681989-07-20020 July 1989 Forwards Board Decision Approving Method for Disposing of accident-generated Water at Plant,Per Recipient Petition. Appeal of Decision Presently Before Appeal Board.W/O Encl. Related Correspondence NUREG-0557, Final Response to FOIA Request.Records Available Through Gpo1989-06-26026 June 1989 Final Response to FOIA Request.Records Available Through Gpo ML20245E9571989-06-26026 June 1989 Final Response to FOIA Request.Records Available Through Gpo ML20245G0301989-06-22022 June 1989 Responds to Re Offsite Radiation Monitoring & Emergency Warning Sys in Vicinity of TMI-2.NRC Opinion That Existing Real Time Monitoring Sys Will Remain Operational for at Least Next Several Yrs Expressed ML20246M2231989-05-0808 May 1989 Responds to Raising Concerns Re Actuation of Emergency Warning Signal in York,Pa on 890317.Emergency Brochure Issued to All Local Residents Adequate.Actuation Was Isolated Malfunction of One Signal ML20235N1981989-02-23023 February 1989 Final Response to FOIA Request for Records.Forwards Document Listed in App A.App a Document Available in PDR ML20206D9201988-11-0909 November 1988 Responds to Re NRC 880331 Response to Questions Raised Concerning Conditions at Plants & Recipient Proposal to Station Senior Operator in Control Room at All Nuclear Plants to Oversee Plant Operations ML20195G2121988-11-0808 November 1988 Final Response to FOIA Request for Documents.Forwards App D Document & Releasable Portions of Documents E/1 Through E/3. App D & Releasable Portions of Documents E/4 Through E/6 Available in Pdr.Portions Withheld (Ref FOIA Exemption 5) ML20154L0711988-09-20020 September 1988 Provides Response to TMI Alert,Inc/Susquehanna Valley Alliance Interrogatory 31(ii) Re NRC Experience &/Or Tests Performed on Moisture Separators & Vapor Superheaters. Related Correspondence ML20207E8801988-08-0303 August 1988 Forwards Programmatic EIS for TMI-2 & Suppls 2 & 3.W/o Encls ML20195E8821988-06-15015 June 1988 Third Partial Response to FOIA Request for Documents.App C, E,F & G Documents Encl & Available in Pdr.App D Documents Available in Pdr.Portions of Records Subj to Request Withheld (Ref FOIA Exemptions 4,5,6 & 7) ML20195F8041988-06-15015 June 1988 First Partial Response to FOIA Request for Documents. Forwards Apps B & C Documents.Documents Available in Pdr.App a Documents Also Available in Pdr.Apps D Through G Documents Withheld (Ref FOIA Exemption 5).Releasable Portion Encl ML20151M6061988-04-19019 April 1988 Responds to FOIA Request for Info Re Scores of Reactor Operators & Senior Reactor Operators.Forwards Requalification Exam Summary Source Sheets Listed in Encl App W/Personal Privacy Info Deleted ML20149G0731988-02-10010 February 1988 Responds to Re Announced Reorganization of NRC at TMI-2.NRC Personnel Stationed at Site,Region I & NRC Headquaters Will Continue to Provide Effective Regulatory Oversight of Cleanup Activities ML20147E2561988-01-15015 January 1988 Partial Response to FOIA Request for Documents Re Environ Qualification at Facility.Forwards Documents Listed in App C.Documents Also Available in PDR ML20149E9901988-01-11011 January 1988 Partial Response to FOIA Request Re MOU Between NRC & Dept of Labor.Forwards App B Documents.Apps a & B Documents Available in Pdr.App C Documents Totally Withheld (Ref FOIA Exemption 5) ML20147D4821988-01-0606 January 1988 Partial Response to FOIA Request for Documents.Forwards App B Documents.Documents Also Available in Pdr.Portions of App B Documents Withheld (Ref FOIA Exemptions 6 & 7) ML20237C5961987-12-17017 December 1987 Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl IA-87-834, Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl1987-12-17017 December 1987 Final Response to FOIA Request for Documents Re Plant. Article from NRC 1979 Annual Rept & Listing of NUREG Repts Re Plant Encl.Nureg Repts May Be Purchased from Pdr.All Encls Available in Pdr.W/O Encl ML20235V1381987-10-13013 October 1987 Final Response to FOIA Request for Records.App a Document, Consisting of Dj Collins 870721 Memo to Wd Travers Re Testing of Processed Water Encl & Available in PDR ML20235R8521987-09-30030 September 1987 Responds to Re EIS for Meltdown of