IR 05000341/2024001

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Integrated Inspection Report 05000341/2024001
ML24121A196
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 04/30/2024
From: Billy Dickson
NRC/RGN-III/DORS/RPB2
To: Peter Dietrich
DTE Electric Company
References
IR 2024001
Download: ML24121A196 (1)


Text

SUBJECT:

FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2024001

Dear Peter Dietrich:

On March 31, 2024, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On April 19, 2024, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

One finding of very low safety significance (Green) is documented in this report. This finding involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or the significance or severity of the violation documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Fermi Power Plant, Unit 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Fermi Power Plant, Unit 2.

April 30, 2024 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Billy C. Dickson, Jr., Chief Reactor Projects Branch 2 Division of Operating Reactor Safety Docket No. 05000341 License No. NPF-43

Enclosure:

As stated

Inspection Report

Docket Number:

05000341

License Number:

NPF-43

Report Number:

05000341/2024001

Enterprise Identifier:

I-2024-001-0073

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

January 01, 2024 to March 31, 2024

Inspectors:

J. Gewargis, Resident Inspector

R. Ng, Senior Project Engineer

T. Taylor, Senior Resident Inspector

Approved By:

Billy C. Dickson, Jr., Chief

Reactor Projects Branch 2

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Attempted Temporary Power Connection from Class 1E to Non-Class 1E Circuit Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000341/2024001-01 Open/Closed

[H.4] -

Teamwork 71111.18 The inspectors identified a Green finding with an associated non-cited violation (NCV) of TS 5.4, Procedures, upon discovery of an electrical connection being made between 1E and non-1E electrical circuits in the plant. The licensee created a plant procedure to perform the connection, however, the requirement that the procedure would only be performed in modes 4 or 5 was not incorporated into the procedure.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000341/2022-002-00 LER 2022-002-00 for Fermi 2 Power Plant, Unexpected High Pressure Coolant Injection Turbine Trip 71153 Closed LER 05000341/2022-004-00 LER 2022-004-00 for Fermi 2 Power Plant, Containment Isolation Valve Actuator Found Disconnected from its Bonnet Resulting in Condition Prohibited by Technical Specifications 71153 Closed

PLANT STATUS

Fermi Unit 2 began the inspection period at or near 100 percent power. On January 16, 2024, the plant commenced a down power to approximately 60 percent to address indications of a main condenser tube leak. On January 17, the down power continued, and the plant was shut down on January 18 due to worsening chemistry from the main condenser tube leakage. On January 20, the plant was restarted based on isolating the leakage to one-half of the main condenser. The plant synchronized with the electric grid on January 22, and raised power to approximately 60 percent on January 23. The plant was returned to 100 percent power on January 29 following repairs to the main condenser. On January 29, power was reduced to approximately 70 percent for a routine rod pattern adjustment. Power was returned to 100 percent on January 30.

On February 13, the plant completed a down power to approximately 60 percent due to indications of main condenser tube leakage. Power was returned to 100 percent after repairs on February 22. On February 23, power was reduced to approximately 75 percent for a routine rod pattern adjustment, and power was returned to 100 percent on February 24. The plant remained at or near 100 percent power until March 22, when a power reduction to start the planned refueling outage commenced. During final preparations to trip the main turbine and reactor following the down power, a high pressure scram of the reactor occurred. No safety limits were violated, and no relief valves were lifted. After verifying the plant was stable, operators continued taking the plant to cold shutdown per the refueling outage schedule. The plant remained in the refueling outage for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) With severe winds and snow forecasted the week of January 8, 2024, the inspectors evaluated the conditions of the circulating water, general service water, and division I 120kV distribution systems for issues that could lead to initiating events.

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Division II standby gas treatment system (SGTS) during division I SGTS cooler maintenance on January 5, 2024
(2) Emergency diesel generator (EDG) 11 after the EDG 11 slow start on January 12, 2024
(3) High pressure coolant injection (HPCI) post HPCI run on February 20, 2024

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (6 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Auxiliary building division I switchgear room on January 5, 2024
(2) Standby gas treatment system (SGTS) division I and II rooms on January 10, 2024
(3) Direct current motor control center area auxiliary building third floor on February 1, 2024
(4) EDG 13 engine room on February 2, 2024
(5) Auxiliary building 4th floor on February 12, 2024
(6) T-room auxiliary building basement during the week ending February 23, 2024

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the onsite fire brigade training and performance during an unannounced fire drill: fire in the dress out area on auxiliary building 2nd level with search and rescue on February 6, 2024

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (2 Samples)

