Similar Documents at Cook |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J4721999-10-15015 October 1999 Forwards NRC Physical Security Insp Repts 50-315/99-27 & 50-316/99-27 on 990920-24.Two Violations Noted & Being Treated as Ncvs,Consistent with App C of Enforcement Policy. Areas Examined Exempt from Disclosure,Per 10CFR73.21 IA-99-379, First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety1999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML20217D9241999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML20196K5961999-06-30030 June 1999 Ltr Contract:Task Order 40, DC Cook Extended Sys Regulatory Review Oversight Insp, Under Contract NRC-03-98-021 ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML20207A9201999-05-21021 May 1999 Ack Receipt of 990319 Response to Notice of Violation & Proposed Imposition of Civil Penalty .On 981124, Licensee Remitted Check for Payment of Civil Penalties. Licensee Requests for Extension for Response,Granted ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML20205P0591999-04-14014 April 1999 Ninth Partial Response to FOIA Request for Documents.App Records Already Available in Pdr.Records in App T Encl & Being Made Available in Pdr.App U Records Being Released in Part (Ref FOIA Exemption 7).App V Records Withheld Entirely ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed ML17325B5141999-03-30030 March 1999 Forwards Rept on Status of Decommissioning Funding.Attached Rept Includes Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML17325B5191999-03-29029 March 1999 Forwards LER 99-001-00,re Degraded Component Cw Flow to Containment Main Steam Line Penetrations.Commitment, Listed ML20204F6401999-03-19019 March 1999 Responds to NRC 981013 NOV & Proposed Imposition of Civil Penalty.Violations Cited in Subject NOV Were Initially Identified in Referenced Five Insp Repts.Corrective Actions: Ice Condensers Have Been Completely Thawed of Any Blockage ML17325B4751999-03-18018 March 1999 Forwards LER 99-004-00,re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitment Made by Util,Listed ML17325B4721999-03-18018 March 1999 Forwards LER 99-005-00,re Reactor Trip Breaker Manual Actuations During Rod Drop Testing Not Previously Reported. Listed Commitments Identified in Submittal ML17325B4641999-03-17017 March 1999 Withdraws Response to Issue 1 of NRC Cal,Dtd 970919. Comprehensive Design Review Effort in Progress to Validate Resolution of Issue for Future Operation 1999-09-30
[Table view] Category:UTILITY TO NRC
MONTHYEARML17328A4481990-09-21021 September 1990 Requests Withdrawal of Mode 6 Proposed Tech Spec Change Since Issue Currently Being Addressed by New STSs ML17328A4331990-08-27027 August 1990 Informs of Preliminary Assessment of 900713 Electrical Contact Accident at Facility.Investigation Concludes That No Safety Rules Violated ML17328A4001990-08-24024 August 1990 Responds to 900725 Ltr Re Commitments Made in Response to Generic Ltr 88-14 on Instrument Air Supply Problems Affecting safety-related Equipment.Simulator Training to Be Provided as Stated ML17334B3781990-08-24024 August 1990 Forwards Info to Certify Plant Simulator Facility.Results of Evaluation of Dual Unit Simulation Facilities Demonstrate That Plant Simulator Performance Compares Favorably W/Units ML17328A4231990-08-21021 August 1990 Forwards Under Separate Cover,Semiannual Radioactive Effluent Release Rept for Jan-June 1990 ML17328A3901990-08-17017 August 1990 Responds to NRC 900720 Ltr Re Violations Noted in Onsite Audit of Spds.Corrective Actions:Apparent Disparity in Selection of Reactor Trip & Sys Capacity or Anticipatory Values Rectified ML17328A3891990-08-15015 August 1990 Forwards Performance Data Sheets for