ML20138J409

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Insp Rept 50-302/97-02 on 970223-0329.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML20138J409
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 04/21/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20138J402 List:
References
50-302-97-02, 50-302-97-2, NUDOCS 9705080201
Download: ML20138J409 (44)


See also: IR 05000302/1997002

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION 2

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Docket No: 50-302 '

License No: OPR-72

Report No: 50-302/97-02

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Licensee: Florida Power Corporation

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Facility: CrystalRiver3NuclearSt5 tion

Location: 15760 West Power Line Street

Crystal River. FL 34428-6708

Dates: February 23 through March 29. 1997  !

Inspectors: S. Cahill Senior Resident Inspector

T. Cooper Resident Inspector

B. Crowley Reactor Inspector, paragra]hs E8.1 - E8.8

M. Thomas. Reactor Inspector, paragra als E8.9 - E8.10

L. Mellen Project Engineer, paragrapls E1.1. E8.11 i

M. Miller. Reactor Inspector, paragraphs E8.12 - E8.13

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Approved by: K. Landis, Chief. Projects Branch 3 l

Division of Reactor Projects  :

9705000201 970421  :

PDR ADOCK 05000302 i

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EXECUTIVE SUMMARY

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Crystal River 3 Nuclear Station

NRC Inspection Report 50-302/97-02

This integrated inspection included aspects of licensee operations. ,

engineering, maintenance, and plant support. The report covers a 5-week

period of resident ins)ection; in addition, it includes the results of

announced inspections )y five reactor inspectors and one project engineer from

Region II.

Ooerations

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A Violation (VIO 50-302/97-02-01) was identified. This violation is of

concern in that it involved seven examples of equipment in the incorrect

position and revealed your inadequate controls to maintain the appropriate

status of plant equipment (Section 01.2).

The Operations department was not using the corrective action system

appropriately as a tool to facilitate their problem investigations.

Consequently, senior management involvement and awareness of the corrective

action plans was limited, and the timeliness of the root cause evaluations and

subsequent development of corrective actions was poor (Section 01.2).

The licensee's restraints and required Plant Review Committee reviews for

normal Mode 5 conditions constituted a good means of oversight for shutdown

safety and defense in depth and was considered a licensee strength (Section

01.3).

The inspectors concluded the licensee continued to restructure their self-

assessment activities in an attempt to improve their programs. Problems

continued to be observed, but they were being recognized and addressed by

licensee management. The PC problems indicated an underuse of the PC system

as a mechanism to correct large program problems and a lack of visibility of

significant problems for management review. Changes to the PC tracking

software and processes were being investigated by the licensee to address

these concerns (Section 07.1).

The inspector concluded the Plant Review Committee was providing appropriate

oversig1t and safety perspective. Changes to restrict membership, assign a

full time chairman and refine expectations were beneficial initiatives by the

licensee and were indicative of an emphasis on improving nuclear safety

performance (Section 07.2).

Maintenance

The inspectors concluded that all observed maintenance and surveillance

activities were performed in accordance with procedures and desired results

were obtained (Section M1.1).

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l A weakness was identified in that Problem Report 96-0423 was not revised to

address the discrepancies identified with missed identification in

4 Modification Approval Record packages of needed procedure revisions

(Section E8.1).

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! An Unresolved Item.(URI 50-302/97-02-02) was identified for further NRC review

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of the licensee's deletion of primary and secondary plant water quality

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requirements from the Final Safety Analysis Report (Section E8.2).

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A weakness was identified in that the extent of condition was not adequately

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addressed in the corrective actions for a Control Room Emergency Ventilation

System surveillance test failure (Section E8.3).

, A Violation (VIO 50-302/97-02-03) was identified for inadequate procedures for

i taking the plant from hot standby to cold shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> following

main control room evacuation due to a fire (Section E8.9).

l The inspectors concluded that the licensee continued to make progress in

resolving the Improved Technical Specifications (ITS) setpoint program

! deficiencies. In. general, the calculations reviewed were well documented.

l with well-founded assumptions, and followed the methodology specified in ISA

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67.04, part II as referenced by instrumentation and controls Design Criteria

i Instrument String Error /Setpoint Determination Methodology. These

! calculations continue to be a significant improvement over calculations

4 reviewed in IR 95-06 (Section E8.11).

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i Additional examples of Violation 97-01-07. Instrument Setpoint Calculation

] Assumptions Not Translated into Procedures, were identified. The temperature

ranges assumed in the Environmental and Seismic Qualification Program Manual.

which were used for the instrument loop uncertainty setpoint calculations,

j were not maintained in the Reactor Building and Intermediate Building (in

addition to the Auxiliary Building, which was previously identified). Also.

! the temperature assumptions had not been appropriately translated into

i instrument calibration or area monitoring procedures. In addition,

j 3roceduralized controls were lacking for use of certain temperature sensitive

j ieasuring & Test Equipment in the Reactor Building (Section E8.11).

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A Violation (VIO 50-302/97-02-04) was identified for failure to conduct

. Technical Specification-required testing on Engineered Safeguards Actuation

System instrumentation (Section E8.12).

An Inspector Follow-up Item (IFI 50-302/97-02-05) was identified for

outstanding issues associated with the emergency diesel generator power uprate

modification (Section E8.14).

Plant Suonort

The inspector concluded the Security Program Peer Assessment was balanced and

beneficial for the licensee security staff in their efforts to improve

performance and regulatory compliance (Section S1.1).

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The inspectors assessed the licensee *s performance concerning the five areas of continuing NRC concern in

the following paragraphs: the assessments are limited to the specific issues addressed in the respective

paragraphs involving those issues primarily on the MC 0350 Restart Checklist.

NRC AREA 0F CONCERN ASSESSMENT PARAGRAPH

E8.1 E8.2 E8.3 E8.5 E8.6 E8.7 E8.8 E8.9 E8.10 E8.11

Management Oversight A A A A G A G A A I

Engineering Effectiveness A A A A A G A I

Knowledge of design basis G G I

compliance With Regulations A A A A A A G I A I

Operator Performance A

NRC AREA 0F CONCERN ASSESSMENT PARAGRAPH

E8.12 E8.13 01.2 01.3

Management Oversight I A I G

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Engineering Effectiveness I A

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Knowledge of design basis I A

Compliance With Regulations I A I G

Operator Performance I G

S = Superior: G = Good: A = Adequate / Acceptable: I = Inadequate: Blank = Not Evaluated / Insufficient

Information

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E8.1: Corrective actions for VIO 50-302/96-09-04 Failure to Update Operating Curves to Reflect 1981

Power Uprate

E8.2: Corrective actions for VIO 50-302/96-09-03. Failure to Perform 10 CFR 50.59 Safety Evaluation

for Changes to Procedures Described in the FSAR For Controlling Dissolved Hydrogen Concentration

E8.3: Corrective actions for VIO 50-302/96-06-07. Failure to Initiate a Problem Report to Resolve

CREVS Test Failure

E8.5: Corrective actions for VIO 50-302/96-15-02. Failure of Reactor Coolant Pump Oil Collection

System to Retain Oil Leaking From Reactor Coolant Pump Motor

E8.6: Corrective actions for VIO 50-302/96-11-04. Failure to Construct the Reactor Building Sump

Screens and Components in Accordance with the Approved Drawing

E8.7: Corrective actions for VIO 50-302/96-06-02. Inadequate Procedure for Performing a Demineralized

Water Flush Following a Boric Acid Addition

E8.8: IFI 50-302/96-201-11. Design Basis for Decay Heat / Core Flood / Reactor Coolant Piping Temperature

E8.9: URI 50-302/97-01-08. Adequacy of Procedures to Take the Plant from Hot Standby to Cold Shutdown

from Outside the Control Room

E8.10: Corrective actions for LER 50-302/95-025. Personnel Errors by Arc'hitect Engineer Result in

Operation Outside Design Basis Due to Inadequate Safety /Non-Safety Circuit Isolation

E8.11: Corrective actions for EA 95-16. Use of Nonconservative Trip Setpoints for Safety-Related

Equipment

E8.12: URI 50-302/96-17-03. Failure to Conduct Required Technical Specifications Surveillance Testing

on Safety Related Circuitry (GL 96-01)

E8.13: NRC Generic Letter 96-01. Testing of Safety-Related Logic Circuits

01.2: Hispositioned Components

01.3: Shutdown Equipment Availability Controls

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Report Details

Summary of Plant Status ,

The unit remained in Mode 5 throughout the inspection period, continuing in

the outage that began on September 2. 1996. An outage on the "B" train of

emergency core cooling system (ECCS) equipment was conducted to perform  !

corrective maintenance and implement a design change on the IB Emergency

Diesel Generator (EDG). The purpose of the design change was to upgrade the

EDG turbocharger nozzle rings and replace the intercooler with a more

efficient version. These changes were expected to result in 150 kilowatts

(kW) of extra diesel ca)acity. The 1A EDG was upgraded during an outage in

January 1997. During t11s inspection period, the licensee had not begun any

other major physical modification work.

L. Operations

01 Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707 the inspectors conducted frequent

reviews of ongoing plant operations. The inspectors followed up on

deficiencies with operator logs documented in NRC Inspection Report (IR)

50-302/97-01 and observed that log content and consistency has improved.

Significant items were logged in both the Operations Shift Supervisor

and Shift Manager logs inconsistencies between Shift Supervisor and

Shift Manager logs were reduced, and the time of turnover was being

logged by Shift Supervisors on Duty (S500). The licensee was nearing

completion at the end of the report period on a new revision of

Operations Instruction (01)-5. Log Keeping. Revision 2. to clarify

requirements and management expectations. The ins)ectors crncluded that

licensee management was appropriately addressing t1e previously

identified logging deficiencies.

The inspectors observed good examples of conservative decision making as

discussed in Section 01.3 regarding shutdown equipment availability

controls. However. Several attention to detail and poor process

problems discussed in Section 01.2 resulted in the identification of a

violation of requirements for maintaining configuration and status

control of plant equipment.

! 01.2 Misoositioned Comoonents

a. Insoection Scooe (71707. 92901)

The inspectors reviewed the licensee's response to four examples of

valves found in the incorrect position in January 1997 which was

previously documented in NRC Inspection Report (IR) 50-302/97-01. The

licensee has subsequently discovered several other examples of equipment

status control problems which the inspectors incorporated in their

followup.

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b. Observations and Findinas

The licensee had taken prompt interim corrective actions for the

incorrectly positioned valves discussed in IR 97-01. The licensee's

investigation and root cause analysis was still not finalized at the

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close of this Inspection Report period due to the scope and content of

the investigation being expanded as more examples of incorrect equipment

status and equipment tagging were identified. The licensee's

preliminary assessment indicated problems in the control of clearance

tagging which was incorporated into preexisting efforts to revise the

clearance and tagging process. Other problems were attributable to a

single individual with whom the licensee was taking personnel action.

the minor maintenance team control of ventilation equioment and <

instrumentation, and control of plant modification wort. The licensee

l identified several corrective actions for each of these items. However.

! the inspector observed that the Operations department had not aggregated

l the individual problems into one corrective action document even though

their effort was focused on a single equipment status control problem.

The inspector also observed that the licensee had not yet formally

documented their corrective action alan to ensure it identified root

l causes. approariately addressed eac1 cause, and would be a comprehensive

solution to t1e entire problem. Other examples 'of equipment status

control problems were identified during this report period and had not

yet been fully investigated and incorporated into the licensee's

efforts. Consequently, the inspectors considered these problems as

further examples of significant deficiencies in the licensee's overall i

! process for configuration and status control of plant equipment The

inspector also concluded the licensee has not yet fully investigated and

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corrected these problems so they are being identified as several ,

l examples of a violation of licensee procedural requirements. VIO 50-  !

l 302/97-02-01. Failure to Follow Equipment Status Control Procedural l

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Requirements. Specific examples are discussed below.

