ML062160540
ML062160540 | |
Person / Time | |
---|---|
Site: | Fermi |
Issue date: | 08/02/2006 |
From: | Christine Lipa NRC/RGN-III/DRP/RPB4 |
To: | Cobb D Detroit Edison |
References | |
IR-06-003 | |
Download: ML062160540 (48) | |
See also: IR 05000341/2006003
Text
August 2, 2006
Mr. Donald K. Cobb
Assistant Vice President
Nuclear Generation
Detroit Edison Company
6400 North Dixie Highway
Newport, MI 48166
SUBJECT: FERMI POWER PLANT, UNIT 2, NRC INTEGRATED
INSPECTION REPORT 05000341/2006003
Dear Mr. Cobb:
On June 30, 2006, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated
inspection at your Fermi Power Plant, Unit 2. The enclosed report documents the inspection
findings which were discussed on July 11, 2006, with you and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and to
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, five findings of very low safety significance were
identified, all of which involved violations of NRC requirements. However, because these
findings were of very low safety significance and because the issues were entered into your
corrective program, the NRC is treating these findings as Non-Cited Violations in accordance
with Section VI.A.1 of the NRCs Enforcement Policy. If you contest the subject or severity of
a Non-Cited Violation, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional
Administrator, U.S. Nuclear Regulatory Commission - Region III, 2443 Warrenville Road,
Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Fermi 2
facility.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and
its enclosure will be made available electronically for public inspection in the NRC Public
D. Cobb -2-
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Christine A. Lipa, Chief
Branch 4
Division of Reactor Projects
Docket No. 50-341
License No. NPF-43
Enclosure: Inspection Report 05000341/2006003
w/Attachment: Supplemental Information
cc w/encl: K. Hlavaty, Plant Manager
R. Gaston, Manager, Nuclear Licensing
D. Pettinari, Legal Department
Michigan Department of Environmental Quality
Waste and Hazardous Materials Division
M. Yudasz, Jr., Director, Monroe County
Emergency Management Division
Supervisor - Electric Operators
State Liaison Officer, State of Michigan
Wayne County Emergency Management Division
D. Cobb -2-
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
Christine A. Lipa, Chief
Branch 4
Division of Reactor Projects
Docket No. 50-341
License No. NPF-43
Enclosure: Inspection Report 05000341/2006003
w/Attachment: Supplemental Information
cc w/encl: K. Hlavaty, Plant Manager
R. Gaston, Manager, Nuclear Licensing
D. Pettinari, Legal Department
Michigan Department of Environmental Quality
Waste and Hazardous Materials Division
M. Yudasz, Jr., Director, Monroe County
Emergency Management Division
Supervisor - Electric Operators
State Liaison Officer, State of Michigan
Wayne County Emergency Management Division
DOCUMENT NAME:E:\Filenet\ML062160540.wpd
G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive
To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy
OFFICE RIII RIII
NAME RLerch:dtp CLipa
DATE 08/02/06 08/02/06
OFFICIAL RECORD COPY
Donald K. Cobb -3-
ADAMS Distribution:
LXR1
DHJ
RidsNrrDirsIrib
GEG
KGO
RMM3
CAA1
LSL (electronic IRs only)
C. Pederson, DRS (hard copy - IRs only)
DRPIII
DRSIII
PLB1
TXN
ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)
U. S. NUCLEAR REGULATORY COMMISSION
REGION III
Docket No: 50-341
License No: NPF-43
Report No: 05000341/2006003
Licensee: Detroit Edison Company
Facility: Fermi Power Plant, Unit 2
Location: Newport, Michigan
Dates: April 1 through June 30, 2006
Inspectors: R. Michael Morris, Senior Resident Inspector
T. Steadham, Resident Inspector
A. Wilson, NRC Headquarters
M. Franke, Senior Resident Inspector, Perry
M. Jordan, NRC Consultant
R. Langstaff, Senior Reactor Inspector
M. Mitchell, Radiation Specialist
Approved by: C. Lipa, Chief
Branch 4
Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000341/2006003; 04/01/2006-06/30/2006; Fermi Power Plant, Unit 2; Fire Protection,
Maintenance Risk Assessment, Operability Evaluations, Refueling and Outage Activities.
This report covers a 3-month period of inspection by resident inspectors and announced
baseline inspections by a regional radiation specialist inspector. Five Green findings, all of
which were associated with non-cited violations (NCVs) were identified. The significance of
most findings is indicated by their color (Green, White, Yellow, Red) using Inspection
Manual Chapter 0609, Significance Determination Process (SDP). Findings for which the
SDP does not apply may be Green after NRC management review. The NRCs program for
overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A. NRC-Identified and Self-Revealed Findings
Cornerstone: Initiating Events
- Green. The inspectors identified an NCV of 10 CFR 50.65(a)(4) for the failure to
perform an adequate risk assessment for the Division I battery load test. The licensee
failed to consider the effect the test would have on the temperature in the reactor
protection system motor generator set rooms. Consequently, the load bank used for the
test caused the room temperature to increase which necessitated the unanticipated
installation of a temporary fan to cool the room. The licensee entered this issue into
their corrective action program to evaluate any programmatic or procedural deficiencies
that may have contributed to this event.
This finding is more than minor because the licensees risk assessment failed to
consider maintenance activities that could increase the likelihood of an initiating event,
specifically a loss of shutdown cooling from a reactor protection system motor generator
set trip on high temperature. The finding is of very low safety significance because it did
not affect the ability of operators to recover from a loss of shutdown cooling if it had
occurred. The cause of the finding is related to the cross-cutting element of Human
Performance. (Section 1R13.2)
Cornerstone: Mitigating Systems
- Green. The inspectors identified an NCV of license condition 2.C(9) due to the
presence of unauthorized transient combustible materials in the residual heat removal
complex. An office chair and a plastic trash bin half filled with paper were secured next
to the electrical panel and associated cable raceway for emergency diesel generator 12
ventilation in the emergency diesel generator 12 switchgear room. The licensee entered
this issue into their corrective action program and removed the unauthorized transient
combustible materials from the residual heat removal complex.
This finding is more than minor because it affected the Mitigating Systems Cornerstone
attribute for protection against external factors. Specifically, a fire involving the
unauthorized transient combustibles could have affected a nearby electrical panel and
associated cable raceway containing mitigating system equipment important to safety.
2 Enclosure
The finding is of very low safety significance because the unauthorized transient
combustible materials would not have ignited from existing sources of heat or electrical
energy. The cause of the finding is related to the cross-cutting element of Problem
Identification and Resolution. (Section 1R05.2)
- Green. The inspectors identified an NCV of Technical Specification 3.1.5.a.2,
Amendment 38, for the standby liquid control (SLC) system being inoperable for longer
than the allowed time without the plant being placed in hot shutdown. The licensee
failed to properly evaluate the operability of SLC during sparging activities when the
issue was raised in 1999. As a result, the licensee initiated a 21-hour sparge on the
SLC tank on August 24, 1999, and failed to take actions in accordance with the
Technical Specifications. After the deficient evaluation was identified on June 1, 2006,
the licensee revised the applicable procedures to declare the SLC system inoperable
during sparging the SLC tank. The licensee entered this issue into their corrective
action program.
This finding is more than minor because it represented a programmatic deficiency in the
licensees chemical control program which affected the ability of the fire brigade to
respond to and mitigate the effects of a fire. Upon management review, the finding is of
very low safety significance because the quantities of the relevant chemicals were low
and the storage location was sufficiently remote from mitigating equipment.
(Section 1R05.3)
Cornerstone: Emergency Preparedness
- Green. The inspectors identified an NCV of license condition 2.C(9), for the failure to
appropriately store chemicals in accordance with the fire hazards analysis. The licensee
failed to evaluate the fire fighting response guidelines in NFPA-49 for various chemicals
brought into the protective area and, therefore, failed to appropriately store them as
required by the licensees fire hazards analysis. As a result, five normally stored
chemicals in the building have recommended fire fighting strategies that are inconsistent
with the licensees approved fire protection pre-plan. The licensee entered this issue
into their correction action program.
This finding is more than minor because it affected the equipment performance attribute
of the reactor safety cornerstone objective of ensuring the availability, reliability, and
capability of mitigating equipment to respond to initiating events to prevent undesirable
consequences. The finding is of very low safety significance because the total time of
sparging activities was short. (Section 1R15.2)
Cornerstone: Occupational Radiation Safety
- Green. A self-revealed NCV was identified for the licensees failure to comply with
Technical Specification 5.4.1.a, written procedures shall be established, implemented,
and maintained covering applicable procedures recommended in Regulatory
Guide 1.33. The licensee did not adequately control the modification of the ventilation
equipment used to vent airborne radioactive particulate to the refuel floor during reactor
vessel floodup. Consequently, while raising reactor vessel water level, the improper
venting led to personnel contaminations, uptakes of radioactive material, and the
3 Enclosure
evacuation of the Reactor Building. The licensee entered this issue into their corrective
action program and conducted an investigation into the event. The corrective actions
recommended the development and implementation of an acceptable methodology for
raising reactor water level.
This finding is more than minor because it affected the Occupational Radiation Safety
Cornerstone of Radiation Safety due to individual worker unplanned, unintended dose.
The finding was evaluated using the SDP and was determined to be a finding of very
low safety significance because there was not a substantial potential for overexposure
and the licensees ability to assess dose was not compromised. (Section 1R20)
B. Licensee-Identified Violations
A violation of very low safety significance, which was identified by the licensee, has been
reviewed by the inspectors. Corrective actions taken or planned by the licensee have
been entered into the licensees corrective action program. This violation and corrective
actions are listed in Section 4OA7 of this report.
4 Enclosure
REPORT DETAILS
Summary of Plant Status
Unit 2 began this inspection period shutdown for refueling outage 11 (RF11). Reactor
startup began on May 3 but was halted at 95 percent power on May 9 due to indications
of a fuel leak. Suppression testing commenced that same day, reducing reactor power
to approximately 63 percent until May 12 when the operators began increasing reactor
power after suppressing the fuel leak. On May 14, the reactor was at full power where it
remained at or near until May 19 when the operators began a reactor shutdown to
replace the leaking fuel assembly. After completing the work, operators began a reactor
startup on May 28. The reactor reached full power on May 30 where it remained at or
near until June 15 when an automatic reactor scram occurred as a result of a failure of
main unit transformer 2B. The failed transformer was disconnected and reactor startup
began on June 16. On June 21, the reactor reached 63 percent power (maximum
planned with transformer 2B out of service) and remained there for the remainder of the
inspection period.
1. REACTOR SAFETY
Cornerstone: Mitigating Systems, Barrier Integrity, Initiating Events, Emergency
Preparedness
1R01 Adverse Weather (71111.01A)
a. Inspection Scope
The inspectors reviewed licensee procedures for mitigating the effects of hot weather.
The inspectors reviewed severe weather procedures, emergency plan implementing
procedures related to severe weather, and annunciator response procedures, and
performed walkdowns. This included the reactor building and turbine building ventilation
preparations. Additionally, the inspectors reviewed condition assessment resolution
documents (CARD) and verified problems associated with adverse weather were
entered into the corrective action program with the appropriate significance
characterization.
These activities represented one hot weather systems preparation inspection sample.
b. Findings
No findings of significance were identified.
