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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J3341999-10-19019 October 1999 Forwards Request for Addl Info Re Sale of Portion of Land Part of Oyster Creek Nuclear Generating Station Site Including Portion of Exclusion Area ML20217E0181999-10-0606 October 1999 Provides Nj Dept of Environ Protection Comments on Oyster Creek Nuclear Generating Station TS Change Request 267 Re Clarifications to Several TS Sections ML20216J7591999-09-30030 September 1999 Informs NRC That Remediation Efforts for Software Sys Etude & Rem/Aacs/Cico Have Been Completed According to Schedule & Now Y2K Ready 05000219/LER-1998-011, Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts1999-09-30030 September 1999 Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts ML20212J6721999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Oyster Creek Nuclear Generating Station on 990913.No Areas Identified in Which Licensee Performance Warranted Addl Insp Beyond Core Insp Program.Historical Listing of Plant Issues Encl ML20216K1421999-09-29029 September 1999 Provides NRC with Name of Single Point of Contact for Purpose of Accessing Y2K Early Warning Sys,As Requested by NRC Info Notice 99-025 ML20217D1661999-09-27027 September 1999 Forwards Proprietary Completed NRC Forms 396 & 398,in Support of License Renewal Applications for Listed Individuals,Per 10CFR55.57.Encl Withheld ML20217B2531999-09-24024 September 1999 Informs That on 980903,Region I Field Ofc of NRC Ofc of Investigations Initiated Investigation to Determine Whether Crane Operator Qualification/Training Records Had Been Falsified at Oyster Creek Nuclear Generating Station ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212A7921999-09-13013 September 1999 Forwards Second RAI Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, Issued on 950817 to Plant ML20212B5571999-09-10010 September 1999 Forwards Rev 11 to Oyster Creek Emergency Dose Calculation Manual, IAW 10CFR50,App E,Section V ML20211N2941999-09-0303 September 1999 Responds to NRC 990802 Telcon Request for Environ Impact Assessment of TS Change Request 251 Concerning Movement of Loads Up to 45 Tons with RB Crane During Power Operations ML20211J9831999-09-0202 September 1999 Discusses 990804 Telcon Re Sale of Portion of Oyster Creek Nuclear Generating Station Land.Requests Info Re Location of All Areas within Property to Be Released Where Licensed Radioactive Matl Present & Disposition of Radioactive Matl ML20211J6771999-08-30030 August 1999 Submits Response to NRC 990802 Telcon Request for Gpu to Provide Environ Impact Assessment for Tscr 251 ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211C0161999-08-19019 August 1999 Advises That Info Submitted by Ltr,Dtd 990618, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool, Holtec Rept HI-981983,rev 4,will Be Withheld from Public Disclosure,Per 10CFR2.790 ML20211B9011999-08-18018 August 1999 Forwards Rev 0 to EPIP 1820-IMP-1720.01, Emergency Public Info Implementing Procedure ML20210U4341999-08-17017 August 1999 Responds to to Chairman Dicus of NRC on Behalf of Fm Massari Concern About Oyster Creek Nuclear Generating Station Not Yet Being Fully Y2K Compliant ML20210Q7331999-08-12012 August 1999 Responds to Re TS Change Request (TSCR)264 from Oyster Creek Nuclear Generating Station.Questions Re Proposed Sale of Property within Site Boundary & Exclusion Area ML20210L6311999-08-0606 August 1999 Discusses Licensee Response to GL 92-01,Rev1,Suppl 1, Rv Structural Integrity, for Plant.Staff Has Revised Info in Rv Integrity Database & Releasing as Rvid Version 2 ML20210D2801999-07-22022 July 1999 Submits Response to Administrative Ltr 99-02 Operating Reactor Licensing Action Estimates. Estimate of Licensing Actions Projected for Fy 2000 Encl.No Projection Provided for Fy 2001 ML20209H5001999-07-14014 July 1999 Forwards Revised TS Pages 3.1-15 & 3.1-17 Which Include Ref to Note (Aa) & Approved Wording of Note H of Table 3.1.1, Respectively ML20210U4411999-07-12012 July 1999 Forwards Article from Asbury Park Press of 990708 Faxed to Legislative Officer by Mutual Constitute Fm Massari Indicating That Oyster Creek Nuclear Generating State Not Fully Y2K Compliant ML20209G1451999-07-0909 July 1999 Forwards Rev 1 to 2000-PLN-1300.01, Oyster Creek Generating Station Emergency Plan. Attachment 1 Contains Brief Summary of Changes,Which Became Effective on 990702 ML20209E0821999-07-0707 July 1999 Forwards TS Change Request 269 for License DPR-16,changing Component Surveillance Frequencies to Indicate Frequency of Once Per Three Months ML20209B7501999-07-0101 July 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Generic Ltr 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Licensee Y2K Readiness Disclosure for Ocngs,Encl ML20196G1361999-06-23023 June 1999 Provides Status of Corrective Actions Proposed in in Response to Insp Rept 50-219/98-80 & Revised Schedule for Completion of Actions Which Are Not Yet Complete ML20196E6421999-06-22022 June 1999 Forwards Revised Pages of TS Change Request 261,dtd 990618. Replacement Requested Due to Several Dates Being Omitted on Certain Pages ML20195G6541999-06-0707 June 1999 Discusses 981204 Initiation to Investigate Whether Contract Valve Technician,Was Discriminated Against for Raising Concern Re Use of Untrained/Unqualified Workers Performing Valve Repairs.Technician Was Not Discriminated Against ML20195G6631999-06-0707 June 1999 Discusses 981204 Intiation to Investigate Whether Contract Valve Technician Was Discriminated Against for Raising Concern Re Use of Untrained/Unqualified Workers Performing Valve Repairs.Technician Was Not Discriminated Against ML20209B0561999-06-0404 June 1999 Informs That NRR Has Reorganized,Effective 990328.Forwards Organizational Chart ML20195D0551999-06-0303 June 1999 Forwards TS Change Request 226 to License DPR-16,permitting Operation with Three Recirculation Loops.Certificate of Svc & Tss,Encl ML20195C5511999-05-25025 May 1999 Forwards