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{{Adams | |||
| number = ML20137K556 | |||
| issue date = 01/17/1986 | |||
| title = Insp Rept 50-285/85-27 on 851201-31.Violation & Deviation Noted:Failure to Display Security Identification Badges Inside Protected Area & Failure to Implement Fluid Sys Cleanliness Control Program,Respectively | |||
| author name = Harrell P, Hunnicutt D | |||
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) | |||
| addressee name = | |||
| addressee affiliation = | |||
| docket = 05000285 | |||
| license number = | |||
| contact person = | |||
| document report number = 50-285-85-27, IEB-83-07, IEB-83-7, NUDOCS 8601240131 | |||
| package number = ML20137K510 | |||
| document type = INSPECTION REPORT, NRC-GENERATED, INSPECTION REPORT, UTILITY, TEXT-INSPECTION & AUDIT & I&E CIRCULARS | |||
| page count = 9 | |||
}} | |||
See also: [[see also::IR 05000285/1985027]] | |||
=Text= | |||
{{#Wiki_filter:. _ . | |||
.' , | |||
APPENDIX C | |||
i | |||
j U. S. NUCLEAR REGULATORY COMMISSION | |||
! REGION IV | |||
I- | |||
! NRC Inspection Report: 50-285/85-27 License: DPR-40 | |||
3 Docket: 50-285 | |||
i | |||
! Licensee: Omaha Public Power District | |||
' | |||
1623 Harney Street | |||
! Omaha, Nebraska 68102 | |||
j Facility Name: Fort Calhoun Station | |||
: | |||
Inspection At: Fort Calhoun Station, Blair, Nebraska | |||
l | |||
Inspection Conducted: December 1-31, 1985 | |||
i | |||
! | |||
Inspector: _ | |||
P. H. Harrlill, SeritorResident ReTEtor Inspector | |||
!'D'N | |||
Date | |||
i | |||
. | |||
/ 7 | |||
( Approved: /). M. Hunnicutt, Chief, Project Section B, Date ' | |||
l [p Reactor Project Branch | |||
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: | |||
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8601240131 960117 | |||
i PDR ADOCK 05000295 | |||
'. O PDR | |||
4 | |||
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4 Inspection Summary | |||
Inspection Conducted December 1-31, 1985 (Report 50-285/85-27) | |||
Areas Inspected: Routine, unannounced inspection including operational safety | |||
verification, maintenance, surveillance, followup on previously identified | |||
items, followup on licensee event reports, and followup on IE Bulletin 83-07. | |||
, | |||
The inspection involved 102 inspector-hours (including 13 backshift hours) | |||
i onsite by one NRC inspector. | |||
Results: Within the six areas inspected, one violation (failure to display | |||
: security identification badges inside the protected area, paragraph 6) and two | |||
deviations (failure to properly implement a fluid system cleanliness control | |||
: program and failure to maintain temporary COE storage areas in accordance with | |||
; licensee requirements, paragraph 2) were identified. | |||
! | |||
, | |||
( | |||
i | |||
: | |||
! | |||
i | |||
: | |||
-_ _ .. . _ - _ . - - . . _ __ _ __ . . ___ | |||
& | |||
o . , | |||
. | |||
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-3- | |||
DETAILS | |||
f | |||
l 1. Persons Contacted | |||
*W. Gates, Plant Manager | |||
C. Brunnert, Operations Quality Assurance Supervisor | |||
M. Core, Maintenance Supervisor | |||
D. Dale Quality Control Inspector | |||
, J. Fisicaro, Nuclear Regulatory and Industry Affairs Supervisor | |||
M. Kallman, Security Supervisor | |||
L. Kusek, Operations Supervisor | |||
T. McIvor Technical Supervisor | |||
R. Mueller, Plant Engineer | |||
G. Roach, Chemical and Radiation Protection Supervisor | |||
J. Tesarek, Reactor Engineer | |||
* Denotes attendance at the exit interview. | |||
The inspector also contacted other plant personnel, including operators, | |||
technicians, and administrative personnel. | |||
2. Followup on Previously Identified Items | |||
(Closed) Severity Level V Violation 8421-Olb: Procedures have not been | |||
established to implement the requirements for cleanliness of | |||
I fluid systems. | |||
The licensee has revised Section 6.3, " Cleanliness Control," | |||
of the Quality Assurance Plant (QAP) to include the appropriate | |||
l requirements and recommendations from ANSI N 45.2.1-1973 and | |||
Regulatory Guide 1.37 Revision 0. Appropriate plant procedures | |||
have been revised to include the QAP Section 6.3 requirements | |||
' | |||
for a fluid system closeup inspection. However, the licensee | |||
has not included a procedural requirement required by the QAP | |||
to ensure that fluid systems are capped or sealed except when | |||
needed to carry out operations or m61ntenance activities. | |||
During tours of the plant by the NRC inspector, it was noted | |||
on five different occasions that the auxiliary feedwater (AFW) | |||
system was opened to the atmosphere when no personnel were | |||