Nuclear Services Cooling System Vent Valve (RWV-73) was inadvertently

left open on January 24. 1997. by an operator verifying an idle Decay

i Heat system heat exchanger was filled per Surveillance Procedure (SP)

( 306. Weekly Surveillance Log. Revision 13. It was discovered by another

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operator after a pum) start a

water flowing from t1e valve.pproximately

The inspectorfive

notedhours

thatlater resultednot

SP-306'did in

specify which valve numbers to operate when directing the verification

, and it did not have any valve position restoration signature or

l verification. The inspector considered this as another deficiency in

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the licensee's ecuipment status control process. Operating Procedure l

(OP) 404. Decay Feat Removal System. Revision 104, requires RWV-73 to be 1

closed for normal operations. This is considered the first example of  !

VIO 50-302/97-02-01. Failure to Follow Equipment Status Control

Procedural Requirements.

! Nitrogen system 3ressure instrument isolation Valve NGV-313 was found  !

incorrectly in tie closed position on January 26. 1997, when a clearance I

i was being im)lemented. It apparently was closed following maintenance -l

activities. ]ut Equipment Alteration Logs were not retained for minor  ;

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maintenance activities so record.s of the valve manipulation were not

retrievable. The inspector considered this to be inadequate control of

, plant equipment positioning. Procedure OP-414, Nitrogen and Hydrogen

Systems. Revision 34. requires NGV-313 to be open for normal operations.

This is considered the second example of VIO 50-302/97-02-01. Failure to

Follow Equipment Status Control Procedural Requirements.

The makeup system air isolation to Valve MUV-243. Prefilter 2A Outlet,

was found incorrectly in the closed position on January 24. 1997, when

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hanging a clearance. The valve was apparently closed without any

procedural controls or documentation to isolate an air leak. Procedure

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OP-402. Makeup and Purification System. Revision 90, requires MUV-243 to

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! be in the open position. Procedure OP-411. Instrument and Station Air

System. Revision 53, requires the valves in the instrument air flow path

to MUV-243 to be in the open position for normal operations. This is

considered the third example of VIO 50-302/97-02-01. Failure to Follow

Equipment Status Control Procedural Requirements. The inspector had

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previously questioned the method of control and verification for root

isolation valves such as this that are commonly operated by instrument

technicians. The licensee recognized that they did not have a procedure

to verify the position of these valves to pneumatic valve controllers

and initiated Precursor Card 97-0733 to implement further corrective

action. Precursor Card 97-0733 was closed by the licensee on March 7

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with no further action based on the large number of root valves that are

not labeled and do not have designated valve numbers. The closure I

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documentation noted that Equipment Alteration Log forms are required to '

document mani]ulation of these valves but as noted above in the NGV-313 l

discussion. t1ese logs were frequently not maintained. The closure I

documentation also noted that the position of many root valves was

verified by post-maintenance testing that ensured the component supplied

with air could perform its function. The inspector considered the lack

of control and identification for instrument and component root valves

to be another deficiency in the licensee's process for equipment status

control. j

. Normally open station air header drain Valve SAV-49 was found in the f

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closed position on January 28, 1997. It was apparently also closed l

, without procedural controls or documentation to isolate a leaking

downstream solenoid valve. OP-411. Instrument and Station Air System.

Revision 53, requires SAV-49 to be in the open position for normal

operatiem . This is considered the fourth example of VIO 50-302/97- 1

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02-01. Failure to Follow Equipment Status Control Procedural

Requirements. l

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Oily water separator tank Vent Valves SDV-107. 108 and 109 were found

open instead of closed as required on March 7. 1997, while reviewing a

draft clearance in the field. These valves were operated to vent the

tank but were difficult to access. The licensee's preliminary

investigation revealed that more accessible downstream valves were used

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to vent the tank, recuiring SDV-107.108, and 109 to be open. Procedure -

OP-422. Turbine Builcing Sump Oil-Water Separator Revision 8. does not

allow this alignment when venting and requires SDV-107, 108 and 109 to

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be closed for normal operations. This is considered the fifth example

of VIO 50-302/97-02-01. Failure to Follow Equipment Status Control

Procedural Requirements. The licensee was evaluating a procedure change ,

to use the more accessible vent alignment. l

Fire damper (FD) power links for FD-47 and FD-83 were found open on i

March 21. 1997. during surveillance testing, when the dampers failed to ,

actuate. The licensee's investigation revealed that the links had been )

opened and documented as closed by a single verification in October of i

1996 while performing SP-607. Fire Damper Inspection. Revision 18. The

licensee could not determine any other maintenance or operational

evolutions that could have removed the links. Step 4.4 requires

restoration of the links to the closed position. Contrary to that step,

the links were found open. This is considered the sixth example of VIO

50-302/97-02-01. Failure to Follow Equipment Status Control Procedural

Requirements.

On March 28. a plant operator removed a seal and throttled nuclear

services closed cycle cooling valve SWV-24 open to increase flow to ,

600 gpm to the in service spent fuel pool (SFP) cooler B to address a  ;

several degree rise in SFP temperature. The plant operator then ,

replaced the seal. The plant operator and control room operator '

directing his actions had exhibited questioning attitudes and discovered

the SFP heat exchanger secondary cooling flow to be only 200 gpm but had '

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elected to throttle it to 600 gpm without referring to proceoeral

guidance. Oncoming shift operators questioned their actions and

verified that OP-408. Nuclear Services Cooling System. Revision 84,

required SWV-24 to be throttled 2 and 1/8 turns o]en. After positioning

SWV-24 to this setting. flow rose to 2000 gpm. T1e operators checked

the corresponding valve on SFP cooler A. SWV-23. and found it positioned

incorrectly. They repositioned it to the required setting of two turns

open. The failure to follow procedural guidance when repositioning

SWV-24 and the discovery of SWV-23 and 24 in the incorrect throttled

position is considered the seventh example of VIO 50-302/97-02-01.

Failure to Follow Equipment Status Control Procedural Requirements.

The inspector did observe a positive practice in that each later problem

was promptly investigated and documented per Operations Instruction 12.

Investigation of Abnormal Events. Revision 1. This was indicative of

good responsiveness to problems on the later examples. Although the

quality of the 01-12 reports varied widely due to the lack of specific

content and format guidance, the inspector noted that management

expectations for shift supervision to take ownership of problems and

initiate corrective actions had been effective. The 01-12

investigations were generally good initial afforts to gather data,

identify short term corrective actions, and recreate the event.

c. Conclusions

The inspector concluded, that the Operations department was not using

the corrective action system appropriately as a tool to facilitate their

plan. Efforts were disjointed and similar problems were not combined

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into one effort to ensure a consistent and comprehensive solution was

developed, documented, and implemented. Consequently, senior management

involvement and awareness of the Operations department's plans was

limited. The inspector concluded the timeliness of the root cause

evaluations and subsequent development of corrective actions was poor

because it had taken over two months and still was not complete.

The inspector concluded that the equipment in the incorrect position was

a violation of procedural requirements. This violation is of concern in

that it involved seven examples of equipment in the incorrect position

and revealed your inadequate controls to maintain the appropriate status

of plant equipment.

The inspectors assessed the licensee's performance relative to their

controls to maintain the appropriate status of plant equipment. in the

five areas of continuing NRC concern:

  • Management Oversight - Inadequate
  • Engineering Effectiveness - N/A
  • Knowledge of the Design Basis - N/A
  • Compliance with Regulations - Inadequate
  • Operator Performance - Inadequate

01.3 Shutdown Eauioment Availability Controls

a. Insoection Scooe (71707)

The inspector observed stringent licensee controls of shutdown equipment

during normal Mode 5 plant condition changes and maintenance outages 6nd

reviewed the licensee's process for this control.

b. Observations and Findinas

The licensee's Administrative Instruction (AI) 504. Guidelines for Mode

5 Outages and Reduced Reactor Coolant System (RCS) Inventory Operations.

Revision 7. contains administrative controls for sensitive shutdown

conditions such as reduced 3rimary inventory evolutions to ensure the

continued availability of slutdown cooling. Section 4.1 Mode 5

Requirements When RCS is Filled and Vented, also contains requirements

for normal Mode 5 cold shutdown conditions. These recuirements exceed

Technical Specification requirements to provide an adcitional level of

safety. For example. AI-504 prefers two EDGs to be 03erable as defense

in depth even though only one is required per the Tec1nical ,

Speci fications. If an activity requires a departure from the l

requirements of AI-504, a justification has to be submitted evaluating  :

the safety effect and presented to the Plant Review Committee (PRC). An j

exam 31e of the Al-504 controls was a request to perform instrument work .

in tie 230kV switchyard that would affect EDG B operability that was l

presented to the PRC. The PRC originally did not approve the request

due to lack of overall coordination and logistical pbnning. The PRC

recuested a single accountable person be assigned to oversee the work

anc ensure adequate coordination to limit the length of the work and j

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minimize the associated risk before they would approve an exce3 tion.

The inspector has observed that the licensee consistently exhiaits a

high degree of conservative questioning and decision making when

reviewing exceptions to AI-504.

c. Conclusions

The inspector concluded that the licensee's AI-504 restraints and

required PRC reviews for normal Mode 5 conditions constituted a good

means of oversight for shutdown safety and defense in depth. The

inspector considered this a licensee strength.

The inspectors assessed the licensee's performance relative to shutdown

equipment availability controls, in the five areas of continuing NRC

concern:

. Management Oversight - Good

. Engineering Effectiveness - N/A

. Knowledge of the Design Basis - N/A

. Compliance with Regulations - Good

. Operator Performance - Good

06 Operations Organization and Administration

06.1 Effective March 3. 1997. Greg Halnon assumed the acting role of

Assistant Plant Director. Nuclear Safety. He will be engaged with

issues involving nuclear safety oversight of the plant and conduct of

the Plant Review Committee. He will also be tasked with assuming the

role of Director. Nuclear Plant Operations in Bruce Hickle's absence.

Additionally, he will be the overall project manager for ensuring the

Final Safety Analysis Report (FSAR) is properly revised and technically

correct for restart of t1e plant.

Mr. Halnon's previous duties of coordinating NRC inspections,

interfacing with NRC Resident Inspectors and coordinating violation

responses will be performed by the Nuclear Regulatory Assurance Group.

07 Quality Assurance in Operations

07.1 Licensee Self- Assessment Activities

a. Insoection Scooe (71707. 40500)

The inspectors reviewed various licensee self-assessment activities and

corrective action process which included

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. Routine reviews of Nuclear Quality Assessments (NOA) activities

and findings:

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. Observation of the NOA monthly audit exit interview:

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  • A review of the Plant Management Self Assessment Program and

schedule- ,

  • Observation of the licensee's internal Restart Readiness Review

Panel meetings;

Observations of the full Nuclear General Review Committee (NGRC)

meeting on March 12: .

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  • Reviews of precursor cards entered in the corrective action l

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  • Obser ration of a management Corrective Action Review Board (CARB) I

meetwig: I

  • Observations of corrective action Precursor Card Screening j

Committee meetings.

b. Observations and Findinas

NOA inspections continued to be thorough and diverse. N0A continued to

provide timely and responsive surveillances to )lant management in ,

potential plant problem areas. The inspector caserved that a goal of l

N0A management to be proactive and identify problems before they develop

into significant issues remains a challenge. N0A has not consistently

been the first to identify a significant plant problem and characterize

it properly to get it corrected before it 3ecame self-revealing.