(1) The inspectors observed and evaluated licensed operator performance in the control room during startup and power ascension following an outage to address condenser leakage during the week ending January 27, 2024
(2) The inspectors observed and evaluated licensed operator performance in the control room during the down power and shutdown for an outage to address main condenser tube leakage on January 17 - 18, 2024

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated training on refueling outage RF22 permanent modifications on February 7, 2024

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Reactor core isolation cooling (RCIC) on February 20, 2024
(2) Spurious alarms and contact issues on reactor protection system (RPS) and high pressure coolant injection (HPCI) circuits, completed the week ending March 23, 2024
(3) Division I of the standby gas treatment system, completed the week ending March 23, 2024

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Failure of station blackout battery charger R2103S007, completed the week ending February 3, 2024.
(2) Troubleshooting of the south separator seal tank emergency drain valve on January 24, 2024
(3) Division I non-interruptible air supply (NIAS) maintenance and resultant impacts to reactor building to torus vacuum breakers, with combustion turbine generator (CTG)11-1 OOS, on February 10, 2024
(4) Fuel pool cooling and cleanup (FPCCU) safety system outage and high risk plan review on February 12, 2024

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (6 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Reactor pressure regulator issues during the week ending January 27, 2024
(2) Usage of Technical Specification 3.0.4. during mode changes, and adherence to Technical Requirements Manual chemistry specifications the week ending January 27, 2024
(3) Engine coolant levels on the diesel fire pump, completed the week ending February 3, 2024
(4) Seismic monitor computer rendered nonfunctional and requiring restart on February 9, 2024
(5) RHRSW pump 'D' alert range differential pressure on February 23, 2024
(6) Storage of equipment by southwest quad, potentially impacting safety-related below during the week ending March 2, 2024

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Review of temporary power supply to the reactor building elevator HVAC system from a safety-related bus, completed the week ending March 31, 2024

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Partial)

(1)

(Partial)

The inspectors evaluated activities associated with refueling outage 22, which commenced on March 23, 2024. The plant remained in the refueling outage the remainder of the inspection period. Activities performed included review of the outage risk plan, observation of shutdown and cooldown activities, drywell walkdowns, review of electrical and system lineups, and portions of reactor disassembly.

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (6 Samples)

(1) Division I SGTS room cooler maintenance during the week ending January 6, 2024
(2) EDG 12 jacket coolant pump replacement during the week ending January 27, 2024
(3) RPS channel A2 main condenser agastat relay C7100M222C replacement, completed the week ending February 10, 2024
(4) Division II control center radiation monitoring system calibration after power supply replacement on February 27, 2024
(5) Division I NIAS planned maintenance on February 6, 2024, completed the week ending March 2, 2024
(6) RCIC leakage test after declared inoperability due to check valve leak by on March 1, 2024

Surveillance Testing (IP Section 03.01) (3 Samples)

(1) EDG 11 slow start surveillance on January 12, 2024
(2) Division I mechanical draft cooling tower (MDCT) fan operability surveillance on February 8, 2024
(3) Emergency equipment service water/cooling water (EESW/EECW) pump and valve surveillance on February 28, 2024

Inservice Testing (IST) (IP Section 03.01) (2 Samples)

(1) Low pressure coolant injection (LPCI) system and torus spray pump and valve surveillance on January 24, 2024
(2) HPCI pump and valve surveillance on February 20, 2024

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1) Local leak rate test of valve P3400F409, division II post accident sampling system liquid inboard isolation valve, completed the week ending March 30,

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01)===

(1) Unit 2 (January 1, 2023 through December 31, 2023)

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02) (1 Sample)

(1) Unit 2 (January 1, 2023 through December 31, 2023)

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (1 Sample)

(1) Unit 2 (January 1, 2023 through December 31, 2023)

MS05: Safety System Functional Failures (SSFFs) Sample (IP Section 02.04) (1 Sample)

(1) Unit 2 (January 1, 2023 through December 31, 2023)

===71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03) (1 Sample 1 Partial)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Change management and associated training related to the fire protection program surveillances and preventative maintenance items. Recently the site integrated the fire protection program preventative maintenance items and fire protection surveillances to the maintenance and operations department, respectively.

(2)

(Partial)

The inspectors commenced a review of information associated with the high pressure RPS scram that occurred during the shutdown of the plant for the refueling outage.

