IR 05000341/2022003

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Integrated Inspection Report 05000341/2022003
ML22311A531
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/08/2022
From: Billy Dickson
NRC/RGN-III/DORS/RPB2
To: Peter Dietrich
DTE Electric Company
References
IR 2022003
Download: ML22311A531 (29)


Text

SUBJECT:

FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2022003

Dear Peter Dietrich:

On September 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On October 19, 2022, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of these findings involved violations of NRC requirements. One Severity Level IV violation without an associated finding is documented in this report. We are treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Fermi Power Plant, Unit 2.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Fermi Power Plant, Unit 2.

November 8, 2022 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Billy C. Dickson, Jr., Chief Reactor Projects Branch 2 Division of Operating Reactor Safety Docket No. 05000341 License No. NPF-43

Enclosure:

As stated

Inspection Report

Docket Number:

05000341

License Number:

NPF-43

Report Number:

05000341/2022003

Enterprise Identifier:

I-2022-003-0042

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

July 01, 2022 to September 30, 2022

Inspectors:

T. Briley, Senior Resident Inspector

R. Cassara, Resident Inspector

J. Gewargis, Resident Inspector

V. Myers, Senior Health Physicist

R. Ng, Senior Project Engineer

J. Reed, Health Physicist

T. Taylor, Senior Resident Inspector

Approved By:

Billy C. Dickson, Jr., Chief

Reactor Projects Branch 2

Division of Operating Reactor Safety

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Actuator-Yoke Separation on a Main Steam Line Drain Primary Containment Isolation Valve Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000341/2022003-01 Open/Closed

[H.12] - Avoid Complacency 71111.12 A self-revealed finding of very low safety significance (Green) with an associated non-cited violations (NCV) of Technical Specification 5.4, "Procedures," occurred when motor-operated valve B2103F019, one of the main steam line drain primary containment isolation valves, became damaged when the actuator separated from the yoke after being operated. The issue was discovered during a startup-related walkdown by licensee personnel at the end of a forced outage. Undersized bolts had been used to attach the actuator to the yoke.

Failure to Submit a Licensee Event Report for the Actuator-Yoke Separation of a Main Steam Line Drain Primary Containment Isolation Valve Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000341/2022003-02 Open/Closed Not Applicable 71111.12 The inspectors identified a Severity Level IV Non-Cited Violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) Part 50.73 (a)(2)(i)(B), Licensee Event Report System, when the licensee failed to submit a Licensee Event Report (LER) within 60 days of identifying a condition prohibited by Technical Specifications.

Reactor Scram Due to Trip of Reactor Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000341/2022003-04 Open/Closed None (NPP)71152A A finding of very low safety significance (Green) with an associated non-cited violation (NCV)of Technical Specification 5.4, "Procedures," was self-revealed on February 4, 2022, when the reactor automatically scrammed from approximately 58 percent power during a plant shutdown to start a refueling outage. Appropriate precautions regarding feed pump suction pressure were not included in the procedure for operating the feedwater system.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000341/2022003-03 Seismic Displacement for Safety-Related Piping Not Verified 71111.18 Open

PLANT STATUS

Unit 2 started the reporting period at or near 100 percent reactor power. On September 21, 2022, the unit commenced a planned downpower to approximately 65 percent for maintenance and a rod pattern adjustment. The unit returned to 100 percent reactor power on September 26, 2022, and remained at or near 100 percent reactor power for the remainder of the period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of seasonal high temperatures for the following systems:

120kV switchyard, 345 kV switchyard, residual heat removal service water (RHRSW),and control center heating, ventilation, and air conditioning (CCHVAC) during the week ending August 31, 2022

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Emergency diesel generator (EDG) 12 during EDG 13 maintenance during the week ending July 23, 2022
(2) Division 2 CCHVAC partial equipment alignment during Division 1 CCHVAC chiller work during the week ending on August 12, 2022

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Reactor building fourth floor, recirculation system motor generator area during the week ending July 23, 2022
(2) Control air compressor room during the week ending July 23, 2022
(3) Reactor building second floor north and south quadrants during the week ending September 30, 2022
(4) Auxiliary building fifth floor Division 1 and 2 CCHVAC system equipment rooms during the week ending September 30, 2022

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the on-site fire brigade response to an announced drill on September 1, 2022, which involved a simulated fire in one of the turbine lube oil rooms.

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (2 Samples)

(1) The inspectors observed and evaluated licensed operator requalification training on Engage/Vaporstream, the licensee event notification system, on September 28, 2022.
(2) The inspectors observed simulator training on anticipated transient without scram scenarios, September 15, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (2 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Division 1 CCHVAC journal bearing assessment and replacement due to a high bearing oil temperature trip of the chiller on August 3, 2022
(2) Motor operator valve actuator removal and installation practices, actuator to yoke mounting bolts and washers during the week ending September 24, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (3 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Operability and functionality assessment performed on the Division 1 EDG sequencer trouble alarm received, ending on September 30, 2022
(2) NOVA inverters, Division 1 testability power supply, CARD 22-22886 during the week ending September 17, 2022
(3) Operability of Division 1 channel 'B' turbine building area temperature high primary containment isolation instrumentation erratic indication as documented in CARDs 22-26351 and 22-26412, ending September 30, 2022

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1) Permanent modification of the new RHRSW and emergency equipment service water (EESW) piping/supports/penetrations

