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Category:CORRESPONDENCE-LETTERS
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20216G3501999-09-29029 September 1999 Confirms Conversations Re NRC Staff Voluntary Response to Orange County Discovery Requests.Staff Will Voluntarily Answer Discovery Requests & Will Not Waive Any Objection or Privilege Under NRC Regulations.Related Correspondence ML20212M1081999-09-29029 September 1999 Confirms Intent to Meet with Utils on 991025 in Atlanta,Ga to Discuss Pilot Plants,Shearon Harris & Sequoyah Any Observations & Lessons Learned & Recommendations Re Implementation of Pilot Program ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML20212H7741999-06-23023 June 1999 Responds to Re Petition Filed by Orange County Board of Commissioners Re Proposed Expansion of Sf Storage Capacity at Shearon Harris Npp.Public Meeting Will Be Held at Later Date.With Certificate of Svc.Served on 990624 ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML20206R2511999-05-19019 May 1999 Responds to Addressed to Chairman Jackson Requesting That NRC Grant Standing to Orange County Board of Commissioners in Shearon Harris Proceeding Currently Before Board.With Certificate of Svc.Served on 990519 ML20206Q5281999-05-17017 May 1999 Responds to 990304 Request for Two Rail Routes to Be Used for Transport of Spent Fuel from Brunswick Steam Electric Plant,Southport,Nc & Hb Robinson Steam Electric Plant, Hartsville,Sc to Shearon Harris Npp,Near New Hill,Sc ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9601999-05-11011 May 1999 Forwards Resolution Adopted by Carrboro Board of Aldermen at 990504 Meeting.Resolution Expresses Town Concern Re Util Plans to Double high-level Nuclear Waste Storage at Shnpp ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl IR 05000400/19982011999-04-12012 April 1999 Discusses Safeguards Insp Rept 50-400/98-201 (Operational Safeguards Response Evaluation) on 980908-11.No Violations Noted.Licensee Performance During Evaluation Indicated Excellent Overall Contingency Response Capability 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl ML18016A8911999-04-0505 April 1999 Forwards non-proprietary App 4A,pages 20-25 & Proprietary Page 4-6 to re-issued Rev 3 of Holtec International Licensing Rept HI-971760.Pages Were Inadvertently Omitted from Reissued Rept.Proprietary Page 4-6 Withheld ML18016A8891999-04-0101 April 1999 Forwards Rev 99-1 to Plant EALs for NRC Review & Approval, Per 10CFR50,App E.Encl Provides Comparison of Currently Approved EALs & Proposed Rev 99-01.Approval of EALs Prior to June 1999,requested.With Four Oversize Drawings ML18016A8811999-03-31031 March 1999 Responds to NRC 990301 Ltr Re Violations Noted in Insp Rept 50-400/98-11.Corrective Actions:Post Trip/Safeguards Actuation Rept for 981023,RT Was Corrected,Required Reviews Completed & Approval Obtained on 990219 ML18016A8671999-03-19019 March 1999 Submits Response to RAI Re Spent Fuel Pool Water Level & Revised Fuel Handling Accident Analyses,Per 990317 Telcon with NRC ML18016A8631999-03-19019 March 1999 Forwards Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept, IAW 10CFR55.45(b)(5)(ii). NRC Form 474 & Required Info Re Simulator Performance Test Results & Schedules Also Encl ML18016A8691999-03-18018 March 1999 Forwards Resolution Adopted by Lee County,North Carolina Board of Commissioners Re Proposed Expansion of high-level Radioactive Waste Storage Facilities at Carolina Power & Light Shearon Harris Nuclear Power Plant ML18016A8511999-03-15015 March 1999 Forwards Proprietary & non-proprietary Version of Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFPs 'C' & 'D'. Repts Are Reissued to Reflect Reduction in Proprietary Info.Proprietary Info Withheld ML18016A8601999-03-15015 March 1999 Informs NRC of Mod to Commitment for Hnp,Re Comprehensive Review of Implementation of TS Sr.Upon Completion of Listed Reviews,Surveillance Procedure Review Project Will Be Considered Complete 1999-09-08
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CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
QJ ACCESSION NBR:99 04060082 DOC.DATE: 99/03/31 NOTARIZED: NO FACIL:50-400 Sh earon Harris Nuclear Power Plant Unit 1 Carolina DOCKET 05000400 I
AUTH. NAME 'UTHOR AFFILIATION SCAROLA,J, Carolina Power & Light Co.
