ML20207H731

From kanterella
Jump to navigation Jump to search
Insp Rept 50-285/88-23 on 880701-31.Violations Noted.Major Areas Inspected:Previously Identified Items,Operational Safety Verification,Plant tours,safety-related Sys Walkdown & Monthly Maint,Surveillance & Security Observations
ML20207H731
Person / Time
Site: Fort Calhoun 
Issue date: 08/19/1988
From: Harrell P, Reis T, Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20207H720 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-2.D.1, TASK-2.E.1.1, TASK-TM 50-285-88-23, IEB-88-004, IEB-88-005, IEB-88-4, IEB-88-5, IEIN-88-046, IEIN-88-46, NUDOCS 8808300008
Download: ML20207H731 (38)


See also: IR 05000285/1988023

Text

--

-

.-

.

..

..

i

.

p

..

1

-q

f

!

APPENDIX B

,

U. S. NUCLEAR REGULATORY COMMISSION

l

REGION IV

i

.

>

t.

l

NRC Inspection Report: 50-285/88-23

License:

DPR-40

l

Docketi 50-285

i

l

Licensee: Omaha Public Power District

l

~

1623 Harney Street

.

,

',

Omaha, Nebraska 68102

~

Facility Name:

Fort Calhoun Station

Inspection At:

Fort Calhoun Station, Blair, Nebraska

!

Inspection Conducted: July 1-31, 1988

l

-

Inspector:

RW

6-4- 6D

i

% H.\\Harrell, Senior Resident Reactor

'Date

infector

i

O

i

l

'v

M

B-+ -88

l

T. Reis, Resideht Reactor Inspector

Date

l

Approved:

_

.

-

T /f [8

T. F. Wes'te . n. Chief Project

DatW

(

!

'

Section E(, D' vision of Reactor Projects

(

1

l

l

l

l

i

8808300008 880919

ADOCK0500g5

DR

,

,

.

2

Inspection Summary

i

i

Inspection Conducted July 1-31, 1988 (Report 50-285/88-23)

Areas Inspected:

Routine, unannounced inspection including review of

1

previously identified items, operational safety verification, plant tours,

safety-related system walkdown, monthly maintenance observations, monthly

surveillance observations, security observations, radiological protection

j

observations, in-office review of periodic and special reports, review of

licensee activities on NRC Bulletin 88-05, review of licensee activities

related to the instrument air water intrusion event, followup on NRC

Information Notice 88-46, followup on NUREG-0737 (TMI), Item II.E.1.1.1, and

nonlicensed training.

i

1

Results: Within the 14 areas inspected, 2 violations (failure to properly

store unused ion exchange resins, paragraph 5; and failure to provide adequate

'

procedures for startup of the instrument air system, paragrapn 13) were

identifted,

j

i

,

,

i

,

,

,

,

3

DETAILS

1.

Persons Contacted

  • K. Morris, Division Manager, Nuclear Operations
  • W. Gates, Plant Manager

C. Brunnert, Supervisor, Operations Quality Assurance

T. Dexter, Supervisor, Security

  • J. Drahota, Supervisor, Maintenance Support

J. Fisicaro, Supervisor, Nuclear Licensing and Industry Affairs

J. Foley, Supervisor, Instrumentation and Control

K. Miller, Supervisor, Maintenance

  • C. Simmons, Onsite Licensing Engineer
  • R. Jaworski, Manager, Station Engineering

J. Kecy, Reactor Engineer

  • D. Matthews, Supervisor, Nuclear Licensing
  • S. Trausch, Supervisor, Operations
  • T. Patterson, Assistant Plant Manager
  • G. Roach, Supervisor, Radiation Protection

R. Scofield, Supervisor, Outage Projects

  • F. Smith, Plant Chemist
  • L, Wigdahl, Supervisor, Technical Training
  • S. Willrett, Manager, Administrative Services
  • Denotes attendance at the monthly exit interview.

The NRC inspectors also contacted other plant personnel, including

operators, technicians, and administrative personnel.

2.

Plant Status

During the period of July 1-31, 1988, the plant operated continuously at

90 percent power.

No plant trips, safety system challenges, or other

'

abnormal plant operations were experienced.

The plant was operated at 90

percent power due to the inability to maintain condenser vacuum at higher

power levels.

The inability to maintain vacuum was attributed to

abnormally high river (condenser cooling water) temperatures and

biofouling in the main condenser.

See paragraph 4.b for a discussion of

p"oblems with the main condenser.

On July 5, 1988, the FCS set a record for Combustion Engineering (CE)

designed plants by operating continuously for 394 days.

The previous

record for CE plants was held by Maine Yankee at 393 days.

At the end of

this inspection period, the FCS had generated power for 420 continuous

days.

3.

Review of Previously Identified Items (92701)

a.

(Closed) Severity Level IV Violation 285/8634-03:

Failure to operate

the waste gas panel (AI-110) in accordance with approved procedures.

,

.

.

O

4

This violation involved the failure of the licensee to properly

perform a valve alignment when placing AI-110 in the standby mode.

This violation was previously reviewed and thc review was documented

in NRC Inspection Report 50-285/87-33.

As noted in the report, the

licensee had not provided training to the chemistry technicians for

operatien of AI-110.

To address the training of chemistry technicians on AI-110, the

licensee issued a performance evaluation checklist (PEC) as Lesson

Plan 19-67-05.

This PEC provides the requirements for the

performance of practical factors by each chemistry technician for

operation of AI-110.

Successful completion of the PEC provides each

chemistry technician with the training necessary to ensure

satisfactory operation of AI-110.

The NRC inspector reviewed Lesson Plan 19-67-05, Revision 0, to

verify that the plan contained the appropriate elements for training

on the operation of AI-110.

No problems were noted.

The NRC

inspector also reviewed training records to verify that all chemistry

technicians had received the training.

No problems were noted.

b.

(Closed) Unresolved Item 285/8710-05:

Review of the amount of

triso1ium phosphate dodecahydrate (TSP) stored in containment.

"

This item was related to an apparent discrepancy between the

Technical Specifications (TS) and the Updated Safety Analysis Report

(USAR) as to how much TSP should be stored in containment.

The TS

states that 40 cubic feet is required; whereas, the USAR states that

3000 pounds of TSP is required.

-

Previous reviews of this item were performed to verify that a

sufficient amount of TSP was stored in containment to meet the

requirements of TS 3.6(2)d.

Previous reviews performed on this item

are provided in NRC Inspection Reports 50-285/87-13, 50-285/87-24,

and 50-285/88-03.

The purpose of this review was to verify that the

licensee had updated the USAR to provide a specific narrative on the

requirements for the amount of TSP to be stored in containment.

On July 22, 1988, the licensee issued a revision to Section 4.4 of

the USAR.

The revised narrative clearly describes the relationship

between the USAR requirement of 3000 pounds of TSP and the TS

requirement of 40 cubic feet of TSP.

The NRC inspector reviewed the USAR revision to verify that the USAR

and TS relationship was clearly defined.

No problems were noted,

c.

(Closed) Severity Level IV Violation 285/8710-07:

Inadequate

procedure for performance of containment local leak detection tests.

,

.

. - - .

- . - -

.

.

-

- .

.

. . .

- . .

. .

.

_

_

.

_.

.

.

.

,

,

5

5

This violation was related to the failure of the licensee to issue a

procedure that provided adequate instructions for performance of

containment local leak rate tests.

The procedure was inadequate in

'

that the instructions provided to the technician did not reflect the

actual as-built conditions of the plant.

a

,

'

in response to this violation, the licensee performed a walk down to

correct the deficiencies in Procedure ST-CONT-3, "Containment

,

Isolation Valves Leakage Rate Test - Type C."

In addition, the

!

licensee also issued a lesson planito be used to instruct technicians

in the proper methods of performing' leak rate testing.

An

instructional class was presented to the technicians to ensure that

the' technicians had received the training prior to the upcoming

refueling outage.

The NRC inspector reviewed selected portions of Procedure ST-CONT-3

,

to verify that the instructions provided in the procedure accurately'

s

reflected the plant as-built conditions.

No problems were noted

during review of the procedure.

The NRC inspector also reviewed

training records to verify that plant technicians had attended the

training class on leakage testing.

,

)

Based on the review performed by the NRC inspector, it appeared that

i

the licensee had taken appropriate actions to address this violation,

j

d.

(Closed) Unresolved Item 285/8724-02:

Review of the licensee's

i

program for submission of reports in accordance with

10 CFR Part 50.73.

-

This item involved an occurrence where the licensee did not report

.

,

problems identified with the emergency feedwater storage tank

(EFWST).

The problems identified in the EFWST were related to

,

!

deficient welds in the tank.

.

4

i

Violation 285/8727-08 was issued in NRC Inspection Report 50-285/87-27

!

!

to address the issue of the licensee's program for submission of

l

reports required by 10 CFR Part 50.73.

A review of this issue will

'

be performed during closecut of the violation.

!

I

e.

(Closed) Open Item 285/8730-01:

Failure to consider all information

in the issuance of a justification for continued operation.

This item was related to a special inspection performed by an NRC

l

Region IV team in November 1987 to follow up on the water intrusion

'

event that occurred in July 1987.

During the inspection, the team

i

noted that the licensee had failed to consider all available

information during preparation of a justification of operation (JCO)

'

for addressing continued plant operation.

The licensee issued a revision to the JC0 on April 7, 1988, to

/

address the concerns identified by the team.

The licensee continued

l

4

i

1

i

. .

.

_

o

>

._

,

,

r

e

,

-;

6

.

!

to revise the JC0 based on new inf)rmation obtained as testing of

,_

accumulator assemblies was completed.

On April 27, 1988, the

,

t

licensee issued the final JC0 to address operability of the plant.

The JC0 was transmitted to the NRC's Office of Nuclear Reactor

i

Regulation (NRR) for review.

Open Item 285/8815-12 was issued in NRC

>

Inspection Report 50-285/88-15 to formally track the completion of

'

.

the review of the JC0 by NRR.

This item will be reviewed during the

'

performance of the follow up on the open item.

f.

