ML20236E644
| ML20236E644 | |
| Person / Time | |
|---|---|
| Site: | McGuire, Mcguire |
| Issue date: | 07/17/1989 |
| From: | Reyes L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML20236E641 | List: |
| References | |
| 50-369-89-14, 50-370-89-14, NUDOCS 8907270262 | |
| Download: ML20236E644 (2) | |
Text
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ENCLOSURE 1 NOTICE OF VIOLATION Duke Power Company Docket Nos. 50-369 and 50-370 McGuire Units 1 and 2 License Nos. NPF-9 and NPF-17 During the Nuclear Regulatory Comission (NRC) inspection conducted on April 22, 1989 through June 1,1989, a violation of NRC requirements was identified.
In accordance with the " General Statement of Policy and Procedure for NRC and Enforcement Actions," 10 CFR Part 2, Appendix C (1988), the violation is identified below:
j Technical Specification 6.8.1 requires that written procedures be established, implemented, and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.
Regulatory Guide 1.33, Revision 2, February 1978, Appendix A, requires that procedures be written and implemented for surveillance tests.
McGuire Procedures PT/1 and 2/A/425503A and B, SM Valve Stroke Timing (Shutdown), contain instructions for testing the Main Steam Isolation Valves.
The valves are required to close within 5 seconds without air assist per the Final Safety Analysis Report, Section 10.3.2.
Contrary to the above, McGuire procedures PT/1 and 2/A/4255/03A and 03B were inadequate in that they specified testing of the Main Steam Isolation Valves with air assist contrary to the assumed conditions in the final safety analysis report.
This is a Severity Level IV (Supplement I) violation.
Pursuant to the provisions of 10 CFR 2.201, Duke Power Company is hereby required to submit a written statement or explanation to the U.S. Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, DC 20555 with a copy to the Regional Administrator, Region II, and a copy to the NRC Resident l
Inspector, McGuire Nuclear Station within 30 days of the date of the letter transmitting this Notice. This reply should be clearly marked as a " Reply to a Notice of Violation" and should include for each violation: (1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved.
Where good cause is shown,
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Duke Power Company 4
Docket Nos. 50-369 and 50-370 McGuire Units 1 and 2 License Nos. NPF-9 and NPF-17 consideration will be given to extending the response time.
If an adequate reply is not received within the time specified in this Notice, an order may be issued to show cause why the license should not be modified, suspended or revoked or why such other action as may be proper should not be taken.
FOR THE NUCLEAR GULATORY COMMISSION
/
uis A. Reyes, D' e or Division of Reac Projects Dated at Atlanta, Georgia this/f ^ day of July 1989 l
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