RECIP . NAME RECIPIENT AFFXLIATION Records Management Branch (Document Control Desk)
SUBJECT:
Responds to NRC 990301 ltr re violations noted in insp rept 50-400/98-11.Corrective actions:PTSAR for 981023,RT was corrected, required reviews completed 5 approval obtained on 990219. A DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response E
NOTES:Application for permit renewal filed. 05000400 G
RECIPIENT COPIES RECIPIENT COPIES p ID CODE/NAME LTTR ENCL XD CODE/NAME LTTR ENCL PD2-1 PD 1 1 FLANDERS,S 1 1 R INTERNAL: ACRS 2 2 AEOD/SPD/RAB 1 1 Y AEOD TTC 1 1 DEDRO 1 1
~~XLE CENTE 1 1 NRR/DRCH/HOHB 1 1 NRR/DRPM~PECB 1 1 NRR/DRPM/PERB 1 1 NUDOCS-ABSTRACT 1 1 OE DIR 1 1 OGC/HDS2 1 1 RGN2 FILE 01 1 1 EXTERNAL: LMITCO MARSHALL 1 1 NOAC 1 1 D NRC PDR 1 1 NUDOCS FULLTEXT 1 1 p
N NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19
Carolina Power 8 Ught Company James Scarola PO Box 165 Vice President New Hill NC 27562 Harris Nuclear Plant MAR 81 ]999 SERIAL: HNP-99-051 United States Nuclear Regulatory Commission ATTENTION: Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT DOCKET NO. 50<00/LICENSE NO. NPF-63 REPLY TO NOTICE OF VIOLATION(NRC INSPECTION REPORT NO. 50-400/98-11)
Dear Sir or Madam:
Attached is Carolina Power & Light Company's reply to the Notice of Violation described in of your letter dated March 1, 1999.
Questions regarding this matter may be referred to Mr. J. H. Eads at (919) 362-2646.
Si erely, MGW
Attachment:
c: Mr. J. B. Brady (NRC Senior Resident Inspector, HNP)
Mr. Rich Laufer (NRR Project Manager, HNP)
Mr. L. A. Reyes (NRC Regional Administrator, Region II) 9'7040b0082 'F9033i PDR ADQCK 05000400 8 PDR 5413 Shearon Harris Road New Hill, NC Tel 919 362-2502 Fax 919 362-2095
0 Attachment to HNP-99-051 REPLY TO NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50-400/98-11 Re orted Violation A:
Technical Specification 6.8.1 requires, in part, that written procedures be established, implemented, and maintained covering the applicable procedures recommended in appendix A of Regulatory Guide 1.33, Revision 2, 1978. That appendix specifically lists a procedure for "Authorities and Responsibilities for Safe Operation and Shutdown."
Regulatory Guide 1.33, Revision 2, 1978, specifically endorses ANSI N18.7-1972/ANS-3.2, "Administrative Controls and Quality Assurance for the Operational Phase of Nuclear Power Plants." In section 5.2.1, that standard states, in part, that the responsibilities and authorities of plant operating personnel include "the responsibility to determine the circumstances, analyze the cause, and determine that operations can proceed safely before the reactor is returned to power after a trip."
Procedure OMM-004, "Post-trip/Safeguards Actuation Review," Revision 10, implements those requirements. Section 5.2 requires, in part, that the direct cause of the event be determined, that proper plant response be verified, and that the results be documented in the Post Trip/Safeguards Actuation Report. It further requires that the Post Trip/Safeguards Actuation Report be thoroughly reviewed to ensure that any indications of improper plant response are clearly documented.
- 1. Contrary to the above, as of November 20, 1998, the licensee had not verified proper plant response for the October 23, 1998, reactor trip, in that the Post Trip/Safeguards Actuation Report incorrectly indicated that the steam-dump valves had closed when reactor coolant system average temperature reached 544'F.
- 2. Contrary to the above, as of November 20, 1998, the Post Trip/Safeguards Actuation Report for the October 23, 1998, reactor trip had not been thoroughly reviewed, in that the required reviews failed to identify that numerous indications of plant response required to be included by procedure OMM-004, had not been included in the report.
