ML19310A377: Difference between revisions
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{{#Wiki_filter:.- | {{#Wiki_filter:.- | ||
-;__~ , | -;__~ , | ||
o Attachment #1 to AECM-80/116 (Page 1 of 4) ONE*E'*[h a,W" | o Attachment #1 to AECM-80/116 (Page 1 of 4) ONE*E'*[h a,W" | ||
* ,*g % RO Bes 132 | * ,*g % RO Bes 132 | ||
, E 85 - Lwwfen. N J 07036 "5B - | , E 85 - Lwwfen. N J 07036 "5B - | ||
, f C | , f C C , , , , , , , , . . , , ,, | ||
C , , , , , , , , . . , , ,, | |||
10650 E Rush Street ' ' | 10650 E Rush Street ' ' | ||
[2$7E'2 Es*i"^ | [2$7E'2 Es*i"^ | ||
~ | ~ | ||
,,- h./ - | ,,- h./ - | ||
35!.?UT!Y.". P.T COG!TC ! .9.7.19~~.". Tetu s?41sa 3 April 1980 Mr. Robert H. Engelken Director, Region V 14 Q | 35!.?UT!Y.". P.T COG!TC ! .9.7.19~~.". Tetu s?41sa 3 April 1980 Mr. Robert H. Engelken Director, Region V 14 Q | ||
Office.of Inspection and Enforcement U. S. Nuclear Regulatory Cormission 1990 N. California Boulevard, Suite 202 Walnut Creek, California 94596 , | Office.of Inspection and Enforcement U. S. Nuclear Regulatory Cormission 1990 N. California Boulevard, Suite 202 Walnut Creek, California 94596 , | ||
==Subject:== | ==Subject:== | ||
10CRT21 Requirements / | 10CRT21 Requirements / | ||
Existence of a Defect I>; | Existence of a Defect I>; | ||
Gentlemen: | Gentlemen: | ||
As required by the subject regulation, the following report is made in triplicate. | As required by the subject regulation, the following report is made in triplicate. | ||
Line 53: | Line 42: | ||
Type of Business Activity: | Type of Business Activity: | ||
Manufacturers; Containment Gas Monitoring Systems Notification of Defect as follows: | Manufacturers; Containment Gas Monitoring Systems Notification of Defect as follows: | ||
I was notified yesterday, 2 April 1980, that while in-house | I was notified yesterday, 2 April 1980, that while in-house | ||
- testing was being conducted, the following failure occured. | - testing was being conducted, the following failure occured. | ||
The contents of the report made to me by one of our Test Technicians follows: | The contents of the report made to me by one of our Test Technicians follows: | ||
==Subject:== | ==Subject:== | ||
Line 65: | Line 52: | ||
still | still | ||
: 1) The pump deadheaded' for no longer than ,,20 seconds, | : 1) The pump deadheaded' for no longer than ,,20 seconds, | ||
,j 80 06110/ffi | ,j 80 06110/ffi | ||
e.. ; | e.. ; | ||
.e Attachm:nt #1 to AECM-80/116 (Page 2 of 4) 2i'The pressure at the pump outlet exceeded 150 psig, 9 3) The pressure buildup caused the connecting rods to separate from the crank shaf t causing a tremendous strain on the diaphragas. | |||
.e | It is conceivable that these diaphrages could have ruptured, thereby breaching the integrity of the system. The panel valves are one cause for such an event, but also the "N" stamp containment g isolation valves, which are sometimes automatically closed, could cause the same malfunction. . | ||
Attachm:nt #1 to AECM-80/116 (Page 2 of 4) | |||
2i'The pressure at the pump outlet exceeded | |||
150 psig, 9 3) The pressure buildup caused the connecting rods to separate from the crank shaf t causing a tremendous strain on the diaphragas. | |||
