ML20197H017

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Insp Rept 50-285/97-19 on 971026-1206.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20197H017
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 12/19/1997
From: Johnson W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20197G998 List:
References
50-285-97-19, NUDOCS 9712310164
Download: ML20197H017 (16)


See also: IR 05000285/1997019

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ENCLOSURE.2

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U.S. NUCLEAR REGULATORY' COMMISSION

' REGION IV .

Docket No.:

50 295-

' License No.: .

. DPR-40 :

Report No.:

50 285/97 19

Licensee:

Omaha Public Power District

' Facility:

Fort Calhoun Station

Location:

Fort Calhoun Station FC 2 4 Adm.

P.O. Box 399, Hwy. 75 - North of Fort Calhoun

Fort Calhoun, Nebraska

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. Dates: .

October 26 through December 6,-1097-

Inspectors:

W. Walker, Senior Resident inspector

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V. Gaddy, Resident inspector

N. Salgado, Resident inspector

. Approved By:

W. D. Johnson, Chlet, Project Branch B

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ATTACHMENT:

Supplemental Information

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- 9712310164 971219

PDR

ADOCK 05000283

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EXECUTIVE SUMMARY -

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l Fort Calhoun ' Station .

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' NRC Inspection Report 50 285/97-19

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Ooerations '

' in general, the conduct of operations was professional and safety-conscious.

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However, the inspectors identified an atmosphere which was nonprofessional in that

breakfast was being ~ cooked in the main control room (Section 01.2). =

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' A weakness existed in the' licensee's controls for replacing burned out light bulbs in

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- that, after initial shift supervisor approval was obtained, no further approval was.

required even if the approved work was delayed 'or_ several days (Section 02.1).'

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The licensee's containment integrity operating instruction'was inadequate in that all

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containment penetrations needed to establish containment integrity were not

. included in the operating instruction (Section 02.2).

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Improper installation of a locking device on a raw water intet valve would not have

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prevented manipuistion of the valve (Section 02.3),

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Maintenance

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The inspectors determined that the licensee had a program for addressing

Model CR120A relay f ailures (Section M2).

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Inadequate corrective actions resulted in licensee personnel failing to properly test e .

containment penetration (Section M8.2).

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Enoineerino

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-In 1995, licensee personnel f ailed to perform an annual evaluation of nonfuel it' ems

in the spent fuel pool (Section E1.1).

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' Elant Suncort

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Radiation protection personnel were prompt in resolving housekeeping deficiencies

inside the radiologically controlled area (Section R2.1).

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Reoort Details

Summarv of Plant Status

Tne Fort Calhoun Station began this inspection period at 100 percent power and

maintained that level until November 14,1997. On November 14,1997, power was

reduced to 84 percent to facilitate repairs on the leaking stator cooling water heat

exchangers. On November 16,1997, repairs were completed and a power ascension

began with 100 percent power attained on November 17,1997. The platit reme;ned at

100 percent power throughout the remainder of the inspection period.

1. Operations

01

Conduct of Operations

01.1

General Comments (717071

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations, in general, the conduct of operations was professional

and safety conscious; specific events and noteworthy observations are detailed in

the sections below.

01.2 Control Room Observations (71707)

The inspectors observed control room activities during the early morning hours on

November 21,1997. The activities ongoing when the inspectors entered the

control room included cooking of breakf ast in the main control room area. This

activity did not provide a professional atmosphere in the control room. in addition,

several nonoperations personnel were eating in the control room and were not

oiscussing official business.

The inspectors reviewed the licensee's conduct of operations procedure and

determined that failing to ensure that all control room business is conducted in such

a manner that neither licensed control room operator attentiveness nor the

professional atmosphere of the control room is compromised is a violation of

Standing Order SO O 1, " Conduct Of Operations," Revision 36,(50-285/9719 01).

As a corrective actior., the manager of operations issued a memorandum to all

operations personnel stating that all cooking of food within the main control room

was to stop. Food was to be cooked in the designated kitchenette area and no food

or drink was alloweo over the main control boards in the control room. The

inspector: concluded that these actions were appropriate.

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'02.

Operational Status of Facilities and Equipment

02.1

Reolacement of Eauinment Indicatino Lichts

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a.

lDweetion Scooe (71707)

The inspectors reviewed the licensee's procedural controls for replacement of

burned out indicating bulbs.