Plant fitness-for-duty Program for Period Jan-June 1990,per 10CFR26.Encl Includes Statistics on Various Categories of Testing,Substances Tested for & cut-off Levels Used ML17328A3571990-08-0202 August 1990 Responds to Open Items in Safety Evaluation of Util Response to Unresolved Issues on post-fire Safe Shutdown Methodology. Open Items 1 & 21 Will Be Closed by Implementing Plant Procedures Providing Equivalent Degree of Protection ML17328A3431990-07-23023 July 1990 Requests Withdrawal of 890830 Proposed Tech Spec Changes Re Sections 3.0 & 4.0.Util Will Resubmit Generic Ltr 87-09 Recommended Improvement Items on Case by Case Basis ML17328A3421990-07-23023 July 1990 Provides Results of Offsite Dose Calculation for Reactor Coolant Pump Locked Rotor Event for Facility Cycle 8.Util Identified Previously Issued SERs Addressing Short Term Containment Analysis & LOCA Containment Integrity ML20055G7551990-07-18018 July 1990 Responds to NRC Re Violations Noted in Insp Repts 50-315/90-10 & 50-316/90-10.Corrective Actions:Required Review Performed & Updated Procedure 12 Mhp 5021.019.001 Revised & Issued ML17328A3191990-07-12012 July 1990 Responds to NRC 900601 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Electrical Testing Techniques Improved & Surveillance Procedures for Feedwater Pumps Will Be Rewritten ML17328A3181990-07-0909 July 1990 Responds to Generic Ltr 90-03,Suppl 1, Relaxation of Staff Position in Generic Ltr 83-28,Item 2.2,Part 2, 'Vendor Interface for Safety-Related Components.' Licensee Will Contact safety-related Vendors on Annual Basis ML17328A3111990-07-0303 July 1990 Provides Certification of Funding Plan for Decommissioning of Plant,Per 10CFR50.33 & 50.75 ML17328A2961990-06-25025 June 1990 Forwards Response to Generic Ltr 90-04 Re Closeout of Generic Safety Issues.Util Supports Concern & Desire to Close long-standing Generic Safety Issues ML17328A2921990-06-22022 June 1990 Forwards WCAP-12483, Analysis of Capsule U from American Electric Power Co DC Cook Unit 1 Reactor Vessel Radiation Surveillance Program. ML20044A3521990-06-22022 June 1990 Submits Info Re Sensitivity Study Performed on Number of Fuel Axial Intervals,Per Topical Rept, American Electric Power Reactor Core Thermal-Hydraulic Analysis Using Cobra III-C/MIT-2 Computer Code. ML17328A2821990-06-15015 June 1990 Submits Ltr Re Proposed Control Room Habitability Tech Spec Changes & Supporting Analyses,Per 900521 Discussion.Revised Calculations of Control Room Thyroid Doses Will Be Submitted within 60 Days of Receipt of Proposed Generic Ltr ML17328A2741990-06-12012 June 1990 Submits Followup,Per 900205 & 0308 Ltrs & Provides Update Re Inoperable Fire Barrier.Fire Seal Repaired & Restored to Operability on 900419 ML17328A2551990-06-0505 June 1990 Forwards Addl Info Re Util 900126 Revised Response to NRC Bulletin 88-002,per NRC 900509 Request ML17328A7361990-06-0101 June 1990 Forwards Addl Info Re 890825 & 1212 Applications for Amends to Licenses DPR-58 & DPR-74,per Request.Amends Make Changes to Administrative Controls ML17328A7331990-05-29029 May 1990 Forwards Nonproprietary WCAP-12577 & Proprietary WCAP-12576, Westinghouse Revised Thermal Design Procedure Instrument... Methodology for American Electric Power DC Cook Unit 2 Nuclear Power Station, Per 900419 Commitment ML17328A7321990-05-24024 May 1990 Responds to NRC Bulletin 90-001, Loss of Fill Oil in Transmitters Mfg by Rosemount. No Rosemount Model 1153 Series B or D or Model 1154 Transmitters Installed at Facility.Transmitters Purchased as commercial-grade Units ML17328A6991990-05-0909 May 1990 Provides Suppl to 900103 Response,Certifying That Fitness for Duty Program Implemented at Plant.Change Also Clarifies When