This is a Severity Level IV violation (Supplement I).
Denial or Admission of Violation:
The violation is admitted.
Reason for the Violation:
As stated in example 1 above, there was an error in the Post Trip/Safeguards Actuation Report (PTSAR) for the October 23, 1998, reactor trip regarding the relationship between steam dumps and RCS temperature. The error occurred because the individual analyzing the data misinterpreted the'ost trip computer generated reports.
As stated in example 2 above, the PTSAR had not been thoroughly reviewed, in that the required reviews failed to identify the error mentioned in example 1 and the failure to meet other requirements of OMM-004 including the untimely completion of a follow up review. The
L-Attachment to HNP-99-051 inadequate reviews occurred due to inadequate focus by involved personnel and station management..
Corrective Ste s Taken and Results Achieved:
The PTSAR for the October 23, 1998, reactor trip was corrected, required reviews completed and approval obtained on February 19, 1999. The follow up review was completed on February 18, 1999.
The Plant General Manager has discussed the importance of complying with the requirements of OMM-004 with appropriate operations personnel. Also, during an HNP Manager/Supervisor meeting held on March 11, 1999, the Plant General Manager counseled the management staff regarding his expectations for procedure compliance and attention to detail.
Corrective Ste s That Will Be Taken to Avoid Further Violations:
A revision will be made to procedure OMM-004 to better focus Management's expectations for data collection, data analysis, and review. This revision will be completed by April 30, 1999.
Date When Full Com liance Was Achieved:
Full compliance was achieved on February 19, 1999, based on completion of corrections, required reviews and approvals and the follow up review of the PTSAR for the October 23, 1998 reactor trip.
Re orted Violation 8:
10 CFR 50, Appendix B Criterion V, "Instructions, Procedures, and Drawings," requires, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures or drawings.
10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," requires, in part, that measures shall be established to assure that conditions adverse to quality are promptly identified and corrected. In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition is determined and corrective action taken to preclude repetition. The Quality Assurance Program Manual (NGGM-PM-0007) and procedure CAP-NGGC-0001, "Corrective Action Management," Revision 1 implement that requirement.
Procedure CAP-NGGC-001 requires a person who identifies an adverse condition to initiate a Condition Report. It also requires that a Condition Report (CR) which involves a significant change outside normal plant variances in a key plant parameter (including water levels) be classified as a "Significant Adverse Condition."
Contrary to the above:
- 1. As of November 18, 1998, the licensee had failed to properly classify as significant a condition where all valid reactor vessel water level indications were disabled while the reactor coolant system was in a reduced-inventory condition, and failed to determine the cause of the condition, in that the Condition Report that described the condition was classified as an Adverse Condition, and the associated evaluation failed to identify that the cause was an inadequate design.
Attachment to HNP-99-051 As of January 22, 1999, the licensee had not initiated a Condition Report for an identified adverse condition, in that, after becoming aware that the Post Trip/Safeguards Actuation Report for the October 23, 1998, reactor trip and associated reviews were inadequate, the licensee did not initiate a Condition Report.
This is a repeat Severity Level IV violation (Supplement I).
Denial or Admission of Violation:
The violation is admitted.
Reason for the Violation:
This violation occurred due to ineffective communication and reinforcement of expectations regarding documentation of Adverse Conditions. In addition, there was inadequate monitoring of the Corrective Action Program (CAP) implementation by Harris Nuclear Plant (HNP) Management.
Specifically, the condition referenced in example 1 (CR 98-03025) did not receive an event classification by management or personnel more knowledgeable of the event to ensure the appropriate level of attention was applied. Additionally, the CR did not have sufficient detail in the event description to communicate that all valid reactor vessel water level indications were disabled while the reactor coolant system was in a reduced-inventory condition. Without consideration of this aspect of failure, this condition did not meet the significance criteria specified in the applicable procedure CAP-NGGC-0001. It is the expectation of HNP Management that a loss of all valid reactor vessel water level indications while the reactor coolant system was in a reduced-inventory condition would result in a documentation of that specific element to ensure proper evaluation of operability and reportability.