working in the area.. The NRC inspector reviewed the maintenance | |||
procedures being used for modification work on the AFW system | |||
and noted that there was no requirement to maintain the system | |||
capped or sealed. The NRC inspector notified licensee | |||
management of the problems noted. The licensee made an | |||
on-the-spot change to the maintenance procedure and closed the | |||
open portions of the AFW system. After notification of these | |||
problems to licensee nanagement, the NRC inspector found | |||
subsequent problems of leaving the system open and unattended | |||
in the same area of activity. | |||
1 | |||
- _ _ _ - | |||
. . , | |||
. | |||
. | |||
-4- | |||
In the response to this violation, the licensee stated, in a | |||
letter to the NRC dated March 15, 1985, that standing orders | |||
and/or procedures would be revised or developed as required to | |||
more formally implement the requirements and recommendations of | |||
ANSI N 45.2.1-1973. The licensec's failure to provide revised | |||
procedures for requiring fluid systems be maintained capped or | |||
sealed and the licensee's failure to implement this requirement | |||
during'nodification activities is an apparent deviation to | |||
i commitments made to the NRC. (285/8527-01) | |||
(Closed) Severity Level IV Violation 285/8429-01: Deficiency | |||
report / quality report (DR/QR) responses were not received within | |||
i | |||
the 30-day requirement. | |||
The NRC inspector reviewed a sampling of DR/QR reports to | |||
determine if responses had been provided within the 30-day | |||
requirement. No cases were noted where the response was | |||
received more than 30 days from the date of issue of the DR/QR. | |||
The licensee has established a program to ensure that responses | |||
are received within the required time period. This program | |||
includes issuance of a monthly DR/QR status report that | |||
indicates all responses due and the individual responsible for | |||
submitting the response, weekly distribution of the DR/QR status | |||
list to all individuals on the list, and discussion by the | |||
operations quality assurance supervisor of outstanding responses | |||
with the plant review committee (PRC) members at the PRC | |||
meetings. The licensee has made the appropriate procedure | |||
changes to establish this program. | |||
(Closed) Severity Level IV Violation 285/8501-01: Failure to follow | |||
procedures for control of temporary critical quality equipment | |||
(CQE) storage areas. | |||
The NRC inspector randomly checked temporary CQE storage areas | |||
on December 5 and December 23, 1985, to verify that storage of | |||
materials in the areas was being done in accordance with | |||
licensee procecural requirements. During the December 5 tour, | |||
the NRC inspector noted that five of the nine areas checked did | |||
not meet the licensee's requirements. Each area contained one | |||
or more of the following problems: piping not capped or sealed, | |||
, non-Q material stored in the area, purchase order numbers not | |||
being transferred to remaining pieces when stock is cut, and | |||
trash accumulation in the area. The noted problems were | |||
discussed with licensee management personnel on | |||
December 6. | |||
. | |||
4 l | |||
_ - . - _ _ . - _ , _ ____.__.___-.__-_____.-_------__.___--._--____-._____--_x | |||
. . | |||
.. | |||
. | |||
-5- | |||
The NRC inspector also reviewed the quality control (QC) log to | |||
6 | |||
verify that the areas were inspected at least monthly by the | |||
j onsite QC department. No problems were noted. The NRC inspector | |||
l checked the temporary QC storage areas again on December 23 and | |||
I | |||
found that three of the six areas did not meet the licensee's | |||
requirements. | |||
The licensee's response letter, dated March 28, 1985, to this | |||
! violation stated that steps would be taken to ensure that the | |||
problems identified by the violation would be corrected and that | |||
' | |||
the areas would be maintained. The licensee's failure to | |||
maintain the temporary CQE storage areas in accordance with | |||
licensee requirements is an apparent deviation to commitments | |||
made to the NRC. (285/8527-02) - | |||
. | |||
3. Licensee Event Report (LER) Followup | |||
Through direct observation, discussions with licensee personnel, and | |||
review of records, the following event reports were reviewed to determine | |||
that reportability requirements were fulfilled, immediate corrective | |||
action was accomplished, and corrective action to prevent recurrence has | |||
been accomplished in accordance with Technical Specifications. | |||
The following LERs are closed: | |||
l 84-008 Tube rupture in the 'B' steam generator | |||