More Stringent cut-off Levels Adopted at Plant Program Apply ML17328A7001990-05-0909 May 1990 Responds to NRC 900406 Ltr Re Inadequacies of Spds,Per Audit on 900221-22.Corrective Actions:Software Mod Will Prevent User from Accessing Displays Other than Iconic Displays from SPDS Dedicated Terminal ML17328A7071990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept Mar 1990 for Donald C Cook Nuclear Plant Unit 1 ML17328A7031990-05-0707 May 1990 Forwards Monthly Operating Rept for Apr 1990 & Corrected Rept for Mar 1990 for DC Cook Nuclear Plant Unit 2 ML17328A6951990-04-30030 April 1990 Certifies That Training Programs for Initial Licensing & Requalification Training of Operators & Senior Operators at Plant Accredited by Inpo,Per Generic Ltr 87-07 ML17328A6861990-04-30030 April 1990 Forwards Annual Environ Operating Rept,Jan-Dec 1989, & DC Cook Nuclear Plant Units 1 & 2 Operational Radiological Environ Monitoring Program 1989 Rept Jan-Dec 1989. ML17328A6801990-04-23023 April 1990 Responds to NRC Bulletin 88-004, Potential Safety-Related Pump Loss. Study Planned to Evaluate Alternative Actions to Be Taken for Protecting RHR Pumps ML17328A6771990-04-23023 April 1990 Forwards DC Cook Nuclear Plant 1990 Annual Emergency Preparedness Exercise. Exercise Scope & Objectives & Detailed Scenario Documentation Encl ML17334B3641990-04-11011 April 1990 Responds to NRC 900301 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated ML17328A6601990-04-11011 April 1990 Forwards Updated QA Program Description for Cook Nuclear Plant, Incorporating Editorial,Organizational & Position Title Changes ML17328A6551990-04-0909 April 1990 Responds to NRC 900309 Ltr Re Violations Noted in Insp Rept 50-316/90-08.Corrective Actions:Procedure for Steam Generator Stop Valve Operability Test Revised to Require That MSIV Be Declared Inoperable After Failing Stroke Test ML17334B3601990-04-0606 April 1990 Forwards Revised Figures for Loss of Load Event Previously Submitted in Attachment 4,App B of Vantage 5 Reload Transition Safety Rept Supplied by Westinghouse in Jan 1990. Update Is Editorial in Nature ML17334B3621990-04-0606 April 1990 Forwards 1989 Annual Rept & Projected Cash Flow ML17328A6341990-03-30030 March 1990 Forwards Application for Renewal of Plant NPDES Permit,For Info,Per Section 3.2 of App B to Plant Tech Specs.W/O Encl ML17328A6331990-03-30030 March 1990 Responds to NUMARC 900104 Request for Addl Info Re Station Blackout Submittals.Target Reliability for Emergency Diesel Generator of 0.0975 Established for 4 H ac-independent Coping Category Will Be Maintained ML17328A6321990-03-30030 March 1990 Forwards Response to Generic Ltr 90-01, NRC Regulatory Impact Survey. Util Ack Recommendation by NUMARC ML17328A6221990-03-27027 March 1990 Responds to 900226 Ltr Transmitting Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $75,000. Corrective Actions:Flow Retention Circuitry Setpoints Set to Compensate for Missized Process Flow Orifice ML17328A6191990-03-27027 March 1990 Forwards Payment in Amount of $75,000 for Civil Penalty Imposed Through Notice of Violation Issued in Insp Rept 50-316/89-02 on 891016-20,24-26 & 1204.Response to Violation & Corrective Actions Provided in Separate Submittal ML17328A6161990-03-20020 March 1990 Responds to Generic Ltr 89-19 Re Safety Implications of Control Sys in LWRs (USI A-47).Both Units Have Steam Overfill Protection Sys That Would Automatically Prevent Water Carryover Into Steam Lines If Control Sys Failed ML17328A6121990-03-13013 March 1990 Forwards Monthly Performance Monitoring Rept,Jan 1990. ML17325B3901990-03-0606 March 1990 Forwards Annual Rept to NRC Per 10CFR50.54(W)(2) Re Nuclear Property Insurance ML17325B3921990-03-0606 