The condition referenced in example 2 meets the threshold of initiating a Condition Report in accordance with procedure CAP-NGGC-0001. The inadequacy of the Post Trip/Safeguards Actuation Report for the October 23, 1998, reactor trip and subsequent reviews was realized by HNP Management, but this realization failed to result in documentation in the form of a Condition Report. This failure to document the recognized Adverse Condition was due to inadequate performance monitoring of the Corrective Action Program implementation by HNP Man'agement.
Corrective Ste s Taken and Results Achieved:
The event referenced in example 1 (CR 98-03025) was re-classified as Significant Adverse. A Root Cause Investigation was performed and resulted in identification of inadequate design as the cause.
Condition Reports 98-03314 and 99-00414 were written to document the conditions referenced in example 2. The investigation for CR 98-03314 evaluated the inadequate performance of OMM-004 Post Trip/Safeguards Actuation Report. CR 99-00414 documents inadequate review and approval by HNP Management. Actions taken by that CR were completed on March 11, 1999, by the Plant General Manager by providing a presentation to Management/Supervision on the role of Management/Supervision related to the Corrective Action Program.
Additionally, Condition Report 98-03264 was written to document the HNP's failure to document adverse conditions in a timely manner. This CR was classified as Significant Adverse and a Root
Attachment to HNP-99-051
'ause Investigation was performed. The following are significant corrective actions which have been completed as a result of the investigation:
- 1. Expectations were developed regarding timeliness, responsibility of documentation, monitoring and shift review of activities associated with Adverse Conditions with the focus of this guidance being to ensure documentation of events prior to the end of the shift by knowledgeable personnel when practical. These expectations were communicated via a site memorandum from the Plant General Manager.
- 2. Select membership of the station management team (including Plant General Manager and Section Heads) have initiated a periodic review of Condition Reports. This review is for the purpose of:
Gaining knowledge of plant activities necessitating the initiation of a Condition Report.
Ensuring that known problems have been appropriately captured within the condition reporting process.
Specifying or highlighting those CR's that warrant additional or a higher level of management involvement or follow through to ensure that the proper level of sensitivity is provided to the problem, it's analysis, strategy to correct and it' remediation.
~ Identifying those CR's which require immediate interim corrective actions to be devised and implemented while the detailed investigation is completed and corrective actions to prevent recurrence can be developed and implemented.
- 3. Established a periodic Unit Evaluator meeting for assignment and classification of condition reports, using a multi-disciplined team.
- 4. Reinforced the expectation for full compliance with the CAP procedures; this was performed by the Plant General Manager at an HNP Manager/Supervisor meeting on March 11, 1999.
Corrective Ste s That Will Be Taken to Avoid Further Violations:
The corrective actions listed above are sufficient to avoid further violations.
Date When Full Com liance Was Achieved:
Full compliance was achieved on February 11, 1999.
Re orted Violation C:
10 CFR 50, Appendix B, Criterion III, "Design Control," requires, in part, that measures shall be established to assure that applicable regulatory requirements are correctly translated into specifications, drawings, procedure's, and instructions, and that design changes shall be subject to measures which provide for verifying or checking the adequacy of design.
EGR-NGGC-0005, "Engineering Service Requests," Revision 9, implements Criterion III, and requires, in part, that the Responsible Engineer provide testing requirements which verify that the modified system/component functions/performs as intended, the design change has been correctly implemented, and the revised design is correct.
Attachment to HNP-99-051 Contrary to the above, as of December 8, 1998, Engineering Service Request (ESR) 94-00099, "RCS vacuum fill,"Revision 10, had not translated applicable regulatory requirements that would provide instrumentation to adequately monitor and control reactor vessel water level into specifications, drawings, procedures, and instructions, and had not verified or checked the adequacy of the design, in that the design described in that ESR did not provide instrumentation that accurately monitored reactor vessel water level, testing to verify that design was not performed, and reviews of the design were not adequate to determine that the design was not correct.
This is a Severity Level IV violation (Supplement I).
Denial or Admission of Violation:
The violation is admitted..
Reason for the Violation:
The reason for the violation is personnel error on the part of the Responsible Engineer (RE) and inadequate independent reviews performed of the modification package due to the lack of diversity in the review process.
