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Category:CORRESPONDENCE-LETTERS
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20216G3501999-09-29029 September 1999 Confirms Conversations Re NRC Staff Voluntary Response to Orange County Discovery Requests.Staff Will Voluntarily Answer Discovery Requests & Will Not Waive Any Objection or Privilege Under NRC Regulations.Related Correspondence ML20212M1081999-09-29029 September 1999 Confirms Intent to Meet with Utils on 991025 in Atlanta,Ga to Discuss Pilot Plants,Shearon Harris & Sequoyah Any Observations & Lessons Learned & Recommendations Re Implementation of Pilot Program ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML20212H7741999-06-23023 June 1999 Responds to Re Petition Filed by Orange County Board of Commissioners Re Proposed Expansion of Sf Storage Capacity at Shearon Harris Npp.Public Meeting Will Be Held at Later Date.With Certificate of Svc.Served on 990624 ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML20206R2511999-05-19019 May 1999 Responds to Addressed to Chairman Jackson Requesting That NRC Grant Standing to Orange County Board of Commissioners in Shearon Harris Proceeding Currently Before Board.With Certificate of Svc.Served on 990519 ML20206Q5281999-05-17017 May 1999 Responds to 990304 Request for Two Rail Routes to Be Used for Transport of Spent Fuel from Brunswick Steam Electric Plant,Southport,Nc & Hb Robinson Steam Electric Plant, Hartsville,Sc to Shearon Harris Npp,Near New Hill,Sc ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9601999-05-11011 May 1999 Forwards Resolution Adopted by Carrboro Board of Aldermen at 990504 Meeting.Resolution Expresses Town Concern Re Util Plans to Double high-level Nuclear Waste Storage at Shnpp ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl IR 05000400/19982011999-04-12012 April 1999 Discusses Safeguards Insp Rept 50-400/98-201 (Operational Safeguards Response Evaluation) on 980908-11.No Violations Noted.Licensee Performance During Evaluation Indicated Excellent Overall Contingency Response Capability 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl ML18016A8911999-04-0505 April 1999 Forwards non-proprietary App 4A,pages 20-25 & Proprietary Page 4-6 to re-issued Rev 3 of Holtec International Licensing Rept HI-971760.Pages Were Inadvertently Omitted from Reissued Rept.Proprietary Page 4-6 Withheld ML18016A8891999-04-0101 April 1999 Forwards Rev 99-1 to Plant EALs for NRC Review & Approval, Per 10CFR50,App E.Encl Provides Comparison of Currently Approved EALs & Proposed Rev 99-01.Approval of EALs Prior to June 1999,requested.With Four Oversize Drawings ML18016A8811999-03-31031 March 1999 Responds to NRC 990301 Ltr Re Violations Noted in Insp Rept 50-400/98-11.Corrective Actions:Post Trip/Safeguards Actuation Rept for 981023,RT Was Corrected,Required Reviews Completed & Approval Obtained on 990219 ML18016A8671999-03-19019 March 1999 Submits Response to RAI Re Spent Fuel Pool Water Level & Revised Fuel Handling Accident Analyses,Per 990317 Telcon with NRC ML18016A8631999-03-19019 March 1999 Forwards Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept, IAW 10CFR55.45(b)(5)(ii). NRC Form 474 & Required Info Re Simulator Performance Test Results & Schedules Also Encl ML18016A8691999-03-18018 March 1999 Forwards Resolution Adopted by Lee County,North Carolina Board of Commissioners Re Proposed Expansion of high-level Radioactive Waste Storage Facilities at Carolina Power & Light Shearon Harris Nuclear Power Plant ML18016A8511999-03-15015 March 1999 Forwards Proprietary & non-proprietary Version of Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFPs 'C' & 'D'. Repts Are Reissued to Reflect Reduction in Proprietary Info.Proprietary Info Withheld ML18016A8601999-03-15015 March 1999 Informs NRC of Mod to Commitment for Hnp,Re Comprehensive Review of Implementation of TS Sr.Upon Completion of Listed Reviews,Surveillance Procedure Review Project Will Be Considered Complete 1999-09-08
