Similar Documents at Cook |
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J4721999-10-15015 October 1999 Forwards NRC Physical Security Insp Repts 50-315/99-27 & 50-316/99-27 on 990920-24.Two Violations Noted & Being Treated as Ncvs,Consistent with App C of Enforcement Policy. Areas Examined Exempt from Disclosure,Per 10CFR73.21 IA-99-379, First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety1999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML20217D9241999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML20196K5961999-06-30030 June 1999 Ltr Contract:Task Order 40, DC Cook Extended Sys Regulatory Review Oversight Insp, Under Contract NRC-03-98-021 ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML20207A9201999-05-21021 May 1999 Ack Receipt of 990319 Response to Notice of Violation & Proposed Imposition of Civil Penalty .On 981124, Licensee Remitted Check for Payment of Civil Penalties. Licensee Requests for Extension for Response,Granted ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML20205P0591999-04-14014 April 1999 Ninth Partial Response to FOIA Request for Documents.App Records Already Available in Pdr.Records in App T Encl & Being Made Available in Pdr.App U Records Being Released in Part (Ref FOIA Exemption 7).App V Records Withheld Entirely ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed ML17325B5141999-03-30030 March 1999 Forwards Rept on Status of Decommissioning Funding.Attached Rept Includes Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML17325B5191999-03-29029 March 1999 Forwards LER 99-001-00,re Degraded Component Cw Flow to Containment Main Steam Line Penetrations.Commitment, Listed ML20204F6401999-03-19019 March 1999 Responds to NRC 981013 NOV & Proposed Imposition of Civil Penalty.Violations Cited in Subject NOV Were Initially Identified in Referenced Five Insp Repts.Corrective Actions: Ice Condensers Have Been Completely Thawed of Any Blockage ML17325B4751999-03-18018 March 1999 Forwards LER 99-004-00,re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitment Made by Util,Listed ML17325B4721999-03-18018 March 1999 Forwards LER 99-005-00,re Reactor Trip Breaker Manual Actuations During Rod Drop Testing Not Previously Reported. Listed Commitments Identified in Submittal ML17325B4641999-03-17017 March 1999 Withdraws Response to Issue 1 of NRC Cal,Dtd 970919. Comprehensive Design Review Effort in Progress to Validate Resolution of Issue for Future Operation 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML17328A4481990-09-21021 September 1990 Requests Withdrawal of Mode 6 Proposed Tech Spec Change Since Issue Currently Being Addressed by New STSs ML17328A4331990-08-27027 August 1990 Informs of Preliminary Assessment of 900713 Electrical Contact Accident at Facility.Investigation Concludes That No Safety Rules Violated ML17328A4001990-08-24024 August 1990 Responds to 900725 Ltr Re Commitments Made in Response to Generic Ltr 88-14 on Instrument Air Supply Problems Affecting safety-related Equipment.Simulator Training to Be Provided as Stated ML17334B3781990-08-24024 August 1990 Forwards Info to Certify Plant Simulator Facility.Results of Evaluation of Dual Unit Simulation Facilities Demonstrate That Plant Simulator Performance Compares Favorably W/Units ML17328A4231990-08-21021 August 1990 Forwards Under Separate Cover,Semiannual Radioactive Effluent Release Rept for Jan-June 1990 ML17328A3901990-08-17017 August 1990 Responds to NRC 900720 Ltr Re Violations Noted in Onsite Audit of Spds.Corrective Actions:Apparent Disparity in Selection of Reactor Trip & Sys Capacity or Anticipatory Values Rectified ML17328A3891990-08-15015 August 1990 Forwards Performance Data Sheets for Plant fitness-for-duty Program for Period Jan-June 1990,per 10CFR26.Encl Includes Statistics on Various Categories of Testing,Substances Tested for & cut-off Levels Used ML17328A3571990-08-0202 August 1990 Responds to Open Items in Safety Evaluation of Util Response to Unresolved Issues on post-fire Safe Shutdown Methodology. Open Items 1 & 21 Will Be Closed by Implementing Plant Procedures Providing