84-015 Polar crane carried load over reactor coolant system | |||
! LER 84-008 reported a steam generator tube failure during a plant startup- | |||
l from a refueling outage. The tube failure occurred in May 1984,'while | |||
performing a hydrostatic test of the reactor coolant systen. The plant | |||
was shutdown and the necessary repairs were made. The plant was | |||
subsequently restarted and operated from July 1984, until September 1985 | |||
(cycle 9), when it was shutdown for refueling. | |||
The licensee, in conjunction with Combustion Engineering, performed an | |||
analysis to determine the cause of the tube failure. The results of the | |||
l analysis indicated the failure was caused due to caustic-induced | |||
l intergranular stress corrosion cracking. To minimize the possibility of | |||
I additional tube failures, the licensee instituted programs during cycle 9 | |||
' to minimize caustic buildup in the steam generators. These programs | |||
consisted of enhanced contrcl of contaminants entering the condensate and | |||
feedwater systems, initiation of more restrictive secondary chemistry | |||
guidelines and operating limits, improvements in steam generator | |||
monitoring capabilities, and a soak / blowdown treatment process during | |||
system startup to reduce the amount of contaminants in the steam | |||
genera tor. The licensee also instituted a program to require an | |||
I | |||
, | |||
. , . _ . | |||
' | |||
* *. . . | |||
, | |||
. | |||
-6- | |||
f | |||
independent review of eddy current data. An independent review of the | |||
data had not been performed during past eddy current tests. | |||
The licensee performed eddy current tests on the steam generator tubes | |||
during the refueling outage currently in progress. Based on the results | |||
< | |||
of the test, the licensee plugged 16 tubes in the ' A' steam generator and | |||
17 tubes in the 'B' steam generator. All the tubes plugged, except for a | |||
total of five in both generators, were plugged due to denting. The | |||
i | |||
' | |||
remaining five tubes (two in the ' A' steam generator and three in the 'B' | |||
steam generator) were plugged due to identified defects. None of the | |||
identified defects were in the same area where the previous tube rupture | |||
occurred. | |||
The licensee intends to maintain the recently established programs to | |||
minimize the probability of another tube failure. | |||
i | |||
LER 84-015 reported an occurrence where the polar crane carried a load | |||
greater than 250 pounds over the reactor coolant system (RCS) when the | |||
pressurizer temperature was greater than 225 degrees F. This was a | |||
violation of the station Technical Specifications. To prevent recurrence, | |||
the licensee has added a note to the procedure for RCS vent and leak test | |||
operating instructions to electrically tagout the polar crane prior to | |||
exceeding 225 degrees F in the RCS. In addition, the licensee has also | |||
installed a sign on the breaker for the polar crane noting the same | |||
requirement. The NRC inspector noted that the breaker was tagged out | |||
during the recent plant heatup as required by the procedure, | |||
j No violations or deviations were identified. | |||
. | |||
4. Followup on IE Bulletin 83-07 | |||
; | |||
' | |||
IE Bulletin 83-07, " Fraudulent Products Sold by Ray Miller, Inc.," | |||
i | |||
' | |||
provided the licensee with infonnation regarding fraudulent material sold | |||
by the Ray Miller Company. The licensee was requested to V:rify that they | |||
had not used any material supplied by Ray Hiller. | |||
The NRC inspector reviewed the licensee's response to IE Bulletin 83-07 to | |||
verify that the responte was adequate and that the actions comitted to by | |||
the licensee have been completed. The licensee has reviewed their quality | |||
assurance (QA) records and verified that they have not received any | |||
, fraudulent products from any of the companies listed in the bulletin. The | |||
< | |||
licensee has also received a letter, dated March 22, 1984, from Combustion | |||
Engineering stating that no Ray Miller material was supplied to the | |||
, | |||
licensee. ' | |||
No violations or deviations were noted. This bulletin is considered | |||
closed. | |||
] | |||
o | |||
! | |||
*.., | |||
. | |||
-7- | |||
5. Operational Safety Verification | |||
The NRC inspector observed control room operations, reviewed cpplicable | |||
logs, and conducted discussions with control room operators. The | |||
inspector verified the operability of selected emergency systems, reviewed | |||
tag-out records, verified proper return to service of affected components, | |||
and ensured that maintenance requests had been initiated for equipment in | |||