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L0911990-09-12012 September 1990 Confirms That Fee Electronically Transferred to Dept of Treasury for Payment of NRC Review Fees ML18009A6581990-09-11011 September 1990 Submits Addl Info Re Use of Hafnium Control Rods at Facility.All Rods Will Be Removed During Spring 1991 Outage ML20059H4181990-09-0606 September 1990 Responds to NRC Re Violations Noted in Insp Rept 50-400/90-13.Corrective Action:Changes to EST-717 in Area of Power Normalization Under Study for Past Several Months ML17348B4941990-08-30030 August 1990 Forwards Semiannual 10CFR26 fitness-for-duty Program Data for 900103-0630.Mgt Decision Made to Utilize Alcohol Breath Instruments as Screening Devices for Unscheduled Work Call Outs in Determining fitness-for-duty ML20059D3511990-08-30030 August 1990 Forwards Decommissioning Financial Assurance Certification Rept Submitted by North Carolina Eastern Municipal Power Agency ML18009A6261990-08-10010 August 1990 Informs That Action Committed to in Response to Generic Ltr 88-14, Instrument Air Supply Sys, Completed ML18009A6241990-08-0303 August 1990 Forwards Addl Info Re Operator Action Times Assumed in Steam Generator Tube Rupture Analyses for Plant,Per 900712 Telcon ML18009A6081990-07-31031 July 1990 Forwards Plan for Shearon Harris Nuclear Power Plant Emergency Exercise - 900919, Per NRC Request.W/O Encl ML20055J4171990-07-30030 July 1990 Forwards Rev 5 to Security Plan.Rev Withheld (Ref 10CFR73.21) ML20055F9431990-07-12012 July 1990 Advises That Stated Amount Electronically Transferred to Us Dept of Treasury,Nrc on 900711 for Payment of Operator License Exam Fees for Listed Insp Invoices ML18009A5991990-07-0606 July 1990 Comments on Electrical Distribution Sys Functional Insp Rept 50-400/90-200 on 900212-0316.Seismic Qualification Package Subsequently Upgraded to Include Qualification Info Based on Receipt of Part 21 from Transamerica Delaval ML18009A5851990-06-28028 June 1990 Advises That Emergency Preparedness Exercise Scheduled on 900919.Exercise Will Consist of Simulated Accident at Plant Site & Will Involve Planned Response Actions.Objectives to Be Fulfilled Encl ML18009A5621990-05-30030 May 1990 Responds to NRC 900504 Ltr Re Violations Noted in Insp Rept 50-400/90-06.Corrective Actions:Procedures OST-1008 & OST-1108 Revised to Delete Stroke Testing of Valve 1ST-359 on Quarterly Basis ML18009A5141990-05-0303 May 1990 Forwards Eddy Current Exam CP&L Shearon Harris Nuclear Power Plant Steam Generators A,B & C, Providing Results of Inservice Insps Performed During Plant Second Refueling Outage in Oct 1989 ML18009A4941990-04-26026 April 1990 Forwards Radiological Environ Operating Rept,1989, Radiological Environ Operating Rept,Vol II,Jan-June 1989, Sample Analyses Data & Radiological Environ Operating Rept,Vol III,Jul-Dec 1989,Sample Analyses Data. ML18009A5031990-04-25025 April 1990 Submits Suppl 2 to Relief Request R2-001 Re Plant 10-yr Inservice Insp Plan,Per 880129 Request ML18009A4911990-04-24024 April 1990 Forwards Addl Info Re Proposed Wakesouth Regional Airport to Be Located Near Facility,Per 900411 Request.Info Previously Provided to NRC During 900320 & 23 Telcons ML18009A4841990-04-24024 April 1990 Forwards Corrected Bases marked-up Page to 900226 Tech Spec Change Request Re Surveillance Intervals ML18009A4251990-03-30030 March 1990 Submits Supplemental Response to Station Blackout Rule Based on Guidelines