Equivalent Degree of Protection ML17328A3431990-07-23023 July 1990 Requests Withdrawal of 890830 Proposed Tech Spec Changes Re Sections 3.0 & 4.0.Util Will Resubmit Generic Ltr 87-09 Recommended Improvement Items on Case by Case Basis ML17328A3421990-07-23023 July 1990 Provides Results of Offsite Dose Calculation for Reactor Coolant Pump Locked Rotor Event for Facility Cycle 8.Util Identified Previously Issued SERs Addressing Short Term Containment Analysis & LOCA Containment Integrity ML20055G7551990-07-18018 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-315/90-10 & 50-316/90-10.Corrective Actions:Required Review Performed & Updated Procedure 12 Mhp 5021.019.001 Revised & Issued ML17328A3191990-07-12012 July 1990 Responds to NRC 900601 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Electrical Testing Techniques Improved & Surveillance Procedures for Feedwater Pumps Will Be Rewritten ML17328A3181990-07-0909 July 1990 Responds to Generic Ltr 90-03,Suppl 1, Relaxation of Staff Position in Generic Ltr 83-28,Item 2.2,Part 2, 'Vendor Interface for Safety-Related Components.' Licensee Will Contact safety-related Vendors on Annual Basis ML17328A3111990-07-0303 July 1990 Provides Certification of Funding Plan for Decommissioning of Plant,Per 10CFR50.33 & 50.75 ML17328A2961990-06-25025 June 1990 Forwards Response to Generic Ltr 90-04 Re Closeout of Generic Safety Issues.Util Supports Concern & Desire to Close long-standing Generic Safety Issues ML17328A2921990-06-22022 June 1990 Forwards WCAP-12483, Analysis of Capsule U from American Electric Power Co DC Cook Unit 1 Reactor Vessel Radiation Surveillance Program. ML20044A3521990-06-22022 June 1990 Submits Info Re Sensitivity Study Performed on Number of Fuel Axial Intervals,Per Topical Rept, American Electric Power Reactor Core Thermal-Hydraulic Analysis Using Cobra III-C/MIT-2 Computer Code. ML17328A2821990-06-15015 June 1990 Submits Ltr Re Proposed Control Room Habitability Tech Spec Changes & Supporting Analyses,Per 900521 Discussion.Revised Calculations of Control Room Thyroid Doses Will Be Submitted within 60 Days of Receipt of Proposed Generic Ltr ML17328A2741990-06-12012 June 1990 Submits Followup,Per 900205 & 0308 Ltrs & Provides Update Re Inoperable Fire Barrier.Fire Seal Repaired & Restored to Operability on 900419 ML17328A2551990-06-0505 June 1990 Forwards Addl Info Re Util 900126 Revised Response to NRC Bulletin 88-002,per NRC 900509 Request ML17328A7361990-06-0101 June 1990 Forwards Addl Info Re 890825 & 1212 Applications for Amends to Licenses DPR-58 & DPR-74,per Request.Amends Make Changes to Administrative Controls ML17328A7331990-05-29029 May 1990 Forwards Nonproprietary WCAP-12577 & Proprietary WCAP-12576, Westinghouse Revised Thermal Design Procedure Instrument... Methodology for American Electric Power DC Cook Unit 2 Nuclear Power Station, Per 900419 Commitment ML17328A7321990-05-24024 May 1990 Responds to NRC Bulletin 90-001, Loss of Fill Oil in Transmitters Mfg by Rosemount. No Rosemount Model 1153 Series B or D or Model 1154 Transmitters Installed at Facility.Transmitters Purchased as commercial-grade Units ML17328A6991990-05-0909 May 1990 Provides Suppl to 900103 Response,Certifying That Fitness for Duty Program Implemented at Plant.Change Also Clarifies When More Stringent cut-off Levels Adopted at Plant Program Apply ML17328A7001990-05-0909 May 1990 Responds to NRC 900406 Ltr Re Inadequacies of Spds,Per Audit on 900221-22.Corrective Actions:Software Mod Will Prevent User from Accessing Displays Other than Iconic Displays from SPDS Dedicated Terminal ML17328A7071990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept Mar 1990 for Donald C Cook Nuclear Plant Unit 1 ML17328A7031990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept for Mar 1990 for DC Cook Nuclear Plant Unit 2 ML17328A6951990-04-30030 April 1990 Certifies That Training Programs for Initial Licensing & Requalification Training of Operators & Senior Operators at Plant Accredited by Inpo,Per Generic Ltr 87-07 ML17328A6861990-04-30030 April 1990 Forwards Annual Environ Operating Rept,Jan-Dec 