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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P6171999-10-21021 October 1999 Forwards non-proprietary & Proprietary Versions of HI-982083, Licensing Rept for Byron & Braidwood Nuclear Stations. Proprietary Rept Withheld,Per 10CFR2.790(b)(4) ML20217M4361999-10-19019 October 1999 Forwards Rev 46 to Braidwood Station Security Plan, IAW 10CFR50.4(b)(4).Description of Changes,Listed.Encl Withheld Per 10CFR73.21 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20217G9791999-10-14014 October 1999 Forwards SE Accepting Relief Requests to Rev 5 of First 10-year Interval Inservice Insp Program for Plant,Units 1 & 2 ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20217A9311999-09-29029 September 1999 Informs That NRC 6-month Review of Braidwood Identified That Performance in Maint Area Warranted Increased NRC Attention. Addl Insps Beyond Core Insp Program Will Be Conducted Over Next 6 Months to Better Understand Causes of Problem ML20216H4301999-09-23023 September 1999 Informs That Arrangements Made for Administration of Licensing re-take Exams at Braidwood Generating Station for Week of 991108 ML20216F7441999-09-17017 September 1999 Forwards Insp Repts 50-456/99-13 & 50-457/99-13 on 990706-0824.Three Violations Noted & Being Treated as Ncvs. Insp Focused on C/As & Activities Addressing Technical Concerns Identified During Design Insp Completed on 980424 ML20212A6991999-09-10010 September 1999 Forwards SE Accepting Licensee Second 10-year Interval ISI Program Request for Relief 12R-07 for Plant,Units 1 & 2 ML20211Q9011999-09-0808 September 1999 Advises That Us Postal Service Mailing Address Has Changed for Braidwood Station.New Address Listed ML20211Q6611999-09-0606 September 1999 Informs That NRC Tentatively Scheduled Initial Licensing Exam for Braidwood Operator License Applicants During Wk of 010115 & 22.Validation of Exam Will Occur at Station During Wk of 001218 ML20211P1901999-09-0303 September 1999 Forwards Insp Repts 50-456/99-12 & 50-457/99-12 on 990707-0816.No Violations Noted.Insp Generally Characterized by safety-conscious Operations,Sound Engineering & Maint Practices & Careful Radiological Work Controls ML20211P1761999-09-0202 September 1999 Discusses Licensee Aug 1998 Rev 3K to Portions of Braidwood Nuclear Power Station Generating Stations Emergency Plan Site Annex Submitted Under Provisions of 10CFR50.54(q). NRC Approval Not Required ML20211K1081999-09-0202 September 1999 Responds to Request for Addl Info to GL 92-01,Rev 1,Suppl 1, Reactor Vessel Structural Integrity, for Braidwood,Units 1 & 2 & Byron,Unit 2 ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) ML20211B8691999-08-20020 August 1999 Forwards Insp Repts 50-254/99-10,50-265/99-10,50-454/99-09, 50-455/99-09,50-456/99-10 & 50-457/99-10 on 990628-0721. Action Plans Developed to Address Configuration Control Weaknesses Not Totally Effective as Listed BW990053, Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 21999-08-13013 August 1999 Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 2 BW990052, Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station1999-08-12012 August 1999 Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes ML20210U8031999-08-0404 August 1999 Forwards SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval for Second 10-year Inservice Testing Program BW990049, Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle1999-08-0404 August 1999 Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210K9761999-07-30030 July 1999 Forwards SE Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design Basis Capability of Safety-Related Movs, for Plant ML20210K0771999-07-30030 July 1999 Submits 30-day Rept Re Discovery of ECCS Evaluation Model Error for Byron & Braidwood Stations,As Required by 10CFR50.46 ML20210G6291999-07-29029 July 1999 Forwards Insp Repts 50-456/99-11 & 50-457/99-11 on 990525-0706.Two Violations Noted & Being Treated as NCV, Consistent with App C of Enforcement Policy ML20210J8951999-07-29029 July 1999 Submits Other Actions,As Described,To Be Taken for Valves to Resolve Potential Pressure Locking Concerns,In Light of Extended Period for Valve Bonnet Natural Depressurization,In Response to GL 95-07, Pressure Locking & Thermal.. BW990045, Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr1999-07-28028 July 1999 Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr ML20216D3781999-07-21021 July 1999 Forwards Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR on ITS