ML20138M726
ML20138M726 | |
Person / Time | |
---|---|
Site: | McGuire, Mcguire ![]() |
Issue date: | 10/21/1985 |
From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20138M724 | List: |
References | |
50-369-85-30, 50-370-85-32, NUDOCS 8511040256 | |
Download: ML20138M726 (1) | |
Category:NOTICE OF VIOLATION OF A REGULATION
MONTHYEARML20154C4131998-09-21021 September 1998
[Table view]Notice of Violation from Insp on 980712-0822.Violation Noted:On or Before 971217,operations Personnel Failed to Designate Appropriate Vent Valves for Venting to Properly Return Sys to Svc as Required by Omp 7-1 ML20237B1561998-08-0707 August 1998 Notice of Violation from Insp on 980531-0711.Violation Noted:Licensee Failed to Establish Procedural Guidance for Abnormal Vent Path Used for Degassing Unit 1 Volume Control Tank to Environ ML20249A2451998-06-0404 June 1998 Notice of Violation from Insp on 980413-24.Violation Noted: Procedure Investigation Processes 2-M96-1440 & 0-M97-1933 Were Not Initiated within 24 H After Realization That Procedure Investigation Process Should Have Been Written ML20216H6051998-04-0606 April 1998 Notice of Violation from Insp on 980125-0307.Violation Noted:Licensee Failed to Adequately Establish or Adhere to Procedural Guidance for Repair of Two safety-related Containment Isolation Valves as Evidenced ML20203F5921998-02-23023 February 1998 Notice of Violation from Insp on 980105-08.Violations Noted: Licensee Failed to Follow Procedures for Security Badge & Access Control IR 05000369/19970191998-01-0505 January 1998 Errata to Notice of Violation for Insp Repts 50-369/97-19 & 50-370/97-19.Statement in Nov,Page 2, Under Authority of Section 182 of Act.42USC 2232,this Response Shall Be Submitted Under Oath or Affirmation, Was Incorrect ML20199B1571998-01-0505 January 1998 Notice of Violation from Insp on 971205-06.Violation Noted: an Event Occurred on 971202 in Which Person or Persons Made Credible Threat to Commit or Cause Significant Physical Damage to Power Reactor & Not Reported within One Hour ML20198N4701997-10-20020 October 1997 Notice of Violation from Insp on 970810-0920.Violation Noted:On 960420,ET Guidelines,Apps C & E Were Not Implemented as Evidenced By;Resolution Analyst Revised & Overruled Reexam Request for SG 2A Tube R7C60 ML20212A0361997-10-0808 October 1997 Notice of Violation from Insp on 970712-0827.Violation Noted:As of 970717,10 of 48 Ice Condenser Inlet Doors on Unit 2 Required Initial Opening Torque in Ixcess of 675 inch-pound Operability Limit ML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility ML20149L5701997-07-28028 July 1997 Notice of Violation from Insp on 970518-0628.Violation Noted:Procedure IP/0/A/3250/12B Inadequate to Provide Sufficient Guidance to Properly Test Emergency Diesel Generator Sequencer Logic Circuitry ML20149G6771997-06-16016 June 1997 Notice of Violation from Insp on 970406-0517.Violation Noted:Procedure PT/1/A/4600/014D Was Inadequate in Providing Sufficient Guidance to Bypass Properly RPS Functions of an Inoperable N-41 Channel to Permit Testing of Channel N-42 ML20148B9621997-05-0505 May 1997 Notice of Violation from Insp on 970223-0405.Violation Noted:Prior to 961130,activities Affecting Quality,Not Accomplished in Accordance W/Instructions,Procedures or Drawings ML20137V1381997-03-24024 March 1997 Notice of Violation from Insp on 970112-0222.Violation Noted:Licensee Failed to Implement Appropriate Emergency Procedures,Conduct Required Drills or Renew Exemptions to Be Excluded from Stated Requirements ML20134L1211997-02-10010 February 1997 Notice of Violation from Insp on 961201-970111.Violation Noted:Inspector Identified Modification Involving Installation of Addl Vital Area Physical Barrier ML20135C2411996-11-15015 November 1996 Notice of Violation from Insp on 960908-1019.Violation Noted:Plant Periodic Test Procedure,Annulus Ventilation Sys Train B Operability Test Not Adequate ML20128H6631996-10-0202 October 1996 Notice of Violation from Insp on 960728-0907.Violation Noted:Licensee Failed to Demonstrate Operability of 1A EDG within Required Time After 1B EDG Was Determined to Be Inoperable ML15118A0501995-12-22022 December 1995 Notice of Violation