(Closed) Severity Level IV Violation 8730-02:

No procedures existed

to preclude the mispositioning'of valves, breakers, or switches by

noncperatinns personnel.

'

,

-

'

This item was related to the failure of the licensee to issue a

i

procedure that addressed operation'of plant equipment by personnel

l

j

not on the operations staff.

'

This violation was formally issued as Violation 285/8727-06 in NRC

Inspection Report 50-285/87-27.

The probical identified by this

'

violation will be addressed when the licensee's action in response to

Violation 285/8727-06 is reviewed.

g.

(Closed) Open Item 285/8733-02:

Shift chemistry technicians not

i

answering pages by the control room.

This item involved the failure of the shift chemistry technician to

)

answer eight pages made by the control room during the lunch period.

l

This item also involved the failure of the shift health physics (HP)

l

technicians to answer control room pages,

i

i'

To ensure that pages are promptly answered, the chemistry and HP

l

technicians were instructed by their manager that attention to the

'

paging system was mandatory and that prompt answering of pages was

2

required.

In addition, the licensee revised Form FC-15, "Operators

,

Work Schedule," to include the names of the individuals acting in the

i

capacity of shift chemistry and HP technicians.

By providing the

,

.

names of the individuals to the control room staff, the technicians

>

j

can be paged by name rather than by position.

The licensee also

established a policy whereby the shift chemistry and HP technicians

l

report to the shift supervisor at the beginning of.each shift.

Prior

to this observation being made by the NRC inspector, the chemistry

i

,

and HP technicians rarely visited the control room.

i

,

The NRC inspector has verified during routine tours of the plant that

i

the technicians are routinely responding to their pages.

.

Verification of answsring the pages was made by ensuring the

I

i

individual listed on Form FC-15 as the shift technician was not being

i

paged more than once or twice before answering.

The NRC inspector

i

has also noted during tours of the control room that the technicians

are visiting the control room in accordance with the newly

j

established policy.

4

1

!

)

1

_

.

_

.

.

..

.

.o

,

o

7

h.

(Closed) Open Item 285/8807-01:

Revision to Procedure E0P-20 to

provide instructions to operations personnel.

This item involved the need to issue a revision to Procedure E0P-20,

"Functional Recovery Procedure," to provide instructions.to

operations personnel to manually shut Valves HCV-385 and HCV-386,if

,

the plant goes into the containment recirculation mode.

The

procedure revision was necessary because the installed air

accumulator assemblies canr.ot meet the design criteria of holding the-

valves shut for 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />.

,

The NRC inspector revieweo Procedure'E0P-20, Revision 2, dated

March 14, 1988, and noted that the licensee had included instructions

for the operations staff.

The instructions state that the operator

shall manually shut Valves HCV-385 and HCV-386 within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the

,

loss of instrument air system if the plant is operating in the.

t

containment recirculation mude.

The NRC inspector noted that the

4-hour time limit is appropriate since the licensee has functicnally

J

tested the valve accumulator assemblies and verified the assemblies

'

will hold the valves shut for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

i.

(Closed) Open Item 285/8815-01:

Submission of the licensee'r,

schedule for completion of testing of the safety-related air

l

accumulator assemblies.

This item involved a commitment made by the licensee to submit a

,

schedule to the NRC for the completion of testing of the air

!

,

accumulator assemblies.

1

In discussions between'the NRC inspector and licensee management on

i

instrument air matters, as discussed in paragraph 13 of this report,

[

licensee management verbally committed that the testing of the air

4

accumulator assemblies would be completed prior to the end of the

upcoming refueling outage.

This item is discussed in this inspection

'

report to formally document the verbal commitment made by licensee

'

management.

I

i

j

4,

Operational Safety Verification (71707)

The NRC inspectors conducted reviews and observations of selected

,

activities to verify that facility operations were performed in

i

con'ormance with the requirements established under 10 CFR, the licensee's

{

administrative procedures, and the TS.

The NRC inspectors made several

control room observations to verify the following:

Proper shift staffing

.

Operator adherence to approved procedures and TS requirements

.

Operability of reactor protective system and angineered safeguards

j

.

equipment

<

i

,

. - . _

_

_.

.

,

.

8

Logs, records, recorder traces, annunciators, panel indications,-and

.

switch positions complied with the appropriate requirements

Proper return to service of components

.

Maintenance orders (MO) initiated for equipment in need of

<

.

maintenance

Appropriate conduct of control room and other licensed operators

.

Management personnel toured the control room on a regular basis

.

A discussion of the events that occurred during this inspection period is

provided below:

a.

At approximately 7:30 p.m. on July 19, 1988, the licensee experienced

a fire in a flammable liquid storage cabinet located in the water

plant.

During a routine tour of the water plant, an operator noted

smoke coming out of the cabinet.

The operator immediately notified

the control room and the fire alarm was sounded.

The fire brigade

arrived on the scene at approximately 7:35 p.m. and extiriguished the

fire at approximately 7:43 p.m.

The Blair, Nebraska, Fire Department

was alerted and was on standby to assist if required.

No assistance

was needed.

Once the fire was extinguished, all containers inside

the locker were moved outside of the water pl6nt building.

The water

plant building is not located near any safety-related equipment or

security vital areas; therefore, the fire posed no threat to the

safety or security of the plant.

Based on the investigation performed by the licensee, the fire was

attributed to the careless handling of epoxy paint by maintenance

personnel.

Personnel were painting the floor of the new maintenance

shop with epoxy paint.

The paint is a mixture of two parts that is

applied to the floor and allowed to dry by means of an exothermic

chemical reaction.

At the end of the work day, maintenance personnel

had some of the mixture left over and stored it in the locker for use

the next day.

Once the paint was stored in the cabinet, the

exothermic reaction continued and generated sufficient heat to cause

the other chemicals stored in the cabinet to ignite.

In response to this event, the licensee took corrective actions for

all flammable storage cabinets in the plant.

The actions taken by

the licensee are listed below.

The supervisor of maintenance met with all maintenance personnel

.

to disuss the preper storage of chemicals in the storage

lockers, the types of chemicals that cannot be stored in

lockers, and the proper technique for disposal of 2 part epoxy

paint.

-

.

.

.

.

9

A check of all storage cabinets in the plant was made and

.

unnecessary chemicals were removed.

No toxic chemicals were

found in any of the cabinets.

Removed and/or relocated cabinets that were not in the immediate

.

area of the fire detection system.

The cabinet in the water

,

plant was not in the area of fire detection equipment.

Initiated a preventive maintenance requirement for a monthly

.

inspection of all cabinets.

The first inspection will be

performed in August 1988.

i

A review was performed by a representative from the authorized

.

.

I

nuclear insurer.

The representative stated that the licensee

l

has established good control of the flammables used at the

plant.

i

The NRC inspector reviewed the actions taken by the licensee.

Based

on the review, it appeared that appropriate corrective actions were

implemented by the licensee.

The licensee reported this event to the NRC Headquarters duty officer

,

l

via the emergency notification system on July 19, 1988.

Subsequent

!

to the event, the licensee performed a review for reportability under

I

the requirements of 10 CFR Part 50.73.

Based on the review, the

licensee determined that the issuance of a licensee event report

(LER) was not required; therefore, the licensee will not be issuing

an LER.

The NRC inspector reviewed the requirements for

reportability stated in Part 50.73 and concurred with the licensee's

determination that the submission of an LER was not required.

b.

The plant recently experienced a reduction in the efficiency of the

,

main condenser that has required the plant to operate at 90 percent

power instead of 100 percent.

The licensee hired a consultant to

initiate a study of the reasons for the loss of efficiency.

The

J

consultant determined that the lost efficiency was partly due to the

abnormally high temperature of the river (condenser cooling water)

and partly due to biofouling of the condenser tubes.

The licensee

has not previously experienced any biofouling problems; however,

because the river temperature has been abnormally high for a long

period of time, an environment for growing microorganisms has been

available.

In response to this problem, the licensee initiated the injection of

chlorine into the circulating water system.

The chlorine is being

,

injected to kill the microorganisms.

The licensee has established plans to inspect the interior of the

main condenser during the upcoming refueling outage.

The licensee

also plans on inspecting the component cooling water heat exchangers

during the outage.

Based on the results of these inspections, the

i

.

_-

_

.-

,

,

10

'

licensee will decide what actions, if any are required, will be taken

,

to prevent biofouling of the heat exchangers,

i

c.

The licensee recently added.the check valves (RW-115, RW-117, RW-121,

and RW-125) for the four raw water (RW) pumps to the inservice

inspection program._ The check valves were added to the program in

'i

order that the valve back leakage could be quantified.

The leakagt!

was.to be determined _so that the-licensee would not have to upgrade

the air accumulator assemblies of the four RW pump discharge valves

(HCV-2850, HCV-2851, HCV-2852, and HCV-285t) to a CQE (safety-related)

i

status.

The testing of check valve leakage was first performed

during this inspection period and the leakage was found to be excessive.

The discharge flow from~t_he RW pumps supply a common header,

The

pump discharge valves are normally open when the pump is running and

normally shut when the pumps are secured.

The valves are

air-operated and fail open on the loss of instrument air pressure.

Because the pump check valves, leaked excessively and because the pump

discharge valves fail open on a loss of instrument air, the licensee

t

could not be certain that sufficient RW flow could be provided to the

4

component cooling water (CCW) heat exchangers for plant shutdown in

all possible scenarios.

_ ith the pump discharge valve failing open

W

and the pump check valve leaking excessively, some of the flow needed

by the CCW heat exchangers would be lost through an idle pump.

I

To address this problem, the licensee upgraded the air accumulator

!

assemblies for the RW pump discharge valves to a CQE status.

The-

licensee did this by installing tested check valves in the air supply

d

i

line and performed calculations to verify that the accumulator

assemblies were seismically installed.

This item remains open

pending a review of the actions taken by the licensee to upgrade the

.

air accumulator assemblies on the RW pump discharge valves by the NRC

1

inspector.

(285/8823-01)

3

During review of this item, the licensee identified an apparent

i

J

discrepancy between the TS and the USAR.