It is conceivable that these diaphrages could have ruptured, thereby breaching the integrity of the system. The panel valves are one cause for such an event, but also the "N" stamp containment g isolation valves, which are sometimes automatically | |||
closed, could cause the same malfunction. . | |||
To remedy the problem, we could install a ~ check valve across the inlet and outlet of the pump. | To remedy the problem, we could install a ~ check valve across the inlet and outlet of the pump. | ||
I, g | I, g | ||
In the event of any valves being closed in the system, the check valve would prevent any damaging build-up of pressure." | In the event of any valves being closed in the system, the check valve would prevent any damaging build-up of pressure." | ||
J ~ | J ~ | ||
The above report makes clear that either of the following two safety hazards exist: | The above report makes clear that either of the following two safety hazards exist: | ||
: 1) up to one litre of containment gas could be released into the outside atmosphere , should the failure as defined above occur; and/or O_' | : 1) up to one litre of containment gas could be released into the outside atmosphere , should the failure as defined above occur; and/or O_' | ||
: 2) if the input / outlet valve is closed while the pump | : 2) if the input / outlet valve is closed while the pump | ||
'14 I is in operation or if the containment isolation valve ; | '14 I is in operation or if the containment isolation valve ; | ||
inside the containment is closed, there is a risk in damaging the system, thereby rendering the system inoperable. ' | inside the containment is closed, there is a risk in damaging the system, thereby rendering the system inoperable. ' | ||
1 l | 1 l | ||
Location of Tacilities where the component exists: | Location of Tacilities where the component exists: | ||
- Pennsylvania Power and Light Susquehanna/ Units 1 & 2 1 | - Pennsylvania Power and Light Susquehanna/ Units 1 & 2 1 | ||
.- Mississippi P'ower and Light Grand Gulf / Units 1 8 2 | .- Mississippi P'ower and Light Grand Gulf / Units 1 8 2 | ||
- Detroit Idison Enrico Termi/ Unit 2 | |||
- Detroit Idison | |||
Enrico Termi/ Unit 2 | |||
[ Alabama Jos. M. Power Company Earley/ Units 1 8 2 . | [ Alabama Jos. M. Power Company Earley/ Units 1 8 2 . | ||
'- - Houston Lighting and Power Company South Texas Project / Units 1 8 2 f( ) | '- - Houston Lighting and Power Company South Texas Project / Units 1 8 2 f( ) | ||
>;, , ( | >;, , ( | ||
Ni l | Ni l | ||
.- ..~. | .- ..~. | ||
** Attcchmint #1 to AECM-80/116 (Page 3 of 4) | ** Attcchmint #1 to AECM-80/116 (Page 3 of 4) | ||
- Tennessee Valley Authority h Sequoyah/ Units 1 & 2 | |||
- Tennessee Valley Authority | |||
h Sequoyah/ Units 1 & 2 | |||
- Tennessee Valley Authority Watts Bar/ Units 1 & 2 | - Tennessee Valley Authority Watts Bar/ Units 1 & 2 | ||
[ - Arizona Nuclear Project Palo, Verde / Units 1, 2 5 3 | [ - Arizona Nuclear Project Palo, Verde / Units 1, 2 5 3 | ||
- Georgia Power Company . | - Georgia Power Company . | ||
? Hatch / Unit 2 To the best of our knowledge, none of the plants to which this component has been supplied is currently in operation with the exception of Georgia Power Coopany, which is currently shut down fo'r maintenance. | ? Hatch / Unit 2 To the best of our knowledge, none of the plants to which this component has been supplied is currently in operation with the exception of Georgia Power Coopany, which is currently shut down fo'r maintenance. | ||