1989, & DC Cook Nuclear Plant Units 1 & 2 Operational Radiological Environ Monitoring Program 1989 Rept Jan-Dec 1989. ML17328A6801990-04-23023 April 1990 Responds to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Study Planned to Evaluate Alternative Actions to Be Taken for Protecting RHR Pumps ML17328A6771990-04-23023 April 1990 Forwards DC Cook Nuclear Plant 1990 Annual Emergency Preparedness Exercise. Exercise Scope & Objectives & Detailed Scenario Documentation Encl ML17334B3641990-04-11011 April 1990 Responds to NRC 900301 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated ML17328A6601990-04-11011 April 1990 Forwards Updated QA Program Description for Cook Nuclear Plant, Incorporating Editorial,Organizational & Position Title Changes ML17328A6551990-04-0909 April 1990 Responds to NRC 900309 Ltr Re Violations Noted in Insp Rept 50-316/90-08.Corrective Actions:Procedure for Steam Generator Stop Valve Operability Test Revised to Require That MSIV Be Declared Inoperable After Failing Stroke Test ML17334B3601990-04-0606 April 1990 Forwards Revised Figures for Loss of Load Event Previously Submitted in Attachment 4,App B of Vantage 5 Reload Transition Safety Rept Supplied by Westinghouse in Jan 1990. Update Is Editorial in Nature ML17334B3621990-04-0606 April 1990 Forwards 1989 Annual Rept & Projected Cash Flow ML17328A6341990-03-30030 March 1990 Forwards Application for Renewal of Plant NPDES Permit,For Info,Per Section 3.2 of App B to Plant Tech Specs.W/O Encl ML17328A6331990-03-30030 March 1990 Responds to NUMARC 900104 Request for Addl Info Re Station Blackout Submittals.Target Reliability for Emergency Diesel Generator of 0.0975 Established for 4 H ac-independent Coping Category Will Be Maintained ML17328A6321990-03-30030 March 1990 Forwards Response to Generic Ltr 90-01, NRC Regulatory Impact Survey. Util Ack Recommendation by NUMARC ML17328A6221990-03-27027 March 1990 Responds to 900226 Ltr Transmitting Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000. Corrective Actions:Flow Retention Circuitry Setpoints Set to Compensate for Missized Process Flow Orifice ML17328A6191990-03-27027 March 1990 Forwards Payment in Amount of $75,000 for Civil Penalty Imposed Through Notice of Violation Issued in Insp Rept 50-316/89-02 on 891016-20,24-26 & 1204.Response to Violation & Corrective Actions Provided in Separate Submittal ML17328A6161990-03-20020 March 1990 Responds to Generic Ltr 89-19 Re Safety Implications of Control Sys in LWRs (USI A-47).Both Units Have Steam Overfill Protection Sys That Would Automatically Prevent Water Carryover Into Steam Lines If Control Sys Failed ML17328A6121990-03-13013 March 1990 Forwards Monthly Performance Monitoring Rept,Jan 1990. ML17325B3901990-03-0606 March 1990 Forwards Annual Rept to NRC Per 10CFR50.54(W)(2) Re Nuclear Property Insurance ML17325B3921990-03-0606 March 1990 Modifies Application for Amend to License DPR-74 Re Cycle 8, Per 900228 Telcon ML17325B3781990-02-28028 February 1990 Forwards Response to NRC Info Notice 89-056 Re Questionable Certification of Matl Supplied to Dod by Nuclear Suppliers. Matl Capable of Performing Design Function & Acceptable for Continued Use ML17328A5971990-02-27027 February 1990 Withdraws 890203 Application for Amend to License DPR-74, Modifying Tech Spec Table 3.2-1 Re DNB Parameters to Express RCS Flow Rate on Volumetric Rather than Mass Basis ML17334B3511990-02-22022 February 1990 Submits Annual Rept of Changes to or Errors in Acceptable LOCA Evaluation Models or Application of Models for Plants. Wflash Analyses Will Be Superceded by Notrump Analyses for Unit 2,Cycle 8 Reload ML17328A5881990-02-21021 February 1990 Responds to NRC 890914 Request for Addl Info Re Safe Shutdown Methodology.App R Fire Barriers Being Maintained & Surveilled Under 3/4.7.10 for Units 1 & 2 ML17328A5861990-02-16016 February 1990 Provides Revised Comments in Response to NRR Comments During 891213 Telcon Re Allowable Stresses for Piping & Piping Supports 1990-09-21
[Table view] |
Text
'er-'"