Section 9.8 of the USAR

states that two RW pumps are required to supply sufficient flow to

the CCW heat exchangers to shut down the plant.

TS 2.4 allows the

licensee to take one RW pump out of service indefinitely without

entering a limiting condition for operation (LCO).

The plant is

'

designed such that RW Pumps A and B are supplied alectrically by

Emergency Diesel Generator (EDG) I and the RW Pumps C and D are

supplied by EDG 2.

In the event that RW Pump A was out of service

for maintenance and EDG 2 failed to supply power to the vital bus

during a loss of offsite power, then only RW Pump B would be

-

t

l

available to supply water to the CCW heat exchangers.

To correct

j

this apparent problem, the licensee voluntarily increased the

requirements of TS 2.4.

Whenever one of the RW pumps is removed from

service, the licensee voluntarily enters a 7-day LCO.

If the pump is

]

not repaired within 7 days, then the plant shall be placed in hot

l

.

.

.

.

.

.

.

.

,

,

.

11

,

shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

Previously these actions were

required when two pumps were removed from service.

Correspondingly,

the LCO action statements for two and three pumps have also been

upgraded by the licensee.

The licensee stated that the apparent discrepancy between the USAR

and the TS will be resolved with NRR during the upcoming refueling

outage.

This item remains open pending the resolution of the

apparent discrepancy.

(285/8823-02)

The NRC inspector reviewed the actions taken by the licensee as

described above.

The NRC inspector noted on three occasions during

this inspection period, where the licensee voluntarily entered the TS

LCO when one RW pump was removed from service.

In each case, the

lice'nsee repaired and returned the pump to service prior to the end

of the 7-day LC0 time limit.

The NRC inspector also contacted NRR to

verify that the action taken by the licensee with respect to

upgrading of the LCO was adequate.

NRR stated that the upgrade was

consistent with the TS requirements established for other plants.

Based on the review performed, it appeared that the licensee had

taken appropriate actions to correct a problem identified by them,

d.

During a routine tour of the auxiliary building, an operator noticed

that the outboard bearing on CCW Pump AC-3C was hot.

The operator

noted the bearing was hot as operations personnel routinely feel pump

bearings during routine tours of operating spaces.

The licensee replaced the bearing and performed tests on Pump AC-3C

to verify proper operability.

The pump failed to operate properly

,

and was declared inoperable until the wear rings could be replaced.

At the time Pump AC-3C was experiencing problems, an NRC inspector

from Region IV was on site performing a review of the inservice

.

testing program.

This inspector monitored the actions taken by

the licensee and will provide the results in NRC Inspection

Report 50-285/88-26.

e.

On July 6, 1988, the NRC resident inspector observed the licensee

perform an evacuation drill per the emergency plan.

The NRC resident

inspector observed a site area alert at 8:41 a.m and witnessed the

licensee attain full personnel evacuation accountability at 9:06 a.m.

This observation was performed at the licensee's request as the

licensee wanted to demonstrate the ability to attain full personnel

accountability within 30 minutes.

The licensee had failed to attain

full accountability during the annual emergency preparedness exercise

held on June 29, 1988.

No violations or deviations were identified.

.

_

  • '

,

=,

.

,

.

12

j.

- 5.

Plant Tours (71707)

-

The NRC inspectors conducted plant tours at various times to assess plant

and equipment conditions.

The following items were observed during the

tours:

'

General plant conditions, including operability of-standby equipment,

.

were satisfactory.

Equipment was being maintained in proper condition, without fluid

.

leaks and excessive vibration.

Plant housekeeping and cleanliness practices were observed, including

.

no fire hazards and the control of combustible material.

Performance of work activities was in accordance with approved

.

procedures.

Portable gas cylinders were properly stored to prevent possible

.

,

missile hazards.

.

Tag-out of equipment was performed _ properly.

.

Management personnel toured the operating spaces on a regular basis.

-

.

During tours of the plant, the NRC inspectors noted the items. listed

-

below:

'

s

a.

The inspection certificate for the passenger elevator in the

,

administration building was out of date.

The certificate expired in

'

March 1988.

The licensee stated that the elevator had been inspected

but the certificate had not been. received from the State of Nebraska.

,

i

b.

During a plant tour, the NRC inspector noted that the licensee had

stored eight barrels of unused ~ ion _ exchange resins in Room 69.

-

Room 69 has an automatic fire detection system, but does not have a

!

sprinkler system installed.

Section II.A of Appendix R to 10 CFR Part 50 states, in part, that a

fire protection program shall be established at each nuclear power

plant and the program shall establish procedures required to

implement the program,

Section 3.3 of the Updated Fire Hazards Analysis (UFHA) and

1

Section 3.3.1 of Procedure 50-G-6, "Housekeeping," state, in part,

that unused ion exchange resins should be stored in an area protected

by an automatic detection / sprinkler installation.

Contrary to the above, the licensee stored eight barrels of unused

ion exchange resins in Room 69 which does not have a sprinkler system

installed.

This is an apparent violation.

(285/8823-03)

,

'

,

. . _ _ , . _ . _

,-_.4

m

_ _ .

, , -

g

-e

v


- - + --

' ~

v

v

~ - ~ ' ~ ~

..

.

.

.

v

.

I

13

.

In response to this problem, the licensee removed four barrels of

resins and left four barrels in Room 69.

In discussions with the

licensee as to why four barrels were lef t,-the ' licensee stated that

the fire loading analysis for Fire Area 20 (which includes Room 69)

indicated that up to 1000 pounds of resins could be stored in the

area. The NRC inspector reviewed the analysis the licensee had

performed for Fire- Area 20 and confirmed the licensee's statement.

It appears that the analysis done for Area 20 and the requirement

'

stated in Section 3.3 of.the UFHA and in Procedure 50-G-6 are in

conflict.

The analysis allows 1000 pounds to be stored in the area

whereas the other requirements. state that no resins can be stored in

Room 69; Nevertheless, the NRC inspector calculated the amount of

resin stored in Room 69 to be.1736 pounds-(8 barrels at 217_ pounds

each).

Therefore,'the licensee was in violation of the requirements

established by the UFHA, whichever one is appropriate.

The licensee stated that the apparent-inconsistency would be

corrected.

The NRC inspector will' verify that the inconsistency is

!

~

corrected during subsequent followup on this violation.

6.

Safety-Related System Walkdown (71710)

,

The NRC inspector walked down accessible portions of the following

safety-related system to verify system operability.

Operability was

determined by verification of selected valve and switch positions.

The

i

system was walked down using the drawings and procedures noted.

'

Containment spray system (Procedure 01-05-1, Revision 16, and

.

Orawing E-23866-210-130, Revision 44)

,

During the walkdown, the NRC inspector noted no discrepancies between the

drawings, procedures, and plant as-built conditions for the selected areas

checked.

No violations or deviations were identified.

f

7.

Monthly Maintenance Observations (62703)

{

The NRC inspectors reviewed and/or observed selected station maintenance

activities on safety-related systems and components to verify the

!

maintenance was conducted in accordance with approved procedures,

regulatory requirements, and the TS.

The following items were considered

during the reviews and/or observations:

l

The TS limiting conditions for operation were met while systems or

.

,

components were removed from service.

Approvals were obtained prior to initiating the work.

f

.

,

,

i

. -

--

_ -

.

.

.. .

,

,.

e

14

,

Activities were accomplished using approved M0s or preventive

.

maintenance (PM) procedures and were inspected, as applicable.

.

"

Functional testing and/or calibrations were performed prior to

.

returning components or systems to service.

Quality control records were maintained.

I

i

.

"

Activities were accomplished by qualified personnel.

.

Parts and materials used were p.roperly certified.

.

Radiological and fire prevention controls were. implemented.

.i

.

The NRC inspector reviewed and/or observed the following maintenance

activities:

i

Construction of scaffolding for removal of asbestos insulation on the-

.

EDG 1 exhaust line (MO 882620)

.

"

Check of the flow transmitters for the two RW system heaners

.

(M0 883012)

[

,

Resetting of a regulator for the instrument air supply to the safety

.

injection and refueling water tank level detectors (M0 882499)

!

!

,

Installation of a check valve in the instrument air accumulator

!

,

.

]

assembly for RW Pump AC-10B (M0 882926)

!

a

,

i

Installation of Gamma-4 setpoint changes on thermal margin / low power

.

j

Channels A/8/C/D (M0 882819)

.

,

A discussion of each item is provided below:

-

a

I

a.

On July 7, 1988, the licensee began erecting scaffolding over EDG 1

,

1

to allow the crafts to remove the insulation from the EDG exhaust

line.

A scaffolding platform is required for the insulation removal

i

because special techniques are needed for handling of the insulation

j

as it contains asbestos.

3

,

!

During a review of the M0 issued for the work, the NRC inspector

,

i

noted that the MO had not been signed by the shift supervisor.

In

'

followup on the reason that the MO was not signed by the shift

j

supervisor, the NRC inspector noted that the MO had been assigned a

j

plant status code of "O."

This code is used whenever an M0 does not

require the crafts to obtain the signature of the shift supervisor.

4

The M0 plant code is assigned by the supervisor of operations or his

.

'

l

designated alternates.

The code is assigned based on the nature of

l

the work being performed.

The "0" code is usually reserved for work

j

j-

that has no af feet on plant operations such as painting in the

i

I

,

t

- -

-

-

-

- .

-

- -

- -

-

-

-

-

-

-

. . . .

__ . . , . . . . . . . _ . -

-

-

.,

... __

.'

--

,

.

15

-

a

.-

administrative building and other such sctivities.

Based on the

review performed for M0 882620, it appeared that the supervisor of

i

operation's designated alternate inadvertently assigned an "0"

designation when another designation was appropriate.

The licensee

stated that the misassignment of the plant status code was caused by

]

the reviewer not fully understanding the work that was to be done by

the M0 due to the brief and nondescriptive information supplied on

-l;

the M0.

In response to this problem, the licensee immediately

discussed with the individuals responsible for assignment of plant

codes, the need to ascertain exactly what activities will be

performed by the M0.