Format & W(Z) Function, to Account for Error That W Discovered in Computer Code Used to Calculate PCT During LBLOCA ML20210C3961999-07-20020 July 1999 Forwards Insp Repts 50-456/99-09 & 50-457/99-09 on 990517-0623.No Violations Noted.Weakness Identified on 990523,when Station Supervisors Identified Individual Sleeping in Cable Tray in RCA ML20216D7061999-07-19019 July 1999 Forwards Rev 45 to Braidwood Station Security Plan,Iaw 10CFR50.4(b)(4).Plan Includes Listed Changes.Rev Withheld, Per 10CFR73.21 ML20210B7071999-07-16016 July 1999 Responds to Requesting Review & Approval of Three Proposed Changes to Ceco QA TR,CE-1A Per 10CFR50.54(a)(3) & 10CFR50.4(b)(7) BW990042, Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.71999-07-16016 July 1999 Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.7 ML20209H2991999-07-16016 July 1999 Withdraws 980529 LAR to Credit Automatic PORV Operation for Mitigation of Inadvertent Safety Injection at Power Accident.Response to NRC 990513 RAI Re LAR Encl IR 05000456/19993011999-07-15015 July 1999 Forwards Operator Licensing Exam Repts 50-456/99-301OL & 50-457/99-301OL for Test Administered from 990607-11 to Applicants for Operating Licenses.Three Out of Four Applicants Passed Exams BW990040, Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted1999-07-15015 July 1999 Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted ML20209H5141999-07-14014 July 1999 Discusses 990701 Telcon Re Arrangements for NRC to Inspect Licensed Operator Requalification Program at Braidwood Nuclear Generating Station for Week of 990927,which Coincides with Licensee Regularly Scheduled Exam Cycle ML20207H7501999-07-12012 July 1999 Forwards Revised Pressure Temp Limits Rept, for Byron Station,Units 1 & 2.Revised Pressurized Thermal Shock Evaluations,Surveillance Capsule Rept & Credibility Repts, Also Encl ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes ML20196H0631999-06-28028 June 1999 Provides Individual Exam Results for Licensee Applicants Who Took June 1999 Initial License Exam.Without Encls ML20212H8241999-06-24024 June 1999 Informs That Effective 990531 NRC Project Mgt Responsibility for Byron & Braidwood Stations Was Transferred to Gf Dick ML20196D4591999-06-18018 June 1999 Forwards Insp Repts 50-456/99-07 & 50-457/99-07 on 990414- 0524.No Violations Noted.Conduct of Activities Generally Characterized by safety-conscious Operations,Sound Engineering & Maintenance Practices ML20196A6671999-06-17017 June 1999 Refers to 990609 Meeting with Util in Braidwood,Il Re Licensee Initiatives in Risk Area & to Establish Dialog Between SRAs & Licensee PRA Staff 05000457/LER-1998-003, Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below1999-06-16016 June 1999 Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below 05000456/LER-1998-004, Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations1999-06-16016 June 1999 Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations 05000456/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed1999-06-15015 June 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed ML20195J3741999-06-14014 June 1999 Forwards Insp Rept 50-457/99-08 on 990415-0518.No Violations Noted.Sg Insp Program Found to Be Thorough & Conservative BW990028, Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.51999-06-10010 June 1999 Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.5 ML20195F3231999-06-0909 June 1999 Informs That in ,Arrangements Finalized for Exam to Be Administered at Plant During Wk of 990607.All Parts of Plant Initial Licensed Operator Exam Approved for Administration 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217P6171999-10-21021 October 1999 Forwards non-proprietary & Proprietary Versions of HI-982083, Licensing Rept for Byron & Braidwood Nuclear Stations. Proprietary Rept Withheld,Per 10CFR2.790(b)(4) ML20217M4361999-10-19019 October 1999 Forwards Rev 46 to Braidwood Station Security Plan, IAW 10CFR50.4(b)(4).Description of Changes,Listed.Encl Withheld Per 10CFR73.21 ML20217H4661999-10-18018 October 1999 Forwards Changes to EPIPs IAW 10CFR50.54(q) & 10CFR50,App E, Section V.Details of Changes Encl ML20216J8241999-09-30030 September 1999 Notifies of Removal of NRC Headquarters & Region III Offices from Controlled Copy Distribution of Certain CE Documents. Specific Documents,Associated Controlled Copy Numbers & NRC Location Affected Are Shown on Attachment to Ltr ML20211Q9011999-09-0808 September 1999 Advises That Us Postal Service Mailing Address Has Changed for Braidwood