need of maintenance. The inspector also verified implementation of | |||
radiation protection controls during observation of plant activities. | |||
Na violations or deviations were identified. | |||
6. Physical Plant Security and Safeguards | |||
The NRC resident inspector accompanied the NRC region-based, safeguards | |||
inspector on his routine, unannounced inspection. This effort was | |||
performed to increase the sensitivity and knowledge level of the resident | |||
inspector in the areas of security and safeguards. The resident inspector | |||
also made spot checks to verify that the physical security plan was being | |||
implemented in accordance with the station security plan. During tours of | |||
the plant, the NRC inspector noted that some individuals inside the | |||
protected area were not displaying their security badges in plain sight. | |||
The NRC inspector notified the licensee of the problem. The licensee | |||
posted a sign at the entrance to the protected area and issued a memo to | |||
all badge holders to remind everyone of the requirement to wear their | |||
badges in plain sight. Subsequent to these actions by the licensee, the | |||
NRC inspector nuted on three different occasions, individuals not | |||
displaying their security badges in plain sight. Failure to display a | |||
security bad e is an apparent violation of Standing Order G-39. | |||
(285/8527-03 | |||
7. Plant Tours | |||
The NRC inspector toured accessible areas of the unit to observe plant | |||
equipment conditions, including potential fire hazards, fluid leaks, and | |||
excessive vibration. The inspector observed plant housekeeping and | |||
cleanliness conditions during the tour. | |||
The NRC inspector walked down the accessible portions of the containment | |||
spray system. The walkdown was performed using Procedure OI-CS-1, | |||
Revision 14, and Drawing E-2866-210-130, Revision 32. During the | |||
walkdown, the NRC inspector noted discrepancies between the system | |||
operating procedure, drawing, and the as-built plant. The discrepancies | |||
noted were of a minor editorial nature. Licensee management was notified | |||
of the discrepancies and stated '. hat the appropriate documentation would | |||
be corrected. | |||
.- _ _ | |||
.- .- . . -. _- | |||
, * * . .; | |||
. | |||
-8- | |||
- | |||
t | |||
During the previous inspection period, the NRC inspector performed a | |||
walkdown of various systems. The items noted during the walkdowns were | |||
still being resolved at the end of the previous inspection period. The | |||
licensee provided the NRC inspector the appropriate information regarding | |||
the items. Based on this input, the discrepancies noted were of a minor | |||
editorial nature, except for one item. During the walkdown, the NRC | |||
inspector noted that there was a new valve installed on the emergency | |||
diesel generator fuel oil filter. This unnumbered valve was not shown on | |||
the drawing, nor was the talve listed on the valve lineup. The NRC | |||
inspector requested to see the documentation related to installation of | |||
the valve. The licensee las not yet provided the documentation. This | |||
item is unresolved pending a determination of whether or not the valve was | |||
installed per appropriate documentation. (285/8527-04) | |||
; During plant tours, the NRC inspector noted that two fire barriers were | |||
, | |||
not functional, as defined by the Technical Specifications. Fire Door | |||
1007-8 was not completely closed due to a hose running through the door | |||
1 and the guillotine fire curtain above Fire Door 1007-5 was inoperable | |||
j due to a hose running through a ventilation port. The NRC inspector | |||
i requested to see documentation to verify that an hourly fire patrol had | |||
been established and was in effect at the time of the discovery by the NRC | |||
inspector. The licensee had not located the necessary documentation. | |||
. | |||
This item remains unresolved pending whether or not an hourly fire watch | |||
had been established. (285/8527-051 | |||
' | |||
No violations or deviations were identified. . | |||
' | |||
i | |||
8. Monthly Maintenance Observation | |||
. | |||
' Station maintenance activities of safety-related systems and components | |||
listed below were observed to ascertain that they were conducted in | |||
accordance with approved procedures, Regulatory Guides, and industry codes | |||
or standards; and in conformance with Technical Specifications. | |||
The following items were considered during this review: the limiting | |||
conditions for operation were met while components or systems were removed ' | |||
l from service; approvals were obtained prior to initiating the work; | |||