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02)===

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 2022-002-00, Unexpected High Pressure Coolant Injection Turbine Trip, (ADAMS Accession No. ML22187A109). The inspectors determined that the cause of the condition described in the LER was not reasonably within the licensee's ability to foresee and correct, and therefore was not reasonably preventable. No performance deficiency nor violation of NRC requirements was identified. This LER is Closed.
(2) LER 2022-004-00, Containment Isolation Valve Actuator Found Disconnected from its Bonnet Resulting in Condition Prohibited by Technical Specifications (ADAMS Accession No. ML22304A009). The circumstances surrounding this LER are documented in Inspection Report 05000341/2022003 under Inspection Results Section 71111.12. This LER is Closed.

INSPECTION RESULTS

Attempted Temporary Power Connection from Class 1E to Non-Class 1E Circuit Cornerstone Significance Cross-Cutting Aspect Report Section Mitigating Systems Green NCV 05000341/2024001-01 Open/Closed

[H.4] -

Teamwork 71111.18 The inspectors identified a Green finding with an associated non-cited violation (NCV) of TS 5.4, Procedures, upon discovery of an electrical connection being made between 1E and non-1E electrical circuits in the plant. The licensee created a plant procedure to perform the connection, however, the requirement that the procedure would only be performed in modes 4 or 5 was not incorporated into the procedure.

Description:

On March 15, 2024, the inspectors conducted a plant tour and noted workers dressed in electrical safety gear near the 480-volt motor control centers (MCCs) 72F-4A and 72E-4B in the reactor building. The inspectors questioned the workers and discovered a temporary power connection was being made per plant procedure 35.TMP.044, Temporary Power for Reactor Building Elevator A/C Unit, Revision 1. The connection was from a spare breaker position on 72F-4A (safety-related, or class 1E) to the load side of the breaker supplying the reactor building elevator's air conditioning (A/C) system on 72E-4B (non-safety-related/non-class 1E). The connection was needed because of an electrical bus outage planned during the upcoming refueling outage. The workers were preparing to splice an electrical cable between the two points. The inspectors questioned the operating shift, maintenance, and engineering personnel on how the licensee justified the connection while the plant operated in mode 1. Pending a response to the inspectors' questions, the licensee stopped work before energizing the temporary power supply.

The creation of plant procedure 35.TMP.044, Revision 1, was intended to enable the connection of temporary power to the reactor building elevator A/C system. However, the procedure, issued on February 28, 2024, did not contain restrictions regarding plant operating mode nor descriptions of how component operability could be impacted. This oversight had serious implications for safety-related loads. The procedure was being performed in mode 1, which requires both divisions of emergency AC power to be operable along with the respective distribution systems. In contrast, in modes 4 and 5, only one division of emergency AC power and one division of AC distribution are required to be operable. The procedure involved cubicle doors being left ajar on the busses, but during its creation, the effects of medium energy line breaks (MELBs) had not been considered. Additionally, potential faults on the non-safety-related loads had not been analyzed for their impacts on safety-related loads. The effects of the added load on the associated EDG during a loss of offsite power event had also not been analyzed, posing potential safety risks.

Upon being questioned by the inspectors, the licensee promptly took corrective actions. They refrained from completing the electrical connection until the plant was in modes 4 and 5, when HELBs/MELBs were no longer a concern, and the bus was not required to be operable.

Furthermore, the procedure was revised to clearly state its applicability only in modes 4 and 5, ensuring compliance with safety regulations.

Corrective Actions: The licensee stopped work and prevented the electrical connections between the class 1E and non-class 1E circuits from being made. The procedure was also revised to state it was only applicable in modes 4 and 5.

Corrective Action References: CR 2024-36954

Performance Assessment:

Performance Deficiency: Licensee procedure MGA02, Procedures, Manuals, and Orders, Revision 55, outlines requirements for creating plant procedures. Section 5.2 requires that procedure to be reviewed for technical adequacy and Section 8.1 requires completion of checklist MGA02001, which requires precautions and limitations to be included. However, procedure 35.TMP.044 did not receive an adequate technical review as the effects of MELBs, additional EDG loading, and impacts of non-safety-related component faults were not analyzed when approving the procedure. Further, appropriate precautions or limitations were not included.

Screening: The inspectors determined the performance deficiency was more than minor because if left uncorrected, it would have the potential to lead to a more significant safety concern. Specifically, absent NRC intervention, an electrical configuration would have existed outside existing analyses, calling into question the ability of various safety-related components to perform their functions. The inspectors utilized IMC0612, Appendix E, example 5a to inform their determination.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Specifically, since the electrical connection was never made, all questions in Exhibit 2, Section A, of IMC 0609 Appendix A were answered 'no.'