Station.New Address Listed ML20211G1221999-08-27027 August 1999 Forwards fitness-for-duty Program Performance Data for Each of Comm Ed Nuclear Power Stations & Corporate Support Employees within Scope of Rule for six-month Period Ending 990630,IAW 10CFR26.71(d) BW990053, Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 21999-08-13013 August 1999 Forwards post-outage Summary Rept for ISI Examinations Conducted During Seventh Refueling Outage of Braidwood Station,Unit 2 BW990052, Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station1999-08-12012 August 1999 Informs That RW Clay,License OP-31044,no Longer Requires Operator License at Braidwood Station ML20210N5651999-08-0606 August 1999 Forwards Rev 8 to Nuclear Generating Stations Emergency Plan, for Plants.With Summary of Changes BW990049, Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle1999-08-0404 August 1999 Informs NRC of Plans to Demonstrate Compliance with 10CFR50.46 Requirements for Fuel Predicted to Experience Fuel Pellet to Rod Cladding Gap Reopening,During Current Cycle ML20210M9131999-08-0202 August 1999 Forwards Response to NRC AL 99-02, Operating Reactor Licensing Action Estimates, for Fys 2000 & 2001 for Comed ML20210K0771999-07-30030 July 1999 Submits 30-day Rept Re Discovery of ECCS Evaluation Model Error for Byron & Braidwood Stations,As Required by 10CFR50.46 ML20210J8951999-07-29029 July 1999 Submits Other Actions,As Described,To Be Taken for Valves to Resolve Potential Pressure Locking Concerns,In Light of Extended Period for Valve Bonnet Natural Depressurization,In Response to GL 95-07, Pressure Locking & Thermal.. BW990045, Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr1999-07-28028 July 1999 Forwards Errata to 1998 Radioactive Effluent Release Rept. Info Has Been Corrected & Revised Spreadsheets Included in Attachment to Ltr ML20216D3781999-07-21021 July 1999 Forwards Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR on ITS Format & W(Z) Function, to Account for Error That W Discovered in Computer Code Used to Calculate PCT During LBLOCA ML20216D7061999-07-19019 July 1999 Forwards Rev 45 to Braidwood Station Security Plan,Iaw 10CFR50.4(b)(4).Plan Includes Listed Changes.Rev Withheld, Per 10CFR73.21 BW990042, Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.71999-07-16016 July 1999 Forwards Braidwood Station,Unit 1 Post Accident Monitoring Rept for Reactor Vessel Level Indication Sys (Rvlis),Due to Facility Train B RVLIS Being Restored to Operable Status After 7-day Completion Time,Per TS 3.3.3 & 5.6.7 ML20209H2991999-07-16016 July 1999 Withdraws 980529 LAR to Credit Automatic PORV Operation for Mitigation of Inadvertent Safety Injection at Power Accident.Response to NRC 990513 RAI Re LAR Encl BW990040, Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted1999-07-15015 July 1999 Forwards Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2.Since Issuance of Rept,It Was Determined That Rt That Occurred on Unit 2 During Startup Was Inadvertently Omitted ML20207H7501999-07-12012 July 1999 Forwards Revised Pressure Temp Limits Rept, for Byron Station,Units 1 & 2.Revised Pressurized Thermal Shock Evaluations,Surveillance Capsule Rept & Credibility Repts, Also Encl ML20196J9061999-07-0101 July 1999 Provides Evidence That Util Maintains Guarantee of Payment of Deferred Premiums in Amount of $10 Million for Each of Thirteen Reactors,Per 10CFR140.21 ML20196J9131999-07-0101 July 1999 Submits Status of Nuclear Property Insurance Currently Maintained for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR50.54(w)(3) ML20209B8241999-06-30030 June 1999 Forwards Five 3.5 Inch Computer Diskettes Containing Revised Annual Dose Repts for 1994 Through 1998 for Individuals Receiving Neutron Dose Not Previously Included in Reported Total Effective Dose Equivalent Values.Without Diskettes 05000457/LER-1998-003, Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below1999-06-16016 June 1999 Forwards LER 98-003-00 Re Unit 2 Reactor Trip.Actions & Associated Action Tracking Number That Braidwood Station Is Committed to Implement in Response to LER Described Below 05000456/LER-1998-004, Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations1999-06-16016 June 1999 Forwards LER 98-004-01,IAW 10CFR50.73(a)(2)(i)(B). LER 98-004 Included Commitment to Transmit Supplemental Rept by 990628,due to on-going Evaluations 05000456/LER-1999-001, Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed1999-06-15015 June 1999 Forwards LER 99-001-00,IAW 10CFR50.73(a)(2)(i)(B). Description