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| {{#Wiki_filter:PR.IC)R.I"EY'CCELERATED RIDSPROCESSING) | | {{#Wiki_filter:P R.IC)R.I"EY'CCELERATED RIDS PROCESSING) |
| REGULATORY INFORMATION DISTRIBUTION SYSTEM(RIDS)ACCESSION NBR:9503270141 DOC.DATE: | | REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9503270141 DOC.DATE: 95/03/20 NOTARIZED: |
| 95/03/20NOTARIZED: | | NO DOCKET g FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E. |
| NODOCKETgFACIL:50-315 DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATION FITZPATRICK,E.
| | Indiana Michigan Power Co.(formerly Indiana 6 Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)P |
| IndianaMichiganPowerCo.(formerly Indiana6MichiganEleRECIP.NAME RECIPIENT AFFILIATION DocumentControlBranch(Document ControlDesk)P
| |
|
| |
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| ==SUBJECT:== | | ==SUBJECT:== |
| NPDESnoncompliance notification:on 950301,bypass discharge Ifromturbineroomsumpthroughemergency overflowpipingintointakeforebaytoLakeMichigan.
| | NPDES noncompliance notification:on 950301,bypass discharge I from turbine room sump through emergency over flow piping into intake forebay to Lake Michigan.DISTRIBUTION CODE: COOID COPIES RECEIVED:LTR (ENCL~SIZE: TITLE: Licensing Submittal: |
| DISTRIBUTION CODE:COOIDCOPIESRECEIVED:LTR (ENCL~SIZE:TITLE:Licensing Submittal: | | Environmental Rept Amdt 6 Related Correspondence NOTES RECIPIENT ID CODE/NAME PD3-1 PD INTERN~FILE CENTER 01 RGN3'RSS/RPB EXTERNAL LITCO'KERS i D NRC PDR COPIES LTTR E CL RECIPIENT ID CODE/NAME HICKMAN,J OGC/HDS2 NOAC COPIES LTTR ENCL 1 I D 0 C N NOTE TO ALL"RIDS" RECIPIENTS: |
| Environmental ReptAmdt6RelatedCorrespondence NOTESRECIPIENT IDCODE/NAME PD3-1PDINTERN~FILE CENTER01RGN3'RSS/RPBEXTERNALLITCO'KERSiDNRCPDRCOPIESLTTRECLRECIPIENT IDCODE/NAME HICKMAN,J OGC/HDS2NOACCOPIESLTTRENCL1ID0CNNOTETOALL"RIDS"RECIPIENTS: | | PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.504-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEEDI O TOTAL NUMBER OF COPIES REQUIRED: LTTR 8 ENCL h f I (' |
| PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPI-37(EXT.504-2083)TOELIMINATE YOURNAMEFROMDISTRIBUTION LISTSFORDOCUMENTS YOUDON'TNEEDIOTOTALNUMBEROFCOPIESREQUIRED:
| | indiana Michigan.,Power Company P.O.Box 16631 Columbus, OH 43216 March 20, 1995 AEP:NRC:1208H Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.20555 Gentlemen: |
| LTTR8ENCL hfI('
| | Donald C.Cook Nuclear Plant Units 1 and 2 TURBINE ROOM SUMP DISCHARGE This notification is forwarded for your information pursuant to Appendix"B" of the Donald C.Cook Nuclear Plant Environmental Technical Specifications. |
| indianaMichigan.,PowerCompanyP.O.Box16631Columbus, OH43216March20,1995AEP:NRC:1208H DocketNos.:50-31550-316U.S.NuclearRegulatory Commission ATTN:DocumentControlDeskWashington, D.C.20555Gentlemen:
| | The subject of this notification concerns a by-pass discharge on March 1, 1995, from the turbine room sump (TRS)through emergency over flow piping into the intake forebay to Lake Michigan.The cause of the discharge was due to a failure of the regulating valve (DRV-710)to open when signaled.The valve was eventually opened by defeating the air regulator to the valve and manually increasing the air pressure, forcing the valve to open.An action request has been initiated to repair DRV-710.Until DRV-710 is repaired, turbine room sump releases are being controlled by a manual isolation valve.The waters are sampled for pH and batch released via procedure 12-OHP 4021.062.001. |
| DonaldC.CookNuclearPlantUnits1and2TURBINEROOMSUMPDISCHARGE Thisnotification isforwarded foryourinformation pursuanttoAppendix"B"oftheDonaldC.CookNuclearPlantEnvironmental Technical Specifications.