Cross-Cutting Aspect: H.4 - Teamwork: Individuals and work groups communicate and coordinate their activities within and across organizational boundaries to ensure nuclear safety is maintained. Specifically, during creation of 35.TMP.044, some individual(s) believed the intent was for it to be performed only in modes 4 and 5. However, the approved procedure did not reflect those restrictions. Further, the work activity was scheduled to occur in mode 1.

Enforcement:

Violation: Technical Specification 5.4, Procedures, requires, in part, that written procedures shall be established, implemented. and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2. Appendix A. February 1978. Section 9 of Regulatory Guide 1.33 addresses procedures for performing maintenance and states, in part, that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures appropriate to the circumstances.

Contrary to the above, maintenance to connect temporary power from safety-related bus 72F-4A to non-safety-related bus 72E-4B was not preplanned and performed in accordance with written procedures appropriate to the circumstances. On March 15, 2024, execution of 35.TMP.044 was in progress; however, the procedure did not consider the potential adverse effects of MELBs, electrical faults, and additional EDG loading the non-safety-related components would have on safety-related components while 72F-4A was required to be operable.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On April 19, 2024, the inspectors presented the integrated inspection results to Peter Dietrich and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

23.101

Circulating Water System

107

71111.01

Procedures

23.131

General Service Water System

114

CARD-18-26135

Div. I SGTS Exhaust Fan Supply Vortex Damper Failed to

Operate

08/14/2018

Corrective Action

Documents

CARD-21-23701

Tubing Ordered for WO Does Not Match Tubing in Plant

04/27/2021

6I721-2649-01

Standby Gas Treatment System Diagram Instrumentation

and Controls

R

6M721-2709

Diagram Standby Gas Treatment and Primary Containment

Purge System Reactor Building

6M721-5734

Emergency Diesel Generator System Functional Operating

Sketch

BL

6M721-5737

Standby Gas Treatment System Functional Operating

Sketch

Drawings

6M721N-2046

P and ID Diesel Generator System Div. I RHR Complex

AF

T46-00

Design Basis Document: Standby Gas Treatment System

Miscellaneous

T46N013B-SS

Calibration Specification Sheet: Standby Gas Treatment

(SGT) Exhaust Fan T4600C004 Div. 2

05/20/2019

23.202

High Pressure Coolant Injection System

119

23.307

Emergency Diesel Generator System

135

23.404

Standby Gas Treatment System

71111.04

Procedures

6M721-5708-1

High Pressure Coolant Injection System Functional

Operating Sketch

FP-AB-2-9b

Auxiliary Building, Division I Switchgear Room, Zone 9, EL.

613'6"

FP-AB-3-14F

Auxiliary Building, DC Motor Control Center (MCC) Room

Zone 14, EL. 643'-6"

FP-AB-4-16C

Auxiliary Building Ventilation Equipment Room, Zone 16, EL.

659'6"

FP-AB-5-16A

Auxiliary Building, North Standby Gas Treatment System

(SGTS) Room, Zone 16, EL.677'6"

71111.05

Fire Plans

FP-AB-5-16B

Auxiliary Building, South Standby Gas Treatment System

(SGTS) Room, Zone 16, EL.677'6"

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

FP-RB-B-5C

Reactor Building Basement Corridors Zone 5, E

L. 562, and

EL. 564

FP-RHR-1-13-

EDG

RHR Complex, EDG-13 Room, EL. 590'

LP-FP-940-2412

Fire Drill Evaluation: 2nd Floor Auxiliary Building Personal

Changing Room, Class A Fire

Miscellaneous

Training Material:

LP-OP-202-2414

RF22 Modifications Training

2.000.02

Plant Startup to 25% Power

110

2.000.03

Power Operation 25% to 100% to 25%

108

2.000.04

Plant Shutdown from 25% Power

23.205

Residual Heat Removal System

149

71111.11Q

Procedures

24.603.02

SRM/TRM/APRM Overlap Verification

23-30437

HPCI Inboard Torus Suction Isolation Valve Abnormal

Stroke

05/23/2023

23-30997

3D93 Neutron Monitoring System Channel Trip Received

06/18/2023

23-32868

E4150F006 Will Not Stay Closed While Performing

24.202.05 Section 5.1

09/06/2023

23-33899

3D93 Neutron Monitoring System Channel Trip Spurious

Alarms

10/22/2023

24-36108

3D93 Neutron Monitoring System Channel Trip Spurious

Alarms

2/06/2024

24-36518

E4150F042 HPCI Booster Pump Suct from Supr Pool Iso

MOV Failed to Close

2/25/2024

24-36597

Failure of Div 1 SGTS Upstream HEPA Filter In-Place Test

2/28/2024

24-36605

Degraded Gasket on Div 1 SBGT Filter Unit Air Inlet Heater

Termination Cover

2/29/2024

2-26436

3D93 Neutron Monitoring System Channel Trip Received

with No Apparent Cause

05/18/2022

2-28826

Differential Pressure for Div 1 Standby Gas Treatment

System Moisture Separator is at the Spec of 0.5" H2O per

23.404 P&L 3.1

08/18/2022

CARD-13-24415

Packing Leak on E5100F053

06/20/2013

71111.12

Corrective Action

Documents

CARD-14-20569

RCIC AOV Packing Leaks

01/28/2014

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

CARD-14-22669

Leakage Identified during RPV Pressure Test E5150F008

03/21/2014

CARD-14-26438

Packing Leak on E5150F046

08/12/2014

CARD-20-31076

Revise Tolerances on E51N006

10/08/2020

CARD-23-20919

2PA1 Pos 1B Feed to RCIC Barometric Condensate Pump

260VDC Switch Is Not Making Contact

2/02/2023

CR-2023-32208

1D58-STM LK DET RCIC LOGIC POWER FAILURE and

1D62-STM LK DET HPCI LOGIC POWER FAILURE

Received Simultaneously

08/09/2023

CR-2023-345850

E5150-F026 Packing Leak Has Increased

2/04/2023

CR-2023-35172

Inaccurate Information from Vendor on MCC Eaton

Disconnects Leads to Updates of Equipment Cause

Evaluation and Outage PMs

2/19/2023

6M721-5709-1

Reactor Core Isolation Cooling System Sketch Functional

Operating Sketch

I-2080-23

Visual Annunciator and Sequence Recorder Alarm

Schematic

S

I-2145-18

Power Range Neutron Monitoring Reactor Protection

System Outputs

H

I-2155-06

RPS Trip System A Trip Relays

W

I-2155-08A

RPS Trip System A2 Scram Trip Logic

C

I-2221-05

HPCI SYS-Pump Discharge Isolation Valves E4150F006

and F007

AD

I-2221-08

HPCI SYS Suppression Pool Isolation Valves E4150F041

and F042

Z

Drawings

I-2225-04

HPCI Logic Circuit Part 2

V

Engineering

Evaluations

TE-E41-12-027

Evaluate Effect of AOV E4100F054 Remaining Open until

RF15

43.404.001

Standby Gas Treatment Filter Performance Test Division 1

ARP 3D93

Neutron Monitoring System Channel Trip

MWC06

Work Screening and Processing

Procedures

MWC07

Online Scheduling Process

35445274

Steam Leak on E5150F054

2/16/2014

37976580

RCIC AOV Packing Leaks

03/18/2014

Work Orders

37976612

RCIC AOV Packing Leaks/Bad Stem Replace Valve

11/04/2015

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

38182487

Leakage Identified During RPV Pressure Test E5150F008

03/22/2014

60850744

Vent Header Recoat Project Requires SGTS D2 Charcoal

Replacement

04/06/2021

226505

Replace Division 1 SGTS Upstream HEPA Filters

05/06/2022

70435403

Work Orders Needed to Test SGTS Charcoal Following

Drywell Moisture Barrier Replacement in RF22

2/20/2023

70880193

Standby Gas Treatment System Div 1 Moisture Separator

D/P at High Mark

2/06/2024

24-35948

Smoke Coming from SBO House 125VDC Battery Charger

01/31/2024

Corrective Action

Documents

24-36104

CTG 11-1 Failed to Achieve Base Load and Failed PMT

2/05/2024

6E721Y-2008

One Line Diagram AC and DC Systems

B

6I721F-2591-05H

Wiring Diagram for DCS Term Cab 1A (S14P001) Front

View (Zones A and B) Rear View (Zones C and D)

A

6M721-2005

Diagram Feedwater Heater Drains, Emergency Drains, and

Heat Air Vents System

6M721-5712-1

Fuel Pool Cooling and Cleanup System Functional

Operating Sketch

T

6M721-5712-1

Fuel Pool Cooling and Cleanup System Functional

Operating Sketch

T

6M721-5712-2

Fuel Pool Filter Demin System Functional Operating Sketch

K

6M721-5712-2

Fuel Pool Filter Demineralizer System Functional Operating

Sketch

K

6M721-5716

Feedwater Heater Drains, Vents, and Emergency Drains

Functional Operating Sketch

6M721-5739-1

Nitrogen Interting System Functional Operating Sketch

6SD721-2500-02

One Line diagram 13.8Kv

BH

Drawings

DSD721F-164

25VDC Diagram [CONFIDENTIAL]

