05000272/LER-1982-042, Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised: Difference between revisions

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#REDIRECT [[05000272/LER-1982-042]]
{{Adams
| number = ML20066A684
| issue date = 10/20/1982
| title = Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised
| author name = Heller R
| author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY
| addressee name =
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
| docket = 05000272
| license number =
| contact person =
| document report number = LER-82-042-03X, LER-82-42-3X, NUDOCS 8211060176
| package number = ML20066A668
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 1
}}
{{LER
| Title = Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000272
| LER year = 2082
| LER number = 42
| LER revision =
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:m                                                                                                                                U. S. NUCLEAR CE!ULATORY COMMISSION (7 771 LICENSEE EVENT REPORT
          '*        CONTROL BLOCK:                  l    l    l    l    l                        (PLEASE PRINT CR TYPE ALL l'ECUIRED INFERMATION) o 1 S7 CAT 58l@
l 7      8 9  lN lJLICENSEE lS l CODE  Gl Sl1 l@IS 0l 0l -lLICENaE 14                            0l Cl 0l 0l 0l -l 0l25 0l@4 NUMBER                          26        l1l1l1l1l@l LICENSE  TYPE JO CON'T 7
0 1 8
5OuRN      60
                                            ! Lhl Ol 5l Ojo l Ol 2l 7 l 2 hl 0 l 6 l 2 l 8 l 8 l 2 gl1 l 0 l 2 l 0 l 8 l 2 l@
61            OtAKET NUMBER                68    69        EVENT DATE          74      75      REPORT D ATE        80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h p l On June 28, 1982, the NRC Resident Inspector discovered Valves 12AF10 and 12AF86 were ;
o 3 g in the open position, but not properly locked as required by Surveillance Procedure                                                                                  g g g SP(O)4.7.1.2a (4) . The Shift Fupervisor was notified and dispatched an operator who                                                                                      ;
g  properly locked the valves. This occurrence constituted inadequate implementation of                                                                          g l0 l6 l l procedural controls which threatened to cause a reduction of redundancy in an                                                                                        ,
      ;o;;; g engineered safety feature and is reportable in accordance with Technical Specificationg g ; 6.9.1.9.c.                                                                                                                                                                ;
7        89                                                                                                                                                                80 DE            CODE        5 BC DE                  COMPONENT CODE                  SU8 CODE                E 7
O 9 8                      l Cl Hlh ]h Wh lV l A lL lV lE lX lh {@ 5]@
9          to          11            12            13                            18          19            20
                                    ,_                                          SEQUENTIAL                        OCCURRENCE          REPORT                    REVISION E                                        REPORT NO.
LER RO                                                                                        CODE              TYPE                      NC.
h ajyy y
21 VENT YE[ AR l 8l2l                  -.j          l 0 l4 l 2 l            y            l0 l3 l              ]             b          {
22        23            24            26        27            28      29          30            31        32 KN A      ON            ON PL T            ME                      HOURS 22          S8 IT          FOR        8. SUPPLt            MANUF CTURER 1Hlg[34Hjg 33
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                                                                        ,          l0l0l0l 37                    40 l  {YJg [N]g 41              42 _
lAlg lVl0l8l0lg 43            44              47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l The valves were found in the open position and were properly locked in place. All                                                                                        l 3 i        l personnel involved with valve position verifications were counseled on the safety                                                                            l
        , 7        l implications of the incident and methods of properly locking valves in position.                                                                              l i 3 l Valve operation and tagging lesson plans have been revised to include proper methods l i 4      l of locking and chaining valves.                                                                                                                              l 7        8 9                                                                                                                                                              80
                  $AU              % POWER                        OTHER STATUS                DIS O      Y                        DISCOVERf DESCRIPTION Q y@ l 0l 9 l 7 l@l                                                N/A                  l    Whl NRC Inspection                                                              l A TlVITY CO TENT RELEASED OP RELEASE                          AMOUNT OF ACTIVITY                                                      LOCATION OF RELEASE 7
1 6 8 9 dh            10 hl    11 N/A 44 l          l 45 N/A 8C l
PERSONNEL EXPOSURES NUMBER              TYPE 1 7 l 0 l 0 l 0 lhdhl DESCRIPTION                        N/A                                                                                                      l PERSONNE L INJURIES NUMBER              oESCRiptiON@
7 1 H 8 9 l0l0l0lhl      11        12 N/A 80 l
LOSS OF OR DAMAGE TO FACILITY TYPE      DESCRIPTION 7
1 9 8 9 hl iO N/A 9211060176 021020
* PDR S
ADOCK 05000272 ISSUE      DE    RilT!ON O                                                                        PDR                                    NRC USE ONLY 7
2 O 8 9
[N hl    10 N/A                                                                      l    l l l l l l l l l l l l l *g 68 69                          80 &
R. Heller NAME OF PREPARER                                                                                    PHONE:
609/935-6000 Ett 3078 o L
}}
 