5 Enclosure
1R04 Equipment Alignments (71111.04)
.1 Partial System Walkdowns (71111.04Q)
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant
systems:
C Safety Relief Valves performed the week of April 3, 2006;
C SLC A performed the week of April 24, 2006;
C Division II Residual Heal Removal (RHR) and Residual Heat Removal Service
Water (RHRSW) Lineup performed the week of May 14, 2006;
C Standby Electrical Power (emergency diesel generator [EDG]) lineup performed
the week of May 14, 2006; and
C Division I RHR and RHRSW Shutdown Cooling performed the week of
May 21, 2006.
The inspectors selected these systems based on their risk significance relative to the
reactor safety cornerstones. The inspectors reviewed operating procedures, system
diagrams, Technical Specification (TS) requirements, Administrative TS, and the impact
of ongoing work activities on redundant trains of equipment in order to identify
conditions that could have rendered the systems incapable of performing their intended
functions. The inspectors also walked down accessible portions of the systems to verify
system components were aligned correctly.
In addition, the inspectors verified equipment alignment problems were entered into the
corrective action program with the appropriate significance characterization.
These activities represented five quarterly partial system walkdown inspection samples.
b. Findings
No findings of significance were identified.
.2 Complete System Walkdown (71111.04S)
a. Inspection Scope
The inspectors performed a complete system walkdown of the following risk-significant
system:
- General Service Water (GSW) performed the week of April 24, 2006
The inspectors reviewed operating procedures, system diagrams, TS requirements, and
applicable sections of the Updated Final Safety Analysis Report (UFSAR) to ensure the
correct system lineup. The inspectors verified acceptable material condition of system
components, availability of electrical power to system components, and that ancillary
equipment or debris did not interfere with system performance.
6 Enclosure
These activities represented one semi-annual complete system walkdown inspection
sample.
b. Findings
No findings of significance were identified.
1R05 Fire Protection (71111.05)
.1 Routine Resident Inspector Tours (71111.05Q)
a. Inspection Scope
The inspectors conducted fire protection tours of the following risk-significant plant
areas:
- Condensate Pump Room;
- Standby Gas Treatment, Pipe Room;
- Top of Torus;
- Hemyc Wrap for the Fire Barrier;
- Division I, RHR Pump Room;
- Division II, RHR Pump Room;
- Main Unit Transformer 2B; and
- Division II Electrical Switchgear Room.
The inspectors verified fire zone conditions were consistent with assumptions in the
licensee's fire hazards analysis. The inspectors walked down fire detection and
suppression equipment, assessed the material condition of fire fighting equipment, and
evaluated the control of transient combustible materials. In addition, the inspectors
verified fire protection related problems were entered into the corrective action program
with the appropriate significance characterization.
These activities represented eleven routine quarterly fire protection inspection samples.
b. Findings
No findings of significance were identified.
.2 RHR Complex, Division II EDG, Switchgear and Ventilation Rooms
a. Inspection Scope
The inspectors also conducted fire protection tours of the RHR complex, Division II
EDG, switchgear and ventilation rooms which are risk-significant plant areas.
7 Enclosure
The inspectors verified fire zone conditions were consistent with assumptions in the
licensee's fire hazards analysis. The inspectors walked down fire detection and
suppression equipment, assessed the material condition of fire fighting equipment, and
evaluated the control of transient combustible materials. In addition, the inspectors
verified fire protection related problems were entered into the corrective action program
with the appropriate significance characterization.
These activities represented one routine quarterly fire protection inspection sample.
b. Findings
Introduction: The inspectors identified an NCV of license condition 2.C(9) having very
low safety significance (Green) for the presence of unauthorized transient combustible
materials in the RHR complex.
Description: On May 15, 2006, the inspectors identified unauthorized transient
combustible materials in the RHR complex EDG 12 switchgear room. Specifically, the
inspectors identified an office chair and a plastic trash bin approximately half full of
paper secured approximately one foot from panel H21-P351, a safety-related electrical
panel for EDG 12 room ventilation, and associated cable raceway.
Section 9A.1.3.2.e of the UFSAR stated that the fire protection program had a
component to minimize the amount of combustibles to which safety-related areas may
be exposed. Procedure MOP11 implemented the fire protection program by prescribing
methods for controlling transient combustible material and the location of plant support
equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
Approval form be obtained before placing any support equipment in the RHR complex.
The procedural requirement existed to ensure the introduction of transient combustible
materials was reviewed by fire protection personnel. However, no Plant Support
Equipment Approval form was submitted for the chair and trash bin identified in the
EDG 12 switchgear room within the RHR complex.
After the inspectors informed the fire protection supervisor of the issue, the fire
protection supervisor initiated CARD 06-23388 to initiate corrective actions. Licensee
personnel performed a walkdown of the RHR complex and identified three additional
trash bins and two chairs in other switchgear rooms within the RHR complex. The trash
bins and chairs were removed from the switchgear rooms.
Analysis: The inspectors determined the licensees failure to properly control transient
combustibles was a performance deficiency because the licensee is expected to comply
with their fire hazards analysis and because it was within the licensees ability to foresee
and prevent. The finding was greater than minor in accordance with Inspection Manual
Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue
Disposition Screening, issued September 30, 2005, because the finding affected the
Mitigating Systems Cornerstone attribute for protection against external factors, i.e., fire.
Specifically, a fire involving the unauthorized transient combustibles could have affected
a nearby electrical panel and associated cable raceway containing mitigating system
equipment important to safety. The inspectors identified that a credible fire scenario
existed in that equipment important to safety was located within the zone of influence of
8 Enclosure
the unauthorized transient combustible materials as described by Table 2.3.2,
Calculated Values (in feet) for Use in the Ball and Column Zone of Influence Chart for
Fires in an Open Location Away from Walls of IMC 0609, Appendix F, Fire Protection
Significance Determination Process, issued February 28, 2005.
The inspectors completed a significance determination of this issue using IMC 0609,
Appendix F. The inspectors reviewed IMC 0609, Appendix F, Attachment 2,
Degradation Rating Guidance Specific to Various Fire Protection Program Elements,
and determined the unauthorized transient combustible materials represented a low
degradation rating because the materials would not have ignited from existing sources
of heat or electrical energy. As such, the finding screened to Green under Question 1 of
IMC 0609, Appendix F, Task 1.3.1, Qualitative Screening for All Finding Categories,
and was considered a finding of very low safety significance. The primary cause of this
finding was related to the cross-cutting aspect of problem identification and resolution
because the licensees response to several recent instances of unauthorized transient
combustibles was not effective in preventing this instance of unauthorized transient
combustibles.
Enforcement: License condition 2.C.(9) required the licensee to implement and
maintain in effect all provisions of the approved fire protection program as described in
the UFSAR. Section 9A.1.3.2.e of the UFSAR stated the fire protection program had a
component to minimize the amount of combustibles to which safety-related areas may
be exposed. Procedure MOP11 implemented the fire protection program by prescribing
methods for controlling transient combustible material and the location of plant support
equipment. Step 3.5.1 of procedure MOP11 required a Plant Support Equipment
Approval form be obtained before placing any support equipment in the RHR complex, a
safety-related area. Contrary to the above, on May 15, 2006, the inspectors identified
support equipment, i.e., a chair and a trash bin, had been placed in the EDG 12
switchgear room within the RHR complex without a Plant Support Equipment Approval
form having been obtained. Once identified, the licensee initiated CARD 06-23388,
performed a walkdown of the RHR complex, and removed unauthorized chairs and trash
bins from the switchgear rooms in the RHR complex. Because this violation is of very
low safety significance and because it was entered into the licensees corrective action
program as CARD 06-23388, this violation is being treated as an NCV, consistent with
Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-01:
Unauthorized Transient Combustibles in Safety-Related Areas.
.3 Fire Protection - Drill Observation (71111.05A)
a. Inspection Scope
The inspectors assessed fire brigade performance and the drill evaluators' critique
during an unannounced fire brigade drill on June 21, 2006. The drill simulated a fire in
the chemical storage room in the radioactive waste building. The inspectors focused on
the command and control of fire brigade activities, fire fighting and communication
practices, material condition and use of fire fighting equipment, and implementation and
adequacy of pre-planned fire fighting strategies.
9 Enclosure
These activities represented one annual fire protection - drill observation inspection
sample.
b. Findings
Introduction: The inspectors identified a Green NCV of license condition 2.C(9) for the
failure to appropriately store chemicals in accordance with the fire hazards analysis.
Description: The inspectors watched Fire Brigade Drill Scenario Number 6 which
involved a simulated fire in the chemical storage room on the first floor of the radioactive
waste building. Firefighters entered the room wearing full protective clothing and
positive-pressure, self-contained breathing apparatus. In accordance with fire protection
Pre-Plan FP-RDWST, Rev. 4, Radioactive Waste Building Zones 22, 23, 24, and 25, the
brigade simulated extinguishing the fire by using a water hose in a fog pattern.
The inspectors later questioned the adequacy of the fire protection pre-plan because it
did not appear to take into account differences in fire fighting strategies with the various
types of chemicals in the room. After reviewing the list of chemicals in the room against
the fire fighting strategies recommended by NFPA-49, Hazardous Chemicals Data 1994
Edition, the inspectors identified four chemicals normally stored in the room where
NFPA-49 recommends using special protective clothing when fighting a fire involving
those chemicals: monoethylamine solution, sodium hydroxide, potassium hydroxide,
and sulfuric acid. Additionally, NFPA-49 recommends against the use of water when
fighting fires involving sulfuric acid.
The inspectors reviewed the storage locations of these chemicals and determined they
were not segregated in such a manner to ensure a fire in that room did not involve any
of those chemicals. Further, the fire protection pre-plan contained no guidance on any
special precautions to be followed when fighting a fire involving any of those four
chemicals. The inspectors determined it was unreasonable to assume the responding
fire brigade would be able to easily determine what chemicals were on fire given the lack
of labeling and amount of smoke that likely would be present in the room during an
actual fire.
The licensees fire hazards analysis, as documented in UFSAR, Section 9A.5.G.3,
required chemicals be stored in accordance with the guidelines of NFPA-49. Although
the literal storage requirements for these chemicals were generally adhered to, e.g.,
stored in a cool, dry, ventilated room in metal cabinets, etc., the inspectors determined
the fire fighting strategies for the four chemicals of interest above were inseparable from
the storage guidelines because the licensee is expected to take all relevant information
into account when determining the appropriate chemical storage requirements. For
example, although NFPA-49 contained no guidance to store sulfuric acid separately
from nitric acid, the fact that water is suitable for fires involving nitric acid but not for fires
involving sulfuric acid logically concludes either, a) water should not be used if the
chemicals are in the same cabinet, b) the sulfuric acid should be stored in a separate
container, or c) the quantity of sulfuric acid is controlled sufficiently low so as to not
require segregation; none of which occurred. Likewise, because chemical suits are
recommended for those four chemicals but standard fire fighter turnout gear is suitable
for all other normally stored chemicals in the room, it is reasonable to expect the
10 Enclosure
licensee will take the emergency response personal protective equipment guidelines into
account when storing chemicals which the licensee also failed to do.
The inspectors questioned the licensee on how chemicals were controlled such that they
did not adversely affect the fire protection strategy and were informed that chemicals
are evaluated based on the effect they would have on the plant but not on the effect
they would have on fire fighting techniques. For example, there were no controls in
place to either ensure the fire brigade did not use water on fires involving sulfuric acid or
to control the amount of sulfuric acid below some threshold to preclude any alteration in
the fire fighting strategy.