of Action & Associated Action Request Number That Braidwood Station Is Committed to Implement Is Response to LER Is Listed BW990028, Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.51999-06-10010 June 1999 Forwards Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function, IAW TS 5.6.5 ML20195E3451999-06-0707 June 1999 Forwards 3.5 Inch Computer Diskette Containing Revised File Format for Annual Dose Rept for 1998,per 990520 Telcon Request from Nrc.Each Station Data Is Preceded by Header Record,Which Provides Info Necessary to Identify Data ML20195D6351999-06-0404 June 1999 Notifies NRC of Actions That Has Been Taken in Accordance with 10CFR26, Fitness for Duty Programs 05000457/LER-1999-002, Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Listed1999-05-21021 May 1999 Forwards LER 99-002-00,IAW 10CFR50.73(a)(2)(iv).Commitments Made by Util Are Listed ML20195B2301999-05-19019 May 1999 Requests Approval of Proposed Changes to QA Topical Rept CE-1-A,rev 66a.Attachment a Describes Changes,Reason for Change & Basis for Concluding That Revised QAP Incorporating Proposed Changes Continues to Satisfy 10CFR50AppB ML20206T3351999-05-17017 May 1999 Provides Written follow-up of Request for NOED Re Extension of Shutdown Requirement of TS Limiting Condition for Operation 3.0.3.Page 9 of 9 of Incoming Submittal Not Included ML20206N7861999-05-14014 May 1999 Forwards 1998 Annual Radiological Environ Operating Rept for Braidwood Station. Rept Contains Info Associated with Stations Radiological Environ & Meteorological Monitoring Programs ML20206Q8521999-05-13013 May 1999 Submits Rept on Numbers of Tubes Plugged or Repaired During SG Inservice Insp Activities Conducted During Plant Seventh Refueling outage,A2R07,per TS 5.6.9 ML20210C7221999-05-0303 May 1999 Forwards Initial License Exam Matls for Review & Approval. Exam Scheduled for Wk of 990607 ML20206F5381999-04-30030 April 1999 Forwards Magnetic Tape Containing Annual Dose Repts for 1998 for Braidwood,Byron,Dresden,Lasalle County,Quad Cities & Zion Nuclear Power Stations,Per 10CFR20.2206(c).Without Magnetic Tape ML20206E3991999-04-29029 April 1999 Forwards 1998 Annual Environ Operating Rept & Listed Attachments Included in Rept.Without Encls ML20206C7901999-04-23023 April 1999 Provides Suppl Info Re Use of W Dynamic Rod Worth Measurement Technique,As Requested During 990413 Telcon.Rev Bars in right-hand Margin Identify Changes from Info Submitted by ML20206B3941999-04-21021 April 1999 Forwards Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors, for Byron & Braidwood Stations.Updated Info Re PCT for Limiting Small Break & Large Break LOCA Analysis Evaluations & Detailed Description of Errors ML20205S9621999-04-20020 April 1999 Responds to 981203 RAI Telcon Re SG Tube Rupture Analysis for Byron Station,Unit 2 & Braidwood Station,Unit 2.Addl Info & Subsequent Resolution of Issues Discussed During 990211 Telcon Are Documented in Encl ML20206B0821999-04-20020 April 1999 Requests to Reschedule Breaker Maint Insp for Either Wk of 990607 or One of Last Two Wks in Jul 1999,in Order to Better Accommodate Insp Activity ML20206B2471999-04-20020 April 1999 Informs That SE Kuczynski Has Been Transferred to Position No Longer Requiring SRO License.Cancel License SOP-31030-1, Effective 990412 ML20206B0251999-04-14014 April 1999 Forwards Reg Guide 1.16 Rept for Number of Personnel & Person-Rem by Work Job Function for 1998. Associated Collective Deep Dose Equivalent Reported According to Work & Job Functions ML20205K3581999-04-0606 April 1999 Submits Request to Reschedule Breaker Maint Insp for Braidwood Nuclear Power Station for Either Wk of 990607 or One of Last Two Wks in Jul 1999 ML20205K5841999-03-31031 March 1999 Submits Rept on Status of Decommissioning Funding for Reactors Owned by Comm Ed.Attachment 1 Contains Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML20210C7181999-03-30030 March 1999 Forwards Integrated Exam Outline Which Plant Submitting for Review,Comment & Approval for Initial License Exam Scheduled for Wk of 990607 ML20205E6401999-03-26026 March 1999 Forwards Proprietary Ltr Re Notification of Corrected Dose Rept for One Individual,Per 1997 Annual Dose Repts for All Comed Nuclear Power Facilities,Submitted 970430.Proprietary Info Withheld ML20205B4241999-03-23023 March 1999 Provides Results of drive-in Drill Conducted on 990208,as Well as Augmentation Phone Drills Conducted Since 981015,as Committed to in Util ML20207J4321999-03-0808 March 1999 Forwards Braidwood Station ISI Outage Rept for A1R07, Per Requirements of ASME Section Xi,Article IWA-6200 ML20205C6861999-03-0404 March 1999 Provides Notification That Byron Station Implemented ITS on 990205 & Braidwood Station Implemented ITS on 990219 1999-09-08
