ML18009A408
| ML18009A408 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 03/19/1990 |
| From: | Richey R CAROLINA POWER & LIGHT CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| CON-NRC-704 NUDOCS 9003270341 | |
| Download: ML18009A408 (8) | |
Text
ACCELERATOR) DISTRIBUTlON DEMON.H1MTION.SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ESSION NBR:9003270341 DOC.DATE: 90/03/19 NOTARIZED: NO ACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION RICHEY,R.B.
Carolina Power 6 Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Responds to NRC 900226 ltr re violations noted in Insp Rept 50-400/90-01.
DISTRIBUTION CODE:
IE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Vi lation esponse DOCKET.,'5:
05000400 NOTES:Application for permit renewal filed.
050004'00 INTERNAL:
RECIPIENT ID CODE/NAME PD2-1 PD ACRS AEOD/DEIIB DEDRO NRR/DLPQ/LPEB10 NRR/DREP/PEP B9 D NRR/DRIS/DIR NRR/PMAS/ILRB12 OGC/HDS 1 RES MORISSEAU,D COPIES LTTR ENCL 1
1 2
2 1
1 1
1 1
1 1
1 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME BECKER,D AEOD AEOD/TPAD NRR SHANKMAN,S NRR/DOEA DIR ll NRR/DREP/PRPBll NRR/DST/DIR SE2 OC -ABSTRACT REG 02 2
FILE 01 COPIES LTTR ENCL 1
1 1
1 1
1 1
1 1
'1 2
2 1
1 1
1 1
'1 1
1 EXTERNAL: LPDR NSIC 1
1
'.1 1
NRC PDR 1
1 NOTE TO ALL"RIDS" RECIPIENIS I
PLEASE HELP US TO REDUCE WASIZI CONTACT THE DOCUMENI'ONSOL DESK; ROOM Pl-37 (EXT. 20079) TO ELMINATEYOUR NAMEFROM DISHUBUTION LISIS FOR DOCUMENTS YOU DON'T'NEEDl TAL NUMBER OF COPIES REQUIRED:
LTTR 25 ENCL 25
Carolina Power 8 Ught Company P. O. Box 165 ~ New Hill, N. C. 27582 R. B. RCHEY Manager Harris Nuclear Prolect iIAR i 9 1990 Letter Number:
HO-900050 (0)
Document Control Desk United States Nuclear Regulatory Commission Washington, DC 20555 NRC-704 SHEARON HARRIS NUCLEAR POWER PLANT DOCKET NO. 50-400 LICENSE NO. NPF-63 REPLY TO A NOTICE OF VIOLATION Gentlemen:
In reference to your letter of February 26,
- 1990, referring to I.E. Report RII:
50-400/90-01, the attached is Carolina Power and Light Company's reply to the violation identified in Enclosure 1.
k It is considered that
,the corrective actions taken/planned are satisfactory for resolution of the item.
Thank you for your consideration in this matter.
Very truly yours, R. B. Richey, Mana er Harris Nuclear Project AJH:tbb Enclosure cc'.
Mr. R. A. Becker (NRC)
Mr. S.
D. Ebneter (NRC RII)
Mr. J.
E. Tedrow (NRC SHNPP)
Pv03~70341
$ 0C>2 ADiil K 05'000400 PDC MEM/HO-9000500/1/OS1
ATTACHMENT TO CPGL LETTER OF
RESPONSE
TO NRC I.E.
REPORT RII: 50-400/90-01, VIOLATION Re orted Violation'.
Technical Specification (TS) '3.3.1 requires the Reactor
-Trip System Instrumentation of Power Range, Neutron Flux, High and Low Setpoints, and the High Negative and Positive Rate Trips be operable in Modes 1
and 2.
TS 2.2.1 requires the Reactor Trip System Instrumentation setpoints to be set consistent with the trip setpoint values shown in Table 2.2-1.
Table 2.2-1, in part, lists the power range setpoints as shown below.
a ~
b.
c ~
'd ~
High Setpoint Low Setpoint High Positive Rate High Negative Rate
(=109X of Rated Thermal Power (RTP)
<= 25X of RTP 5X of RTP 5X of RTP TS 3.7.1 requires that the Power Range Neutron Flux High Setpoint be lowered to
(=87K of RTP for an inoperable main steam safety valve.