The NRC inspector discussed the erection of the scaffolding with four

of the shift supervisors.

In all four cases, the shift supervisor

!

was aware that scaffolding was being erected over EDG 1.

The NRC

inspector reviewed a sampling of 32 M0s to determine whether or not

~

the correct plant status code had been provided.

No problems were

-

noted during this review.

g

Based on the reviews performed by the NRC inspector, it appeared that

}

this instance of assignment of the wrong code was an isolated case.

The NRC inspector's review did not indicate that s programmatic

,

problem existed.

The NRC inspectors will mcnitor the assignment of

plant codes while performing routine maintenance inspection

-

activities in the future,

m

The instructions for erecting the scaffolding were attached to

M0 882620.

The NRC inspector reviewed the instructions and it

appeared that adequate instructions were given for installation and

-

removal of the scaffolding.

b.

On July 11, 1988, MO 883012 was performed to check the accuracy of

-

the RW header flow transmitters.

The accuracy of the transmitters

I

was checked using an ultrasonic flow testing device.

The testing was

-

performed to verify the data obtained during leak testing of the RW

-

pump check valves.

See paragraph 4.c of this inspection report for a

discussion of the test performed on the RW pump check valves.

The NRC inspector noted that the personnel performing the test was

--

qualified and the equipment used for the test was in current

-

calibration.

No problems were identified during observation of this

'

maintenance activity.

'-

c.

On July 22, 1988, the NRC inspector observed two technicians reset

2

the air regulator for the safety injection and refueling water tank

_

level detector (A/FIC-383) in accordance with the instructions

_=

provided on MO 882499.

The regulator was reset to 25 psig to ensure

-

that a sufficient air supply would be available to A/FIC-383 in the

event instrument air pressure was lost.

The NRC inspector noted that

-

=

the technicians performed the task in accordance with the procedure

steps and that all equipment being used was in current calibration.

,

1

__

___

__ __ ___

-

,

,

.

16

MO 882499 had been signed by the shift supervisor to authorize the

work.

The NRC inspector also verified that the level setpoint for

A/FIC-383 was checked prior to returning the level detector to

service.

No problems were noted with the performance of the

technicians,

d.

On July 14, 1988, the NRC inspector witnessed I&C technicians

replacing the check valve for the instrument air assembly for the RW

Pump AC-10B discharge valve.

The check valve was replaced and the

air assembly was tested for 30 minutes to verify proper operation.

The NRC inspector noted that the work was properly authorized and

postmaintenance test instructions were included.

e.

On June 29, 1988. the thermal margin / low pressure (TM/LP) trip

function of the reactor protection system was found to be inoperable

in that the licensee had discovered that each channel had been

improperly set.

The NRC inspector observed I&C technicians resetting

the TM/LP setpoints in accordance with Procedures CP-TM/LP-A, B, C,

and D.

The NRC inspector observed that the reactor engineer

monitored the progress of the technicians and provided technical

,

guidance,

j

All four channels of TM/LP were recalibrated and declared operable,

after the performance of the appropriate surveillance test, within 8

hours of being declared inoperable.

For further information

1

regarding this event, refer to NRC Inspection Report 50-285/88-22.

During this inspection period, the licensee completed construction of the

new maintenance shop.

The new maintenance shop is approximately three

times larger than the old one and provides more than adequate space for

each craft.

The crafts commenced moving their tools and equipment into

the new shop to prepare for the upcoming refueling outage.

On July 18, 1988, the licensee notified the NRC inspector that they had

experienced problems with one of the four banks of the plant cathodic

protection system.

To repair the system, the licensee obtained the

services of a consultant.

The consultant and an engineer from the

downtown OPPD offices went on site, adjusted the system rectifier, and

then departed the site.

Approximately 30 minutes later, the rectifier

burned out.

In followup on this item, the NRC inspector determined that the OPPD

engineer did not process an M0 to authorize the work to be completed nor

'j

did the engineer notify the shift supervisor that the work was going to be

performed.

The rectifier has not yet been repaired as the licensee is awaiting parts.

l

The licensee stated that the loss of one bank of cathodic system shouldn't

be a problem for the protection of the piping for approximately 2 months,

i

t

-

. -

- -

-

-

-

- -

_ _

_

.__

_

.

_

'

,

.

.

0

17

!

In response to this problem, the licensee took immediate corrective

i

action.

The security badge for the engineer was pulled by the plant

manager so that he no longer has site access.

The engineer will not be

'

allowed to have site access until his division manager confirms, in

writing, to the plant manager that the individual has been fully retrained

in all aspects of the administrative controls applicable to site activities. '

At the end of this inspection period, the engineer had not regained site

,

access.

.

j

The NRC inspector reviewed the actions taken by the licensee.

It appeared

that the actions were prudent and conservative in this instance.

The

licensee has not experienr.ed an incident similar to this one in the past.

No violations or deviations were identified.

~

F

8.

Monthly Surveillance Observations (61726)

'

The kRC inspectors observed selected portions of the performance of and/or

j

reviewed completed documentation ior the TS-required surveillance testing

,

on safety-related systems and components.

The NRC inspectors verified the

'

following items during the testing:

.

Testing was performed by qualified personnel using approved

-

.

procedures.

Test Instrumentation was calibrated.

.

The TS limiting conditions for operation were met.

.

1

Removal and restoration of the affected system and/or component were

j

..

i

accomplished.

!

Test results conformed with TS and procedure requirements.

.

4

.

,

1

Test results were reviewed by personnel other than the individual

)

directing the test.

'

1

i

Deficiencies identified during the testing were properly reviewed and

.

resolved by appropriate management personnel.

!

i

l

The NRC inspector observed and/or reviewed the documentation for the

following surveillance test activities.

The procedures used for the test

l

activities are noted in parenthesis.

'

Ofesel fire pump full-flow test (ST-FP-4)

a

.

,

Monthly test of EDG 2 (ST-EST-6)

)

l

.

Monthly check of the subcooled margin monitor (ST-SM-1)

.

?

i

]

A discussion of each surveillance observed is provided below:

4

l

.

.

.

.

-

.

.m

.

.

. .

.

.

.

.

.

.

._

__

_

._.

-

-

.-

,

-

.

-

,

yg

i

a.

On July 21. 1988, the NRC inspector observed the full-flow test of

the diesel fire pump.

The inspector noted that the test was

performed in accordance with the procedure, as written, and the

i

results obtained were within the specified acceptance criteria.

+

.

During the testing, the NRC inspector noted that a-first-line

,

!

maintenance supervisor was actively involved in performing an

i

2

overview of the testing.

The NRC inspector notes that the presence

1

of the first-line supervisor in the. field is a positive aspect that

was not previously provided by the= licensee,

b.

On fuly 13, 1988- the NRC inspector observed the monthly test of

'

,

EDG 2.

The ii.spector observed the portion of the test that was

!

9

performed in the control room by a licensed operator. The NRC

,

inspector noted that the oprator performed the test by using the

,

proct., dure, as written.

No problems were noted during the test.

4

.

c.

On July 13, 1988, the NRC inspector observed portions of the test

1

'

performed to verify thdt the subcooled margin monitor operated

[

correctly.

The test was performed using the procedure, as written,

i

During observation of this test, the NRC inspector again noted that

1

the first-line maintena..ce supervisor was in the field observing the

performance of the testSng.

No violations or deviatitps were iduntified.

l

9.

Security Observations (71881)

I

The NRC inspectors verified the physical security plan was being

i

'

ieplemented by selected observation of the following items:

I

i

)

The security crganization was properly manned,

.

i

Personnel within the protected area (PA) displayed their

.

]

identificatien badges.

Vehicles were properly authorized, searched, and escorted or

.

.

]

controlled within the PA.

l

]

Persons and packages were prcperly cleared and checked before entry

.

i

j

into the PA was permit.ted.

The effectiveness of the security program w3s maintained when

.

sect.rity equipment failure or impairment raquired compensatory

a

l

measures to be employed.

a

i

The PA barrier was maintained and the isolati0n zone kept free of

.

'vansient material.

i

i

.

  • ~

.

.

.

.

19

The vital area barriers were maintained and not compromised by

.

breaches or weaknesses.

Illumination in the PA was adequate to observe the appropriate areas

.

at night.

Security monitors at the secondary and' central alarm stations were

.

functioning properly for assessment of possible intrusions.

On July 27, 1988,.the NRC inspector assisted in monitoring three security

drills initiated by security specialists from the Region IV Office.

The'

fit st drill involved neutralization of an armed intruder into the

protected area, the second drill involved response to a vital area in

alarm when the first responder became incapacitated, and the third drill

demonstrated the deployment and function of compensatory measurcs when the

alarm and detection systems' failed.

The details of the results of.the

drills are provided in NRC Inspection Report 50-285/88-24.

No violations or deviations we e identified.

10.

Radiological Protection Observations (71709)

The NRC inspectors verified that selected activities of.the' licensee's

radiological protection program were implemented in conformance vith the

facility policies and procedures and in compliance with regulatory

requirements.

The activities listed below were observed and/or reviewed:

-

Health physics (HP) supervisory personnel conducted plant tours to

.

check on activities in progress.

Radiation work permits ccntained the appropriate information to

.

ensure work was performed in a safe and controlled manner.

Personnel in radiation controlled areas (RCA) were wearing the

.

required personnel monitoring equipment and protective clothing.

Radiation and/or contaminated areas were properly posted and

.

controlled based on the activity levels within the area.

Personnel were properly frisked prior to exiting an RCA.

.

No violations or deviations were identified.

11.

In-Office Review of Periodic and Special Reports (90713)

In-office review of periodic and special reports was performed by the_NRC

resident inspectors and/or the NRr. Fort Calhoun project engineer to verify

the following, as app opriate:

Correspondence included the information required by appropriate NRC

.

requirements.

-~

_

_

._ _

,

,

.

,.

\\

'

.

-

0

,

-

20

/

'

Test results and supporting.information were consistent with design

.

- predictions and specifications.

~

Determination that planned corrective actions were adequate for.

-

.

resolution of identified problems.