Provided in NUMARC 87-00, Guidelines & Technical Bases for NUMARC Initiatives.... No Changes to Previous Calculations Necessary & One Deviation Noted ML18009A4231990-03-29029 March 1990 Suppls Response to NRC 900216 Ltr Re Violations Noted in Insp Rept 50-400/89-23.Corrective Actions:Surveys Performed to Determined Extent & Level of Contamination & Personnel Involved Decontaminated ML18009A4111990-03-23023 March 1990 Responds to NRC 900227 Ltr Re Violations Noted in Insp Rept 50-400/90-02.Corrective Actions:Personnel Involved W/ Quadrant Power Tilt Ratio Calculations & Operability Determination Counseled ML18009A4121990-03-23023 March 1990 Forwards Rev 17 to PLP-201, Emergency Plan & Fission Product Barrier Analysis.Rev to Emergency Plan Incorporates Comments Received During Recent Licensed Operator Requalification Training in Emergency Plan Procedures ML18009A4151990-03-22022 March 1990 Responds to NRC SALP Rept for Jul 1988 - Nov 1989.Contrary to Statement in Rept Significant Amount of Refresher Training Was Conducted During SALP Assessment Period Including Termination & Splicing & Motor & Bus Relays ML18009A4081990-03-19019 March 1990 Responds to NRC 900226 Ltr Re Violations Noted in Insp Rept 50-400/90-01.Corrective Actions:All Calibr Required by Tech Specs for Power Range Nuclear Instrumentation Satisfactorily Completed ML18022A7891990-03-0909 March 1990 Forwards Vols 1 & 2 of Inservice Insp Summary 1st Interval 1st Period,2nd Refueling Outage Completed 891222. ML18022A7881990-03-0606 March 1990 Confirms Understanding of Status of NRC Activities Re Proposed Wakesouth Regional Airport Located Near Plant Site. Pending Issues Should Be Resolved by 900331 to Enable Util to Complete Negotiations W/Airport Authority ML18022A7851990-03-0202 March 1990 Responds to NRC 900131 Ltr Re Violations Noted in Insp Rept 50-400/89-34.Corrective Actions:Valve SI-332 Closed & Gravity Drain Path Isolated & Shift Foreman Required to Review MMM-012 Re Priority/Emergency Maint Work Control ML18022A7721990-02-26026 February 1990 Forwards Application for Amend to License NPF-63,revising Tech Spec Surveillance 4.0.2 to Permit Surveillances to Be Extended Up to 25% of Specified Interval & Removing 3.25 Limitation from Spec,Per Generic Ltr 89-14 ML20011F3821990-02-26026 February 1990 Confirms Amount Electronically Transferred to Us Dept of Treasury,Nrc on 900223 for Payment of NRC Review Fees of 10CFR50 Applications & 10CFR55 Svcs Per 10CFR170,for Period of 890101-0617 for Listed Invoices ML18022A7701990-02-14014 February 1990 Notifies of Issuance of Renewal of NPDES Permit for Plant. Permit Encl ML18009A3831990-02-0909 February 1990 Responds to 900112 Ltr Re Violation Noted in Insp Rept 50-400/89-35.Corrective Actions:Valves ICS-775 & ICS-776 Added to Inservice Insp Program for Back Seat & Full Flow Testing & ICS-525 Revised to Satisfy Tech Spec Requirements ML18009A3751990-02-0101 February 1990 Forwards Retyped Tech Spec Pages Re 890630 Application for Amend to License NPF-63 Concerning RCS Pressure Temp Limits ML18009A3701990-02-0101 February 1990 Informs That Planned Corrective Actions Re Violations Noted in Insp Rept 50-400/89-28 Will Not Be Completed Until 900301 IR 05000400/19890281990-02-0101 February 1990 Informs That Planned Corrective Actions Re Violations Noted in Insp Rept 50-400/89-28 Will Not Be Completed Until 900301 ML18009A3631990-01-26026 January 1990 Responds to NRC Bulletin 88-008, Thermal Stratification in Piping Connected to Rcs. Design Differences That Either Minimize Potential of Occurrence or Enhance Possibility of Detection Should Scenario Be Created at Plant Determined ML18009A3531990-01-25025 January 1990 Forwards Reactor Containment Bldg Integrated