Contrary to the
- above, at approximately 3:23 a.m.
on December 20,
- 1989, when the plant entered Mode 2
with an inoperable main steam safety valve, until approximately 3:30 a.m.
on December 23,
- 1989, when the power range instrument adjustments were completed, the Reactor Trip System Instrumentation setpoints were not set consistent with the trip values shown in Table 2.2-1 and TS 3.7.1.
Actual established Reactor Trip setpoints were calculated to be the following for the Power Range Neutron Flux'.
a.
b.
c ~
d.
High Setpoint Low Setpoint High Positive Rate High Negative Rate 127.5X of Rated Thermal Power (RTP) 37.5X of RTP 7.5X of RTP 7.5X of RTP This is a Severity Level IV violation (Supplement I) ~
Denial or Admission:
The violation is admitted.
The high setpoint was calculated at 125.5X, rather than 127.5X.
Reason for the Violation'.
A low leakage core loading pattern was installed for cycle three operation to improve fuel efficiency.
Although the vendor Nuclear Design and Operations Report identified a reduction in neutron leakage flux and provided recommended adjustments to the power range nuclear instrumentation (PR NIS) to compensate for this
- effect, these compensating adjustments were not made.
Initial criticality and power operation up to 28.1X indicated reactor power (42.5X actual reactor power) occurred prior to the point when the first calorimetric heat balance was performed, on MEM/HO-9000500/2/Osl
December 23,
- 1989, at approximately 2:30 a.m.
The PR NIS were adjusted at approximately 3:30 a.m. that morning.
The root cause was the lack of formal control over power ascension activities for refueling start-ups, and insufficient management attention to the planning and implementation of power ascension.
Testing requirements for pow'er ascension were identified by the reactor engineering group and placed on the outage schedule.
This schedule could be changed without appropriate management reviews and approvals.
The test procedure (EPT-008) which would have provided the compensating adjustments to the PR NIS was on the
- schedule, but was subsequently
- removed, based on the belief by the reactor engineer that the intent of the procedure had been achieved by previous activities.
Specifically, EPT-008 makes adjustments to the intermediate range instrumentation as well as the PR NIS.
The intermediate range detectors had been relocated further away from the reactor
- core, and so required recalibration to compensate for the movement.
This compensation had been previously determined and the instruments recalibrated, so when EPT-008 came due on the schedule, it was not performed.
The shift operations personnel did not detect the significant discrepancy between indicated reactor power from the PR NIS and other indications of power, especially the core delta temperature, which was providing an accurate indication of actual power level.
Plant procedures did not require any monitoring of specific indications of power level, and comparison of diverse indications.
The operators did note that the main generator load was higher than that which had previously been achieved for the indicated reactor power
- level, but this was attributed to efficiency improvements from modifications to the plant cooling tower made during the
- outage, and from the extreme cold weather which was experienced during the period.
Training for cycle three operations did identify an expected reduction in the neutron flux leakage and the impact on the PR NIS, but this training had not emphasized the significance of the
- impact, and the training had been conducted several months prior to cycle three start up.
Following the
- incident, an evaluation was made to determine the safety significance.
It was determined that the diverse trip features of the Reactor Protection
- System, specifically the overtemperature and overpower delta temperature reactor
- trips, provided protection for the core for the existing conditions at which the plant
- operated, and for power levels at which it was planned to operate prior to stabilizing to perform the calorimetric heat balance.
Corrective Actions Taken and Results Achieved:
The PR NIS was immediately adjusted to indicate the actual power level once the calorimetric heat balance indicated a
miscalibration.
All calibrations required-by Technical Specifications for the PR NIS have been satisfactorily completed.
MEM/HO-9000500/3/OS1
Briefings on the event and its significance have been conducted for plant management and supervisors, licensed operators, and reactor engineering personnel.
Further investigation of this event was conducted to evaluate human, performance.
An investigation by personnel not associated with the plant was also conducted.
Corrective Ste s Taken to Avoid Further Violations:
A formal program to identify the cycle specific requirements of the Power Ascension Test Program is being developed and will be in place prior to the next refueling start up.
The plant start up procedure has been changed to require comparison of the PR NIS to other diverse indications of reactor
- power, and resolution of any gross discrepancies.
Additional training of technical staff and management personnel is
- planned, as well as
- changes, where appropriate, to licensed operator training and requalification training.
Practices for scheduling cycle-specific training will be reviewed and revised as appropriate.
The test procedures for power ascension activities are being reviewed and will be revised as necessary prior to their next use.
Reference:
LER 89-023-00 MEM/HO-9000500/4/OS1
,A