ML20211C885

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Insp Rept 50-302/86-39 on 861117-21 & 1201-05.Violations Noted:Failure to Perform Adequate 10CFR50.59 Review & Failure to Perform post-maint Testing.Deviation Noted: Failure to Meet FSAR Radiation Monitoring Requirements
ML20211C885
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 01/15/1987
From: Belisle G, Jackson L, Runyan M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20211C810 List:
References
50-302-86-39, NUDOCS 8702200250
Download: ML20211C885 (22)


See also: IR 05000302/1986039

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gMaio UNITED STATES

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Report No;: -50-302/86-39 .

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Licensee: ' Florida Power Corporation

- 3201 34th Street, South .

St. Petersburg, FL 33733

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Docket No.: 50-302 License No.: DPR-72

Facility Name: Crystal River 3 .

Inspect. ion Conducted: November 17-21 and December 1-5, 1986

Inspectors: k T.Ld.Emd

M. F. Runyan

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Date signed

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L. H. Jackson g Dite ' Signed

Accompanying Personnel: C. G. Walenga, IE

G. A. Belisle, Region II

M. C. Shannon, Region II

Approved by: h V T (). [

G. 'A. Belisle, SectiortfChief

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D&te Signed

Division of Reactor Safety

SUMMARY

Scope: This special, announced inspection was conducted in the areas of licensee

action on previous enforcement matters, quality assurance effectiveness, and

licensee action on previously identified inspection findings.

Results: One violation and one deviation were identified.

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REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • J. Alberdi, Manager, Nuclear Site Support

J. Andrews, Nuclear Plant Engineer

K. Baker, Manager, Engineering Assurance

W. Bandhauer, Assistant Nuclear Plant Operations Manager

  • P. Breedlove, Nuclear Records Management Supervisor
  • R. Bright, Manager, Nuclear Licensing

T. Catchpole, Senior Quality Auditor (Site)

M. Collins, Nuclear Safety and Reliability Superintendent

D. Conkle, Nuclear Project Engineer

D. Cook, Nuclear Plant Engineer

C. Doyel, Supervisor, Nuclear Engineering

K. Dyer, Engineering Aide

P. Ezzell, Nuclear Compliance Specialist

J. Gibson, Nuclear Technical Specification Coordinator

B. Gutherman, Quality Programs

D. Harper, Licensing

V. Hernandez, Senior Nuclear Quality Assurance (QA) Specialist

M. Jones, Nuclear Modifications Specialist

  • R. Jones, Nuclear Modifications Specialist

M. Kirk, Nuclear Operations Technical Advisor

D. Kurtz, Supervisor, Quality Audits

  • K Lancaster, Manager, Site QA

M. Lord, Nuclear Engineer

  • M. Mann, Nuclear Compliance Specialist

P. McKee, Director, Nuclear Plant Operations

L. Moffatt, Nuclear Safety Supervisor

R. Murgatroyd, Nuclear Maintenance Superintendent

H. Pinney, Quality Programs

F. Quinn, Instrumentation and Control (I&C) Engineer

  • V. Roppel, Manager, Technical Support
  • W. Rossfield, Nuclear Compliance Manager

0. Salute, Nuclear Compliance Specialist

D. Shook, Manager, Nuclear Electrical /I&C Engineer

  • P. Small, Maintenance Department Coordinator

F. Sullivan, Nuclear Electrical /I&C Engineering Supervisor

C. Tillman, Manager, Nuclear Operations Material Control

K. Vogel, Electrical Engineer

  • E. Welch, Manager, Nuclear Electrical /I&C Engineering .
  • G. Westafer, Director, Quality Programs
  • K. Wilson, Manager, Site Nuclear Licensing

H. Wollesen, Nuclear Maintenance Specialist

Other licensee employees contacted included technicians and office

personnel.

  • Attended exit interview

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- 2. Exit Interview

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The-inspection scope and findings were summarized on December 5; 1986, with

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these persons indicated in paragraph 1 above. The inspector described the

F areas inspected and discussed in detail the ~ inspection findings. No

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_ dissenting comments were received from the licensee,

f Violation: Failure to Perform an Adequate "O CFR 50.59 Review and .

Failure to Perform Post-Modificstion Testing,

Paragraph 5.b. (1)

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Deviation: FSAR Requirements Are Not Being det in'That RM-L4 Has

Been Inoperable Since September 1979, Paragraph 5.b. (2)

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The licensee did not identify as proprietary any of the materials prov'ided .

to or reviewed by the inspectors during this inspection.

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- 3. Licensee Action on Previous Enforcement Matters (92702)

a. (Closed) Severity Level IV Proposed Violation 302/86-01-01: Inadequate

Verification of Design Change.

The licensee's response dated April 4,1986,. denied .this violation.

The licensee included information to support their denial. The

violation was for failure to recognize the need for a bypass switch

l proposed for valves MUV-58 and MUV-73 during the design review process.

The inspector reviewed' the response letter and discussed this item in
detail with the engineering department manager and concurs that failure
to add the bypass switch in the original design is not a violation.
- The worst case failure is that MUV-58 and MUV-73 would be in their
emergency safeguards (ES) actuation position and would thus cause 1

l borated- water to be injected into the reactor coolant system (RCS).

l The operator has sufficient controls to reduce the injection rate to a

[ low level and this would cause a slow shutdown o'f the plant if no other

i operator action was taken. Without the bypass switch, these valves

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would be in the ES actuate position so they do not compromise plant

i safety.

i b. (Closed) Severity Level V Violation 302/85-07-02, Inadequate Procedure

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for Retention of Records Required by Technical Specifications.

The licensee's response dated July 16, 1985, was considered acceptable

by Region II. The inspector reviewed AI-1100, Retention of Plant

l Operating Records, Revision 15, dated Jaauary 11, 1985. The inspector

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also reviewed Revision 16 of this procedure. Revision 16 was approved

j by the Nuclear Plant Manager on August 14, 1985. This arocedure

contains FSAR Section 1.7.1.17 record requirements which includes

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controls for training records and those records required to be retained

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by Technical Specifications.