Determination.'as to whether any information contained in the

.

correspondence report should be classified as an abnormal occurrence.

Correspondence did not contain' incorrect, inadequate, or incomplete-

.

information.

'

The NRC inspectors'. reviewed the'following correspondence:

June Monthly Operating Report, dated July 14, 1988

.

Cycle 11 Setpoint Errors, dated July 1 and July 25, 1988

.

Responses to-Request for Additional Information Concerning

.

NUREG-0737, Item II.D.1, Performance Testing of Rel_ief and Safety

Valves, dated June 28 and June 30, 1908

OPPD Nuclear Reorga'1ization, dated July 1, 1988

.

Core Reloa Methodology Changes for Cycle 12, dated July 8, 1988

.

Resp)nse to NRC Bulletin 88-04, dated July 8, 1988

.

Status of the Detailed Control Room Design Review and Safety

.

Parameter Display System Audit Findings, dated July 6, 1988

Licensee Critique of 1988 Annual Emargency Exercise, dated July 19,

.

1988

Correction,to Special Report on Inoperability of Postaccident

.

Monitoring Instrumentation, dated July 19, 1988

Special Report on Inoperability of Fire Barrier, dated July 25, 1988

.

Application for Amendment of Ope"eting Licensee,' dated July IS,1988

l

.

During rev' v of reports, NRC personnel identified a 10 CFR Part 21 report

submitte-

a supplier that appeared to be applicable to the licensee's

facili ty

i NRC resident inspector provided a copy of the report to the

plant lic.

~ineer for review of applicability by the licensee.

The.

"

issu.ed by Gamma-Metrics on May 10, 1988, and pertained

report pn.

c.

.a

to possible solder connection problems in cable assemblies.

No viciations or deviations were identified.

' l

I

e-

-gi-

m-

-i------'

g

t-

-.m

S

~%y

-

,-)-

y

-r-p.,q-

wT'

m-

'N9

-P

-'* *'

~f'T@

w

.-

,.

..

.

21

j

i

J

12.

Review of Licensee Activities on NRC Bulletin 88-05 (92703)

On May 6, 1988, th'e NRC issued NRC Bulletin 88-05, "Nonconforming

Materials Supplied by Piping Supplies, Inc. at Folsom, New Jersey, and.

West Jersey Manufacturing Company at Williamstown, New Jersey," to alert

licensees that fraudulent material may have been supplied by Piping

Supplies, Incorporated and West Jersey Manufacturing (WJM) Company.

On

June 15, 1988, the_NRC issued Supplement l'to NRC Bulletin 88-05.

Then

bulletin and supplement required that licensees search their procurement

records to determine if they had purchased any material from them.

companies and to notify the NRC if any materials were identified during

~

the search.

'

On July 21, 1988, the licensee notified NRC Headquarters and Region IV

personnel that ten flanges supplied by .the WJM Company had been found

installed in the plant.

Six of the flanges are installed in the waste

disposal system, two of the flanges are installed on containment

electrical Penetration E-11, and two flanges are installed on the

containment penetration used to pressurize the containment for the

integrated leak rcte test.

The licensee has taken samples of the flange material for analysis o.n

eight of the ten flanges.

Two of the flanges are currently inaccessible

because they are inside containment and the plant is at 90 percent power.

The licensee is also performing hardness tests on the flanges.

At the end

of this inspection period, the licensee had not completed the analysis of

the flange testing.

The licensae was in the process of developing and issuing a justification

of continued operation (JCO) for the flanges at the end of this inspection

pericd.

The licensee stated that the JC0 would be issued within the

30-day period allowed by the bulletin.

The licensee performed a

preliminary evaluation and determined that the flanges could perform their

intended safety function as the flanges are rated for 150 pounds, but the

flanges installed on containment penetrations would be exposed to a

maximum of 60 pounds pres * Jre and the flanges installed in the waste

.

,

disposal system are exposd to about 50 pounds.

At the time the ten flanges were identified, the licensee had completed

approximately 10 percent of the review to be dele of the procurement

records.

The licensee stated that they will notify the NRC as other

components are identified.

The NRC will review the results of the testing

and the JC0 during a future inspection.

No violations or deviations were identified.

13.

Review of Licensee Activities Related to the Instrument Air Water

.

,

Intrusion Event (9273)

On July 6, 1987, the licensee experienced an eve" where water from the

fire water system entered the instrument air system.

On November 13, 1987,

~.

-

.

-

_ _ _ _

_ - .

,_

.

. .

.

.

~

..

.

22.

an enforcement conference was held at NRC Headquarters to discuss the

NRC's concerns related.to the. event and the. licensee's corrective actions

that would be taken in response to the. concerns.

The licensee, in.a

letter dated November 20, 1987, submitted written confiriation of the

corrective actions-that they would implement.

On February 22, 1988,-the NRC'tssued a Notice of Violation _and Proposed

Imposition of Civil Penalty based on the 'results of followup NRC

inspections on the instrument air event.

The resdits of the_ inspections

perfortned by the NRC are documented in NRC Inspection Reports 50-285/87-27

and 50-285/87-30. On April 27, 1988, the licensee responded to the Notice

of Violation.

In this response, in additicn to addressing the specific

violations contained in the Notice, the licensee provided a status of

actions related to commitments made during the enforcement conference on

November 13, 1987. ~The purpose of this_ portion of this inspection.was to

verify that the licensee had adequately implemented those commitments.

A

discussion of each commitment reviewed is provided below;

a.

Assignment of a System Engineer (Item No. I.A.I.a. IA Project

No I.C.13)

This item was related to a commitment to assign an individual as a

full-time system engineer for the instrument air (IA) system.

On November 18, 1987, a memo was issued by the licensee to assign an

individual as the system engineer for the IA system.

The memo noted

that the assignment became. effective on December 1, 1987.

Since the

engineer was

signed, he has actively participated in identifying

and resolvi;

, sues related to the IA system.

,

.

In discussions with licensee personnel, the NRC inspector noted that

the individual presently assigned as system engineer will be

transferred in the near future. .In discussions with the manager of

system engineering, it was established that the present system

engineer would not be reassigned until a fully qualified and

knowledgeable individual is available to' replace the present system

engineer.

This item is considered closed,

b.

Change to Procedure MP-FP-7 to Ensure Deluge Valve Operability

(Submittal Item No. I.A.2.a, IA Project No. I.B.1)

This item involved a change to Procedure HP-FP-7 to provide complete

instructions to the operator on the proper method of resetting the

deluge valve after trip testing has been completed.

l

!

.

.

.

_-_ .

_

,

.

_

,

,

. -

_ _ . .

_

._

_

_

._

.

_

_

. . . '

_,

.

d

23

This. Rem was formally issued as a'part_of Violation 285/8727-04

(Violation B.2.a) in NRC Inspection Report'50-285/87-27.

The

iaentified concerns will be_. reviewed when. followup on the violation

is performed.

This item is considered closed.

c.

Review of IA Operating Procedures (Submittal Item'No. I.A.2.b, IA

Project No. I.A.16)

>

This item' involved a commitment.by the licensee to review and.

upgrade, as necessary, the IA system. operating procedures to ensure-

that plant operators are provided.with clear, concise procedures'.

The NRC inspector. reviewed selected portions of the procedures listed

below.

The review was performed to verify that the procedures were

clear and concise.

Number

Revision

Title

01-CA-1

20

Compressed Air System-

Normal Operations

01-CA-2

6

Compressed Air System Test

,

01-CA-3

5

Auxiliary Building and

Containment Instrument Air

Outage

01-CA-4

2

Containment. Instrument Air

Outage

01-CA-5

0

Backup Cooling Supply.

to Air Compressors

01-ES-1

19

Engineered Safeguards

i

Controls-Normal Operation

j

GP-1

32

Master Checklist for Startup

or Trip Recovery

The NRC inspector also reviewed Piping and Instrument Diagram

(P&ID) 11405-M-264, Sheet 1, Revision 20; Sheet 2, Revision 8;

Sheet 3, Revision 14; Sheet 4, Revision 14; and Sheet 5, Revision 14.

In conjunction with the review performed on the procedures listed

above, the NRC inspector also reviewed operating procedures for other

safety-related systems.

The purpose of the review was to verify that

the valve checklists-contained a verification of the position of the

air supply valves for the accumulator assemblies servicing

safety related valves and components.

A review of the checklists was

'

.-_

.

. . .

_

_

.

.

. _ _ _

- _

.

. _ . , - .

..

.

.

,

..

-

"

3

c

.

24'

performed because it was noted that' the air supply valves were not

listed in the valve checklist contained in Procedure 01-CA-1.

The checklist. review revealed 'that many of the air supply valves were

listed; however, not all air supply valves were included on'the

checklists. -For example, the NRC inspector noted that no air supply

valves were on the checklists' for the c_ontainment spray and safety

injection systems.

In addition, many of the air-operated valves in

the plant contain a handwheel that manually overrides the air.

operator of.the valve.

By positioning the handwheel in the shut

position, the valve will stay shut regardless of any signal the valve

may receive to open using the air operator. .During review of the

licensee's procedures, the NRC inspector noted that no verification

~

of the position of the manual handwheel was provided fur the valves

that are normally shut during plant operation.

TS 5.8.1_ states, in part, that written procedures shall be

established that meet the minimum requirements of Regulatory

Guide 1.33.

Section 3 of Regulatory Guide 1.33 states, in part, that instructions

for startup should be prepared, as appropriate, for the instrument-

air system.

Contrary to the above, the licensee did not_ provide appropriate

instructions for startup of the instrument air system in that a

position verification for all instrument air supply valves to

safety-related components and equipment was not included in the

operating instructions for plant systems.

For example, instructions

were not provided for verification of the air supply valves in the

containment spray and safety injection systems.

In addition,

procedural verification of the manual override handwheels was'not

provided in plant procedures.

This-is an apparent violation.

(285/8823-04)

In response to the apparent violation discussed above, management

stated that a revision to the appropriate checklists would be made

prior to startup from the next refueling outage.