i activities were accomplished using approved procedures and were inspected | |||
; as applicable; functional testing and/or calibrations were performed prior | |||
! to returning components or systems to service; quality control records | |||
! | |||
were maintained; activities were accomplished by qualified personnel; | |||
; parts and materials used were properly certified; radiological controls 7 | |||
l were implemented; and fire prevention controls were implemented. | |||
l | |||
Maintenance orders (M0s) were reviewed to determine status of outstanding | |||
- | |||
jobs and to ensure that priority is assigned to safety-related equipment | |||
; maintenance which may affect system performance. | |||
; | |||
- - _ _ _ _ _ . _ _ _ _ _ _ _ _ . _ _ . _ _ _ _ . _ _ . _ _ _ _ . . _ . _ . _ _ . | |||
i | |||
* . , | |||
, | |||
. | |||
l | |||
-9- | |||
I | |||
l | |||
The following maintenance activities were observed: ; | |||
. Replacement of packing in valves HCV-1103, FW-169, and FW-170 | |||
(M0 851570, 851471, and 851507, respectfully) | |||
. Coupling of the control element assemblies (f10 852446, Procedure ! | |||
; | |||
MP-RC-10-7) | |||
. Inspection of auxiliary feedwater storage tank interior (M0 852785) | |||
. Replacement of jumper wires in Limitorque motor-operated valves | |||
(MR-FC-85-77) | |||
No violations or deviations were identified. | |||
9. Monthly Surveillance Observation | |||
The NRC inspector observed the Technical Specification required | |||
surseillance testing on the station battery (Procedure ST-DC-1-F.1) and I | |||
verified that testing was performed in accordance with adequate | |||
procrcures, test instrumentation was calibrated, limiting conditions for , | |||
operation were met, removal and restoration of the affected components j | |||
were accomplished, test results conformed with Technical Specifications 1 | |||
other than the individual directing the test, and any deficiencies l | |||
identified during the testing were properly reviewed and resolved by I | |||
appropriate management personnel. The inspector also witnessed portions of l | |||
the shutdown margin verification (Procedure ST-SDM-1-F.1'. l | |||
1 | |||
No violations or deviations were identified. | |||
10. Unresolved Items | |||
i | |||
An unresolved item is a matter about which more information is required in | |||
order to determine whether it is acceptable, a violation, or a deviation. | |||
Two unresolved items are discussed in this report in paragraph 7. | |||
i | |||
11. Exit Interview j | |||
The NRC inspector met with Mr. W. G. Gates (Plant Manager) at the end of ! | |||
this inspection. At this meeting, the inspector sunnarized the scope of : | |||
the inspection and the findings. l | |||
l | |||
l | |||
l | |||
l | |||
I | |||
5 | |||
}} |
Latest revision as of 22:03, 30 June 2020
ML20137K556 | |
Person / Time | |
---|---|
Site: | Fort Calhoun |
Issue date: | 01/17/1986 |
From: | Harrell P, Hunnicutt D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
To: | |
Shared Package | |
ML20137K510 | List: |
References | |
50-285-85-27, IEB-83-07, IEB-83-7, NUDOCS 8601240131 | |
Download: ML20137K556 (9) | |
See also: IR 05000285/1985027
Text
. _ .
.' ,
APPENDIX C
i
j U. S. NUCLEAR REGULATORY COMMISSION
! REGION IV
I-
! NRC Inspection Report: 50-285/85-27 License: DPR-40
3 Docket: 50-285
i
! Licensee: Omaha Public Power District
'
1623 Harney Street
! Omaha, Nebraska 68102
j Facility Name: Fort Calhoun Station
Inspection At: Fort Calhoun Station, Blair, Nebraska
l
Inspection Conducted: December 1-31, 1985
i
!
Inspector: _
P. H. Harrlill, SeritorResident ReTEtor Inspector
!'D'N
Date
i
.
/ 7
( Approved: /). M. Hunnicutt, Chief, Project Section B, Date '
l [p Reactor Project Branch
i
i
!
l
i
!
l
i
!
i
!
l
8601240131 960117
i PDR ADOCK 05000295
'. O PDR
4
_ .- _ - . _ _ _ _ . _ _ _
'
'.
2
i
4 Inspection Summary
Inspection Conducted December 1-31, 1985 (Report 50-285/85-27)
Areas Inspected: Routine, unannounced inspection including operational safety
verification, maintenance, surveillance, followup on previously identified
items, followup on licensee event reports, and followup on IE Bulletin 83-07.
,
The inspection involved 102 inspector-hours (including 13 backshift hours)
i onsite by one NRC inspector.
Results: Within the six areas inspected, one violation (failure to display
- security identification badges inside the protected area, paragraph 6) and two
deviations (failure to properly implement a fluid system cleanliness control
- program and failure to maintain temporary COE storage areas in accordance with
- licensee requirements, paragraph 2) were identified.
!
,
(
i
!
i
-_ _ .. . _ - _ . - - . . _ __ _ __ . . ___
&
o . ,
.
.