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Enclosure 1 of this procedure specifically requires that restart

package from trip (RPFT) records and Unplanned Operating Event. Reports

(U0ER) be maintained for five years.

The inspector concluded that the licensee had corrected the previous

problem and developed corrective actions to preclude recurrence of

similar problems. Corrective actions stated in the licensee response

have been implemented.

c. (Closed) Unresolved Item 302/85-07-01: Post-Trip Review Procedure

Comments.

The inspector reviewed OP-210, Reactor Startup, Revision 21. This

procedure requires (Step 6.1.4.1) that for a reactor startup following

a reactor trip certain procedural controls have to be completed. This

step requires a sign-off (initials) in the procedure. The inspector

reviewed AI-704, Reactor Trip Review and Analysis, Revision 0. This

procedure establishes administrative requirements following transient

events for implementation of a Post-Trip Review program.

d. (Closed) Unresolved Item 302/85-15-05: Commitment Tracking.

This item contained the following parts:

(1) Part 21 Followup Commitment

(2) Post Accident Sampling System (PASS)

(3) NUREG-0578 Item 2.1.6.a Commitment

(4) Commitment System

During inspection 50-302/85-38, parts (1) and (3) were closed and their

closure is documented in that report. Parts (2) and (4) could not be

closed due to outstanding licensee audit findings from Audits OP 247

and 259 awaiting corrective action completion. During discussions with

licensee quality programs personnel, the inspector was informed that

those audit findings had been resolved and that the audits had been

closed.

4. Unresolved Items

Unresolved items were not identified during the inspection.

5. Quality Assurance Effectiveness

The objective of this inspection was to assess quality assurance effective-

ness. For this report, quality assurance effectiveness is defined as the

ability of the licensee to prevent, identify, and correct their own

problems. The term quality assurance effectiveness is used in this

application, but it is not meant to be limited to the licersee's Quality

Assurance Department. It is the total sum of all efforts to achieve quality

results.

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This was a performance-based rather than compliance-based inspection.

Instead of verifying compliance to programmatic requirements, the principle

effort was to determine whether the results quality assurance was designed

to accomplish were actually achieved. The following sources of information

were used to base an objective measure of quality assurance effectiveness:

Nuclear Operations Performance Mcnitoring Reports

Monthly Synopsis of Operating Experience Reports

Nuclear Operations Monthly Reports

Quality Programs Trend Analysis Reports

In addition, the inspectors reviewed trending indicators tracked by various

groups and any other information deemed pertinent to the overall evaluation

of quality performance.

The inspection effort was divided into'the following areas:

Operations and Maintenance

Design Control

Licensing and Commitments

Quality Assurance Department

Each area is addressed separately in this report. Included in this

assessment is an evaluation of licensee actions to correct situations where

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performance has not met stated goals or where trends have been adverse.

a. Operations and Maintenance

Within the functional areas of operations and maintenance, the

inspector analyzed trending indicators from various sources and

gathered other pertinent information upon which to base an evaluation

of quality assurance effectiveness.

Forced outage rate, the percentage of time planned for electrical

generation that the unit was unavailable due to forced events, is one

of the better indicators of quality assurance effectiveness. Many

quality related activities have a direct impact on the forced outage

rate, such as preventive maintenance, corrective maintenance, planning

management, training, procurement, material availability, surveillance

testing, and design control.

The 1986 forced outage is heavily skewed by a five-month outage to

repair reactor coolant pumps, which renders this indicator misleading

as an overall quality indicator. Forced outage for the first three

quarters of 1986 was 62.2%. The unit operated continuously from the

startup following the reactor coolant pump outage until November 12,

1986, when a dropped control rod precipitated a forced outage which was

still ongoing as of December 5, 1986. Over the past three years,

forced outage has been 20.2%, just over the goal of 20%.

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The number of times the reactor trips inadvertently is another good

indicator of quality. The inspector expanded the study period to

include the last year of power operations which extends back to

mid-1985. During this time period, a total of nine unplanned reactor

trips occurred, as summarized below:

Date Cause

1. 8/20/85 Main turbine trip tu isolate steam leak

Licensee Event Report ((LER) 85-15)

2. 8/20/85 High RCS pressure due to faulty feedwater

control (LER 85-16)

3. 10/9/85 Manual trip after main steam isolation valves

close on failed transmitter (LER 85-20)

4. 10/26/85 Operator action, carrying out trip procedures

when a trip had not occurred, failed inverter

(LER 85-23)

5. 11/8/85 High RCS pressure following feedwater booster

pump trip (LER 85-25)

6. 11/22/85 Operator actions following feedwater trans-

ient, high RCS pressure (LER 85-26)

7. 12/3/85 Loss of two reactor coolant pumps due to

electrical bus failure (LER 85-28)

8. 12/7/85 Operator actions, procedural noncompliance

causes reactor protection trip logic spurious

trip (LER 85-30)

9. 1/1/86 Automatic trip following reactor coolant pump

shaft failure (LER 86-01)

During a period of 4h months, the reactor tripped nine times, which

appears to reflect poor quality assurance effectiveness. However,

following the reactor coolant pump outage, the unit operated for 4

months without a reactor trip.

Therefore, assessing the 4h month periods before and after the reactor

coolant pump outage, plant quality assurance effectiveness as measured

by reactor trips went from very poor to excellent.

There seems to be several reasons to explain the sudden turnaround.

The Reactor Trip Reduction Task Force (RTRTF) was established in F ch

1985, to pursue the goal of reducing reactor trip frequency at Cry.tal

River. Members were chosen from the Site Nuclear Operations and

Nuclear Engineering and Licensing staffs. Later, a representative from

Quality Assurance was added. The group meets approximately once a

month to review root causes of past trips, track ongoing corrective

actions, and review industry-wide information pertaining to trip

reduction. The inspector reviewed minutes from the May 6,1986, and

September 22, 1986, meetings. Within the minutes, action items and

modification lists were tracked.