Analysis: The inspectors determined the licensees failure to properly store chemicals in
accordance with guidelines contained in NFPA 49 was a performance deficiency
because the licensee is expected to comply with their fire hazards analysis and because
it was within the licensees ability to foresee and prevent. The finding is more than
minor because it represented a programmatic deficiency in the licensees chemical
control program which affected the ability of the fire brigade to respond to and mitigate
the effects of a fire. This finding affected the emergency planning cornerstone because
it affected the ability of the fire brigade to respond to a fire which could potentially affect
the licensees emergency plan.
The finding is not suitable for SDP evaluation, but has been reviewed by NRC
management and is determined to be a finding of very low safety significance (Green)
because the quantities of the relevant chemicals were low and the storage location was
sufficiently remote from mitigating equipment.
Enforcement: Fermi 2 Facility Operating License NPF-43, condition 2.C(9), required,
in part, that the licensee implement and maintain in effect all provisions of the
approved fire protection program as described in Section 9A of the UFSAR as
amended and approved in the Fermi 2 safety evaluation report through supplement 6.
UFSAR 9A.5.G.3 required hazardous chemicals be stored in accordance with the
guidelines of NFPA 49-1994, Hazardous Chemicals Data 1994 Edition. Contrary to
the above, on June 21, 2006, the licensee failed to utilize the guidelines contained in
NFPA 49-1994 when storing chemicals in the radioactive waste building. Because
this violation is of very low safety significance and because it was entered into the
licensees corrective action program as CARD 06-24243, this violation is being
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000341/2006003-02: Improper Storage of Chemicals Affecting Fire Fighting
Response.
1R06 Flood Protection (71111.06)
a. Inspection Scope
The inspectors performed an inspection related to the licensee's precautions to mitigate
the risk from internal flooding events. The inspectors performed a walkdown of the
following plant areas to assess the adequacy of watertight doors and verify drains and
sumps were clear of debris and were operable:
11 Enclosure
- High Pressure Coolant Injection Pump Room;
- Reactor Core Isolation Cooling Pump Room;
- Division I Core Spray Pump Room;
- Division II Core Spray Pump Room; and
- Auxiliary Building T Room.
The inspectors also reviewed the work activities associated with internal flooding to
verify identified problems were being entered into the corrective action program with the
appropriate characterization and significance.
These activities represented one internal flood protection inspection sample.
b. Findings
No findings of significance were identified.
1R07 Heat Sink Performance (71111.07A)
a. Inspection Scope
The inspectors reviewed completed test reports and observed the performance of
inspections for the RHR service water heat exchanger.
The inspectors selected this heat exchanger because its associated systems were risk
significant in the licensee's risk assessment and were required to support the operability
of other risk-significant, safety-related equipment. During these inspections, the
inspectors observed the as-found condition of the heat exchanger and verified no
deficiencies existed that would mask degraded performance. The inspectors discussed
the as-found condition as well as the historical performance of the heat exchanger with
engineering department personnel and reviewed applicable documents and procedures.
In addition, the inspectors verified heat sink problems were entered into the corrective
action program with the appropriate significance characterization, and completed
corrective actions were adequate and appropriately implemented.
These activities represented one heat sink performance inspection sample.
b. Findings
No findings of significance were identified.
1R11 Licensed Operator Requalification (71111.11Q)
a. Inspection Scope
On June 13, 2006, the inspectors observed an operations support crew during the
annual requalification examination in mitigating the consequences of events in
SS-OP-802-330, Anticipated Transient Without Scram with Small Steam Leak, Rev. 0,
dated January 26, 2006, on the simulator. The inspectors evaluated the following areas:
12 Enclosure
C licensed operator performance;
C crews clarity and formality of communications;
- ability to take timely actions in the conservative direction;
- prioritization, interpretation, and verification of annunciator alarms;
- correct use and implementation of abnormal and emergency procedures;
C control board manipulations;
C oversight and direction from supervisors; and
C ability to identify and implement appropriate TS actions and Emergency Plan
actions and notifications.
The crews performance in these areas was compared to pre-established operator
action expectations and successful critical task completion requirements.
These activities represented one quarterly licensed operator requalification inspection
sample.
b. Findings
No findings of significance were identified.
1R12 Maintenance Effectiveness (71111.12Q)
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following three
risk-significant systems:
C Station Blackout Diesel Generators CTG 11-1, 2, 3, 4, and 120 kV switchyard;
C RHR System A and B; and
C Molded Case Circuit Breakers.
The inspectors assessed performance issues with respect to the reliability, availability,
and condition monitoring of the system. Specifically, the inspectors independently
verified the licensee's actions to address system performance or condition problems in
terms of the following:
C implementing appropriate work practices;
C identifying and addressing common cause failures;
C scoping of systems in accordance with 10 CFR 50.65(b);
C characterizing system reliability issues;
C tracking system unavailability;
C trending key parameters (condition monitoring);
C ensuring 10 CFR 50.65(a)(1) or (a)(2) classification and/or re-classification; and
C verifying appropriate performance criteria for systems classified as (a)(2) and/or
appropriate and adequate goals and corrective actions for systems classified as
(a)(1).
In addition, the inspectors verified maintenance effectiveness issues were entered into
the corrective action program with the appropriate significance characterization.
13 Enclosure
These activities represented three quarterly maintenance effectiveness inspection
samples.
b. Findings
No findings of significance were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13Q)
.1 Routine Maintenance Risk Assessments
a. Inspection Scope
The inspectors reviewed the licensee's evaluation and management of plant risk for the
maintenance and operational activities affecting risk-significant and safety-related
equipment listed below:
- maintenance risk for week of April 2, 2006;
- maintenance risk for week of April 17, 2006;
- maintenance risk for week of April 30, 2006; and
- maintenance risk for week of June 26, 2006.
These activities were selected based on their potential risk significance relative to the
reactor safety cornerstones. As applicable for each activity, the inspectors reviewed the
scope of maintenance work, discussed the results of the assessment with the licensee's
probabilistic risk analyst and/or shift technical advisor, and verified plant conditions were
consistent with the risk assessment. The inspectors also reviewed TS requirements and
walked down portions of redundant safety systems, when applicable, to verify risk
analysis assumptions were valid and applicable requirements were met.
These activities represented four quarterly maintenance risk assessment and
emergency work control inspection samples.
b. Findings
No findings of significance were identified.
.2 Inadequate Maintenance Risk Assessment
a. Inspection Scope
The inspectors reviewed the activities surrounding the Division I battery load test
performed during RF11 to determine if the licensee appropriately considered the risk
impacts of performing the test. The inspectors interviewed licensee staff, reviewed
documents, and performed walkdowns. The inspectors considered ancillary equipment
affected by the test to determine what affect, if any, the test would have on it.
These activities represented one quarterly maintenance risk assessment and
emergency work control inspection sample.
14 Enclosure
b. Findings
Introduction: The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the
failure to perform an adequate risk assessment for the Division I battery load test.
Description: On April 3, 2006, the inspectors identified a temporary fan installed in the
blocked-open doorway to the dc motor control center (DC MCC) area. Upon entering
the room, the inspectors noticed that additional doors inside the DC MCC area leading
to each of the reactor protection system motor generator (RPSMG) set rooms were
open. After questioning why the doors were blocked open and a fan installed, the
inspectors learned operators took those actions to provide additional cooling to the
RPS MG sets because the Division I 130/260 VDC battery load surveillance test,
procedure 42.309.05, was in progress.
Because the air-cooled load bank used for the test was temporarily installed in the
DC MCC area, temperatures in the room started to increase after the test commenced.
However, two area room coolers were out of service due to a scheduled outage of the
GSW system which left the DC MCC, vital battery, battery charger, and RPS MG set
rooms with no cooling. In order to help prevent a loss of shutdown cooling, which would
have occurred had the RPS MG sets tripped, the operators had previously blocked
opened the doors to the RPS MG set rooms which further increased the temperature in
the DC MCC area. Operators then blocked open the double doors to the DC MCC area
and installed a large utility fan in the doorway to provide additional cooling to the area.
The test was successfully completed, temperatures dropped, and the fan was removed.
The outage risk associated with this test did not consider the effects it would have on
the key safety function of maintaining decay heat available due to the additional heat
from the load bank with no room cooling. Moreover, the outage risk associated with the
GSW outage assumed that the RPS MG sets would not be running. Consequently,
prudent risk management actions were not developed prior to performing the battery
load test. However, because operators installed a fan in the open doorway early
enough into the test, shutdown cooling remained in operation.
Analysis: The inspectors determined the failure to perform an adequate risk analysis of
maintenance activities prior to performing maintenance was a performance deficiency
because the licensee is expected to comply with the requirements of the maintenance
rule. This finding is more than minor because the licensees risk assessment failed to
consider maintenance activities that could increase the likelihood of an initiating event,
specifically a loss of shutdown cooling. In addition, this finding affected the initiating
event cornerstone because it is associated with an increase in the likelihood of an
initiating event. The inspectors utilized the maintenance risk and shutdown risk SDP to
assess the risk of this finding. The finding is of very low safety significance because the
finding did not affect the ability of operators to recover from a loss of shutdown cooling
had it occurred. The inspectors determined the cause of this finding impacted the
Human Performance cross-cutting area because the cause of the inadequate risk
assessment was due to a personnel error.
Enforcement: 10 CFR 50.65(a)(4) requires, in part, that before performing
maintenance activities, the licensee shall assess and manage the increase in risk
15 Enclosure
that may result from the proposed maintenance activities. Contrary to the above,
beginning on April 1, 2006, and continuing through April 6, 2006, the licensee
performed surveillance procedure 42.309.05 without adequately assessing and
managing the increase in risk prior to performing the activity. Because this violation is
of very low safety significance and because it was entered into the licensees corrective
action program as CARD 06-21892 and 06-24495, this violation is being treated as an
NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000341/2006003-03: Inadequate Maintenance Risk Assessment.
1R14 Personnel Performance During Non-Routine Plant Evolutions and Events (71111.14)
a. Inspection Scope
The inspectors reviewed the licensees actions in response to the following non-routine
events to ensure the licensee took appropriate actions in accordance with licensee
procedures:
- unplanned reactor building contamination, CARD 06-21534;
- control rod position indication malfunction, CARD 06-23491 & 06-23489;
- main turbine bypass valves opened at power, CARD 06-24113; and
- mode 5 reactor scram during installation of shorting links, CARD 06-23588.
The inspectors reviewed operator logs, procedures, corrective action documents, other
documents, and interviewed personnel. The inspectors also evaluated the licensees
operational decision making involved with these non-routine events.
These activities represented four inspection samples.
b. Findings
No findings of significance were identified.
1R15 Operability Evaluations (71111.15)
.1 Routine Review of Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following documents to ensure the identified condition did
not render the involved equipment inoperable or result in an unrecognized increase in
plant risk, and the licensee appropriately applied TS limitations and appropriately
returned the affected equipment to an operable status:
- CARD 06-23114, Motor Operator Valve Motor Replacement for RHR Shutdown
Cooling Inboard Suction Bypass Valve; and
- CARD 06-23898, Division II Emergency Equipment Cooling Water Makeup
Pump In-Service Test Flow Unattainable.
These activities represented two operability evaluation inspection samples.