INDIANA II MICHIGAN P WER COMPANY P. O. BOX 18 BOWLING GREEN STATION NEW YORK, N. Y. 10004 July 25, 1979 AEP: NRC: 001858 Donald C. Cook Nuclear Plant Units 1 8 2 Docket Nos. 50-315 and 50-316 License Nos. DPR-58 and DPR-74 Mr. James G. Keppler, Regional Director U. S. Nuclear Regulatory Commission Office of Inspection and Enforcement Region III 799 Roosevelt Road Glen Ellyn, Illinois 60137
Dear Mr. Keppler:
This letter supplements our letter of May 1, 1979 (AEP:NRC:00185) in response to, IE Bulletin 79-06A, Revision l. On June 20, 1979 we received, by telecopy, a request for additional information as a result of the NRC Staff review of our May 1, 1979 response. The attachment to this letter contains our responses to the requests resulting from your evaluation of our May 1, 1979 submittal. In a phone conversation held Friday, June 22, 1979 with members of the NRC Staff in Bethesda, Md., we were requested to supply responses to some parts of Action Items 4, 7, 8, and 10 before Unit 2 would be allowed to return to power. We provided you with our responses to those action items in our June 25, 1979 letter.
These responses are included again, with minor corrections, in the attachment:to this letter.
Please note that we are members of a Westinghouse Owner's Group on the Three Mile Island Accident formed at the recoiimtendation of the Comission. Active discussions are now taking place between the Group, Westinghouse, and the NRC, where some of the issues contained in your requests are being evaluated. We therefore reserve the right to modify our responses, actions or commitments once a final position is reached.
Very truly yours, JED/emc ohn . Dolan Attachment ice President Sworn ~a d subscribed to before me this+~day of July, 1979 in York County, York New New
~908S@~p(rr Notary Publ c GREGORY M. GURICAH Notary Public, State of New York Hp. 314643431 Ouallficd in New York Countyo Commission Expires March 30. 19'
Mr. J. G. Keppler AEP: NRC: 001858 cc: R. C. Callen G. Charnoff R. M. Jurgensen R. S. Hunter D. V. Shaller - Bridgman S. A. Varga - NRC N. C. Moseley - NRC
ATTACHMENT ACTION ITEN 2:
Listed below is instrumentation which could be used, under certain circumstances, to recognize void formation in the Reactor Coolant System (RCS):
A) Pressurizer Pressure B) Core Outlet Temperature
- 1) incore thermocouples
- 2) wide range hot leg temperatures C) Pressurizer Level D) Nuclear Instrumentation Pressurizer pressure and core outlet temperature would primarily be used to verify subcooled liquid in the RCS. Pressurizer level would be used to verify adequate coolant inventory. Large sudden changes in these parameters might provide indication of potential or actual voiding in the RCS. Data has been collected from the in-core neutron flux system corresponding to many reactor conditions. This data could be used as a basis of comparison'ith the signals obtained from a core where local bubbles or voids existed.
Operators are instructed to keep system pressure greater than the saturation pressure corresponding to the highest indicated temperature under forced and natural circulation modes. This can be accomplished by increasing pressure or decreasing temperature. One method of control will be by increasing pressure with the pressurizer heaters, if available, or system cooldown by steam release from the Steam Generators.
If a voiding condition develops anyway, there are modes of operation which can be used to remove the void. Our response to Action Item 12, con-cerning hydrogen removal from the RCS describes these modes of operation and the circumstances under which they would be employed.
Part of the Westinghouse Owners'roup scope includes preparation of generic emergency instructions for natural circulation. These instructions are expected to be available by September 1, 1979. Subsequent to their receipt we will write and issue a new operating procedure whose purpose will be to identify and maintain natural circulation consistent with the Group's generic instructions. In the interim we have put together a review package for all licensed personnel consisting of the following information.
(1) 'Chronological sequence of the THI-2 accident.