Large Reactors & NRC Compliance W/Nepa.As Result of TMI-2 Accident on 790329,NRC Included Class 9 Accidents in Assessments in Fes Re Licensing of Plants.Related Info Encl ML20216D4921987-06-22022 June 1987 Responds to 870610 Motion Requesting That ASLB Reconsider 870521 Decision Re Leak Rate Falsification at Plant. Comments Re Decision Should Be Sent to NRC Staff.Served on 870623 ML20214S0691987-06-0202 June 1987 Forwards Rd Parks Notice of Deposition.Deposition Period of 870622-24 Confirmed.Certificate of Svc Encl.Related Correspondence ML20209H0531987-04-29029 April 1987 Partial Response to FOIA Request for Documents Re INPO Accreditation of Training Programs.Forwards App B Document. Document Also Available in PDR ML20206U0981987-04-20020 April 1987 Forwards Transcript of Recipient 870409 Deposition,For Review.Any Corrections Should Be Made in Tabular Format as Indicated on Encl Sheet.W/O Transcript.Related Correspondence ML20206T6591987-04-20020 April 1987 Forwards Transcript of Recipient 870410 Deposition,For Review.Any Corrections Should Be Made in Tabular Format as Indicated on Attached Sheet.W/O Transcript.Related Correspondence DD-87-03, Advises That Time for Commission to Review Director'S Decision DD-87-03 Expired on 870331.Commission Declined Review.Served on 8704031987-04-0202 April 1987 Advises That Time for Commission to Review Director'S Decision DD-87-03 Expired on 870331.Commission Declined Review.Served on 870403 ML20205A3211987-03-24024 March 1987 Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR IA-87-163, Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR1987-03-24024 March 1987 Final Response to FOIA Request for IE Inspectors Failure to Rept Info Re 790328 Hydrogen Explosion at TMI-2. App a Document Available in PDR ML20212K5181987-03-0606 March 1987 Forwards Director'S Decision 87-03 Denying Remaining Portion of 830323 Petition to Halt All Work Based on Rd Parks Allegations & Fr Notice.Portion of Petition Re Polar Crane Load Test Previously Denied in Director'S Decision 83-18 ML20213A0101987-01-29029 January 1987 Final Response to FOIA Request for Documents Re Plant. Forwards App G Document.Documents Also Available in PDR ML20212R6291987-01-27027 January 1987 Forwards Transcript of 870113 Deposition.Review & Signature Requested.W/O Encl.Related Correspondence NUREG-1019, Forwards Response to 860915 & 30 Questions Re Steam Generator Tube Rupture & Turbine Bypass Valve1987-01-13013 January 1987 Forwards Response to 860915 & 30 Questions Re Steam Generator Tube Rupture & Turbine Bypass Valve ML20211Q7551986-12-18018 December 1986 Final Response to FOIA Request for Insp Rept 50-289/86-14 on 860825-0905.App a Document Available in PDR ML20214P4751986-11-26026 November 1986 Responds to 860919 Request That Filter Be Installed on Condenser Offgas Sys Line at TMI-1 to Reduce Possible Radioactive Releases to Environ.Nrc Does Not Believe Placing Filter on Sys Will Provide Measurable Improvement in Safety ML20214A6351986-11-14014 November 1986 Forwards Three Draft Documents to Be Discussed at 861117 Meeting in Buena Park,Ca.W/O Encls.Related Correspondence ML20215H9741986-10-22022 October 1986 Requests to Be Contacted to Arrange Appearance as Witness in Commission Inquiry Into Leak Rate Data Falsifications at Facilities in 1978-1979,per 860806 Subpoena.Served on 861023 ML20215L1871986-10-0909 October 1986 Responds to Appeal Re Denial of FOIA Request for Three Categories of Records Concerning Equipment Qualification at Facility.Forwards Documents 14-16 Listed on App.Documents 1- 13,17 & 20-22 Withheld (Ref FOIA Exemption 5) ML20210U4431986-10-0202 October 1986 Forwards Info Requested at 860923 SALP I Meeting,Including Clarification of Apps Listed in Table in Ref to 10CFR50 & Listing of Subjs of Amends 111-117 to License DPR-50 ML20214Q1991986-09-19019 September 1986 Forwards Response to 860616 & 0710 Ltrs Re Tube Failure in once-through Steam Generator on Reinjection of Emergency Feedwater During TMI-2 Accident Possibly Causing Primary to Secondary Leaks & Large Release of Iodine ML20212P6521986-08-29029 August 1986 Confirms 860828 Telcon Re Agreement to Appear as Witness in Commission Inquiry Into Leak Rate