16 Enclosure
b. Findings
No findings of significance were identified.
.2 Standby Liquid Control Operability During Air Sparging Operations
a. Inspection Scope
The inspectors reviewed the licensees practice of placing an air sparge on the SLC tank
to determine if system operability was justified. The inspectors reviewed previous
engineering evaluations to determine the technical adequacy of the conclusions. The
inspectors reviewed operator logs, TS, design basis documents, UFSAR, and other
documents. The inspectors interviewed operators, engineers, and other licensee staff.
These activities represented one operability evaluation inspection sample.
b. Findings
Introduction: The inspectors identified a Green NCV of TS for the SLC system being
inoperable for longer than the action time to be in hot shutdown with both SLC
subsystems inoperable.
Description: In April 1999, the licensee reviewed an operating experience report issued
by another licensee discussing the inoperability of the SLC system during air sparging
activities. Air sparging the SLC tank was done to facilitate mixing of the sodium
pentaborate in the tank and was performed prior to the monthly chemistry analysis and
after any chemical addition to the tank. The air sparge header was located near the
bottom of the tank in proximity to the SLC pump suction line. The concern was that if
the pumps were operating while the air sparge was operating, air could be drawn into
the pumps and compromise their ability to perform their design function. The licensee
initiated CARD 99-13240 to evaluate the applicability of the issue to Fermi.
The licensee determined that although pump performance would be impacted if the
pumps were required while an SLC tank air sparge was in progress, the pumps
remained operable. Based on input from the pump vendor, the licensee concluded that
entrained air in the pumped water would cause increased pump vibration and a
negligible reduction in delivered flow rate. Because the vendor stated the increased
vibration would only affect long-term pump reliability, the licensee concluded that
long-term pump degradation was not a concern because SLC had a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> mission
time.
In an effort to lessen the probability of requiring the SLC pumps during an actual event
while the air sparge was operating, the licensee identified the need to revise the system
operating procedures to minimize duration of sparge operations from hours to minutes.
The action to revise procedure 23.149, Standby Liquid Control System, was originally
due on June 30, 1999.
The inspectors reviewed the licensees evaluation and noted the CARD did not contain
either any documentation from the vendor or any attempt to quantify the reduction in
17 Enclosure
flow rate to ensure the minimum required flow was maintained. The inspectors asked
the licensee for the vendors recommendations in writing but were later told the pump
vendor declined to support their previous conclusion in writing. The inspectors were
concerned that if the pump vendor was unwilling to state in writing that the pumps would
operate for at least 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> during sparging, then pump operability was not justified.
The inspectors brought their concern to the licensee who entered the issue into their
corrective action program as CARD 06-23785 on June 1, 2006. After further review, the
licensee concluded that SLC operability during sparging could not be supported and
revised procedure 23.149 accordingly. Upon review of control room logs, the inspectors
determined that although the licensee significantly reduced the total sparging time since
1999, the tank was air sparged for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> on August 24, 1999, which exceeded the
time to be in hot shutdown of 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> with both SLC subsystems inoperable while in
Mode 1 or 2. In addition, the inspectors concluded the maximum unavailability in any
1-year period after identification of the issue in 1999 was approximately 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />.
Analysis: The inspectors determined the licensees failure to appropriately evaluate
SLC operability during sparging operations was a performance deficiency because the
licensee is expected to adequately evaluate issues that affect the operability of TS
equipment and because it was within the licensees ability to foresee and prevent. The
finding is more than minor because it affected the equipment performance attribute of
the reactor safety cornerstone objective of ensuring the availability, reliability, and
capability of mitigating equipment to respond to initiating events to prevent undesirable
consequences.
The inspectors assessed the finding using the SDP. Because the inspectors
considered this finding to represent an actual loss of a safety function of SLC, the
inspectors performed a phase 2 SDP analysis. A phase 3 analysis was subsequently
performed by the senior reactor analyst (SRA). The SRA performed the risk evaluation
using the Fermi Standardized Plant Analysis Risk (SPAR) Model, Level 1, Revision 3P,
Change 3.21, created October 2005. The SRA ran the SPAR model assuming common
cause failure of both SLC pumps, with an exposure time of 90 hours0.00104 days <br />0.025 hours <br />1.488095e-4 weeks <br />3.4245e-5 months <br />. Using the above
information the SRA obtained a change in core damage frequency (CDF) of 3.1E-8
(Green) for internal events. The dominant sequences involved a failure of the reactor to
scram after a transient, loss of condenser heat sink, and loss of main feedwater, and
failure of the SLC system.
Anticipated transient without scram events are not assumed to be caused by external
events and, therefore, the risk contribution from external events is insignificant.
Similarly, because the internal events CDF is less than 1E-7, large early release
frequency (LERF) is not significant per IMC 0609, Appendix H. The SRA concluded
the total CDF considering internal events, external events, and LERF is estimated at
3.1E-8 (Green).
Enforcement: Technical Specification 3.1.5.a.2, Amendment 38, required that while in
Modes 1 and 2, with the SLC system otherwise inoperable, the licensee must restore
the system to operable status within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or be in at least hot shutdown within the
next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and was in effect on August 24 and 25, 1999. Contrary to the above,
beginning on August 24, 1999, and continuing until August 25, 1999, while in Modes 1
18 Enclosure
and 2, the SLC system was inoperable for 21 hours2.430556e-4 days <br />0.00583 hours <br />3.472222e-5 weeks <br />7.9905e-6 months <br /> while the SLC tank was being air
sparged; therefore, on August 25, 1999, with the SLC system inoperable for greater
than 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />, the plant was not in at least hot shutdown. Because this violation is of
very low safety significance and because it was entered into the licensees corrective
action program as CARD 06-23785, this finding is being treated as an NCV, consistent
with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000341/2006003-04:
Improper Evaluation of Standby Liquid Control Operability During Tank Sparging.
.3 Inappropriate Use of Risk in Operability Evaluations
a. Inspection Scope
The inspectors reviewed CARD 06-23913 to ensure that the identified condition did not
render the involved equipment inoperable or result in an unrecognized increase in plant
risk and that the licensee appropriately applied TS limitations and appropriately returned
the affected equipment to an operable status.
These activities represented one operability evaluation inspection sample.
Introduction: The inspectors identified an Unresolved Item (URI) when the licensee
removed pipe insulation, credited for environmental qualification of nearby equipment,
while at power without an adequate engineering evaluation.
Description: On June 8, 2006, the licensee initiated CARD 06-23913 to request a work
request to replace contaminated insulation on the suction and discharge pipe for the B
RHR pump. As a result, Work Request (WR) 000Z062027 was released and work
began on June 13, 2006. While performing a plant tour on June 15, 2006, the
inspectors identified the insulation was missing from the suction pipe for the B RHR
pump and questioned the licensee if the insulation removal had an approved
engineering evaluation. Because the equipment was in a potentially harsh environment,
the uninsulated pipe would increase the temperature profile of the room during accident
conditions which could affect the environmental qualification of electrical equipment in
the room. The licensee stated the evaluation was documented in CARD 06-23913 and
concluded that removing the insulation while at power was acceptable.
The inspectors reviewed the subject evaluation and became concerned that one of the
assumptions for the evaluation was that an accident was not considered as credible
during the period of time the insulation was to be removed. Upon further review, the
inspectors learned the licensee used non-accident heat loads to determine the
environmental effects of removing the insulation. The licensees justification was that if
the total time the insulation was removed was less than 168 hours0.00194 days <br />0.0467 hours <br />2.777778e-4 weeks <br />6.3924e-5 months <br />, then the probability
of either a high energy line break or loss of coolant accident was negligible and, hence,
did not need to be assumed to occur.
The definition of operability stated, however, the equipment must be capable of
performing its specified function(s). The inherent assumption was the occurrence,
conditions, or event would exist and the safety function could be performed. Therefore,
19 Enclosure
the inspectors concluded the use of probabilities of the occurrence of accidents while
the insulation was removed was an unacceptable assumption in the subsequent
operability evaluation.
While reviewing this evaluation, the inspectors discovered the licensee used the
same method of evaluating on-line insulation removal since at least September 20,
2001, and found five additional CARDs where the licensee approved removing
insulation from equipment in potentially harsh areas while at power, likewise with
unacceptable evaluations. Because the extent of condition of this issue is potentially
significant and could extend to work other than on-line insulation removal, this item is
unresolved pending the inspectors review of the licensees full extent of condition
review and subsequent risk evaluation and is identified as Unresolved Item
(URI) 05000341/2006003-05: Inappropriate Use of Risk in Operability Evaluations.
1R19 Post-Maintenance Testing (71111.19)
a. Inspection Scope
The inspectors reviewed post-maintenance testing (PMT) activities associated with the
following scheduled maintenance:
- Division I Switchyard Modifications, EDP 31880;
- Feedwater Check Valve PMT, WR T210040100;
- Drywell Cooler Number 4 Replacement, WR 000Z052131;
- Reactor Recirculation Pump Discharge Valve B310SF031A, Stem Replacement,
WR 000Z050487;
- Main Steam Isolation Valve (MSIV), Limit Switch Replacement; and
- WR 000Z060156, Replace Control Rod Drive Pump Inboard Bearing Oil Level
Sight glass.
The inspectors reviewed the scope of the work performed and evaluated the adequacy
of the specified PMT. The inspectors verified the PMT was performed in accordance
with approved procedures, the procedures clearly stated acceptance criteria, and the
acceptance criteria were met. The inspectors interviewed operations, maintenance, and
engineering department personnel and reviewed the completed PMT documentation.
In addition, the inspectors verified PMT problems were entered into the corrective action
program with the appropriate significance characterization.
These activities represented seven PMT inspection samples.
b. Findings
No findings of significance were identified.
20 Enclosure
1R20 Refueling and Outage Activities (71111.20)
.1 Routine Refueling Outage Inspection Activities
a. Inspection Scope
The inspectors observed the licensees performance during RF11, which was in
progress at the beginning of this inspection and concluded on May 5, 2006.
This inspection consisted of a review of the licensees outage schedule, safe shutdown
plan and administrative procedures governing the outage, periodic observations of
equipment alignment, and plant and control room outage activities. Specifically, the
inspectors determined whether the licensee effectively managed elements of shutdown
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
power control, and containment integrity.
The inspectors performed the following activities daily, during the outage:
- attended control room operator and outage management turnover meetings to
verify the current shutdown risk status was well understood and communicated;
- performed walkdowns of the main control room to observe the alignment of
systems important to shutdown risk;
- observed the operability of reactor coolant system (RCS) instrumentation and
compared channels and trains against one another;
- performed walkdowns of the turbine, auxiliary, and reactor buildings and the
drywell to observe ongoing work activities, to ensure work activities were
performed in accordance with plant procedures, and to verify procedural
requirements regarding fire protection, foreign material exclusion, and the
storage of equipment near safety-related structures, systems, and components
were maintained;
- verified the licensee maintained secondary containment in accordance with TS
requirements; and
- reviewed selected issues the licensee entered into its corrective action program
to verify identified problems were being entered into the program with the
appropriate characterization and significance.
Additionally, the inspectors performed the following specific activities:
- monitored refueling activities to verify the licensee adhered to established
procedures and TS requirements for handling of irradiated fuel;
- performed drywell closeout;
- verified shutdown cooling tagouts;
- verified completion of restart restraint items; and
- observed control rod withdrawal to criticality and portions of the plant power
ascension.