(2) IE Bulletin 79-06 "Review of operating errors and system malfunctions identified during the Three Mile Island Incident".
(3) Westinghouse's article entitled,"Steady State Natural Circulation, Calculation and Verification."
(4) A set of operating charts wi'Oi written explanation of a Cook Unit 1 trip from 100" power on March 23, 1979. The Unit scram was caused by the tripping of two vital instrument buses. The reactor was in a stable condition on natural circulation for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 52 minutes at which time a reactor coolant pump was restarted.
This information has been made a required review for all licensed per-
.sonnel. Group review sessions have been held in which open discussion was encouraged and received. In this reviev, natural circulation was dis-cussed in detail and it was pointed out that the major difference between forced and natural circulation is that the Reactor Coolant Pumps are not in operation while on natural circulation. In both cases the system pressure must be maintained higher than hot leg saturation. The pressurizer level must be maintained on scale to indicate adequate RCS water inventory. The steam generator level must be maintained to assure adequate secondary side water inventory for heat removal. No further procedure revisions in this re-gard are required a t this time, as the above key points are adequately covered.
ACTION ITEN 3:
In our Nay 1, 1979 submittal (AEP:HRC:00185),in response to Item 3 we indicated that, "All operations personnel were instructed to manually initiate safety injection during normal operation when the pressurizer pressure in-dication reaches the actuation setpoint, regardless of pressurizer level, on April 17, 1979".
Our instructions indicated that with an uncontrolled pressure reduction down to the safety injection actuation setpoint, safety injection should be manually initiated, regardless of the water level in the pressurizer. As such, safety injection would be manually initiated by the operator at the setpoint for pressurizer pressure-low. Excerpts from the instructions of April 7, 1979 are as follows:
"On Unit 1 with an uncontrolled reactor coolant system pressure reduction, when the pressure reaches 1800 psig manually initiate safety injection, re-gardless of pressurizer level."
"On Unit 2 with an uncontrolled reactor coolant system pressure reduction, when the pressure reaches 1900 psig manually i ni tiate safety injection ,
regardless of pressurizer level."
Since our t1ay 1, 1979 response to Item 3, we have modified the automatic safety injection actuation logic to a 2 out of 3 channel logic on low pressure only. Our 'submittal of June 6, 1979 (AEP:HRC:00185A) proposed changes to our Technical Specifications and described the new actuation logic.
On June 21, 1979 the t/RC issued Amendment Hos. 29 and ll to the operating licenses for Units 1 and 2 and the related safety evaluation report on this matter.
r a, ~
ACTION ITEt1 4:
In our tray 1, 1979 response to Item 4 we indicated that we were reviewing containment isolation in light of the THI-2 Incident. This review is completed arith the results provided beloww w ic supp which su lement ement our tiay 1, 1979 submittal.
Our responses to Action Itergnd 12 indicate that it would be desirable, should an unsafe plant condition develop, to be able to operate certain equipment inside the containment that becomes isolated by a Phase A and or a Phase 8 signal (automatic safety actuation).' Re-setting or overriding of the Phase A and/or Phase 8 containment inmen iso ation would be required to place this equipment into service. For t'g example, control air inside containment to the Power Operated Relief Valves (PORY) is isolated under Phase A.
The Reactor Coolant Pumps (RCP) can be operated under a Phase A contain-ment isolation. The RCP seal water discharge is isolat d b Ph A ment isolati 1 tion.
n However the seal water supply line is not isolated and the charging pumps can continue to supply seal water to the RCP's uider a Phase A
'elief containment isolation. A safety valve set at 150 psi disch p ressurizer tank to prevent the supply lines from overpressur izing.
Operator action vrould be required to reset Phase A containment isolation t th and place the seal water return line back into service by operation of each isolation valve control switch for valves gCti-250 and gCtl-350. Phase A containment isolation will not be reset unless an unsafe plant condition develops in accordance with our response to Action Item 7.
Simi larly, Component Cooling l'ater (CClt) to the RCP's is isolated under Phase B. Operation without CCW will result in damage to the pum p s ~ Th Us should be manually tripped when Phase 8 is reached. Component Cooling Water to and from the RCP oil coolers and thermal barrier is isolated under Phase 8 containment isolation. Non-essential Service Mater (WESW) to and from the RCP Motor Air Coolers and Air Cooler Vents are isolated under a Phase 8 containment isolation.