from Insp on 951113-17.Violation Noted: Licensee Allowed Vendor to Implement Access Authorization Program After Determining That Vendor Failed to Assure That Individuals Were Trustworthy & Reliable,Approx 11 Months ML20029E2941994-05-0606 May 1994 Notice of Violation from Insp on 940313-0409.Violation Noted:Unidentified Leakage Rate Exceeded TS Limit on at Least Twelve Occasions During Past 12 Months Prior to 931207 While in Modes 1,2,3 or 4 ML16154A5751994-03-16016 March 1994 Notice of Violation & Proposed Imposition of Civil Penalties in Amount of $75,000.Noncompliance Noted:On 930324,approx 96 Drawings Re Oconee,Mcguire & Catawba Plants Which Contained Safeguards Info Not Protected ML20059C0261993-12-16016 December 1993 Notice of Violation from Insp on 931017-1120.Violation Noted:On 930909,remote Visual QA Exam Performed on Weld of Tube Plug 39-72 in Unit 1 a Steam Generator Inadequate ML20059K7221993-11-0909 November 1993 Notice of Violation from Insp on Stated Date.Violation Noted:Loss of Normal Letdown Charging or Seal Injection Flow Procedure Was Inadequate Since Failed to Require Any Cautions,Instructions or Guidance ML20059K4291993-10-20020 October 1993 Notice of Violation from Insp on 930822-0925.Violation Noted:Vendors Replacing Roof on Unit 1 Fuel Handling Building Failed to Adhere to Requirements to Use Fire Extinguishers & Obtain Hot Work Permit ML20057C1611993-09-14014 September 1993 Notice of Violation from Insp on 930718-0821.Violation Noted:Surveillance Procedures PT/1/A/4350/36A & PT/1/A/4350/36B Were Not Revised to Incorporate Changes to TS 4.8.1.1.2.e ML20056G9011993-08-19019 August 1993 Notice of Violation from Insp on 930621-25 & 0729.Violation Noted:Loss of Offsite Power Event on Unit 1 Occurred on 910211 for Which Licensee Failed to Immediatley Declare Notification of Unusual Event ML20056E4741993-08-12012 August 1993 Notice of Violation from Insp on 930628-0702 & 930712-16. Violation Noted:Licensee Failed to Notify NRC of Change in Medical Status of Licensed Operators within 30 Days as Required,Per 10CFR55.25 & 10CFR50.74 ML20056E3171993-08-0909 August 1993 Notice of Violation from Insp on Stated Date.Violation Noted:Licensee Had No Specific Procedure in Place Nor Any Preventative Maint Schedule Developed for Lake Level Instrumentation,For Purpose of Entering Emergency Plan ML20045H8591993-06-17017 June 1993 Notice of Violation from Insp on 930517-21.Violation Noted: Licensee Failed to Label as Required by Above Listed Requirements,Three Vacuum Cleaners in Unit 1 Containment That Contained Radioactive Matl ML20036B2321993-05-0303 May 1993 Notice of Violation from Insp on 930314-0417.Violation Noted:On 930322,fitting on Unit 2 Chemical & Vol Control Sys Failed,Causing Reactor Coolant Leak of Approximately 75 Gallons Per Minute ML20034G0051993-02-26026 February 1993 Notice of Violation from Insp on 930119-22.Violation Noted: Failure to Properly Search Package,Resulting in Introduction of Handgun Into Protected Area,In Direct Violation of Physical Security Plan ML20127P7331993-01-13013 January 1993 Notice of Violation from Insp on 921115-1219.Violation Noted:On 921105,licensee Completed PIR-0-M92-0140 W/O Identifying Root Cause or Actions Necessary to Prevent Recurrence ML20217B8731991-02-19019 February 1991 Notice of Violation from Insp on 910106-0202.Violation Noted:Measures Not Adequate to Assure Prompt Corrective Action Taken in Correction of Generic Fuse Installation Problems Originally Identified in March 1989 ML20056A5841990-07-24024 July 1990 Notice of Violation from Insp on 900522-0625.Violations Noted:Both Units Operated W/Two of Four Control Room Ventilation (VC) Sys Intakes Closed from 900525-0603 & Failure to Report Inoperable VC Trains in Required Time ML20044A5401990-06-15015 June 1990 Notice of Violation from Insp on 900425-0521.Violation Noted:Failure to Follow Procedure by Not Signing Off Required Step & Failure to Follow Procedure for Documentation of Problem Investigation Process ML20042F7801990-04-24024 April 1990 Notice of Violation from Insp on 900224-0326.Violation Noted:Failure to Properly Follow Process to Make Major Mod in Maint Procedure MP/0/A/7600/31 Re Limitorque