| | The pH range of the TRS water during the inadvertent discharge to the lake was 8.5 to 9.0.Outfalls 001 and 002 were analyzed for pH and outfall observations were performed at 0830 on March 1, 1995.The pH for outfall 001 water was 8.2.An outfall observation of 1 was made, meaning that the water was free of any unusual characteristics of the discharge, i.e., unusual turbidity, color, oil film, floating solids, foams, settleable solids or deposits.The pH for outfall 002 was 7.9, and an outfall observation of 1 was also made.The maximum estimated flow to the intake forebay was 0.016 million gallons.Five of the plant's seven circulating water pumps were on at the time of the by-pass.As required by the Cook Nuclear Plant National Pollutant Discharge Elimination System (NPDES)Permit No.MI6005827, written 9503270141 950320 PDR ADOCK 05000315 S PDR |
| Thesubjectofthisnotification concernsaby-passdischarge onMarch1,1995,fromtheturbineroomsump(TRS)throughemergency overflowpipingintotheintakeforebaytoLakeMichigan.
| | ~U.S.Nuclear Regulatory Commission Page 2 AEP:NRC'1208H notification of this event was provided on March 2, 1995, to the Surface Water Quality Division of the Michigan Department of National Resources. |
| Thecauseofthedischarge wasduetoafailureoftheregulating valve(DRV-710) toopenwhensignaled.
| | This type of discharge is included in the proposed NPDES permit under outfall OOH.Should you have any questions or concerns regarding this notification, please contact Dane Mazzitti at (614)223-2085.Sincerely, E.E.Fitzpatrick Vice President pit cc: A.A.Blind G.Charnoff J.B.Martin NFEM Section Chief J.R.Padgett}} |
| Thevalvewaseventually openedbydefeating theairregulator tothevalveandmanuallyincreasing theairpressure, forcingthevalvetoopen.Anactionrequesthasbeeninitiated torepairDRV-710.UntilDRV-710isrepaired, turbineroomsumpreleasesarebeingcontrolled byamanualisolation valve.ThewatersaresampledforpHandbatchreleasedviaprocedure 12-OHP4021.062.001.
| |
| ThepHrangeoftheTRSwaterduringtheinadvertent discharge tothelakewas8.5to9.0.Outfalls001and002wereanalyzedforpHandoutfallobservations wereperformed at0830onMarch1,1995.ThepHforoutfall001waterwas8.2.Anoutfallobservation of1wasmade,meaningthatthewaterwasfreeofanyunusualcharacteristics ofthedischarge, i.e.,unusualturbidity, color,oilfilm,floatingsolids,foams,settleable solidsordeposits.
| |
| ThepHforoutfall002was7.9,andanoutfallobservation of1wasalsomade.Themaximumestimated flowtotheintakeforebaywas0.016milliongallons.Fiveoftheplant'ssevencirculating waterpumpswereonatthetimeoftheby-pass.AsrequiredbytheCookNuclearPlantNationalPollutant Discharge Elimination System(NPDES)PermitNo.MI6005827, written9503270141 950320PDRADOCK05000315SPDR
| |
| ~U.S.NuclearRegulatory Commission Page2AEP:NRC'1208H notification ofthiseventwasprovidedonMarch2,1995,totheSurfaceWaterQualityDivisionoftheMichiganDepartment ofNationalResources. | |
| Thistypeofdischarge isincludedintheproposedNPDESpermitunderoutfallOOH.Shouldyouhaveanyquestions orconcernsregarding thisnotification, pleasecontactDaneMazzittiat(614)223-2085.