Data Falsifications at TMI-2.Recipient Interviews & Statement Encl.W/O Encls. Served on 860902 ML20203L6971986-08-27027 August 1986 Forwards Subpoena Requiring Appearance at Sept 1986 Hearing Re TMI-2 Leak Rate Falsification.Served on 860828 ML20205C5931986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served on 860811 ML20205C6281986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served on 860811 ML20205C6471986-08-0808 August 1986 Requests Return of Page 3 of Encl 2 to NRC Rept, Results of NRR Investigation & Evaluation of 10 Licensed Operators Involved in TMI-2 Preaccident Leak Rate Testing Irregularities. Served in Aug 1986 ML20205C5511986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Hearings in Sept 1986 Re Leak Rate Test Data Falsifications During 1978 & 1979.W/o Encl.Served on 860811 ML20205C6321986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Hearings in Sept 1986 Re Leak Rate Test Data Falsifications During 1978 & 1979.W/o Encl.Served on 860811 ML20205C4371986-08-0707 August 1986 Forwards Subpoena Requiring Appearance as Witness at Sept 1986 Hearing Re Responsibility for Leak Rate Test Data Falsifications at Facility in 1978-79.Estimated Date of Testimony Is 860930.W/o Encl.Served on 860811 1990-07-09
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217M0721999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Pass Dates ML20212J9991999-10-0101 October 1999 Responds to Recent Ltr to President Clinton,H Clinton, Chairman Jackson &/Or Wd Travers Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performance of Plant to Ensure That Public Health & Safety Adequately Protected ML20212L0061999-10-0101 October 1999 Discusses GL 97-06 Issued by NRC on 971231 & Gpu Response for Three Mile Island .Staff Reviewed Response & Found No New Concerns with Condition of SG Internals or with Insp Practices Used to Detect Degradation of SG Internals ML20212L1831999-10-0101 October 1999 Responds to Recent Ltr to Wd Travers Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Performance of Millstone to Ensure Adequate Protection to Public Health ML20212L2081999-10-0101 October 1999 Responds to Recent Ltrs to President Wj Clinton,Chairman Jackson & Commissioners & Wd Travers,Expressing Concerns Re Millstone NPPs & Continued Lack of Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance ML20212K1241999-10-0101 October 1999 Responds to Recent Ltrs to Chairman Jackson,Commissioners & Wd Travers,Expressing Concern Re Millstone Npps.Nrc Continues to Monitor Performace of Millstone to Ensure That Public Health & Safety,Adequately Protected ML20212L2171999-10-0101 October 1999 Responds to Recent Ltr to President Wj Clinton,Chairman Jackson & Commissioners,Wd Travers & Ferc,Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island ML20212L1971999-10-0101 October 1999 Responds to Recent Ltr to Chairman Jackson & Commissioners Expressing Concerns Re Millstone NPPs & Continued Lack of Emergency Mgt Plan for Eastern Long Island.Nrc Continues to Monitor Plant Performance to Ensure Public Health & Safety ML20212K8771999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Three Mile Island on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Provides Historical Listing of Plant Issues & Insp Schedule ML20212K8551999-09-30030 September 1999 Informs That During 990921 Telcon Between P Bissett & F Kacinko,Arrangements Were Made for Administration of Licensing Exams at Facility During Wk of 000214.Outlines Should Be Provided to NRC by 991122 ML20212J0011999-09-27027 September 1999 Forwards Insp Rept 50-289/99-07 on 990828.No Violations Noted ML20211A4261999-08-19019 August 1999 Forwards Insp Rept 50-289/99-04 on 990606-0717.Two Severity Level 4 Violations Occurred & Being Treated as Noncited Violations ML20210N7601999-08-10010 August 1999 Informs That NRC Staff Reviewed Applications Dtd 990629, Which Requested Review & Approval to Allow Authority to Possess Radioactive Matl Without Unit Distinction Between Units 1 & 2.Forwards RAI Re License Amend Request 285 ML20210N7191999-08-0606 August 1999 Forwards Notice of Partial Denial of Amend to FOL & Opportunity for Hearing Re Proposed Change to TS 3.1.12.3 to Add LCO That