Book of Controlled Drawings Currently Ref But Not Contained in Plant Ufsar.Drawings Were Current at Time of Submittal ML20206N7711999-05-11011 May 1999 Forwards Rev 0 to Oyster Creek Emergency Plan, IAW 10CFR50.47(b) & 10CFR50.54(q).Changes Became Effective on 990413 ML20206H9441999-04-28028 April 1999 Forwards Application for Amend to License DPR-16,requesting Approval to Handle Loads Up to & Including 45 Tons Using Reactor Bldg Crane During Power Operations,Per NRC Bulletin 96-002 ML20206B6991999-04-26026 April 1999 Forwards Copy of Rev 11 to UFSAR & Rev 10 to Oyster Creek Fire Hazards Analysis Rept. Without Fire Hazard Analysis ML20206D3801999-04-26026 April 1999 Forwards Rev 11 to UFSAR, & Rev 10 to Fire Hazards Analysis Rept, for Oyster Creek Nuclear Generating Station, Per 10CFR50.712(e) ML20206A9931999-04-22022 April 1999 Forwards Number of Personnel & Person Rems by Work & Job Function Rept for Period Jan-Dec 1998. Included in Rept Is Listing of Number of Station,Util & Contractor Personnel as Well as Diskette Reporting 1998 Occupational Radiation ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 ML20205P8411999-04-15015 April 1999 Forwards TS Change Request 267 to License DPR-16,modifying Items in Sections 2 & 3 of Ts,Expanding Two Definitions in Section 1 & Modifying Bases Statements in Sections 2,3 & 4. Certificate of Svc Encl ML20205P5381999-04-14014 April 1999 Ack Receipt of Re Request for Exception to App J. Intended Correction Would Need to Be Submitted as Change to TS as Exceptions to RG 1.163 Must Be Listed in Ts,Per 10CFR50,App J ML20205P9401999-04-12012 April 1999 Informs NRC That Gpu Nuclear Is Modifying Oyster Creek FSAR to Reflect Temp Gradient of 60 F & to Correct Historical Record ML20205P0651999-04-0909 April 1999 Discusses 990225 PPR & Forwards Plant Issues Matrix & Insp Plan.Results of PPR Used by NRC Mgt to Facilitate Planning & Allocation of Insp Resources 05000219/LER-1998-015, Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page1999-04-0505 April 1999 Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page ML20205J3281999-04-0101 April 1999 Discusses Arrangements Made on 990323 for NRC to Inspect Licensed Operator Requalification Program at Oyster Creek Nuclear Generating Station During Week of 990524 ML20205H1081999-03-31031 March 1999 Forwards Current Funding Status for Decommissioning Funds Established for OCNPP,TMI-1,TMI-2 & SNEC ML20205F0611999-03-25025 March 1999 Submits Info on Sources & Levels of Property Insurance Coverage Maintained & Currently in Effect for Oyster Creek Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20205E1171999-03-24024 March 1999 Forwards Rev 39 to Oyster Creek Security Plan & Summary of Changes,Iaw 10CFR50.54(p).Rev Withheld ML20207F0331999-03-0404 March 1999 Forwards Insp Rept 50-219/98-12 During Periods 981214-18, 990106-07 & 20-22.Areas Examined During Insp Included Implementation of GL 89-10 & GL 96-05.No Violations Noted ML20207K2471999-02-25025 February 1999 Forwards Fitness for Duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Ny 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217E0181999-10-0606 October 1999 Provides Nj Dept of Environ Protection Comments on Oyster Creek Nuclear Generating Station TS Change Request 267 Re Clarifications to Several TS Sections 05000219/LER-1998-011, Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts1999-09-30030 September 1999 Forwards LER 98-011-02, Three Small Bore Pipe Lines Did Not Meet Design Bases for Siesmic & Thermal Allowables. Engineering Std Will Not Be Completed Until End of 4th Quarter of 1999 Due to Scheduling Conflicts ML20216J7591999-09-30030 September 1999 Informs NRC That Remediation Efforts for Software Sys Etude & Rem/Aacs/Cico Have Been Completed According to Schedule & Now Y2K Ready ML20216K1421999-09-29029 September 1999 Provides NRC with Name of Single Point of Contact for Purpose of Accessing Y2K Early Warning Sys,As Requested by NRC Info Notice 99-025 ML20217D1661999-09-27027 September 1999 Forwards Proprietary Completed NRC Forms 396 & 398,in Support of License Renewal Applications for Listed Individuals,Per 10CFR55.57.Encl Withheld ML20212E1971999-09-16016 September 1999 Forwards Rev 11 of Gpu Nuclear Operational QAP, Reflecting Organizational Change in Which Functions & Responsibilities of Nuclear Safety & Technical Support Div Were Assigned to Other Divisions ML20212B5571999-09-10010 September 1999 Forwards Rev 11 to Oyster Creek Emergency Dose Calculation Manual, IAW 10CFR50,App E,Section V ML20211N2941999-09-0303 September 1999 Responds to NRC 990802 Telcon Request for Environ Impact Assessment of TS Change Request 251 Concerning Movement of Loads Up to 45 Tons with RB Crane During Power Operations ML20211J6771999-08-30030 August 1999 Submits Response to NRC 990802 Telcon Request for Gpu to Provide Environ Impact Assessment for Tscr 251 ML20211K2391999-08-23023 August 1999 Forwards fitness-for-duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Nj ML20211B9011999-08-18018 August 1999 Forwards Rev 0 to EPIP 1820-IMP-1720.01, Emergency Public Info Implementing Procedure ML20210D2801999-07-22022 July 1999 Submits Response to Administrative Ltr 99-02 Operating Reactor Licensing Action Estimates. Estimate of Licensing Actions Projected for Fy 2000 Encl.No Projection Provided for Fy 2001 ML20209H5001999-07-14014 July 1999 Forwards Revised TS Pages 3.1-15 & 3.1-17 Which Include Ref to Note (Aa) & Approved Wording of Note H of Table 3.1.1, Respectively ML20210U4411999-07-12012 July 1999 Forwards Article from Asbury Park Press of 990708 Faxed to Legislative Officer by Mutual Constitute Fm Massari Indicating That Oyster Creek Nuclear Generating State Not Fully Y2K Compliant ML20209G1451999-07-0909 July 1999 Forwards Rev 1 to 2000-PLN-1300.01, Oyster Creek Generating Station Emergency Plan. Attachment 1 Contains Brief Summary of Changes,Which Became Effective on 990702 ML20209E0821999-07-0707 July 1999 Forwards TS Change Request 269 for License DPR-16,changing