J

SCR 24-0008

50.59 Screen: TM 24-0003

Engineering

Evaluations

TM 24-0003

N22F414B Temporary Support Plate Installation

Operations logs, February 5, 2024 thru February 7, 2024

Plan of the Day

2/09/2024

P50-02.03

Control Air System

C

71111.13

Miscellaneous

Risk

Risk Management Plan: 66384440 Rework G4100F002B

2/12/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Management

Plan

FPCCU Isolation Valve and G4100F012B

TSC 89-011

Non-Interruptible Control Air System Operability and

Compliance of Limiting Condition for Operations

23.205

Residual Heat Removal

149

Procedures

23.708

Fuel Pool Cooling and Cleanup System

23-32706

Diesel Fire Pump Coolant Water Reservoir Needs to Be

Replenished

08/31/2023

23-33313

DFP Right Angle Drive Particle Count Above Expected

Value

09/27/2023

23-35159

Diesel Fire Pump Right Angle Drive Oil Particle Count High

Out of Specification

2/20/2023

24-35422

Diesel Fire Pump Coolant Level Issue

01/09/2024

24-35449

DFP Coolant Level Low

01/09/2024

21-20069

T5000F404B Seat Leakage

01/04/2021

CARD 20-22467

IST to investigate implementing 2 Pump Testing of the

RHRSW Pumps

03/06/2020

CARD-15-21042

Inadequate Procedural Guidance for Past Operability

Reviews

2/09/2015

CARD-17-21711

Process for Flagging Past Operability Reviews in CARDs

Inadequate

09/15/2023

CARD-20-22410

RHRSW Pump D DP Approaching IST Alert Limit

03/04/2020

CR-2024-35747

Pressure Regulator #1 Not Tracking with Pressure Regulator

  1. 2 and Unable to Be Selected as Controlling Regulator

01/20/2024

CR-2024-35761

Pressure Regulator Issues during Startup

01/21/2024

Corrective Action

Documents

CR-2024-36427

RHRSW Pump D in the Alert Range Low for Calculated D/P

2/20/2024

24-36644

Wrong Revision of MOP23002 Used

03/01/2024

24-36644

NRC Identified: Wrong Revision of MOP23002 Used

03/01/2024

Corrective Action

Documents

Resulting from

Inspection

24-36759

NRC Identified-Variety of Plant Storage Issues in the

Reactor Building

03/06/2024

6M721-2083

Diagram Residual Heat Removal Division II

6M721-5705

Functional Operating Sketch Traversing Incore Probe

System

H

71111.15

Drawings

6M721-5741

Primary Containment Monitoring System Functional

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operating Sketch

6M721N-2053

P and ID RHR Service Water System Division II RHR

Complex

AH

16-022

ISI/NDE-IST Program Evaluation Sheet: Evaluation of SOE

15-07 Data and Establishing New Acceptance Criteria for

E1151C001D

2-019

IST Program Acceptance Criteria for RHRSW B Pump

24.205.06

Division II RHRSW Pump and Valve Operability Test

66340315

Perform 24.205.06 Division 2 RHRSW Pump and Valve

Operability

2/20/2024

Engineering

Evaluations

TE-ANE-24-001

TRLCO 3.0.4(b) Mode Change Restraint Assessment for FO

24-01

CHS-PRI-06

Chemistry Specifications: Reactor Water

N3012A

Fermi 2 Nuclear Training - Operations Systems Student

Test, Governor/Pressure Control

Miscellaneous

VMB11-60.1

Installation, Operation and Maintenance Driver Manual

[CONFIDENTIAL]