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Integrated plant computer system drywell curves not indicating in the complete pressure range during the week ending August 13, 2022
(2) Division 1 B21N117B turbine building area temperature high instrumentation following channel failure during the week ending May 21, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors completed a review of work hours controls during the RF21 refueling outage, which concludes the outage sample started in the first quarter of 2022.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Emergency preparedness drill on August 16,

RADIATION SAFETY

71124.06 - Radioactive Gaseous and Liquid Effluent Treatment

Walkdowns and Observations (IP Section 03.01) (1 Sample)

The inspectors evaluated the following radioactive effluent systems during walkdowns:

(1) Reactor building ventilation

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage, &

Transportation

Radioactive Material Storage (IP Section 03.01)

The inspectors evaluated the licensees performance in controlling, labeling and securing the following radioactive materials:

(1) Radioactive materials in the radioactive waste on-site storage facility
(2) Radioactive materials in warehouse G

Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)

The inspectors walked down the following accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality:

(1) Resin processing equipment

Waste Characterization and Classification (IP Section 03.03) (2 Samples)

The inspectors evaluated the following characterization and classification of radioactive waste:

(1) Bead resin
(2) Oil waste

Shipping Records (IP Section 03.05) (4 Samples)

The inspectors evaluated the following non-excepted radioactive material shipments through a record review:

(1) Radioactive waste shipment, EF2-22-034, of low specific activity bead resin in a general design package
(2) Radioactive waste shipment, EF2-22-047, of waste class 'A' bead resin in a type 'B' package
(3) Radioactive waste shipment, EF2-22-018, of dry active waste in a general design package
(4) Radioactive waste shipment, EF2-21-006, of waste class 'A' bead resin in a type 'A' package

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

MS08: Heat Removal Systems (IP Section 02.07)===

(1) July 1, 2021 through June 30, 2022

MS09: Residual Heat Removal Systems (IP Section 02.08) (1 Sample)

(1) July 1, 2021 through June 30, 2022

MS10: Cooling Water Support Systems (IP Section 02.09) (1 Sample)

(1) July 1, 2021 through June 30, 2022 BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
(1) October 1, 2021 through June 30, 2022

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) October 1, 2021 through June 30, 2022 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
(1) October 1, 2021 through June 30, 2022

71152A - Annual Follow-up Problem Identification and Resolution Annual Follow-up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Follow-up to selected CARDs implying production-over-safety, during the week ending August 20, 2022
(2) Follow-up to a reactor scram caused by a perturbation in the feedwater system, during the week ending September 24, 2022
(3) Reactor scram caused by mayflies, during the week ending September 30,

INSPECTION RESULTS

Actuator-Yoke Separation on a Main Steam Line Drain Primary Containment Isolation Valve Cornerstone Significance Cross-Cutting Aspect Report Section Barrier Integrity Green NCV 05000341/2022003-01 Open/Closed

[H.12] - Avoid Complacency 71111.12 A self-revealed finding of very low safety significance (Green) with an associated non-cited violations (NCV) of Technical Specification 5.4, "Procedures," occurred when motor-operated valve B2103F019, one of the main steam line drain primary containment isolation valves, became damaged when the actuator separated from the yoke after being operated. The issue was discovered during a startup-related walkdown by licensee personnel at the end of a forced outage. Undersized bolts had been used to attach the actuator to the yoke.

Description:

On June 27, 2022, the licensee was performing a walkdown of the reactor building steam tunnel near the end of a forced outage. The actuator for motor-operated valve B2103F019 was observed near the top of the valve stem and in continuous operation. The actuator had detached from the valve yoke and had walked up the valve stem during the operation. The motor remained energized, causing the valve stem to shake back and forth. The licensee secured power to the valve actuator, took control of the valve, and, using the manual handwheel, walked the actuator back down the valve stem to the valve yoke. Afterward, the licensee installed bolting to reconnect the actuator and valve yoke. The licensee considered the valve inoperable. The licensee performed an engineering evaluation to support leaving the valve in the condition for the remainder of the cycle. The valve is one of two in a series that perform a containment isolation function for main steam line drains. The valves are normally closed during operation, and the licensee manipulates them during plant startups and shutdowns. Per technical specifications, the licensee verified that the upstream valve was closed, allowing for continued operation.

Initial investigation revealed a lack of proper thread engagement on the bolts that held the actuator to the yoke. With insufficient thread engagement, valve operating forces allowed the actuator to become detached from the valve yoke and move up the threads of the stem when operators attempted to close the valve from the control room. The valve initially indicated correctly, but the actuator had separated and moved up the valve stem in the field. The abnormal configuration resulted in the control system continuing to attempt to close the valve.

With the actuator continuously running, valve position indication fluctuated between open and closed for nearly 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The licensee identified this condition after-the-fact when the licensee reviewed plant computer data. The licensee performed an extent of the condition review and determined that other valves that had similar work performed during the outage remained operable. The inspectors reviewed the licensee's efforts and did a field walkdown of one of the valves.

Later investigation by the licensee revealed that improper thread engagement existed due to maintenance staff using the wrong length bolts to connect the actuator to the yoke. During the outage, the licensee performed thrust testing on the valve. This test included separating the actuator and the valve yoke, inserting a test device, and reconnecting all three together using the normally installed bolts along with four additional bolts (the additional bolts for the test device are shorter than the four normally installed bolts). Upon reassembly following testing, maintenance personnel incorrectly used the shorter bolts to reattach the actuator to the yoke, and the licensee did not find the other four bolts.

Corrective Actions: The licensee secured the actuator back in place on the yoke, performed an engineering evaluation, and performed an investigation.