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- 1 Commonwealth Edison n - Braidwood Nuclear Power Station h.N' % . lX.V g Braceville, Illinois 60407 Route #1, Box 84 g% g. gug - Telephone 815/458 2801
)
April 30, 1994 _
Mr. William Russell, Director Office of Nuclear Reactor Regulation I U.S. Nuclear Regulatory Commission I Washington, D.C. 20555 Attn: Document Control Desk
Subject:
Braidwood Station Unit 1 Supplemental Information to the Request for Emergency Technical Specification Amendment Facility Operating License: NPF-72 Technical Specification 3/4.4.5 i NRC Docket No 50-456
Reference:
- 1) D. Saccomando letter to W. Russell dated April 25, 1994, transmitting request for ;
Emergency Technical Specification Amendment for Specification 3/4.4.5 j i
- 2) Teleconference dated April 29, 1994, between the Nuclear Regulatory Commission and Commonwealth Edison Company (CECO)
- 3) NRC telecopy to CECO dated April 29, 1994, transmitting Questions in Response to Braidwood April 25, 1994 Submittal
- 4) Draft NUREG-1477, " Voltage-Based Interim Plugging for Steam Generator Tubes-Task Group Report," June 1, 1993 )
i
Dear Mr. Russell:
Reference 1 transmitted Ceco's request to process an Emergency l Technical Specification Amendment to Specification 3/4.4.5 for Braidwood Unit 1. The proposed amendment modifies the Technical '
Specification to incorporate a 1.0 volt steam generator tube interim plugging criteria (IPC) for Cycle 5.
Through numerous teleconferences with the Nuclear Regulatory Commission (NRC) Staff, both prior to and after submittal of the Emergency Amendment request, Braidwood became aware that the NRC Staff's review of the supporting analysis for the proposed Technical Specification would not be able to be expedited in a timely manner. The enclosed attachments provides information which should facilitate the approval of this amendment request on an interim basis until the Staff can complete a comprehensive review of the amendment request.
I 9405120232 940430 PDR ADOCK 05000456 .1' I P PDR -
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W. Russell April 30, 1994 ;
Attachment A addresses the use of Draft NUREG-1477, " Voltage-Based Interim Plugging for_ Steam Generator Tubes-Task Group Report" to determine steam line break leak rate analysis. This analysis shows that Braidwood Unit 1 can operate for approximately 3.4 Efiective Full Power Months if the allowable reactor coolant Dose Equivalent Iodine-131 concentration is.
reduced to 0.35 microcuries/ gram, t Attachment B contains Braidwood's revised Significant Hazards Consideration which incorporates the Draft NUREG-1477 steam line break leak rate analysis.
Attachment C provides Braidwood's response to question #3 which was transmitted in Reference 3. This attachment contains a discussion of Braidwood's steam generator tube leakage action plan.
Braidwood acknowledges that the proposed revision to the Technical Specification pages which were transmitted with Reference 1 will need to reflect the conditions addressed in this supplement. We propose the following footnote to Technical Specification 4.4.5.0 for your consideration.
"For Unit 1 Cycle 5,'the steam generators will be considered OPERABLE for the first' Effective Full Power Days of operation. During that time, reactor coolant DOSE EQUIVALENT I-131 will be limited to 0.35 microcuries per gram."
Braidwood recognizes that approval of the previously submitted IPC amendment for Unit 1 has been the subject of considerable discussion, and is aware that full resolution of this amendment '
request may not be immediately eminent. However, we do believe based upon our conversations with the Staff, the information provided in this supplement should help reconcile the approval of the amendment for a limited amount of time, thus facilitating the start-up of Unit 1. Further we believe that once the' Staff has had adequate time to review our previously submitted package they will approve the IPC amendment for the remainder of Unit 1 Cycle 5 operation. CECO appreciates the Staff's efforts in reviewing and approving this amendment request in an expeditious manner. !
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W. Russell April 30, 1994 Please address any comments or questions regarding this matter to this office.
Respectfully,
[ .,
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Denise M. Saccomando Nuclear Licensing Administrator Attachments cc: R. Assa, Braidwood Project Manager-NRR S. Dupont, Senior Resident Inspector-Braidwood -;
J. Martin, Regional Administrator-Region III '
Office of Nuclear Facility Safety-IDNS l
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ATTACHMENT A MAIN STEAM LINE BREAK LEAK RATE ANALYSIS Through numerous teleconferences with the Nuclear Regulatory Commission (NRC) Staff, Braidwood recognized that the Staff would not be able to approve the emergency amendment request for IPC within an expeditious time frame. To facilitate restart of_ Unit 1 it was agreed that Braidwood would. apply portions of Draft NUREG-1477, " Voltage-Based Interin Plugging Criteria for Steam Generator Tubes-Task Group Report," to determine the appropriate amount of time that Unit 1 could operate without exceeding the calculated primary-to-secondary leakage during main steam line break (MSLB) conditions.
Calculation of the leakage is based upon:
Use of NRC leak rate correlation database, This data base included data that CECO previously dispositioned as outlier data (V.C. Summer tube R28C41 with a leak rate of 2496 liters per hour).
Use of log-logistic method of analysis, and In discussions between CECO and the Staff during the Reference teleconference, it was mutually agreed that it was appropriate for CECO to apply the log-logistic analysis method.
Use of a Probability of Detection of 0.6.
POD that is recommended in the Draft NUREG-1477.
Based upon the above inputs, Braidwood calculated both beginning-of-cycle (BOC) and end-of-cycle (EOC) MSLB leak rates. The most limiting steam generators were determined to be "A" and "D".
SG "A" BOC SG "A" EOC SG "D" BOC SG "D" EOC 18.9 gpm 47.2 gpm 14.8 gpm 33.3 gpm l
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The current Technical Specification Dose Equivalent (DE) Iodine-131 (I-131) limit for. reactor coolant activity is 1.0 microcurie / gram. As previously stated in Reference 1, this activity limits the allowable primary-to-secondary leakage during a MSLB in the faulted steam generator to 9.1 gpm. This value ensures Titile 10, Code of. Federal Regulations, Part 100 (10 CFR 100) limits are not exceeded. Braidwood' determined that a reduction in the allowable DE I-131 activity to 0.35 microcuries/ gram would raise the allowable leakage rate to 26 gpm. Braidwood concluded that reduction in the' allowable DE I-131 activity to 0.35 microcuries/ gram is appropriate. This value will be controlled administratively and referenced in the Technical Specification.
Using the most limiting BOC leakrate value (SG "A"), a fuel. cycle length of 1.15 Effective Full Power Years, and a linear estimate of leakage increase throughout the cycle, Braidwood concluded that Unit 1 "A" steam generator could be operated for approximately 3.4 Effective Full Power Months before exceeding the 26 gpm limit.
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ATTACHMENT B EVALUATION OF SIGNIFICANT HAZARDS CONSIDERATIONS FOR PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSE NPF-72 Commonwealth Edison Company (CECO) has evaluated this proposed license amendment request and determined that it involves no significant hazards considerations. According to Title 10, Code of Federal Regulations, Part 50, Section 92, Paragraph c
[10 CFR 50. 92 (c) ] , a proposed amendment to an operating license involves no significant hazards considerations if operation of the facility in accordance with the proposed amendment would not:
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- l. Involve a significant increase in the probability or consequences of an accident previously evaluated; or
- 2. Create the possibility of a new or different kind of accident from any accident previously evaluated; or
- 3. Involve a significant reduction in a margin of safety.
During the Braidwood Unit 1 Cycle 4 Refuel Outage (AlR04) which began March 4, 1994, a steam generator (SG) tube inservice inspection was performed in accordance with Technical Specification Surveillance Requirement (TSSR) 4.4.5.0. The results of this inspection indicated that under the current :
technical specification acceptance criteria a total of 1423 SG tubes, of which 1390 are due to outside diameter stress corrosion :
cracking (ODSCC) at the tube support plates (TSPs), would have to be removed from service by plugging or repaired by sleeving. l Additionally, the distribution of these SG tubes would cause a j large disparity in the number of tubes removed from service l between SGs "B" and "C." This disparity between SGs "B" and "C" l would probably cause a noticeable reactor coolant system (RCS) l flow imbalance and result in potential RCS loop power asymmetries. Plugging of all tubes would require re-analysis since SG "C" would exceed the currently analyzed plugging limit.
Sleeving of even the minimum number of tubes necessary in SG "C" to conform with the current analysis would greatly increase the cost of SG repair and result in a significant ex+ ension of the
. outage critical path. This option would also limit the unit to approximately 90% of rated thermal power.
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9 CECO proposes to amend the following Braidwood Technical Specifications:
Specification 3.4.5 REACTOR COOLANT 3YSTEM-STEAM GENERATORS.-
Specification 3.4.6.2 REACTOR COOLANT SYSTEM-OPERATIONAL LEAKAGE This proposed license amendment request will modify Specification 3.4.5 to allow an eddy current bobbin coil probe voltage based SG' TSP interim plugging. criteria (IPC) to be applied for Braidwood Unit 1 Cycle 5.