{{LER-Nav}}

Latest revision as of 02:44, 6 January 2021

Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised
ML20066A684
Person / Time
Site: Salem PSEG icon.png
Issue date: 10/20/1982
From: Heller R
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20066A668 List:
References
LER-82-042-03X, LER-82-42-3X, NUDOCS 8211060176
Download: ML20066A684 (1)


LER-2082-042, Supplemental LER 82-042/03X-1:on 820628,valves 12AF10 & 12AF86 Discovered Open.Caused by Personnel Negligence in Failure to Notice That Chains on Valves Improperly Installed.Valve Operation & Tagging Lesson Plans Revised
Event date:
Report date:
2722082042R00 - NRC Website

text

m U. S. NUCLEAR CE!ULATORY COMMISSION (7 771 LICENSEE EVENT REPORT

'* CONTROL BLOCK: l l l l l (PLEASE PRINT CR TYPE ALL l'ECUIRED INFERMATION) o 1 S7 CAT 58l@

l 7 8 9 lN lJLICENSEE lS l CODE Gl Sl1 l@IS 0l 0l -lLICENaE 14 0l Cl 0l 0l 0l -l 0l25 0l@4 NUMBER 26 l1l1l1l1l@l LICENSE TYPE JO CON'T 7

0 1 8

5OuRN 60

! Lhl Ol 5l Ojo l Ol 2l 7 l 2 hl 0 l 6 l 2 l 8 l 8 l 2 gl1 l 0 l 2 l 0 l 8 l 2 l@

61 OtAKET NUMBER 68 69 EVENT DATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h p l On June 28, 1982, the NRC Resident Inspector discovered Valves 12AF10 and 12AF86 were ;

o 3 g in the open position, but not properly locked as required by Surveillance Procedure g g g SP(O)4.7.1.2a (4) . The Shift Fupervisor was notified and dispatched an operator who  ;

g properly locked the valves. This occurrence constituted inadequate implementation of g l0 l6 l l procedural controls which threatened to cause a reduction of redundancy in an ,

o;;; g engineered safety feature and is reportable in accordance with Technical Specificationg g ; 6.9.1.9.c.  ;

7 89 80 DE CODE 5 BC DE COMPONENT CODE SU8 CODE E 7

O 9 8 l Cl Hlh ]h Wh lV l A lL lV lE lX lh {@ 5]@

9 to 11 12 13 18 19 20

,_ SEQUENTIAL OCCURRENCE REPORT REVISION E REPORT NO.

LER RO CODE TYPE NC.

h ajyy y

21 VENT YE[ AR l 8l2l -.j l 0 l4 l 2 l y l0 l3 l ] b {

22 23 24 26 27 28 29 30 31 32 KN A ON ON PL T ME HOURS 22 S8 IT FOR 8. SUPPLt MANUF CTURER 1Hlg[34Hjg 33

{ Z jg 35

[36Zj@

, l0l0l0l 37 40 l {YJg [N]g 41 42 _

lAlg lVl0l8l0lg 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h g l The valves were found in the open position and were properly locked in place. All l 3 i l personnel involved with valve position verifications were counseled on the safety l

, 7 l implications of the incident and methods of properly locking valves in position. l i 3 l Valve operation and tagging lesson plans have been revised to include proper methods l i 4 l of locking and chaining valves. l 7 8 9 80

$AU  % POWER OTHER STATUS DIS O Y DISCOVERf DESCRIPTION Q y@ l 0l 9 l 7 l@l N/A l Whl NRC Inspection l A TlVITY CO TENT RELEASED OP RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE 7

1 6 8 9 dh 10 hl 11 N/A 44 l l 45 N/A 8C l

PERSONNEL EXPOSURES NUMBER TYPE 1 7 l 0 l 0 l 0 lhdhl DESCRIPTION N/A l PERSONNE L INJURIES NUMBER oESCRiptiON@

7 1 H 8 9 l0l0l0lhl 11 12 N/A 80 l

LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION 7

1 9 8 9 hl iO N/A 9211060176 021020

ADOCK 05000272 ISSUE DE RilT!ON O PDR NRC USE ONLY 7

2 O 8 9

[N hl 10 N/A l l l l l l l l l l l l l l *g 68 69 80 &

R. Heller NAME OF PREPARER PHONE:

609/935-6000 Ett 3078 o L