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b.

- Observations and Findinos

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On November 3,1997, an electrical maintenance technician was replacing a burnod.

out indicating light bulb on the 125 Vdc manual transfer switch panel for Diesel

Generator 2. This switch would be used to transfer de control power for the diesel

generator from the normal source, which is Battery 2, to the emergency power

source, which is Battery 1. During the replacement of the bulb, a fuse failure made

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the transfer to the emergency (alternate) supply source for 125 Vdc power

inoperable. Based on Technical Specifications, the diesel was still considered

operable without the alternate source.

. The inspectors questioned the licensee regarding why work was being performed on

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Diesel Generator 2 when Diesel Generator 1 was out of service and inoperable for

preplanned maintenance. The licensee stated that the indicating light bulb

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replacement had originally been scheduled and approved by'the shift supervisor for

October 31. The indicating light bulb replacement was postponed until November 3.

Based on discussions with the electrical maintenance supervisor, it was expected

that the electrical maintenance technician would notify the control rocm again prior

to beginning replacement of the indicating light bulb on November 3. The electrical

maintenance technician failed to notify the control room prior to replacing the

indicating light bu'b. The inspectors considered this to be a weakness in the

licensee's work cuntrol process.

A risk assessment had been performed as required by the licensee's procedures prior

to beginning work on Diesel Generator 1. However, no risk assessment was

performed taking into account t.

adicating light bulb replacement on Diesel

Generator 2. Based on the inspectors' discussions with the risk assessment

personnel, the indicating light bulb replacement would not have been approved for

performance on November 3 with Diesel Generator 1 inoperable.

The licensee made the following changes to preclude this from recurring:

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All electrical maintenance personnel were counseled on proper

communicatic as with the control room immediately prior to replacing

indicating lights.

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' A warning sign will be posted at the' door of any inoperable diesel generator z

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. to inform plant personnel that work on the operable diesel ganerator is

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Conclusions .

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A weakness existed in the licensee's controls for replacing burned c ,t adicating

light bulbs in that, after initial shift supervisor approval was obtained, rn. Nrther

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- approval was required even if the approved work was delayed for several days.

- 02.2; Containment Inteoritv Verification

a.

insoection Scone (717071

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,The inspectors performed a. verification of containment integrity.

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b.

- Observations and Findinas

On November 19,1997, the inspectors performed a verification of containment

integrity using Operating Instruction Ol CO 5, " Containment Integrity," Revision 11.

While venfying the integrity of electrical and piping penetrations in the main steam

room using Checklist Ol CO-5 CL Di the inspectors identified that E.ectrical

Penetrations G1 through G4 and Piping Penetration H1 were not included on the

checklist. This operating instruction was used to verify that containment piping .

penetrations were properly capped and that the nitrogen pressure of containesnt

electrical penetrations was greater than 20 psig.

The inspectors informed system engineering persennel of the observation. System

engineering determined that the panetrations had been included in Revision 10 of

the operating instruction. However, while reiormatting the operating instruction for

Revision 11, these penetrations were omitted. Revision 11 became effective on

April 2,1997 : Revision 10 of the operating instruction was last performed during

the 1996 refueling outage. The inspectors reviewed Operating Instruction OI CO-5

and noted that it did not have a performance frequency. lThe inspectors asked if.

Revision 11 had been used to verify containment integrity. The licensee stated that

Revision 11 had been used to verify containment integrity during reactor startup

from the steam pipe rupture in May 1997. The licensee stated that performing

Operating Instruction Ol-CO 5 was a condition for satisfying Surveillance

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Test OP ST-CONT 0002, " Secured Closed, Containment Penetration isolation

Verification ".-The inspector verified that Surveillance Test OP-ST-CONT-0002 was

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documented as completed on May 8,1997. Section C.5 of. Surveillance

Test OP-ST CONT 0002 states, in part, t_ hat, in preparation for reactor startup,

= containment integrity has been established in accordance with Operating

Instruction OI-CO 5. Although in May 1997 the licensee performed Revision 11 of

Operating instruction OI CO 5 to verify the referenced surveillance, it was

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inedequate in that it did not include four electrical penetrations and one piping -

penetration for containment integrity verification (50-285/9719-02).