Leak Rate Test Conducted in Oct 1989.Util Believes That Packing Leaks Discovered Are Isolated Failures & That Repair Should Prevent Recurrence ML18009A3501990-01-22022 January 1990 Forwards Revised Tech Spec Table 3.7-6, Area Temp Monitoring, Per 891218 Tech Spec Amend Request ML18022A7591990-01-17017 January 1990 Submits Results of Aircraft Hazards Study Associated W/ Proposed Wakesouth Regional Airport & Facility ML20005G5731990-01-16016 January 1990 Forwards Response to Insp Rept 50-400/89-32.Encl Withheld (Ref 10CFR73.21) ML18009A3351990-01-0505 January 1990 Forwards Rev 16 to Vol 1,Part 2 of Plant Operating Manual PLP-201, Emergency Plan. Revised NUREG-0654 Comparison W/ Plant Emergency Action Level Flow Path Also Encl for Review ML18009A3171989-12-21021 December 1989 Responds to NRC 891108 Ltr Re Violations Noted in Insp Rept 50-400/89-21.Corrective Actions:Incident Reviewed by Both Plant & Nuclear Engineering Dept Personnel to Avoid Future Miscommunication ML18009A3181989-12-15015 December 1989 Forwards Retyped Amend Bar Pages to Tech Spec Table 3.3-3 Re Auxiliary Feedwater Manual Initiation,Per 891026 Application for Amend to License NPF-63 ML18009A3011989-12-15015 December 1989 Forwards Proprietary WCAP-12403 & Nonproprietary WCAP-12404, LOFTTR2 Analysis for Steam Generator Tube Rupture W/Revised Operator Action Times for Shearon Harris Nuclear Power Plant. WCAP-12403 Withheld (Ref 10CFR2.790(b)(4)) ML18022A7371989-12-13013 December 1989 Forwards Change 3 to Rev 2 to State of Nc Emergency Response Plan in Support of Shearon Harris Nuclear Power Plant, Incorporating Administrative Enhancements. W/One Oversize Encl ML18009A2971989-12-0808 December 1989 Responds to NRC 891108 Ltr Re Violations Noted in Insp Rept 50-400/89-23.Corrective Action:Min of Four Decontamination Personnel Will Be Assigned 24 H Per Day During Fuel/Cask Handling to Maintain Cleanliness in Fuel Handling Bldg ML18009A2841989-11-30030 November 1989 Forwards Rev 0 to Core Operating Limits Rept in Support of Cycle 3 Operations ML18005B1531989-11-27027 November 1989 Forwards Retyped Amend Bar Pages to 890630 Request for Rev to License NPF-63 Re RCS pressure-temp Limits ML18022A7311989-11-27027 November 1989 Forwards Response to Generic Ltr 89-21, Request for Info Re Status of Implementation of USI Requirements. ML18005B1511989-11-17017 November 1989 Forwards 15-day Special Rept Identifying Number of Steam Generator Tubes Plugged During Current Inservice Insp Period ML18005B1501989-11-13013 November 1989 Suppls 890403 Response to NRC Bulletin 88-010, Nonconforming Molded-Case Circuit Breakers. Addl Nontraceable Molded Case Circuit Breakers (MCCB) & MCCBs Traceable to Refurbishers Noted During Records Review 1990-09-06
[Table view] |
Text
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i CP&L Carolina Power & Light Company imensammstimummmmmmzumiss HARRIS NUCLEAR PROJECT P.O. Box 165 New Hill, NC 27562
.AUG 2 81987 File Number: SHF/10-13510C 10CFR50.59 Letter Number: H0-870480 (0)
U.S. Nuclear Regulatory Commission ATTN: NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET No. 50-400 LICENSE NO. NPF-63 QUARTERLY REPORT IN ACCORDANCE WITH 10CFR50.59 Centlemen:
In accordance with 10CFR50.59 and CP&L Letter (NLS-86-454) of commitment dated December 9, 1986, the following report is submitted for the second quarter of 1987. This report contains brief summaries of changes to procedures and plant modifications, which change the plant as it is described in the FSAR. There were no tests or experiments conducted during this interval, which are not described in the FSAR which require reporting in this report. Changes to FSAR Chapter 14 have been previously submitted by separate letters.