Component Surveillance Frequencies to Indicate Frequency of Once Per Three Months ML20209B7501999-07-0101 July 1999 Responds to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Generic Ltr 98-01 Requested Response on Status of Facility Y2K Readiness by 990701.Licensee Y2K Readiness Disclosure for Ocngs,Encl ML20196G1361999-06-23023 June 1999 Provides Status of Corrective Actions Proposed in in Response to Insp Rept 50-219/98-80 & Revised Schedule for Completion of Actions Which Are Not Yet Complete ML20196E6421999-06-22022 June 1999 Forwards Revised Pages of TS Change Request 261,dtd 990618. Replacement Requested Due to Several Dates Being Omitted on Certain Pages ML20195D0551999-06-0303 June 1999 Forwards TS Change Request 226 to License DPR-16,permitting Operation with Three Recirculation Loops.Certificate of Svc & Tss,Encl ML20195C5511999-05-25025 May 1999 Forwards Book of Controlled Drawings Currently Ref But Not Contained in Plant Ufsar.Drawings Were Current at Time of Submittal ML20206N7711999-05-11011 May 1999 Forwards Rev 0 to Oyster Creek Emergency Plan, IAW 10CFR50.47(b) & 10CFR50.54(q).Changes Became Effective on 990413 ML20206H9441999-04-28028 April 1999 Forwards Application for Amend to License DPR-16,requesting Approval to Handle Loads Up to & Including 45 Tons Using Reactor Bldg Crane During Power Operations,Per NRC Bulletin 96-002 ML20206D3801999-04-26026 April 1999 Forwards Rev 11 to UFSAR, & Rev 10 to Fire Hazards Analysis Rept, for Oyster Creek Nuclear Generating Station, Per 10CFR50.712(e) ML20206B6991999-04-26026 April 1999 Forwards Copy of Rev 11 to UFSAR & Rev 10 to Oyster Creek Fire Hazards Analysis Rept. Without Fire Hazard Analysis ML20206C8261999-04-22022 April 1999 Submits Financial Info IAW Requirements of 10CFR50.71(b) & 10CFR140.21 ML20206A9931999-04-22022 April 1999 Forwards Number of Personnel & Person Rems by Work & Job Function Rept for Period Jan-Dec 1998. Included in Rept Is Listing of Number of Station,Util & Contractor Personnel as Well as Diskette Reporting 1998 Occupational Radiation ML20205P8411999-04-15015 April 1999 Forwards TS Change Request 267 to License DPR-16,modifying Items in Sections 2 & 3 of Ts,Expanding Two Definitions in Section 1 & Modifying Bases Statements in Sections 2,3 & 4. Certificate of Svc Encl ML20205P9401999-04-12012 April 1999 Informs NRC That Gpu Nuclear Is Modifying Oyster Creek FSAR to Reflect Temp Gradient of 60 F & to Correct Historical Record 05000219/LER-1998-015, Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page1999-04-0505 April 1999 Forwards LER 98-015-01,as Original Submittal on 981028 Inadvertently Indicated That Suppl Would Be Submitted.Suppl Should Not Have Been Required as Only Change Is on Cover Page ML20205H1081999-03-31031 March 1999 Forwards Current Funding Status for Decommissioning Funds Established for OCNPP,TMI-1,TMI-2 & SNEC ML20205F0611999-03-25025 March 1999 Submits Info on Sources & Levels of Property Insurance Coverage Maintained & Currently in Effect for Oyster Creek Nuclear Generating Station,Iaw 10CFR50.54(w)(3) ML20205E1171999-03-24024 March 1999 Forwards Rev 39 to Oyster Creek Security Plan & Summary of Changes,Iaw 10CFR50.54(p).Rev Withheld ML20207K2471999-02-25025 February 1999 Forwards Fitness for Duty Performance Data Repts for TMI, Oyster Creek & Corporate Headquarters Located in Parsippany, Ny ML20206S2541999-01-20020 January 1999 Confirms Resolution of Thermo-Lag Fire Barriers in Fire Zones OB-FZ-6A & OB-FZ-6B (480 Switchgear Rooms) IAW Previous Commitments Contained in Gpuns Ltrs to NRC & 971001 ML20199J2631999-01-18018 January 1999 Requests That Listed Changes Be Made to Correspondence Distribution List for Oyster Creek Generating Station ML20199D0271999-01-11011 January 1999 Requests Listed Addl Info in Order to Effectively Review TS Change Request 264 Re Ownership of Property within Exclusion Area ML20199A6521999-01-0707 January 1999 Notifies That Reactor Operators G Scienski,License SOP-11319 & D Mcmillan,License SOP-3919-4 Have Terminated Licenses at Oyster Creek Nuclear Generating Station, Effective 990101 ML20198T1061999-01-0606 January 1999 Forwards Rev 15 to Gpu Nuclear Corporate Emergency Plan for TMI & Oyster Creek Nuclear Station. with Summary of Changes Which Reflect Use of EALs Approved in NRC Ltr to Gpun on 980908 & Other Changes Not Related to Use of New EALs ML20198K0331998-12-23023 December 1998 Forwards Change Request 268 for Amend to License DPR-16. Amend Would Change TS to Specify Surveillance Frequency of Once Per Three Months ML20198H0181998-12-22022 December 1998 Forwards Attachment Addressing New Info & Modifying 980505 Submittal Re Request for Change to Licensing Bases for ECCS Overpressure,In Response to NRC Bulletin 96-03, Potential Plugging of ECCS by Debris in Bwrs ML20198H8521998-12-16016 December 1998 Dockets Completion of Physical Inventory Performed in July 1997,as Addl Info to Nuclear Matl Balance Rept Submitted on 980416 ML20196H4461998-12-0202 December 1998 Provides Final Response to NRC GL 96-01, Testing of Safety-Related Logic Circuits ML20196B4471998-11-23023 November 1998 Provides Required Response 2 to NRC Bulletin 96-003, Potential Plugging of ECC Suction Strainers in Bwrs. During Recently Completed 17R Refueling Outage,New Strainers Were Installed ML20195J8451998-11-12012 November 1998 Forwards Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan, as Change Previously Made Without Appropriate Notification to NRC ML20195C7201998-11-11011 November 1998 Forwards 120-day Required Response to GL 98-04, Potential for Degradation of ECCS & CSS After LOCA Because of Construction & Protective Coating Deficiencies & Foreign Matl in Containment, ML20195E1221998-11-10010 November 1998 Notifies NRC of First Time Usage of Code Case N-504 & Inclusion Into OCNGS ISI Program,As Accepted by RG 1.147, Inservice Insp Code Case Acceptability ML20155J6851998-11-0505 November 1998 Forwards TS Change Request 266,to Modify Safety Limits & Surveillances of LPRM & APRM Sys & Related Bases to Ensure APRM Channels Respond within Necessary Range & Accuracy & Verify Channel Operability ML20155H5641998-11-0202 November 1998 Informs That Bne Has No Comments on Proposed Change 259 to Ts,Correcting Required Water Level in Condensate Storage Tank So That Design Basis Is Correctly Implemented ML20155G3741998-10-29029 October 1998 Forwards Response to NRC 980619 RAI Re GL 96-06, Assurance of Equipment Operability & Containment Integrity During Design-Basis Accident Conditions 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML20059L2551990-09-14014 September 1990 Advises of Preparation for Final Refueling Outage to Complete Second 10-yr Interval for Inservice Insps ML20059F5121990-09-0505 September 1990 Requests Exemption from Filing Requirement of 10CFR55.45(b)(2)(iii) to Allow Submittal of NRC Form 474, Simulator Facility Certification, After 910326 Deadline & to Allow Administering of Simulator Portion of Test ML20059F7441990-08-31031 August 1990 Forwards Util Review of NRC Backfit Analysis for Hardened Wetwell Vent.Nrc Analysis Does Not Support Conclusion That Hardening Existing Vent Is cost-beneficial Mod for Plant ML20059E9061990-08-30030 August 1990 Forwards Response to 900808 Request for Addl Info Re NRC Bulletin 90-002, Loss of Thermal Margin Caused by Fuel Channel Box Bow ML20059G1841990-08-29029 August 1990 Ack NRC Request to Perform Type C Testing During Unscheduled Outage,As Plant Conditions Will Allow.Type C Exemptions Should Remain in Effect Until New Outage Start Date ML20059C8231990-08-27027 August 1990 Advises That SPDS Enhancements Described in Completed,Per 900628 Request.Offline & Online Testing Completed & Enhancements Considered to Be Operational ML20059C8571990-08-24024 August 1990 Provides Results of Evaluation of Ability to Meet Acceptance Criteria for Eccs,In Response to 900804 Notice of Violation. Plant Meets Acceptance Criteria Contained in 10CFR50.46 W/ Valve Logic Design Deficiency in Containment Spray Sys ML20058N0781990-08-0909 August 1990 Submits Info Re pressure-temp Operating Limits for Facility, Per Generic Ltr 88-11.Util Recalculated Adjusted Ref Temp for Each Belt Line Matl as Result of New Displacement Per Atom Values ML20063P9521990-08-0909 August 1990 Advises That Response to NRC 900523 Request for Assessment of Hazardous Matl Shipment Will Be Sent by 910531 ML20058L9521990-08-0303 August 1990 Forwards Rev 2 to Security Contingency Plan.Rev Withheld (Ref 10CFR73.21) ML20058L9551990-08-0303 August 1990 Responds to SALP Rept 50-219/88-99.Although Minor,Several Factual Errors Noted.Dialogue Promotes & Identifies Areas Where Improvements Should Be Made ML20056A2071990-07-30030 July 1990 Forwards Response to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. Record Review Performed & Sys Walkdowns Completed to Assemble Requisite List ML20055H7961990-07-20020 July 1990 Advises of Change to Preventive Maint Program for Electromatic Relief Valves.Rebuild Schedule Will Be Modified to Require Rebuilding Two or Three Valves During Refueling Outage & Remaining Valves During Next Refueling Outage ML20058N9911990-07-20020 July 1990 Partially Withheld Response to NRC Bulletin 90-002 Re Loss of Thermal Margin Caused by Box Bow (Ref 10CFR2.790(b)(1)) ML20055J0481990-07-19019 July 1990 Requests 2-wk Extension for Submittal of Response to Re Installation of Hardened Wetwell Vent W/ Appropriate Extension Period to Be Decided Pending Outcome of 900724 Meeting Discussion W/Bwr Owners Group ML20064A1221990-07-11011 July 1990 Discusses 900710 Telcon W/Nrc Re Util Corrective Actions in Response to NRC Finding That Operator Received Passing Grade on Administered Requalification Exam in 1989 Should Have Received Failing Grade.Corrective Actions Listed ML20055F8491990-07-10010 July 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 188,reducing Low Condenser Vacuum Scram Setpoint ML20043H7471990-06-21021 June 1990 Confirms Telcon W/A Dromerick Re Util Plans to Inspect CRD Hydraulic Control Units During Plant Walkdown to Address USI A-46, Seismic Qualification of Equipment in Operating Nuclear Power Plants. Walkdown Planned in Oct 1992 ML20043H2301990-06-14014 June 1990 Documents Licensee Commitment to Improve Seismic Restraints for Diesel Generator Switchgear Encls,Per 900613 Telcon W/ Nrc.Engineering Will Be Finalized & Mods Completed Prior to 900622 ML20043F7581990-06-0707 June 1990 Responds to Request for Info Re Util Compliance W/Generic Ltr 88-01 & Insp Plans for Upcoming 13R Outage.Frequency of Insp of Welds Classified as IGSCC Categories C,D & E Will Not Be Reduced During 13R Outage ML20043C5801990-05-25025 May 1990 Provides Descriptions & Conclusions of Three Remaining Issues of SEP Topic III-7B.Issues Include,Evaluation of Drywell Concrete Subj to High Temp & Thermal Transients ML20043C2461990-05-25025 May 1990 Forwards Rev 7 to EPIP 9473-IMP-1300.06 & Rev 4 to Radiological Controls Policy & Procedure Manual 9300-ADM-4010.03, Emergency Dose Calculation Manual. ML20043B2981990-05-21021 May 1990 Responds to NRC 900420 Ltr Re Violations Noted in Insp Rept 50-219/90-06.Corrective Actions:Incident Critique Rept Incorporated as Required Reading for Appropriate Operations Personnel & Change Made to Procedure 201.1 ML20043D0701990-05-17017 May 1990 Provides NRC W/Addl Info Re SPDS & Responds to Concerns Raised During 900117 & 18 SPDS Audit Documented in 900130 Ltr ML20043B3901990-05-0909 May 1990 Responds to NRC 900408 Ltr Re Violations Noted in Insp of License DPR-16.Corrective Actions:Two Narrow Range Drywell Pressure Monitoring Instruments to Be Provided During Cycle 14R Refueling Outage,Per Reg Guide 1.97,Category 1 ML20042G7071990-05-0808 May 1990 Forwards Summary of Initiatives & Accomplishments Re SALP, Per 891031 Commitment at mid-SALP Meeting.Plant Div Responsibilities Now Include Conduct of Maint Outages & Emergency Operating Procedure Training Conducted ML20042G2291990-05-0707 May 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 