March 1990 Modifies Application for Amend to License DPR-74 Re Cycle 8, Per 900228 Telcon ML17325B3781990-02-28028 February 1990 Forwards Response to NRC Info Notice 89-056 Re Questionable Certification of Matl Supplied to Dod by Nuclear Suppliers. Matl Capable of Performing Design Function & Acceptable for Continued Use ML17328A5971990-02-27027 February 1990 Withdraws 890203 Application for Amend to License DPR-74, Modifying Tech Spec Table 3.2-1 Re DNB Parameters to Express RCS Flow Rate on Volumetric Rather than Mass Basis ML17334B3511990-02-22022 February 1990 Submits Annual Rept of Changes to or Errors in Acceptable LOCA Evaluation Models or Application of Models for Plants. Wflash Analyses Will Be Superceded by Notrump Analyses for Unit 2,Cycle 8 Reload ML17328A5881990-02-21021 February 1990 Responds to NRC 890914 Request for Addl Info Re Safe Shutdown Methodology.App R Fire Barriers Being Maintained & Surveilled Under 3/4.7.10 for Units 1 & 2 ML17328A5861990-02-16016 February 1990 Provides Revised Comments in Response to NRR Comments During 891213 Telcon Re Allowable Stresses for Piping & Piping Supports 1990-09-21
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ACCELERATED D T83BUTION DEMONS TION SYSTIM REGULATORY INFORMATION DISTRIBUTXON SYSTEM (RIDS)
A SSION NBR:9004050289 DOC.DATE: 90/03/27 NOTARIZED: YES DOCKET PT FACIL:50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana & 05000316 AUTH. NAME AUTHOR AFFILIATION ALEXICH,M.P. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATXON DAVIS,A.B. Document Control Branch (Document Control Desk)
SUBJECT:
Responds to 900226 proposed imposition ltr transmitting notice of violation of civil penalty in amount of 75,000.
DISTRXBUTION CODE- IE01D TITLE: General (50 COPIES RECEIVED:LTR Dkt)-Insp Rept/Notice ENCL L SIZE:
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INTERNAL: AEOD 1 1 AEOD/DEIIB 1' AEOD/TPAD 1 1 DEDRO 1 1 D NRR SHANKMAN,S 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA DIR 11 1 1 NRR/DREP/PEPB9D 1 1 S NRR/DRIS/DIR 1 1 NRR/DST/DIR SE2 1 1 NRR/PMAS/ILRB12 1 1 NU -ABSTRACT 1 1 OGC/HDS1 1 1 02 1 1 RES/DSR/HFB/HFS 1 1 RGN3 FXLE 01 1 1 AL: LPDR 1 1 NRC PDR 1 1 NSIC 1 1 R
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NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WAS'ONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DIFfRIBUTION LISIS FOR DOCUMENTS YOU DON'T NEEDI TOTAL NUMBER OF COPIES REQUIRED: LTTR 21 ENCL 21
Indiana Michigan Power Company P.O. Box 16631 Coiumbus, OH 43216 INDMMA AIICHIGAK POWER AEP:NRC:1125 10 CFR 2.201 Donald C. Cook Nuclear Plant Unit 2 Docket No. 50-316 License No. DPR-74 NRC INSPECTION REPORT NO. 50-316/89028 (DRP); RESPONSE TO NOTICE OF VIOLATION U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Attn: A. B. Davis March 27, 1990
Dear Mr. Davis:
This letter is in response to your letter dated February 26, 1990, which forwarded a Notice of Violation and proposed imposition of a civil penalty in the amount of $ 75,000. The Notice of Violation and associated civil penalty resulted from a routine safety inspection conducted at the Cook Nuclear Plant on October 16 through 20, October 24 through 26, and December 4, 1989, by members of your staff. The violation involves the installation of an improperly sized flow orifice in the Cook Nuclear Plant Unit 2 turbine-driven auxiliary feedwater pump (TDAFP) discharge prior to initial plant startup. The mis-sized orifice resulted in the establishment of an incorrect setpoint in the TDAFP flow retention circuitry which created the potential for TDAFP runout and subsequent unavailability of this source of auxiliary feedwater following a postulated feedwater or main steam line break.