In particular, the inspectors reviewed the licensees restart restraint process and verified
the closure of selected issues. Documents reviewed during these inspection activities
are listed at the end of this report.
21 Enclosure
Because inspection activities for this refueling outage constituted one inspection sample
in Inspection Report 05000341/2006002, and since only one sample is counted per
outage, the inspection activities for this inspection period do not constitute an additional
refueling and outage inspection sample.
b. Findings
Introduction: The inspectors identified a Green NCV of Technical Specification 5.4.1.a,
for the failure to adequately control the modification of the ventilation equipment used to
vent airborne radioactive particulate to the refuel floor during reactor vessel floodup.
Description: At 1450, on March 26, 2006, operators initiated core spray at approximately
3000 gpm to raise reactor water level, to permit removal of the reactor vessel head. The
reactor vessel head vent pipe had been disconnected, to permit installation of a
ventilation unit for the venting of gases to the refuel floor. The ventilation unit consisted
of a nominal 3600 scfm fan, a charcoal filter, and a HEPA particulate filter. Neither filter
had been recently tested. The ventilation unit was configured with two hoses placed to
take suction close to the reactor vessel head vent. The exhaust of the ventilation unit
ran to a point below an intake for the Standby Gas Treatment System (SGTS), to permit
capture of the exhaust by the SGTS.
At approximately 1500, the ventilation unit intake hoses were observed being pushed
away from the reactor vessel head vent, due to flow from the vent. Core spray was shut
down at 1502 and at 1504 visible moisture was seen being emitted from the vent. A
continuous air monitor on the refuel floor alarmed at 1510 and RP ordered the
evacuation of all but essential personnel from the refuel floor. By 1525 all personnel
were removed from the floor and shortly after this, the entire reactor building was
evacuated due to the spread of contamination. Decontamination of several workers was
required. Twenty-eight workers were whole body counted, with 26 showing uptakes of
varying levels of Co-60, Co-58, and Mn-54.
There were three conditions that contributed to the cause of the event. First of all,
coolant activity levels were higher than expected due to a crud burst during shutdown
and the temporary loss of RWCS allowed Co-60 to enter and remain in the coolant,
possibly plating out on reactor internals. The second condition related to the
temperature of the material vented from the reactor vessel head. Reactor vessel
outside shell temperatures indicated 215 degrees F, which equates to internal metal
temperatures above the atmospheric boiling point of water. This indicates that some of
the coolant flashed to steam as the level in the reactor vessel rose, which could increase
the carryover of coolant activity to the vented gas. The third condition was the
inadequate processing of vented material from the reactor vessel head. The venting of
the airborne radioactive particulate would not have resulted in building contamination
and personnel uptakes if the ventilation unit had effectively removed this material to the
SGTS.
The use of the ventilation system was not in accordance with its design configuration.
The ventilation system for previous outages had suction hoses connected to a hood that
was placed over the reactor vessel head vent, to improve the capture of vented material.
The use of the hood was discontinued due to its impact on water level instrumentation.
22 Enclosure
An engineering evaluation was not performed on the impact of the change in
configuration of the ventilation system. In addition, the exhaust arrangement from the
ventilation unit to the SGTS had not been evaluated for effectiveness. Licensee
Procedure MES12, Performing Temporary Modifications, requires the modification
process be followed and an evaluation be performed.
Furthermore, licensee procedural guidance did not exist for the overall process of taking
the operating reactor to a condition allowing fuel movement. The event could have been
prevented if appropriate acceptance criteria for allowable reactor vessel temperature
and coolant activity levels existed. Thus, the root cause of the event was determined to
be a procedural and programmatic weakness.
The licensee initiated CARD 06-21534, Continuous Air Monitor Alarm on Refueling
Floor, to track the investigation of the event in their CAP. The primary corrective action
recommendation is to develop and implement an acceptable methodology for raising
reactor vessel water level. In addition, the design and configuration of the current
ventilation exhaust capture system will be evaluated and modified, as appropriate to
assure that it is adequate for the expected reactor vessel fill rate and radioactive
material concentrations. The methodology may involve an alternate vent path, such as
using the attached piping to vent the reactor vessel to the drywell.
Analysis: The inspectors determined the licensees lack of control of the Temporary
Modification process constituted a design control issue. The licensees failure to
adequately control the process used to vent airborne radioactive particulate to the refuel
floor during reactor vessel floodup represents a performance deficiency as defined in
NRC Inspection Manual Chapter 0612, Appendix B, Issue Screening. The issue was
determined to be more than minor because if left uncorrected the issue could become a
more significant safety concern if coolant activity levels were higher or if the vessel was
flooded quicker.
The finding was assessed using NRC Inspection Manual Chapter 0609, Appendix C,
Occupational Radiation Safety Significance Determination Process due to individual
worker unplanned, unintended dose. The finding was determined to be of very low
safety significance because the inspectors answered, NO, to all four phase 1
screening questions.
Enforcement: Technical Specification 5.4.1.a requires that procedures recommended in
Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, be established,
implemented and maintained. Section 4.a of that document, in part requires
instructions for filling, venting, and draining the reactor pressure vessel. Contrary to the
above, the initial installation of the ventilation system and the changes made to the
ventilation system that was used as part of the reactor vessel floodup during outages
was not processed through the Temporary Modification Procedure. This finding is being
treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy and is
identified as NCV 05000341/2006003-06: Inadequate Controls for Venting the Reactor
Pressure Vessel Head. This issue is in the licensees corrective action program as
CARD 06-22667.
23 Enclosure
.2 Forced Outage 06-01
a. Inspection Scope
The inspectors observed the licensees performance during Forced Outage 06-01 from
May 20, 2006, through May 29, 2006, which was scheduled to locate and replace a
failed fuel assembly. During power ascension following RF11, operators identified a
potential fuel leak because off gas radiation levels were slightly elevated from normal.
Operators began suppression testing later that day, which identified the failed assembly.
Operators initiated a manual unit shutdown to replace the failed fuel. While the unit was
shutdown, additional assemblies subjected to similar flux profile histories were also
replaced although fuel sipping operations identified only one fuel assembly with a fuel
cladding defect.
This inspection consisted of a review of the licensees outage schedule, safe shutdown
plan and administrative procedures governing the outage, periodic observations of
equipment alignment, and plant and control room outage activities. Specifically, the
inspectors determined whether the licensee effectively managed elements of shutdown
risk pertaining to reactivity control, decay heat removal, inventory control, electrical
power control, and containment integrity.
The inspectors performed the same daily activities, during the outage as described in
Section 1R20.1 for the refueling outage.
These activities represented one forced outage inspection sample.
b. Findings
No findings of significance were identified.
.3 Forced Outage 06-02
a. Inspection Scope
The inspectors observed the licensees performance during Forced Outage 06-02 from
June 15, 2006, through June 17, 2006. On June 15, a reactor scram occurred due to a
main turbine generator trip which occurred when main unit transformer 2B failed. The
inspectors responded to the control room and to the transformer area to assess the
licensees response to the event.
This inspection consisted of a review of the licensees outage schedule, safe shutdown
plan and administrative procedures governing the outage, and plant and control room
outage activities. Specifically, the inspectors determined whether the licensee
effectively managed elements of shutdown risk pertaining to reactivity control, decay
heat removal, inventory control, and electrical power control.
24 Enclosure
The inspectors performed the following activities during the outage:
- attended control room operator and outage management turnover meetings to
verify the current shutdown risk status was well understood and communicated;
- performed walkdowns of the main control room to observe the alignment of
systems important to shutdown risk;
- observed the operability of RCS instrumentation and compared channels and
trains against one another; and
- observed control rod withdrawal to criticality and portions of the plant power
ascension.
These activities represented one forced outage inspection sample.
b. Findings
No findings of significance were identified.
1R22 Surveillance Testing (71111.22Q)
a. Inspection Scope
The inspectors reviewed the test results for the following activities to determine whether
risk-significant systems and equipment were capable of performing their intended safety
function and to verify testing was conducted in accordance with applicable procedural
and TS requirements:
- MSIV Limit Switch (routine);
- Integrity Test for Containment Penetrations X-7A, X-7B, X-7C, and X-7D (LLRT);
- Scram Nitrogen Accumulator Integrity Test (routine);
- Scram Discharge Volume Vent and Drain Valves Operability (routine);
- Secondary Containment Integrity Test (LLRT);
- MSIV Channel Functional Test (isolation valve);
- LOOP/LOCA Test (routine);
- Reactor Core Isolation Cooling System Automatic Actuation and Flow Test
(routine); and
- High Pressure Coolant Injection Flow Rate Test at 165 psig Reactor Steam
Pressure (routine).
The inspectors reviewed the test methodology and test results to verify equipment
performance was consistent with safety analysis and design basis assumptions. In
addition, the inspectors verified surveillance testing problems were being entered into
the corrective action program with the appropriate significance characterization.
These activities represented seven routine, two local leak rate test (LLRT), and one
containment isolation valve surveillance inspection samples.
25 Enclosure
b. Findings
No findings of significance were identified.
1EP6 Drill Evaluation (71114.06)
a. Inspection Scope
The inspectors observed the licensee perform classifications and protective action
recommendations during licensed operator requalification training on June 20, 2006.
The inspectors observed activities in the control room simulator. The inspectors also
attended the post-drill critique in the simulator. The focus of the inspectors activities
was to note any weaknesses and deficiencies in the shift managers performance as
emergency director and ensure the licensee evaluators noted the same weaknesses
and deficiencies and entered them into the corrective action program. As part of the
inspection, the inspectors reviewed the drill package included in the list of documents
reviewed at the end of this report.
These activities represented one drill evaluation inspection sample.
b. Findings
No findings of significance were identified.
2OS1 Access Control to Radiologically Significant Areas (IP 71121.01)
.1 Plant Walkdowns and Radiation Work Permit Reviews
a. Inspection Scope
The inspectors reviewed licensee controls and surveys in the following three
radiologically significant work areas within radiation areas, high radiation areas and
airborne radioactivity areas in the plant and reviewed work packages which included
associated licensee controls and surveys of these areas to determine if radiological
controls including surveys, postings and barricades were acceptable:
- Turbine Building Main Steam Reheater Replacement;
- Drywell Activities; and
- Refuel Floor Activities.
These activities represented one inspection sample.
The inspectors reviewed the radiation work permits (RWPs) and work packages used to
access the three areas and other high radiation work areas to identify the work control
instructions and control barriers that had been specified. Electronic dosimeter alarm set
points for both integrated dose and dose rate were evaluated for conformity with survey
indications and plant policy. Workers were interviewed to verify they were aware of the
actions required when their electronic dosimeters noticeably malfunctioned or alarmed.
26 Enclosure
These activities represented one inspection sample.
The inspectors walked down and surveyed (using an NRC survey meter) the three areas
to verify the prescribed RWPs, procedure, and engineering controls were in place,
licensee surveys and postings were complete and accurate, and air samplers were
properly located.
These activities represented one inspection sample.
The inspectors reviewed RWPs for the following airborne radioactivity areas to verify
barrier integrity and engineering controls performance, e.g., high efficiency particulate
air filter ventilation system operation, and to determine if there was a potential for
individual worker internal exposures of greater than 50 millirem committed effective
dose equivalent. There were no areas where there was a potential for individual worker
internal exposures of greater than 50 millirem committed effective dose equivalent.