180,revising Tech Specs Re Fuel cycle-specific Parameters ML20042G2601990-05-0404 May 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 187,revising Tech Specs to Accommodate Implementation of 24-month Plant Refueling Cycle ML20042E9431990-04-20020 April 1990 Forwards Revised Epips,Consisting of Rev 7 to 9473-IMP-1300.01,Rev 4 to 9473-1300.11 & Rev 2 to 9473-ADM-1319.04.Deleted EPIPs Listed,Including Rev 3 to 9473-1300.19,Rev 2 to 9473-1300.21 & Rev 5 to 9473.1300.24 ML20042E6371990-04-16016 April 1990 Informs of Plans to Install Safety Grade Check Valve in Supply Line Inside Emergency Diesel Generator Fuel Tank Room Coincident W/Replacement or Repair of Emergency Diesel Generator Fuel Oil Tank ML20042E5001990-04-13013 April 1990 Forwards Rev 1 to Topical Rept 028, Oyster Creek Response to NRC Reg Guide 1.97. ML20012E8711990-03-28028 March 1990 Lists Property Insurance Coverage,Effective 900401,per 10CFR50.54(w)(2) ML20012D4391990-03-19019 March 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 186,allowing Idle Recirculation Loop to Be Isolated During Power Operation by Closing Suction,Discharge & Bypass Valves ML20012B6781990-03-0202 March 1990 Requests Exemption of Specified Local Leak Rate Test Intervals to Include Next Plant Refueling Outage Scheduled for Jan 1991,per 10CFR50,App J ML20012A1501990-02-23023 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 184,removing 3.25 Limit on Extending Surveillance Intervals,Per Generic Ltr 89-14 ML20011F2571990-02-21021 February 1990 Advises That 891003 Request for Appropriate Tech Specs for Chlorine Detection Re Control Room Habitability,Not Warranted ML20006G0101990-02-21021 February 1990 Discusses 900110 Meeting W/Nrr Re 13R Insp Criteria for RWCU Welds Outboard of Second Containment Isolation Valve. All Welds Required 100% Radiography Based on Review of Piping Spec.Response to Generic Ltr 88-01 Will Be Revised ML20006F5931990-02-20020 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 177.Amend Changes Tech Spec 4.7.B to Include Battery Svc Test Every Refueling Outage & Mod of Frequency of Existing Battery Performance Test ML20011F6641990-02-20020 February 1990 Responds to NRC 900122 Notice of Violation & Forwards Payment of Civil Penalty in Amount of $25,000.Corrective Actions:Change Made to Sys Component Lineup Sheets in 125- Volt Dc Operating Procedure to Include Selector Switches ML20006F9181990-02-15015 February 1990 Forwards Application for Amend to License DPR-16,consisting of Tech Spec Change Request 183,permitting No Limitation on Number of Inoperable Position Indicators for 16 ASME Code Safety Valves During Power Operation ML20006D2551990-01-30030 January 1990 Forwards Response to Generic Ltr 89-13 Re Plant Svc Water Sys.Insp Program for Intake Structure at Plant Implemented During Past Two Refueling Outages & Emergency Svc Water Currently Chlorinated to Prevent Biofouling ML19354E8571990-01-24024 January 1990 Forwards Omitted Pages of 900116 Ltr Re State of Nj DEP Comments on Draft full-term OL SER & Clarification of Page 10,fourth Paragraph on New Seismic Floor Response Spectra ML20006B2171990-01-23023 January 1990 Responds to Unresolved Items & Weaknesses Identified in Insp Rept 50-219/89-80.Corrective Actions:Procedure Re Containment Spray sys-diagnostic & Restoration Actions Revised to Stand Alone Re Installation of Jumpers ML19354E3891990-01-19019 January 1990 Responds to Violations Noted in Insp Rept 50-219/89-27. Corrective Actions:Procedure 108 Revised to Allow Temporarily Lifting of Temporary Variation ML19354E8441990-01-19019 January 1990 Forwards Revised Tech Spec Table 4.13-1, Accident Monitoring Instrumentation Surveillance Requirements, in Support of Licensee 890630 Tech Spec Change Request 179,per NRC Project Manager Request ML20006B2881990-01-18018 January 1990 Forwards Results from Feedwater Nozzle Exam,In Accordance w/NUREG-0619 Insp Format ML20005G8161990-01-16016 January 1990 Provides Assessment of State of Nj Concerns Re full-term OL Plant,Per NRC 891222 Request.Comments Did Not Raise Any Concerns That Refute Conclusions Reached by NRC That Facility Will Continue to Operate W/O Endangering Safety ML19354D8281990-01-15015 January 1990 Responds to Violation Noted in Insp Rept 50-219/89-21. Corrective Action:Procedure A000-WMS-1220.08, Mcf Job Order Revised to Provide Detailed Guidance for Performance of Immediate Maint ML20042D4891989-12-28028 December 1989 Forwards Response to Generic Ltr 89-10, Safety-Related Motor-Operated Valve Testing & Surveillance, Fulfilling 6-month Reporting Requirement ML20005E1401989-12-22022 December 1989 Forwards Integrated Schedule Semiannual Update for Dec 1989 1990-09-05
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GPU Nuclear Corporation l
. ,, Nuclear ;;;ggrae8 i Forked River, New Jersey 08731-0388 i 609 971-4000 i Writer's Direct Dial Number: )
September 22, 1987 Mr. James Lieberman, Director Office of Enforcement U.S. Nuclear Regulatory Commission 7940 Norfolk Avenue, Phillips Bldg.
Bethesda, MD 20014
Dear Mr. Lieberman:
Subject:
Oyster Creek Nuclear Generating Station Docket No. 50-219 Reply to Notice of Violation-IE Inspection Report No. 50-219/87-16 and Proposed Imposition of ..
Civil Penalty !
In accordance with 10 CFR 2.201, the enclosure provides the GPU Nuclear Corporation (GPUN) reply to the Notice of Violation (N0Y) and Imposition of Civil Penalties enclosed in your letter of August 24, 1987. The enclosed check in the amount of $205,000.00 represents GPUN's payment of the imposed civil penal ty.
In your letter, a statement is made regarding the unacceptability of manual action as a substitute for automatic capability. GPUN does not question the specific application to the NOV; however, we would like to discuss the circumstances and conditions under which this applies. We will contact the ,
staff in the near future to arrange a meeting for this purpose.
If you should have any questions, pertaining to this response please contact Mr. George W. Busch at (609)971-4909.