In addition to the problems noted with the checklists not listing the

air supply valves, the NRC inspector also noted that the supply

-

valves for all the safety-related ac;.umulator assemblies were not

shown on P&IC M-264.

During the performance of a safety system outage modification

inspection (S50MI) in December 1985, the SSOMI team noted that

P&ID M-264 did not show the air supply valves to the accumulator

assemblies for the auxiliary feedwater turbine-driven pump steam

supply valves (HCV-1045A and HCV-10458).

The SS0MI team provided

details of this deficiency as Deficiency 2.2-5 in NRC Inspection

Report 50-285/85-22.

.

_.

. _ . - _ _ . .

_

.

. _ _ _ _ _ _ _ .

. . .

i

. .

p&

g

.

25

,

!.

'

l

l

In response to Deficien:y 2.2-5, licen'see stated that it was not

~

their policy to add small valves in nonsafety-related systems to

P& ids.

This deficiency remains open pending discussion between the

SS0MI team and the licensee.

In discussions between the licensee and the NRC inspector, licensee.

management stated that P&ID M-264 would be updated prior to the end

of the upcoming. refueling outage to include the accumulator air

supply. valves for all safety-related, air-operated valves.

Licensee

management stated that the other IA system valves would be added.to

the.P&ID in the future.

No specific date was given by the licensee

for completing the update of the P&ID.

The P&ID will be updated

based on~a walkdown to be performed by the system engineer during the

refueling outage.

This item remains open pending issuance of the

updated P&ID and a review of the P&ID by the NRC inspector.

(285/8823-05)

During review of this item, the NRC inspector noted that the licensee

had filed Procedure 01-CC-4, Revision 8, in the wrong place in the

official copy of the operating procedures manual.

The official copy

of the manual is used by plant personnel to verify that they are

using the latest revision of a procedure when performing an activity.

When the NRC inspector looked at the place in the official manual

where the procedure should have been filed, it was noted that

Revision 7 was in the proper location.

The NRC inspector was

concerned that since the latest revision of Procedure 01-CC-4 was

misfiled, someone may have checked the officia'. manual and

inadvertently used the wrong revision of Procedu.o 01-CC-4.

Licensee

personnel concurred with this assessment.

Upon notification by the NRC resident inspector, the licensee

immediately initiated corrective actions.

Procedure 01-CC-4,

Revision 8, was filed in the correct position in the manual and

Revisix / was removed.

Other' volumes of the manuals were checked to

verify the appropriate filing of other procedures.

The licensee

stated that no other problems were noted.

The licensee also verified

that the procedures in the other official copies of the manuals were

properly filed.

The licensee found the same problem with

Procedure OI-CC-4 being misfiled, but not with other procedures.

The NRC inspector reviewed selected portions of the official manual

copies located in the administration building and the control room to

verify that procedures were not misfiled.

No problems were noted.

It appeared that the licensee had immediately taken appropriate

corrective actions to resolve the apparent problem with filing of

procedures in manuals.

This item is considered closed.

d.

Upgrade the Incident Reporting Process (Submittal Item No. I.A.2.c,

IA Project No. I.C.3)

,.

,

.

26

This item involved a review of the operating incident reporting

system to provide prompt determination of the safety significance of

an incident.

To upgrade the incident' reporting process, the licensee revisedi

Procedure 50-R-4 to provide clear instructions for evaluation of an

incident. .The-revision designated the shift technical advisor (STA),

in conjunction with the shift supervisor, as the individual

responsible.for evaluation of off-normal events.

Procedure 50-R-4

previously did not designate a. specific individual responsible for.

event evaluation.

The NRC inspector reviewed the procedures listed below:

Number

Revision

Title

S0-R-4

16

Station Incident Reports

50-R-11

11

Notification of Significant

Events

S0-R-12

3

Reporting of Physical

Security Events

Based on a review of these procedures, it appeared that the licensee

had established an adequate incident reporting program.

Although it

appeared that an adequate program has been established, the licensee

has experienced some difficulty in reporting off-normal events as

evidenced by issuance of Violation 285/8811-03 in NRC Inspection

Report 50-285/88-11.

The specific problems of the incident

evaluation process will be reviewed when followup on the violation

is performed.

The NRC inspector reviewed training records to verify that the STAS

had received training on the new incident reporting process.

It

appeared that the STAS have been trained in use of the new reporting

program.

This item is considered closed.

e.

Development of Operating Instructions for High Dew Point (Submittal

Item No. I.A.2.d, IA Project No. II.A.10)

The item was related to the development of instructions for

operations personnel on what actions to take in the event the dew

point indicator or routine testing indicate the dew point exceeds the

system design limit of -20 degrees Fanrenheit.

The NRC inspector reviewed Procedure 01-CA-1 and noted that the

licensee had provided adequate instructions to operations personnel.

. .

.. .

.

_

_

_

'

,

_,

..

27

,

On July 6, 1988, the licensee experienced a problem where the. shift

chemist monitored the dew point and found that.the system dew point

exceeded the system limit. 'The operations staff took immediate1

action and restored the system dew point by_ switching from the

on-line to the standby air dryer.

Subsequent tests indicated that

the dew point.had returned to -34 degrees Fahrenheit.

It appeared,

based on the actions taken by the operations staff, that the.

instructions provided in Procedure 01-CA-1 were adequate.

The NRC inspector reviewed training records to verify that the

appropriate personnel had received training in the actions required

in the event of a high dew point event.

Based on the training

records reviewed, it appeared that the appropriate personnel had

received training.

This item is considered closed,

f.

Review IA System Lineup and Tag-Out Status for Adequacy (Submittal

item No. I.A.2.e, IA Project No. I.A.19)

This item was related to a licensee commitment to review

administrative procedures for lineup and verify that IA system

compo ents were appropriately tagged to prevent inadvertent

operation.

-

The licensee performed a walk down of the IA system to verify that

the system was properly tagged with danger or caution tags to prevent

inadvertent operation of system components. _The licensee also

reviewed ,ccedure 50-0-20, "Equipment Tagging Procedure," to

determint G ether or not changes to the procedure were necessary.

Pased on the two actions described above, the licensee determined

that the IA system tagging and Procedure S-0-20 were adequate;

therefore, no changes were made.

In followup on this item, the NRC inspector performed a walkdown of

selected areas of the IA system.

During the walkdown, the NRC

inspector noted no problems with the danger or caution tags installed

on the system.

In addition, no instances were noted where tags were

not installed and should have been.

The NRC inspector reviewed Procedure S0-0-20, Revision 19, to verify

that the procedure provided clear instructions for tagging of

equipment.

Based on the review performed, it appeared that

Procedure 50-0-20 provided adequate instructions.

This item is considerad closed.

g.

Upgrade of the Preventive Maintenance Program (Submittal Item

No. I.A.3.a, IA Project No. I.A.4)

_

'

.

.

I

e

28

This item was related to a licensee commitment to conduct a review of

ie preventive maintenance (PM) program for the IA system.

The

review was performed by industry consultants to determine what

' additional PMs, if any, were required to be initiated for the system.

Based on t he review performed by the licensee's consultants, existing

PMs were tevised to increase the frequency of performance.

Review of

the PMs is discussed in paragraph 13.1 of this report.

During a review of this item, the-NRC inspector noted that the

industry consultants recommended PMs be established that had not b'en

previously performed by the licensee. ~The. recommended PMs included

periodically abuilding the system air regulators and periodically

checking for moisture by ' blowing down accumulators and system lo,e

points.

The licensee has not yet instituted these PMs.

In discussions with the licensee, the NRC inspector determined that

the licensee would not be implementing the recommendation made by the

consultant with respect to blow down of the accumulators and system

low points.

The licensee stated that, since dew point monitoring has

shown that a high quality of air is~being supplied to the IA system,

no periodic blow-downs are required.

In addition, the licensee also

stated that, since' the water intrusion event, no water or

particulates have been found in any components disassembled for

repair where water was not expected to be found.

With respect to the

performance of PM activities on the regulators, the licensee stated

that they had no plans to include the regulators in the PM prngram at

this time.

The' licensee stated that a decision would be made within

6 months as to what actions will be taken on inclusion of the

regulators in the PM program.

This item remains open pending the

licensee's decision on including the regulators in the program and a

review of the licensee's decision by an NRC inspector.

(285/8823-06)

This item is considered closed,

b.

Air Dryer Desiccant Replacement (Submittal Item No. I.A.3.b, IA

Project No. - None)

This item was related to a licensee commitment to replace the

desiccant in the air dryers to ensure maximum moisture removal.

The NRC inspector reviewed M0 874814 to verify that the desiccant had

been replaced.

The NRC inspector also observed, at the tice of

replacement in December 1987, the craftsmen replacing the desiccant.

It appeared that the desiccant was appropriately replaced.

This item is considered closed.

i.

Revision to the Air Dryer Preventive Maintenance Schedule (Submittal

Item No. I.A.3.c, IA Project No. - None)

l

-

-

-

-

.

.

. .

.

-

.

_-_

%-

e.

.

,

.

29

This item involved the licensee ' revising.the PM schedule for the air

j

. dryers. The revision of the PM program for the air dryers was based

1

on the input received by the licensee from an IA consultant.

To upgrade the PM program for-the~ air dryers, the licensee revised

two PMs to re' quire'the maintenance be performed at a greater

frequency.

Procedure PM-UXHV was revised to require inspection and

lubrication of the dryer components biweekly.

This activity was

previously performed on a quarterly basis.

Procedure PM-TXCB was

revised to require replacement of the' dryer desiccant every refueling

outage. . Procedure PM-TXDB previously required an inspection of the

desiccant each refueling outage.

The NRC inspector reviewed Procedures PM-UXHV and PM-TXDB to verify

that the procedures provided adequate instructions and that the

inspection frequency was correctly specified.

No problems were

noted.

The NRC inspector also reviewed a sample of completed Procedure PM-UXHV

to verify that the activity was completed.

Based on the review, it

~

appeared that the licensee inspected and lubricated dryer cor.ponents

biweekly.

PM-TXDB has not been performed yet.