However, the ins)ector has observed that the NOA staff has identified

several notewortly findings and were continuing to utilize outside

assistance to provide different audit perspectives.

The NGRC conducted an extensive review of site activities. The

inspector observed that a new offsite member was attending his first

meeting and as yet had not been assigned to a subcommittee. The new

member replaced a former member who resigned. The former member's

subcommittee, the Quality and Regulatory Verification Subcommittee,

again had to meet without the outside member chairman as previously

mentioned in IR 50-302/97-01. The inspector concluded that the NGRC

questioning and discussing issues were beneficial and served to

highlight several ongoing problem areas to the new site management team

such as poor commitment tracking, lack of a sitewide integrated

schedule, and management of significant site process backlogs. The

inspector did not identify any deficiencies.

The inspector reviewed the licensee's new self-assessment process and

the 1997 master schedule. The inspector did not identify any

deficiencies with the process and concluded the schedule was both

diverse and aggressive. The inspector also concluded that successful

implementation could give the licensee broad assessments of varying

areas and be essential to sustaining long term improvement. Only one -

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assessment had been completed under the new program. The inspector's

review of that assessment is ongoing and will be documented in a

subsequent report.

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The inspectors continue to observe problems with the licensee's

Corrective Action Program implementation as noted above in Section 01.2.

The inspectors have also observed problems with the cross referencing of  :

precursor cards (PC) in the system to Licensee Event Reports (LERs) and

Violations. Numerous extra PCs have been generated and issued for

problems already in the system such as PC 97-2089 which was issued on

reportability problems although PC 97-0841 had been issued and was the

focal point for the licensee's investigation. The inspectors have

observed another problem with the failure to include corrective action

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work in PC documentation and scope and the failure to aggregate problems ,

into one larger level PC. j

c. Conclusions

The inspectors concluded the licensee continues to restructure their

self-assessment activities in an attempt to improve their programs.

Problems continue to be observed. but they are recognized and being  :

addressed by licensee management. The PC problems indicated an underuse !

of the PC system as a mechanism to correct large program problems and a

lack of visibility of significant problems for management review.

Changes to the PC tracking software and processes were being i

investigated by the licensee to address these concerns.  ;

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07.2 Plant Review Committee Activitie.1  ;

a. Insoection Scoce (71707. 40500) ,

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Inspectors have attended numerous planned and emergent PRC meetings to l

assess the licensee's control of safety significant activities. The

inspector reviewed recent planned changes to the PRC procedure, AI-300. 1

Plant Review Committee Charter. Revision 39. and reviewed primary and  ;

alternate membership changes against the licensee's commitments in FSAR c

Section 12.8.1. The inspector discussed various initiatives and goals ,

for PRC reviews with the PRC Chairman. He was recently reassigned to  !

the position of Assistant Plant Director Nuclear Safety to allow him to

'

devote more time to PRC oversight. 1

b. Observations and Findinas

The inspector has observed that recent PRC reviews are thorough and '

detailed. A significant focus has been ) laced on the completeness and i

adequacy of 10 CFR 50.59 evaluat e s. T1e formality of PRC meetings has  !

notably increased with the adoptiu of standard review item formats, the

requirement for each PRC review item to have a presenter, and PRC

presentation expectations. Questioning of presenters by PRC members was  ;

detailed and beneficial and held to consistently high standards of  !

performance. The inspector observed a PRC meeting was canceled on  ;

March 5 because an issue did not have a presenter. The PRC would not i

!

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consider the issue until their requirement for an individual to present

was fulfilled. The inspector reviewed the revised membership of the PRC

and did not identify any problems with the licensee's choices as members

and alternates. The inspector did observe that the number of alternates

was decreased in an attempt to utilize more effective individuals and

ensure greater consistency. Revision 40 to AI-300 was issued March 27. '

1997. The inspector's review of the new procedure commenced at the end

of the report period and will be documented in the next NRC inspection

l report period. The .inspoctor identified a concern with screening of

items to ensure they were considered for PRC review when required. The

PRC Chairman had similar concerns and was investigating methods to

ensure required items did not bypass the PRC. The licensee currently

l

does not have a formal process to ensure this although the inspector was

i not aware of any recent examples where a required PRC review was not

obtained. The inspector was satisfied with the current initiative of

l

,

the PRC chairman but will review the ultimate fix.

'

c. Conclusions

The inspector concluded the PRC was functioning well and was providing

,

appropriate oversight and safety perspective. The changes to restrict

l membership, assign a full time chairman, and refine expectations were

l beneficial initiatives by the licensee and were indicative of an

emphasis on improving nuclear safety.

l JL. Maintenance l

l M1 Conduct of Maintenance i

M1.1 General Comments

a. Insoection Scoce (62703. 62707. 61726)

l

The inspectors observed all or portions of the following work requests

! (WR) and surveillances and reviewed associated documentation. The

l following activities were included:

. WR NU 0341383: Change out cells #61 and #107 on the B battery

train. DPBA-1B

. WR NU 0339715:-Upgrade EGDG-1B in accordance with Modification

Approval Record (MAR) 96-10-05-01

  • SP 907A: Monthly Functional Test of 4160V Engineered Safeguards

l (ES) Bus A Undervoltage Relaying

,

b. Observations and Findinas

.

l The inspectors observed the activities identified above and concluded

j that all work was accomplished in accordance with the work instructions

l and procedures. All work observed was performed with the work packages

l

present and in active use. Pre-job planning was thorough and in

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sufficient detail to prepare the technicians for the assigned tasks.

Technicians were experienced and knowledgeable of their assigned tasks.

The inspectors frequently observed supervisors and system engineers

monitoring job progress, and quality control personnel were present

whenever required by procedure.

c. Conclusions

The inspectors concluded that all observed maintenance and surveillance

activities were performed in accordance with procedures and desired

results were obtained.

JJL Enoineerino

/

El Conduct of Engineering

El.1 Precursor Card 97-1517 (37551)

The inspector reviewed PC 97-1517. which requested an evaluation of FPC

Mechanical Calculation M94-0003. Pressure Locking and Thermal Binding

Evaluation. Revision 1. The PC reported that the mechanical calculation  !

did not account for both closing and reopening of the Emergency

'

l Feedwater (EFW) isolation valves by automatic Emergency Feedwater

i

Initiation and Control (EFIC) actuations. The PC stated that the

l

evaluation of the possibility of pressure locking and thermal binding on

the Emergency Feedwater Pump (EFP) flow isolation to the "B" steam '

generator. Emergency Feedwater Valve (EFV)-32 and EFV-33. should be

reevaluated. Valves EFV-32 and EFV-33 are flexible wedge valves and are

susceptible to pressure locking and thermal binding. The original i

'

evaluation relied on the fact that once closed, these two valves would

l not open again during the accident. The valves closed to isolate i

feedwater to the effected generator. using Feed Only Good Generator

(F0GG) logic criteria.

I

During the design verification review. the licensee discovered that the

valves may have to be reopened if the steam generator pressure recovers i

or if there were certain overcooling event. The licensee intends to l

evaluate these conditions prior to restart. The inspector reviewed the

flow diagram discussed the condition with the shift manager, reviewed

the applicable portions of M94-0003, and reviewed the PC. The inspector

concluded that the licensee had done a good job of identifying and

documenting the problem and found this to be an example of both

j appropriate and critical self analysis.  !

'

Additionally. Emergency Feedwater Pump (EFP) flow isolation to the "A"

i steam generator. EFW-11 and EFW-14. are double-disk. Parallel flexible

l wedge valves. These valves are equipped with an integrated relief from ,

the bonnet to the upstream side and are not susceptible to pressure

locking and thermal binding.

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E8 Miscellaneous Engineering Issues l

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E8.1 (Closed) VIO 50-302/96-09-04 Failure to Uodate Ooeratina Curves to

Reflect 1981 Power Vorate

, a. Insoection Scoce (92903) I

This violation involved failure to translate design requirements into

procedures in that Operating Procedure OP-103A. Start-up Curves, was not

updated until July 1995 to reflect the 1981 reactor power u] rate. The

, inspectors reviewed the licensee's corrective actions for t11s

violation.

b. Observations and Findinos

The inspectors verifie- at the licensee had completed corrective

actions for this violation. as stated in their letter of response dated

November 4. 1996, which included:

l

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Revising 0P-103A to provide updated curves. As noted in NRC

Inspection Report 50-302/96-03, the curves were revised in 1995.

-

Sampling additional packages for safety system modifications to

ensure the appropriate operations procedures were identified and

revised.

.

The corrective actions were detailed in Problem Report (PR) 96-0423.

For extent of condition, the licensee selected a sample of Technical

. Specification (TS) Amendments and associated MARS and verified that all

necessary procedures were revised in a timely manner. The review found

'

i that all necessary procedures had been revised in a timely manner and l

Operations had notified the Nuclear Safety Assessment Team (NSAT) to

,

close the PR. However, in reviewing the PR and associated corrective

actions. the inspectors noted that the Operations documentation of

review of the TS Amendments and MARS found that, even though all

necessary procedures were revised in a timely manner, many procedures

tied to modifications did not appear on the Procedure Revision

'

Verification Sheet for the MAR. and identification of required Jrocedure

changes was inconsistent for TS Amendments. After questioning Jy the  !

inspectors, the licensee agreed that these weaknesses should be

'

addressed before closure of the PR. The PR Corrective Action Plan was

revised to address these weaknesses. Also, the licensee pointed out

that in-process corrective actions for another PR (96-0189) included a

review to determine the extent of condition for MARS not identifying

procedures needing revision. In addition. Nuclear Engineering Procedure

.

(NEP)-212. Processing of Modification Projects By Nuclear Projects, had

,

recently been revised to enhance the review for determining which

departments need to review MAR packages for procedure changes. Based on

the corrective actions completed and those ongoing. this item is closed.

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{ c. Conclusions

'  !

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l The inspectors concluded that the licensee's completed and ongoing i

e corrective actions were adequate to resolve this violation. However,

i failure to revise PR 96-0423 to address the discrepancies identified,  ;

relative to identification in MAR packages of needed procedure  !

i revisions, was considered a weakness. l

j I

The inspector assessed the licensee *s performance, with respect to this I

j issue, in the five NRC continuing areas of concern:

1 * Management Oversight - Adequate

i * Engineering Effectiveness - Adequate

* Knowledge of the Design Basis - N/A
  • Compliance with Regulations - Adequate

j e Operator Performance - N/A

E8.2 (Closed) VIO 50-302/96-09-63. Failure to Perform 10 CFR 50.59 Safety

i Evaluation for Chances to Procedures Described in the FSAR For

? Controllino Dissolved Hydroaen Concentration

, a. Insoection Scoce (92903)

4

) This violation involved failure to perform a 10 CFR 50.59 evaluation for

changing the reactor coolant dissolved hydrogen concentration specified

i in the FSAR from 15 - 40 cc/kg to 25 - 50 cc/kg. The inspectors

i reviewed the licensee's corrective actions for this violation.

1

) b. Observations and Findinas

) The inspectors ve'rified that the licensee had completed corrective

j actions for this violation, as stated in their letter of response dated

i November 4.- 1996. which included:

1 ,

1 -

Performing a 10 CFR 50.59 evaluation for revising Tables 4-10 and j

9-3 of the FSAR to specify 25 - 50 cc/kg dissolved hydrogen

'

j

concentration in the reactor coolant.