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One of the items tested by this group was a modification to improve the

reliability of the Emergency Feedwater Initiation and Control (EFIC)

System. This modification was the main factor in reducing trip

frequency and is discussed later in this section.

The inspector reviewed the status of several important items tracked by

the RTRTF and concluded that corrective actions were being aggressively

pursued. The overall effort of this group appears effective.

The inspector chose the following six reactor trip LERs to review the

status of committed corrective actions:

85-20

85-23

85-25

85-26

85-28

85-30

Corrective action was either complete or proceeding satisfactorily for

all items with one exception. In LER 85-26, the licensee committed to

perform an engineering evaluation to determine the adequacy of the

design of a failed relay which had previously resulted in the failure

of a pilot operated relief valve (PORV) to open on demand. The LER

report date was December 23, 1985. The commitment date was extended to

October 30, 1986 and then later extended to December 12, 1986.

Considering the safety-significance of this item, this appears to be an

isolated case of untimely corrective action.

The licensee performs a detailed post-trip analysis in a document

called an Unplanned Operating Event Report (UDER). The U0ER is used

for all reactor ' trips and other significant operating events. The

inspector reviewed the following U0ERs:

U0ER No. Trip Date Title

U0ER 85-08 11-8-85 Feedwater Booster Pump Trip

U0ER 85-10 11-22-85 Main Feedwater Upset During

Shutdown

These two reactor trips involved circumstances where the licensee

admitted that inadequate corrective actions for the first trip led

directly to the second trip. The November 22, 1985, trip involved

operator actions which may have been precluded had the training

following the November 8, 1985, trip stressed the importance of

allowing the EFIC system to automatically control once through steam

generator (OTSG) levels upon actuation.

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Otherwise, the two U0ERs reviewed appeared to be conscientious and

comprehensive efforts to find and correct the root cause of the

problem. Safety considerations and assessment conclusions displayed a

broad-based perspective.

Another indicator of quality assurance effectiveness is the frequency-

of unplanned safety system actuations. The trending indicator for this

subject tracks unplanned actuations of high pressure injection, low

pressure injection, core flood, and ES bus undervoltage. Zero actua-

tions of these systems were reported for the calendar year beginning

with the fourth quarter of 1985. However, a number of unplanned

actuations of the emergency diesel generators (EDG) and the EFIC system

have occurred since 1985 which shed light on the licensee's quality

assurance effectiveness. The inspector reviewed the following

incidents.

LER Description

85-02 Automatic start of Emergency Diesel

Generator (EDG)

85-05 Unplanned actuation of an EDG

85-06 Unplanned actuation of an EDG

85-07 Unplanned actuation of an EDG

85-08 Unplanned actuation of Low Pessure

Injection (LPI)

85-12 Unplanned actuation of Emergency Feedwater

85-14 Unplanned actuation of Emergency Feedwater

85-19 Unplanned actuation of an EDG

85-20 Unplanned actuation of Emergency Feedwater

85-26 EFIC Actuation

85-27 EFIC Actuation

85-31 EFIC Actuation

86-01 EFIC Actuation

86-05 EDG Actuation

86-08 EFIC Actuation

The EDG actuations were caused primarily by personnel errors. There

were no repeat scenarios. Corrective actions appeared suitable to the

incidents. Other causes were material in nature and corrective actions

included the replacement of all four air start solenoid air filters

with filters designed for a higher pressure. The sum of these

corrective actions appears to have been effective.

EFIC actuations occurred until after the installation of a time delay

on the low OTSG level actuation. Many of the unplanned actuations of

this system were caused by a pressure spike (as when the turbine valves

shut) that gave spurious indication of low OTSG 1evel. The 2 second

time delay should eliminate this problem. In addition to these changes

plant procedures were modified where they were found deficient. Other

modifications to address flow rate limitations and power supply

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reliability are planned. The total sum of these efforts have appar-

ently now been proven effective. However, the attainment of relia-

bility of this system appeared to have taken an excessive amount of

time. Corrective action philosophy for some of the problems encoun-

tered early (after system installation approximately two years ago)

appeared to be overly specific and not all encompassing.

The inspector reviewed the circumstances which occurred on November 12,

1986, while the plant was being shut down to repair a dropped rod and a

leaking primary relief valve. A feed pump steam' supply perturbation

resulted in a low OTSG 1evel and an EFIC actuation. During the

emergency feedwater actuation, the emergency feed pump tripped on

overspeed. Crystal River has experienced problems in .the past with

overspeed trips of the Terry turbines used in the emergency feed pumps.

The overspeed condition which occurred in the past resulted from a

leaky steam supply valve which caused the pump shaft to idle and

allowed the initial burst of steam following actuation to raise the

pump speed to the overspeed setpoint. The November 12, 1986, EFW pump

overspeed trip was not related to the previous scenario. For unknown

reasons, a bypass warmup valve was shut which allowed the buildup of

water in the piping. When the actuation signal was received and the

steam supply valve opened, the water provided too much torque to the

pump shaft and an overspeed trip resulted. The licensee could not

explain why the normally throttled bypass valve (ASV-167) was found

shut. For corrective action, SP-300-40, Operations Daily Surveillance

Log was revised to include verification that ASV-167 was not~ closed and

that there was a wisp of steam in the tailpipe. This action should

prevent this event from recurring.

The licensee's dealings with unplanned safety system actuations

indicates a good quality attitude. Though corrective actions have not

always been prompt, they have been thorough and aggressive. The plant

is meeting its goal in this area.