| |
| Sincerely, E.E.Fitzpatrick VicePresident pitcc:A.A.BlindG.CharnoffJ.B.MartinNFEMSectionChiefJ.R.Padgett}} | |
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Category:NPDES NONCOMPLIANCE NOTIFICATION
MONTHYEARML17326A1191999-09-10010 September 1999 NPDES Noncompliance Notification:On 990909,unnatural Turbidity Was Observed at Cook Plant Outfall 001 & 002. Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Terminated Clay Feed ML17326A0431999-07-0909 July 1999 NPDES Noncompliance Notification:On 990707,unnatural Turbidity Was Observed at Outfall 002.Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Clay Feed Was Terminated on 990708 ML17326A0421999-07-0909 July 1999 NPDES Noncompliance Notification:On 990707,sample Taken Showed Residual Clam-Trol CT-2 Value of 0.17 Ppm.Caused by Interruption of Clay Feed to Unit 1 Discharge Vault.Valve Was Cleared & Clay Feed Was re-established ML17335A1441998-07-31031 July 1998 NPDES Noncompliance Notification:On 980623,ice-making Sys Discharge Line Developed Leak & Oversprayed Containment Spillings Approx 50 Gallons.Caused by Vibration & Wear Against Line.Discharge Line Supports Have Been Redesigned ML17334B8161998-07-0808 July 1998 NPDES Noncompliance Notification:On 980617,discovered Lube Oil Discharge.Caused by Leaking Tubes Due to Corrosion of Tubes.Leaking Tubes Repaired & Established Insp/Preventive Maint Program for Lube Oil Coolers ML17334B7571998-04-27027 April 1998 NPDES Noncompliance notification:980327,boiler Condensate Spill Occurred.Caused by Small Amount of Condensate on Metal Skirting Surrounding Containment Berm.Failed Condensate Valve Was Replaced ML17334A6861998-03-13013 March 1998 NPDES Noncompliance Notification:On 980209,boiler Condensate Spill Occurred.Caused by Failed Sight Glass on Rental Plant Heating Boiler.Replaced Site Glass & Installed Plexiglass Shield Around Site Glass to Protect Operators ML17334A5881997-12-0909 December 1997 NPDES Noncompliance Notification:On 971108 Plant Personnel Chlorination Sys Was Shut Down,Due to Valve Lineup Error Made During Startup of Continuous Chlorination After Shutdown.Corrected Lineup & Repositioned Valve ML17333A3881996-03-13013 March 1996 NPDES Noncompliance Notification:On 960310,continuous Ph Monitoring of Outfall 00D(turbine Room Sump)Interrupted. Caused by Electronic Failure of Monitoring Instrumentation. Grab Samples Performed & Monitor Recalibrated on 960311 ML17333A3871996-02-28028 February 1996 NPDES Noncompliance Notification:On 960226,continuous Ph Monitoring of Outfall 00D(Turbine Room Sump) Interrupted. Caused by Fouling of Ph Instrumentation Glass Electrode. Electrode Cleaned & Ph Monitor Returned to Svc ML17332A9791995-09-21021 September 1995 NPDES Noncompliance Notification:On 950916,unnatural Turbidity Observed at Plant Outfalls 001 & 002 During Molluscicide Treatment at Plant.Preventive Actions Not Possible Due to Detoxificaion Requirements in NPDES Permit ML17332A9551995-09-0808 September 1995 NPDES Noncompliance Notification:On 950829,hydraulic Oil Spill Occurred While Divers Using Hydraulic Brushes to Remove Zebra Mussels from Plant Screenhouse Intake Forebay Walls.Oil Absorbent Booms Deployed Into Forebay ML17332A9541995-09-0707 September 1995 NPDES Noncompliance Notification:On 950831,determined That Discharge from Outfall 00C (Heating Boiler Blowdown) Exceeded Concentration of Monethanolamine Submitted in NPDES Application Due to Valve Being Aligned in Open Position ML17332A8301995-06-0808 June 1995 NPDES Noncompliance Notification:On 950530,spill of Ethylene Glycol Occurred When Contracted Svc Technician Troubleshooting Portable Welding Machine.Ethylene Glycol Coolant Replaced W/Propylene Glycol Coolant ML17332A6991995-03-23023 March 1995 NPDES Noncompliance Notification:On 950205 to 16,33 Wild Ducks Entrained in Intake Cribs & Subsequently Collected on Intake Screens within Screenhouse.Suspect Ducks Entrained While Feeding on Zebra Mussels ML17332A6961995-03-20020 March 1995 NPDES Noncompliance Notification:On 950301,bypass Discharge from Turbine Room Sump Through Emergency Over Flow Piping Into Intake Forebay to Lake Michigan ML17331B3311994-03-30030 March 1994 NPDES Noncompliance