Our response to the Notice of Violation is provided in the attachment to this letter. In addition, item 4 of the attachment responds to your request that we specifically address actions taken to improve our corrective action system and operator attention to detail during the conduct of testing. In response to your further request, item 4 of the attachment also provides a discussion of our evaluation of our receipt inspection program in an effort to identify areas in need of improvement. The $ 75,000 civil penalty is being remitted through a separate submittal.
9000050289 900327 PDR Q
AGOCK 0 0003lb got PbC
Mr. A. B. Davis AEP:NRC:1125 This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath is enclosed.
Sincerely,
'. P.'Alex eh Vice President ldp Attachment cc: D. H. Williams, Jr.
A. A. Blind - Bridgman R. C. Callen G. Charnoff A. B. Davis - Region III-NRC Resident Inspector Bridgman NFEM Section Chief
COUNTY OF FRANKLIN Milton P. Alexich, being duly sworn, deposes and say that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the .foregoing"Response to NRC Inspection Report No. 50-316/89028 (DRP); Response to Notice of Violation and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.
Subscribed and sworn to before me this .~~4-day of 199 u p
NOTARY PUBLIC
~ BITA D. HILL
ATTACHMENT TO AEP:NRC:1125 RESPONSE TO VIOLATION
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Attachment to AEP:NRC:1125 Page 1 NRC Violation "Technical Specification 3.7.1 ~ 2 requires at least three independent steam'generator auxiliary feedwater pumps and associated flow paths be operable in Modes 1, 2 and 3. With one auxiliary feedwater pump inoperable, restore that pump to operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and hot.shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.
Contrary to the above, whi.le the facility has been in Modes 1, 2 and 3, the licensee did not have three independent steam generator auxiliary feedwater pumps and associated flow paths operable during the period from August 31, 1978 through November 10, 1989, and action was not taken to restore all pumps to operable status or place the facility in hot standby or hot shutdown. The Turbine-Driven Auxiliary Feedwater Pump (TDAFP) was inoperable during this period due to the inability of the flow retention system for the TDAFP to prevent run out of the TDAFP and its resulting failure in the event of a feedwater or steam line break.
This is a Severity Level III violation (Supplement I).
Civil Penalty - $ 75,000."
Response to Violation On October 19, 1989, an NRC inspector witnessing inservice testing of the Unit 1 turbine-driven auxiliary feedwater pump (TDAFP) observed that the pump flow as indicated by the permanently mounted process flowmeter was significantly lower than that indicated by the portable instrument connected to the test line orifice used for the inservice test. The process flow meter was reading approximately 150 gpm less than the 700 gpm indicated by the test flow meter at the Technical Specification test point. Subsequent review by Cook Nuclear Plant personnel found that the portable test meter reading was accurate.
On the basis of orifice differential pressure versus flow calculations, we determined that the discrepancy in the process flow indication resulted in the TDAFP flow retention circuitry setpoint being at approximately 1225 gpm versus the required 975 gpm. The 1225 gpm setpoint was too high to prevent pump runout and hence created the potential for loss of the TDAFP following a feedwater or main steam line break. Although the TDAFP may potentially have been unavailable for these accident conditions, we conclude that no significant adverse implications with regard to protection of public health and safety would have resulted. As a backup to the TDAFP, two motor-driven auxiliary feedwater pumps (MDAFP), each feeding two steam generators, are available as a source of auxiliary feedwater. As a further backup source of auxiliary feedwater, cross-ties installed at the Cook Nuclear Plant allow one unit's
Attachment to AEP:NRC:1125 Page 2 MDAFPs to provide auxiliary feedwater to the opposite unit. In reaching our conclusion that public health and safety would not have been adversely impacted as a result of the situation cited in the Notice of Violation, we reviewed the UFSAR analyses of a postulated feedwater line or steam line break with the TDAFP unavailable. In the case of a, steam line, break, this is a cooldown accident in which the concern is a return of the core to power from a subcritical condition due to a negative moderator temperature coefficient. The potential for a return to power is aggravated by higher auxiliary feedwater flow rates. As a result, the UFSAR analysis assumes that the TDAFP goes to runout during the steam line break. Therefore, the UFSAR analysis. results for this accident are not adversely affected by the condition. With regard to a postulated feedwater line break, this would initially be a cooldown accident followed by an eventual heatup of the primary system due to the lack of feedwater caused by the break. The UFSAR analysis of this event conservatively neglects the initial cooldown in order to maximize the heatup effects. The accident analysis takes no credit for any auxiliary feedwater flow for the first ten minutes of the accident and then assumes delivery of only 600 gpm to the three intact. steam generators following isolation of the faulted steam generator by the operators.