Very truly yours, i
P. e Vice President & Director Oyster Creek SWORN TO AND SUBSCRIBED BEFORE ME THIS M SEPTEMBER 1987 DAY OF A
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' NOTARY PUBLIC OF NEW JERSEY
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DIANA M. DeBLASIO p Enclosures NOTARY PUBLIC 0F NE My Commission Expiree Y
SW gW ER g4-See Page 2 for cc's / / # @4 GPU Nuclear Corporation is a subsidiary of the General Pubhc Utilities Corporation h 8 W
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.cc: Mr. W1111am' T. Russell, Administrator; Region U;S. Nuclear Regulatory Commission 631 Park Avenue King of. Prussia, PA 19406 >
Mr. Alexander,W.. Dromerick, Project Manaser U.S. Nuclear Regulatory Commission Division of Reactor Projects I/II-7920 Norfolk Avenue, Phillips Bldg.
Bethesda, MD 20014 Mail Stop No. 316 ~
Document Control Desk U.S. . Nuclear Regulatory Commission Washington, DC 20555 NRC Resident Inspector. .
Oyster Creek Nuclear Generating Station J
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3 ENCLOSURE 1 1
REPLY TO NOTICE OF VIOLATION j l
I. VIOLATIONS ASSOCIATE 0 WITH INOPERABLE SUPPRESSION CHAMBER-DRYWELL V/CUUM i BREAKERS A. 10 CFR 50.59(a)(1) allows a licensee to make changes in the facility or procedures as described in the safety analysis report, without prior Commission approval, unless the proposed change involves a !
change in the technical specifications incorporated in the license or an unreviewed safety question. l The Oyster Creek Updated Final Safety Analysis Report, Section 6.2.1, describes that for a design basis loss of coolant accident, the reactor coolant discharged into the drywell is vented through vent tubes to the suppression chamber (torus) where it is effectively :
condensed for pressure reduction purposes by the suppression pool.
Technical Specification limiting condition for operation (LCO) 3.5. A.3 requires that primary containment integrity be maintained at j all times when the reactor is critical or when the reactor water I
temperature is above 212'F and fuel is in the reactor vessel, except for certain limited conditions. Technica? Specification LC0 3.5. A.5 l requires that, whenever primary containment is required, all ,
suppression chamber - drywell vacuum breakers be operable except in '
certain conditions. Technical Specification LC0 3.5. A.5.2 specifies that one of the conditions required for operability of the vacuum breakers is that the valve disk close by gravity when released after l being open by remote or manual means.
Contrary to the above, between 3:30 AM and 7:15 AM on April 24, 1987, a change was made at the Oyster Creek facility as described in the Updated Safety Analysis Report which resulted in a condition that was contrary to the technical specifications and involved an unreviewed safety question, and the change was made without prior Commission approval. Specifically, during that time, two suppression chamber-drywell vacuum breakers (Nos. V-26-9 and V-26-10) were tied open at the direction of the Group Shift Supervisor while the reactor was at 23% power with all vacuum breakers required to be operable.
This condition was contrary to the description in the Updated Safety Analysis Report and Technical Specification LCO 3.5. A.5 and also involved an unreviewed safety question in that opening of these breakers resulted in bypassing of the suppression pool and the degradation of the pressure suppression capability provided by the suppression chamber required in the event of a loss of coolant accident. This degradation would cause a possible rupture of the containment structure and thus created the possibility for increased consequences of an accident analyzed in the safety analysis report.
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i RESPONSE: GPUN concurs with the cited violation.
The cited violation occurred as a result of a cognitive error by shift operations personnel and the shift technical advisor in failing to properly evaluate the nuclear safety implication of blocking open the torus to drywell vacuum breakers while primary containment was required. As a result of GPUN's investigation of this event, a number of contributing factors were identified as follows:
- 1. The operating shift personnel did not fully understand the 1 function of the vacuum breaker valves with regard to primary i containment integrity.
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- 2. There was a general interest in using this temporary variation to meet schedular requirements. In the past, the torus to drywell vacuum breakers had been opened to allow a more rapid exchange of 1 air between the torus air space and the drywell to assist l deinerting the torus._ However, on those previous occasions, this !
action was not initiated until reactor coolant temperature was i below 212*F at which point primary containment integrity is not i required. The previous history of blocking open the vacuum '
- breaker valves under these conditions contributed to the I
operator's error in not fully evaluating all pertinent aspects of this action.
- 3. Some conflict existed between the temporary variation procedure (0yster Creek Procedure 108) and the safety review procedure (0yster Creek Procedure 130) in that procedure 108 allowed review s and approval of temporary variations by the Group Shift Supervisor )
and did not require a review by independent individuals as does !
procedure 130.
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- 4. A lack of the expected independence between operations supervision I and the shift technical advisor.
Upon discovery of the violation, immediate action was taken to restore the vacuum breaker valves to full operability. The operators who installed the temporary variation realized their error during discussions of plant status with oncoming operations management. The l temporary variatfor, was revoked and the vacuum breaker valves were restored to operable status.
Full compliance was achieved on April 24, 1987 approximately 45 minutes following the identification of the violation.
Subsequently, prior to restart, other corrective actions were taken to address the contributing factors leading to the operators error.
Operations personnel were reinstructed on the importance of the >
vacuum breakers and their function in assuring primary containment integrity. Significant procedural revisions, as discussed below (Section II response), were made to strengthen the safety review process and the control of temporary variations. The importance of independence was discussed with Operations and shift technical advisor personnel.
3 B. 10 CFR 50.72(b)(1)(ii) requires that the licensee notify the NRC Operations Center within one hour of the occurrence of any event or condition during operation that results in the plant being in an unanalyzed condition that significantly compromises plant safety, a condition outside the design basis of the plant, or a condition not covered by the plant's operating and emergency procedures.
Contrary to the above, after . identification on April 24, 1987 of the event in which the suppression chamber-drywell vacuum breakers were tied open while the reactor temperature was above 212*F, notification of the NRC Operations Center was not made until April 27,.1987,. f significantly exceeding the one hour reporting requirement. This event was required to be reported within one hour since it resulted-in the plant being in an unanalyzed condition that significantly ,
compromised primary containment integrity in the event of a loss of
- coolant accident, was outside the design basis of the plant, and.was a condition not covered by the plant's operating and emergency procedures.
RESPONSE
GPUN concurs with the violation in that the event did compromise primary containment integrity in the event of a loss of coolant accident. ,
3 Operations management notified the Oyster Creek NRC Resident Inspector of this event immediately following his arrival (approximately 8:0C AM) at the site. Although operations personnel had evaluated the event with regard to 10 CFR 50.72 reporting criteria, it was not deerred, at that time, to constitute an immediate i (one hour) report.