Very truly yours, R. A. Watson Vice President Harris Nuclear Project RAW:acm Enclosure cc: Dr. J. Nelson Crace (NRC - RII)
Mr. C. Maxwell (NRC - SHNPP) 8709030144 070828 PDR ADOCK 05000400 PDR R ,
MEM/H08704800/1/OS1 11 )
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CHANCE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-000153, Demineralized Bypass Around the Condensate Storage Tank I (CST) and Reactor Makeup Water Storage Tank (RMWST)
FUNCTIONAL
SUMMARY
- This plant modification adds a demineralized water bypass line around the CST and the RMWST. This change was made to decrease the probability of power reductions due to chemistry excursions.
SAFETY
SUMMARY
- The portions of the Condensate Storage and Reactor Makeup Systems affected by this change do not serve a safety function. This change does not increase the probability or consequences of analyzed accidents, nor introduce a dif ferent type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
FSAR
REFERENCE:
Figure 9.2.3-2, 10.1.0-4, and Section 9.2.6 I
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MEM/H08704800/3/0S1
P CHANGE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-000362, Tubing Reroute From Gross Failed Fuel Detector (CFFD) to Primary Sample Panel FUNCTIONAL
SUMMARY
- This plant modification rerouted RCS sample tubing outside of containment to put the CFFD and the Primary Sample System (PSS) in parallel. Previously, the CFFD and the PSS were connected in series and the GFFD had to be manually bypassed when a Reactor Coolant System hot leg sample was taken. This tubing reroute eliminates the need to manually bypass the CFFD to take samples from the primary system, thus reducing manpower to obtain the sample. This modification also reduces the sample transport time from the RCS to the containment penetration. The minimum decay time was reduced from '
40 seconds to 28 seconds.
SAFETY
SUMMARY
- Neither the GFFD or the Primary Sampling System are required to function following an accident. This plant modification makes use of the Primary Sampling Panel easier. The change does not impact on the availability of the GFFD. The modification does not change the containment isolation capability or quality class of the installation. Thus, there is no impact on the safety design basis for the plant.
FSAR
REFERENCE:
Figure 9.3.6-1, Section 9.3.6 and 9.3.2 k
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CHANGE TO FACILITY AS DESCRIBED IN THE FSAR )
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l TITLE: PCR-000388, Condenser Off-Cas Flow Measurement Access FUNCTIONAL
SUMMARY
- This plant modification provides a test connection in condenser vacuum pump exhaust line 7AE 12-9-1 above isolation valve 7AE-B3-1 to allow measurement of the condenser off gas flow. Previously, no permanent l method existed for. measuring air-in leakage greater than 30scfm. i 1
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SAFET(
SUMMARY
- The condenser vacuum pump exhaust line is a nonsafety related f line located in the Turbine Building. The addition of a flow test connection on line 7AE12-9-1 will have no effect on any FSAR Chapter 15 accident analysis. This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident er equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
FSAR
REFERENCE:
Figure 10.1.0-4 l
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CHANCE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-000667, Containment Spray System Pump Miniflow Lines FUNCTIONAL
SUMMARY
- The original CT system design was such that the containment spray pump would start on Safety Injection Actuation Signal (SIAS) and run in the dead head miniflow recirculation mode until a Containment Spray Actuation Signal (CSAS) (Hi-3) was received to open the isolation valve. In this operation, it was necessary to provide overpressure protection on the suction side by the existence of relief valves (2CT-R6SA and 2CT-R7SB).