-

Increased sensitivity within the Chemistry Department to the

process for the review of the FSAR during procedure revisions.  !

-

Establishment of a Procedure Writer position in the Chemistry i

Department to assure a standard and consistent approach to

procedure changes.

-

Instruction of the new Chemistry Department Procedure Writer in  !

the proper review of FSAR during procedure changes.  ;

-

Training of the new Chemistry Department Procedure Writer in 10

CFR 50.59 evaluations and causal analysis. l

!

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13

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Use of details of this violation in Supervisor Workshop on Safety

Culture being developed as part of Management Corrective Action

Plan (MCAP).

The inspectors verified the above corrective actions through interviews

with the Chemistry Department Manager and the Chemistry Department

Procedure Writer review of PR 96-0422. review of documentation of

initial.10 CFR 50.59 training, and review of FSAR changes. The

Chemistry Department Procedure Writer assumed his position on August 5,

1996. He received Causal Analysis training on November 13, 1996 and

initial 10 CFR 50.59 training on January 23. 1997. He was scheduled for

additional 10 CFR 50.59 training on March 31 - April 1,1997.

During review of corrective actions. the inspectors noted that a FSAR

change and associated 10 CFR 50.59 evaluation were documented to change

the reactor coolant hydrogen concentration to 25 - 50 cc/kg. Before the

change was included into the next FSAR Revision (Revision 23). as part

of an overall review of FSAR chemistry requirements, another change and

10 CFR 50.59 evaluation deleted Tables 4-10 and 9-3. which included the

hydrogen concentration and other reactor coolant water quality

requirements. . from the FSAR. The change also deleted Table 4-11. which

covered steam generator Feedwater Quality Specifications. The change

was incorporated in Revision 23 to the FSAR. The water quality

requirements deleted from the FSAR were included in a site procedure.

Licensee Chemistry Department personnel revealed that the reason for i

moving the water quality to procedural control was that the water  !

quality requirements need to be changed frequently because of changes

needed based on site specific and industry experience. The water  ;

quality requirements are specified in Site Procedure CH-400, Revision 9.

Nuclear Chemistry Master Scheduling Program. The inspectors verified <

that Chemistry Procedure CH-400 contains all of the requirements from

deleted FSAR Tables 4-10, 4-11. and 9-3 and that any changes to

procedure CH-400 were controlled by a 10 CFR 50.59 evaluation.

Based on the corrective actions completed for the specific violation, ,

this item is closed. However, removal of water chemistry requirements l

from the FSAR without NRC approval may not meet the requirements of 10

CFR 50.59. This issue is considered unresolved pending further review- ,

by the NRC and is identified as Unresolved Item (URI) 50-302/97-02-02.

Deletion of Water Quality Requirements from the FSAR.  !

, c. Conclusions

l

The inspectors concluded that the licensee's completed and ongoing

corrective actions for the specific violation were adequate to resolve

the violation. VIO 50-302/96-09-03 is closed. However, subsequent

4 actions to remove water quality requirements from the FSAR without NRC

j approval may not meet the requirements of 10 CFR 50.59.

f

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14

The inspector assessed the licensee's performance, with respect to the

specifics of the violation, in the five NRC continuing areas of concern:

. hnagement Oversight - Adequate

  • Engineering Effectiveness - Adequate
  • Knowledge of the Design Basis - N/A
  • Compliance with Regulations - Adequate

. Operator Performance - N/A

E8.3 (Closed) VIO 50-302/96-06-07. Failure to Initiate a Problem Reoort to

Resolve CREVS Test Failure

a. Insoection Scooe (92903).

This violation involved failure to follow procedures in that a PR was

not issued to document a failed surveillance (SP-186) on Control Room

Emergency Ventilation System (CREVS) Filter AHFL-4A. Procedure CP-111

required initiation of a PR for test failures. The issue was initially

identified as URI 50-302/96-03-10. An additiona.1 example of this URI

was identified in paragraph M1.1 of NRC IR 50-302/96-04. This example

involved failure to issue a PC or PR for a failed surveillance on Makeup

Tank Instrumentation Calibration (SP-169G). URI 50-302/96-03-10 was

upgraded to a violation in IR 50-302/96-06, but the example from IR

50-302/96-04 was not specifically identified. The inspectors reviewed

the licensee's corrective actions for the violation.

b. Observations and Findinos

The inspectors verified that the licensee had completed corrective

actions for this violation. as stated in their letter of response dated

August 26. 1996, which included:

-

Discussion with Engineering personnel involved with this issue to

ensure they were clear on the expectations for implementing the

requirements of CF-111.

-

Revision of SP-186 to clarify the requirement for generating

appropriate corrective action documentation for surveillance

failures.

The inspectors verified the above corrective actions through interviews

with responsible Engineering personnel. review of PR 96-0142, and review

of SP-186 and associated procedure CP-148. Ventilation Filter Testing

Program. In addition to the specific corrective actions identified in

the letter of response. a new corrective action program has been

implemented with increased emphasis on initiating PCs for any problem

identi fied. Although the URI specific example identified in IR

50-302/96-04 was not addressed in the violation or the licensee's

response the new corrective action program and the increased emphasis

on identification of problems should be sufficient to resolve the

additional example identified in IR 50-302/96-04.

4.

15

Also, the inspectors noted that the corrective actions did not i

adequately address the " extent of condition." When questioned by the  !

inspectors. the licensee performed word searches on all surveillance

procedures and determined that only 96 out of a total of approximately

250 surveillance procedures adequately addressed the need to initiate a

PC for failed surveillances. A PC (97-1556) was immediately issued to

specify and document corrective actions for this problem,

c. Conclusions  !

The inspectors concluded that the licensee's completed corrective

actions for the specific failed surveillance identified in the violation

were adequate. However, failure to adequately address the " extent of

condition" is considered a weakness. The vfolation is closed.

The inspector assessed the licensee's performance, with respect to this

issue, in the five NRC continuing areas of concern:

.

  • Management Oversight - Adequate

. Engineering Effectiveness - Adequate

e Knowledge of the Design Basis - N/A -

  • Compliance with Regulations - Adequate

. Operator Performance - N/A

E8.4 (Closed) VIO 50-302/96-05-01. Failure to Follow Procedures to Initiate

Corrective Actions for Bent Main Steam Line hanaers (92903). ,

I

This violation was closed in NRC IR 50-302/97-01 based on the NRC Safety '

Evaluation Report (SER) dated January 22. 1997. During the current

inspection the inspectors field verified the replacement of the bent )

hanger rods. The inspectors noted that the rod for Support MHS-13B was  ;

in hard contact with two structural members on an adjacent whip

restraint. The system and sgport were in their cold position. Review

of the Engineering analysis revealed that when the pipirg is heated up

the system growth will be in a direction to move the rod away from the

structural members. (The replacement of the bent rod had been

accomplished while the piping was hot). However. in the cold position.

the condition of the support, i.e., the amount of force being exerted on

the hanger rod by the structural members was unknown. The hanger rod

was removed and determined to be in good condition with no permanent

deformation.

By the end of the inspection, the licensee had issued WR NU 0341874. DCN

97-081. Revision 1 to Calculation S96-0130. and Plant Equipment

Equivalency Replacement Evaluation (PEERE) 1495 to move the hanger rod

upper lug support so that the rod would not be in contact with the whip

restraint structural steel. This will resolve this issue.

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E8.5 (Ocen) VIO 50-302/96-15-02. Failure of Reactor Coolant Pumo 011

Collection System to Retain Oil Leakina From Reactor Coolant Pumo Motor

a. Insoection Scoce (92903)

l

i

This violation involved failure of the reactor coolant pump (RCP) oil  :

collection system to retain the leakage from RCP "D" motor lube oil

system. The inspectors revi ed the licensee's corrective actions for

this violation.

b. Observations and Findinas

The inspectors ve fied that the licensee's corrective actions were

completed to date for this violation, as stated in their letter of i

1

response dated December 20, 1996, which inc10ded:

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Identifying and repairing the source of leakage in RCP "D" lube

oil piping system.

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Identifying and repairing the leaking section of RCP "D" oil

collection system.

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Inspection of the oil collection system for the other 3 RCP

motors.

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Stressing the importance of cleaning all oil collection enclosure

joint surfaces of all residual oil before applying sealants.

The inspectors verified the above corrective actions through ~ interviews

with the res3cnsible Maintenance personnel and review of WRs NU 0338636

(repair of t1e leaks in RCP D lube oil system) and NU 0338186

(inspection and repair of the oil collection enclosures for all 4 RCP

motors). At the time of the inspection, all inspection and repa'ir work j

had been completed on RCPs A and D. Inspection and necessary repair 1

work was in process on RCP B and scheduled to begin on RCP C the week of  ;

March 24. 1997.

l

On March 19. 1997, during their Reactor Coolant System Readiness Review. l

the licensee found that the following RCP lube oil components were l

located outside the lube oil collection system: upper oil reservoir

drain line and valve for RCPs B. C and D. a check valve in the low

pressure oil piping for RCP B and two check valves in the low pressure

oil piping for RCP C. PC 97-1519 was written and the issue was still  !

being evaluated at the close of the inspection. The violation remains  ;

open pending resolution this new issue.

c. Conclusions

The inspectors concluded that the' licensee's completed and ongoing

corrective actions were adequate to resolve the violation. However, the

violation remains open pending resolution of the new issue relative to i

components outside the oil collection system.

.

17

The inspector assessed the licensee's performance, with respect to the

specific violation, in the five NRC continuing areas of concern:

. Management Oversight - Adequate

. Engineering Effectiveness - Adequate

  • Knowledge of the Design Basis - N/A

. Compliance with Regulations - Adequate

. Operator Performance - N/A

E8.6 (Ocen) VIO 50-302/96-11-04. Failure to Construct the Reactor Buildina

Sumo Screens and Comoonents in Accordance with the ADDroVed Draw 1na

a. Insoection Scoce (92903)

This violation involved failure to construct (original construction) the

Reactor Building (RB) Sump Screen support frame in accordance with

drawing recuirements. Sup3 ort frame welds were missing or of poor

quality anc some gaps in t1e structure exceeded the maximum screen mesh

criteria. The inspectors reviewed the licensee's corrective actions for

this violation,

b. Observations and Findinas

The inspectors verified that the licensee's corrective actions were

completed to date for this violation as stated in their letter of ,

response dated November 27, 1996, which included: l

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PR 96-0374 was issued to document and resolve this issue.

-

The support structure and welds were inspected and repaired to  !

meet drawing requirements. 1

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_An operability review was performed to evaluate the "as-found" i

condition to determine if the structure was capable of performing ,

its design basis function in the degraded condition. l

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Plant records were reviewed to attempt to identify the contractor

responsible for installation of the sump screens. Since the

records did not clearly identify the contractor, samples of other

,

similar installations were inspected for other deficiencies.

-

Current surveillances for the sump would be evaluated for

adequacy.

The inspectors verified the above corrective actions through interviews

with the responsible plant personnel and review of the documents listed

above. In addition, the NRC observed inspection of the sumps for

missing welds and reviewed documentation of repairs as detailed in NRC

Inspection Report 50-302/96-11.

Review and revision of the RB sump surveillance procedures was not

scheduled until June 1. 1997.

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The licensee's sample inspection of similar installations included 6

, components / structures. Discrepancies (missing structural members) were

identified on 2 structures (a lead shielding support for Makeup System l
Jiping and a support for the Nuclear Service and Decay Heat Exchanger. '

l Joth in the Auxiliary Building). At the time of the NRC inspection, the

! licensee was evaluating these inspection findings to determine the scope  !