Corrective Action to be Taken: | |||
I We are in the process of puttizig a by-pass on the discharge 1 of the pump to prevent deadheading, thereby preventing any damage. | I We are in the process of puttizig a by-pass on the discharge 1 of the pump to prevent deadheading, thereby preventing any damage. | ||
O This corrective action will be introduced on the Cleveland Nuclear Plant and will be added on all future jobs. | O This corrective action will be introduced on the Cleveland Nuclear Plant and will be added on all future jobs. | ||
/ | / | ||
Notification of Tacilities/ Purchasers: | Notification of Tacilities/ Purchasers: | ||
Notification will be made to the above facilities immediately of the defect and the corrective actions being taken and that a kit will provided them as soon as possible which will totally correct any possibility of failure / damage. | |||
Notification will be made to the above facilities immediately of the defect and the corrective actions being taken and that a kit will provided them as soon as possible which will totally | |||
correct any possibility of failure / damage. | |||
3' | 3' | ||
[ For further information, the work necessary to complete this corrective action is very minor in nature and can be easily | [ For further information, the work necessary to complete this corrective action is very minor in nature and can be easily | ||
.h accomplished on site by a qualified pipefitter. . | .h accomplished on site by a qualified pipefitter. . | ||
: 3. . | : 3. . | ||
Should your organization require any further information, I suggast you contact directly our Technical Director, Mr. Al Robinson. | Should your organization require any further information, I suggast you contact directly our Technical Director, Mr. Al Robinson. | ||
h Sincerely, a | h Sincerely, a | ||
t>.q . | t>.q . | ||
1 h. . . | 1 h. . . | ||
COMSIP, Inc. i | COMSIP, Inc. i | ||
. . . . Delphi Systems Division , | . . . . Delphi Systems Division , | ||
. & (~b J .- . | . & (~b J .- . | ||
.._ Claude_Varinoi . _ _ _ . . _ _ _ _ . , _ . . _ , _ , , | .._ Claude_Varinoi . _ _ _ . . _ _ _ _ . , _ . . _ , _ , , | ||
.. - - - - =- . .. . . . | .. - - - - =- . .. . . . | ||
~ | ~ | ||
~ | ~ | ||
O O . | O O . | ||
iI U | iI U | ||
n | n | ||
: s. I | : s. I o | ||
23f LL OF M ATC-f 41 A LS _- '\. [ | 23f LL OF M ATC-f 41 A LS _- '\. [ | ||
o (l')-NUPRo $5-4CA -90, coustP MoDIMeO (2)- eWAAGt or: cmPRIESSlots! F1TTIMq UNI 04 TEtt. - $5 GOO-3 j | o (l')-NUPRo $5-4CA -90, coustP MoDIMeO (2)- eWAAGt or: cmPRIESSlots! F1TTIMq UNI 04 TEtt. - $5 GOO-3 j gi * | ||
gi * | |||
- ss . 4oo . 3 | - ss . 4oo . 3 | ||
'' g | '' g | ||
@- TUBE EMD REQUCER - SS - 400 - R-G i | |||
@- TUBE EMD REQUCER - SS - 400 - R-G | X ; | ||
. }( - . 'n 7g TUBING a NOM : | . }( - . 'n 7g TUBING a NOM : | ||
g. | g. | ||
<lF '[ . | <lF '[ . | ||
a N- '- . Att couPONENT9 REQUIRED To MAKtz Tne uoDIFIC AT'ON *tt t- SC P840VIDED ISY | a N- '- . Att couPONENT9 REQUIRED To MAKtz Tne uoDIFIC AT'ON *tt t- SC P840VIDED ISY | ||
Line 209: | Line 128: | ||
I t IMITI A t_ issVE . . , . | I t IMITI A t_ issVE . . , . | ||
9_A_fli- ,,..!L/t t% _ | 9_A_fli- ,,..!L/t t% _ | ||