Notification:On 940303,determined HVAC Sys Leaking Water Containing Approx 1,000 Mg/Liter Sodium Nitrite at Calculated Rate of 0.5 Gpm ML17331A8841993-06-0808 June 1993 NPDES Noncompliance Notification:On 930526 Chlorine Exceedance Incorrectly Stated Event Occurred on May 21 Instead of Actual Date of May 19.Licensee Apologizes for Inconvenience Error May Have Caused ML17331A1251993-03-24024 March 1993 NPDES Noncompliance Notification:On 930322,plant Personnel Discovered Small Oil Sheen at North Storm Water Outfall 001S.Oil Residue from Parking Lot Gradually Entered Lake Michigan.Oil Absorbent Booms in Place at Outfall ML17329A6821992-11-12012 November 1992 NPDES Noncompliance Notification:On 921109,review of Records Determined That First Quarter 1992 Samples for Stormwater Outfall 001S Not Collected.Quarterly Sampling Requirement Added to Computerized Tracking Sys ML17329A5521992-07-0202 July 1992 NPDES Noncompliance Notification:On 920630,minor Inadvertent Discharge of Treatment Chemical Clam-trol CT-1 May Have Occurred.Fire Protection Clam-trol Treatment Was Suspended Immediately & Will Not Be Resumed Until Alterations Made ML17329A5481992-06-29029 June 1992 NPDES Noncompliance Notification:On 920624,grab Sample of Outfall 002 Circulating Water Discharge Indicated TRC Concentration of 0.33 mg/1.Caused by Flow Balance Between Plant Sys.Unit 1 in Shutdown Condition ML17329A5401992-06-10010 June 1992 NPDES Noncompliance Notification:On 920606,grab Sample of Outfall 002 Circulating Water Discharge Indicated Total Residual Chlorine Above Timits.Caused by Manfunctioning Svc Water Flow Meter.Flow Meter Will Be Replaced ML20086T9911992-01-0303 January 1992 Noncompliance Notification:On 911219,approx 400 Diving Ducks Collected in Circulating Water Sys Screenwash Baskets.Caused by Abundant Food Supply Provided by Circulating Water Discharge.Flow Rates Reduced ML17329A3231991-12-10010 December 1991 NPDES Noncompliance Notification:On 911129,discovered That HX Associated W/Component Cooling Water Sys Leaking & Drop in Sys Surge Tank Level Occurred.Approx 5,300 Gallons of Water Leaked from Sys.Hx Isolated for Repairs ML17329A0961991-07-11011 July 1991 Final NPDES Notification Re Exceeding Heat Addition Effluent Limitation on 910701-05 on Outfall 001 & 002. Cause Under Investigation.Power Reduction Initiated on 910705 to Meet Limitations ML17328B0091991-04-0909 April 1991 NPDES Noncompliance Notification:On 910327,automatic Temp Recorder for Outfall 001 Failed & No Temp Measurements Recorded from 910328-31.Plant Procedures Will Be Revised to Describe Compensatory Sampling Measures in Event of Failure ML17334B3961991-02-26026 February 1991 NPDES Noncompliance Notification:On 910220 & 21,unmonitored Discharges Occurred from Turbine Room Sump.Caused by Inoperable Ph Meter.Turbine Sump Room Isolated & Job Order Written to Repair Meter ML17328A7641990-10-30030 October 1990 NPDES Noncompliance Notification:On 901025,five Unmonitored Discharges from Turbine Room Sump Occurred Releasing 250,000 Gallons of Water.Caused by Downstream Blockage of Flow to TRS Sample Line.In Interim,Ph Sampling Performed ML17325B3311989-11-0707 November 1989 Notifies That Total Recoverable Petroleum Hydrocarbons Sample Collected on 891006 Contained 0.9 mg/1 Trph.Util Believes Amount to Be Anomalous Value ML17326B5701989-03-0909 March 1989 NPDES Noncompliance Notification:Prefilter Backwash Limitations Exceeded for Feb 1989.Plan to Ensure Future Compliance W/Npdes Permit Requirements Will Be Submitted to Plainwell District Ofc ML17326B5541989-03-0606 March 1989 NPDES Noncompliance Notification:On 890224,leak Found in Main Turbine Lubricating Oil Coolers.Cause Not Stated. Leaking Cooler Isolated & Tube Plugged & Eddy Current Testing Performed to Determine Integrity of Remaining Tubes ML17326B4981988-11-18018 November 1988 NPDES Noncompliance Notification:On 881114,sample of Prefilter Backwash Effluent (Outfall 00F) Analyzed for Suspended Solids & Indicated 171 mg/1.Rough Lake Conditions Stirred Bottom Sediments Coming Into Plant Intake Water ML17326B4941988-11-0707 November 1988 NPDES Noncompliance Notification:On 881031,prefilter Backwash Discharge (Outfall 