'

i for expanding the inspection sample.

c. Conclusions

The inspectors concluded that the licensee had completed the corrective 1

actions for the specific violation on the Reactor Building Sump Screens. '

I

However. the violation remains open )ending review of corrective actions

for the discrepancies found during t1e " extent of condition"

inspections.

l

The inspector assessed the licensee's performance, with respect to the

,

specific violation, in the five NRC continuing areas of concern:

l

'

  • Management Oversight - Good

. Engineering Effectiveness. - Adequate

  • Knowledge of the Design Basis - N/A
  • Compliance with Regulations - Adequate
  • Operator Performance - N/A

E8.7 (Closed) VIO 50-302/96-06-02. Inadeauate Procedure for Performina a

Demineralized Water Flush Follow 1na a Boric Acid Addition

a. Insoection Scooe (92903)

This violation involved the failure of Procedure OP-402 to specify  !

flushing with demineralized water following a boric acid addition. The  !

inspectors reviewed the licensee's corrective actions for this

violation.

1

b. Observations and Findinas I

The inspectors verified that the licensee's completed corrective actions

for this violation, as stated in their letter of response dated August

26, 1996, had been completed. The corrective actions included revising

Procedure OP-402 to provide details for flushing after the addition of

i boric acid.

The inspectors reviewed Revision 90 of Procedure OP-402 Makeup and

, Purification System, which contained the necessary details for flushing I

after the addition of boric acid. This violation is closed.

1

c. Conclusions l

l

The inspectors corcluded that the licensee completed the corrective

actions for this violation and the corrective actions were adequate.

i

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The inspector assessed the licensee's performance, with respect to the

specific violation. in the five NRC continuing areas of concern:

. Management Oversight - Adequate

. Engineering Effectiveness - N/A

  • Knowledge of the Design Basis - N/A

. Compliance with Regulations - Adequate

. Operator Performance - N/A

E8.8 (Closed) IFI 50-302/96-201-11. Desian Basis for Decay Heat / Core

Flood / Reactor Coolant Pioina Temoerature

a. Insoection Scoce (92903)

This item is the same as Inspector Follow-up Item IF-201-01 identified

by the Integrated Performance Assessment Process (IPAP) Team. The IPAP

Team questioned the use of 300 F (280 F operating temperature) as the

design temperature for the piping upstream of the Core Flood check valve

CFV-3 since the valve is relatively close to the reactor vessel. The

design temperature for the piping downstream of the valve to the reactor

vessel is 650 F (600 F operating temperature). The inspectors

reviewed the licensee's actions relative to this IFI.

b. Observations and Findinas

i

The inspectors verified licensee's corrective actions for this issue,

which included:

-

PR 96-0216 was issued to document and resolve this question.

-

Calculation M96-0044 was performed for the vertical riser

(approximately 20 feet) upstream of valve CFV-3 to demonstrate 1

that the entire riser meets design basis Code allowables if heated

to the 600 F operating temperature.

Based on review of the above documents and discussions with responsible

engineering personnel, the inspectors considered the above actions j

appropriate for resolution of this issue.

c. Conclusions

'

The inspectors concluded that the licensee's completed corrective

actions for this issue were good. A detailed calysis of the piping in

question was performed to assure that the piping met Code requirements.

l The inspector assessed the licensee's performance, with respect to

i resolution of this issue in the five NRC continuing areas of concern:

. Management Oversight - Good

. Engineering Effectiveness - Good

  • Knowledge of the Design Basis - Good -

. Compliance with Regulations - Good

[

. Operator Performance - N/A

.

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E8.9 (Closed) URI 50-302/97-01-08. Adeauacy of Procedures to Take the Plant

from Hot Standby to Cold Shutdown from Outside the Control Room

a. Insoection Scone (40500. 92903)

The inspector followed up on this URI which involved a concern

identified by the NRC where it was determined that the licensee did not

have procedures in effect which provided adequate instructions for

taking the plant from hot standby to cold shutdown from outside the main

control room.

b. Qbservations and Findinas

The inspector reviewed this item for compliance with 10 CFR 50 Appendix

R. NRC SER requirements, the CR-3 operating license. FSAR and

operations procedures. Crystal River's Operating License Condition

2.C.(9). Fire Protection and FSAR Section 9.8.8. Safe Shutdown, states

in part that the capability of the plant to achieve safe shutdown in the

event of a fire was analyzed in the licensee's Fire Hazards Analysis:

NRC SERs dated July 27. 1979. October 14. 1980. November 24, 1980.

January 22. 1981. January 6. 1983. July 18. 1985, and March 16. 1988:

and the licensee's 10 CFR 50 Appendix R Fire Study. The inspector

reviewed the applicable SERs issued by the NRC which discussed the

licensee's Appendix R program. The inspector reviewed FSAR Section

7.4.6. Auxiliary Control Stations (Remote Shutdown System) and FSAR

Section 9.8. Plant Fire Protection Program. Section 7.4.6.5 of the l

FSAR stated in part that the design basis for the remote shutdown system

was 10 CFR 50. Appendix R. Section L. and 10 CFR 50. Appendix A.

Criterion 19. Section 7.4.6.5 of the FSAR further stated that the

design basis for remote shutdown assumed a loss of offsite power.

Section 9.8.6 of the FSAR stated that plant procedures developed in

accordance with 10 CFR 50. Appendix R. Sections III.G and III.L

establish means to bring the plant from operating to cold shutdown.

As discussed in URI 50-302/97-01-08. the inspector reviewed licensee

abnormal 3rocedures (AP) to determine if any of the procedures were

im) acted )y MAR 94-09-02-01. MAR 94-09-02-01. DC Cooling Instrument

Enlancement, addressed the issue of non-safety related positioners cn

safety-related air-operated valves DCV-17, 18. 177. and 178.

One of the APs reviewed by the inspector was AP-990. Shutdown From

Outside Control Room. Revision 8 The inspector noted that this AP

provided procedural steps for taking the plant to hot standby and then

directed operations personnel to maintain the plant in hot standby until

a specific cooldown plan was formulated. The AP did not contain steps

for taking the plant from hot standby to cold shutdown and the AP did

not provide a reference or transition to any other procedure that would

be used by the operators to take the plant from hot standby to cold

shutdown. The inspector discussed this issue with licensee personnel

who indicated that operating procedure OP-209. Plant Cooldown.

Revision 87 provided guidance to the operators for taking the plant

from hot standby to cold shutdown. The inspector reviewed OP-209 and

. . _ __ _. _. _ _ . _ _. . _ _ _ .. __ __ ._. .

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noted that Enclosure 1 to the 3rocedure provided information concerning

cooldown following a fire in tie main control room or cable spreading

i

room. This enclosure 3rovided general guidance for certain fire

-

scenarios and stated tlat this information was intended to assist plant

personnel in designing a specific cooldown procedure following main

control room evacuation.

I The inspector determined that the procedures (AP-990 and OP-209 being

i used either separately or in conjunction with each other) did not -

provide adequate instructions for taking the plant from. hot standby to  ;

cold shutdown from outside the main control room. The inspector further '

concluded that licensee Administrative Procedures AP-990 and OP-209 did

1 not meet the requirements of 10 CFR 50. A)pendix R.Section III.L. The

guidance in Operating Procedure OP-209 w11ch directed o)erations
personnel to develop a specific cooldown 3rocedure to tace the plant to

cold shutdown based on an assessment of t1e fire scenario and equipment

i availability, did not meet the criteria in Section III.L. Section III.L

states that procedures shall be in effect to implement the capability of.

'

being able to take the plant to cold shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> following

main control room evacuation due to a fire. The inspector noted that

CR-3 License Condition 2.C.(9) states in part that Florida Power
Corporation shall implement and maintain in effect all provisions of the

i approved fire protection program as described in the FSAR for the

l facility and as approved in the SERs.

i ,

4

The inspector informed the licensee that failure to have procedures in

effect to implement the capability of being able to take the plant to

. cold shutdown following main control room evacuation due to a fire was a

a violation of NRC requirements and will be identified as VIO 50-302/97-

$

02-03. Adequate Procedures Not in Effect to Take the Plant from Hot

i Standby to Cold Shutdown froni Outside the Control Room. Based on

4

identification of this VIO. URI 50-302/97-01-08 will be closed. 1

-

c. Conclusions

The inspector concluded that adequate procedures were not in effect to

. meet the requirements of 10 CFR 50. Appendix R.Section III.L. in that

i licensee Procedures AP-990 and OP-209 used either separately or in

conjunction with each other, did not provide adequate instructions for

4

taking the plant from hot standby to cold shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

. following main control room evacuation due to a fire. This issue was

identified as a violation.

i

The inspector assessed the licensee's performance, with respect to this

. issue, in the five areas of continuing NRC concern:

. Management Oversight - Adequate

1 . Engineering Effectiveness - N/A

. Knowledge of the Design Basis - Good

. Compliance with Regulations - Inadequate

. Operator Performance - Adequate

.

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E8.10 (Ocen) LER 50-302/95-025.' Personnel Errors by Architect Enaineer Result l

in Ooeration Outside Desian Basis Due to Inadeauate Safety /Non-Safety  !

Circuit isolation i

l

'

(Ocen) VIO 50-302/95-2:.-03. Failure to Isolate the Class IE from the

Non-Class IE Electrica' Circuitry for the RB Purae and Mini-Purae Valves ,

1

a. Insoection Scooe (37550. 92903)  ;

The inspector reviewed the subject LER. which involved improper

isolation of Class IE from Non Class IE electrical circuitry for the i

reactor building purge valves. The inspector followed up on the {

licensee's corrective actions for this LER. l

b. Observations and Findinas

The inspector reviewed the corrective actions specified in the LER and  !

the licensee's response to the NRC Violation 50-302/95-21-03 that was  ;

issued for this concern. The corrective actions were reviewed for  !

compliance with the FSAR. TS. and applicable licensee procedures. The '

inspector noted that some of the corrective actions specified in the .

responses had been completed. Other corrective actions involved  !

implementation of modifications to address the issue. Some of the  !

modifications had been implemented. During review of the corrective  !

actions, the inspector noted that the licensee's evaluation of ,

alternatives to the present non-isolated design of the control circuits

for reactor building purge Air Handling Valves AHV-1A and AHV-1D was not .

com)leted by the scheduled date of December 20. 1996, as' specified in l

bot 1 the LER and the NOV response. The new date for completion of the

evaluation was changed to May 1998. The ins)ector discussed this change

with licensee personnel who indicated that tie schedule change was due

to an increase of other higher priority issues such as EFIC/EFW and EDG

loading. The inspector also questioned whether Supplement 02 to this

LER had been submitted by December 20. 1996, as indicated in supplement

01 to LER

50-302/95-025. dated December 22. 1995. A copy of Supplement 02 to this i

LER was not included with the documentation provided to the inspector.  !

Licensee personnel indicated that they were continuing to review their

records to determined if Supplement 02 to LER 50-302/95-025 had been

submitted to the NRC. This item remains open.

c. Conclusions

]

The inspector concluded that the licensee had completed some of the

specified corrective actions to address this issue. However. due to

workload and higher priority issues related to the EFIC/EFW and EDG  !

loading. the scheduled completion date for other corrective actions was

not met and the completion date was extended. Additionally, the

licensee was reviewing its records to determine if Supplement 02 to LER I

50-302/95-025 had been issued.

I

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The inspector assessed the licensee's performance, with respect to this  !