The licensee replaced

the dryer desiccant in accordance with the instructions provided by

an M0.

See paragraph 13.h (above) of this section of this report.

This item is considered closed.

j.

Initiate Preventive Maintenance or Surveillance Testing for the

Air-Operated Dampers Associated with the Emergency Diesel Generators

(Submittal Ite,a No. I. A.4.a

IA Project No. I. A.11 and I. A.23)

'

This item involved the inclusion of the air dampers associated with

the EDGs into a routine testing program.

This item also involved the

initiation of a program to routinely blow down the accumulators for

i

the exhaust dampers on the EDGs.

To routinely verify satisfactory operation of the air dampers, the

licensee issued Procedure SP-STROKE-1.

This procedure requires that

the exhaust dampers (YCV-871E and YCV-871F) be cycled monthly and the

time for the dampers to cycle open recorded.

The recorded data was

plotted and a trend established.

Procedure SP-STR0KE-1 also requires

that the operation of the EDG fresh air inlet dampers-(YCV-871A,

YCV-871B, YCV-871C, YCV-8710, YCV-871G, and YCV-871H) be verified.

Cycle timing for these dampers are not recorded.

'io verify operability of the dampers, the licensee revised

Procedure ST-ESF-6.

This procedure is used to verify operability of

the EDGs in accordance with TS requirements.

The revision added a

requirement that the operability of all EDG dampers be performed on a

monthly basis.

Procedure ST-ESF-6 also required that the stroke time

-

.

-

...-

.:

,

,

30

.

for YCV-871E and YCV-871F be recorded each quarter.

The licensee

provided' instructions for monitoring of stroke times in

Procedures SP-STR0KE-1.and ST-ESF-6 because this will ensure

-

that the stroke times will be recorded in the future.

During the

upcoming outage, the licensee will.' review the results obtained by

Procedure SP-STROKE-1 since November.1987 to determine whether or not

it is necessary to continue the performance of Procedure SP-STR0KE-1.

-The licensee issued Procedures PM-DAMP-1 and PM-DAMP-2 to provide for

blowdown of the accumulators for the EDG exhaust dampers on a

quarterly basis.

The NRC inspector reviewed the following procedures during followup

on this item:

Number

Revision

Title

SP-STR0KE-1

4

Inservice Testing of

Air-0perated CQE Valves

PM-DAMP-1

1

Blowdown of Accumulator

for YCV-871E

'

PM-0 AMP-2

1

Blowdown of Accumulator

for YCV-871F

ST-ESF-6

77

Diesel Start and Diesel

Fuel Oil Transfer Pump

The NRC inspector also reviewed the trending documentation for

Dampers YCV-871E and YCV-871F.

Based on the review of the documentation listed above, it appeared

that the licensee has established an adequate program for testing the

dampers for the EDGs.

The NRC inspector reviewed the documentation

for the testing that had been completed.

The review indicated that,

based on the documentation, the dampers are properly operating.

A

review of the completed documentation for blow down of the exhaust

dampers indicated that no moisture or foreign material has been

found.

This item is considered closed.

k.

Performance of a Particulate Monitoring Program (Submittal Item

i

No. I.A.4.b, IA Project No. I.A.7 and I.A.8)

This item involved the commitment by the licensee to establish a

particulatt monitoring program.

The program was to be established to

.,

verify that 'here wasn't sufficient particulate matter to affect the

operation of IA components and equipment.

The licensee's program was

performed by the onsite chemistry group.

)

,. .

.

.

31

A limit of 0.005 milligrams per liter (mg/1) was established based on

the accepted limit for air used to supply breathing apparatus for

plant personnel.

The results of the tests performed in October, November, and December

1987 indicate that the particulate level in the IA system is less

than 0.0033 mg/1.

This value represents the lowest level of

detection of the instrument used.

In February 1988 the licensee

sampled the IA system for particulate and found that the particulate

level remained at less than 0.0033 mg/1.

Because the particulate

,

level has not increased, the licensee has not performed a particulate

'

sample since February 1988.

The NRC inspector reviewed the documented results of the sampling

.

performed by the licensee and verified that the results indicated

.I

that particulate matter was found to be less than 0.0033 mg/1.

Based on the continuous low r = ding., of particulates in the IA

system, the licensee stated that'a routine sampling program will not

be continued.

The licensee stated that, in the event of an

occurrence that warrants reinitiation of testing, the testing will be

resumed.

This item is considered closed.

1.

Establishment of a Dew Poir.t Sampling Program (Submittal Item

No. I.A.4.c, IA Project No. I.A.5 and I.A.6)

This item was related to the establirhment of a dew point sampling

program to verify the dew point is maintained within the established

design criteria of -20 degrees Fahrenheit.

The licensee has established a program for weekly sampling of the IA

system dew point.

The sampling program has been instituted by the

licensee's chemistry department.

The licensee also installed a

temporary gross dew point indicator in the system.

This on-line

indicator is monitored each shift by operations personnel and is used

to indicate a malfunctioning air dryer.

l

The NRC inspector reviewed Procedure CMP-3.74, "Dew Point By Alnor

Dewpointer," to verify that proper instructions had been provided for

operation of the dewpointer.

No problems were noted.

The NRC

inspector also reviewed the results of the dew point measurements

that had been taken by the licensee.

The data that established the

measured baseline for the dew point readings were obtained in

accordance with the instructions provided in M0s 875429, 875400, and

875547.

The NRC inspector noted that the results of the baseline

measurements indicated that the dew point was continually below

_.

.. .

,

GP

.

32

,

-20 F. ' Based on the review performed in review'of this item, it

appeared'that the licensee has established an adequate dew point

monitoring program.

This item is considered closed.

m.

hrformance of a System Functional Inspection (Submittal Item

Ne. I.A.5.a, IA Project No. I.A.15)

This item involved the licensee contracting with an outside

con;ultant to perform a functional inspection of the IA system.

The licensee contracted with Stone and Webster (S&W) to perform an

inspection of the IA system.

The inspection report, "Instrument Air

System Evaluation," was issued on ' January 15, 1988.

The results of

the evaluation performed by S&W identified 63 concerns related to the.

installation, operation, maintenance, and design of the system.

The licensee reviewed the concerns identified by S&W and determined

~

that only one of the concerns was safety significant.

The concern

was related to the operability of Valve PCV-1849, the IA containment

isolation valve.

The licensee notified the NRC of the concern and a

review of the problem was performed by the NRC.

The details of the

review are provided in NRC Inspection Report 50-285/88-11.

The

remaining 62 items are in the process of being dispositioned by the

licensee.

The NRC inspector will review the disposition of the items

when the licensee completes a commitment (Submittal Item No. II.A.5.C,

IA Project No. I.A.28) made in response to the IA event.

A review of

the items will be made by the NRC during a future inspection.

The NRC inspector reviewed the report generated as a result of the

S&W evaluation of the IA system.

It appeared that the evaluation was

indepth, performed by qualified individuals, and the identified

~

concerns were based on sound judgement.

This item is considered closed.

n.

Evaluation of Interface Valves and Bubblers (Submittal Item

No. I.A.S.b, IA Project No. None)

This item involved a licensee commitment to evaluate valves

constructed with internal diaphragms and tank level instruments to

determine the potential for allowing water to enter the IA system.

,

The licensee performed a walk down of the IA system in December 1987

and identified valves constructed with an internal diaphragm.

The

diaphragms in the valves presented a potential path for water to

enter the IA system in the event the diaphragm failed.

The licensee

evaluated the diaphragm failure and established that water entry into

the IA system was not possible.

l

.

._

_

._

-

.__

__

_

._ _

, , _ -

-- _

_

.

-

'

.-

.,

.

'

33-

The NRC inspector reviewed th( actions taken by the licensee to

~

evaluate the diaphragms.

The results of the review are provided in

NRC Inspection Reports 50-285/87-33 and'50-285/88-03.

The' review.

performed by-the NRC inspector' determined that the probability of

water leaking'past the diaphragm'into the IA system _was extremely

remote.

As a followup to the' identification of diaphragm valves being

supplied by the IA system, the lic.nsee stated that an additional

walk down of the IA system would be performed during the next

scheduled refueling outage.

The-NRC inspector had. issued Open

Item 285/8733-05 to track the licensee's actions.to complete another

walkdown.

This item will be reviewed during closeout of the open

item.

The licensee performed an evaluation of the tank level instrumen'ts

(bubblers) to verify that the liquid in the tanks could not enter.the

IA system if system pressure was lost.

The results of the evaluation

indicated that water cannot enter the IA system through the bubblers.

The NRC inspector discussed the evaluation with the licensee and

noted no problems.

This item is considered closed.

o.

Include Consideration of Check Valve Failures in the Safety Analysis

for Operability (Submittal Item No. I.A.S.c, IA Project No. I.A.26)

'

This item was related to the need for the licensee to revise the

safety analysis for operability (SAO) to include all IA check valves

r

installed on accumulators for safety-related valves. At the time the

licensee made this commitment, all check valves had not been included

in the SA0.

The SA0 was generated to verify that the plant could

continue to operate safely.

On April 27, 1988, the licensee issued an SA0 for~ evaluation of

continued plant operation.

The SA0 included an evaluation of all the

accumulator assembly check valves that had not been tested and

verified to operate satisfactorily.

The conclusions of the

evaluations performed by the licensee indicated that the plant was

safe to continue to operate.

The SA0 generated by the licensee was forwarded to NRR for review.

Open Item 285/8815-02 was issued in NRC Inspection Report 50-285/88-15

i

to formally document the cesults of the review to be performed by

NRR.

This item will be reviewed during followup on the open item.

This item is considered closed.

J

l

l

1

'

-

-

-

,

. g*.,

. .

,

34

~

p.

Consideration of Common-Mode Failure During Modification Process

(Submittal Item No. I.A 6.a, IA Project No. I.C;5)

This item was related to a commitment made~by the 1icensee to revise

and. upgrade engineering procedures to ensure that modifications

formally address potential common-mode failures.

' This. item was formally. issued as Violation 285/8727-01'(Violation B.3)

in NRC Inspection Report 50-285/87-27.