Corrective Action References: CARD 22-27461

Performance Assessment:

Performance Deficiency: Procedure 46.306.06, "MOV Diagnostic Testing with the QUIKLOOK 3 System," was not performed correctly. The procedure referred to "provided" and "original" bolts when directing installation and removal of the test device. In the restoration section of the procedure, step 5.8.3 directs the restoration of subcomponents to the original configuration. The licensee did not install the original bolts to connect the valve yoke to the actuator.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Configuration Control attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, use of incorrect bolts resulted in a safety-related containment isolation valve becoming inoperable.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power.

Specifically, the finding screened to Green based on answering 'no' to both questions in Section C of Exhibit 3 of IMC 0609. The finding did not create an actual open pathway in containment, nor did it involve hydrogen igniters.

Cross-Cutting Aspect: H.12 - Avoid Complacency: Individuals recognize and plan for the possibility of mistakes, latent issues, and inherent risk, even while expecting successful outcomes. Individuals implement appropriate error reduction tools. Specifically, individuals performing the valve reassembly failed to recognize and/or check for the minimum amount of thread engagement when bolting the actuator to the yoke. The licensee determined with the incorrect bolts installed, minimum actual thread engagement would have existed and could have been noticed. Further, the licensee did not take appropriate actions to validate the correct size bolts when following the step to restore the valve to its "original configuration."

Enforcement:

Violation: Technical Specification (TS) 5.4, Procedures, requires, in part, that the applicable procedures recommended in Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operation), are established, implemented, and maintained. Section 9 of RG 1.33 states, in part, that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances. Contrary to the above, on April 11, 2022, Procedure 46.306.06, "MOV Diagnostic Testing with the QUIKLOOK 3 System," a procedure that affects the performance of safety-related equipment, was not properly performed. Specifically, the procedure directed the original bolts to be installed between the actuator and yoke after testing, and they were not. Shorter bolts were installed, and as a result the yoke and actuator separated during valve operation, rendering the valve inoperable. Compliance with technical specifications was restored on June 29, 2022, when the licensee performed the required actions to close and deactivate the other containment isolation valve in series.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Failure to Submit a Licensee Event Report for the Actuator-Yoke Separation of a Main Steam Line Drain Primary Containment Isolation Valve Cornerstone Severity Cross-Cutting Aspect Report Section Not Applicable Severity Level IV NCV 05000341/2022003-02 Open/Closed Not Applicable 71111.12 The inspectors identified a Severity Level IV Non-Cited Violation (NCV) Title 10 of the Code of Federal Regulations (10 CFR) Part 50.73 (a)(2)(i)(B), Licensee Event Report System, when the licensee failed to submit a Licensee Event Report (LER) within 60 days of identifying a condition prohibited by Technical Specifications.

Description:

On June 26, 2022, the licensee was performing a post forced outage walkdown of the steam tunnel on the first floor of the reactor building and discovered the actuator for B2103F019, the outboard main steam line drain primary containment isolation valve (PCIV), was disconnected from the yoke of the valve and shaking. On June 27, 2022, the licensee documented the discovery and inoperability in Condition Assessment Resolution Document (CARD) 22-27461. On July 21, 2022, the licensee completed a past operability evaluation and determined that B2103F019 was inoperable from March 27, 2022, when maintenance personnel installed the incorrect actuator bolts during the most recent refueling outage. The incorrect bolting installation is described in this report as NCV 05000341/2022003-01.

Additionally on July 21, 2022, the licensee completed a reportability evaluation that concluded the actuator-yoke separation was not reportable to the NRC based on the safety function of isolating the primary containment flow path being maintained with the operable inboard PCIV.

The inspectors agreed with the conclusion regarding the safety function. However, per technical specifications, the inoperable outboard PCIV would have required the flow path to be isolated with a closed and deactivated valve in the flow path within four hours. If the licensee did not isolate the flow path within that time frame, the technical specifications would have required the plant to be in Mode 3 (Shutdown) within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Since the licensee became aware of the past inoperability on July 21, 2022, the licensee had 60 days from that date to submit the LER per 10 CFR Part 50.73 (a)(2)(i)(B). The licensee failed to submit the LER in time by not recognizing the reporting criterion.

Corrective Actions: The licensee documented the failure to report in the corrective action program and reassessed the issue of reportability.

Corrective Action References: CARD 22-30092, CARD 22-27461

Performance Assessment:

None. The inspectors determined this violation was associated with a minor performance deficiency since it only dealt with reporting requirements. A finding of very low safety significance (Green) associated with the incorrect bolts is discussed in this report as NCV 05000341/2022003-01.

Enforcement:

The Reactor Oversight Processs (ROPs) significance determination process does not specifically consider the regulatory process impact in its assessment of licensee performance. Therefore, it is necessary to address this violation which impedes the NRCs ability to regulate using traditional enforcement to adequately deter non-compliance.

Severity: Based on the NRC Enforcement Policy dated January 14, 2022, Section 6.9, Subsection d, Number 9, lists a failure to make a required report per 10 CFR Part 50.73, LER System, as an example of a Severity Level IV violation.

Violation: 10 CFR Part 50.73, "Licensee Event Report System," states, in part, holders of an operating license for a nuclear power plant shall submit a LER for any event of the type described in this paragraph within 60 days after the discovery of the event.

Section (a)(2)(i)(B) of 10 CFR Part 50.73, "Licensee Event Report System," states, in part, that the licensee shall report any operation or condition which was prohibited by the plant's Technical Specifications.