In summary, to operate a RCP under Phase 8 isolation would require re-setting Phase 8 isolation, operating each CCW iso1ation valve control switch to place CCW into service and then restarting the RCP. It should also be noted that when containment pressure high-high at 3 psig is reached and Phase 8 isolation is initiated, the containment sprays will also actuate.
Operation of the RCP's in a spray environment is uncertain.
Our letter of June 8, 1979 (AEP:NRC:00114A) described actions we have taken regarding the matter of overriding safety actuation signals by use of the reset feature mentioned above. As it applies here a thorough revie~
of the need to use the reset feature's required prior to the Senior Re-actor Operator granting approval to reset Phase A or Phase annunciate 8 contaiamnc isolation signals. When the reset is used, an alarr., will in the control room. An evaluation of the status of thethis safety actuation sign~1 inputs will be performed prior to de-energizirg alarr.-.. If an unsafe plant condition develops or beco'~~s aggravated because of placing into operation a RCP or a PORV under Phase A and/or Phase 8 contairr~nt isolation conditions, then the RCP or PORV will bc taken out of service and Phase A and/or Phase 8 will be manually initiated.
The Cook Plant isolation system is designed to limit the leakage of radioactive materials through fluid lines penetrating the containment building. Lines for which isolation is required are designed such that
,no single failure can prevent isolation. The design criteria for containment isolation is such that it is not reset by the elimination or resetting of the initiating signals, for example by resetting Safety Injection. Containment Isolation can only be reset by manual cantrols on the main control board as described earlier. Control features are provided for the containment isola&on valves such that:
a) The valves will remain in the closed position if the Phase A and or Phase B signal is reset.
b) The containment isolation signals override all other automatic control signals.
c) Each valve can be opened or closed normally after the Phase A and/or Phase B containment isolation si'gnals are reset.
Thus the current design provides for containment isolation and includes provisions such that containment isolation is not degraded by reset of initiating signals. Those lines that provide needed safety features or core cooling capability are not isolated'hould an unsafe plant condi tion develop requiring the use of some of the lines that are isolated, design features and administrative controls are provided to allow these lines to be placed into service.
The lines automatically isolated by Phase A and Phase B containment isolation are listed in Table 3.6-1 of our Technical Specifications for both Unit and Unit 2. Phase A containment isolation and main feedwater 1
isolation are automatically initiated by a safety injection signal de-rived from the Reactor Protection System or Containment Pressure - High at 1.2 psi. Phase B containment isolation, main steam isolation and contain-ment spray are automatically initiated by Containment Pressure High-High at 3 psi.
Listed below are all lines penetrating the containment that do not automatically isolate on Phase A containment isolation signal. Similarly, lines penetrating the containment that do not automatically isolate on a Phase B containment isolation are listed below. Some of these lines are not in service or aligned with an operable flow path during power operation and are listed separately.
LINES NORMALLY IN SERVICE OR ALIGNED WITH AN OPERABLE FLOW PATii THAT 00 NOT BECOME ISOLATED ON A PHASE "A" SIGNAL OR MAIN FEFDWATER ISOLATION SIGNAL
- l. Reactor Coolant Pump Seal Suey
- 2. Upper Containment Spray Inlet
- 3. Lower Containment Spray Inlet
- 4. RHR to Containment Spray
- 5. RHR Cooldown Suction
- 6. RHR to RC Hot Legs {LHSI)
- 7. RHR from Recirculation Sump
- 8. Safety Injection - {High Head and Intermediate Head)
- 9. Boron Injection Line 10 Auxiliary Feed 'ter'
'1.
Steam Generator Chemical Feed
- 12. Weld Channel Pressurization Air
- 13. CCW to Main Steam Penetrations
- 14. CCW from Main Steam Penetrations
- 15. CC!!i to Pressure Equalizing Fans
- 16. CCW from Pressure Equalizing Fans
- 17. Air Particulate- Radiogas Sample Return
- 18. Contain,",!ent Pressure Transmitters
- 19. CCW from Reactor Coolant Pump Oil Coolers
- 20. CCW from Peactor Coolant Pump Thermal Barriers
- 21. CCW to RCP Oil Coolers and Thermal Barriers
- 22. Sample to Air Particulate - Radiogas Detector
- 23. Non-Essential Service Water from Containment Coolers
- 24. Non-Essential Service Water from Containment Coolers
- 25. Non-Essential Service Water to Instrument Room Cooler
- 26. Non-Essential Service Water from Instrument Room Cooler
- 27. Non-Essential Service Water to RCP Motor Air Coolers
- 28. Non-Essential Service Water from RCP Motor Air Coolers
- 29. Main Steam from Steam Generators.