00F) Indicated Suspended Solids Concentration of 138 Mg/L ML17325A9811988-10-0505 October 1988 NPDES Noncompliance Notification:On 880919,water Makeup Prefilter Backwash Sample Exceeded Limitations.Caused by High Solids in Intake from Lake Michigan.Plant Personnel Reminded About Need to Evaluate & Rept Analyses Promptly ML17325A9291988-09-13013 September 1988 NPDES Noncompliance Notification:On 880910,Unit 1 Discharged Taken During Circulating Water Chlorination Showed Chlorine Concentration of 0.135 Mg/L.Caused by Temporary Reduced Water Flow Through Sys.Pump Chlorine Feed Reduced ML17325A8441988-06-15015 June 1988 NPDES Noncompliance Notification:On 880602,oil Spill of Approx 300 Gallons from Underground Storage Tank Occurred. Cleanup & Recovery Measures Underway.Repairs Will Be Made to Leak Area.Cleanup Will Be Completed by 880617 ML17325A4911987-11-23023 November 1987 NPDES Noncompliance Notification:On 871117,analysis of Grab Sample of Unit Discharge Taken During Circulating Water Chlorination Showed Total Residual Chlorine Concentration Above Limits.Caused by Vibration Causing Valve to Close ML17325A2961987-09-14014 September 1987 NPDES Noncompliance Notification:On 870901,spill from Turbine Room Sump,Outfall 00D Occurred.Approx 9,000 Gallons of Water Overflowed to Lake Michigan.Grab Sample Indicated Ph of 6.57 & No Trace of Oil & Grease.Caused by Repairs ML17325A2681987-08-11011 August 1987 NPDES Noncompliance Notification:On 870805,chlorination of Circulating Water Commenced Due to Biological Fouling.Total Residual Chlorine Levels Recorded on 870805,08 & 09 Listed ML17334B1161987-07-0606 July 1987 NPDES Noncompliance Notification:On 870630,monitoring Turbine Room Sump Process Ph Meter Found to Be Inoperative. Turbine Room Sump May Have Discharged to Absorption Pond During Previous 5 H W/O Continuous Monitoring ML17325A0831987-04-27027 April 1987 NPDES Noncompliance Notification:On 870410,oil Entered Yard Drain When Pressurized Tank Sprayed Out 10 Gallons Number 2 Fuel Oil During Attempt to Measure Level in east-middle Heating Boiler Fuel Oil Tank.Cleanup Began Immediately ML20213G9891986-11-14014 November 1986 NPDES Noncompliance Notification:On 861107,recording Instrument from Which Circulating Water Intake & Discharge Temps Obtained Failed.Caused by Faulty servo-motor.Recording Instrument Repaired & Returned to Svc ML20214P9961986-09-0909 September 1986 Corrected NPDES Noncompliance Notification:On 860903,turbine Room Sump Overflowed Into Circulating Water Sys Intake Forebay.Caused by Airlocked Suction Lines.Grab Sample Taken. Condition Rept Will Determine Corrective Action ML17324A9981986-07-14014 July 1986 NPDES Noncompliance Notification:On 860709,discovered That Grab Sample for Suspended Solids Not Obtained for Steam Generator Blowdown During 860629 Startup.Blowdown Sys Used for Weekly Sampling Frequency ML20211K5131986-06-19019 June 1986 NPDES Noncompliance Notification:On 860616,during Draining & Cleaning Steam Generators,Suspended Solids Sample from Startup Blowdown Flash Tank Revealed Concentration of 172 Ppm.Probably Caused by Boric Acid ML20205S8491986-06-0202 June 1986 NPDES Noncompliance Notification:On 860528,w/both Nuclear Units Out of Svc,Heating Boiler Started.Blowdown Sample Had Suspended Solids Concentration of 129.Caused by Chemical Shock ML17321A9411985-10-24024 October 1985 NPDES Noncompliance Notification:On 851023,sample Taken of Suspended Solids Concentration Elevated.Caused by Chemical Shock Due to Batch Addition of Chemical Treatment ML20198A8631985-10-24024 October 1985 NPDES Noncompliance Notification:On 851019,steam Generator Found to Have Suspended Solids Concentration of 2,442 Ppm. Caused by Recent Steam Generator Cleaning ML20138N6271985-10-24024 October 1985 NPDES Noncompliance Notification:On 850716,plant Heating Boiler Started While Both NSSS Out of Svc.Blowdown Sample Taken on 851022,contained Suspended Solids Concentration of 169 Ppm.On 851023,sample Contained 195 Ppm 1999-09-10
[Table view] Category:TEXT-ENVIRONMENTAL REPORTS