This proposed license amendment request will also modify Specification 3.4.6.2 to reduce the allowable reactor-to-secondary leakage from 1 gallon per minute (gpm) total through all SGs and 500 gallons per day (gpd) through any one SG to 600 gpd total through all SGs and 150 gpd through any one SG.
Technical Specification Bases Sections 3/4.4.5, STEAM GENERATORS, and 3/4.4.6.2, OPERATIONAL LEAKAGE, will also be modified to reflect these changes, respectively.
4 With the implementation of this proposed license amendment request the Braidwood Unit 1 SGs will still satisfy the requirements of Regulatory Guide (RG) 1.121, " Basis for Plugging Degraded PWR Steam Generator Tubes," Revision 0, August 1976. ,
964 SG tubes will remain in service that would have otherwise been removed from service by plugging or repaired by sleeving due >
to ODSCC at the TSPs. This represents an approximate'$2.91M. cost savings in SG repairs alone. This will also minimize the RCS loop asymmetries and allow the unit to return to power operation at approximately rated thermal power. Additionally, implementation of this' proposed' license amendment request represents the avoidance of a minimum 18~ day critical path outage extension, and the associated replacement power costs. CECO believes this to be the quickest way to return Braidwood Unit 1 to power operation prior to the commencement of CECO's peak load j season, 1
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- 1. The proposed chango does not involvo a significant increaso l in the probability or consequences of an accident previously l ovaluated.
The proposed license amendment request to implement SG IPC for Braidwood Unit 1 Cycle 5 meets the requirements of RG 1.121 by demonstrating that tube leakage is acceptably low
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and tube burst is a highly improbable event during normal operation or a main steam line break (MSLB), event over the limited time period of this license amendment.
Under accident conditions, conservatively assuming MSLB, significant margins exist for free span burst considerations for voltage growth in excess.of 95% cumulative probability.
For the largest confirmed indications left in service, the projected voltage at 95% growth is 2.6 volts at the end-of-cycle (EOC) 5, compared to the 4.54 volts structural limit for a free span burst pressure of 1.43 times steam line break pressure differential. Even at 99% cumulative probability, the observed voltage growth is bounded by 2.7 volts and the structural limit is satisfied for the 1.0 volt rotating pancake coil (RPC) confirmed indications left in service.
In addition, the following analyses were done to provide assurance that there are additional margins provided by the following considerations:
A demonstration of limited TSP displacement was done which reduces the likelihood of a tube burst. Limited TSP displacement would also reduce leakage compared to free span indications.
The Electric Power Research Institute (EPRI)
Performance Demonstration Program analyzed the performance of some 20 eddy current data analysts evaluating data from a unit with 3/4" inside diameter and 0.049" wall thickness tubes. This data demonstrated the voltage dependence of the probability of detection (POD) and argues for a POD of greater than 0.6 for ODSCC indications larger than 1.0 volt.
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CECO's risk evaluation of the operability of Braidwood Unit 1 Cycle 5 compared core damage frequency, with containment bypass, with and without the IPC applied at Braidwood Unit 1. The total Braidwood core damage frequency is estimated ~to be 2.74E-5 per reactor year with a total contribution from containment bypass sequences of 2.9E-8 per reactor year in the current individual plant evaluation (IPE). Operation with the requested IPC resulted in an insignificant increase in the MSLB with containment bypass sequence frequency.
The analyses presented above applied to a full cycle of operation. 'Because plant operation approved by the proposed amendment would be for a significantly shorter period, the probability of an accident is much less than that calculated for a full cycle.
To support the restart and limited operation of Braidwood Unit 1, RCS Dose Equivalent (DE) Iodine 131 (I-131) will be limited to 0.35 microcuries per gram.
Therefore, since implementation of the 1.0 volt IPC for a limited time period for Braidwood Unit 1 Cycle 5 does not adversely affect SG tube integrity and results in acceptable dose consequences for a worst case postulated accident, the proposed license amendment request does not result in any increase in the probability or consequences of an accident previously evaluated within the Braidwood Updated Final ,
Safety Analysis Report.
- 2. The proposed change does not create the possibility of a now or difforent kind of accident from any accident previously evaluated.
The proposed SG tube IPC does not introduce any significant changes to the plant design basis. Use of the criteria does not provide a mechanism which could result in an accident outside the tube support plate elevations; no ODSCC is occurring outside the thickness of the tube support plates.