2.000.03

Power Operation 25% to 100% to 25%

108

23.109

Turbine Operating Procedure

100

23.110

Unitized Actuator System

23.612

Seismic Monitoring

44.090.003

Seismic Monitoring-Active Seismic Monitoring System

Channel Check

44.180.005

Main Turbine Bypass System Response Time Test and

Functional Test

44.180.005

Main Turbine Bypass System Response Time Test and

Functional Test

CR-2023-33665

Active Seismic Central Recorder has Abnormal Indications

Following 44.090.001

10/11/2023

CR-2024-36158

Active Seismic Monitor System Found in Abnormal State

2/07/2024

MCE03

Chemistry and Environmental Monitoring Conduct Manual

MES27

Verification of System Operability

2A

MES58

Technical Evaluations

5B

Procedures

MES82

Technical Specification Surveillance Frequency Control

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Program

MLS05

Notifications/General Regulatory Reporting Requirements

MOP23

Plant Storage

64808082

Perform 24.205.06 Division 2 RHRSW Pump and Valve

Operability

09/11/2023

65564354

Perform 24.205.06 Division 2 RHRSW Pump and Valve

Operability

2/11/2023

Work Orders

70844865

License Renewal Perform RHR Pump B&D First Floor Hoist

and Trolley Inspections

2/02/2024

Corrective Action

Documents

Resulting from

Inspection

24-36954

NRC Discovered Potential Issue with TMP 24-005

03/15/2024

DC-5512 Volume

Evaluation of 1E/Non-1E Separation Criteria

C

Engineering

Evaluations

TSR-100511

Post DC-5512 Vol 1 for Implementing Temp Power

Procedure 35.TMP.044

Procedures

35.TMP.044

Temporary Power for Reactor Building Elevator A/C Unit

and 1

71111.18

Work Orders

68341691

Pre RF22 Install Temp Power for RB ELEV Cooling

(72E-4B)