Contrary to the above, since September 20th, 2022 (60 days from the completion of a past operability assessment regarding PCIV B2103F019), through the date of the exit meeting for this report (October 19, 2022), the licensee failed to submit a LER. At the time of the exit meeting, the licensee had a corrective action to draft and submit the LER.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Unresolved Item (Open)

Seismic Displacement for Safety-Related Piping Not Verified URI 05000341/2022003-03 71111.18

Description:

Updated safety analysis report Table 3.2-1 delineates the residual heat removal service water (RHRSW) piping is designed to American Society of Mechanical Engineers (ASME)

Section III, Subsection ND, 1971 edition. ASME Section III Subsection ND-3611 states, in part, The requirements for acceptability of class 3 piping systems are that they shall be designed in accordance with the rules of NC-3600 except as otherwise permitted in this Sub article. ASME Section III Subsection NC-3622, states, in part, The provisions of NB-3622 shall apply except that, in addition ASME Section III Subsection NB-3622.1 requires impact forces caused by either external or internal conditions shall be considered in the piping design.

The inspectors reviewed calculation no. DC-2966 Volume Number IA DCD 2, Piping Stress Report RHR 03/19, Revision 0. The licensee performed this calculation to analyze the Division 1 RHRSW supply and return piping inside the reactor building. The inspectors noted that the maximum displacement (based on the seismic loading condition) for the piping was 1.233 inches. The licensee did not perform a physical inspection to determine whether the maximum displacement was acceptable and verify that no external impact forces exist between the piping and a system, structure, or component (SSC).

This issue is unresolved because the inspectors cannot determine whether there is a violation and will need information based on a physical inspection performed by the licensee to validate if the maximum piping displacement impacts any SSCs.

Planned Closure Actions: The inspectors will review the physical inspection information when it becomes available from the licensee to determine whether a violation exists.

Licensee Actions: The licensee plans to perform a physical inspection to validate if the maximum piping displacement impacts any SSCs.

Corrective Action References: CARD 22-27033, NRC Identified: Evaluation of Potential Rattle Space Violation, dated 06/10/2022.

Reactor Scram Due to Trip of Reactor Feed Pumps Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000341/2022003-04 Open/Closed None (NPP)71152A A finding of very low safety significance (Green) with an associated non-cited violation (NCV)of Technical Specification 5.4, "Procedures," was self-revealed on February 4, 2022, when the reactor automatically scrammed from approximately 58 percent power during a plant shutdown to start a refueling outage. Appropriate precautions regarding feed pump suction pressure were not included in the procedure for operating the feedwater system.

Description:

On February 4, 2022, the plant started a downpower to begin a refueling outage. The plant had been at approximately 58 percent power for several weeks due to the planned power profile before the outage. Both turbine-driven reactor feedwater pumps (RFPs) provided flow to the reactor and maintained the reactor level. One of the first evolutions scheduled was to secure one of the RFPs. Despite not performing the just-in-time training (JITT) practice session for this evolution (since the licensee scheduled this evolution for the night shift), the day shift crew decided to start the downpower and secure an RFP.

Additionally, while the crew that practiced the evolution lowered power to approximately 50 percent before securing an RFP, the day shift crew started securing an RFP at around 58 percent power. While procedurally allowed (the maximum power to secure an RFP was 60 percent), starting at a higher power resulted in a lower RFP suction pressure. Reactor feedwater pump suction pressure is an important parameter because if the pressure gets too low, an RFP can trip, and if the pressure gets too high, perturbations can start in the heater drains system.

While lowering the speed of the south RFP, the minimum flow valve started to open gradually before suddenly going full open. A sudden pressure drop at the suction of the RFPs occurred, causing the north RFP to trip. Operators attempted to raise feed flow with the south RFP, but had to trip it manually because vibration levels had increased. With the loss of both RFPs, the reactor scrammed on a low reactor water level condition (Level 3). The crew stabilized the plant without other injection systems using the condensate and feedwater systems. The operators maintained pressure control with the turbine bypass valves. No significant complications occurred during the scram, and the operators stabilized the plant in hot shutdown. On the following shift, the plant continued into the refueling outage.

The licensee conducted a root cause analysis to evaluate the event. The inspectors reviewed the licensee's root cause analysis. The licensee determined that the minimum flow control valves operated as expected, and a gap in the procedure for removing an RFP from service existed. Specifically, procedure 23.107, "Reactor Feedwater and Condensate Systems," did not alert operators to the behavior of the RFP minimum flow control valves and the impact they could have on suction pressure. In 2001, the licensee changed the method of removing an RFP from service.

The new method (which existed in the procedure during the February 4, 2022, event)involved taking manual control of the RFP speed. While lowering the speed, as flow decreased, the minimum flow control valve would start to open. However, given Fermi's plant-specific design, the minimum flow control valve would suddenly go fully open at some point, causing an approximate 250-pound pressure drop at the RFP suction. Before the procedure change in 2001, operators adjusted a bias setting to get the minimum flow control valve to open before taking manual control of the RFP. This method avoided the sudden opening of the minimum flow control valve and the resultant suction pressure drop. With the procedure change, the licensee failed to recognize all impacts on the system, including the sudden pressure drop that would occur at the RFP suctions due to the new behavior of minimum flow control valves. As a result, the licensee did not include appropriate parameters in the procedure for operators to observe while securing an RFP, especially from higher initial power levels.