Would Allow Continued HPI Operation ML20210B8231999-07-21021 July 1999 Forwards Exemption from Certain Requirements of 10CFR50.54(w) for Three Mile Island Nuclear Station,Unit 2 in Response to Licensee Application Dtd 990309,requesting Reduction in Amount of Insurance for Unit to Amount Listed ML20209H9401999-07-15015 July 1999 Forwards Copy of Environ Assessment & Findings of No Significant Impact Re Application for Exemption Dtd 990309. Proposed Exemption Would Reduce Amount of Insurance for Onsite Property Damage Coverage as Listed ML20209G2451999-07-15015 July 1999 Advises That Suppl Info in Support of Proposed License Transfer & Conforming Adminstrative License Amends,Submitted in & Affidavit,Marked Proprietary,Will Be Withheld from Public Disclosure,Per 10CFR2.790(b)(5) ML20216D9861999-07-12012 July 1999 Forwards RAI Re 981019 Application Request for Review & Approval of Operability & SRs for Remote Shutdown Sys. Response Requested within 30 Days of Receipt of Ltr ML20209F2571999-07-0909 July 1999 Forwards Staff Evaluation Rept of Individual Plant Exam of External Events Submittal on Three Mile Nuclear Station, Unit 1 ML20209G5861999-07-0909 July 1999 Forwards Insp Rept 50-289/99-05 on 990510-28.No Violations Noted ML20209D8451999-07-0808 July 1999 Forwards Insp Rept 50-289/99-06 on 990608-11.No Violations Noted.Overall Performance of ERO Very Good & Demonstrated, with Reasonable Assurance,That Onsite Emergency Plans Adequate & That Util Capable of Implementing Plan ML20209D6291999-07-0808 July 1999 Forwards Notice of Withdrawal & Corrected TS Pages 3-21 & 4-9 for Amend 211 & 4-5a,4-38 & 6-3 for Amend 212,which Was Issued in Error.Amends Failed to Reflect Previously Changes Granted by Amends 203 & 204 ML20209D5141999-07-0808 July 1999 Forwards RAI Re 981019 Application & Suppl ,which Requested Review & Approval of Revised Rc Allowable Dose Equivalent I-131 Activity Limit with Max Dose Equivalent Limit of 1.0 Uci/Gram.Response Requested within 30 Days ML20196J5631999-07-0101 July 1999 Informs That Util 981203 Joint Application with Amergen Energy Co Marked Proprietary Will Be Withheld from Public Disclosure Pursuant to 10CFR2.790(b)(5) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20196J5741999-06-30030 June 1999 Informs That as Result of Staff Review of Util Response to GL 92-01,rev 1,suppl 1,info Provided in Support of PT Limits License Amend & B&W Topical Rept,Staff Revised Info for Plant,Unit 1,in Reactor Vessel Integrity Database ML20196H6811999-06-29029 June 1999 Forwards Insp Rept 50-289/99-03 on 990425-0605.No Violations Noted.However,Adequacy of Assessment of Reactor Bldg Emergency Cooler Operability Prior to Conducting Maintenance on One Reactor Bldg Spray Sys,Questionable ML20212H8711999-06-21021 June 1999 Discusses Updated Schedule Commitment Submitted by Gpu on 990602 for Implementing Thermo-Lag 330-1 Fire Barrier C/As & Completion of Thermo-Lag Effort at TMI-1.Informs NRC Will Incorporate Commitment Into Co Modifying License ML20195K2821999-06-17017 June 1999 Forwards Request for Addl Info Re Kinetic Expansion Region Inspection Acceptance Criteria ML20212H6621999-06-0404 June 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Ss Bajwa Will Be Section Chief for Three Mile Island Nuclear Station ML20207E7201999-05-27027 May 1999 Discusses Reorganization of Nrr,Effective 990328. Organization Chart Encl ML20207B6541999-05-27027 May 1999 Forwards SER Accepting Util Program to Periodically Verify design-basis Capability of safety-related MOV at TMI-1 & That Util Adequately Addressed Actions Requested in GL 96-05 ML20207C0321999-05-18018 May 1999 Forwards Fifth Rept Which Covers Month of Apr 1999. Commission Approved Transfer of TMI-1 Operating License from Gpu to Amergen & Transfer of Operating License for Pilgrim Station from Beco to Entergy Nuclear Generating Co ML20206S3411999-05-14014 May 1999 Forwards Insp Rept 50-289/99-02 on 990314-0424.Violations Occurred & Being Treated as non-cited Violations.Security Program Was Inspected During Period & Found to Be Effective ML20206N5831999-05-13013 May 1999 Requests Description of Proposed Corrective Actions for Fire Zones AB-FZ-3,AB-FZ-5,AB-FZ-7,FH-FZ-2,CB-FA-1 & FH-FZ-6. Confirmation That Corrective Actions & Commitments Made Will Be Completed by 991231,requested IR 05000298/19980091999-05-12012 May 1999 Refers to Insp Rept 50-298/98-09 Conducted Between 981227-990130.During Insp,Apparent Violation of 10CFR50.50 Identified & Being Treated as non-cited ML20206H3571999-05-0606 May 1999 Forwards RAI Re 981203 Application & Suppls & 0416,requesting Review & Approval of Revised Core Protection SL & Bases for TMI-1 to Reflect Average of 20% of Tubes Plugged Per Sg.Response Requested within 10 Days of Receipt ML20207A5401999-04-29029 April 1999 Informs That Licensee 980930 Response to GL 96-06,appears to Be Reasonable & Appropriate for Specific Design & Configuration of RB Emergency Cooling at Plant,Unit 1 & That Staff Satisfied with Licensee Resolution of Waterhammer ML20206D4001999-04-20020 April 1999 Informs of Completion of Review of Gpu Request for Exemption Submitted on 961231,970908,971230,980521,981014,981125 & 981223 from Requirements of 10CFR50,App R,Section III.G.2 for TMI Unit 1.Forwards Exemption & Safety Evaluation ML20205S6791999-04-16016 April 1999 Forwards Insp Rept 50-289/99-01 on 990131-0313.No Violations Noted.Identification by Licensee Staff of Elevated Tritium Activity in Monitoring Well Led to Investigation & Identification of Leak from Buried Radwaste Path ML20205P3391999-04-0909 April 1999 Discusses Results of Plant Performance Review for Three Mile Island Completed on 990225.Historical Listing of Plant Issues That Were Considered During PPR Encl IR 05000289/19980061999-03-26026 March 1999 Ack Receipt of 981112 & s Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-289/98-06 .Action Does Not Change NRC Determination That Change to Hpis Valve Configuration Involved URI ML20204E3911999-03-17017 March 1999 Informs That Region I Plans to Conduct Open Predecisional Enforcement Conference to Discuss Apparent Violations Re Efs Issues as Described in Insp Rept 50-289/98-09,per ML20204B6771999-03-15015 March 1999 Submits Withdrawal of Amend Request for Operating License DPR-46.Proposed Change Would Have Modified Facility TSs Pertaining to Neutron Monitoring Neutron Detectors ML20207H7391999-03-0505 March 1999 Forwards Insp Rept 50-289/98-09 on 981227-990130.Two Apparent Violations Being Considered for Enforcement Action.First Violation Deals with Failure to Follow Procedures for Control of Emergency Boration Source ML20203F4911999-02-0505 February 1999 Forwards Request for Addl Info Re Licensee 981125 Amend Application Re TS Change Request 277 for OTSG Inservice Insp During 13R for Three Mile Island,Unit 1 ML20202H6771999-02-0303 February 1999 Documents Basis for NRC Staff Generic Approval of Requests to Relocate TS Requirements from Tss.Staff Generic SER Finding Relative to Relocated TS Requirements Encl ML20196K3511999-01-22022 January 1999 Refers to Gpu Responses to Second NRC RAI Re GL 92-08 & Review of Gpu Analytical Approach for Ampacity Derating Determinations.Forwards SE & SNL Technical Ltr Rept Concluding That No Outstanding Safety Concerns Identified ML20199H6471999-01-20020 January 1999 Forwards RAI Re Gpu TS Change Request 277 OTSG Cycle 13 for Plant Unit 1.NRC Has Determined That Addl Info Needed to Complete Review ML20199G7401999-01-12012 January 1999 Forwards Insp Rept 50-289/98-08 on 981101-1226.No Violations Noted.Operator Workaround Program Found to Be Acceptable ML20206S0221999-01-0808 January 1999 Responds to Re Changes to Physical Security Plan Identified as Rev 38,submitted Under Provisions of 10CFR50.54(p).Based on NRC Determination,Changes Do Not Decrease Overall Effectiveness of Security Plan 1999-09-30
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-Q sg SEP 101986 Docket No. 50-289 Ms. Deborah Davenport 1802 Market Street Camp Hill, Pennsylvania 17011
Dear Ms. Davenport:
This is in response to your letters, dated June 16 and July 10, 1986, to R. Conte of my staff and to me. We answered your questions verbally at a meeting with you and Mr. Eric Epstein in Middletown, Pennsylvania, on August' 27, 1986. As you agreed at the end of that meeting, the meeting was beneficial in clarifying many of the questions you had in your letters.