As a result of GPUN and NRC investigations of this ' event, it was determined that reporting pursuant to 10 CFR 50.72 was necessary and the reqeired report was made. Station management, both verbally and in writing, have re-enforced the need to evaluate conditions and 1
, events with respect to both 10 CFR 50.72 and 10 CFR 50.73 to determine deportability. Personnel have been directed to adopt a philosophy of "when in doubt-report". It has been noted that since l this event and the subsequent management direction, personnel are i more sensitive regarding deportability evaluations.
1 It should be noted that plant emergency operating procedures are
" symptom based" and cover events outside the plant design basis.
Emergency operating procedures direct operator actions in the event of a degradation in the pressure suppression function.
Full compliance was achieved April 27, 1987.
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II. ' VIOLATIONS ASSOCIATED WITH TEMPORARY VARIATION PROCEDURES L Technical. Specification 6.8. requires that written procedures be 1 established implemented and maintained that meet or exceed the -
. requirements of Appendix A of. Regulatory Guide 1.33, which specifies the -
need for procedures for' control lof equipment and modifications of the facility.
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A. Station Procedure 108, Equipment Control, Section 6.3.3, requires that the Group Shift Supervisor. perform a safety. evaluation before ;
authorizing installation. of a temporary Lvariation. Station Procedure . j 130, Conduct of' Independent Safety Reviews and Respor.sible Technical 'l Reviews by Plant Review Group, used to- perform the safety' evaluation,.
specifies in Section 5.1.1 that the signature'of- the Responsible l Technical Reviewer (RTR) . signifies concurrence that (1) an unreviewed safety questions does.not _ exist; (2) a technical specification change-is not required; (3) technical and safety considerations have been - 4 properly addressed; (4) any associated safety determinations or safety evaluations are accurate and completed; and -(5) the RTR was appropriately independent of the originator. Section : 5.1._2 specifies ;
that the signature of the IndependentLSafety Reviewer signifies I concurrence _that safety considerations have been. adequately evaluated:
and are properly _ addressed in any associated safety determination or safety evaluation and that the reviewer is appropriately. independent -
of the originator.and RTR.
(- Contrary to the above, temporary variations were made between September 1986 and April 1987, for which the safety evaluations were not performed as required by Station Procedure 108. .Specifically, (1) for Mechanical Temporary Variations Nos. 87-7,- 87-12 ' and 87-33, the safety evaluations documented on Form 130-3 indicated that written safety evaluations were not required when they were in fact required in that unreviewed safety questions did exist and/or a 1 change to technical specifications were reqcired; (2) for Mechanical .
Temporary Variations No.s86-508, 86-510, 87-7, 87-8, 87-12, and 87-13, the Form 130-3s had the same signature as preparer and _RTR indicating that the RTR was not-independent of the originator; and (3) for Mechanical Temporary Variations Nos.86-455, 86-456,86-472, ,86-480, 86-482, 87-15, and 87-17, the written safety evaluations did not have the appropriate reviews performed as demonstrated by the l presence of only'one or two signatures rather than the three required signatures. -
L' . Station Procedure 108, Equipment Control, Section 6.3.1, requires that, prior to installation of a temporary variation' , the Group.
Shift Supervisor (GSS) review.the function and effects of the temporary variation and the method of installation ~ with the-epropriate maintenance supervisor and Shift. Technical AdvisorJ '
(STA). Steps 17 and 18 of. the Instructions for Preparing' Temporary -
Variation Checkoff Sheets of Station Procedure-108 require that the- . i maintehence supervisor and Shift._ Technical Advisor sign the check-off sheet to 'iMicate that the requirements of Section 6.3.1 have been met to review the functions and effects of the variation.
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q Contrary to the above, on several occasions between August 1986'and April 1987, for Mechanical Temporary Variations' Nos.86-508, 86-510,.
87-7, 87-8, 87-12, 87-13, 87-14, 87-17, and 67-33,- the GSS did not have a review of temporary variations performed by the appropriate maintenance supervisor. Instances were noted where the GSS signed' for the maintenance supervisor. In addition,.the STA signed and.
thereby app' roved the check-off. sheet' for Mechanical. Temporary -
Variation 87-33 even though.it resulted in a. violation of technical specification requirements.
C. Station Procedure 108; Equipment Control, Section' 6.4.2, requires' the originator of.a temporary variation obtain from~'the Plant. Engineering -
Department, either before insta11ation'or as soon as practical after installation, various determinations' relating to checks and testing :
to be performed on temporary variations.
Contrary to the above, between ' August 1986 and April _1987, for Mechanical Temporary Variations Nos.86-404,-86-448,86-473, 86-482,86-484, 86-508, 87-6,87-10, ~ 87-12, 87-23, 87-24 . and 87-33,_ the Plant-Engineering Department had not completed thel requirements specified in Section .6.4.2 in that requirements ,for. post-installation, periodic, and post-restoration checks, and testing- af ter-temporary .
Variations were not provided, or commented upon,by the Plant Engineering Department.
D. Station Procedure 108, Equipment Control, Section 6.19, requires that the Operations Department forward a copy of the applicable temporary variation check-off sheet to the safety review manager who shall initiate any follow-up action he deems necessary.
Contrary to the above, between September 1986 and April 1987,. for Mechanical Temporary Variations referenced in Violations II. A II.B.
l and II.C., the safety review manager did not' adequately review these-check-off sheets, identify procedural deficiencies, and initiate needed follow-up action. The applicable check-off sheets were ,
improperly completed with regard to procedure requirements, including the requirement for responsible technical reviews.
E. Station Procedure 107, Procedure Control, Section 5.1.3 requires -l that, should any procedure prove to be inadequate, it shall be
' revised temporarily if necessary, so that the station is operated in i compliance with approved procedures at all times.
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Contrary to the above, Station Procedure 108, Equipment Control, had. l' not been revised to reflect that, for. temporary variations ~since i September 1986, the safety determinations and reviews were documented
) using Station Procedure.130 and Form 130-3 rather than the previous L
. specific requirement for a safety evaluation.
RE'SPONSE:
GPUN concurs with the violation, although there appears to be some misunderstanding with regard to several of the specific temporary variations cited.Section II.C of the Notice of Violation states that temporary variations86-448, 86-482,86-484, 87-23, and 87-24 were not reviewed by the Plant Engineering Department. This is incorrect since these temporary variations were reviewed and approved by Plant Engineering personnel. The other temporary variations cited in this section were deficient as stated in the Notice of Violation.