Safety system unavailability, or the percentage of time a safety system

is unavailable, provides another measure of quality assurance effec-

tiveness. The licensee is currently developing this trending indicator

for Crystal River. Therefore, this information was not available for

inspection with the exception of the diesel generators. Seven quarters

of data had been compiled for both diesel generators, as follows:

Hours Out of Service (known and unknown)

Quarter-Year A EDG B EDG

1-85 0 18.1

2-85 73.7 2152

3-35 206 0

~4-85 56 23

1-86 18 98

2-86 16 22

3-86 15 24

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Goals have not yet been established for diesel generator availability.

However, the' above data appears to establish a positive trend,

suggesting that the licensee's recent efforts to improve diesel

generator availability have been effective.

Given the lack of trending indicator data, the inspector attempted

to establish a data base for safety system unavailability by reviewing

information provided by the licensee's Nuclear Plant Reliability Data

System (NPRDS) and Machine History Trending Program. The following

safety systems were chosen for this review:

High Pressure Injection

Emergency Diesel Generators

Decay Heat Removal / Low Pressure Injection

Decay Heat Removal / Core Flood

Emergency Feedwater

NPRDS information for the past 12 months indicated a low number of

failures for these systems. In many cases, however, the cause of the

failure could not be determined or a root cause was not determined.

Definitive information was not provided concerning the amount of time

the system was unavailable for service. The Machine History for these

systems delineated each work request written against the system as

referenced to the tag number of the failed component. This tabulation

provided ambiguous information concerning the reliability of the High

Pressure Injection (HPI) System since HPI constitutes only a subset of

the Makeup System, under which the information is compiled. The

licensee was unable, short of a very time-consuming process, to

indicate which work requests were associated with the HPI system.

Under the licensee's Preventive Maintenance (PM) Trending Program,

PM-150, semi-annually, the 20 tag numbers and the 5 systems for which

the most work requests were written are reviewed to identify adverse

trends. The inspector reviewed PM-150 results dated April 1 and

September 22, 1986. In both cases, no trends were identified. There

is probably some connection between the lack of findings and the

nondescript method whereby the information is compiled. The Machine

History Trending Program appears to be underutilized as a tool for

identifying root cause failure modes, adverse trends, and vulnerable

systems. Used in its current form, it is providing little information

to improve the reliability of safety systems. The inspector was

informed that the Engineering Department periodically reviews informa-

tion provided by this system though this activity was not inspected.

The quality assurance effectiveness to ensure high availability of

safety systems is indeterminable but will be brought to light when this

parameter is tracked as a trending indicator. At that time, licensee

attention in this area should increase and it can be reasonably assumed

that the utilization and ef:'ectiveness of the NPRDS and Machine History

Trending Systems will be enhanced.

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Another measure of quality assurance effectiveness is the licensee's

management of known deficiencies within the plant. Expeditious

corrective action displays a conscientious attitude toward quality.

One way to measure this is by examining the backlog of work requests.

The licensee defines a backlog work request as one that exceeds three

months age. In the past six months, the backlog was decreased from

approximately 350 to approximately 230, though an increasing trend

exists over the past two months. The inspector reviewed a printout

of all open work requests as of December 3,1986. Each work request

is categorized as either being ready for working or on hold for parts,

engineering, or operational considerations. Very few work requests

were on hold for parts which indicates good storeroom availability.

Work requests on hold were mainly due to engineering reasons and these

mostly had field problem reports associated with them. Only eight work

requests greater than 18 months old were designated as ready for working,

each of which were most likely only recently released from hold. Each

work request was prioritized as follows:

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(2) Schedule

(3) Outage

(4) Unknown, auditing review

The oldest category 1 work request was written February 12, 1986, and

was the only outstanding Category 1 work request written before July

1986. The licensee has apparently placed proper emphasis on closing

out work requests of safety significance. Other areas where the

licensee is meeting their goals include the percentage of maintenance

work requests greater than three months old (20 percent versus

<30 percent goal) and the ratio of highest priority to total non-outage

corrective maintenance work requests (17 percent versus <20 percent

goal). In all, the licensee appears to have positive management

control of the corrective maintenance system.

The inspector also reviewed the backlog for category 1 and 2 (Technical

Specification and important to safety) instrument calibrations. This

trending indicator is tracked by the licensee's PM-200 Effectiveness

Data Program. The number of category 1 and 2 instruments backlogged

peaked at about 45 in May 1986, but has been reduced to near zero since

August 1986. The supervisor in charge of this area indicated that the

backlog should be kept near zero in the future. Licensee actions in

this area are commendable and consistent with a high quality attitude.

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The inspector selected several performance indicators in the area of

preventive maintenance for review. Routine maintenance performance,.or

the percentage of all preventive maintenance surveillances scheduled

during the period that were not performed within the assigned grace

period, is tracked in the Performance Monitoring Report. The licensee

established a goal of two percent of PMs exceeding the grace period.

During the past six months through September, this goal was achieved in

four of the months including the last three. The licensee has also

established the goal of expending twice as many manhours on preventive ,

maintenance as corrective maintenance, or a ratio of 2 to 1. In the

September 30, 1986, Performance Monitoring Report, this ratio was

reported as 3.55. However, the inspector received the manhour totals

and determined that the true ratio was 0.28. Corrective maintenance

for the first three quarters of 1986, incurred 124,251 manhours whereas

preventive maintenance (which includes surveillance testing) comprised

35,025 manhours. The large disparity between the actual ratio and the

stated goal most likely results from two factors. The lengthy outage

for the first half of the year involved a large amount of corrective

maintenance. Also, it appears that the licensee's preventive mainten-

ance program has not been fully developed to the extent where

predictive and preventive measures are taken before corrective measures

become necessary. There is some indication that the licensee is

prepared to upgrade their preventive maintenance program. A new ten

year maintenance program is under development which will include some

of the Japanese maintenance philosophy of scheduled predictive

(overhaul) maintenance planning. Additional preventive maintenance

items will be added as well as a periodic effectiveness review of the

preventive maintenance program. These efforts should improve the

preventive to corrective maintenance ratio and will likely reduce the

total number of manhours expended on maintenance as a whole.