Work areas having a history of, or the potential for, airborne transuranic isotopes were
evaluated to verify the licensee had considered the potential for transuranic isotopes
and provided appropriate worker protection. There where no areas having a history of,
or the potential for, airborne transuranic isotopes.
These activities represented one inspection sample.
The adequacy of the licensees internal dose assessment process for any actual internal
exposures greater than 50 millirem committed effective dose equivalent was assessed.
There were no internal exposures greater than 50 millirem committed effective dose
equivalent.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.2 Problem Identification and Resolution
a. Inspection Scope
The inspectors reviewed three corrective action reports related to access controls and
high radiation area radiological incidents. Staff members were interviewed and
corrective action documents were reviewed to verify that follow-up activities were being
conducted in an effective and timely manner commensurate with their importance to
safety and risk based on the following:
- initial problem identification, characterization, and tracking;
- disposition of operability/reportability issues;
- evaluation of safety significance/risk and priority for resolution;
- identification of repetitive problems;
- identification of contributing causes;
- identification and implementation of effective corrective actions;
27 Enclosure
- resolution of NCVs tracked in the corrective action system; and
- implementation/consideration of risk-significant operational experience feedback.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.3 Job-In-Progress Reviews
a. Inspection Scope
The inspectors observed the following three jobs that were being performed in radiation
areas, airborne radioactivity areas, or high radiation areas for observation of work
activities that presented the greatest radiological risk to workers:
- Drywell Cooler Number Four Removal;
- Cutout and Replace Check Valve E1100F031A; and
- Perform Refuel Activities.
The inspectors reviewed radiological job requirements for the three activities including
RWP requirements and work procedure requirements, and attended As-Low-As-Is-
Reasonably-Achievable (ALARA) job briefings.
These activities represented one inspection sample.
Job performance was observed with respect to these requirements to verify radiological
conditions in the work area were adequately communicated to workers through pre-job
briefings and postings. The inspectors also verified the adequacy of radiological
controls including required radiation, contamination, and airborne surveys for system
breaches; radiation protection job coverage which included audio and visual surveillance
for remote job coverage; and contamination controls.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.4 Radiation Worker Performance
a. Inspection Scope
During job performance observations, the inspectors evaluated radiation worker
performance with respect to stated radiation protection work requirements and
evaluated whether workers were aware of the significant radiological conditions in their
workplace, the RWP controls and limits in place, and that their performance had
accounted for the level of radiological hazards present.
28 Enclosure
These activities represented one inspection sample.
The inspectors reviewed radiological problem reports which found the cause of the
event was due to radiation worker errors to determine if there was an observable pattern
traceable to a similar cause, and to determine if this perspective matched the corrective
action approach taken by the licensee to resolve the reported problems. These
problems, along with planned and taken corrective actions were discussed with the
Radiation Protection Manager.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.5 Radiation Protection Technician (RPT) Proficiency
a. Inspection Scope
During job performance observations, the inspectors evaluated RPT performance with
respect to radiation protection work requirements and evaluated whether they were
aware of the radiological conditions in their workplace, the RWP controls and limits in
place, and if their performance was consistent with their training and qualifications with
respect to the radiological hazards and work activities.
These activities represented one inspection sample.
The inspectors reviewed two radiological problem reports which found the cause of the
event was radiation protection technician error to determine if there was an observable
pattern traceable to a similar cause, and to determine if this perspective matched the
corrective action approach taken by the licensee to resolve the reported problems.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA) (IP 71121.02)
.1 Inspection Planning
a. Inspection Scope
The inspectors reviewed plant collective exposure history, current exposure trends,
ongoing and planned activities in order to assess current performance and exposure
challenges. This included determining the plants current 3-year rolling average for
collective exposure in order to help establish resource allocations and to provide a
perspective of significance for any resulting inspection finding assessment.
29 Enclosure
These activities represented one inspection sample.
The inspectors reviewed the outage work scheduled during the inspection period and
associated work activity exposure estimates for the following five work activities which
were likely to result in the highest personnel collective exposures:
- Drywell Cooler Number Four Removal;
- Cutout and Replace Check Valve E1100F031A;
- Refuel Floor Activities;
- Main Steam Reheater Replacement; and
- In-Service Inspections.
These activities represented one inspection sample.
The inspectors determined site specific trends in collective exposures and source-term
measurements. The inspectors reviewed procedures associated with maintaining
occupational exposures ALARA and processes used to estimate and track work activity
specific exposures.
These activities represented two inspection samples.
b. Findings
No findings of significance were identified.
.2 Radiological Work Planning
a. Inspection Scope
The inspectors evaluated the licensees list of planned work activities for RF11 ranked
by estimated exposure that were in progress and reviewed the following three work
activities of exposure significance:
- 06-1113, CRD Exchange;
- 06-1205, East/West MSR Replacement; and
- 06-1124, Drywell Cooler Number Four Removal.
For these three activities, the inspectors reviewed the ALARA work activity evaluations,
exposure estimates, and exposure mitigation requirements in order to verify the licensee
had established procedures and engineering and work controls that were based on
sound radiation protection principles in order to achieve occupational exposures that
were ALARA. This also involved determining that the licensee had reasonably grouped
the radiological work into work activities, based on historical precedence, industry
norms, and/or special circumstances.
The inspectors compared the results achieved including dose rate reductions and
person-rem used with the intended dose established in the licensees ALARA planning
for these three work activities. Reasons for inconsistencies between intended and
actual work activity doses were reviewed.
30 Enclosure
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.3 Verification of Dose Estimates and Exposure Tracking Systems
a. Inspection Scope
The licensees process for adjusting exposure estimates or re-planning work, when
unexpected changes in scope, emergent work or higher than anticipated radiation levels
were encountered, was evaluated. This included determining that adjustments to
estimated exposure (intended dose) were based on sound radiation protection and
ALARA principles and not adjusted to account for failures to control the work. The
frequency of these adjustments was reviewed to evaluate the adequacy of the original
ALARA planning process.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
.4 Job Site Inspections and ALARA Control
a. Inspection Scope
The inspectors observed the following five jobs that were being performed in radiation
areas, airborne radioactivity areas, or high radiation areas for observation of work
activities that presented the greatest radiological risk to workers.
- Drywell Cooler Number Four Removal;
- Cutout and Replace Check Valve E1100F031A;
- Refuel Floor Activities;
- Main Steam Reheater Replacement; and
- In-Service Inspections.
The licensees use of engineering controls to achieve dose reductions was evaluated to
verify procedures and controls were consistent with the licensees ALARA reviews,
sufficient shielding of radiation sources was provided for, and the dose expended to
install/remove the shielding did not exceed the dose reduction benefits afforded by the
shielding.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
31 Enclosure
.5 Radiation Worker Performance
a. Inspection Scope
Radiation worker and RPT performance was observed during work activities being
performed in radiation areas, airborne radioactivity areas, and high radiation areas that
presented the greatest radiological risk to workers. The inspectors evaluated whether
workers demonstrated the ALARA philosophy in practice by being familiar with the work
activity scope and tools to be used, by utilizing ALARA low dose waiting areas, and that
work activity controls were being complied with. Also, radiation worker training and skill
levels were reviewed to determine if they were sufficient relative to the radiological
hazards and the work involved.
These activities represented one inspection sample.
b. Findings
No findings of significance were identified.
4. OTHER ACTIVITIES (OA)
4OA2 Identification and Resolution of Problems (71152)
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As discussed in previous sections of this report, the inspectors routinely reviewed issues
during baseline inspection activities and plant status reviews to verify they were being
entered into the licensee's corrective action system at an appropriate threshold,
adequate attention was being given to timely corrective actions, and adverse trends
were identified and addressed.
b. Findings
No findings of significance were identified.
.2 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a screening review of each item entered into the licensees
corrective action program to identify trends that might indicate the existence of a more
significant safety issue. The inspectors considered repetitive or closely related issues
that may have been documented by the licensee outside the normal corrective action
program, such as in:
C trend reports or performance indicators,
C major equipment problem lists,
32 Enclosure
C repetitive and/or rework maintenance lists,
C departmental problem/challenges lists,
C system health reports,
C quality assurance audit/surveillance reports,
C self assessment reports,
C maintenance rule assessments, or
C corrective action backlog lists.
The inspectors verified the licensee was identifying issues at an appropriate threshold
and entering them into their corrective action program by comparing those issues
identified by the NRC during the conduct of the plant status and inspectable area
portions of the program with those issues identified by the licensee.
b. Issues
Unidentified drywell leakage was fluctuating after startup from RF11 but has since
leveled out. From the lowest value, unidentified leakage has increased from about
0.06 gpm to an average daily value of 0.14 gpm. Additionally, the inner seal pressure
for the B reactor recirculation pump has been fluctuating by as much as 40-60 psig;
however, there does not appear to be a correlation between the seal pressure
oscillations and drywell leakage. These issues are in the licensees corrective action
program as CARDs 06-24313 for the unidentified leakage and 06-23791 for the seal
pressure oscillations.
4OA3 Event Followup (71153)
.1 Reactor Scram due to Main Transformer Fault
a. Inspection Scope
As described in Section 1R20.3 of this report, the inspectors responded to the control
room on June 15, 2006, when the reactor automatically shut down as a result of the
failure of main unit transformer 2B. The inspectors observed plant parameters and
status, evaluated the performance of mitigating systems and licensee actions, confirmed
that the licensee properly classified the event in accordance with emergency action level
procedures and made timely notifications to NRC and state/county governments, as
required by 10 CFR 50.72 (Event Number 42643). The inspectors determined and
communicated details regarding the event to NRC management, risk analysts and
others in Region III and Headquarters as input to an evaluation per Management
Directive 8.3 for determining the appropriate level of event response. Based on the
events that occurred, routine resident inspection efforts were deemed appropriate.
b. Findings
No findings of significance were identified.
33 Enclosure
.2 Review of Licensee Event Reports (LER)
a. (Closed) LER 50-341/2006-001: At 0039 hours4.513889e-4 days <br />0.0108 hours <br />6.448413e-5 weeks <br />1.48395e-5 months <br /> on April 1, 2006, Fermi 2 feedwater line
check valves B2100F010A and B2100F076A failed their LLRT. The air leakage rate of
the inboard check valve B2100F010A was 324.21 standard cubic feet per hour (SCFH),
and the leakage rate of outboard check valve B2100F076A was above the
measurement capability of the leak rate monitor. The penetration (X-9A) minimum-
pathway air leakage value was determined to be 324.21 SCFH which is greater than the
allowable containment leakage rate (La) value of 296.3 SCFH per TS 5.5.12 and higher
than the allowable secondary containment bypass leakage rate of 0.1 La or 29.63 SCFH
per TS Surveillance Requirement 3.6.1.3.11. The B2100F076A failure was attributed to
soft seat degradation which was primarily caused by extending its service time to three
operating cycles. The B2100F010A valve failure was attributed to soft seat degradation
due to a slight misalignment of the valve disc to the in-body seat, compounded by wear
between the internal shaft and valve disc. The slight misalignment caused the soft seat
along the top portion of the disc to contact the seat first, resulting in a scraping action as
the disc flexed to its full seat position. For both valves, the soft seats were replaced,
and the soft seat service time has been limited to two operating cycles. The internal
shaft for the B2100F010A valve was replaced, and the alignment between the disc and
the valve seat was adjusted. Both valves were retested and met their associated LLRT
acceptance criteria prior to restart of the unit.