This flow is well within the capability of the two MDAFPs, each of which is rated at approximately 450 gpm. In addition, we have performed an analysis of the postulated feedwater line break that demonstrates acceptable results with only one MDAFP providing flow, when credit is taken for actual (vs. Technical Specification allowable) pump performance and steam generator inventory. An independent evaluation performed by the fuel vendor 'for Unit 2 has confirmed the conclusions of our analyses.
- 1. Admission or Denial of the Alle ed Violation Indiana Michigan Power admits to the, violation as cited in the NRC Notice of Violation. We also accept, without protest, the imposed civil penalty of $ 75,000 associated with the cited violation. Payment of the civil penalty will be made through a separate submittal.
- 2. Reasons for the Violation The cause of the violation is attributed to inadequacies in the corrective action system that was in place in 1978.
Discrepancies in flow readings between the process and test line flow indicators were noticed during preoperational testing for Unit 2. The discrepancy was documented in a Condition Report dated August 31, 1978.
Our review of the 1978 Condition Report and subsequent evaluations'erformed since October 1989 concludes that, the flow discrepancy was caused by an improperly sized process flow orifice's part of the original
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' Attachment to AEP:NRC:1125 Page 3 investigation conducted in 1978, both the process and test line orifices were pulled and inspected, and the sizes stamped on their identification tabs were verified. No problems were noted during this activity. However, based on a comparison of the flow reading derived from the two orifices in combination with other indications of pump performance it was concluded that the process orifice flow indication was in error. Because of the problem with the orifice, the plant suspended use of the process flow orifice for pump performance testing, using the test line orifice instead. The Condition Report was closed out with a statement that the flow discrepancy would remain under investigation. There was apparently no follow-up action to ensure that proper corrective actions were completed to close-out the Condition Report.
Corrective Actions Taken and Results Achieved Upon discovery of the discrepancy between the flow rates indicated by the test line and process flow orifices, an investigation of the condition was initiated in accordance with our corrective action system. Our investigation showed that the flow indicated by the test line orifice was correct. This in conjunction with TDAFP performance data led to the conclusion that the process flow orifice which provides input to the flow retention circuitry was the source of the observed discrepancy in flow indications. Consequently, on October 25, 1989, the flow retention circuitry setpoints were re-calibrated to compensate for the mis-sized process flow orifice and now provide flow retention at the required TDAFP discharge flow (975 gpm). In addition, the process and test flow indications for the other auxiliary feedwater pumps in both units were compared to ensure that the problem was limited to the Unit 2 TDAFP. This evaluation confirmed that the observed discrepancy between process and indication in the Unit 2 TDAFP does not exist in any test'low of the other auxiliary feedwater pumps.
4, Corrective Action Taken to Avoid Further Violations As discussed above, our investigation of the condition cited in the Notice of Violation has concluded that the process flow orifice is improperly sized. The original equipment purchase orders required orifice plates to be manufactured to specified dimensions, and be supplied with drawings. After review of receipt inspection documentation it has been concluded that physical dimensions were not verified by actual measurement of the orifice diameter upon receipt of the original order. A replacement order for the Unit 2 TDAFP orifice has been
Attachment to AEP:NRC:1125 Page 4 issued, again specifying dimensions and requiring material certification/certificate of conformance and a certified engineering drawing. Once this material arrives on-site, it will be receipt inspected to the requirements of the
-current plant procedure which requires a physical layout check of dimensions. The physical layout check includes measurement of the orifice diameter to confirm conformance to dimensional requirements, The receipt inspection procedures currently in effect have been revised since the time the currently installed orifice was delivered. Our review of the current procedures has concluded that they are sufficiently more stringent than those previously in existence to preclude inadequate receipt inspection from being a contributor to a condition of the type addressed in the cited violation.