ESR 94-00099 provided a design which improperly located the reference tap connections on the vacuum fillcart manifold for the Reactor Coolant System (RCS) level instrumentation used during the vacuum fillprocess. The connection design configuration for the vacuum fillcart, hoses and adapter plate for the connection to the pressurizer, when placed in service, caused a local vacuum to be sensed by level instrumentation which effectively disabled all RCS level instrumentation. The current ESR,process as described by procedure EGR-NGGC-0005, Revision 9 provides adequate guidance'to qualified REs to ensure that applicable design inputs are identified, documented and evaluated. However, in this case, the RE failed to ensure that the design configuration met the requirements of Generic Letter 88-17, which requires two independent indications of RCS level or the requirements of 10 CFR 50 Appendix A, Criterion 13, as committed to in FSAR Section 3.1.9 which requires, in part, that instrumentation be provided to adequately monitor reactor vessel water level.
The RE did not perform an adequate plant/system design analysis or failure modes and effects evaluation. The differences between the HNP vacuum fillconfiguration and the South Texas and Wolf Creek configurations, from which the HNP modification was modeled were not properly evaluated to determine the effects on indicated RCS level. Having a proven vacuum filldesign from Wolf Creek in hand, gave a comfort level to the RE and independent reviewers which minimized their perceived need to perform an in-depth review of possible failure modes.
Consequently, the RE and independent reviewers did not identify the unanticipated interactions between the vacuum fillcart configuration and RCS level indication.
Neither the RE or independent reviewers recognized a practical approach to testing the overall system for possible effects. The RE did not specify design parameters to be tested and acceptance criteria. Therefore, no testing was performed to determine the effect of the configuration on RCS level indication prior to using the vacuum fillequipment. The lack of post modification testing or acceptance testing was not challenged by the independent reviewers. The absence of testing and acceptance criteria to verify the modified system pe<orms as intended is not in compliance with EGR-NGGC-0005 section 9.4.7.
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'ttachment to HNP-99-051 The RE for design of the Vac'uum Fill modification also performed the mechanical engineering discipline review, Residual Heat Removal (RHR) plant system review and first safety review. The design verifier was the ESR initiator as well as the RCS plant system engineer reviewer and second safety reviewer. The initiator/design verifier also provided a copy of the Wolf Creek design, which was the primary input to the HNP design, to the RE. Although the reviews/involvement by the two individuals were procedurally acceptable, the diversity of the review process is believed to have been diminished. In this high risk first time evolution there was a lack of management oversight of the design and implementation process. The supervisor did not recognize the lack of reviewer independence.
Corrective Ste s Taken and Results Achieved:
This event has been reviewed with the involved RE, involved reviewers and other engineering personnel involved in the design and review process for ESRs. This was accomplished through the Engineering Support Personnel (ESP) Training Program. The training discussion emphasized the following points:
~ Consider possible effects of the design on instrumentation and other system components.-
'rovide testing that adequately covers design parameters to validate assumptions.
Emphasis must be placed on system testing following installation (post modification testing) in the ESR process. The testing must be looked at for complete system testing or individual component testing.
~ Utilize industry design experience.
The need to initiate a Condition Report to identify a deficiency of a design assumption.
~ In potential high risks modifications, minimize situations where one ESR reviewer performs multiple reviews.
~ Provide clear assumptions in the ESR design. Provide clear procedure and document changes in the ESR by either markups, separate descriptive lists, or write ups. These will define the impact of the design change and provide a document trail for design package reviewers and customers.
Engineering management's expectation that the design verifiers for ESRs maintain independence has been reemphasized to engineering supervision.
A review was performed of EGR-NGGC-0011 (Conduct of Engineering Products Review) to verify that the procedure provides for the necessary oversight of ESRs that are risk significant or involve high risk evolutions. This review concluded that EGR-NGGC-0011 does provide the necessary oversight of ESRs that are risk significant or involve high risk evolutions. It should be noted that EGR-NGGC-0011 was effective on January 5, 1998 and was not in affect at the time ESR 94-00099 was initially approved.
Corrective Ste s That Will Be Taken to Avoid Further Violations:
Procedure EGR-NGGC-0005 will be revised to expand guidance regarding post modification testing to include that the RE consider mockup testing if implementation testing is not practical. This change will be completed by July 15, 1999.
Date When Full Com liance Was Achieved:
Full compliance was achieved on January 27, 1999, when the plant procedure (GP-001), which utilizes vacuum fill, was placed on hold pending resolution of the vacuum fill modification.