Corrective Actions: The licensee performed a root cause analysis. The licensee created actions to revise procedures to account for feed system behavior while removing RFPs from service.

Corrective Action References: CARD 22-21157

Performance Assessment:

Performance Deficiency: The inspectors identified that the licensee failed to maintain a procedure for operation of the reactor feedwater system that included operating parameters appropriate for a quality procedure as described in Regulatory Guide (RG) 1.33, Quality Assurance Program Requirements (Operation). Specifically, critical parameters associated with operating the feedwater system were not included. The licensee is committed to RG 1.33 via TS 5.4, Procedures, and operation of the feedwater system is described as a safety-related process per RG 1.33.

Screening: The inspectors determined the performance deficiency was more than minor because it was associated with the Procedure Quality attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. Specifically, a latent procedural deficiency resulted in a reactor scram.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The finding screened as Green, or very low safety significance, based on answering 'no' to question B of Exhibit 1 of IMC 0609. Specifically, the normal feed and condensate systems remained able to control reactor water level while the turbine bypass valves controlled pressure following the scram (i.e., no loss of main condenser vacuum).

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to this finding because the inspectors determined the finding did not reflect present licensee performance. Specifically, the procedure change occurred in 2001.

Enforcement:

Violation: Technical Specification (TS) 5.4, Procedures, requires, in part, that the applicable procedures recommended in RG 1.33, Quality Assurance Program Requirements (Operation), are established, implemented, and maintained. Section 4 of RG 1.33 lists startup, shutdown, and operation of a boiling water reactor feedwater system as an applicable procedure. RG 1.33 further states ANSI N18.7-1976/ANS-3.2, "Administrative Controls and Quality Assurance for the Operational Phase of Nuclear Power Plants" requires preparation of the procedures. ANSI N18.7-1976/ANS-3.2 contains requirements for the content of procedures listed in RG 1.33. Section 5.3.2, Procedure Content, requires, in part, that procedures shall identify plant conditions that must exist prior to use. Further, that precautions should be established to alert the individual performing a task to those important measures which should be used to protect equipment and avoid abnormal situations.

Contrary to the above, from October 25, 2001, until April 19, 2022, Procedure 23.107, "Reactor Feedwater and Condensate Systems," was not maintained. Specifically, appropriate parameters (namely RFP suction pressure) were not included as prerequisites in the section for securing an RFP.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Observation: Response to Select CARDs in the Corrective Action Program 71152A The inspectors noted several Condition Assessment Resolution Documents (CARDs) written by licensee personnel near the end of the 2022 refueling outage that appeared to express concerns with production-over-safety. Some examples included questioning a policy of having operators man a confined space rescue team (CSRT) while they were also on the fire brigade, and questioning why a reactivity management senior reactor operator (RMSRO) was not stationed in the control room during a portion of the reactor startup. Further, the inspectors noted that the licensee had not potentially addressed a CARD from the 2020 refueling outage dealing with safety concerns associated with hand-barring the main turbine.

Additionally, the inspectors wanted to follow-up on an issue they identified during the refueling outage regarding how the licensee changed a test procedure. In consultation with regional management, the inspectors decided to review the licensee's follow-up to the various issues in the corrective action program.

The inspectors discovered no findings nor violations. However, the inspectors identified several observations that may contribute to the number of CARDs written questioning whether production or safety is the overarching priority when the licensee make decisions. In some cases, the inspectors noted a difference in the resolution documented in the CARDs and understood by the initiators, versus what had actually been done. Regarding the concern regarding the CSRT and fire brigade manning, operations management indicated they found additional personnel to man both positions, and this was not documented in the CARD nor communicated to the concerned operator. Additionally, while the practice may have been allowed, the inspectors noted an unbiased third party, such as a member of the safety department, could have weighed in and documented the acceptability.

For the hand-barring of the main turbine, the licensee took actions to address the concerns involving multiple departments, but the licensee did not document those actions nor was a formal work order created despite that being one of the corrective actions. For the RMSRO issue, while the licensee eventually staffed an additional senior reactor operator (SRO) from outside the shift, the initial attempt to resolve the question utilized a watchstander on shift to pick up the additional duty. If the assumption was that the plant was actually in the condition described by the concerned operator (an ongoing reactor startup), this would not have been allowed by the reactivity management procedure, MOP 19. As in the fire brigade example above, an unbiased third party may have been a more appropriate choice to evaluate the CARD. The inspectors noted a corrective action to benchmark other facilities and assess whether the licensee could add clarity to the procedure.

Regarding a change to how control rod scram time-testing was going to be performed (due to the normal measuring system being degraded), the inspectors questioned the use of a work order to allow use of other equipment versus following the more formal procedure change process. Ultimately, the licensee changed the procedure and wrote a CARD to explore the use of work orders. As a result, no findings nor violations were identified. The licensee also created an action to add clarity to their procedure change process.

Observation: Review of Reactor Scram due to Mayflies 71152A On June 24, 2022, the reactor automatically scrammed due to an electrical disturbance associated with the 345kV electrical distribution system on site. A large swarm of mayflies caused an electrical fault in the switchyard containing the main generator disconnects. As a result, the main turbine tripped, which caused the reactor to shut down.

Mayflies caused a similar electrical fault in 2020. The inspectors reviewed the circumstances, corrective actions from the 2020 event, and the evaluation performed for the 2022 event. The inspector identified no findings or violations. The 2020 event did not result in a reactor scram, and the licensee attributed the event to installing new LED lights near the 345kV switchyard.