The general assessment in the area of operations and maintenance is

that quality assurance effectiveness has been average. The trend over

the past two years has been positive and the current attitude and

philosophy of licensee management personnel is consistent with goed

quality assurance practices,

b. Design Control

In the functional area of design control, the inspector reviewed and

analyzed various management indicators and program details in order to

base an evaluation of quality assurance effectiveness.

Temporary and permanent modifications are tracked using the Nuclear

Modifications File System. The system is capable of providing status

for open or closed items for temporary and permanent modifications.

The system is used to provide the status of modification packages and

the associated field change notices. For future inspection purposes,

the system is also capable of providing the status for all design

changes made to a specific plant system. A present weakness is the

inability to retrieve those design packages that were cancelled. This

is presently being addressed by the engineering staff.

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There is an effort to reduce the total number of design packages and

specifically to reduce the number of older design packages, some of

which date back to 1977. The FPC Nuclear Operations Quarterly Report

for June and September 1986, indicated that the total number of

modification packages outstanding was reduced by 306, from 870 in June

to 564 in September. The inspector reviewed the cancelled packages to

insure that modifications were being properly dispositioned with

adecuate justification and that needed or important to safety modifica-

tions were not being cancelled. An in-depth review of 17 of the

cancalled modifications indicates an acceptable program.

The inspector reviewed modification packages to assure proper docu-

mentation. There has been a recent effort to update older modification

packages with design reviews, design input requirements, and various

evaluation forms. Recently, completed modifications were very detailed

and it appeared that the engineering design effort improved in the

documentation area.

Field Change Notices (FCNs) were reviewed for indication of problems in

the modification package due to improper engineering input. FCNs for

several safety system modifications were reviewed to veri fy that

initial designs were adequate and that FCNs received the same level of

review as the original modification package. There appeared to be

problems in this area due to the number of FCNs associated with work

packages generated prior to 1985. For this reason, the inspector

focused attention on recently completed modification packages. It

appears that the general type of FCN is a minor change to the design

package. Many of the FCNs are generated during the walkdown phase of

the modification, which is done prior to starting work on the design

package. No FCNs were found that would indicate an engineering error

such as out of date schematics, inadequate design input data, or

inattention to detail. FPC management appears to have reached an .

acceptable level of control for processing design packages. It was

also noted that outside engineering assistance is only being supplied

from Gilbert Associates and Babcock and Wilcox (B&W) due to previous

problems with other engineering groups.

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The inspector reviewed the program for updating modified schematics and

system diagrams. Prints and drawings usec by control room personnel

are required to be updated prior to turning a system over to opera-

tions. Selected system modifications were reviewed and it appears that

control room required prints are updated within four weeks of the

original request, which is procedurally submitted two weeks prior to

the design package implementation. Interim drawings and field changes

to drawings are maintained by the engineering group until final

revisions are received. Nothing was found to indicate that unrevised

drawings were used for design input. The system for tracking drawing

revisions appears weak and could be improved by initiating a more

through review of outstanding drawing revisions.

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13

'Nonconformance Operating Reports (NCORs) directed at engineering were

reviewed in detail. Eight items were identified and three of these

were original design problems identified by the Gilbert engineering

department. The other items indicate that engineering could stress

more attention to detail in design package preparation and review. The

NCORs were not of type and quantity to indicate substantial design

program problems.

A new tracking system is now in place to track problems within the

engineering organization. It has input from QA audit findings, NRC

violations, INPO concerns, and internal engineering concerns.

Interviews with licensee personnel by the inspector indicate that the

system will be able to trend specific problems so that adequate

corrective action can be taken.

Temporary modifications, known as T-MARS, temporary modification

approval records, are normally initiated and implemented at the plant

site level. These modification packages have unique problems not

identified in the permanent modification packages.

Until recently, design reviews and design input requirements were not

included in the T-MAR packages, even though this program requires the

same level of engineering input as the permanent modifications program.

The inspector also observed that the authorization forms for extending

a T-MAR had not been completed as required by procedure. The four

oldest T-MARS still in effect were reviewed and found to have had this

deficiency.

There is concern that T-MARS are installed in the plant for extended

lengths of time. Five T-MARS presently installed were older than two

years. T-MARS also have an abnormally long expiration date, before

action is required to be taken.

Within this area, one violation and one deviation were identified and

are discussed in the following paragraphs:

(1) Failure to perform an adequate 10 CFR 50.59 review and failure to

perform post maintenance testing.

10 CFR 50.59 basically states that the licensee can modify systems

if the licensee determines that the modification does not involve

an unreviewed safety question. Records shall be maintained of the

safety evaluation which includes a detail of the basis used for

the determination.

ANSI 18.7-1976, Section 5.2.19.3 requires that tests shall be

performed following plant maintenance or modifications to confirm

that any change does not reduce the safety of operations. Also,

Section 5.2.6 requires that when equipment is ready to be returned

to service that operating personnel shall verify and document the

equipment's functional acceptability.

>

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Crystal River 3 was in the process of heating up on 6/18/86, in

preparation for scheduled startup on 6/20/86. On the evening of

6/18/86, T-MAR T86-06-20-01 and work request 80209 were generated

in response to improper channel "C" T-HOT indication, RC-4A-TE3.

Technicians found that "C" T-HOT loop resistance temperature

detector had become inadvertently grounded and would require

containment entry for resolution of the prcblem.

T-MAR T86-06-20-01 was initiated to remove the installed circuit

ground in order to prevent the inadvertent ground from causing

false readings in the T-HOT channel. The justification section of

the safety evaluation makes the following statements, "The normal

function of the circuit can be performed without any ground" and

"Since the circuit will remain grounded, the same electrical

configuration exists". The engineering instructions, reference

drawing D8042350, Rev. G, and Bailey Instructions E92-346 and

E92-351 from Instruction Manual 206 Volume 1. These references do

not address removal or transfer of the system ground and do not

contain sufficient detail for determination by electrical

engineering that removal or transfer of system ground does not

affect system operation. Engineering personnel have verified that

a schematic for Rosemount linear bridge circuit is not contained

in the B&W instruction manual and would have to be obtained from

the original manufacturer, Rosemount.