As corrective action, the licensee initiated Condition Report 199701506 to

document the deficiency, initiated a change to correct the procedur6, performed a

review of Operating instr 0ction Ol-CO-5, and verified that the penetrations met their

acceptance criteria. The inspectors verified that no Technical Specifications were

violated.

c.

Conclusions

The licensee's containment integrity operating instruction was inadequate in that all

containment penetrations needed to establish containment integrity were not

included in the operating instruction.

02.3 Imorocerlv Installed Lockina Device on Valve HCV-2812C

a.

Insoection Scoce (71707)

The inspectors reviewed the installation of locking devices on valves in the high

pressure safety injection system,

b.

Observations and Findings

On December 3,1997, the inspectors verified that locking devices were correctly

installed on several valves in the high pressure safety injection system. However,

the inspectors identified that the locking device on Valve HCV-2812C (raw water

inlet to High Pressure Safety injection Pump 2C bearing cooler) did not appear to

provide a physical restraint to prevent operation of the valve. The inspectors

questioned the licensee on this particular locking device and the auxiliary building

operator was sent to investigate. The auxiliary building operator deterrnined that the

locking device on the valve was incorrectly installed and did not provide a physical

restraint to prevent operation of the valve. The licensee's immediate corrective

action was to reinstall the locking device correctly. The licensee initiated Condition

Report 199701642 to further resolve the issue. The auxiliary building operator

erified that the valve was in its required closed position.

The inspectors reviewed Standing Order S0-O-44, " Administrative Controls For

Locking Of Cornponents," and noted that Valve HCV-2812C was required to be

locked closed. The standing order also stated that locking devices shall at the very

least provide a limited physical restraint on the operation of the valve. Failing to

ensure that the locking device installed on Valve HCV 2812C provided the required

physical res%nt was a violation (50 285/9719 03).

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Conclusions

The inspectors identified a violation of the licensee's administrative controls for

locking valves. The locking device on Valve HCV 2812C was improperly installed

and would not have prevented manipulation of the valve. The licensee promptly

initiated corrective action to properly lock the valve.

07.1 Licensee Safety Canmittee Activity

During the inspection period, the inspectors attended several sessions of the safety

audit and review committee. This is the offsite safety review committee for the Fort

Calhoun Station. The sessions attended included discussions on:

An integrated assessment schedule with oversight provided by the nuclear

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safety review group,

Closeout of several action items from previous meetings, and

Review of the quarterly trend report for the third quarter.

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The inspectors observed that Fort Calhoun Station senior management was present

as an active participant at the safety audit and review committee meeting. The

inspectors determined that the reviews and root cause analysis af events completed

by the nuclear safety review committee were rigorous and self-critical. The

inspectors concluded that the self-assessment activities observed were effective.

II. Maintenance

M1

Conduct of Maintenance

M 1.1 General Comments

a.

Insoection Scoce (62707)

The inspectors observed all or portions of the following activities:

Repair of Charging Pump CH-1B,

Troubleshooting the bypass transformer for Inverter 1,

Oilleak repairs on Feedwater Pump FW-48,

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Thermography on safety-related breakers, and

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Cleaning raw water / component cooling water Heat Exchanger AC-1C.

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Observations and Findings

The inspectors found the work' performed under these activities to be professional.

.nnd thorough. - All work observed was performed with the work package present .

and in active use. Maintenance technicians were experienced and knowledgeable of--

their assigned tasks., The inspectors frequently observed supervisors and system

engineers monitoring job progress, and quality control personnel were present when

required by procedure.-

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In addition, see the' specific discussions of maintenance obseved in Section M2,

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Conclusions

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- The maintenance activities observed were conducted in a controlled and professional

manner.

Mi.2 - Surveillance Activities

a.

Insnection Scoce (61728)

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The inspecto'rs observed all or portions of the following surveillance activities:

OP ST DG-0002, Diesel Generator 2 Check," Revision 24;

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OP ST OF 3002, " Diesel Generator 2 Fuel Oil System Pamp inservice Test,

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Revision 15;

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OP ST-DG-0001, " Diesel Generator 1 Check," Revision 23; and

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OP-PM AFW-0004, " Third Auxiliary Feedwater Pump Operability

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Verification," Revision 12. .

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.Qbservations and Findinos -

b.