Following that event, the licensee took actions to secure more lighting around the site, including the switchyard where the 2022 fault occurred. Unlike the 2020 event, where mayflies blanketed one of the electrical insulators and caused a short to ground due to excessive lighting in the area, the licensee determined that in 2022, a large swarm of mayflies traversed the site and, due to the density, caused a fault from ground to a suspended conductor despite the switchyard being completely dark.

The inspectors reviewed the immediate response to the trip, repairs, and proposed corrective actions. The inspectors identified no issues.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On October 19, 2022, the inspectors presented the integrated inspection results to Mr. P. Dietrich, Chief Nuclear Officer, and other members of the licensee staff.

On August 19, 2022, the inspectors presented the Radiation Protection Baseline inspection results to Mr. P. Dietrich, Chief Nuclear Officer, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Procedures

MWC 16-100

Work Control Conduct Manual Implementing Procedure:

Seasonal Readiness

48703549

Evaluate Request for Shutdown 46304 Revisions 1 & 2 for

Impact to Fermi 2

51689384

20KV Relay House Battery Charger Irregularity

63421855

Oil Seepage from Breaker GK

6417741

Enrico Fermi PP Circuit Breaker GH (120KV): Breaker Trip

Coil Test (ITCTRANSMISSION)

64847930

Replace Tagline Switches S4000P003,4,5,6

71111.01

Work Orders

255931

20KV Mat Fence Line Enhancements

6M721-5736-2

Control Center A/C Water System Functional Operating

Sketch

S

Drawings

6M721-5736-3

Control Center A/C Air System Functional Operating

Sketch

K

23.307

Emergency Diesel Generator System

135

23.413

Control Center HVAC

103A

23.413 Attachment

Control Center HVAC System Valve Lineup

103A

23.413 Attachment

Control Center HVAC System Electrical Lineup

103A

23.413 Attachment

Control Center HVAC System Instrument Lineup

103A

23.413 Attachment

4B

Division 2 CCHVAC Standby Verification Checklist

103A

71111.04

Procedures

23.413 Enclosure A

Control Center HVAC Damper Lineup Normal Mode

Division 2 Dampers

103A

Corrective Action

Documents

2-29295

Tracking AIM to Purchase Training Enhancement Items for

Fire Drills

09/02/2022

FB-RB-2-10a

Reactor Building Emergency Equipment Cooling Water,

North, Zone 10, EL. 613'6"

71111.05

Fire Plans

FP-AB-5-16d

Auxiliary Building Division 1 Control Center Heating,

Ventilating, and Air Conditioning System Equipment

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Room, Zone 16, EL. 677'6"

FP-AB-5-16e

Auxiliary Building Division 2 Control Center Heating,

Ventilating, and Air Conditioning System Equipment

Room, Zone 16, EL. 677'6"

FP-AB-BMT-4

Control Air Compressor Room, Zone 4, Elevation 551'0"

FP-RB-2-10b

Reactor Building Emergency Equipment Cooling Water,

South, Zone 10, EL. 613'6"

FP-RB-4-17b

Reactor Building Recirculation System Motor Generator

Area Zone 17, Elevation 659'6"

FP-TB

Turbine Building

Fermi 2 Safety Handbook

Miscellaneous

Fire Brigade Drill

Record Form

LP-FP-940-0933/Fire Drill Main Lube Oil Reservoir Room

TB2

09/01/2022

29.100.01 SH 1A

RPV Control-ATWS

29.100.01 SH 5

Secondary Containment and Rad Release

29.100.01 SH1

RPV Control

EP-101

Classification of Emergencies

EP-290

Emergency Notifications

63A

EP-290 Enclosure A

Electronic Notification Process

11/01/2021

EP-290 Enclosure B

Nuclear Plant Event Technical Data Form General

Information Requirements

2/06/2019

EP-290001

Initial Notification Form Review Checklist

10/22/2021

71111.11Q

Procedures

EP-290001

Follow-up Notification Form Review Checklist

09/02/2021

17-25134

Division 1 CCHVAC Chiller High Bearing Oil Temperature

06/08/2017

21-21951

Division 1 CCHVAC Chiller Trip

03/03/2021

21-24247

T4100B009 Division 1 CCHVAC Chiller Trip (MCR Alarm

8D5)

05/15/2021

2-27400

T4100B009 Division 1 CCHVAC Chiller Trip (MCR Alarm

8D5)

06/24/2022

2-27461

FO 22-01 Start Up Walkdown: MOV Actuator

Disconnected from Bonnet

06/27/2022

Corrective Action

Documents

2-28723

Low Oil Flow on from New CCHVAC Sleeve Bearings

08/14/2022

71111.12

Engineering

2-018

B2103F019 Actuator Separation Impact on Appendix J,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Evaluations