The FSAR assumes that the worst case channel error is il F and

surveillance procedure SP-110 requires a bistable trip range of

=.5 F for a reactor trip function, in order to meet technical

specification requirements. The safety evaluation analysis that

was performed cannot guarantee the accuracy required by this

circuit.

The T-MAR T86-06-20-01 engineering instructions require that the

normal ground "must be re-introduced so the calibration out

voltage of the test circuit will be read correctly". The safety

evaluation has already stated that the system ground is not

required for the normal function of the circuit. This also brings

forth the point that the system is being functionally tested in

other than its normal configuration.

After completion of troubleshooting and completion of the T-MAR,

the channel was not functionally tested as required by ANSI

N18.7-1976. Plant surveillance procedure SP-100, Sections 7.7.2.3

and 7.7.2.4 require that a work request be initiated to trouble-

shoot an inoperable channel and that the applicable section of

SP-110 be completed to verify proper operation. A review of

completed SP-110 procedures and work request 80209 indicate that

the post maintenance testing was not performed as required.

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15

The inspector also noted that T-MAR T86-08-11-01, which modifies

the T COLD bridge circuit RC-5B-TT3, may also have a deficient

safety evaluation because a similar schematic is required for

circuit analysis. This circuit is used for feedwater control and

is not considered safety related.

The licensee failed to perform an adequate 10 CFR 50.59 review

that would assure that the modification would not involve an

unreviewed safety question. The licensee also failed to perform

post maintenance testing of the affected channel. These items are

identified as violation 302/86-39-01, failure to perform an

adequate 10 CFR 50.59 review and failure to perform post mainten-

ance testing.

(2) FSAR Requirements Are Not Being Met in That RM-L4 Has Been

Inoperable Since September 1979.

The Crystal River FSAR Section 11.4.1., radiation monitoring

design basis states that the radiation monitoring system measures

radioactivity at selected plant locations in order to verify

compliance with 10 CFR 20. The spent fuel cooling water monitor

RM-L4 is provided to detect any radioactivity released in the

spent fuel storage area.

T-MAR 79-08-78 removed RM-L4 from service on 9/5/79 and it also

states that until RM-L4 is relocated, it is inoperative. The

licensee stated that daily grab samples were taken on the spent

fuel pool in order to compensate for removal of the continuous

monitor.

The T-MAR package also had various problems that are detailed in

the following subsections.

'

(1) The 10 CFR 50.59 review was not included in the T-MAR package

and was assumed to have been lost.

(2) The Design Input Record and the Design Data Sheets were not

added to the T-MAR package until 10/16/86.

(3) The T-MAR action completion date was not properly extended as

i required by procedure.

The plant position as stated by the licensee to the inspector was

that a request would be made to change the FSAR to remove the

RM-L4 requirement. Adequate management attention was not given to

this item.

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The FSAR commitment was that RM-L4 would be operational. The

radiation monitor has been out of service since September 1979

and this is a deviation from FSAR requirements. This item is

identified as Deviation 302/86-39-02.

The overall assessment of the design control area is that the total

program is average. In the areas of documentation, implementation,

trending, corrective action and procedural control, the modification

program appears to be well above average. The temporary modifications

program and the backlog of extremely old modifications are below

average. The problems associated with inadequate safety evaluations

also make.this area suspect and should be addressed by FPC management.

c. Licensing and Commitments

Within the functional area of licensing and commitments, which included

noncomforming operations reports (NCORs), LERs, and Special Reports,

the inspector analyzed trending indicators from various sources and

gathered other partinent information upon which to base an evaluation

of quality assurance effectiveness.

Problems identified via operational events are documented and evaluated

on NCORs. These NCORs precipitate into Licensee Event Reports (LERs)

when required by 10 CFR 50.72. The program controlling NCORs and LERs

is governed by compliance procedure CP-111, Documenting, Reporting, and

Reviewing Nonconforming Operations Reports, Revision 34. NCORs are

initially reviewed by the Nuclear Shift Supervisor for restrictions

imposed by Technical Specifications, identifying immediate notification

requirements, determining NCOR validity, and providing reportability

when required by 10 CFR 50.72 and 10 CFR 20.403, etc. The Nuclear

Safety Supervisor is then responsible for assuring the following:

(1) Investigation to determine the cause of the event or condition

when required.

(2) Designation of adequate corrective actions.

(3) Determination of the NRC and Plant Manager review requirements for

the Event Evaluation Summary.

(4) Evaluation and verification of corrective action assignment.

(5) Preparation of LERs and Special Reports.

The Nuclear Compliance Department is responsible for tracking,

coordinating, and documenting NCORs and corrective action on the

Compliance Tracking System.

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17

The inspector reviewed a summary log of all NCORs written from

January 1 through November 15, 1986. The total NCORs issued as of

November 15, 1986, was 199. From these 199 NCORs, a total of 20 LERs

had been generated. A log of the total number of LERs written during

1985 (33) was reviewed by the inspector. This review focused on

repetitive LERs. Cases in point were LERs 85-02, 06, 07, and 19 which

documented problems with the diesel generators. LER 85-02 is repeti-

tive in that this is the third failure of a drain petcock on air start

solenoid air filter EGFL-4, in the "B" Emergency Diesel Generator air

start system.

LER 85-006 documented an automatic actuation of the "A" Engineered

Safeguards (ES) 4160 VAC Bus Undervoltage Protective Relaying which was

caused when electricians were preparing cables for termination. The

conductors were energized causing the conductors to short, thereby

blowing the fuses, and causing the start. LER 85-007 documents an

actuation of the "A" Emergency Diesel Generator automatic start '

circuit. The cause of this actuation was the result of a fuse failure.