Gearbox for Butterfly Valves Corrective Maint ML20034C2061990-04-20020 April 1990 Notice of Violation from Insp on 900226-0302 & 12-16. Violations Noted:License Failed to Maintain Adequate Documentation of Prejob Reactor Coolant Pump ALARA Activities ML20005E6581989-12-26026 December 1989 Notice of Violation from Insp on 891113-17.Violation Noted:Licensee Declared Unusual Event,But Failed to Notify State/Local Agencies Until 30 Minutes After ML19332E3371989-11-22022 November 1989 Notice of Violation from Insp on 890907-11.Violation Noted: Failure of Test Procedure to Specify Plant Condition Limitations or Caution Operators of Potential for Overpressurizing Low Pressure Sys ML19332E6061989-11-15015 November 1989 Notice of Violation from Insp on 890722-0912.Violations Noted:Annulus Ventilation Sys & Control Area Ventilation Sys Inoperable Since Initial Licensing ML19325D2511989-10-0606 October 1989 Notice of Violation from Insp on 890722-0912.Violation Noted:Failure to Meet Min Shift & Fire Brigade Staffing Requirements ML20246N6471989-08-21021 August 1989 Notice of Violation from Insp on 890707-18.Violation Noted: Core Operated in Excess of 102% of 3,411 Thermal MW Limit Briefly & in Excess of 101% for Nearly 3 H ML20245L4281989-08-0808 August 1989 Notice of Violation from Insp on 890622-28.Violation Noted: Design Control Measures for Changes to Plant Inadequate, Leading to Confusing Instructions to Craft Personnel Which Resulted in Installation of nonsafety-related Positioner ML20236E6441989-07-17017 July 1989 Notice of Violation from Insp on 890422-0601.Violation Noted:Procedures PT/1 & 2/A/4255/03A Deemed Inadequate in That Procedures Specified Testing of MSIVs W/Air Assist, Contrary to Assumed Conditions in FSAR ML20244E5861989-06-0808 June 1989 Notice of Violation from Insp on 890330-0421.Violation Noted:Electrical Drawing MCM-1399.03-0300-001 Inadequate in That It Was Not Properly Updated Contributing to Personnel Error & Temporary Loss of RHR Sys on 881201 ML20247N8241989-05-24024 May 1989 Notice of Violation from Insp on 890424-28.Violation Noted: 1987 Semiannual Effluent Release Rept Listed Two Abnormal Releases But Did Not Include Descriptions of Events ML20246J6511989-05-0505 May 1989 Notice of Violation from Insp on 890213-17 & 0227-0303. Violations Noted:On 890215,maint Crew Observed Working on Work Request W/O Following Appropriate Procedure & with Inadequate Preplanning,Procedures & Instructions ML20245G9641989-04-21021 April 1989 Notice of Violation from Insp on 890228-0329.Violation Noted:Failure to Follow Procedures Re Diesel Generator Starting Air Tank 1B2 Drain Valve ML20244A8801989-03-30030 March 1989 Notice of Violation from Insp on 890120-0227.Violations Noted:Control Room Door Seals Repaired on 890117 W/O Authorization on Work Request & Auxiliary Feedwater Resistance Temp Detectors Installed W/O Authorized Request ML20235P5221989-02-14014 February 1989 Notice of Violation from Insp on 881122-890119.Violation Noted:Procedure Not Properly Implemented in That 1A Emergency Diesel Generator Started on 881206 Using 2A Emergency Diesel Generator Test Procedure ML20206A5551988-11-0404 November 1988 Notice of Violation from Insp on 880924-1020.Violation Noted:Personnel Training Not Completed Prior to Returning low-Tave Setpoint Circuitry to Svc Following Setpoint Change & Unit Not Placed in Hot Shutdown within 6 H 1998-09-21 Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS MONTHYEARIR 05000369/19990061999-10-0404 October 1999
[Table view]Insp Repts 50-369/99-06 & 50-370/99-06 on 990801-0911. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000369/19990051999-08-26026 August 1999 Insp Repts 50-369/99-05 & 50-370/99-05 on 990620-0731.Two Violations Noted Being Treated as Ncv.Major Areas Inspected: Operations,Maint,Engineering & Plant Support IR 05000369/19990041999-07-13013 July 1999 Insp Repts 50-369/99-04 & 50-370/99-04 on 990509-0619.Four Violations of NRC Requirements Occurred & Being Treated as Ncvs.Major Areas Inspected:Aspects of Licensee Operations, Maint,Engineering & Plant Support IR 05000369/19990101999-06-16016 June 1999 Insp Repts 50-369/99-10 & 50-370/99-10 on 990322-26.No Violations Noted.Major Areas Inspected:Aspect of Licensee Health Physics Activities During Unit 2 Refueling Outage IR 05000369/19990031999-06-0202 June 1999 Insp Repts 50-369/99-03 & 50-370/99-03 on 990328-0508. Non-cited Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000369/19990021999-04-23023 April 1999 Insp Repts 50-369/99-02 & 50-370/99-02 on 990214-0327.No Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000369/19990011999-03-10010 March 1999 Insp Repts 50-369/99-01 & 50-370/99-01 on 990103-0213.