During construction, the system design was revised such that both the pump and valve receive a CSAS to actuate. This results in the situation where the pumps are not subject to run in the dead head recirculation mode and thus require no overpressure protection. Therefore, valves 2CT-R6SA and 2CT-R7SB have been locked closed and abandoned in place.
SAFETY
SUMMARY
- The relief valves abandoned per this plant modification were not needed as part of the original system design during licensing. The relief valves are no longer required for overpressurization protection. This change does not increase the probability or consequences of analyzed accidents, nor introduce a'different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists. j l
FSAR
REFERENCE:
Figure 6.2.2-1 i
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MEM/HO-8704800/6/051
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CHANCE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-000755, Filter Backwash Tank Vent Lines FUNCTIONAL
SUMMARY
- This plant modification installs check valves in the Liquid Waste Processing Systems filter backwash transfer tanks overflow lines' vacuum breakers. As previously designed, during filter backwash the transfer tank overflow line vacuum breakers could blow water into the tank rooms which caused a contamination problem in the area.
SAFETY
SUMMARY
- The purpose of this modification is to limit the spread of contamination. The modification will not contribute to the failure of a backwash transfer tank. In any event, the failure of a filter backwash storage tank is bounded by the failure of the' entire Liquid Waste Processing System as described in FSAR Section 15.7.2. Therefore, no unreviewed safety '
question exists.
FSAR
REFERENCE:
Figure 11.4.2-5, 11.4.2-6, and 11.4.2-9 f
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TITLE: PCR-001197, Volume Reduction Sys ter< (VRS) DemineEalired Water Pressure N
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FUNCTIONAL
SUMMARY
- This plandinodificatien insta11ed es prEdsure regulat big '
valve in the demineralized wate/y supply line to E-6 lbt Wster Heater. Ptsor ,
to this modification demineralized water supp1 A te K 6 Hot, Water Heatdr was approximately 200 PSIG. The heater is rated ut 160 psig and has a relief ,
valve setting of 125 psig. The .new pressure reghla, ting valve has a pressure setting of 100 psig. g; j -
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i SAFETY
SUMMARY
- The modification .'as made to sup;so rt pro;mr cvera:. r,n of the '
VRS. The Demineralized Water System is y nonsafdy system. This c'llange' does ,
not increase the probability or consequences of analyzed accidents, nor i introduce a different type of accident or equipren( malfunction O.an aircady '
evaluated in the FSAR. Thus, no unteviro6 safety 'questj on, exists. ;
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REFERENCE:
Figure 9.2.3-1 s N- N
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CHANGE TO FACILIT'f AS DESCRIBED IN THE FSAR TITLE: PCR-001235, Main Steam Drip Legs at Steam Driven Auxiliary Feedwater l (SDAFW): Pump
( FUNCTIONAL
SUMMARY
- This plant change supplements the two drip legs. at the SDAFW pump with steam traps. The modification was initiated due to sporadic trips of the SDAPW pump on overspeed apparently due to condensation in the !
s'.eam supply line. The design was changed, prior to OL issuance, to isolate the steam supply at the main steam lines when the SDAFW pump was in standby. l TMis lineup did not provide a way for condensation to return to the condenser dt e to the elevation difference between the drip leg and the condenser. The situation oss compounded due to steam leakage past the stesia supply isolation
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valves. The. previous design included drip legs which relied on steam supply p' essure and dondenser vacuum to draw the water out. This modification added arditional piping and drain traps; this allowed condensation to be directed to a ic:al floor drain. .