LINES NORMALLY IN SERVICE OR ALIGNED WITH AN OPERABLE FLOW PATH THAT DO NOT BECOME ISOLATED ON A PHASE 'B'R MAIN STEAf1 ISOLATION SIGNAL OR PHASE 'A'IGNAL 2.
Reactor Coolant Pump Seal Supply Upper Containment Spray Inlet
- 3. Lower Containment Spray Inlet RHR to Containment Spray
- 5. RHR Cooldown Suction
- 6. RHR to RC Hot Legs (LHSI)
- 7. RHR from Recirculation Sump
- 8. Safety Injection - (High Head and Intermediate Head)
- 9. Boron Injection Line
- 10. Auxiliary Feed Water
- 11. Steam Generator Chemical Feed
- 12. Weld Channel Pressurization Air
- 13. CCW to Main Steam Penetrations
- 14. CCW from Main Steam Penetrations
- 15. CCW to Pressure Equalizing Fans
- 16. CCW from Pressure Equalizing Fans
- 17. Containment Pressure Transmitters LINES NOT NORMALLY IN SERVICE WHICH DO NOT RECEIVE PHASE A AND B SIGNALS L INE MEANS OF ISOLATION
- l. S. I. And Accumulator Test Line 2 Manual Valves - Locked Closed
- 2. Fuel Transfer Tube Blind Flange
- 3. Service Air to Containment Manual Valve-Locked Closed and Blind Flange
- 4. Ice Loading Supply Line Blind Flange
- 5. Containment Pressurization Test Line Blind Flange
- 6. Ice Loading Return Line Blind Flange
- 7. Refueling Water Supply 2 Manual Valves - Locked Closed'
- 8. Demineralized Water Supply Manual Valves Locked Closed
- 9. Refueling Cavity Drain 2 Manual Valves - Locked Closed 10.Dead Weight Test Connection Manual Valve - Closed 11.Lower Containment Radiation Sample 2 Manual Valves - Closed 12.Upper Containment Radiation Sample 2 Manual Valves Closed
- 13. Instrument Room Radiation Sample 2 Manual Valves - Closed
- 14. Incore Flux Detection System Access Blind Flange
+ ~ * ~ I
ACTION ITEN 7 Operating procedures and training instructions have been reviewed and in no case is the operator instructed to reset or override any automatic ESF actuation signal. The procedures have been changed to include the statement "unless it would result in unsafe plant conditions".
This requirement does not apply to spurious or inadvertent actuMion when the cause is known.
After 50 F of sub-cooling has been achieved, termination of Safety Injection operation prior to 20 minutes is only permissible if it has been determi ned that continued operation would result in an unsafe plant condition. This requirement does not apply to spurious or inadvertent actuation when the cause is known.
The following procedural steps exist requiring that a minimum of 2 Reactor Coolant Pumps remain in operation as long as the pump is providing forced flow and continued operation shall not result in any unsafe plant condition.
PROCEDURE STEPS KEY POINTS 4.2.7 l1aintain a minimum of 2 Reactor l. It is essential that a Coolant pumps running for minimum of two R.C.P.'s primary coolant circulation. be maintained in service in order to provide forced cooling of the Reactor core.
- 2. Pump operation must be continued even though the normal minimum operating requirements may not be met.
I
- 3. If the continued operation of the R.C.P.'s threatens to cause an increase in the severity of the accident condition, the pump or pumps should be removed from service.
- 4. If component cooling water flow to the R.C.P.'s is lost bearing failures will occur very rapidly and therefore the pump or pumps must be removed from service. It is estimated that bearing failure may occur within 5 minute of loss of component cooling water.
ACTIOh ITEN 8 A complete 'valve lineup walk around of all safety related valves including locked valves has been performed prior to the startup following the Nay ]9, 1979 Unit 2 outage and following the April 6th outage of Unit l.