The LER was reviewed by the inspectors. No findings of significance were identified
and no violation of NRC requirements occurred. The licensee documented the LLRT
failure in CARD 06-21751. This LER is closed.
4OA6 Exit Meetings
.1 Exit Meeting Summary
On July 11, 2006, the inspectors presented the inspection results to Mr. D. Cobb and
other members of licensee management at the conclusion of the inspection. The
inspectors asked the licensee whether any material examined during the inspection
should be considered proprietary. No proprietary information was identified.
.2 Interim Exit Meetings
On April 7, 2006, an interim exit meeting was conducted for the Access Control to
Radiological Areas and ALARA inspection with Mr. Kevin Hlavaty, Plant Manager, and
other licensee staff.
4OA7 Licensee-Identified Violations
The following violation of very low significance was identified by the licensee and is a
violation of NRC requirements, which meet the criteria of Section VI of the NRC
Enforcement Manual, NUREG-1600, for being dispositioned as an NCV.
34 Enclosure
Cornerstone: Public Radiation Safety
The licensees procedure 67.000.103, Surveying of Outgoing Shipments, directs the
staff to survey outgoing vehicles used to carry an exclusive use shipment of radioactive
material. The procedure relies on the proper identification of the incoming shipment as
an exclusive use shipment. This procedure is used to implement the requirements of
49 CFR 173.443 and 49 CFR 177.843 that require the specific release survey of
vehicles in exclusive use situations. Contrary to the above, and as described in
CARD 06-21389, on March 20, 2006, an exclusive use radioactive material shipment
was received by the licensee. The shipment contained one package of Limited Quantity
radioactive material and four boxes of non-radioactive material and the radiation
protection staff assigned to accept the shipment incorrectly identified the shipment as a
non-exclusive use shipment. After the packages were removed from the conveyance,
the vehicle was released without the required survey. This was identified by licensee
supervision but not before the vehicle had departed the site. The carrier was contacted
and the vehicle returned to the licensees site before further transportation activity had
commenced and a survey was completed. No contamination was found and no dose
rates above background were identified. The finding is of very low safety significance
because it did not result in an unmonitored release nor were any dose limits
approached.
ATTACHMENT: SUPPLEMENTAL INFORMATION
35 Enclosure
KEY POINTS OF CONTACT
Licensee
D. Gipson, Chief Nuclear Officer
D. Cobb, Assistant Vice President, Nuclear Generation
K. Hlavaty, Plant Manager
S. Bartman, Nuclear Production
J. Davis, Manager, Outage Management
R. Gaston, Licensing Manager
S. Hassoun, Principal Engineer, Licensing
H. Higgins, Radiation Protection Manager
J. Korte, Manager, Nuclear Security
J. Plona, Engineering Director
NRC
C. Lipa, Chief, Division of Reactor Projects, Branch 4
1 Attachment
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000341/2006003-05 URI Inappropriate Use of Risk in Operability Evaluations
(Section 1R15.3)
Opened and Closed
05000341/2006003-01 NCV Unauthorized Transient Combustibles in Safety-Related
Areas (Section 1R05.2)05000341/2006003-02 NCV Improper Storage of Chemicals Affecting Fire Fighting
Response (Section 1R05.3)05000341/2006003-03 NCV Inadequate Maintenance Risk Assessment
(Section 1R13.2)05000341/2006003-04 NCV Improper Evaluation of Standby Liquid Control Operability
During Tank Sparging (Section 1R15.2)05000341/2006003-06 NCV Inadequate Controls for Venting the Reactor Pressure
Vessel Head (Section 1R20.1)
Closed
05000341/2006-001 LER Excessive Feedwater Check Valve Leakage at Containment
Discussed
None.
2 Attachment
LIST OF DOCUMENTS REVIEWED
The following is a list of documents reviewed during the inspection. Inclusion on this list does
not imply that the NRC inspectors reviewed the documents in their entirety but rather that
selected sections of portions of the documents were evaluated as part of the overall inspection
effort. Inclusion of a document on this list does not imply NRC acceptance of the document or
any part of it, unless this is stated in the body of the inspection report.
1R01: Adverse Weather Protection
CARD 06-23861, 06/05/06; Procedure Enhancement for TBHVAC (NRC Comment)
Procedure 27.000.06, Rev 0, 02/27/03; Performance Evaluation Procedure, Hot Weather
Operations
Open/Closed Work Requests by Related Work Code; 05/04/06
1R04: Equipment Alignment
Drawing 6M721-5706-3, 2/16/00; RHR Service Water Make Up Decant and Overflow Systems
Functional Operating Sketch
Drawing 6M721-5706-1, 3/5/04; Residual Heat Removal (RHR) Division II Functional Operating
Sketch
03-00120, 01/02/03; Pinhole leak in piping
03-13694, 6/17/03; Document the Condition of General Service Water Piping
04-24918, 10/25/04; P4100F402A installed at the bottom of the pipe
06-11615, 05/19/06; EDG Electrical Lineup Load Description Changes
06-21618, 03/28/06; E1100F050A Failed PI Leak Test SR 3.4.5.1
06-22730, 4/24/06; NRC-Identified Concerns in GSW Pumphouse
06-23447, 05/18/06; 23.205 Att 1B enhancement
06-23494, 05/20/06; E1100F050A actuator failed to open valve
23.131, Rev.86; General Service Water System
43.000.005, Rev. 30; Visual Examination of Piping and Components (VT-2)
23.208, Rev. 81; RHR Complex Service Water Systems
23.205, Rev. 94; Residual Heat Removal System
1R05: Fire Protection
CARD 06-23365; Door is not latching; Dated May 15, 2006 (NRC-Identified)
CARD 06-23388; Transient Combustibles in the RHR; Dated May 16, 2006 (NRC-Identified)
MOP11; Fire Protection; Revision 10
Fire Brigade Drill Scenario 6, Rev. 11/29/94; First Floor Radioactive Waste Chemical Lab
Storage Area
Fire protection Pre-Plan FP-RDWST, Rev. 4; Radwaste Building Zones 22, 23, 24, and 25
1R06: Flood Protection Measures
CARD 06-21354; High Pressure Coolant Injection Room Flooded due to Drains backing Up;
3/18/06
CARD 06-22600; Moderate Energy Line Break Evaluation; 4/21/06 (NRC-Identified)
3 Attachment
Nuclear Generation Memo TMPE-94-0308; May 18, 1994; Flood Protection Review
6M721-2223, Rev U, 11/24/06; Diagram Equipment Drains All Floors Auxiliary and Reactor
Buildings
6M721-2224, Rev W, 11/24/04; Diagram Floor Drains All Floors Auxiliary and Reactor Buildings
6M721-2032, Rev BO, 04/19/06; Sump Pump Diagram Radwaste System
6M721-2032-1, Rev AI, 04/19/06; Sump Pump Diagram Radwaste System
1R07: Heat Sink Performance
WR TG25060421; Perform RHR Division II Heat Exchanger Performance Test; 3/22/06
1R11: Licensed Operator Requalification
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Leak; 1/26/06
1R12: Maintenance Effectiveness
Design Specification 3071-128-EZ-06; Electrical Design Instructions Molded Case Circuit
Breakers
Maintenance Rule Conduct Manual MMR, Appendix E, Rev 4; Maintenance Rule SSC Specific
Functions
Memo dtd 01/30/06, TMIS-06-0011; Summary of Expert Panel Meeting 184 Conducted
January 24, 2006
CTG11-1 Get Well Plan; July 2003
Deviation Event Report 93-0528, 09/15/93
Vendor Manual VME5-18, Rev 0; Spectrum Technologies, Series 5600, MCC
CARD 97-10182, 10/27/97; Defective Molded Case Circuit Breaker
CARD 03-01098,05/30/03; Reactor Protection System - Function Failure
03-19510,07/20/03; Safety Eval 95-0002 is Used as an Operability Evaluation for LPCI with the
RHR Minimum Flow Valves Open
CARD 04-22685, 07/02/04; Generator Transformer - Function Failure
CARD 04-23307. 08/03/04; Motor Control Centers & Dist. Cabinets
CARD 05-23490, 06/21/05; Auxiliary Electrical - Function Failure
CARD 06-21363, 04-02-06; Auxiliary Electrical - Function Failure
CARD 06-21527, 04/09/06; Residual Heat Removal System - Function Failure
CARD 06-22270, 04/12/06, Maintenance Rule Function T4100-09 should be included in
Maintenance Rule Scope Investigation
Procedure 35.306.008, Rev 46; Maintenance Procedure, ITE Gould Motor Control Center Load
Compartment
Procedure 35.306.018, Rev 5; Maintenance Procedure, Spectrum Technology Motor Control
Center Load Compartment
1R13: Maintenance Risk Assessment and Emergent Work Evaluation
Fermi 2 Daily Plant Status, April 2, 2006
Schedulers Evaluation for Fermi 2, April 2, 2006
Fermi 2 Daily Plant Status, April 17, 2006
Schedulers Evaluation for Fermi 2, April 17, 2006
4 Attachment
Fermi 2 Daily Plant Status, April 30, 2006
Schedulers Evaluation for Fermi 2, April 30, 2006
Fermi 2 Daily Plant Status, June 26, 2006
Schedulers Evaluation for Fermi 2, June 26, 2006
CARD 06-21892, 4/4/06; NRC Questions related to Temporary Cooling Installed for Division I
Battery Test (NRC-Identified)
CARD 06-24495, 7/7/06; Work Risk Assessment and Temporary Equipment Controls
(NRC-Identified)
WR 0219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-1 Only)
WR 1219060414; Perform 42.309.05 Division I (5 Year) 130/260 VDC batter Check (2A-2 Only)
1R14: Non-Routine Events
CARD 06-24113; Main Steam Bypass Valves Opened Unintentionally During Power Ascension;
6/18/06
CARD 06-23588; Mode 5 Reactor SCRAM During Installation of SRM Shorting Links; 5/24/06
CARD 06-23501; Full In Light for Control Rod 50-27 on Full Core Display is Intermittent;
5/20/06
1R15: Operability Evaluations
Drawing - 5744, Rev. BK; Emergency Equipment Cooling Water Division I; 11/23/05
WR 000Z060107; Remove and Reinstall Insulation on E1100F031B; 2/9/06
WR 000Z062027; Replace Contaminated Insulation; 6/12/06
CARD 06-24156; Affects of Accidents not Addressed in Insulation Removal Evaluation for
E1100F031B; 6/20/06 (NRC Identified)
CARD 01-17302; There are no Site Guidelines for Insulation Removal on Operable Equipment;
8/14/01
CARD 06-23898; EECW M/U Pump IST Flow Unattainable; 6/7/06
CARD 02-14782; Engineering Evaluation for On-Line Insulation Removal; 6/27/02