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SAFETY
SUMMARY
- This modification decreases the chance of condensate buildup when the isolation valves leak-by and therefore decreases the chance of Turbine overspeed trips or water slugging damage. This modification does not f increase the probability or consequences of analyzed accidents, nor introduce I a dif ferent. type of accident or equipment malfunction than already evaluated )
in the FSAR. Thus, no unreviewed safety questien exists. {
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REFERENCE:
Figure 10.1.0-4
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l CHANGE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-001286, Auxiliary Feedwater (AFW) Check Valve Back Leakage FUNCTIONAL
SUMMARY
- This plant modification adds additional check valves in the AFW piping. This modification was necessitated by the leakage of main feedwater back through the existing check valves (e.g., valves 3AF-V8SA-1, !
3AF-V31SB-1, 3AF-V175A-1, 3AF-V37SB-1, 3AF-V21SA-1, 3AF-V34SB-1 on FSAR Figure 10.1.0-3) in the AFW system. The back leakage caused excessive AFW pipeline temperatures and presented the possibility of steam formation in the lines and AFW pump steam binding.
FAFETY
SUMMARY
- The integrity of the AFW system has been increased by the additional check valves. The additional check valves were installed using the same design and installation requirements for the original design. The performance of the AFW system was determined to be acceptable based on a functional test. Furthermore, the addition has eliminated a problem which required extensive personnel actions to maintain the operability of the AFW system. The modification does not increase consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. The modification does provide a small increr.se in the probability of AFW system failure because of increased numbers of check valves. However, the increase in probability was calculated to be less than the probability of other single component failure in the AFW system. This small increase when balanced against the increased reliability '!
of the AFW due to the prevention of back leakage results in no increase in the l probability of AFW system failure. Thus, no unreviewed safety question exists.
PSAR
REFERENCE:
Figure 10.1.0-3, Section 10.4.9A 1
MEM/HO-8704800/10/OS1 ,
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CHANGE TO FACILITY AS DESCRIBED IN THE FSAR TITLE: PCR-001370, Condensate Booster Pump Hydraulic Coupling Control FUNCTIONAL
SUMMARY
- This plant modification relocates pressure transmitters PT-2307 and PT-2308 from condensate booster pump discharge piping to the suction piping of the feeduster pumps. The purpose cf the modification was to reduce the condensate booster pump discharge pressure so that the pressure drop across the feedwater regulating valves is reduced. Reducing the pressure drop across the feedwater regulating valves was necessary to improve valve stability and performance.
SAFETY
SUMMARY
- The relocation of PT-2307 and PT-2308 involves nonsafety related condensate controls. These controls affect the performance of the Main Feedwater System; however, the Main Feedwater System is not assumed to operate for any FSAR Chapter 15 accident. This modification will improve the reliability of the Main Feedwater System and therefore this change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
l FSAR
REFERENCE:
Figure 10.1.0-4 MEM/H08704800/11/OS1
. 1 CHANGE TO P.'.CILITY AS DESCRIBED IN THE FSAR l
TITLE: PCR-001547, Condenser Vacuum Pump Reservoir Supply f FUNCTIONAL
SUMMARY
- This plant modification to the Main Condenser Evacuation System (MCES) adds piping and valves to allow demineralized water to be used as a reservoir supply source for the Condenser Vacuum Pumps. This modification was to reduce condenser vacuum pump discharge temperatures and thereby increase the reliability of the Condenser Vacuum Pump.
SAFETY
SUMMARY
- floth the MCES and the Demineralized Water :iys tems are non-nuclear safety, nonseismic Category I systems. Neither of these systems are required to function for a design basis event as described in FSAR Chapter 15. Loss of condenser vacuum is an analyzed accident (refer to FSAR Section 15.2.5). This accident assumes the complete loss of condenser vacuum. Since the modification is to increase the reliability of the vacuum pump, this modification does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR, thus no unreviewed safety question exists.