05/04/2023

2-21434

Valve E1100F060A is Very Difficult to Close

2/09/2022

Corrective Action

Documents

2-24619

Actuator Broken during Reassembly

04/03/2022

24-37146

NRC Concerns-Large Box within 2 Feet of Potential

Important to Safety Equipment and Box Close to NIAS

Piping

03/23/2024

24-37278

NRC Identified-Motor/Actuator Missing Cover in Drywell

Basement

03/26/2024

24-37279

NRC Identified-Potentially Missing Insulation in Drywell

Basement

03/26/2024

24-37280

NRC Identified-Leak from P4400-F274 in Drywell Basement

03/26/2024

Corrective Action

Documents

Resulting from

Inspection

24-37282

NRC Identified-Potentially Loosened Support in Drywell

Basement

03/26/2024

M-2084

Residual Heat Removal Div 1

BS

71111.20

Drawings

M-2090

System Diagram Nuclear Boiler System

AP

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

M-5007

Primary Containment Pneumatic Supply System

Z

M-5707

Core Spray System Functional Operating Sketch

AJ

M-5730-5

Interruptible Control Air Reactor Building Functional

Operating Sketch

AG

SD-2500-01

One Line Diagram Plant 4160V and 480V System Service

Engineering

Changes

2-0009

Remove Testable Function from Check Valve E2100F006A

Miscellaneous

G4100-000150

Clearance for Reactor Vessel Flood-Up

03/24/2024

2.000.03

Power Operation 25% to 100% to 25%

108

2.000.04

Plant Shutdown from 25% Power

23.205

Residual Heat Removal

149

23.708

Fuel Pool Cooling and Cleanup

Procedures

24.203.04

Core Spray Valve Operability and Position Verification Test

CR-2024-35869

EDG-12 Standby Jacket Coolant Pump Above Shutdown

Limit Recommended by Engineering

01/24/2024

Corrective Action

Documents

CR-2024-35888

Higher than Expected Resistance to Rotation on New

Standby Jacket Coolant Pump assembly MM#100312369

01/25/2024

6I721-2095-14

Schematic Diagram Nuclear Steam Supply Shut Off System

Trip System A

O

6I721-2155-22

Schematic Diagram Reactor Protection System Testability

Modification

M

6M721-5706-1

Residual Heat Removal Division II Functional Operating

Sketch

6M721-5706-1

Residual Heat Removal Division II Functional Operating

Sketch

6M721-5711-1

Reactor Water Cleanup Reactor Building Functional

Operating Sketch

6M721-5715-1

Reactor Feedwater System Functional Operating Sketch

6M721-5730-3

Non-Interruptible Control Air System Division 1 and 2

Functional Operating Sketch

AL

6M721-5734

Emergency Diesel Generator System Functional Operating

Sketch

BL

6M721N-2046

P and ID Diesel Generator System Division I RHR Complex

AF

71111.24

Drawings

I-2400-10

Sample Line Tie-In and Return Diagram Post Accident

J

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Sampling System

I-2400-11

Post Accident Sampling System Piping Interconnection

Diagram

N

23.205

Residual Heat Removal System

149

24.202.01

HPCI Pump and Valve Operability Test at 1025 PSIG

25

24.204.01

Division I LPCI and Suppression Pool Cooling and Spray

Pump and Valve Operability Test

24.205.08

Division I RHR Cooling Tower Fan Operability and Valve

Lineup Verification Test

24.206.01

RCIC System Pump and Valve Operability

24.208.02

Division I EESW and EECW Makeup Pump and Valve

Operability Test

24.307.14

EDG 11 Start and Load Test-Slow Start

35.318.017

Maintenance Procedure

54A

43.401.300

Local Leakage Rate Test Type C-General

43.401.405

Local Leakage Rate Testing for Penetration X-210B

43.401.515

RCIC Pressure Isolation Valve Leak Test

44.020.059

Surveillance Procedure

47.000.02

Mechanical Vibration Measurements for Trending

46A

64.120.041

Containment Area High Range Radiation Monitor Division 2

Calibration

6M721-5709-1

Reactor Core Isolation Cooling Sketch Functional Operating

Sketch

MES27

Verification of System Operability

2A

MES58

Technical Evaluations

5B

MMA06

Interim Alterations

8B

Procedures

MQA11-100

Operability Determination Process

60495674

Perform 64.120.041 Containment Area High Range

Radiation Monitor Division II Calibration

01/17/2024

63543821

License Renewal-T4100B016 Inspect, Lube, and Check

Belts

01/03/2024

65398830

Calibrate Division 1 Control Air Instruments

05/30/2022

Work Orders

65475211

Replace RPS Channel 'A2' Main Condenser Agastat Relay

2/05/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

C7100M222C

65638746

Perform 24.802.02 D1 EESW Pump and Valve Operability

11/29/2023

65788678

Perform 24.307.14 Section 5.1 EDG 11 Start and Load

Test-Slow Start

01/08/2024

65984824

Perform 24.204.01 DIV. I LPCI and Torus Cooling Spray

Pump and Valve Operability Test

01/11/2024

66186578

Perform 24.205.08 Division I RHR Cooling Tower Fan

Operability and Valve Lineup Verification Test

2/08/2024

287377

Perform 24.202.01 HPCI Pump/Flow Test and Valve Stroke

at 1025 PSIG

2/20/2024

66447792

Final 43.401.405 LLRT for X-210B (Test-4 P34F409)

03/27/2024

66456204

Perform 24.802.02 D1 EESW Pump and Valve Operability

2/28/2024

70612648

Replace the Pump and Motor Assembly for R3001C027

EDG12 JC STBY PMP

01/25/2024

Corrective Action

Documents

23-31768

Elevated Temperatures C Condenser Pump >265 Degrees

Fahrenheit

07/23/2023

Licensing Performance Indicator - Safety System Function

Failure IRIS Data Entry, Verification and Approval

01/2023 -

2/2023

Operating Data Report

01/2023 -

2/2023

71151

Miscellaneous

23 Operators Narrative Log

Various

Dates

CR-2023-31533

NQA Notice of Elevation - Change Actions Associated with

the Ownership Transition of the Fire Protection Program

Off-Track

07/12/2023

CR-2023-323116

Investigate Classifications of Fire Protection Performance

Tests PT vs PTT

08/04/2023

CR-2023-35199

Job Analysis for Fire Protection Activities Assigned to

Operations Department

2/20/2023

CR-2024-35445

License Renewal-AMP B.1.16 External Surfaces Monitoring

PTT WO's Cancelled

01/08/2024

CR-2024-36389

Potential Challenges to Industrial and Nuclear Safety due to

Improper Fire Protection Training

2/19/2024

71152A

Corrective Action

Documents

CR-2024-36490

Safety Concern: NQA Fire Protection Escalation Ineffective

2/23/2024

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

at Correcting Deficiencies in Fire Protection Program

2.000.04

Plant Shutdown from 25% Power

Procedures

MES55

Transient Analysis Program

58748762

Perform 28.501.04 Fire Suppression and Sprinkler System

Valve Operability Test

06/15/2022

281876

Perform 28.501.04 Valve Operability for T8000F037

04/06/2022

2468187

Perform 28.501.04 Fire Suppression and Sprinkler System

Valve Operability Test-License Renewal

04/07/2023

65034551

Perform 28.501.04 Valve Operability for T8000F037

07/23/2023

Work Orders

65973610

Perform 28.501.02 Fire Suppression Water System Valve

Lineup Verification

01/24/2024

Corrective Action

Documents

CARD-22-26226

Unexpected HPCI Turbine Trip

05/11/2022

Miscellaneous

LER 2022-004-00

Containment Isolation Valve Actuator Found Disconnected

from its Bonnet Resulting in Condition Prohibited by

Technical Specifications.

10/31/2022

Procedures

35.202.009

HPCI Steam Turbine-General Maintenance

53455389

Calibrate HPCI Turbine Governor Speed Loop

2/16/2021

58642933

Replace and Calibrate HPCI Ramp Generator and Signal

Converter

2/15/2021

267358

Unexpected HPCI Turbine Trip. Troubleshoot and Repair

05/11/2022

71153

Work Orders

269101

Replace Failed HPCI Speed Sensor

05/12/2022