The procedural noncompliance described above were a result of inadequate implementation of the safety review process with respect to temporary .
variations and inadequate management review of temporary variations. In l September 1986, the corporate procedure (Procedure No.1000-ADM-1291.01) establishing the safety review requirements was revised to implement a two step process for conducting safety reviews. The first step requires an initial determination of safety significance and the second step requires a written safety evaluation for safety significant issues. Oyster Creek Station Procedure 130 was revised to include the requirements of procedure 1291.01. At that time, it was recognized that station procedure 108 also required revision, however, GPUN management had previously directed that the number of existing temporary variations be reduced and that procedure l 108 be revised to establish more definitive control of such variations.
Since this would require substantial revisions of procedure 108 in addition to changes reflecting the requirements of procedure 1291.01, operations personnel were directed to implement the requirements of procedure 130 when conducting rev.ews of temporary variations and to attach the procedure 130 review form to the temporary variation until such time as all revisions to procedure 108 could be implemented. It should be noted that procedure 108 required a safety evaluation and it was viewed that procedure 130 was a more complete way of documenting the required safety evaluation. It was expected that procedure 108 would be revised and implemented expeditiously and that management direction in the interim would result in proper reviews being conducted. The expected revisions and implementation of procedure 108 were delayed due to the volume and complexity of comments received during the review process. As a result, incersistencies between plant procedure 130 and 108 led to misunderstanding and errors in the evaluation and deposition of temporary variations.
In view of the Technical Specification violation which occurred and the procedural violations which were identified, GPUN management directed the plant remain in a shutdown condition until corrective actions were implemented. These corrective actions consisted of the following:
- 1. A Temporary Variation Task Force consisting of shift technical advisors and management personnel was established to review documentation associated with all existing temporary variations.
These personnel were retrained prior to performing this review.
Where deficiencies were identified, safety evaluations were prepared where appropriate and where safety evaluations were not required, documented justification for this determination was developed.
. '. 2. Oyster Creek Responsible Technical Reviewers (RTR) and Independent Safety Reviewers (ISR) involved in the safety review process for temporary variations were retrained prior to performing any l further reviews. J
- 3. Procedure No. '108 (Equipment Control) was revised as follows: j
- a. Temporary variations prior to installation must be prepared or reviewed by a qualified individual who is not assigned to Control Room shift duties.
- b. The procedure was revised to be compatible with Procedure 130 (Conduct of Independent Safety Reviews and Responsible 1 Technical Reviews by Plant Review Group).
- c. Additional guidance was provided to restrict the use of a temporary variation when a procedure change is more appropriate.
- d. The temporary variation form was revised to explicitly require a technical review of the temporary variation package including j the procedure 130 " Nuclear Safety Environmental Determination l Review" (NSEDR) form, which identifies the safety significance and the written Safety Evaluation (SE) when one is required.
- 4. Procedure No.130 (Conduct of Independent Safety Reviews and Responsible Technical Reviews by Plant Review Group) was changed to require a written justification for "no" answer:: given to questions 3 through 6 on the NSEDR.
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- 5. Management personnel procedurally responsible for reviews have been retrained as to what is expected and what their
- responsibilities include. Examples were provided illustrating a lack of pertinent information and, in some cases, incorrect determinations on documentation associated with temporary variations and their associated safety reviews. These personnel now better recognize their responsibility to provide greater attention to documentation to assure proper content, control of interim measures with regard to testing and recovery, and to assure accurate determinations regarding safety.
Full compliance was achieved on May 14, 1987.
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- o. , l III. VIOLATION ASSOCIATED WITH INOPERABLEEREACTOR BUILDING - SUPPRESSION- I CHAMBER VACUUM BREAKEP.S 10 CFR 50;59 (a)(1): allows a licensee to make changes in tha' facility or procedures as' described in'the safety analysis report, without prior '
Commission approval, unless the proposed change. involves a change in the. ]
' technical specifications incorporated in the ifcense or an unreviewed ;
safety. question. '
l The Oyster Creek Updated Final Safety Analysis Report.Section 6.2.1.1 describes' the. reactor building-suppression chamber.(torus) vacuum relief ;
. system as permitting gas: flow only inward from the atmosphere to the q containment.
Technical Specification limiting condition for operation (LC0) 3.5.A.3 requires .that: primary containment integrity be maintained at all times when the reactor is critical.or when the reactor water temperature-is 3 above 212*F and fuel is in the, reactor vessel, .except for certain conditions. Technical Specification LC0 3.5. A.4 requires the two reactor ;
building . suppression chamber vacuum breakers inleach line be operable- 1 at all times when primary containment integrity is required. ' Further,-if. 4
- a vacuum breaker is inoperable, it shall be locked closed. j l i Contrary to the above, during numerous deinerting' evolutions conducted' l
since April 1977 while the reactor; temperature was greater than 212*F and primary containment integrity was required, a change was made to the facility as described in the Updated Safety Analysis Report.
Specifically, during deinerting of the suppression chamber, a Reactor Building-Suppression chamber vacuum breaker was manually' tied open to permit air flow into the suppression chamber. This created the potential for containment air to flow to the atmosphere, contrary to the description in the Updated Safety Analysis Report, and resulted in a condition that was contrary to the technical specification and . involved
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an unreviewed safety question, and the change was made without prior-Commission approval. This condition was< contrary to Technical.
Specifications and involved an unreviewed safety question since it' !
l resulted in a loss of redundant isolation capability to assure that '
radioactivity would not be released from primary containment'through this pathway in the event of a loss of coolant accident, and thus created the possibility for an accident or malfunction of a different type than evaluated previously in the safety analysis report.
RESPONSE: ,
GPUN concurs with the violation.
Plant procedure 312 (Reactor Containment' Integrity and Atmosphere Control) was changed in 1977 to allow opening of the. reactor building to toras vacuum breakers in order to establish a pathway to provide faster 1 air exchange' during containment deinerting. At the time, the proposed change was reviewed and approved by the Plant Operations Review Committee (PORC) in accordance with technical specifications.
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~ The reviews' conducte'd'during thi.s period did identify the concern that these ' valves were required to be operable while primary containment was required,; therefore, specific provisions were' made to establish administrative controls and a dedicated operator.'to assure' operability. in-response to an accident situation. It'was. felt'that these controls in conjunction with the functioning of a single automatic. isolation valve
-were' sufficient to; assure system operability.
Plant procedure 312 has.been revised to preclude opening .of reactor--
building to torus vacuum breaker valves while primary containment integrity is required. Additionally changes'in the-safety review process.
since 1977 have specifically: identified operating procedures' as ' requiring independent' reviews to determine the safety implications.'of revisions as
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well as documented evaluations pursuant to 10CFR50.59, as requ1 red. -
Full compliance was achieved May. 8,1987.
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