FSAR
REFERENCE:
Figure 10.1.0-4 l
MEM/H08704800/12/OS1
e CHANCE TO FACILITY AS DESCRIBED IN THE FSAR
Title:
PCR-001771, Condenser Vacuum Pump Air Release FUNCTIONAL
SUMMARY
- This plant modification installed traps / separators on the condenser vacuum pump water reservoir overflow drains, which return air to the monitored discharge line. As previously designed, the overflow drains were releasing some pump discharge air which was not being monitored by the vacuum pump ef fluent radiation monitor or the Turbine Building vent monitor. The modification routes the liquid to a Turbine Building drain and the air /
noncondensable gaseous to the vacuum pump discharge line.
SAFETY
SUMMARY
- This modification provides assurance that noncondensable W I
gases discharged from the vacuum pump is monitored for radiation. The air evacuation system is non-nuclear safety clasi, and nonseismic Category I. This change does not impact any safety related equipment required for safe shutdown of the plant. No unreviewed safety question exists.
FSAR
REFERENCE:
Figure 10.1.0-4 l
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._- -____.____.__.________m. _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ __ __ . _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ , _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ _ _ _ _ _ ______ __
. l CHANGE TO PROCEDURE AS DESCRIBED IN THE FSAR I
TITLE: OP-120.03, Rev. 1, Advance Change 1, Chemical Drain Operating Procedure FUNCTIONAL
SUMMARY
- This procedure change adds steps which will allow liquid wastes from the chemical drain tanks to be pumped directly to the Laundry and flot Shower Tanks for processing. Previously, the procedure only allowed liquid wastes from the chemical drain tanks to be sent to the reverse osmosis (RO) concentrates evaporators via the RO concentrates tanks.
SAFETY
SUMMARY
- This change in procedure does not affect equipment which performs a safety function. This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
FSAR
REFERENCE:
Section 11.2.2.2 l
MEM/1108704800/14/OSI
CHANGE TO PROCEDURE AS DESCRIBED IN THE FSAR TITLE: OP-135, Rev. 1, Advance Change 2, Condensate Polishing Demineralizing System (CPDS)
FUNCTIONAL
SUMMARY
- The CPDS consists of six mixed bed demineralizers. '
Normally, only five of the units are in operation. The FSAR states that the sixth demineralized will be kept in the standby mode ready for automatic change out. This procedure change allows the spare demineralized to be kept in the "off" position; it will be manually placed in service when needed.
SAFETY
SUMMARY
- The CPDS is not required for safe shutdown of the reactor and is designed as non-nuclear safety equipment. This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
l FSAR REFERE" E: Section 10.4.6 1
NEM/H08704800/15/OS1
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CHANGE TO PROCEDURE AS DESCRIBED IN THE FSAR l
TITLE: PLP-106, Rev. 2, Advance Change 2, Technical Specification Equipment List Program FUNCTIONAL
SUMMARY
- This procedural change introduces a delay in Volume Control Tank (VCT) isolation on a Safety Injection Signal (SI). Review of the Safety Injection System sequencing logic by Westinghouse identified that upon receipt of an SI, the VCT outlet isolation valves do not begin to close until the Refueling Water Storage Tank (RWST) isolation valves are fully open. This results in an additional 15 second delay in the delivery of borated water to the Reactor Coolant System (RCS) not previously described in the FSAR.
SAFETY
SUMMARY
- An additional 15 second delay in the delivery of borated water to the reactor core by the Emergency Core Cooling System is introduced. This has been evaluated by Westinghouse (Letter FCQL-465). They determined that the impact on calculated values for mass and energy releases for FSAR Chapter 15 accident scenarios is insignificant. The limiting transient is a secondary piping break, and for this event the design DNB basis is still met. The analysis results for accidents analyzed in the FSAR have thus remained bounded with the 15 second delay included. Thus, no unreviewed safety issue exists.
FSAR
REFERENCE:
Section 6.3.3, 15.1.5, and 16.3 f '?J
. , i i t g MEM/H0-8704800/16/0S1
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