IR 05000302/1990022
| ML20055H577 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 07/06/1990 |
| From: | Belisle G, Taylor P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML20055H576 | List: |
| References | |
| 50-302-90-22, NUDOCS 9007270019 | |
| Download: ML20055H577 (4) | |
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Re' port No :50-302/90-22-Licensee:
Florida Power Corporation
e 3201 34th Street, South, d
~St. Petersburg, FL 33733 j
Docket No.:
50-302
- License No.:. DPR-72
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' Facility Name: Crystal River 3-Inspection Conducted: Jupe 12-16, 1990 i
II/#M Inspector:
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Approvedby:/
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GM. 'BemTe,~ Chief
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Engineering Branch..
Division of Reactor Safety
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SUMMARY.
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Scope:
This routine, ~ announced -inspection was-conducted in the' areas of review and (
witnessing integrated engineered safeguards (ES)= and-loss of offsite power (LOOP) tests.
EEsults:
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iIn-the areas-inspected, one violation vas identified but is not being cited.
--l-Inadequate-procedure steps (SP-417) contributed to the reactor building':"--
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emergency cooling fant(AHF-1C) not being in its required position for ES
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. actuation'duringES/ LOOP. test, Train"B"(paragraph 2c)
r This licensee identified violation-is.not.being cited because criteria.
specified in section V.G.1'of the NRC Enforcement Policy were satisfied.
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REPORT DETAILS 1.
Persons Contactef
- Licensee Employees
- G.- Boldt,J Vice President, Nuclear Production M._Fitzgerald, Supervisor, Nuclear Engineering Services
- R. Fuller, Senior Nuclear Licensing Engineer
- G. Halnon, Assistant Nuclear Shift Supervisor
- H.'Koon, Superintendent, Nuclear' Maintenance
- W. Marshall, Superintendent, Nuclear Operations
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- P. McKee,~ Director, Nuclear Plant Operations
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- D. Porter, Nuclear Shift Supervisor
- F. Sullivan, Manager, Nuclear Systems Engineering Other licensee. mployees contacted 'during this inspection included
engineers, operators, technicians, and administrative personnel, j
NRC Resident Inspector-
- P. Holmes-Ray, Senior Resident Inspector L
'* Attended exit. interview L
2.
IntegratedES/LOOPTest-(61701)
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Procedure Review
~ The inspector reviewed SP-417, Integrated Plant Response To An ES Actuation, Revision 28, dated June 13, 1990 to verify the following:
L Appropriate levels of management review and approval had been
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The design change (MAR 88-05-24-01)~ requirements which i
reassigned selected ES loads to new load blocks and times were l
verified to be tested during conduct of SP-417.
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b ES components. pumps, and ventilation fans required to go to
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their emergency position during ES actuation with a loss of offsite power were identified in the test steps of the l
procedure.
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SP-417 contained prerequisites, initial system conditions and
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l precautions to be established prior to conducting the test.
Acceptance criteria provided were qualitative or quantitative as i.
appropriate.
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'I The: inspector's comments to SP-417 were presented to the -licensee I-and resolved prior to the tests.
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Test Witnessing
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- SP-417 was perfoimed on June 16, 1990.- Prior' to the test. - the l
licensee conducted a briefing with plant operators, engineers and
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electrical technicians assigned to assist in:the performance of the i
'. integrated ES/ LOOP test. The briefing was held in a conference room.
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l with the Shift Supervisor leading the discussion. The briefing was a h
comprehensive review of the test procedure ~ and covered, in detail, duties and responsibilities required of test personnel, data l
acquisition, the operating sequence of-plant systems, and responses to be expected during the test.
The inspector observed plant operators establishing prerequisites and j
initial conditions for testing Train
"A" engineered safeguerds.
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systems and EDG-1A.
These activities, as well as test equipment'
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calibration, were reviewed on a sample basis to verify that procedure requirements were being met.
The testing of Train "A" started with an ES actuation consisting of a
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building pressure signal (30 PSIG)gnal (4 PSIG), high-high' reactor reactor building high pressure si l
and a simulated loss of offsite
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L power to the 4160 volt eme'rgency bus.
A review of test results indicated that ES equipment achieved their emergency positions and assigned load blocks, load shedding from the emergency buses had occurred, and the permanent a connected'and auto-connected emergency
~ loads to the EDG 1A did not exceed Technical Specification requirements of 3248 KW.
~The observed load on the EDG-1A 'was approximately 2000 KW.
In addition, one of.the new ES logic features was also tested during SP-417.
This feature simulated olarge break -
LOCA signals (RCS pressure 500 PSIG) andsverified that the decay-heat'-
removal pump (DHR-1A) starts and' the emergency.feedwater pump-(EFP-1)
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tripped off. The results of this test were satisfactory.
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Following ES/ LOOP testing of Train "A", Train "B", ES systems were aligned and the ES/ LOOP test was performed. The test results for the Train "B" ES systems ' indicated satisfactory responses. The observed load on the EDG-1B_ was approximately 1750 KW.
It was noted during the first portion of the Train"B" ES/ LOOP test that air handling fan (AHF-1C) did not indicate sequencing on after the 4 PSIG reactor building high pressure signal was initiated.
A check at the ES cabinets indicated that AHF-1B had been selected.
The selector switch was placed in the AHF-1C position and the response of the fan and its KW load was verified during the ESF/ LOOP portion of the test.
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The licensee's review indicated that SP-417 procedure steps, wnich aligned the air handling units, did not adequately address switch positions for the test and permitted AHF-1B to be selected. AHF-1B
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e was out of service for maintenance.
The inspector concluded that the.
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inadequate procedure steps (SP-417 steps 4.4.17.4.2, 4.4.17.4.3, and
4.4.31) was a licensee identified violation.
During the exit interview, the licensee stated the following actions were planned or in progress:. Issue a memorandum to the operations groups, discussing.
the identified procedure problem, and initiate a change to SP-417, identify the procedure problem so root cause analysis can be conducted through the Human Performance Evaluation System.
The-inspector had no further question in this area.
3, Exit Interview The inspection scope and results were summarized on June 16, 1990, with those-persons indicated in paragraph 1.
The inspector described the' areas inspected and discussed in detail the inspection results listed below.
Proprietary information - is not contained in this report.
Dissenting.
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comments were not received from the licensee,
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Inadequate procedure steps (SP-417) contributed to the reactor 1l
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building emergency cooling fan (AHF-1C) not being-in its required-.
position-for ES-actuation during ES/ LOOP tests, Train "B" (paragraph-lj
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The licensee identified. violation is-not be cited because criteria
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specified in section V.G.1 of the NRC Enforcement Policy were satisfied.
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