-3-
DETAILS
f
l 1. Persons Contacted
- W. Gates, Plant Manager
C. Brunnert, Operations Quality Assurance Supervisor
M. Core, Maintenance Supervisor
D. Dale Quality Control Inspector
, J. Fisicaro, Nuclear Regulatory and Industry Affairs Supervisor
M. Kallman, Security Supervisor
L. Kusek, Operations Supervisor
T. McIvor Technical Supervisor
R. Mueller, Plant Engineer
G. Roach, Chemical and Radiation Protection Supervisor
J. Tesarek, Reactor Engineer
- Denotes attendance at the exit interview.
The inspector also contacted other plant personnel, including operators,
technicians, and administrative personnel.
2. Followup on Previously Identified Items
(Closed) Severity Level V Violation 8421-Olb: Procedures have not been
established to implement the requirements for cleanliness of
I fluid systems.
The licensee has revised Section 6.3, " Cleanliness Control,"
of the Quality Assurance Plant (QAP) to include the appropriate
l requirements and recommendations from ANSI N 45.2.1-1973 and
Regulatory Guide 1.37 Revision 0. Appropriate plant procedures
have been revised to include the QAP Section 6.3 requirements
'
for a fluid system closeup inspection. However, the licensee
has not included a procedural requirement required by the QAP
to ensure that fluid systems are capped or sealed except when
needed to carry out operations or m61ntenance activities.
During tours of the plant by the NRC inspector, it was noted
on five different occasions that the auxiliary feedwater (AFW)
system was opened to the atmosphere when no personnel were
working in the area.. The NRC inspector reviewed the maintenance
procedures being used for modification work on the AFW system
and noted that there was no requirement to maintain the system
capped or sealed. The NRC inspector notified licensee
management of the problems noted. The licensee made an
on-the-spot change to the maintenance procedure and closed the
open portions of the AFW system. After notification of these
problems to licensee nanagement, the NRC inspector found
subsequent problems of leaving the system open and unattended
in the same area of activity.
1
- _ _ _ -
. . ,
.
.
-4-
In the response to this violation, the licensee stated, in a
letter to the NRC dated March 15, 1985, that standing orders
and/or procedures would be revised or developed as required to
more formally implement the requirements and recommendations of
ANSI N 45.2.1-1973. The licensec's failure to provide revised
procedures for requiring fluid systems be maintained capped or
sealed and the licensee's failure to implement this requirement
during'nodification activities is an apparent deviation to
i commitments made to the NRC. (285/8527-01)
(Closed) Severity Level IV Violation 285/8429-01: Deficiency
report / quality report (DR/QR) responses were not received within
i
the 30-day requirement.
The NRC inspector reviewed a sampling of DR/QR reports to
determine if responses had been provided within the 30-day
requirement. No cases were noted where the response was
received more than 30 days from the date of issue of the DR/QR.
The licensee has established a program to ensure that responses
are received within the required time period. This program
includes issuance of a monthly DR/QR status report that
indicates all responses due and the individual responsible for
submitting the response, weekly distribution of the DR/QR status
list to all individuals on the list, and discussion by the
operations quality assurance supervisor of outstanding responses
with the plant review committee (PRC) members at the PRC
meetings. The licensee has made the appropriate procedure
changes to establish this program.
(Closed) Severity Level IV Violation 285/8501-01: Failure to follow
procedures for control of temporary critical quality equipment
(CQE) storage areas.
The NRC inspector randomly checked temporary CQE storage areas
on December 5 and December 23, 1985, to verify that storage of
materials in the areas was being done in accordance with
licensee procecural requirements. During the December 5 tour,
the NRC inspector noted that five of the nine areas checked did
not meet the licensee's requirements. Each area contained one
or more of the following problems: piping not capped or sealed,
, non-Q material stored in the area, purchase order numbers not
being transferred to remaining pieces when stock is cut, and
trash accumulation in the area. The noted problems were
discussed with licensee management personnel on
December 6.
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The NRC inspector also reviewed the quality control (QC) log to
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verify that the areas were inspected at least monthly by the
j onsite QC department. No problems were noted. The NRC inspector
l checked the temporary QC storage areas again on December 23 and
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found that three of the six areas did not meet the licensee's
requirements.
The licensee's response letter, dated March 28, 1985, to this
! violation stated that steps would be taken to ensure that the
problems identified by the violation would be corrected and that
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the areas would be maintained. The licensee's failure to
maintain the temporary CQE storage areas in accordance with
licensee requirements is an apparent deviation to commitments
made to the NRC. (285/8527-02) -
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3. Licensee Event Report (LER) Followup
Through direct observation, discussions with licensee personnel, and
review of records, the following event reports were reviewed to determine
that reportability requirements were fulfilled, immediate corrective
action was accomplished, and corrective action to prevent recurrence has
been accomplished in accordance with Technical Specifications.