Surveillance activities were generally completed thoroughly and professionally. The

inspectors noted that. in all of the safety related surveillances observed, a test

monitor was present and actively involved in ensuring that procedures were

completed exactly as written and that any changes needed to ensure the accuracy

' of the procedures were identified for revision,

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Conclusions -;

The surveillance activities observed by the inspectors were completed in a controlled

- manner and in accordance with procedures.

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M2

Maintenance and Material Condition of Facilities and Equipment

M2.1 Review of Material Condition durina Plant Tout.s

a,

jnsoection Scoce (62707)

The inspectors followed up on the failure of a relay in the back panels of the control

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room.

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b.

Observations and Findinas

On November 29.1997, at 5 a.m., the opvators in the control room detected a

burning smell and immedia:ely began searching for the cause. The smell was

strongest in the walk-in back panel area behind Contro' Boards 1, 2, ar.d 3 in the

control room. While the operator was M the back panel, Relay A14A K11 caught

fire and was immediately extinguished with a carbon dioxide fire extinguisher. The

fire lasted less than 1 minute and the licensee entered Abnormal Operating

Procedure AOP-06, " Fire Emergency," for 1 minute.

The main equipment effected by the relay failure was the loss of pressurizer ievel

control when Pressurizer Channel X failed low. This caused the letdown isolation

valve to go closed and one of the two charging pumps in service to trip, as

expected. The operators then secured the second charging pump and letdown was

isolated for approximately 20 minutes while the operators transferred pressurizer

level control to Channel Y and then restored letdown. No power fluctuations were

observed and all equipment functioned as expected.

The inspectors discussed the relay f ailure with the system engineer and were

informed that the relay was a General Electric, Model CR120A,120 Vac,

continuously energized relay. The inspectors discussed with the system engineer

whether similar failures had beer, observed. The system engineer provided the

8cllowing information on the relays and f ailure history:

There are 596 Model CR120A relays installed in 1.ie plant.

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In the mid to late 1980's the licensee identified degradation from excessive

heat on Model CR120A relays in dc applications and began a systematic

replacement of these relays.

Criteria for selecting which relays to replace was: de application, normally

energized, critical quality element, and operational difficulties could be

caused by the failure of the relay.

165 relays were identified for replacement.

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Four Model CR120A relays in de applications and one relay in an ac

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application had f ailed in the last 3 years.

Additional data provided from the plant computer database indicated that a

total of 12 relays 10 de applications and two relays in ac applications had

f ailed since 1985.

The inspectors discussed with the system engineer whether the rotay which f ailed

would be sent out for a root cause determination. The system engineer stated that,

due to the age of the relay, the f ailure was considered to be age related, and no

further analysis was planned. The system engineer also stated that no plans existed

for replacement of the Model CR120A relays in ac applications since only two

f ailures had been identified since 1985,

c.

Conclusions

The inspectors determined that the licensee had a program for addressing

Model CR120A relay f ailures. Systems engineering personnel had implemented and

nearly completed a program for replacement of the de relays most susceptible to

f ailure. A similar program for replace.nent of ac relays had not been implemented

due to the limited number of f ailures.

M8

Miscellaneous Maintenance issues

M8.1 (Closed) Insoector Foliowon item (IFil 50 285/9718-04: diesel generator field

flashing circuit. On September 17,1997, the inspectors observed a normal start of

Diesel Generator 1. During the test, the electrical field for the generator failed to

flash. The electrical maintenance technicians identified that a diode in the field

flashing circuit was degraded. Based on testing of the field flashing circuit and the

vendor's recommendation, the diode was replaced in both diesel generators. T he

inspectors followed up on the maintenance history regarding degradation of the

diode in the field flashing circuit for the diesels. No previous indications of the diode

being degraded were identified. Additionally, the inspectors reviewed

documentation for the design application for the diesel generator field flashing circuit

diodes and found them to be appropriate.

MB.2 (Closed) Licensee Event Renart (LER) 50-285/96-13: fai'ure to satisfy surveillance

requirement for Containment Penetration M-80. On November 16,1996, the

licensee discovered that a pipe nipple, used to pressurize Containment

Penetration M-80 for leak rate testing, did not penetrate the system piping. The

licensee's record review indicated that tests performed during the 1993 and

1995 refuelir's outages using this pipe nipple were invalid as a result of this

problem.

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Containment Penetration M 80 and associated boundary valves werd not checked

' for leakage as required by Technical Specification 3.5(5) since no pressure was

applied to the penetration.