Including bypass, and IST Requirements

20.413.01

Control Center HVAC System Failure

47.306.06

MS Drain Valve PCIV Actuator

ARP 8D5

Division 1 Control Room A/C Trouble

Procedures

VMS25-39

Centrifugal Water Chillers

06/23/2010

Work Orders

58375116

Install TTC and Other Test Equipment in Preparation for

As Found Test

03/11/2022

21-31211

9D21 Division 1 EDG Sequencer Trouble

2/20/2021

2-22199

Frequency Oscillations Occurring for Installed Power

Supplies and Contingency Power Supplies Need

Evaluated

2/21/2022

2-22886

Nova Inverters Found OOT for B21K801B and R31K001

03/01/2022

2-26351

3D56 Testability Logic Channel A/B RPS/Power Failure -

B21N617B Gross Failure Downscale

05/16/2022

Corrective Action

Documents

2-26412

3D56 Testability Logic Channel A/B RPS/Power Failure in

Alarm

05/17/2022

Corrective Action

Documents

Resulting from

Inspection

2-27708

NRC Question - CARD 22-26351 Past Operability

07/05/2022

6I721-2080-27

Visual Annunciator and Sequence Recorder Alarm

Schematic

P

6I721-2155-21

Schematic Diagram Reactor Protection System Testability

Modification

L

6I721-2714-20

EDG Automatic Digital Load Sequencing System Manual

Test Diagram

D

6I721-2714-22

Electrical Schematic EDG Automatic Digital Load

Sequencing System H11P898A

F

6I721-2714-23

EDG Automatic Digital Load Sequencer System

2/18/1985

6I721-2714-24

EDG Automatic Digital Load Sequencing System

6I721-2714-25

Electrical Schematic E.D.G Automatic Digital Load

Sequencing System

Drawings

6I721-2714-6

Automatic Sequencing Cabinet

08/07/1984

71111.15

Engineering

TE-E21-22-003

2KV Nova Inverters Failed Bench Tests

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Evaluations

TE-R31-22-029

The Class IE Vital Power Distribution (VPD) System Nova

Inverter R31K002 Frequency Oscillation

Miscellaneous

Operator Logs

05/16/2022

Procedures

MMA11

Instrument Testing

DC-0703 Volume

No. III DCD 2

Pipe Supports for Piping Isometric M-3184-1 and M-3184-

DC-0703 Volume

No. IV DCD 1

Pipe Supports for Piping Isometric M-3184-1 and M-3184-

DC-0704 Volume

No. III DCD 1

Pipe Supports for Piping Isometric M-3185-2

DC-0704 Volume

No. IV DCD 1

Pipe Supports for Piping Isometric M-3185-2

DC-0780 Volume

No. I DCD 1

Piping Hanger Calculation per Drawing M-N-2178-2

DC-0781 Volume

No. I DCD 1

Hanger Calculations for M-N-2179-2

DC-0785 Volume

No. IA DCD 1

Hanger Calculations for M-N-2183-2

DC-0786 Volume

No. IA DCD 1

Piping Hanger Calculations

DC-2586 Volume

No. I DCD 1

Pipe Supports for Piping Isometric M-3359-1

DC-2586 Volume

No. II DCD 1

Pipe Supports for Piping Isometric M-3359-1

DC-2922 Volume

No. IA DCD 1

RHR Complex Piping Stress Report SX-08

DC-2923 Volume

No. IA DCD 1

RHR Complex Piping Stress Report SX-09

DC-2927 Volume

No. IA DCD I

RHR Complex Piping Stress Report SX-13

DC-2928 Volume

No. IA DCD 1

RHR Complex Piping Stress Report

71111.18

Calculations

DC-2956 Volume

No. lA DCD 1

Pipe Stress Analysis of EESW Supply Line Division 2 to

Heat Exchangers P4400B001D for M-3352-1 and M4630-

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

DC-2957 Volume

No. I DCD 1

Pipe Stress Analysis of EESW Return Line Division 11 (M-

3353-1, M-4631-1 and M-4657-1)