The following LERs are closed:
l 84-008 Tube rupture in the 'B' steam generator
84-015 Polar crane carried load over reactor coolant system
! LER 84-008 reported a steam generator tube failure during a plant startup-
l from a refueling outage. The tube failure occurred in May 1984,'while
performing a hydrostatic test of the reactor coolant systen. The plant
was shutdown and the necessary repairs were made. The plant was
subsequently restarted and operated from July 1984, until September 1985
(cycle 9), when it was shutdown for refueling.
The licensee, in conjunction with Combustion Engineering, performed an
analysis to determine the cause of the tube failure. The results of the
l analysis indicated the failure was caused due to caustic-induced
l intergranular stress corrosion cracking. To minimize the possibility of
I additional tube failures, the licensee instituted programs during cycle 9
' to minimize caustic buildup in the steam generators. These programs
consisted of enhanced contrcl of contaminants entering the condensate and
feedwater systems, initiation of more restrictive secondary chemistry
guidelines and operating limits, improvements in steam generator
monitoring capabilities, and a soak / blowdown treatment process during
system startup to reduce the amount of contaminants in the steam
genera tor. The licensee also instituted a program to require an
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independent review of eddy current data. An independent review of the
data had not been performed during past eddy current tests.
The licensee performed eddy current tests on the steam generator tubes
during the refueling outage currently in progress. Based on the results
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of the test, the licensee plugged 16 tubes in the ' A' steam generator and
17 tubes in the 'B' steam generator. All the tubes plugged, except for a
total of five in both generators, were plugged due to denting. The
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remaining five tubes (two in the ' A' steam generator and three in the 'B'
steam generator) were plugged due to identified defects. None of the
identified defects were in the same area where the previous tube rupture
occurred.
The licensee intends to maintain the recently established programs to
minimize the probability of another tube failure.
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LER 84-015 reported an occurrence where the polar crane carried a load
greater than 250 pounds over the reactor coolant system (RCS) when the
pressurizer temperature was greater than 225 degrees F. This was a
violation of the station Technical Specifications. To prevent recurrence,
the licensee has added a note to the procedure for RCS vent and leak test
operating instructions to electrically tagout the polar crane prior to
exceeding 225 degrees F in the RCS. In addition, the licensee has also
installed a sign on the breaker for the polar crane noting the same
requirement. The NRC inspector noted that the breaker was tagged out
during the recent plant heatup as required by the procedure,
j No violations or deviations were identified.
.
4. Followup on IE Bulletin 83-07
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IE Bulletin 83-07, " Fraudulent Products Sold by Ray Miller, Inc.,"
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provided the licensee with infonnation regarding fraudulent material sold
by the Ray Miller Company. The licensee was requested to V:rify that they
had not used any material supplied by Ray Hiller.
The NRC inspector reviewed the licensee's response to IE Bulletin 83-07 to
verify that the responte was adequate and that the actions comitted to by
the licensee have been completed. The licensee has reviewed their quality
assurance (QA) records and verified that they have not received any
, fraudulent products from any of the companies listed in the bulletin. The
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licensee has also received a letter, dated March 22, 1984, from Combustion
Engineering stating that no Ray Miller material was supplied to the
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licensee. '
No violations or deviations were noted. This bulletin is considered
closed.
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5. Operational Safety Verification
The NRC inspector observed control room operations, reviewed cpplicable
logs, and conducted discussions with control room operators. The
inspector verified the operability of selected emergency systems, reviewed
tag-out records, verified proper return to service of affected components,
and ensured that maintenance requests had been initiated for equipment in
need of maintenance. The inspector also verified implementation of
radiation protection controls during observation of plant activities.
Na violations or deviations were identified.
6. Physical Plant Security and Safeguards
The NRC resident inspector accompanied the NRC region-based, safeguards
inspector on his routine, unannounced inspection. This effort was
performed to increase the sensitivity and knowledge level of the resident
inspector in the areas of security and safeguards. The resident inspector
also made spot checks to verify that the physical security plan was being
implemented in accordance with the station security plan. During tours of
the plant, the NRC inspector noted that some individuals inside the
protected area were not displaying their security badges in plain sight.