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The licensee performed a root cause analysis that determined the cause of the event

to be a lack of complete and thorough corrective action. Piping system nipples

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which did not penetrate piping boundaries had been previously identified by the

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licenseo in 1993. However, the corrective actions taken failed to identify and

resolve the concern for Containment Penetration M 80.

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The licensee's current corrective action included modifying the pipe nipple to

pressurize Containment Penetration M-80. .The Technical Specification required leak

rate test was subsequently performed satisfactorily.- The licensee also performed a

review of all similarly configured penetrations to verify that no other blocked or

undrilled pipe nipples were being used for leak rate testing. No other problems were

identified;

Failing to perform the Technical Specification required leak rate test is a violation.

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Th;s nonrepetitive, licensee-identified and corrected violation is being treated as a

noncited violation consistent with Section Vll.B.1 of the NRC Enforcement Policy

(50 285/9719-04).

111. Engineering

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Conduct of Engineering

E1.1

Soent Fuel Pool inventorv Review

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a.

insoection Scooe (71707)

The inspectors performed an evaluation to assess the licensee's control of material

stored in the spent fuel pool.

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b,

dbservations and Findinas

On November 17.1997, the inspectors performed an inventory of items stored in

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the spent fuel pool and assessed the foreign material exclusion controls of the spent

. fuel pool and the area immediately adjacont to the spent fuel pool. Spent fuel pool

inventory was controlled ny Standing Order S0-0-47, " Spent FuelInventory

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Control," and cleanliness was controlled by Standing Order S0-M 10, " Foreign

. Material Exclusion."

The inspectors obtained a copy of the spent fuel pool inventory ledger. This ledger

contained a list of all nonfuel items stored in the spent fuel pool. The ledger

contained 10 entries. The inspectors verified that these nod

items were in the

spent fuel pool.

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During the inspection, the inspectors noted the area immediately surrounding the

pool was free of debris. Allitems wero properly anchored or secured. However, the

inspectors did note a few discrepancias with the _ foreign material exclusion logs.

The inspectors noted five entries from September 1996 and one entry from

November 7,1997, which indicated inaterial had entered the foreign material

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exclusion area but had not been logged as being removed from the area. During the

inspection, the inspectors could not find these items. The reactor engineer indicated

that the log should have been updated to show that the items had been previously

removed.

The inspectors also noted a plastic bucket hanging from a rope inside the spent fuel

- pool. The inspectors asked the reactor engineer about the bucket. The reactor

enginaer stated that two plastic buckets were actually inside the spent fuel pool.

The reactor engineer cisad that one plastic bucket had been inside the pool since

1994 and the oth sr since 1930

i..a reactor engineer stated that the buckets were

on the spent fuel )ool inventory Itciger. The inspectors asked if the licensee had

performed an evalJation to determine what effect the spent fuel pool environment

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(radiation, thermalt would have on the two plastic buckets. The reactor engineer

stated that, in 1916, he gave a verbal authorization to allow the buckets to remain

inside the spent fuit pool because Standing Ordr.r *0-0-47 did not require that a

written evaluation Ls performed. The reactor engineer stated that he based this

decision on the fact ti,et the plastic buckets were located inside a stainless steel

basket and, if the plastic buckets degraded, their contents would be captured by the

stainless steel basket.

Standing Order SO O 47 required the licensee to annually evaluate nonfuelitems in

the spent fuel pool. The licensee stated that, in 1995, the reactor engineer did not

perform this annual evaluation. Failing to perform the annual inventory evaluation of

nonfuelitems in 1995 is a violation. Once identified, the licensee performed the

annual evaluation. This licensee-identified and corrected violation is being treated as

a noncited viciation consistent with Section Vll.B.1 of the NRC Enforcement Policy

(50-285/9719 05).

Standing Ordar S0-O 47 did not require that nonfuelitems deposited into the spent

fuel pool be evaluated by the reactor engineer prior to being placed in the spent fuel

pool. However, the standing order did require that annual evaluations of nonfuel

items inside the spent fuel pool be performed. Since the spent fuel pool inventory

control standing order failed to require nonfuelitems to be evaluated by the reactor

engineer prior to being placed in the spent fuel pool, nonfuel items could be in the

spent fuel pool for a year before being evaluated to determine their compatibility

with the spent fuel pool. The inspectors discussed with the rmtor engineer

whether nonfuel items were evaluated prior to placing them in the spent fuei pool.