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000369/19980101998-12-18018 December 1998 Insp Repts 50-369/98-10 & 50-370/98-10 on 981004-1121.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support IR 05000369/19980091998-10-30030 October 1998 Insp Repts 50-369/98-09 & 50-370/98-09 on 980823-1003.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support IR 05000269/19980141998-09-22022 September 1998 Insp Repts 50-269/98-14,50-270/98-14,50-287/98-14, 50-369/98-14,50-370/98-14,50-413/98-14 & 50-414/98-14 on 980824-28.No Violations Noted.Major Areas Inspected:Plant Support.Specific Area Includes Access Authorization Program IR 05000369/19980081998-09-21021 September 1998 Insp Repts 50-369/98-08 & 50-370/98-08 on 980712-0822.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support ML20154C4131998-09-21021 September 1998 Notice of Violation from Insp on 980712-0822.Violation Noted:On or Before 971217,operations Personnel Failed to Designate Appropriate Vent Valves for Venting to Properly Return Sys to Svc as Required by Omp 7-1 IR 05000369/19980111998-08-27027 August 1998 Insp Repts 50-369/98-11 & 50-370/98-11 on 980601-26 & 0805-07.No Violations Noted.Major Areas Inspected:Maint & Engineering Programs.Rept Reviewed Maintenance,Surveillance & Matl Condition of Mcquire,Unit 1 Ice Condenser System ML20237B1561998-08-0707 August 1998 Notice of Violation from Insp on 980531-0711.Violation Noted:Licensee Failed to Establish Procedural Guidance for Abnormal Vent Path Used for Degassing Unit 1 Volume Control Tank to Environ IR 05000369/19980071998-08-0707 August 1998 Insp Rept 50-369/98-07 & 50-370/98-07 on 980531-0711. Violations Noted.Major Areas Inspected:Licensee Operations, Maint,Engineering & Plant Support IR 05000369/19980061998-06-25025 June 1998 Insp Repts 50-369/98-06 & 50-370/98-06 on 980419-0530.No Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support PNO-II-98-030, on 980603,loss of Offsite Power Occurred,Due to Loss of 1B Bus.Caused by Faulted 230 Kv Switchyard Current Transformer.Resident Inspectors Onsite & Responded to Event & Will Continue to Evaluate Activities W/Event1998-06-0404 June 1998 PNO-II-98-030:on 980603,loss of Offsite Power Occurred,Due to Loss of 1B Bus.Caused by Faulted 230 Kv Switchyard Current Transformer.Resident Inspectors Onsite & Responded to Event & Will Continue to Evaluate Activities W/Event ML20249A2451998-06-0404 June 1998 Notice of Violation from Insp on 980413-24.Violation Noted: Procedure Investigation Processes 2-M96-1440 & 0-M97-1933 Were Not Initiated within 24 H After Realization That Procedure Investigation Process Should Have Been Written IR 05000369/19980031998-05-18018 May 1998 Insp Repts 50-369/98-03 & 50-370/98-03 on 980308-0418.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20216H6051998-04-0606 April 1998 Notice of Violation from Insp on 980125-0307.Violation Noted:Licensee Failed to Adequately Establish or Adhere to Procedural Guidance for Repair of Two safety-related Containment Isolation Valves as Evidenced IR 05000369/19980021998-04-0606 April 1998 Insp Repts 50-369/98-02 & 50-370/98-02 on 980125-0307. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support IR 05000369/19970201998-02-23023 February 1998 Insp Repts 50-369/97-20 & 50-370/97-20 on 971214-980124. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support,Including Review of Radiological Protection Practices & Plant Physical Security ML20203F5921998-02-23023 February 1998 Notice of Violation from Insp on 980105-08.Violations Noted: Licensee Failed to Follow Procedures for Security Badge & Access Control IR 05000369/19980011998-02-17017 February 1998 Partially Withheld Insp Repts 50-369/98-01 & 50-370/98-01 on 980114-15 (Ref 10CFR2.790).No Violations Noted.Major Areas Inspected:Plant Support,Including Malevolent Use of Vehicles at Plant & Vehicle Barrier Sys IR 05000369/19970181998-01-12012 January 1998 Insp Repts 50-369/97-18 & 50-370/97-18 on 971102-1213. Violations Noted.Major Areas Inspected:Integrated Insp Included Aspects of Licensee Operation,Maint,Engineering & Plant Support ML20199B1571998-01-0505 January 1998 Notice of Violation from Insp on 971205-06.Violation Noted: an Event Occurred on 971202 in Which Person or Persons Made Credible Threat to Commit or Cause Significant Physical Damage to Power Reactor & Not Reported within One Hour IR 05000369/19970191998-01-0505 January 1998 Errata to Notice of Violation for Insp Repts 50-369/97-19 & 50-370/97-19.Statement in Nov,Page 2, Under Authority of Section 182 of Act.42USC 2232,this Response Shall Be Submitted Under Oath or Affirmation, Was Incorrect ML20199B1641998-01-0505 January 1998 Insp Repts 50-369/97-19 & 50-370/97-19 on 971205-06. Violations Noted.Major Areas Inspected:Licensee Response to 971202 Event Involving Seal Damage Event at Four Air Lock Doors of Unit 2 Containment Bldg IR 05000369/19970171997-12-0101 December 1997 Insp Repts 50-369/97-17 & 50-370/97-17 on 970921-1101.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20198N4701997-10-20020 October 1997 Notice of Violation from Insp on 970810-0920.Violation Noted:On 960420,ET Guidelines,Apps C & E Were Not Implemented as Evidenced By;Resolution Analyst Revised & Overruled Reexam Request for SG 2A Tube R7C60 IR 05000369/19970151997-10-20020 October 1997 Insp Repts 50-369/97-15 & 50-370/97-15 on 970810-0920. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support ML20212A0361997-10-0808 October 1997 Notice of Violation from Insp on 970712-0827.Violation Noted:As of 970717,10 of 48 Ice Condenser Inlet Doors on Unit 2 Required Initial Opening Torque in Ixcess of 675 inch-pound Operability Limit ML20211K9431997-09-26026 September 1997 Notice of Violation from Insp on 970721-26.Violation Noted: Licensee Failed to Follow Procedures for Security Badges & Access Control of Facility IR 05000369/19970121997-09-22022 September 1997 Insp Repts 50-369/97-12 & 50-370/97-12 on 970804-08.No Violations Noted.Major Areas Inspected:Observation & Evaluation of Biennial Emergency Preparedness Exercise IR 05000369/19970101997-09-0808 September 1997 Insp Repts 50-369/97-10 & 50-370/97-10 on 970629-0809.No Violations Noted.Major Areas Inspected:Operations, Engineering,Maint & Plant Support IR 05000369/19973001997-08-29029 August 1997 NRC Operator Licensing Exam Repts 50-369/97-300 & 50-370/97-300 (Including Completed & Graded Tests) for Test Administered on 970728-31.Exam Results:Five SRO & One RO Passed Exam & One SRO Failed Exam ML20217R1161997-08-18018 August 1997 EN-97-076:on 970818,order Prohibiting Involvement in NRC- Licensed Activities for a Period of One Year Will Be Issued. Action Based on Investigation Conducted by Oi,Which Determined Falsification of QA Document PNO-II-97-051, on 970906,McGuire Units 1 & 2 Automatically Tripped.Porvs Utilized Until Steam Dumps Could Be Made Available.Steam Relieved Through Main Steam PORVs Until Power to Bus Kxa Restored & MSIVs Reopened1997-08-0909 August 1997 PNO-II-97-051:on 970906,McGuire Units 1 & 2 Automatically Tripped.Porvs Utilized Until Steam Dumps Could Be Made Available.Steam Relieved Through Main Steam PORVs Until Power to Bus Kxa Restored & MSIVs Reopened IR 05000369/19970091997-07-28028 July 1997 Insp Repts 50-369/97-09 & 50-370/97-09 on 970518-0628. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support ML20149L5701997-07-28028 July 1997 Notice of Violation from Insp on 970518-0628.Violation Noted:Procedure IP/0/A/3250/12B Inadequate to Provide Sufficient Guidance to Properly Test Emergency Diesel Generator Sequencer Logic Circuitry ML20149G6771997-06-16016 June 1997 Notice of Violation from Insp on 970406-0517.Violation Noted:Procedure PT/1/A/4600/014D Was Inadequate in Providing Sufficient Guidance to Bypass Properly RPS Functions of an Inoperable N-41 Channel to Permit Testing of Channel N-42 ML20149G6881997-06-16016 June 1997 Insp Repts 50-369/97-08 & 50-370/97-08 on 970406-0517. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support IR 05000369/19970071997-06-0202 June 1997 Insp Rept 50-369/97-07 on 970406-0503.Violations Noted.Major Areas Inspected:Sg Replacement Project Activities in Areas of Maint & Engineering IR 05000369/19970041997-05-0505 May 1997 Insp Repts 50-369/97-04 & 50-370/97-04 on 970223-0405. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support ML20148B9621997-05-0505 May 1997 Notice of Violation from Insp on 970223-0405.Violation Noted:Prior to 961130,activities Affecting Quality,Not Accomplished in Accordance W/Instructions,Procedures or Drawings IR 05000369/19970051997-04-28028 April 1997 Insp Rept 50-369/97-05 on 970309-0405.No Violations Noted. Major Areas Inspected:Maint,Engineering & Plant Support IR 05000369/19970991997-04-18018 April 1997 SALP Repts 50-369/97-99 & 50-370/97-99 for Period 950813-970308 IR 05000369/19970031997-04-0101 April 1997 Insp Rept 50-369/97-03 on 970125-0308.No Violations Noted. Major Areas Inspected:Sg Replacement Project Preoutage Activities in Areas of Maint,Engineering & Plant Support ML20137V1381997-03-24024 March 1997 Notice of Violation from Insp on 970112-0222.Violation Noted:Licensee Failed to Implement Appropriate Emergency Procedures,Conduct Required Drills or Renew Exemptions to Be Excluded from Stated Requirements ML20137V1531997-03-24024 March 1997 Insp Repts 50-369/97-01 & 50-370/97-01 on 970112-0222. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support 1999-08-26 |
See also: IR 05000821/2009020
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ENCLOSURE 1
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1
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Duke Power Company
Docket Nos. 50-369 & 50-370
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McGuire Nuclear Station
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The following violations were identified during an inspection conducted on
August 21 - September 20, 1985.
The Severity levels are assigned in accordance
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with the NRC Enforcement Policy (10 CFR Part 2, Appendix C).
1.
Technical Specification 3.8.1.1 states that with one diesel generator
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inoperable, all systems, subsystems, trains, components and devices that
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depend upon the remaining operable diesel generator as a source of emergency
power must also be operable for that train to be operable and states that if
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two trains are inoperable for two hours, the unit must be in at least hot
standby within the next six hours and cold shutdown within the following 30
hours.
Technical Specification 3.4.3 requires for a pressurizer to be operable,
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that at least two groups of pressurizer heaters be operable each having a
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capacity of at least 150 KW.
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Contrary to the above, on September 11, 1985, two trains of pressurizer
heaters with their required emergency power supplies were not available from
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9:50 a.m. until 7:33 p.m. on September 11, 1985.
This is a Severity Level IV violation (Supplement I) applicable to Unit 1.
2.
Technical Specification 6.8.1 requires that current written approved
procedures be established implemented and maintained covering shift relief,
turnover and maintenance of minimum shift complement.
Contrary to the above, on September 6,1985, at 3:00 p.m.,
none of the
Senior Reactor Operators (SRO) designated on the shift supervisor's turnover
checklist as being required to be in the control room at the time were
present. A non-designated SR0 was present in the control room.
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This is a Severity level IV violation (Supplement I), applicable to Units 1
and 2.
8511040256 851021
ADOCK 05000369
DCT E l 1985
8
Date:
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