With regard to operator performance, through the Operations Department review of events documented by the plant's Operating Experience Program, the Operations Department recognizes the importance of operator attention to detail in performing their job. The following are action's taken by Operations Department to promote operator attention to detail:
The Operations Department distributes a "Lessons Learned Report" each four months. This report discusses the personnel errors which occurred during the previous four months. The operator review of this report increases his/her awareness of specific problem areas which require increased attention.
Each five weeks a "Work Practice Reminders" list is sent to the Operations shift personnel attached to the "Shift Requirements" letter. This list reviews items which have been noted as good operator practices. Although, the list does not specifically use the term "attention to detail," the list focuses on items which specifically promote attention to detail.
In addition, to the above efforts by the Operations Department to improve operator attention to detail, further actions have been taken since the recent TDAFP flow retention finding. The actions are as follows:
The plant manager sent a letter to all Cook Nuclear Plant and site contractor personnel'he letter addressed plant personnel responsibilities to identify and document plant deficiencies.
Attachment to AEP:NRC:1125 Page 5
- b. The Operations Superintendent held a meeting with all Operations Department Supervisory personnel. During this meeting, the Operations Superintendent stressed the need for supervisory personnel to stress attention to,detail to the personnel who work for them.
c, The Training Department has prepared a case study of the TDAFP flow retention finding. The case study (RQ-C-1514) is being presented to the Licensed Operators during requal period 1. The case study discusses the need for operators to monitor all available parameters during a test and to follow through on reporting of discrepancies to ensure a satisfactory completion. The case study training will be completed by 3-30-90.
,It should also be noted that subsequent to the time at which the cited violation originally occurred, the Cook Nuclear Plant and AEPSC have modified the corrective action system. Specifically, modifications began in November of 1986 when Cook Nuclear Plant and AEPSC combined the Plant's condition reporting system with AEPSC's nonconformance reporting system to create a new report system. One of the improvements under the. 'roblem new system was to provide centralized computer tracking for all open corrective/preventive action items. Prior to this time frame these open items were tracked on multiple systems. In addition, deficiencies documented through the revised problem report system are categorized to distinguish significant problems from those of less significance. In this way issues representing potential significant safety impacts receive more immediate attention, and are subject to a more in-depth review, than less significant (e.g., administrative, housekeeping) conditions.
As an additional part of our investigation of this condition, a review of condition reports initiated and closed prior to implementation of our present corrective action system was performed. The purpose of this review was to provide assurance that no other examples exist in which an adverse condition of potential safety significance had been identified and subsequently dispositioned through incomplete or inadequate corrective action. In performing this review, a sample of 100 condition reports (CRs) was chosen at random (using a computer-based random number generator) from a total population of approximately 3800 CRs. Applying the statistical criteria of Information Bulletin 79-02A, the results of our review conclude at the 95% confidence level
Attachment to AEP:NRC:1125 Page 6'hat corrective actions taken in closing CRs during the time period prior to implementation of our present corrective action system are adequate to ensure that concerns of potential safety significance have been appropriately resolved.
The new procedures written to implement the problem report system require the documentation of open corrective/
preventive action items. For these open action items, due dates are established and responsibility for close out is assigned. These open items are then entered into the centralized computer tracking system. This system is
'utilized to provide status reports of the open items to both AEPSC and Cook Nuclear Plant management to ensure their timely completion. As a final control, problems which are determined to have a potential significant impact on nuclear safety are reviewed by both the Plant Nuclear Safety Review Committee and the AEPSC Nuclear Safety Design Review Committee. This review specifically checks the disposition of the problem report to ensure appropriate 'corrective/preventive actions have been completed or listed as open on the problem report. Had this program been in place at the time of Unit 2 pre-operational testing, the violation associ.'ated with the TDAFP process flow orifice would likely not have occurred.
Date When Full Com liance Will Be Achieved Full compliance was achieved on October 25, 1989, when the TDAFP process flow indicating switches were reset for proper actuation.