, issue, in the five areas of continuing NRC concern: '

  • Management Oversight - Adequate i
  • Engineering Effectiveness - Adequate  :
  • Knowledge of the Design Basis - N/A >
  • Compliance with Regulations - Adequate .
  • Operator Performance - N/A

,

E8.11 L0cen) EA 95-16. Use of Nonconservative Trio Setooints for Safetv-

!

Related Eauloment

i

(Ocen) VIO 97-01-07. Instrument Setooint Calculation Assumotions Not

Translated into Procedures

a. Insoection Scoce (92903. 37550)  !

As part of the conti tuing review of corrective actions for EA 95-16.

the insx ctors reviewed several new instrument loop uncertainty setpoint

calculatioas and the implementation of the corrective actions for VIO

50-302/97-(1-07. Instrument Setpoint Calculation Assumptions Not

!

Translated Into Procedures. In IR 95-06 the inspectors found that some

safety-related trip setpoint calculations did not follow the methodology.

specified in Instrument Society of America (ISA) 67.04, part II as

referenced by instrumentation and controls Design Criteria Instrument

, String Error /Setpoint Determination Methodology. To assess the progress

the licensee had made in this area, the inspector reviewed a. sample of

the most recent instrument string error /setpoints. The inspectors also

revie;ed the preliminary corrective actions for VIO 50-302/97-01-07 and

the 10 CFR 50.72(b)(2)(1) report made by the licensee to document the

degraded or unanalyzed condition associated with this violation.

,

b. Observations and Findinas

1) EA 95-16. Use of Nonconservative Trip Setpoints for Safety-Related

Equipment. >

The inspector reviewed several recent instrument loop uncertainty

(instrument string error) setpoint calculations with the following

< comments:

i

Revision 0. dated 2/14/97. The inspector had one minor

comment on Section V. Detailed Calculations subsection 1.

'

Process Errors. First Design Condition - Ecuation for

specific volume at 175 F used 0.I650 ft 3/ lam for the

! specific vplume at 170* F. The value should have been

0.01650 ft /lbm.

Additionally. the service water flow transmitters were .

located in the Auxiliary Building in E0 zone 11. which had
an assumed normal ambient temperature of 55* to 97 F.

!

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  • j

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24

l

These ambient temperatures were not reflected in the service

water current flow transmitter calibration procedures, nor

had the calibration procedures been updated to reflect the

changes to the " graded approach" methodology. These will be '

reviewed as part of the corrective action for VIO 50-302/97-

01-07.

Apart from these questions, the calculation was clear,

concise, with well-founded assumptions, and used standard

ISA methodology.

  • I-95-0015. Core Flood Tank Level & Pressure Loop Error

Calculation. Revision 0. SP-169A. Surveillance Procedure,

j Core Flood Tank Instrument Calibration.

l I-95-0015 required that the M&TE in the reactor building be

, maintained at various temperatures below the normal

operating temperatures specified in the Environmental and

'

Seismic Qualification Program Manual (ESOPM). Contrary to

'

this for the core flood tank level transmitters and pressure

sensors. the licensee failed to include instructions for
accomplishing this task in the surveillance )rocedure which

i was used for the instruments' calibration. 3 ruck 510 has an

i upper operating temperature of 81* F. In ambient

temperatures greater than 81* this required an ice bath.

l refrigeration unit. cooling fan, or some other method for

cooling the instrument before using it in the calibration
process. The methodology for cooling this instrument had

not been evaluated, had not been approved, and were not part

,

of the calibration procedure. Not translating design

'

requirements I-95-0015 into procedures was an additional

example of VIO 50-302/97-01-07 Instrument Setpoint

l Calculation Assumptions Not Translated Into Procedures.

i

The inspector noted one additional minor discrepancy in this j

<

calculation. On page 21 of 87 the 13.9 C value used for j

'

the temperature delta for the M&TE error associated with the

3

Druck DPI 510 could not be reproduced. The value should be

the maximum allowable calibration temperature minus the

4 lowest allowable temperature in the ESOPM zone. This was i

11* F or approximately 6.1* C. The inspector calculated the j

.

M&TE error associated with the Druck DPI 510 as 0.112 span. J

The value-in the calculation was 20.123% span. The effect  ;

! on the final loop uncertainty was minor and in the j

conservative direction. The inspector found no other

'

1 analytical discrepancies in this calculation.

! 2) Corrective actions for VIO 50-302/97-01-07. Instrument Setpoint

,

Calculation Assumptions Not Translated Into Procedures:  ;

i The inspectors reviewed Florida Power Corporation Crystal River

Unit 3. Restart Action Plan / Issue Description. Issue Number: 0-26

,

4

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25  !

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l Rcv. O. Action Plan / Issue Title: Calculation Temp Ranges Not

Consistent With Actual Ranges which was written to restore an

adequate design margin or ensure conformance with the design '

basis. The specific issue was that normal temperature ranges used

.

'

l

in existing Analysis / Calculation were not consistent with the t

actual temperature ranges to which the equipment was subjected.

l This was identified as a generic concern with recorded  ;

temperatures .in the reactor building and the auxiliary recorded  ;

temperature, i

The licensee's program to resolve this issue included-

l

  • Identification of all instrument surveillance procedures  !

3erformed since last refueling outage. The licensee r

Selieved that this would define the safety related

instrument channels potentially involved.

l

  • Identification of the dates the affected surveillance

procedures were performed.

'

  • Identification of the average daily temperature data for

each of the dates for the identified surveillances. This .

'

was defined as the lowest hourly average of ten second

i meteorological data. The inspector was told that the

licensee intends to evaluate the meteorological data

available during the period of the last instrument

calibration

  • Evaluation of data obtained to identify those instrument

loops which could potentially be adversely impacted by

temperature variations larger than those addressed in the -

calculations, i

  • Evaluation of the impact of temperature variations

associated with identified instrument loops. The inspector

was informed that due to present plant status, all

applicable instrumentation required for mode 5 operation 1

would be evaluated on a priority basis. l

j * Identify and initiate required corrective actions and  ;

determine impact to design basis.

i On March 6. 1997. the licensee reported some of these conditions

,

under 10 CFR 50.72(b)(2)(i) to document a condition discovered

while shutdown, that, had it been discovered during reactor

operation would have resulted in the nuclear plant being seriously i

'

degraded or in an unanalyzed condition that significantly i

-

compromised plant safety. In the report the licensee stated that l

they consider all instrumentation located in the auxiliary

building and the reactor building to be in a degraded condition.

r The licensee's actions taken to resolve these conditions will be

evaluated during the review of EA 96-16. Use of Nonconservative

,

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26

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Trip Setpoints for Safety-Related Equipment and during the review

of the 10 CFR 50.72 report review.

,

The calculations relating to instrument loop uncertainty that

remained to be reviewed included:

Calculations being revised -

I-86-0003 Off Site Dose and Maximum Allowable Filtration

I-87-0003 EFW. Flow Control and Interlock

I-88-0012 Gamma-Metrics Indicator. Loop Error

I-88-0021 Pressurizer Level Loop Accuracy

I-89-0013 Containment Air Temperature Loop Accuracy

I-90-0018 Decay Heat Closed Cooling. Water Surge Tank Level -

Loop Accuracy Calculation '

I-92-0011 Control Room Habitability Evaluation of Potential

Inleakage

I-95-0012 Core Flood Tank Level and Pressure Loop Error

Evaluation

Calculations being developed -

I-95-0010 Diesel Fuel Day Tank - DFT - 31/3B Analysis

Additionally, the calculations that were completed in late 1996 i

and early 1997 have not been implemented in the field. Therefore. 1

the field im)lementation portion of these setpoints were not  !

reviewed. T1ese included: I

'

I-85-0004- Rev 4. 11-19-96. EFW Tank Level Accuracy .

I-85-0005 Rev 3, 11-19-96. EFW Tank Level Settings

I-88-0019 Rev 3. 02-13-97. Incore Thermocouple Loop Accuracy

I-88-0022 Rev 4. 02-21-97. RC (Thot) Temperature Loop Accuracy, ,

RC-4A. 4B. TE1. 4 '

I 91-0012 Rev 3. 11-20-96. BWST Level Accuracy

I-91-0021 Rev 1.-02-27-97. RC Flow Loop (NNI) Accuracy

I-94-0011 Rev 0. 02-14-97. RB Fan Service Water Flow Loop

Accuracy

I-95-0015 Rev 0. 01-24-97. Core Flood Tank Level and Pressure i

Loop Error Evaluation

i

c. Conclusions l

The inspectors concluded that the licensee continued to make progress in  !

resolving the Improved Technical Specifications (ITS) setpoint program

deficiencies. In general, the calculations reviewed were well

documented, with well-founded assumptions, and followed the methodology

specified in ISA 67.04 part II. as referenced by instrumentation and

controls Design Criteria Instrument String Error /Setpoint Determination

Methodology. These calculations continue to be a significant

improvement over calculations reviewed in IR 95-06.

l

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27

The inspectors concluded that the Reactor Building. Intermediate

Building, and Auxiliary Building tem)erature ranges which the ESOPM

environmental assumptions used for t1e instrument loop uncertainty

setpoint calculations were not maintained. Also, the design assumptions

had not been appropriately translated into instrument calibration or

room monitoring procedures. In addition, proceduralized controls were

lacking for use of M&TE in the reactor building. These issues are

additional examples of VIO 97-01-07, Instrument Setpoint Calculation

Assumptions Not Translated into Procedures.

The inspectors assessed the licensee's performance relative to lack of

design control for assumptions in instrument setpoint calculations, in

the five areas of continuing NRC concern:

. Management Oversight - Inadequate

. Engineering Effectiveness - Inadequate

e Knowledge of the Design Basis - Inadequate

e Compliance with Regulations - Inadequate

. Operator Performance - N/A ,

E8.12 (Closed) URI 50-302/96-17-03. Failure to Conduct Reauired Technical

Soecifications Surveillance Testina on Safety Related Circuitry

(GL 96-01)

a. Insoection Scoce (92903) 4

!

The ins)ectors reviewed the concerns listed in URI 50-302/96-17-03 and

the Tec1nical Specifications to determine the appropriate method for

closure,

1

b. Observations and Findinos

On April 12, 1996, the licensee in response to GL 96-01. Testing of

Safety Related Logic Circuits. identified two circuits which were not

being appropriately tested in accordance with TS requirements. These

circuits were the " auto reset of ES blocks 4 and 6 load sequencing i

relays and the load shed circuit that trips EFP~ 1 when EGDG-1A is

-

supplying the ES Bus and a High Pressure Injection (HPI) signal is

received." On October 22. 1996, the licensee identified that two

contacts in each of the six pressure bistables in the ESAS (Engineered

Safeguards Actuation System) logic were not being tested in accordance

with TS requirements. These bistable contacts were all part of the ESAS

Reactor Coolant System (RCS) Pressure - Low and: Low Low actuation

circuits.

TS Surveillance Requirement (SR) 3.3.5.2 requires that a channel

functional test of ESAS instrumentation be performed once every 31 days.

The failure to test ES blocks 4 and 6 did not comply with this TS

requirement.

_

TS SR 3.8.1.10 requires testing of load shedding from emergency buses

on loss of offsite power in conjunction with . . an ES actuation

.