2 i ..... . . .... .. ,.,, ... .. .... | 2 i ..... . . .... .. ,.,, ... .. .... | ||
,- y-SID, Inc. - OcIphi Systems Division 1[ | |||
,- y- | |||
SID, Inc. - OcIphi Systems Division | |||
1[ | |||
/ TURill(> V . noinc. r: anel a .iraciois ~ | / TURill(> V . noinc. r: anel a .iraciois ~ | ||
~ | ~ | ||
~"~ | ~"~ | ||
-" m,,e rut...r - - ~ | -" m,,e rut...r - - ~ | ||
u , e.sig _ ,_M o l>l F1 C A TL O N ~h23,~* . | u , e.sig _ ,_M o l>l F1 C A TL O N ~h23,~* . | ||
, . , , , s ,, ,,,. | , . , , , s ,, ,,,. | ||
4 > ee a G 4 44it iC17 Ai' *)[sj ggAqg | 4 > ee a G 4 44it iC17 Ai' *)[sj ggAqg | ||
_ _ _ _ _ _ _ _ _ . _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - - _ - - _ _ _ - - .___ _ _}} | _ _ _ _ _ _ _ _ _ . _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - - _ - - _ _ _ - - .___ _ _}} |
Latest revision as of 19:41, 21 February 2020
ML19310A377 | |
Person / Time | |
---|---|
Site: | Grand Gulf |
Issue date: | 04/03/1980 |
From: | Varinois C COMSIP, INC. |
To: | Engelken R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
Shared Package | |
ML19310A370 | List: |
References | |
NUDOCS 8006110166 | |
Download: ML19310A377 (4) | |
Text
.-
-;__~ ,
o Attachment #1 to AECM-80/116 (Page 1 of 4) ONE*E'*[h a,W"
- ,*g % RO Bes 132
, E 85 - Lwwfen. N J 07036 "5B -
, f C C , , , , , , , , . . , , ,,
10650 E Rush Street ' '
[2$7E'2 Es*i"^
~
,,- h./ -
35!.?UT!Y.". P.T COG!TC ! .9.7.19~~.". Tetu s?41sa 3 April 1980 Mr. Robert H. Engelken Director, Region V 14 Q
Office.of Inspection and Enforcement U. S. Nuclear Regulatory Cormission 1990 N. California Boulevard, Suite 202 Walnut Creek, California 94596 ,
Subject:
10CRT21 Requirements /
Existence of a Defect I>;
Gentlemen:
As required by the subject regulation, the following report is made in triplicate.
.] .
Firm Identification: Comsip, Inc.
Delphi Systems Division I.
10650 E. Rush Street So. El Monte, California 91733 (213)442-0882 1,3 Responsible Officer making Report:
Claude Varinois, President .
Type of Business Activity:
Manufacturers; Containment Gas Monitoring Systems Notification of Defect as follows:
I was notified yesterday, 2 April 1980, that while in-house
- testing was being conducted, the following failure occured.
The contents of the report made to me by one of our Test Technicians follows:
Subject:
80-637 "K" Pump Malfunction During the testing of 80-637, one of the panel outlet valves was closed while the panel was shut-
- down. The pump was then started with the valve closed. The following occurred;
( ..
still
- 1) The pump deadheaded' for no longer than ,,20 seconds,
,j 80 06110/ffi
e.. ;
.e Attachm:nt #1 to AECM-80/116 (Page 2 of 4) 2i'The pressure at the pump outlet exceeded 150 psig, 9 3) The pressure buildup caused the connecting rods to separate from the crank shaf t causing a tremendous strain on the diaphragas.
It is conceivable that these diaphrages could have ruptured, thereby breaching the integrity of the system. The panel valves are one cause for such an event, but also the "N" stamp containment g isolation valves, which are sometimes automatically closed, could cause the same malfunction. .
To remedy the problem, we could install a ~ check valve across the inlet and outlet of the pump.
I, g
In the event of any valves being closed in the system, the check valve would prevent any damaging build-up of pressure."