This item will be reviewed

during followup on the violation.

This item is considered closed.

q.

Establishment of An Event Investigative Team (Submittal Item

No. I.B.1.b, IA Project No. I.C.4)

This item involved a' licensee commitment to establish a management

investigative safety team (MIST) to be responsible for collecting and

preserving data, analyzing event significance, and identifying root

causes.

The licensee established the charter and niembership of the MIST by

issuance of Procedure NPD-QP-18, "Management Investigative Safety

Team (MIST)," on April 22, 1988.

Procedure NPD-QP-18 established

three permanent team members with the provision that specific

expertise could be added to the team, depending on the nature of the

event.

The three permanent team members are the manager of station

nuclear engineering, manager of training, and the division manager of

production engineering.

The NRC inspector reviewed Procedure NPD-QP-18 to verify that the

appropriate requirements had been provided.

No problems were noted.

This item is considered closed.

r.

Upgrade the Emergency Plan Implementing Procedures (Submittal Item

No. I.B.2.a, IA Project No. I.C.14)

This item involved a review by the licensee of the emergency plan

implementing procedures (EPIP).

The EPIPs were reviewed to verify

that the procedures properly addressed the consideration of common-mode

failures into the declaration of plant emergency classification;.

This item was formally issued as Violation 285/8727-07 (Violation B.5)

in NRC Inspection Report 50-285/87-27.

The review of this item

will be performed during followup of the violation.

This item is considered closed.

4

'

s.

Additional Walkdown of the IA System (Submittal Item No. II.A.1.a,

j

IA Project No. II.A.13)

'

i

,..

_

-- - - _. , , , .

.-

. . .

-

.-

-.

-.

._,

7.

.

.

35

This item was related'to a commitment made.by the licensee to perform-

a walk down of the IA system.

The: walk down was to be performed to

identify the existence of any IA/ water. interfaces.

This item was formally issued'as Open Item 285/8733-05 in NRC

Inspection Report 50-285/87-33.

This item.will be reviewed during'

the followup performed for the open item.

This item is. considered closed.

t.

Upgrade the Abnormal ~0perating Procedure'for Loss of Instrument Air

(Submittal Item No. II.A.2.a, IA Project No. I.A.12)

This item involved the revision ofgProcedure A0P-17, "Loss of

Instrument Air," to provide clear and concise instructions to the

operations staff in the event'the IA system ' pressure'is lost.

This item was formally issued as Violation 285/8727-05

(Violation 3.2.b) in NRC Inspection Report 50-285/87-27.

This item will be reviewed during the performance of followup on the

violation.

This item is considered' closed.

14.

Followup on NRC Information Notice 88-46 (92701)

On July 8, 1988, the NRC issued NRC Information Notice (IN) es-46,

"Licensee Report of Defective Refurbished Circuit Breakers," to alert

licensees of the discovery by the Pacific Gas and Electric Company of

defective refurbished electrical equipment, such as circuit breakers, that

j

may have been supplied to nuclear power plants.

Subsequent to the

i

issuance of IN 88-46, the NRC received information that OPPD may have

purchased two refurbished breakers (Model GE THEF136ml100) from the GE

'

Supply Company (GESCO) in Omaha, Nebraska.

The infermation also stated

i

that the breakers had been originally supplied by the General Magnetics

Company of Commerce, Californis.

On July 19, 1988, the NRC inspector

informed the licensee of the information on the breakers.

The licensee immediately commenced a search of their procurement records

to verify the breakers had been received and to identify if the breakers

had been ir. stalled in the plant. On July 21, 1988, the licensee informed

j

the NRC inspector that they had identified where the breakers had been

i

used in the plant.

1

On February 14, 1985, one of the breakers was installed in the electrical

supply circuit for the nuclear detector well cooling fan (VA-12A) motor.

VA-12A is nonsafety-related equipment; however, the circuit breaker is

j

classed as CQE (safety-related) because the breaker is installed in a

motor control center containing other safety-related breakers.

On

July 29, 1985, the bteaker failed.

The second breaker was removed from the

.-

.- .-

-

-

,

-,

.-

,.

.

.

,

je

-

.

.

..

36

warehouse and tested prior to installation.

The second breaker failed the

test and was never installed in the plant.

The licensee replaced the-

VA-12A breaker with another Model GE THEF136m1100 breaker.that had been

installed in the plant, but the equipment serviced by the' breaker was no

longer used.

The breaker used to replace the VA-12A breaker was purchased

from General Electric as original equipment.at the time the plant was

constructed.

The NRC inspector performed a review of the' activities related to the

purchase and installation of the two breakers purchased from GESCO.

The

results of the review are provided below.

At the time of the purchase of.'the breakers, no requirement existed

.

for testing breakers purchased as commercial grade items.

The

licensee'.s procedures in effect'at the time allowed the replacement

,

of electrical compomnts as long as the component was being replaced

,

due to normal wear or damage, perforrance had been satisfactory, and

the component used for' replacement was a like-for-like replacement.

However, as a matter of routine, the licensee performed testing on

breakers to verify proper operation.

During an interview with the

individuals involved with replacement of the breaker, it was

determined that testing was performed on the breaker and that the

breaker passed the testing.

The testing included a visual

examination, manual operations check, and an overcurrent trip check.

The breaker was installed in accordance with M0 844225, but the M0

did not document that testing was performed or the results of the

testing.

When the first breaker failed, MO 852558 was issued to troubleshoot

.

the cause of the breaker failure.

H0 852558 did not document the

cause of the failure of the breaker.

The individuals performing the

maintenance recalled that the breaker failed due to a poor connecticq

between the breaker and one of the incoming electrical feeder lines.

The poor connection caused localized overheating and damaged the

breaker.

The individuals recalled that there was no damage to the

breaker itself.

When the second breaker was removed from the warehouse, the breaker

.

was tested prior to installation.

The individuals recalled that the

breaker failed the test because it could not be mechanically reset

following the overcurrent trip test.

For this reason, the breaker

,

was never installed in the plant.

1

Licensee personnel stated that both breakers were trashed as neither

.

was fit for use.

The breakers were purchased by Purchase Order (PO) 98507-J1 that

.

specified the receipt inspectior. requirements of checking for

cleanliness, physical damage, workmanship, electrical insulation

undamaged, protective covers and seals installed, markings in

accordance with the P0, and packaging met the requirements of

- _ _

_

-.

_.

__

_.

--

. . _ -

y

.

,

r

..

.

o

37

ANSI N-45.2.2.

Documentation provided by the licensee' indicated that'

both breakers: met the receipt inspection acceptance criteria.

Since the breakers are no longer in service 'at the plant, no immediate

safety concerns exist with respect to this specific purchase.

The

.,

licensee is continuing with.the search of procurement records to determhe

whether or not other defective equipme'nt-may have been furnished by GESCO

and/or the General Magnetics Company.

The licensee is currently in the process of upgrading their procedures for

dedication of material purchased as commercial grade items.

The new

program should be initiated in the near future.

The NRC inspector performed a review to determine whether or not a

10 CFR Part 21 report should have been made by the licensee at the time

the breaker was found to be defective. . Based on this review, it appears

that this event was not reportable in that a substantial safety hazard did

not exist because there was not a major reduction in the degree of

protection provided to public health and safety.

No safety hazard existed

since the defective breaker was never installed in the plant.

No violations or deviations were identified.

15.

Followup on NUREG-0737 (TMI) Item II.E.1.1.1

(25565)

Followup was performed to verify that the licensee had installed an

auxiliary feedwater (AFW) system that met the reliability criteria

established by TMI Item II.E.1.1.1.

Based on an onsite inspection performed by NRC Headquarters personnel and

the reliability analysis provided by the licensee, NRR has determined that

the AFW system met the established reliability criteria.

In a letter

dated May 9, 1988, NRR issued an evaluat#vn of the AFW system and noted

that the system is generally well designed, maintained, and operated.

The

NRR evaluation also noted that the licensee had made a commitment, in a

letter dated February 17, 1988, to the NRC to install a third AFW pump

1

i

auring the 1990 refueling outage.

NRR noted that even though a third pump

will be installed, the current system meets the reliability criteria

stated in the standard review plan.

This item is considered closed.

16.

Nonlicensed Training

During this inspection period, the NRC inspector participated in the

licensee's annual vaqualification program for general employee training

(GET).

To evaluate the knowledge of each individual participating in the

class, the licensee adrainistered an examination that covered the material

provided in the GET program.

When the NRC inspector was presented his

examination booklet, he noted that the booklet contained six questions

with the correct answers circled.

Based on the fact that the NRC

y.....

_

.

38

inspector had been presented an examination with corre'ct answers, the NRC

inspector questioned the licensee about the control .of. examination

booklets.

In response to this identified problem,;the licensee performed a review of

the 720 examination booklets for GET training.

Of the 720 booklets,13

were destroyed as unusable because answers were marked in the booklets.

The licensee stated that no more than six answers were marked in any one

booklet.

To correct this problem,'the 1icensee' took the actions discussed below:

~

All examinations in use were destroyed and replaced with new

.

examinations containing new questions.

,

Each examination was serialized'so that traceability.could be

.

established as to which examination was used by each individual at

the conclusion of GET.

All booklets will be checked by the GET instructor prior to being

.

used to verify that no marks have been made in the booklets.

A

signoff sheet was initiated so that each instructor verifies, in

writing, that each booklet was checked.

The instruction sheet for the booklets was updated to stress-to each

.

student that no marks shall be made in the booklets.

Key control for the cabinets containing the examination booklets was

.

established.

The NRC inspector reviewed the actions taken by the licensee to address

this problem.

Based on the review, it appeared that the licensee had

established a program for controlling the examinations used for GET.

17.

Exit Interview

The NRC inspectors r.iet with Messrs. K. J. Morris (Division Manager,

Nuclear Operation) and W. G. Gates (Plant Manager) and other members of

the licensee staff at the end of this inspection.

At this meeting, the

NRC inspector summarized the scope of the inspection and the findings.

..

_.

.

.

-

. .

-

-

-

- - - - ,- -

-

!