We have summarized our responses to your letters in the attachment. The docu-ments referenced in the attachment were provided to you separately at the meeting.
Thank you for your interest in our activities.
Sincerely, Original Sisacd By[
Alle.n R. Blough, Chief Reactor Projects Section 1A Division of Reactor Projects
Attachment:
As Stated cc: PDR LPDR Senior Resident Inspector bcc: R. Jones, NRR:PBRS J. Thoma, NRR:PBD6 y
h RI:DRP 9 RI:DRP I: RS M RConte/cpn A81ough HKister 9//6/86 9//6/86 9//[/86 0FFICIAL RECORD COPY LTR DEBRA DAVENPORT - 0001.0.0 09/11/86 .rcoi I
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a 4-ATTACHMENT RESPONSES TO D. DAVENPORT LETTERS Letter dated June 16, 1986 Re: B&W Trial Record, B&W Exhibit 407, Kunder Exhibit
- 1. The reference describes tube failure in Once-Through Steam Generator (OTSG)
.on re-injection of EFW during TMI-2 accident possibly causing primary to secondary leaks and large release of iodine. What are 1979 and current definitions of tube . failure (size of leak, amoun't of contaminants in such leak)?
Response
There has been no change in the tube rupture definition since 1979. The TMI-1 Safety Analysis Report (SAR) Section 14.1.2.10 (provided separately) assumes a tube rupture to be the double ended break of one tube for ac-cident analysis purposes. However, to provide reasonable assurance of continued integrity of the OTSG tubes, the licensee is required by Techni-cal Specifications (TS) 4.19 (provided separately).to perform in-service testing (IST) of OTSG tubes primarily using the eddy current techniques (ECT). Section 4.19.4 of TS defines various official terminology as to the status of an OTSG tube from ECT data results. It should be noted that the TS is oriented toward detecting degradation before an actual break.
It is unlikely that a tube break would occur before leak detection; it is even more unlikely that there would be multiple tube failures.
To complement the IST on OTSG tubes, certain operational limits are imposed by TS 3.1.4 and 3.1.6 to assure the licensee stays within the bounds or assumptions of the SAR. TS 3.1.4 limits the amount of radioactivity in the Reactor Coolant System (RCS) to assure that 10 CFR 100 limits are not exceeded. It is recognized that releases will occur on a tube rupture via either the atmospheric dump valves or the steam generator cafety valves such as was experienced in the Ginna event. Further, TS 3.1.6 limits the amount of primary to secondary leakage (1 gpm), which is an assumption for the design basis tube rupture event. Excerpts on these applicable TS were provided separately.
The 10 CFR 100 is NRC regulations providing nuclear power plant siting criteria to assure the dose to the public at the site boundary is within limits.
- 2. OTSG's need more water to operate effectively. TS address dry steam gen-erator situations during an accident / transient and in reference to tube thermal shock, can feedwater always be adequately regulated in flow and thus temr9rature?
I
O i 2
Response
Your statement that the OTSG needs more water to operate needs clarifica-tion. It appears you reached this understanding from discussions with the NRC staff. The amount of secondary plant water flow (feedwater or main steam flow) is determined by the design power at which the main turbine generator is designated to operate. During steady-state full power condition, the amount of water (steam and liquid) in a B&W OTSG is less than that of the other vendor type because it is of a relatively smaller size for that size generation capacity. For a main steam line break, this is somewhat beneficial because the lesser water inventory in the OTSG results in a less severe temperature transient (cooldown) on the primary system. These types of events are rare. On the other hand, for a loss of feedwater transient, there is a more noticeable effect on primary temperatures. The loss of feedwater events are more frequent and this is part of the reason the B&W reassessment is occurring.