J ~
The above report makes clear that either of the following two safety hazards exist:
- 1) up to one litre of containment gas could be released into the outside atmosphere , should the failure as defined above occur; and/or O_'
- 2) if the input / outlet valve is closed while the pump
'14 I is in operation or if the containment isolation valve ;
inside the containment is closed, there is a risk in damaging the system, thereby rendering the system inoperable. '
1 l
Location of Tacilities where the component exists:
- Pennsylvania Power and Light Susquehanna/ Units 1 & 2 1
.- Mississippi P'ower and Light Grand Gulf / Units 1 8 2
- Detroit Idison Enrico Termi/ Unit 2
[ Alabama Jos. M. Power Company Earley/ Units 1 8 2 .
'- - Houston Lighting and Power Company South Texas Project / Units 1 8 2 f( )
>;, , (
Ni l
.- ..~.
- Attcchmint #1 to AECM-80/116 (Page 3 of 4)
- Tennessee Valley Authority h Sequoyah/ Units 1 & 2
- Tennessee Valley Authority Watts Bar/ Units 1 & 2
[ - Arizona Nuclear Project Palo, Verde / Units 1, 2 5 3
- Georgia Power Company .
? Hatch / Unit 2 To the best of our knowledge, none of the plants to which this component has been supplied is currently in operation with the exception of Georgia Power Coopany, which is currently shut down fo'r maintenance.
Corrective Action to be Taken:
I We are in the process of puttizig a by-pass on the discharge 1 of the pump to prevent deadheading, thereby preventing any damage.
O This corrective action will be introduced on the Cleveland Nuclear Plant and will be added on all future jobs.
/
Notification of Tacilities/ Purchasers:
Notification will be made to the above facilities immediately of the defect and the corrective actions being taken and that a kit will provided them as soon as possible which will totally correct any possibility of failure / damage.
3'
[ For further information, the work necessary to complete this corrective action is very minor in nature and can be easily
.h accomplished on site by a qualified pipefitter. .
- 3. .
Should your organization require any further information, I suggast you contact directly our Technical Director, Mr. Al Robinson.
h Sincerely, a
t>.q .
1 h. . .
COMSIP, Inc. i
. . . . Delphi Systems Division ,
. & (~b J .- .
.._ Claude_Varinoi . _ _ _ . . _ _ _ _ . , _ . . _ , _ , ,
.. - - - - =- . .. . . .
~
~
O O .
iI U
n
- s. I o
23f LL OF M ATC-f 41 A LS _- '\. [
o (l')-NUPRo $5-4CA -90, coustP MoDIMeO (2)- eWAAGt or: cmPRIESSlots! F1TTIMq UNI 04 TEtt. - $5 GOO-3 j gi *
- ss . 4oo . 3
g
@- TUBE EMD REQUCER - SS - 400 - R-G i
X ;
. }( - . 'n 7g TUBING a NOM :
g.
<lF '[ .
a N- '- . Att couPONENT9 REQUIRED To MAKtz Tne uoDIFIC AT'ON *tt t- SC P840VIDED ISY
~~
y[p .jling.
COMSiP. sNc. INCt.UUlHQ THE At*,%)PRI ATE.
, m"
'd A ceR. p FIC ATIOtsj s . TilG (,. A tSOR. 6 HALL.
!],
,, jy;f.,[ SistEu puup BG PROVIDEC) BY Tl8 G C.UCTOM CK -
I t IMITI A t_ issVE . . , .
9_A_fli- ,,..!L/t t% _
2 i ..... . . .... .. ,.,, ... .. ....
,- y-SID, Inc. - OcIphi Systems Division 1[
/ TURill(> V . noinc. r: anel a .iraciois ~
~
~"~
-" m,,e rut...r - - ~
u , e.sig _ ,_M o l>l F1 C A TL O N ~h23,~* .
, . , , , s ,, ,,,.
4 > ee a G 4 44it iC17 Ai' *)[sj ggAqg
_ _ _ _ _ _ _ _ _ . _ _ _ _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - - _ - - _ _ _ - - .___ _ _