ML17335A144: Difference between revisions

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RECIPIENT            COPIES              RECIPIENT              COPIES ID  CODE/NAME          LTTR ENCL        ID  CODE/NAME          LTTR ENCL PD3-3 PD                  1    1        STANG, J                  1    1 INTERNA: FILE    CENTE              1    1      OGC/HDS3 RGN3                      1    1 EXTERNAL: NOAC                                      NRC PDR                    1    1 D
RECIPIENT            COPIES              RECIPIENT              COPIES ID  CODE/NAME          LTTR ENCL        ID  CODE/NAME          LTTR ENCL PD3-3 PD                  1    1        STANG, J                  1    1 INTERNA: FILE    CENTE              1    1      OGC/HDS3 RGN3                      1    1 EXTERNAL: NOAC                                      NRC PDR                    1    1 D
N NOTE TO ALL "RIDS" RECIPIENTS:
N NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR                    ENCL    , 7
                                                  '
TOTAL NUMBER OF COPIES REQUIRED: LTTR                    ENCL    , 7


Indiana Michigan Power Company 500 Circle Drive
Indiana Michigan Power Company 500 Circle Drive

Latest revision as of 23:33, 3 February 2020

NPDES Noncompliance Notification:On 980623,ice-making Sys Discharge Line Developed Leak & Oversprayed Containment Spillings Approx 50 Gallons.Caused by Vibration & Wear Against Line.Discharge Line Supports Have Been Redesigned
ML17335A144
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 07/31/1998
From: Sampson J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1208AB, NUDOCS 9808070053
Download: ML17335A144 (7)


Text

CA.TE GORY 1g REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION$ HBR:9b08070053 DOC.DATE: 98/07/31 NOTARIZED: NO DOCKET FACIL:50-315" Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316'Donald

' C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATION SAMPSON,J.R. Indiana Michigan Power Co. (formerly Indiana 6 Michigan Ele RECIP.NAME RECIPIENT AFFILIATION

SUBJECT:

NPDES noncompliance notification:on 980623,ice-making sys's A discharge line developed leak S oversprayed containment spillings approx 50 gallons. Caused by vibration wear Ec against line. Discharge line supports have been redesigned. T DISTRIBUTION CODE: IE23D COPIES RECEIVED:LTR ENCL SIZE: E TITLE: Environmental Event Report (per Tech Specs)

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-3 PD 1 1 STANG, J 1 1 INTERNA: FILE CENTE 1 1 OGC/HDS3 RGN3 1 1 EXTERNAL: NOAC NRC PDR 1 1 D

N NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR ENCL , 7

Indiana Michigan Power Company 500 Circle Drive

~

Buchanan, Ml 491071395 INDIANA MICHIGAN POEM July 31, 1998 AEP:NRC:1208AB Docket Nos: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop 0-P1-17 Washington, D.C. 20555 Gentlemen:

Donald C. Cook Nuclear Plant Units 1 and 2 SPILL OF SODIUM TETRABORATE TO THE GROUND NPDES NOTIFICATION Indiana Michigan Power Company is the holder of National Pollutant Discharge Elimination System (NPDES) permit number MI0005827 for Donald C. Cook Nuclear Plant. Section 5.4.2 to part II of appendix B (environmental technical specifications) to facility operating licenses DPR-58 and DPR-74 requires reports of non-routine events that are reportable to state agencies to be submitted to the NRC.

In a letter dated July 1, 1998, the Michigan Department of Environmental Quality (MDEQ) was notified of a spill of a weak sodium tetraborate solution to the ground. The notification of this spill was provided to MDEQ per part II, section A.6 of the NPDES permit. In accordance with the environmental technical specifications, a copy of the report is provided to the NRC.

Should you have any questions or concerns regarding this notification, please contact John Carlson at 616/465-5901, extension 1153.

Sincerely, J. R. Sampson Site Vice President

/jmc Attachment 9808070053 q8073i&

PDR ADOCK 05000$ i5) 8 PDR~

U. Si. Nuclear Regulatory Commission AEP: NRC: 1208AB Page 2 cc: Z. A. Abramson MDEQ - DW & RPD NRC Resident Inspector C. Z. Paperiello

U.S. Nuclear Regulatory Commission AEP: NRC: 1208AB Page 3 bc: T. P. Beilman S. J. Brewer/M. S. Ackerman/W. T. MacRae J. J. Euto M. J. Gumns D. R. Hafer/K. R. Baker PRONET - w/attachment J. F. Stang, Jr., NRC - Washington, D.C. - w/attachment J. S. Wiebe

ATTACHMENT TO AEP:NRC: 1208AB NPDES NOTIFICATION

Aineiican Electric Po Cook Nuclear Plant One Cook Place Bridginan, Ml 49106 616465 5901 ANERICAN ELECTRIC PWKR

'r. Fred Morley, District Supervisor Surface Water Quality Division Michigan Department of Environmental Quality 1342 SR 89 West Suite B Plainwell, Ml 49080 July 1, 1998

Dear Mr. Morley:

Donald C. Cook Nuclear Plant NP DES Permit No. MI0005827 I

This written notification is provided per NPDES Permit MI0005827, Part II, Section A.6, Spill Notification, which requires that all spills to the surface or groundwaters of the state be reported.

Cook Nuclear Plant has installed a temporary, skid-mounted, ice-making system to replenish the borated ice in the plant's ice condensers. The skid has been provided with a spill containment system.

On June 23, 1998, at 1900 hrs, the ice-making system's discharge line, containing a weak sodium tetraborate solution, developed a leak and oversprayed the containment, spilling approximately 50 gallons to the ground. We calculate that approximately 0.7 lbs. of boron and 0.8 lbs. of sodium were discharged to the ground.

When the leak was discovered, the system was shut down and the leak was stopped.

The leak was repaired prior to restarting the system. The cause of the leak was excessive vibration and wear against the discharge line. The discharge line supports have been redesigned to prevent excessive wear on the line.

On June 26, 1998, at 1410 hrs, the.ice-making system's discharge line, containing a weak sodium tetraborate solution, was accidentally cut during work to improve the system design. The cut leaked approximately 30 gallons to the ground. We calculate that approximately 0.5 lbs. of boron and 0.5 lbs. of sodium were discharged to the ground. The line was replaced and the system was realigned to prevent further failures.

The ground where the spill occurred was excavated and properly disposed.

If you have any questions, please contact me at (616) 465-5901, ext. 1153.

Sincerely, John P. Garison Environmental Compliance Manager Itlm

, Mr. Fred Morley Page 2 July 1, 1998 I certify under penalty of law that I have personally examined and am familiar with the information submitted on this and all attached documents; and based on my inquiry of those individuals immediately responsible for obtaining the information, I believe the submitted information is true, accurate and complete. I am aware that there are significant penalties for submitting false information, including the possibility of fine and imprisonment.

.gg J. R. Sampson Site Vice President