For TMI-1 since restart, there have not been significant feedwater regula-ting problems in controlling OTSG 1evel. There have been no events in which a loss of feedwater caused the automatic initiation of emergency feedwater. The licensee has not been in a dry steam generator situation.
Please note, at TMI-1, the main feedwater and emergency feedwater systems are separate systems with separate injection points into the OTSG. Level control is being enhanced with the completion of additional modifications to the EFW system during the next refueling outage.
The licensee has detailed operating procedures to restore a dry steam generator to service, primarily to avoid a tube thermal shock situation.
There are no TS which specifically address dry steam generator situations.
- 3. Since there are EF and water use problems associated with B&W plants, would those factors affect OTSG integrity under certain conditions (e.g.,
on rapid injection of EFW would thermal shock be inevitable)?
Response
Thermal shock to the OTSG tube is a concern primarily when feeding a dry steam generator, which is a post-event recovery concern. Procedures have been written to alleviate this concern. The NRC staff, in the B&W reassessment, is focusing its attention on the initiation event, loss of feedwater and the resulting challenge to safety systems from the ensuing operational transient.
4 3
- 4. Wouldn't repeated . transients and feedwater problems increase the risk [of tube failure] particularly in a B&W plant?
Response
The repeated thermal cycles on the plant is one of many factors that is considered in the plant design regarding aging of a nuclear power plant and the resultant degradation of components. Consequently design and operational limits have been established to minimize the number of thermal cycles and to keep track of the cycles. Periodic ins'rvicee testing is also a key factor in monitoring for degradation of various components such as nozzles, OTSG tubes, etc. This permits replacement or repairs before actual failures of the component.
- 5. If a B&W OTSG has to use more water, wouldn't the problem with thermal shock be more likely to occur resulting in tube failure or other faults at B&W plants?
-Response The B&W OTSG use of water is addressed in question No. 2. The thermal shock concern is primarily when feeding a dry steam generator and is not unique to the B&W design. As with other reactor types and fossil fueled plants, the secondary plant is designed to heat feedwater to assure steam generating components are not thermally shocked or excessively stressed during steady-state power operation. Operation limits have been- esta-blished to assure the feedwater is sufficiently hot enough to enter the OTSG.
- 6. Because of numerous TMI-2 sequence of events, it appears that the "B" 0TSG 1eak at TMI-2 was never fully dealt with as of this date. Will Region I be looking at the steam generators at TMI-2 in reference to the B&W reassessment?
Response
Region I will not be considering the TMI-2 "B" 0TSG 1eakage in the B&W reassessment. The handling of a steam generator tube rupture event is being addressed by NRC staff under a separate multi plant action item.
At our 8/27/86 meeting we provided you an excerpt from the NRC's TMI-2 Accident Investigation Report. You will note confusion on the part of the operators early in the accident as to whether or not the shell of the "B" OTSG was leaking. The p'rimary to secondary leakage was never quantified and it was not the focal point of the numerous technical problems identi-fied in that report. Later licensee chemistry ^results of the "B" 0TSG secondary side water confirmed the presence of trace radioactive contami-nants, indicating that slight leakage occurred. The investigation report indicated that the secondary side of the "B" 0TSG was isolated. It has
I 4 essentially remained that way ever since. The NRC staff at TMI-2 reports that precautions have been taken by the licensee to assure any leakage will be in-leakage from the secondary side to the primary side of the "B" OTSG.
Any attempt by the licensee to restore the TMI-2 plant to service, along
~w ith its OTSG's, would have to be fully evaluated by NRC staff, which would have to include a review of the "B" 0TSG 1eakage problem.
- 7. Will Region I be looking at the concerns I raised in reference to the B&W reassessment?
Response
The Loss of Feedwater event as it relates to overall plant response and challenge to safety systems will be considered in the B&W Reassessment.
The OTSG tube rupture accident response procedures are being re-reviewed separately as a multi plant action item by the NRC staff. The lead office in the B&W reassessment is the Office of Nuclear Reactor Regulation (NRR).
Region I is in a supportive role.