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28

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signal once every 24 months. The failure to test load shedding of EFP-1 ,

did not comply with this TS requirement. '

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TS SR 3.3.5.2 requires that a channel functional test of ESAS

instrumentation be 3erformed once every 31 days. TS SR 3.3.5.3 requires

'

that a channel cali] ration be performed of ESAS instrumentation once

every 24 months. The failure to test the pressure bistable contacts did

i not comply with these TS requirements.

c. Conclusions  ;

The inspectors concluded that the licensee did not comply with TS

recuirements for testing logic circuits. URI 50-302/96-17-03 is closed i

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anc VIO 50-302/97-02-04 Failure to Conduct TS Logic Testing, is opened.

The inspector assessed the licensee's performance, with respect to the  ;

licensee's prior noncompliance with TS requirements. in the five areas i
of continuing NRC concern
l

. * Management Oversight - Inadequate

  • Engineering Effectiveness - Inadequate

4

~

  • Knowledge of the Design Basis - Inadequate
  • Compliance with Regulations - Inadequate
  • Operator Performance - N/A

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E8.13 (Ocen) NRC Generic Letter 96-01. Testina of Safety-Related Loaic

4 Ci rcuits

a. Insoection Scoce (92903)

Generic Letter (GL) 96-01. issued January 10, 1996, requested the

<

following certain actions from all operating nuclear power reactors

,

relative to the problems with testing of safety-related logic circuits:

l

! * Compare electrical schematic drawings and logic diagrams for the i

, reactor protection system. EDG load shedding and sequencing, and i

. actuation logic for the engineered safety features systems against  !

j plant surveillance test procedures to ensure that all portions of

the logic circuitry, including the parallel logic, interlocks.

'

bypasses, and inhibit circuits are adequately covered in the

surveillance procedures to fulfill the TS requirements. This '

review should also include relay contacts, control switches, and

other relevant electrical components within these systems utilized

in the logic circuits performing a safety function.

i. i

e Modify the surveillance procedures as necessary for complete

i testing to comply with technical specifications.

i

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During this inspection, the inspectors examined the licensee's actions

to date relative to the testing of TS safety-related logic circuits

4

described in GL 96-01.

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29

b. Observations and Findinas

The licensee responded in FPC Letter 3F0496-25. dated April 1996. that a '

plan was being developed and that a firm schedule would be determined  ;

following completion of a pilot program. Florida Power Corporation

Letter 3F0796-09. dated July 1996. reaffirmed the FPC commitment to

complete the review requested by GL 96-01 ]rior to restart from the next l

refueling outage in the Spring of 1998. T1e licensee had GL 96-01 1

review listed as their Restart Issue #R-1.

The inspectors reviewed the GL 96-01 program and schedule. The

licensee's GL 96-01 program was implemented by an engineering contractor

firm at the contractor firm's home office. A licensee ]roject engineer

managed the program. In addition, the contractor firm lad an on-site

engineer to review and validate the work performed at the home office.

The on-site engineer reviewed the documents sent from the home office

and compared them against the TS. drawings, and surveillance procedures.

Each logic circuit and component was red lined by the on-site engineer -

to ensure nothing was overlooked. The inspectors verified that the

contractor completed five logic circuitry review packages for the

emergency diesel generators, the emergency feedwater systems, the main

steam isolation function. and the main feedwater isolation function.

The EDG packages (M218-96-02.013) were dated March 10. 1997. The

emergency feedwater, main steam isolation and main feedwater isolation

packages (M218-96-02.015) were dated March 13, 1997.

The inspector performed a preliminary review of the on-site engineer's

work packages and drawings to determine if the packages were validated

and if any additional discrepancies were being identified. Several test

discrepancies were identified by the on-site engineer and documented in

PC 97-0054. PC 97-0057, and PC 95-1516. PC 97-0054 listed test

deficiencies for the EDGs in procedures SP-907A and B. PC 97-0057

listed test deficiencies for the emergency feedwater in procedures

SP-146A and B. PC 97-1516 listed a potential procedure weakness for

testing the ESAS system. The inspectors reviewed several logic circuits

in the emergency feedwater system to verify there were no additional

discrepancies and that the contractor and on-site engineer were

implementing a detailed review. The licensee's GL 96-01 program was a

large complex program and was not completed at the time of this

inspection. Completion was not expected until Summer of 1997.

Therefore, the inspectors only performed a partial inspection to

determine if the licensee was in the process of implementing an adequate

program.

c. Conclusions

-

The inspectors concluded the licensee was in the process of implementing

a GL 96-01 program that met the intent of GL 96-01. The contractor's

on-site engineer was thorough and had identified several additional

discrepancies during his validation review. However, the GL 96-01

program still has a lot of work remaining before it will be completed.

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1

" The inspector assessed the licensee's performance, with respect to the

licensee's response to GL 96-01, in the five areas of continuing NRC

,

concern:

i * Management Oversight - Adequate

i

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  • Engineering Effectiveness - Adequate
  • Knowledge of the Design Basis - Adequate
  • Compliance with Regulations - Adequate
  • Operator Performance - N/A

l

E8.14 Emeraency Diesel Generator Power Vorate

,

a. Insoection Scooe (37551)

, -

The inspectors reviewed the MAR for the emergency diesel generator

interim power uprate. MAR 96-10-05-01 implementation, for EDG 1A. was

'

! discussed in IR 97-01. The MAR package and implementation for EDG 1B

were reviewed for technical accuracy and compliance with regulatory and

administrative requirements.

'

b. Observations and Findinas

! Phase 1 of the MAR replaced the nozzle rings in the turbochargers with

i larger rings to increase the combustion air flow rate. made minor

adjustments to the fuel rack on the engine, and replaced the single pass

combustion air intercooler with a dual pass intercooler. This

'

modification increased the efficiency of the diesel engine and was a
necessary modification to support Phase 2 of the modification which

increases the power rating for the emergency diesel generators. This

modification depends on the review and approval by the NRC. This

modification does not change the continuous and 30 minute ratings on the

EDG. The 200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> and 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> ratings will be changes from 3000 kW to

3250 kW for the 2000 hour0.0231 days <br />0.556 hours <br />0.00331 weeks <br />7.61e-4 months <br /> rating and from 3250 kW for 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> to 3400

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kW.

The ins)ectors noted the improvements on scheduling and implementation

of the EDG-1B modification. The outage was completed within one day of

the schedule. No post maintenance testing was omitted from the

schedule, and all work appeared to be accomplished in accordance with

the work instructions.

The inspectors reviewed the safety evaluation performed per the

requirements of 10 CFR 50.59. The licensee identified certain

assumptions in the safety evaluation that were used as the basis for the

conclusion reached in the Phase 2 evaluation. Plans were made to verify

these assumptions during the Phase 1 post modification testing.

Following the completion of Phase 1 of the modification, the licensee

performed the post modification testing procedure. During this test,

data were gathered to prove operability of the EDG and to be used in

calculations to support Phase 2 of the modification.

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Precursor Card 97-996 was written to document a concern identified

l during the review of the modification. A discrepancy was identified

with diesel fuel oil volume requirements. TS 3.8.3.2 requires each EDG  ;

day tank to have a minimum volume of 233 gallons. TS 3.8.3.1 requires i

each fuel oil storage tank to contain at least 18,589 gallons of fuel i

with a combined fuel oil storage level of at least 37,177 gallons. l

These numbers were derived assuming a maximum American Petroleum i

Institute (API) specific gravity of 32. The licensee reviewed sampling '

data since 1986 and identified that they had been receiving fuel oil

with s)ecific gravities ranging from 28 to 38. If the maximum number

,

that tie licensee had received was used in the supporting calculations.

l the TS number would be non-conservative. Using an API specific gravity

of 38. the licensee concluded that a minimum of 261 gallons per tank

'

were needed for the day tanks and 38.694 gallons needed to be maintained

in the storage tanks. The licensee procedure SP-345A and 345B. Monthly

Functional Test of the Emergency Diesel Generator EGDG-1A and EGDG-18.

requires that a minimum volume of 345 gallons be maintained in each day

tank and that the fuel oil storage tank volumes be maintained above

i

'

20.300 gallons per tank. These administrative limits are maintained

above the number calculated for the more conservative API specific

gravity values.

Precursor Card 97-999 was issued on March 3. 1997. which documented that

following the MAR functional testing on EDG 1A. data collected indicated ,

that the EDG engine room temperature could potentially exceed the design 1

maximum temperature of 120 F at maximum loading of the diesel generator. I

This data was in conflict with data collected in 1992. used to verify I

the impact of an earlier power uprate. The licensee is continuing to  ;

analyze this data and data collected following the EDG 1B MAR to analyze

I final impact.

Precursor Card 97-1501 was issued on March 3, 1997. which indicates that  ;

EDG exciter maximum field current capability could potentially exceed i

the-design limitation of 54 amperes at maximum loading of the diesel

generator. This PC was written for EDG-1A. but also applies to EDG-1B.

The licensee is continuing to assess the impact of the power uprate to

determine if the limiting current would be exceeded. j

c. Conclusions I

Three issues are in process of being evaluated by the licensee to ,

determine final impact of identified discrepant conditions resulting  ;

l

from the implementation of MAR 96-10-05-01. These issues will be

i tracked as an Inspector Follow-up Item. IFI. 50-302/97-02-05.

Outstanding Issues Associated with tbn Emergency Diesel Generator Power

Uprate Modification.

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E8.15 Toxic Gas Monitor Imorovements

a. Insoection Scoce (37551)

The inspectors followed up on the toxic gas monitoring system

improvements as discussed in Inspection Report 97-01.

b. Observations and Findinas

The licensee continueC in its efforts to identify needed improvements in

the toxic gas monitoring system. Working with the vendor, the licensee

identified that besides a potential susceptibility to preconditioning

the detectors, the detectors are manufactured with a wide variance in

, response times.  ;

.

l The licensee was in the process of revising the Surveillance Procedures

t

PT-366. Toxic Gas Detection System Calibration (Train A) and PT-367.

.

Toxic Gas Detection System Calibration (Train B). to require response

time testing prior to performing the saan test. In addition. the

licensee has procured detectors with s1 ort response times. Installing
these detectors and testing the res3onse time without any

1

~

preconditioning, the licensee was a31e to readily meet the acceptance

criteria for the calibration procedure. The toxic gas monitors were

j declared operable and returned to service on March 18. 1997.

I

c. Conclusions

1

i The licensee is continuing to evaluate the reliability of the toxic gas

j monitoring system and develop a permanent solution to the issue.

,

E8.16 Radiation Monitorina Confiauration Control (37551. 71750)

l On March 22,1997. RM-L7. the secondary drain tank liquid effluent line-

! radiation monitor, sustained damage and failed. During the restoration

1 efforts, per WR NU 0341950. the licensee discovered that the detector

i installed in the radiation monitor was not a high temperature rated

detector, as required to be installed under MAR 86-09-22-01. Further
investigation by the licensee revealed that a high temperature detector

.

was installed in RM-L2, the primary side liquid waste effluent line

radiation monitor. This monitor did not require a high temperature

,

detector.

) The licensee determined that the manufacturer part numbers for the two

detectors were 943-36 for the low temperature application and 943-36H

for the high temperature application. The part number that the licensee

1 assigned to these two detectors did not differentiate between the high

j temperature and low temperature applications.

1 The licensee contacted the manufacturer to determine the im3act of

j- switching the detectors in these two radiation monitors. T1e

'

manufacturer informed the licensee that the high temperature detector

! has thermal insulation around the crystal and photomultiplier tube. The

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effect of the thermal insulation was to attenuate the response to low

energy gamma (80 kev). According to the manufacturer, the effect was

small compared to the attenuation of the stainless steel case of the

detector and would not affect the use in a liquid monitor. The

manufacturer's representative stated that the attenuation from the

thermal insulation would only be a factor. in gas application for gamma

from Xe-133.