The reactor engineer stated that it was his practice to evaluate nonfuel items prior

to placing them in the spent fuel pool.

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Condusions

The npent fuel pool inventory control program did not require nonfuelitems be

evalJated to determine their compatibility with the spent fuel pool prior to being

pla;ed in the spent fuel pool. The inspectors considered this to be a weakness in

ths spent fuel pool inventory control program. Failure to perform the 1995 annual

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e'ialuation of nonfuel items in the spent fuel pool resulted in a noncited violation,

IV. Plant SuoRQd

R2

Status of Radiological Protection and Chemistry Facilities and Equipment

R2.1 Badioloaicallv Conitolled Area Housekeeoina

a.

Inspegion and Scoce (71750)

The inspeu: ors assessed housekeeping inside the radiologically controlled area.

b.

Qhigtvations and Findinas

During the inspection period, the inspectors made numerous hourokeeping tours

throughout the radiologically controlled area, in general, the inspectets noted thct

housekeeping was good with a few exceptions. On October 31,1997, the

inspectors noted severalitems had been left inside the contamination boundary of

Containment Spray Pumps SI 38 and SI 3C. Inside the contamination boundary of

Containment Spray Pump SI 38, there was a plastic bag, a pair of rubber gloves,

and a pair of cloth gloves, inside the contamination boundary of Containment Spray

Pump SI 3C, there was a lab coat, rubber gloves, and cloth gloves.

On November 17,1997, the inspectors noted housekeeping weaknesses in

Drumming Room 27. The inspectors noted an open bag of trash labeled radioactive

materiallying on the floor in the room. Fart of the trash had spilled onto the floor.

The inspectors asked radiation protection personnelif the trash was contaminated.

Radiation protection personnel stated the trash had been removed from clean areas

inside the plant and it was not contamiliated in each instance, radiation protection

personnel immediately resolved the inspectors' housekeeping concerns.

c.

Conclusions

Radiation protection personnel were prompt in resolving housekeeping deficiencies

inside the radiologically controlled area.

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V. Manaamment Meetinas

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Exh Meetinc Summary

The inspectors presented the inspection results to members of licensee management

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-on December 8,1997. The licensee, acknowledged tha findings as presented. .

The inspectors asked the licensee whether any materials examined during the

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inspection period should be considereo proprietary. No proprietary information was

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identified.

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- ATTACHMENT

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SUPPLEMENTAL INFORMATION

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PARTIAL LIST OF PERSONS CONTACTED--.

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Licensee

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M. Bare, System Engineer?

D. Buell, System Engineer .

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J. Chase, Manager, Fort Calhoun Station

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D. Dryden, Station Licensing Engineer-

M. Ellis,' Supervisor, Maintenance Support

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- J. Foleyt System Engineer-

-

T. Gurtis,- Electrical Maintenance Supervisor

i R. Phelps, Manager, Station Engineering

R. Short, Manager.. Operations

'

C. Stafford, Reactor Engineer.

INSPECTION PROCEDURES USED

'

IP 37551:

_ Or. site Engineering -

.

'

. IP 61726:

- Surveillance Observations

. IP 62707:

Maintenance Observations.

IP 71707:

. Plant Operations -

- IP 71750:

Plant Support Activities

,

ITEMS OPENED AND CLOSED

'

Openad

~.50 285/9719 02

VIO

inadequr,:a containment integrity operating instruction

l

(Section 02.2)

.

-

50 285/9719 03

VIO

improperly installed locking device (Section 02.3)

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- C101ad

y

"

50 285/9718-04

IFl -

~ diesel generator field flashing circuit (Section M8,1)

50 285/96 13:

LERL failure to satisfy surveillance requirement for Containment

i

- Perietration' M 80 (Section M8.2)

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Onanad_and_ Closed

-

50 285/9719-01.

_.VIO.

- cooking in main. control room area'(Section 01.2) -

-

_

.> '

-50 285/9719-04:-

NCV ' fsiling to satisfy surveillance requirement for containment'

3

'

' Penetration M-80 (Section M8.2):

50 285/9719 05;

- NCV falling to perform annual inventory evaluation of nonfuel items -

,

.,'

(Section E1.11

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