The NRC inspector notified the licensee of the problem. The licensee
posted a sign at the entrance to the protected area and issued a memo to
all badge holders to remind everyone of the requirement to wear their
badges in plain sight. Subsequent to these actions by the licensee, the
NRC inspector nuted on three different occasions, individuals not
displaying their security badges in plain sight. Failure to display a
security bad e is an apparent violation of Standing Order G-39.
(285/8527-03
7. Plant Tours
The NRC inspector toured accessible areas of the unit to observe plant
equipment conditions, including potential fire hazards, fluid leaks, and
excessive vibration. The inspector observed plant housekeeping and
cleanliness conditions during the tour.
The NRC inspector walked down the accessible portions of the containment
spray system. The walkdown was performed using Procedure OI-CS-1,
Revision 14, and Drawing E-2866-210-130, Revision 32. During the
walkdown, the NRC inspector noted discrepancies between the system
operating procedure, drawing, and the as-built plant. The discrepancies
noted were of a minor editorial nature. Licensee management was notified
of the discrepancies and stated '. hat the appropriate documentation would
be corrected.
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During the previous inspection period, the NRC inspector performed a
walkdown of various systems. The items noted during the walkdowns were
still being resolved at the end of the previous inspection period. The
licensee provided the NRC inspector the appropriate information regarding
the items. Based on this input, the discrepancies noted were of a minor
editorial nature, except for one item. During the walkdown, the NRC
inspector noted that there was a new valve installed on the emergency
diesel generator fuel oil filter. This unnumbered valve was not shown on
the drawing, nor was the talve listed on the valve lineup. The NRC
inspector requested to see the documentation related to installation of
the valve. The licensee las not yet provided the documentation. This
item is unresolved pending a determination of whether or not the valve was
installed per appropriate documentation. (285/8527-04)
- During plant tours, the NRC inspector noted that two fire barriers were
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not functional, as defined by the Technical Specifications. Fire Door
1007-8 was not completely closed due to a hose running through the door
1 and the guillotine fire curtain above Fire Door 1007-5 was inoperable
j due to a hose running through a ventilation port. The NRC inspector
i requested to see documentation to verify that an hourly fire patrol had
been established and was in effect at the time of the discovery by the NRC
inspector. The licensee had not located the necessary documentation.
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This item remains unresolved pending whether or not an hourly fire watch
had been established. (285/8527-051
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No violations or deviations were identified. .
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8. Monthly Maintenance Observation
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' Station maintenance activities of safety-related systems and components
listed below were observed to ascertain that they were conducted in
accordance with approved procedures, Regulatory Guides, and industry codes
or standards; and in conformance with Technical Specifications.
The following items were considered during this review: the limiting
conditions for operation were met while components or systems were removed '
l from service; approvals were obtained prior to initiating the work;
i activities were accomplished using approved procedures and were inspected
- as applicable; functional testing and/or calibrations were performed prior
! to returning components or systems to service; quality control records
!
were maintained; activities were accomplished by qualified personnel;
- parts and materials used were properly certified; radiological controls 7
l were implemented; and fire prevention controls were implemented.
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Maintenance orders (M0s) were reviewed to determine status of outstanding
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jobs and to ensure that priority is assigned to safety-related equipment
- maintenance which may affect system performance.
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The following maintenance activities were observed: ;
. Replacement of packing in valves HCV-1103, FW-169, and FW-170
(M0 851570, 851471, and 851507, respectfully)
. Coupling of the control element assemblies (f10 852446, Procedure !
. Inspection of auxiliary feedwater storage tank interior (M0 852785)
. Replacement of jumper wires in Limitorque motor-operated valves
(MR-FC-85-77)
No violations or deviations were identified.
9. Monthly Surveillance Observation
The NRC inspector observed the Technical Specification required
surseillance testing on the station battery (Procedure ST-DC-1-F.1) and I
verified that testing was performed in accordance with adequate
procrcures, test instrumentation was calibrated, limiting conditions for ,
operation were met, removal and restoration of the affected components j
were accomplished, test results conformed with Technical Specifications 1
other than the individual directing the test, and any deficiencies l
identified during the testing were properly reviewed and resolved by I
appropriate management personnel. The inspector also witnessed portions of l
the shutdown margin verification (Procedure ST-SDM-1-F.1'. l
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No violations or deviations were identified.
10. Unresolved Items
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An unresolved item is a matter about which more information is required in
order to determine whether it is acceptable, a violation, or a deviation.
Two unresolved items are discussed in this report in paragraph 7.
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11. Exit Interview j
The NRC inspector met with Mr. W. G. Gates (Plant Manager) at the end of !
this inspection. At this meeting, the inspector sunnarized the scope of :
the inspection and the findings. l
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