According to the manufacturer, the failure mode of the low temperature

detector due to heat would be indicated by increasing counts in response

to the check source. The increase would be caused by the gain changing

in a conservative direction. This would cause the detector to trip at a

lower. more conservative setpoint. than expected.

ThelicenseereplacedthedetectorinRM-L7biththehightemperature

detector from RM-L2. A low temperature detector was then installed in

RM-L2. The licensee is continuing to access the root cause and

consequences of this issue under PC 97-2222 and PC 97-2229.

IV. Plant Sucoort

P1 Conduct of Emergency Preparedness Activities

Pl.1 Emeroency Precaredness Drill Initiatives (71750. 92904)

The inspectors discussed some drill initiatives with licensee Emergency

Preparedness personnel. The licensee has announced plans to perform an

unannounced staffing drill of the Technical Support Center (TSC) at some

off-hours time during a two month period. The licensee will require

individuals to respond to the site to assess the time needed to activate

the TSC with an adecuate staff against regulatory requirements. The

inspectors concludec this was a valid test of the ability to respond to ,

an actual event and was a good initiative. The licensee has also  ;

revised their normal event drill schedule to increase the frequency of

drills to quarterly and include a full TSC activation which will include

use of the control room simulator. The inspector concluded this was an

improvement over previous licensee practices. The inspectors will

assess implementation of these initiatives when completed.

S1 Conduct of Security and Safeguards Activities

S1.1 Security Procram Peer Assessment

a. Insoection Scooe (71750)

On March 10 through 14. 1997, an assessment of the licensee's security

program was conducted by a group of four other utility Security

Managers, a fifth support person, and a retired former NRC security

inspector. The inspector reviewed the scope of the assessment and

attended the entrance and exit meetings.

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b. Observations and Findinas

The licensee requested the assessment from outside personnel to assist ,

them in correcting previously documented security program problems. A

conscious effort was made to select managers from good performing plants

that have had problems in the past and successfully rectified them. A

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manager from a plant in each of the four NRC regions was selected to

balance regulatory perspectives and get diverse input. The team used

existing NRC inspection guidance to focus their reviews and provided the I

licensee with numerous insights and comments for improvement. Strengths  !

. were identified by the team in training and use of a Central Alarm

,~ . Station simulator and performance of the guard force. Deficiencies were

identified in the lack of issued procedures for recent upgrades and the

need for a Physical Security Plan (PSP) revi.sion, inconsistent vehicle

, and personnel search processes, and the extent of required compensatory

.

measures. One notable finding the team discovered when verifying how

the licensee fulfilled their PSP was that the licensee did not have a -

!

commitment cross reference matrix that ensured all requirements and

commitments were addressed and delineated specifically how they were

i met. The licensee commenced development of a matrix to address the

i finding.

3 c. Conclusions

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The inspector concluded the Security Program Peer Assessment was

balanced and beneficial for the licensee security staff in their efforts

to improve performance and regulatory compliance.

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V. Manaaement Meetinas

! X1 Exit Meeting Summary

-

The inspection scope and findings were summarized on March 21 and

March 31, 1997. Proprietary information is not contained in this

report. Dissenting comments were not received from the licensee.

X2 Pre Decisional Enforcement Conference Summary

X3 Management Meeting Summary

l X3.1 A public meeting was held on site at Crystal River March 21. 1997. The

purpose of the meeting was to discuss items related to restart. A

l separate meeting summary was issued on March 31. 1997.

PARTIAL LIST OF PERSONS CONTACTED

'

Licensees

R. Anderson. Senior Vice President. Nuclear Operations

'

J. Baumstark. Director. Quality Programs

J. Campbell. Assistant Plant Director. Maintenance and Radiation Protection

J. Cowan. Vice President. Nuclear Production

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l R. Davis. Assistant Plant Director. Operations and Chemistry

B. Gutherman, Manager. Nuclear Licensing-

G. Halnon. Assistant Plant Director. Nuclear Safety

8. Hickle. Director. Nuclear Plant Operations

J. Holden. Director. Nuclear Engineering and Projects

t D. .Kunsemiller. Director. Nuclear Operations Site Support

[ E

l H. Christensen. Engineering Branch Chief. Region II (March 21, 1997)

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B. Crowley. Reactor Inspector. Region II (March 3 through March 7, 1997.

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March 17 through 21. 1997)

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P. Fillion. Reactor Inspector Region II (March 17 through March 21. 1997)

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F. Hebdon. Director. Dirrctorate II-3. NRR (March 21. 1997)

J. Jaudon. Director. Division of Reactor Safety. Region II (March 21. 1997)

K. Landis. Branch Chief. Region II (February 26 through 27. 1997. March 21.

j 1997)

^

B. Manili. Licensing Reviewer. NRR (March 17 through March 19. 1997)

L. Mellen. Project Engineer. Region II (March 3 through 7. March 17 through

21, 1997)

! M. Miller. Reactor Inspector. Region II (March 17 through March 21. 1997)

L. Raghavan. Project Manager. NRR (March 5 through 6, 1997. March 20 through
21. 1997)

. L.'Reyes, Regional Administrator. Region II (March 21. 1997)

j R. Schin. Reactor Inspector. Region II (March 3 through March 7. March 19

through March 21, 1997)

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L. Stratton. Physical Security Specialist. Region II (March 17 through

March 21. 1997)

M. Thomas. Reactor Inspector Region II (March 17 through March 21, 1997)

INSPECTION PROCEDURES USED

s IP 37550: Engineering i

l IP 37551: Onsite Engineering -

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IP 40500: Effectiveness of Licensee Controls in Identifying. Resolving and

Preventing Problems <

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i IP.61726: Surveillance Observations i

IP 62703: Maintenance Observations

IP 62707
Conduct of Maintenance
. IP 71707
Plant Operations  !
IP 71750
Plant Support Activities
IP 92901: Followup - Operations

i IP 92903: Followup - Engineering >

j IP 92904: Followup - Plant Support

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ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

IY2g Item Number Status Descriotion and Reference

VIO 50-302/97-02-01 Open Failure to Follow Equipment Status

Control Procedural Requirements.

(paragraph 01.2)

URI 50-302/97-02-02 Open Deletion of Water Quality

Requirements from the FSAR.

(paragraph E8.2)

VIO 50-302/97-02-03 Open Adequate Procedures Not in Effect to

Take the Plant from Hot Standby to

Cold Shutdown from Outside the

Control Room. (paragraph E8.9)

VIO 50-302/97-02-04 Open Failure to Conduct TS Logic Testing.

(paragraph E8.12)

IFI 50-302/97-02-05 Open Outstanding Issue- "ssociated with

the Emergency Diesel Generator Power

Uprate Modification. (paragraph

E8.14)

Closed

IY2g Item Number Status Descriotion and Reference

VIO 50-302/96-09-04 Closed Failure to Update Operating Curves

to Reflect 1981 Power Uprate.

(paragraph E8.1)

VIO 50-302/96-09-03 Closed Failure to Perform 10 CFR 50.59.

Safety Evaluation for Changes to

Procedures Described in the FSAR For

Controlling Dissolved Hydrogen

Concentration. (paragraph E8.2)

VIO 50-302/96-06-07 Closed Failure to Initiate a Problem Report

to Resolve CREVS Test Failure.

(paragraph E8.3)

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VIO 50-302/96-05-01 Closed Failure to Follow Procedures to

Initiate Corrective Actions for Bent

Main Steam Line hangers. (paragraph

E8.4)

VIO 50-302/96-06-02 Closed Inadequate Procedure for Performing

a Demineralized Water Flush

Following a Boric Acid Addition.

(paragraph E8.7)

IFI 50-302/96-201-11 Closed Design Basis for Decay Heat / Core

Flood / Reactor Coolant Piping

Temperature. (paragraph E8.8)

URI 50-302/97-01-08 Closed Adequacy of Procedures to Take the

Plant from Hot Standby to Cold

Shutdown from Outside the Control

Room. (paragraph E8.9)

URI 50-302/96-17-03 Closed Failure to Conduct Required

Technical Specifications

Surveillance Testing on Safety

Related Circuitry (GL 96-01). l

(paragraph E8.12)

Discussed

lypjg Item Number Status Descriotion and Reference

VIO 50-302/96-15-02 Open Failure of Reactor Coolant Pump Oil

Collection System to Retain Oil

Leaking From Reactor Coolant Pump

Motor. (paragraph E8.5)

VIO 50-302/96-11-04 Open Failure to Construct the Reactor

Building Sump Screens and Components

in Accordance with the Approved

Drawing. (paragraph EB.6)

i LER 50-302/95-025 Open Personnel Errors by Architect

! Engineer Result in Operation Outside

Design Basis Due to Inadequate

Safety /Non-Safety Circuit Isolation.

(paragraph E8.10)

VIO 50-302/95-21-03 Open Failure to Isolate the Class IE from

the Non-Class IE Electrical

Circuitry for the RB Purge and Mini-

Purge Valves. (paragraph E8.10)

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VIO 50-302/97-01-07 Open Instrument Setpoint Calculation

Assumptions Not Translated into

Procedures. (paragraph E8.11)

EA 95-16 Open Use of Nonconservative Trip

Setpoints for Safety-Related

Equipment. (paragraph E8.11)

LIST OF ACRONYMS USED

AI - Administrative Instruction

AP - Abnormal Procedure

API - American Petroleum Institute

CARB - Corrective Action Review Board -

CFR - Code of Federal Regulations

CREVS - Control Room Emergency Ventilation System

CR3 - Crystal River Unit 3

EA - Enforcement Action

ECCS - Emergency Core Cooling System

EDG - Emergency Diesel Generator

EFIC - Emergency Feedwater Initiation and Control

EFP - Emergency Feedwater Pump

EFV - Emergency Feedwater Valve

EFW - Emergency Feedwater

ES - Engineered Safeguards

ESAS - Engineered Safeguards Actuation System

ESOPM - Environmental and Seismic Qualification Program Manual

FD - Fire Damper

FOGG - Feed Only Good Generator

FPC - Florida Power Corporation

FSAR - Final Safety Analysis Report

GL - Generic Letter

HPI - High Pressure Injection

IFI - Inspection Followup Item

IPAP - Integrated Performance Assessment Process

IR - NRC Inspection Report

ISA - Instrument Society of America

ITS - Improved Technical Specifications

Kw - Kilowatts

LER - Licensee Event Report

MAR - Modification Approval Record

MCAP - Management Corrective Action Plan

MUV - Make-up Valve

NEP - Nuclear Engineering Procedure

i NGRC - Nuclear General Review Committee

l NOV - Notice of Violation

NQA - Nuclear Quality Assessments

NRC - Nuclear Regulatory Commission

NRR - Office of Nuclear Reactor Regulation

NSAT - Nuclear Safety Assessment Team

01 - Operating Instruction

OP Operating Procedure

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PC - Precursor Card

PEERE - Plant Equipment Equivalency Replacement Evaluation

PR - Problem Report

PRC - Plant Review Committee

PSP - Physical Security Plan

RB - Reactor Building

RCP - Reactor Coolant Pump

RCS - Reactor Coolant System

RG - Regulatory Guide

SER - Safety Evaluation Report

SFP - Spent Fuel Pool l

SP - Surveillance Procedure ,

SR - Surveillance Requirement  !

SSOD - Shift Supervisor on Duty

SW - Nuclear Services Closed Cycle Cooling

TS - Technical Specification

TSC - Technical Support Center

URI - Unresolved Item

VIO - Violation

WR - Work Request

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