Letter dated July 10, 1986, to R. Conte Re: B&W Trial Transcript - Hartman
- 1. In reference to OTSG safety valve problem, this was one of the biggest design deficiencies that cost the licensee millions of dollars for the job.
Response
It is our understanding that the TMI-2 safety valve problem (1978) was indeed a design deficiency with a valve designed by a specific vendor.
The current TMI-1 safety valve is from a different vendor and the problem noted during restart appears to be unrelated. For TMI-1, there appears to be a valve coordination problem on plant trips between turbine bypass valves, atmospheric dump valves, and safety valves with respect to their.
respective staggered lift settings from 1025 psig to 1100 psig. This issue is being reviewed in the B&W reassessment. In the interim, plant operators are aware of the problem and they can and have taken manual control of the turbine bypass valves to lower OTSG pressure to prevent the repeated lifting of the safety valves (re: NRC Inspection Report Item No.
50-289/85-25-05).
- 2. Reference is made to the . lack of automatic bypass in the condensate polishing system and design deficiency for condensate polishing isolation valves to fail close on loss of instrument air.
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I 5
Response
At TMI-1 there is an automatic bypass to the condensate polishing system.
The loss of condensate or feedwater is an analyzed event. Since the TMI-2 accident, improvements have been and will be made to detect the loss of main feedwater and automatically initiate emergency feedwater.
Letter dated July 10, 1986, to A. Blough
- 1. Are feedwater flow problems (in particular excessive FW with potential for OTSG tube rupture) being addressed by NRC (re: B&W reassessment)?
Response
See response to letter dated June 16, 1986, question No. 7.
- 2. Re: B&W Trial Record - Hartman Exhibit
" The reference describes TMI-2 condensate hotwell fill design problems resulting in a loss of vacuum, operation of the atmospheric dump (AD) valve, and subsequent failure of an operating bellows for the ADV.
Concern is expressed at TMI-1 on repetitive problems: (a) hotwell level operational problems; (b) recent 1986 bellows failures in TMI-1 main con-denser; and, (c) atmospheric dump operating with tube rupture at TMI-1.
(a) Since the restart, the licensee has not experienced significant problems on hotwell level control resulting in a loss of vacuum.
(b) The use of " bellows" in any industrial complex, including nuclear power plants, varies widely with all types of designs, material uses and' functions. The TMI-1 condenser bellows is a metallic expansion joint used for the extraction steam system which penetrates the con-denser. This is a different type bellows than a diaphragm arrangement frequently used with air operated valve operations applications (as was the apparent case for the TMI-2 event). These two events are not related.
(c) The operation of the atmospheric dump valve or safety valve during an OTSG tube rupture is an analyzed event (see response to letter, dated June 18, 1986, question No. 1).
- 3. Re: See No. 2 above.
Hartman described steam entering the TMI-2 control building because of an apparent ADV tailure. Concern was expressed on risk to workers and public due to steam release inside the plant along with (radwastes) contaminants. Has this been considered for TMI-1 operations?
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Response
As noted above, the OTSG tube rupture is an analyzed event, which assures not exceeding 10 CFR 100 limits. Likewise is the main steam line rupture event.
Procedures are in place to combat internal plant release with respect to
- worker protection. Although.unlikely, industrial accidents with the main steam system could occur in any plant using steam.
. Releases to the off-site boundary are governed by 10 CFR 20 and 100 requirements.
NRC staff Control Room Habitability review is near completion, with major licensee modifications and testing completed.
! 4. Have there been assessments of the potential for internal and external releases from TMI-1 in a situation involving steam tube leaks,or failures?
' Response l
4 These are covered by the design basis events described in Section 14 of the Safety Analysis Report. See also the response to question No. 3 above.
Telephone Call of July 30, 1986, to F. Young
- 1. Are there filters on the condenser offgas system?
Response
There are no filters on the condenser offgas system. The primary type of radioactive material passing this point is noble gas. Filters are effec-tive only for particulates and iodine type materials, not noble gas.
- 2. Are there problems with GPU measuring releases / recording releases?
Response
You apparently referred to a Licensee Event Report (LER) No. 86-04, dated March 27, 1986, in which the condenser offgas radiation monitor was inad-
- vertently valved out of service for one shift. There was backup instru-
. mentation available. The LER was reviewed in NRC Inspection Report Nos. 50-289/86-05 and 86-06.
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