The cause of the failure was investigated and was indeterminable. LER

85-007 also confirms that six previous starts have occurred.

LERs document significant problems with personnel errors. LER 85-008

documents an operator error which caused an Emergency Diesel Generator

start. The operator was counseled in the proper control of switching

devices. LER 85-009 documents failure to recognize the need to perform

a surveillance. LER 85-001 documents an operator error in that "A"

Emergency Diesel Generator was out of service and the operability of

the sump pumps in the tunnel containing the DC control feeds to the 230

KV switchgear and the correct breaker alignment for the remaining power

sources were required to be verified once every eight hours by

Technical Specifications. Again, this documents personnel error. LER

85-018 documents a personnel error in that the Nuclear Shift Supervisor

was not notified of a seismic trigger located on the crane ring girder

being out of service. Personnel error problems and failure to follow

i procedure at FPC is the cause of 24 NRC identified violations issued in

1985 and 17 in 1986. A review of NCORs and LERs for this same time

period also documents personnel errors and failure to follow procedures

as a problem at FPC. Failure to initiate adequate correction action to

preclude repetition of personnel errors and failure to follow proce-

dures is perceived to be a singificant weakness in the implementation

of an adequate QA program.

,

The inspector reviewed a random sample of commitments which FPC has

made to the NRC. These commitments are tracked on a computer program,

N0D-09, Nuclear Operations Commitment System (NOCS). The procedure

provides adequate guidance to perform tracking of commitment and

l necessary guidance to preclude deletion of previously identified

i

commitments. However, this procedure does not document actual dates of

implementation, nor does it document dates when commitments will be

implen.ented. Cases in point are commitments made in response to LER

83-025 which require administrative controls to be upgraded to better

address criteria for cable tray loadings. This commitment has only

been partially completed. Therefore, this system appears weak. t

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d. Quality Assurance Department

The purpose of this portion of the inspection was to assess the

effectiveness of the Quality Programs Department (QPD) to prevent,

identify, and correct problems. To accomplish this, QPD's nonconfor-

mance trending program, audit and surveillance program, and associated

overview activities were reviewed. Interviews were also conducted with

responsible upper management. Both strengths and weaknesses were

identified in all areas.

The Quality Programs Department has implemented a tracking and trending

program. This pragram has been evolving, and a modification to improve

its trend reporting capabilities was recently completed. To evaluate

the effectiveness of QPD's trend program, QPD's trend analysis reports

for the fourth quarter of 1985 through the third quarter of 1986 and

the CR-3 Nuclear Operations Quarterly Report for the third quarter of

1986 were reviewed.

It was evident that significant resources are being used to generate

trend information. This reflects positively on management's commitment

to quality. As experience with the trending program has been gained,

the reports have begun to provide more meaningful information to

management.

Areas for improvement also were identified in QPD's trend program.

These improvements include the need to develop a trending approach that

evaluates the significance of reported deficiencies, provide for more

in depth analyses, and provide for more responsive action as trends are

identified.

These recommendations for improvement are based on the fact that most

of the quarterly trend reports represented superficial analysis of

trends. Specifically, the reports emphasized numbers of deficiencies,

either open or closed, and their relationship to a moving average.

There did not appear to be a method of connecting the significance of

the deficiencies to the data provided or performing any analyses to

determine significant plant trends of a technical or operational

nature. With the exception of the trend report for the third quarter

of 1986, the trend reports appear to have not provided management with

information that would enhance safe plant operations.

The trend report for the third quarter of 1986 provides more signifi-

cant analytical information. The analyses in this report appear to be

the direct result of the modifications made to the trending / tracking

computer program. While the analyses represented a better grasp of

analytical techniques, there appears to be room for improvement in

following up on potential problem areas after they are identified by

the trending program. This could be accomplished through more

aggressive management attention.

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QPD's audit program was reviewed to assess its ability to prevent,

identify and correct problems of a significant technical nature.

Emphasis was placed on audits that were conducted in the areas of

design, modifications, and corrective action. The review included an

assessment of QPD's corrective action follow up capabilities, an

assessment of the qualifications of the audit staff, and an evaluation

of the involvement of overview organizations in the audit and correc-

tive action process.

An initial evaluation was made of the qualification of the audit staff

and other auditors that contributed to the audits being reviewed. The

audit staff was composed of experienced programmatic QA personnel who

had little actual design and operational expertise. This apparent

staffing weakness was mitigated by the use of technical consultants on

the various audits that were reviewed.

The inspector reviewed design and modifications audits conducted during

the last 18 months. Specifically, audit QPD-2/2 (modifications) and

QPD-279 (design control) were reviewed. The review of these audits

showed that the audit program was evolving from a strictly compliance-

to procedures audit function to one that had a mix of compliance and

'

actual work performance. QPD currently plans to revise their audit

practices for 1987 to ensure that audits are more technically oriented.

These audits will emphasize selective detailed review of specific plant

activities. This audit process has neither been approved by upper

management nor implemented; the effectiveness of the audit program

could not be evaluated. These changes of audit focus are considered to

be strengths of the program.

Associated with the audit program is the FPC Nuclear General Review

Committee (NGRC) subcommittee on audits. This subcommittee provides an

NGRC member to be a liaison for each audit. Discussion with the

subcommittee chairman revealed that future NGRC subcommittee plans are

to have the audit team leader report, in person, the audit results to

the subcommittee. Past practice was to have the liaison member

complete a checklist evaluating the audit. The current and proposed

NGRC activity is considered a strength.

QPD's ability to correct and prevent problems from recurring was

evaluated through an analysis of nonconforming items and corrective

action audit reports associated LERs and NCORs, and QPD's followup on

their audit findings.

Discussions were held with the Director, Quality Programs and the

Supervisor, Quality Audits on corrective action follow up. The

inspector also reviewed Corrective Action audits QP-271, QP-283, and

QP-290; associated LERs and NCORs that were reviewed as part of the

audit activities; and the followup to the audit findings of audits

QP-272 and QP-279. The review indicated that QPD is not always

effectively performing corrective action followup. In many instances,

. . .