MONTHYEARML17326A1191999-09-10010 September 1999 NPDES Noncompliance Notification:On 990909,unnatural Turbidity Was Observed at Cook Plant Outfall 001 & 002. Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Terminated Clay Feed ML17326A0421999-07-0909 July 1999 NPDES Noncompliance Notification:On 990707,sample Taken Showed Residual Clam-Trol CT-2 Value of 0.17 Ppm.Caused by Interruption of Clay Feed to Unit 1 Discharge Vault.Valve Was Cleared & Clay Feed Was re-established ML17326A0431999-07-0909 July 1999 NPDES Noncompliance Notification:On 990707,unnatural Turbidity Was Observed at Outfall 002.Caused by Bentonite Clay Being Fed Into Discharge Vaults During Molluscicide Treatment.Clay Feed Was Terminated on 990708 ML17325B6131998-12-31031 December 1998 Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. ML17335A5241998-12-31031 December 1998 Annual Environ Operating Rept for Jan-Dec 1998 for DC Cook Nuclear Plant,Units 1 & 2. with 990430 Ltr ML17326A1241998-12-31031 December 1998 Revised Page 2 to 1998 Annual Environ Operation Rept, for DC Cook Nuclear Plant,Correcting Omission in App I ML17335A1441998-07-31031 July 1998 NPDES Noncompliance Notification:On 980623,ice-making Sys Discharge Line Developed Leak & Oversprayed Containment Spillings Approx 50 Gallons.Caused by Vibration & Wear Against Line.Discharge Line Supports Have Been Redesigned ML17334B8161998-07-0808 July 1998 NPDES Noncompliance Notification:On 980617,discovered Lube Oil Discharge.Caused by Leaking Tubes Due to Corrosion of Tubes.Leaking Tubes Repaired & Established Insp/Preventive Maint Program for Lube Oil Coolers ML17334B7571998-04-27027 April 1998 NPDES Noncompliance notification:980327,boiler Condensate Spill Occurred.Caused by Small Amount of Condensate on Metal Skirting Surrounding Containment Berm.Failed Condensate Valve Was Replaced ML17334A6861998-03-13013 March 1998 NPDES Noncompliance Notification:On 980209,boiler Condensate Spill Occurred.Caused by Failed Sight Glass on Rental Plant Heating Boiler.Replaced Site Glass & Installed Plexiglass Shield Around Site Glass to Protect Operators ML17334A6941997-12-31031 December 1997 Annual Radioactive Effluent Release Rept for Jan-Dec 1997. ML17334B7671997-12-31031 December 1997 Annual Environ Operating Rept for 970101-1231 for DC Cook Nuclear Plant,Units 1 & 2. W/980427 Ltr ML17334A5881997-12-0909 December 1997 NPDES Noncompliance Notification:On 971108 Plant Personnel Chlorination Sys Was Shut Down,Due to Valve Lineup Error Made During Startup of Continuous Chlorination After Shutdown.Corrected Lineup & Repositioned Valve ML17334B6221996-12-31031 December 1996 Annual Environ Operating Rept for 960101-961231. W/970418 Ltr ML17334B6201996-12-31031 December 1996 Annual Radioactive Effluent Release Rept for Period of 960101-1231. W/970320 Ltr ML17333A8051996-12-31031 December 1996 Number of Personnel & Man-Rem by Work & Job Function. ML17333A3881996-03-13013 March 1996 NPDES Noncompliance Notification:On 960310,continuous Ph Monitoring of Outfall 00D(turbine Room Sump)Interrupted. Caused by Electronic Failure of Monitoring Instrumentation. Grab Samples Performed & Monitor Recalibrated on 960311 ML17333A3871996-02-28028 February 1996 NPDES Noncompliance Notification:On 960226,continuous Ph Monitoring of Outfall 00D(Turbine Room Sump) Interrupted. Caused by Fouling of Ph Instrumentation Glass Electrode. Electrode Cleaned & Ph Monitor Returned to Svc ML17333A4021995-12-31031 December 1995 Corrected Annual Radioactive Effluent Release Rept for DC Cook Nuclear Plant Units 1 & 2. ML17334B5871995-12-31031 December 1995 Annual Environ Operating Rept,Jan-Dec 1995. W/960424 Ltr ML17334B5801995-12-31031 December 1995 Annual Radioactive Effluent Release Rept Jan-Dec 1995. W/960322 Ltr ML17332A9791995-09-21021 September 1995 NPDES Noncompliance Notification:On 950916,unnatural Turbidity Observed at Plant Outfalls 001 & 002 During Molluscicide Treatment at Plant.Preventive Actions Not Possible Due to Detoxificaion Requirements in NPDES Permit ML17332A9551995-09-0808 September 1995 NPDES Noncompliance Notification:On 950829,hydraulic Oil Spill Occurred While Divers Using Hydraulic Brushes to Remove Zebra Mussels from Plant Screenhouse Intake Forebay Walls.Oil Absorbent Booms Deployed Into Forebay ML17332A9541995-09-0707 September 1995 NPDES Noncompliance Notification:On 950831,determined That Discharge from Outfall 00C (Heating Boiler Blowdown) Exceeded Concentration of Monethanolamine Submitted in NPDES Application Due to Valve Being Aligned in Open Position ML17332A8301995-06-0808 June 1995 NPDES Noncompliance Notification:On 950530,spill of Ethylene Glycol Occurred When Contracted Svc Technician Troubleshooting Portable Welding Machine.Ethylene Glycol Coolant Replaced W/Propylene Glycol Coolant ML17332A6991995-03-23023 March 1995 NPDES Noncompliance Notification:On 950205 to 16,33 Wild Ducks Entrained in Intake Cribs & Subsequently Collected on Intake Screens within Screenhouse.Suspect Ducks Entrained While Feeding on Zebra Mussels ML17332A6961995-03-20020 March 1995 NPDES Noncompliance Notification:On 950301,bypass Discharge from Turbine Room Sump Through Emergency Over Flow Piping Into Intake Forebay to Lake Michigan ML17334B5381994-12-31031 December 1994 Annual Radioactive Effluent Release Rept Jan-Dec 1994. W/ 950320 Ltr ML17334B5411994-12-31031 December 1994 DC Cook Nuclear Plant Units 1 & 2 Annual Environ Operating Rept Jan-Dec 1994. W/950424 Ltr ML17331B3311994-03-30030 March 1994 NPDES Noncompliance Notification:On 940303,determined HVAC Sys Leaking Water Containing Approx 1,000 Mg/Liter Sodium Nitrite at Calculated Rate of 0.5 Gpm ML17334B5031993-12-31031 December 1993 DC Cook Nuclear Plant Annual Radioactive Effluent Release Rept for Jan-Dec 1993. W/940325 Ltr ML17334B5041993-12-31031 December 1993 Annual Environ Operating Rept Jan-Dec 1993 DC Cook Nuclear Plant Units 1 & 2. W/940419 Ltr ML17331A8841993-06-0808 June 1993 NPDES Noncompliance Notification:On 930526 Chlorine Exceedance Incorrectly Stated Event Occurred on May 21 Instead of Actual Date of May 19.Licensee Apologizes for Inconvenience Error May Have Caused ML17331A1251993-03-24024 March 1993 NPDES Noncompliance Notification:On 930322,plant Personnel Discovered Small Oil Sheen at North Storm Water Outfall 001S.Oil Residue from Parking Lot Gradually Entered Lake Michigan.Oil Absorbent Booms in Place at Outfall ML17331A0721992-12-31031 December 1992 DC Cook Semiannual Radioactive Effluent Release Rept for Jul-Dec 1992. W/930226 Ltr ML17334B4721992-12-31031 December 1992 DC Cook Nuclear Plant,Units 1 & 2 Annual Environ Operating Rept,920101-1231. W/930421 Ltr ML17329A6821992-11-12012 November 1992 NPDES Noncompliance Notification:On 921109,review of Records Determined That First Quarter 1992 Samples for Stormwater Outfall 001S Not Collected.Quarterly Sampling Requirement Added to Computerized Tracking Sys ML17329A5521992-07-0202 July 1992 NPDES Noncompliance Notification:On 920630,minor Inadvertent Discharge of Treatment Chemical Clam-trol CT-1 May Have Occurred.Fire Protection Clam-trol Treatment Was Suspended Immediately & Will Not Be Resumed Until Alterations Made ML17334B4381992-06-30030 June 1992 DC Cook Nuclear Plant,Units 1 & 2 Semiannual Radioactive Effluent Release Rept,Jan-June 1992. W/920826 Ltr ML17329A5481992-06-29029 June 1992 NPDES Noncompliance Notification:On 920624,grab Sample of Outfall 002 Circulating Water Discharge Indicated TRC Concentration of 0.33 mg/1.Caused by Flow Balance Between Plant Sys.Unit 1 in Shutdown Condition ML17329A5401992-06-10010 June 1992 NPDES Noncompliance Notification:On 920606,grab Sample of Outfall 002 Circulating Water Discharge Indicated Total Residual Chlorine Above Timits.Caused by Manfunctioning Svc Water Flow Meter.Flow Meter Will Be Replaced ML20086T9911992-01-0303 January 1992 Noncompliance Notification:On 911219,approx 400 Diving Ducks Collected in Circulating Water Sys Screenwash Baskets.Caused by Abundant Food Supply Provided by Circulating Water Discharge.Flow Rates Reduced ML17334B4501991-12-31031 December 1991 Hydrogeologic Evaluation of Cook Nuclear Plant,Bridgman, Mi. ML17334B4201991-12-31031 December 1991 DC Cook Nuclear Plant Units 1 & 2 Annual Environ Operating Rept,1991. W/920424 Ltr ML17329A4261991-12-31031 December 1991 Annual Personnel Monitoring Rept for 1991. W/920320 Ltr ML17329A3981991-12-31031 December 1991 Semiannual Radioactive Effluent Release Rept,Jul-Dec 1991. W/920226 Ltr ML17329A3231991-12-10010 December 1991 