CARD 03-16498; Engineering Evaluation for On-Line Insulation Removal; 9/9/03
CARD 05-21940; Engineering Evaluation for On-Line Insulation Removal; 3/23/05
CARD 06-23913; Replace Contaminated Insulation; 6/8/06
CARD 06-23785; Standby Liquid Control Operability During Sparging Activities; 6/1/06 (NRC-
Identified)
CARD 99-13240; Inoperability of Standby Liquid Control During Air Sparging; 4/15/99
1R19: Post-Maintenance Testing
EDP - 31880 120 KV Switchyard Upgrade
Engineering Change Request 33690-1, Rev A, 03/14/06; Replacement of Drywell Cooler Coils
T470B003 and T4700B004
Equivalent Replacement Evaluation (ERE) 34173, Rev 0, 04/18/06; E1150F608 MOV Motor
Replacement
Oil Sample Analysis Reports for C1106C001A, E Control Rod Drive Pump; 01/01/06 -
06/29/06
CARD 06-22258, 04/12/06; CTG equipment issues discovered during IPTE 04-02
CARD 06-22982, 4/30/06; Inboard MSIV A will not slow close
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
5 Attachment
CARD 06-22634, 4/22/06; A Inboard MSIV limit switch, PIS B21N572A, will not change state
Drawing SD-F-0179, Rev. A, 9/25/05; Diagram Line Breaker Control 120KV, POS GK
Drawing SD-2500-01, Rev. A, 2/28/06; One Line Diagram Plant 4160V & 480V
Drawing SD-2500-02, Rev. A, 2/23/06; One Line Diagram 13.8KV
Drawing SD-F-0001, Rev. A, 2.23/06; One Line Diagram 120 KV Switchyard
IPTE 04-02, 120KV Switchyard Upgrade
Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
24.206.01, Rev 63, 05/08/06; RCIC System Pump and Valve Operability Test
43.000.005, Rev 30, 03/22/06; Visual Examination of Piping and Components (VT-2)
43.401.303, Rev 32, 10/24/05; Local Leakage Rate Testing for Penetration X-9A
WR B203040100, 04/10/06; B2100F010A - Nuclear Boiler Feedwater Supply Inboard Primary
Containment Check Valve
WR 000Z050487, 04/29/06;B3105F031A - Reactor Recirculation Pump A Discharge Valve
WR T210040100, 04/10/06; B2100F076A - Nuclear Boiler Feedwater Supply Check Valve
WR 000Z052131, 04/19/06; Inservice Testing, Drywell Cooler #4
WR 000Z060156, 6/19/06; E Control Rod Drive Inboard Pump Bearing Oil level Bulls eye Dirty
1R20: Refueling and Outage Activities
Apparent Cause Determination for Damage Found in the Main Generator During RF11 Robot
Inspections CARD 06-21922
Inspection Requirement Form, Requisition Number: 9086929; 04/19/2006
Drawing 6M721-3722, Rev A; Flow Diagram & Details of Purging Unit - Reactor Pressure
Vessel - Unit 2
Safety Tagging Record 2006-002089
CARD 06-21534, 03/26/2006; Continuous Air Monitor Alarm on Refueling Floor
CARD 06-22590, 04/21/2006; NRC identified concern with Div 1 Core Spray and Defense in
Depth Investigation
CARD 06-22642, 04/22/2006; Are EDG Surveillances Testing What They Are Setup to Test
CARD 06-22667, 04/23/2006; RPV Venting Unit Configuration Control Discrepancies
CARD 06-23114, 05/03/2006; NRC Concern: Review of ERE-34173 E1150F608 MOV Motor
Replacement
CARD 06-23793, 06/02/2006; NRC Concern - Material Released Without the Requirements of
EED Being Verified
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and
Drain Valves SCRAM Operability Test
Procedure 32.000.07, Rev 33; Crane Operation Procedure, Reactor Building Crane Operation
Procedure 35.717.001, Rev 29; Maintenance Procedure, Reactor Building Crane - Quarterly
Preventive Maintenance
Procedure 35.717.003, Rev 3; Maintenance Procedure, Reactor Building Crane - Annual PM
Inspection
Procedure 43.401.303, Rev 32; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-9A
Work Control Conduct Manual MWC13, Rev 0; Outage Nuclear Safety
Maintenance Conduct Manual MMA07, Rev 14; Hoisting, Rigging and Load Handling
6 Attachment
1R22: Surveillance Testing
Drawing 6M721-5703-1, Rev. Y; Control Rod Drive System Functional Operating Sketch
CARD 06-22739, 4/24/06; Acrid smell from EDG #13 local control cabinet
CARD 06-23031, 5/1/06; MSIV B2103F028B RPS Limit Switch did not actuate when expected
CARD 06-22653, 04/23/06; HCU 46-27 Conduit for wiring to accumulator pressure switch
needs repair
CARD 06-22999, 05/01/06; Enhancements to 24.405.03
CARD 06-21681; Potential Enhancement for MSIV Switch Calibrations; 3/20/06 (NRC-
Identified)
CARD 06-21720; NRC Question Regarding MSIV Switch Testing; 3/31/06 (NRC-Identified)
CARD 06-22046; Loss of SLC Squib Valve A Continuity Light During Performance of
24.139.03; 4/7/06
Procedure 24.106.06, Rev 25; Surveillance Procedure, SCRAM Discharge Volume Vent and
Drain Valves SCRAM Operability Test
Procedure 24.106.08, Rev. 3; CRD Hydraulic Unit Accumulator Integrity Test
Procedure 24.137.01, Rev. 34; Main Steam Isolation Channel Functional Test
Procedure 24.405.03, Rev. 33; Secondary Containment Operability Test
Procedure 24.307.03, Rev. 38; EDG 13 - Loss of Offsite Power and ECCS Start with Loss of
Offsite Power Test
Procedure 24.202.02, Rev. 42; HPCI Flow Rate Test at 165 psig Reactor Steam Pressure
Procedure 24.206.04, Rev. 44; RCIC System Automatic Actuation and Flow Test
Procedure 43.401.500, Rev 34; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-7A, X-7B, X-7C, and X-7D
Procedure 43.401.500, Rev 35; Surveillance Procedure, Local Leakage Rate Testing for
Penetration X-7A, X-7B, X-7C, and X-7D
Procedure 24.402.06; Rev. 32; Drywell to Suppression Chamber Bypass Leak Test
Procedure 35.139.002; Rev. 27; SLC System Explosive Valve Insert Replacement
Procedure 24.139.03, Rev. 40; SLC Manual Initiation, RWCU Isolation, and Storage tank
Heater Operability Test
WR 0311060425; Perform 24.402.06 Drywell to Suppression Chamber Bypass Leak Test;
3/25/06
WR 0518041022; Perform 44.010.063 RPS MSIV Outboard Valve Limit Switch, Div. I and II,
Calibration
WR 1245060421; Perform 24.139.03 SLC Loop B Pump Flow, Manual Initiate, and Squib
Firing; 4/21/06
1EP6: Drill Evaluation
Scenario SS-OP-802-3300, Rev. 0; Anticipated Transient Without Scram with Small Steam
Leak; 1/26/06
2OS1: Access Control to Radiologically Significant Areas
CARD 05-26818; Primary Containment Atmosphere Sample Pump; T5001-C003 Will Not Start;
dated December 5, 2005
CARD 06-11546; WGI Employee Felt Something in His Left Eye after Removing Protective
Clothing at Drywell Step-off Pad; dated April 5, 2006
CARD 06-21534; High Radiation Alarm on Refuel Floor; dated March 26, 2006
7 Attachment
CARD 06-21640; Unnecessary Contamination of Personnel; dated March 29, 2006
CARD 06-21639; Evaluate Dose an Dose Rate Alarms for Fast Entry Electronic Dosimeters;
dated March 29, 2006
CARD 06-20962; Worker Electronic Dosimeter Alarm on Incorrect Task; dated February 23,
2006
CARD 06-21177; Unexpected Dose Rate Alarm; dated March 8, 2006
CARD 06-21787; Entering High Radiation Area on Incorrect Task; dated April 1, 2006
CARD 06-21807; Evaluate Reactor Building Ventilation Impact on the Spread of Contamination
during RF11 Vessel Fill Up; dated April 2, 2006
CARD 06-21857; Drywell Stepoff Pad Poor Radiation Protection Practices; dated April 3, 2006
CARD 06-21873; Potential Release of Radioactive Contamination; dated April 4, 2006
CARD 06- 21868; Workers Entered Top of Torus High Radiation Area on Wrong Radiation
Work Permit; dated April 4, 2006
CARD 06-21944; Foreign Material Found Inside Main Condenser Upper Steam Space; dated
April 5, 2006
CARD 06-21958; Worker Received Puncture Wound; dated April 6, 2006
EP-225; Radiological Medical Emergencies; Revision 13
RF11 ALARA Self-Assessment; dated April 4, 2006
2OS2 As-Low-As-Is-Reasonably-Achievable Planning And Controls (ALARA)
RWP 06-1110; In-Service Inspections; Revision 0
RWP 06-1103; Install and Remove Temporary Shielding, Install Permanent Shielding;
Revision 0
RWP 06-1105; Job Progress for Scaffold Activities in the Reactor Building Steam Tunnel and
Drywell; Revision 0
RWP 06-1124; Replace Number 4 Drywell Cooler; Revision 4
RWP 06-1164; E1100F031A Cutout and Replace Check Valve; Revision 0
RWP 06-1251; Perform Refuel Activities on Reactor Building 5; Revision 0
CARD 06-21765; Work Initiated Without Radiation Protection Review; dated April 1, 2006
CARD 06-21911; E100F031A Glovebag Not Installed Properly; dated April 5, 2006
CARD 06-21947; E1100F060A Re-pack Extra Time and Dose Above Initial Estimate; dated
April 5, 2006
Procedure 63.000.100; Respirator Evaluation Work Sheet (RWP 06-1117); Revision 0
4OA2: Identification and Resolution of Problems
CARDs initiated between 1/1/06 and 06/30/06
4OA3: Event Followup (71153)
NRC-06-0037 Letter; Licensee Event report No. 2006-001, Excessive Feedwater Check Valve
Leakage At Containment Penetration; dated May 24, 2006
4OA7 Licensee-Identified Violations
CARD 06-21389; Failure to Perform Required Surveys in Accordance with
Procedure 67.000.102; dated March 21, 2006
Procedure 67.000.103; Survey of Outgoing Radioactive Material Shipments; Revision 16
Procedure 67.000.102; Survey of Incoming Radioactive Material Shipments; Revision 0
8 Attachment
LIST OF ACRONYMS USED
ALARA As Low As Reasonable Achievable
CARD Condition Assessment Resolution Document
CDF Core Damage Frequency
CFR Code of Federal Regulations
CTG Combustion Turbine Generator
DRP Division of Reactor Projects
EDG Emergency Diesel Generator
GSW General Service Water
HPCI High Pressure Coolant Injection
IMC Inspection Manual Chapter
LER Licensee Event Report
LERF Large Early Release Frequency
LLRT Local Leak Rate Test
MCC Motor Control Center
MSIV Main Steam Isolation Valve
NCV Non-Cited Violation
NRC Nuclear Regulatory Commission
PI Performance Indicator
PMT Post-Maintenance Testing
RCIC Reactor Core Isolation Cooling
RHRSW Residual Heat Removal Service Water
RPSMG Reactor Protection System Motor Generator
RPT Radiation Protection Technician
RWP Radiation Work Package
SCFH Standard Cubic Feet Per Hour
SCFM Standard Cubic Feet Per Minute
SDP Significance Determination Process
SGTS Standby Gas Treatment System
SPAR Standardized Plant Analysis Risk
SRA Senior Reactor Analyst
TS Technical Specifications
UFSAR Updated Final Safety Analysis Report
WR Work Request
9 Attachment