ACTION ITEM 10 There is an administrative requirement which has been in effect over one year, since July 7, 1978, which instructs the Shift Supervisor, at the start of each shift, to place in his log all Technical Specification items that are inoperable. The requirement also includes instructions to log any equipment that becomes inoperable during the shift and. also any equipment that is returned tolerable status during the shift. These logs must be reviewed by the incoming Shift Supervisor and verified by signoff. In this manner, the status of safety related systems is known at a shift change.
1 ACTIOH ITEll 12 0
Our response to Item 12, contained in our Hay 1, 1979 letter responding to IE Bulletin 79-06A, addressed hydrogen control in the containment. This additional response to Item 12 addresses hydrogen control in the RCS and supplements our Hay 1, 1979 submittal.
The engineered safeguards at~ok Plant are designed to meet the limits of 10 CFR 50.46 which require that the hydrogen generation from clad water reaction in a LOCA be limited to less than 1" of the clad metal, and no where exceed 17'. of the clad thickness.
Hydrogen removal from the Reactor Coolant System (RCS) can be accomplished by operation of RCS letdown, Reactor Coolant Pumps, power operated relief valves and/or normal pressurizer pressure control.
Systems required to support these functions such as offsite power, component cooling water, compressed air and pressurizer heaters and sprays may not be available inside of the containment. Their use is dependent upon the circumstances surrounding an event where their use may be desirable. These systems are not essential for a safe shutdown of the plant during a design basis accident and are isolated on Containment Isolation (Phase A or Phase B). Our supplemental response to Action Item 4 provides further information on containment isolation.
Containment Isolation Phase A is automatically initiated by a Safety Injection signal derived from the Reactor Protection System or Containment Pressure High at 1.2 psi. Containment Isolation Phase B is automatically initiated from Containment Pressure - High-High at 3.0 psi. If the circumstances surrounding an event are such that the use of the above mentioned non-essential systems inside of the contain-ment is desirable and the containment is isolated then deliberate operator action is required. After careful review of the need to break containment isolation the operator would have to reset and override the Containment Isolation signal (Phase A or B) and.manually place the desired system or component into service. Also, operating these systems during a station blackout would require operator action. The modes for hydrogen removal described below can be utilized from the main control room.
The modes for removing hydrogen from the reactor coolant system are:
- 1. Hydrogen can be stripped to the pressurizer vapor space by pressurizer spray operation loop number 3 reactor coolant pump is if operating and control air inside cpntainment is available.
~ g ~
- f. 4 ~ '
ACTION ITEI1 12 CONT'D.
- 2. Hydrogen in the pressurizer vapor space can be vented and discharged to the pressurizer relief tank by operating the power operated relief valves if control air inside containment is available.
- 3. Hydrogen can be removed from the reactor coolant system by the letdown line and stripped in the volume control tank where it enters the waste gas system (if the letdown line is available).
- 4. In the event of a LOCA, hydrogen would vent with the steam to the containment.
If for some reason a non-condensible gas bubble becomes situated somewhere in the primary coolant system, there are several options for continued core cooling and removing the bubble.
If the gas bubble becomes located in the upper head, the following methods of core cooling are unaffected. Steam generators can be used to remove decay heat using reactor coolant pump forced flow (if RCP is available) or natural circulation. The safety injection system can be used to cool the core while venting through the pressurizer power operated relief valve if this method is available. Core cooling by any of these methods can proceed indefinitely if the primary coolant pressure is held constant. If the bubble were to grow to the top of the hot leg, it would slide acr'oss the hot leg and up into the steam generators. As depressurization continues, the gas bubbles grow in the steam generators and upper head but the core remains covered and cooled by safety injection water. If there is enough gas, the pressurizer surge line would eventually be "uncovered". Some of the gas would burp into the pressurizer and out the valve. This burping process would continue until the system were at the desired pressure. At that time, the current cooling mode could be continued or the system could be placed in the RHR cooling mode if at the appropriate pressure for RHR operation.
Note that a gas bubble cannot be located in the steam generator with the reactor coolant pumps running. If a gas bubble forms in the steam generator during natural circulation, the reactor coolant pumps could be turned back on for degassing (if available) or safety injection flow could be initiated with the power operated relief valve open (if control air is available).