Neither a single or multiple tube rupture event would be e>:pected in a steam generator in which the IPC has been applied.
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CECO will implement a maximum leakage rate limit of 150 gpd through any_one SG to help preclude the potential for excessive leakage during all plant conditions. The RG 1.121 criterion for establishing operational leakage rate limits _that require plant shutdown are based upon leak-before-break considerations to detect a free. span crack before potential tube rupture during faulted plant conditions. The 150 gpd limit will provide for leakage I detection and plant shutdown in the event of the occurrence i of an unexpected single crack resulting in leakage that is associated with the-longest permissible free. span crack length. Since tube burst due to ODSCC is precluded during normal operation due to the proximity of the TSP-to the tube and the potential exists-for the crevice to become uncovered during MSLB conditions, the leakage from the maximum permissible crack must preclude tube burst at MSLB conditions. Thus, the 150 gpd limit provides for plant shutdown prior to reaching critical crack lengths for MSLB conditions.
- 3. The proposed change does not involve a significant reduction in a margin of safety. ,
Upon implementation of the RG 1.121 criteria, even under the worst case postulated accident conditions, the occurrence of '
ODSCC at the TSP elevations is not expected to lead to a steam generator tube rupture event during normal or faulted plant conditions. The distribution of crack indications at-the TSP elevations are confirmed to result in acceptable primary-to-secondary leakage during all plant conditions for the limited time period of this license amendment and_that radiological consequences are not adversely impacted.
Loss of Coolant Accident (LOCA) coincident with (+) a Safe Shutdown Earthquake (SSE) on the SG (as' required by GDC 2),
may cause a tube collapse in the SGs at some plants. A-number of tubes have been identified, in the " wedge" locations of the SG TSPs, to represent a potential for tube collapse _during a LOCA + SSE event. These tubes have been excluded from application of the voltage based SG TSP IPC.
Addressing RG 1.83, " Inservice Inspection of PWR Steam Generator Tubes," Revision 1, July 1975, considerations, implementation of the bobbin coil probe voltage based IPC of 1.0 volt is supplemented by: enhanced eddy current inspection guidelines _to provide consistency in voltag'e normalization, a 100% eddy current inspection sample size at the TSP elevations, and RPC inspection requirements for the larger indications left in service to characterize the principal degradation as ODSCC.
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l Implementation of.the SG TSP IPC will decrease the number of l tubes which must be repaired. Therefore, the margin of flow I that would otherwise be reduced in the event of increased !
tube plugging would be maintained.
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Therefore, based on the evaluation above, CECO has concluded that l this proposed license amendment request does not involve a significant hazards consideration.
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1 ATTACHMENT C RESPONSE TO NRC QUESTION 3 l FROM APRIL 29, 1994 TELECOPY Question 3. The application proposes that the 150 gpd leakago l limit be incorporated into TS, and that operator action be administratively required for a leak rato increase in a range of 25 to 100 gpd in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> (with an added condition of leakage abovo 50 gpd) . Explain this apparent change from the leak rate increase limit of 25 gpd por hr instituted in December 1993. ,
i Answer 3. During Braidwood Unit 1 Cycle 4, reactor coolant system (RCS) iodine activity was elevated due to leaking fuel.
In October 1993 when the leak occurred on the 1C Steam Generator (SG), Braidwood was able to detect a 25 gpd in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> change in leak rate because of the initial elevated RCS iodine activity levels.
After the IC SG tube leak event and in consultation with Commonwealth Edison's Byron and Zion Stations, the 50 gpd threshold was added. It was determined that during fuel cycles in which no leaking fuel is present, the RCS iodine activity will be less than that which was present during the 1C SG tube leak event. With less iodine activity, the ability to detect and accurately quantify a primary-to-secondary leak is reduced.
Although a leak rate of less than 50 gpd can be measured, the accurate repeatability of this leak rate determination will not be possible due to analytical limitations. Measured leak rate changes of greater than 25 gpd within one hour may be observed when the actual leak rate has not changed by 25 gpd if the leakage is less than 50 gpd. The 50 gpd threshold was based on no leaking fuel and the ability to accurately detect a 25 gpd change within one hour.
The administrative limits regarding changing leak rates are detailed in Braidwood Operating Abnormal Procedure (Bw0A) SEC-8, STEAM GENERATOR TUBE LEAK, and are summarized as follows:
If the leak rate is greater than 50 gpd and
- 1. it increases by greater than or equal to 25 gpd but less than 100 gpd in a one hour period, then the unit will be shut down within five hours; or l
- 2. it increases by greater than or equal to 100 gpd in a one !
hour period, then the unit will be shut down within four l hours. l l
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