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20

the effectiveness of the corrective action taken to prevent recurrences

was not normally being assessed and the QPD did not appear to be

aggressive in performing a review to determine the extent and implica-

tions of an identified deficiency on current and past plant activities.

For example, the review of the three corrective action audits indicated

that LERs and NCORs were not reviewed to determine if the corrective-

action taken prevented recurrence of the problem or if the event was

the precursor of a wider problem. Generally, the audits appeared to

only evaluate compliance to the documented program.

Discussions with QPD management revealed an understanding of the

principles of in-depth corrective action follow up. Even so, there

appeared to be some reluctance on the part of QPD to accept a more

active and aggressive role.

The formation of a Management Review Committee to review the status of

NRC, INPO and QPD commitments was considered a strength as it provided

for better communications between the various groups.

The overall evaluation of the quality assurance organization's current

ability to prevent, identify, and correct problems is that the

organization is average. Some potential strengths that were identified

remain to be effectively implemented and with appropriate management

attention, identified weaknesses can be corrected.

Overall Conclusion

The objective of this inspection was to assess quality assurance effective-

ness. After reviewing the four areas inspected and various observations,

the inspection team concluded that the overall quality assurance effective-

ness is average with respect to other licensees inspected. In general,

weaknesses were balanced with strengths though the overall trend is toward

improving performance. This perceived trend is reflected in the trending

indicator data and appears to be the result of increased management

attention in areas of poor performance.

6. Licensee Actions in Previously Identified Inspection Findings (92701)

a. (Closed) Inspector Followup Item 302/85-07-03: Revision to Procedure

Control and Document Retention Program (PCDR).

The inspector reviewed Nuclear Quality Assurance Practice, Instruc-

tions, and Procedures Requirement Code: PCDR. An errata sheet was

added to this document dated August 30, 1985, adding 10 CFR 50,

Appendix B, Criterion VI and the Final Safety Evaluation Report Section

,

1.7.1.6 to Section 3, Basis. This section includes the documents which

'

form the basis for this practice. The inspector also reviewed AI-404,

Review of Technical Information, Revision 4 and N00-6, Technical

l Information Program, Revision 1.

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AI-404 establishes methods which ensure consistent thorough documented

reviews of information pertaining to safety-related components

installed at Crystal River. Information reviewed will include but is

not limi',ed to vendor manuals, vendor manual changes, and vendor

letters. N00-6 establishes methods of handling and processing

technical information to assure current and accurate information is

provided at Crystal River 3. This technical information includes

vendor supplied engineeririg and equipment information such as drawings,

correspondence, manuals, and similar technical documents and changes

thereto.

b. (Closed) Inspector Followsp Item 302/86-01-02: Revision of Program

Controls for Rework Process.

The inspector reviewed M0P-405, Job Completion, Walkdown, Turnover, and

Nonconforming Item Reporting, . Revision 8. Section 4.2.6.7.a, now

includes requirements that exceptions to dispositioned rework require

Nuclear Engineering approval. This appreval is documented by Field

Change Notices (FCNs), modification approval records (MARS), Work

Package, Work Request, etc.

c. (Closed) Inspector Followup Item 302/86-01-03: Completion and Closecut

of Appendix R Fire Detection Installation.

The inspector reviewed an FPC QA Record Transmittal Sheet signed by the

Nuclear Modifications Supervisor on April 1, 1986. This sheet

documented transmittal of MAR 82-10-19-10, FCN 1 and 2, and Work

Requests Nos. 51295, 60569, 62122, 65041, 66963, 68699, 69107, and

76961 to the Records Management Section for their inclusion into the

Plant Quality file. The inspector verified that applicable cable pull

and cable termination cards were included in the completed MAR

documentation. The inspector was unable to verify that anchor bolt

installation sheets were included in the MAR documentation since these

records were apparently lost. A letter has been included in the MAR

documentation stating that these documents were lost. The loss of

anchor bolt installation sheets was documented on engineering change

notice (ECN) 2679 dated March 4, 1986.

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21

AI-404 establisnes methods which ensure consistent thorough documented

reviews of information pertaining to safety-related components

installed at Crystal River. Infcrmation reviewed will include but is

not limited to vendor manuals, vendor manual changes, and vendor

letters. N00-6 establishes methods of handling and processing

technical information to assure current and accurate information is

provided at Crystal River 3. This technical information includes

vendor supplied engineering and equipment information such as drawings,

correspondence, manuals, and similar technical documents and changes

thereto.

b. (Closed) Inspector Followup Item 302/86-01-02: Revision of Program

Controls for Rework Process.

The inspector reviewed MOP-405, Job Completion, Walkdown, Turnover, and

Nonconforming Item Reporting, Revision 8. Section 4.2.6.7.a, now

includes requirements that exceptions to dispositioned rework require

Nuclear Engineering approval. This approval is documented by Field

Change Notices (FCNs), modification approval records (MARS), Work

Package, Work Request, etc.

c. (Closed) Inspector Followup Item 302/86-01-03: Completion and Closeout

of Appendix R Fire Detection Installation.

The inspector reviewed an FPC QA Record Transmittal Sheet signed by the

Nuclear Modifications Supervisor on April 1, 1986. This sheet

documented transmittal of RAR 82-10-19-10, FCN 1 and 2, and Work

Requests Nos. 51295, 60569, 62122, 65041, 66963, 68699, 69107, and

76961 to the Records Management Section for their inclusion into the

Plant Quality file. The inspector verified that applicable cable pull

and cable termination cards were included in the completed MAR

documentation. The in:pector was unable to verify that anchor bolt

installation sheets were included in the MAR documentation since these

records were apparently lost. A letter has been included in the MAR

documentation stating thao these documents were lost. The loss of

dnchor bolt installation sheets was documented on engineering change

notice (ECN) 2679 dated March 4, 1986

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