NPDES Noncompliance Notification:On 911129,discovered That HX Associated W/Component Cooling Water Sys Leaking & Drop in Sys Surge Tank Level Occurred.Approx 5,300 Gallons of Water Leaked from Sys.Hx Isolated for Repairs ML17334B4071991-09-30030 September 1991 Evaluation of Tritium Migration in Aquifer of DC Cook Nuclear Plant & Surrounding Communities. W/Two Oversize Drawings ML17329A0961991-07-11011 July 1991 Final NPDES Notification Re Exceeding Heat Addition Effluent Limitation on 910701-05 on Outfall 001 & 002. Cause Under Investigation.Power Reduction Initiated on 910705 to Meet Limitations ML20077S7241991-06-30030 June 1991 DC Cook Nuclear Plant Units 1 & 2 Semiannual Radioactive Effluent Release Rept,Jan-June 1991 1999-09-10
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P R.IC)R.I"EY'CCELERATED RIDS PROCESSING)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9503270141 DOC.DATE: 95/03/20 NOTARIZED:
NO DOCKET g FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
Indiana Michigan Power Co.(formerly Indiana 6 Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)P
SUBJECT:
NPDES noncompliance notification:on 950301,bypass discharge I from turbine room sump through emergency over flow piping into intake forebay to Lake Michigan.DISTRIBUTION CODE: COOID COPIES RECEIVED:LTR (ENCL~SIZE: TITLE: Licensing Submittal:
Environmental Rept Amdt 6 Related Correspondence NOTES RECIPIENT ID CODE/NAME PD3-1 PD INTERN~FILE CENTER 01 RGN3'RSS/RPB EXTERNAL LITCO'KERS i D NRC PDR COPIES LTTR E CL RECIPIENT ID CODE/NAME HICKMAN,J OGC/HDS2 NOAC COPIES LTTR ENCL 1 I D 0 C N NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.504-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEEDI O TOTAL NUMBER OF COPIES REQUIRED: LTTR 8 ENCL h f I ('
indiana Michigan.,Power Company P.O.Box 16631 Columbus, OH 43216 March 20, 1995 AEP:NRC:1208H Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.20555 Gentlemen:
Donald C.Cook Nuclear Plant Units 1 and 2 TURBINE ROOM SUMP DISCHARGE This notification is forwarded for your information pursuant to Appendix"B" of the Donald C.Cook Nuclear Plant Environmental Technical Specifications.
The subject of this notification concerns a by-pass discharge on March 1, 1995, from the turbine room sump (TRS)through emergency over flow piping into the intake forebay to Lake Michigan.The cause of the discharge was due to a failure of the regulating valve (DRV-710)to open when signaled.The valve was eventually opened by defeating the air regulator to the valve and manually increasing the air pressure, forcing the valve to open.An action request has been initiated to repair DRV-710.Until DRV-710 is repaired, turbine room sump releases are being controlled by a manual isolation valve.The waters are sampled for pH and batch released via procedure 12-OHP 4021.062.001.
The pH range of the TRS water during the inadvertent discharge to the lake was 8.5 to 9.0.Outfalls 001 and 002 were analyzed for pH and outfall observations were performed at 0830 on March 1, 1995.The pH for outfall 001 water was 8.2.An outfall observation of 1 was made, meaning that the water was free of any unusual characteristics of the discharge, i.e., unusual turbidity, color, oil film, floating solids, foams, settleable solids or deposits.The pH for outfall 002 was 7.9, and an outfall observation of 1 was also made.The maximum estimated flow to the intake forebay was 0.016 million gallons.Five of the plant's seven circulating water pumps were on at the time of the by-pass.As required by the Cook Nuclear Plant National Pollutant Discharge Elimination System (NPDES)Permit No.MI6005827, written 9503270141 950320 PDR ADOCK 05000315 S PDR
~U.S.Nuclear Regulatory Commission Page 2 AEP:NRC'1208H notification of this event was provided on March 2, 1995, to the Surface Water Quality Division of the Michigan Department of National Resources.
This type of discharge is included in the proposed NPDES permit under outfall OOH.Should you have any questions or concerns regarding this notification, please contact Dane Mazzitti at (614)223-2085.Sincerely, E.E.Fitzpatrick Vice President pit cc: A.A.Blind G.Charnoff J.B.Martin NFEM Section Chief J.R.Padgett