DC-2958 Volume

No. IA DCD 1

Pipe Stress Analysis of EESW Supply Line Division 1 to

Plate Heat Exchangers P4400BOO1A and P4400B001C

DC-2959 Volume

No. I DCD 1

Pipe Stress Analysis of EESW Return Line Division 1 from

Plate Heat Exchangers P4400B00IA and P4400B001C

DC-2965 Volume

No. IA DCD 2

Piping Stress Report for RHR-01 & 06

DC-2966 Volume

No. IA DCD 2

Piping Stress Report RHR 03/19

DC-6766 Volume

No. I DCD 1

Pipe Stress for Division 1 EESW and RHRSW Supply and

Return Lines

DC-6771 Volume

No. I

Division 1 RHR Complex and Reactor Building RHRSW

and EESW Penetrations Evaluations

SS-0026 Volume

No. II DCD 6

Reactor/Auxiliary Building-Final Load Verification for

Concrete Walls

2-24369

NRC Identified: EESW/RHRSW Design Specification

3071-517 does Not Acknowledge the use of Later ASME

Section III Codes used in Piping and Support Calculations

for the Systems

03/29/2022

2-26894

NRC Identified: Typo Error on Reference Document

Number in Calculations

06/07/2022

2-27033

NRC Identified: Evaluation of Potential Rattle Space

Violation

06/10/2022

2-27114

NRC Identified: Wrong Calculation Version Submitted to

ARMS

06/14/2022

2-27182

NQA - NRC Identified: Documentation Error on

Nondestructive Examination (NDE) Reports

06/16/2022

Corrective Action

Documents

Resulting from

Inspection

2-28927

NRC Identified, Legacy Pipe Support Calculation Used an

Improper Basis for Allowable Stress

08/22/2022

Engineering

Changes

80028

Division 1 Tie-in Buried Pipe Replacement for RHRSW

and EESW Systems

C

Miscellaneous

ASME

RHR Service Water Buried Piping Replacement EDP

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Repair/Replacement

Program 19-002

80026, 80027, 80028. 80029

ASME

Repair/Replacement

Program 19-003

Emergency Equipment Service Water Buried Piping

Replacement EDP 80026, 80027, 80028, 80029

ASME

Repair/Replacement

Program 21-041

RHR Service Water Buried Piping Replacement EDP

80028

ASME

Repair/Replacement

Program 21-044

EESW Division 1 Buried Piping Replacement EDP 80028

Design Specification

3071-517

The Detroit Edison Company Design Specification for

RHR Complex Fermi 2

E

21-QCR-0052

MT Welds on Replacement Pipe for RHRSW

05/26/2021

21-QCR-0053

MT Welds on Replacement Pipe for RHRSW

06/01/2021

21-QCR-0054

MT Weld on Replacement Pipe for RHRSW

06/10/2021

21-QCR-0071

NDE of RHRSW Replacement Pipe

06/16/2021

21-QCR-0072

MT of RHRSW Replacement Buried Pipe

06/22/2021

21-QCR-0076

MT of RHRSW Replacement Buried Pipe

06/23/2021

21-QCR-0078

MT of RHRSW Replacement Buried Pipe

06/29/2021

21-QCR-0083

MT of RHRSW Replacement Buried Pipe

07/07/2021

21-QCR-0084

MT of RHRSW Replacement Buried Pipe

07/07/2021

21-QCR-0089

MT Final Weld for 14" Supply Piping

06/30/2021

21-QCR-0090

28" RHRSW & EESW Return Piping Division 1

07/14/2021

21-QCR-0100

MT of Piping Iso EESW Supply to EECW Heat Exchanger

(Hx). Division1 Yard

07/15/2021

21-QCR-0102

28" RHRSW & EESW Return Piping Division 1

07/15/2021

21-QCR-0125

MT of RHRSW Replacement Buried Pipe

10/04/2021

21-QCR-0143

MT of 14" EESW Supply to EECW Division 1

09/29/2021

21-QCR-0144

24" RHRSW Supply to RHR Division 1

09/29/2021

21-QCR-0147

28" RHRSW & EESW Return Piping Division 1

10/05/2021

21-QCR-0159

MT of RHRSW Replacement Buried Pipe

10/12/2021

NDE Reports

21-QCR-0166

MT on 24" RHRSW Replacement Piping

10/14/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

21-QCR-0169

MT of RHRSW Replacement Buried Pipe

10/21/2021

21-QCR-0174

MT on 28" RHRSW Replacement Piping

10/19/2021

2-QCR-0317

MT of FW-E11-4647-09

2/26/2022

2-QCR-0384

MT on 28" Excavation on Repair Weld

03/11/2022

2-QCR-0389

Final MT on 28" Repair Weld

03/13/2022

2-QCR-0410

MT Excavation of Weld for RHRSW Replacement Pipe

03/08/2022

2496756

ECN-80026 / 28-Division 1 - Phase 4-RF21-RHRSW -

Buried Pipe-PMT Hydro (Final Whole System)

03/21/2022

Work Orders

2497382

ECN - 80026 / 28 - Division 1 - Phase 4 - RF 21 - EESW -

Buried Pipe - PMT Hydro (Final Whole System)

03/21/2022

2-25696

DWSIL Curve in IPCS Uses Wrong Drywell Pressure Input

04/26/2022

2-26351

3D56 Testability Logic Channel A/B RPS/Power Failure -

B21N617B Gross Failure Downscale

05/16/2022

2-26412

3D56 Testability Logic Channel A/B RPS/Power Failure in

Alarm

05/17/2022

2-26690

SCR Requested for IPCS DWSIL Drywell Pressure

Calculation

05/31/2022

2-28608

IPCS Incorrect Input to DWSIL Ineffectively

Communicated to Operations and Training Personnel

08/10/2022

Corrective Action

Documents

2-28837

DWSIL in Simulator Functions as Designed, Not as

Indicated by 22-25696

08/18/2022

Corrective Action

Documents

Resulting from

Inspection

2-27708

NRC Question - CARD 22-26351 Past Operability

07/05/2022

Drawings

6I721-2155-21

Schematic Diagram Reactor Protection System Testability

Modification

L

Engineering

Evaluations

Operator Logs

05/16/2022

400-23842-F03-28

Safety Parameter Display System [Confidential]

71111.19

Procedures

MMA11

Instrument Testing

2-21098

Potential FMS Gap in Hours Tracked in Fatigue

Management

2/04/2022

71111.20

Corrective Action

Documents

2-27315

Fatigue Management - Fatigue Assessment Not

06/21/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Performed as Required for Post Even - Injured Knee

Miscellaneous

Drill Scenario for August 16, 2022 Emergency

Preparedness Drill

n/a

EP-101

Classification of Emergencies

71114.06

Procedures

EP-301-01

Technical Support Center

08-27501

Closure of Barnwell Waste Management Facility - Class

B/C Waste Minimization Strategy

11/11/2008

Corrective Action

Documents

20-32274

Evaluate Excess Radioactive Material Stored Outside the

Plant Radiologically Controlled Area (RCA)

11/17/2020

Engineering

Evaluations

Scaling Factor

Report and Waste

Stream Sample

Results from GEL

Laboratories, LLC,

January 12, 2022

10CFR61 Analysis for Multiple Waste Streams

01/12/2022

Miscellaneous

Work Order 54316238

Performance of Source Leak Testing

01/04/2021

MMM06

Material Receipt, Identification, and Status

MMM10

Radioactive Material Procurement and Accountability

MRP21

Radwaste Shipping Operations

MRP24

Fermi-2 10CFR61 Compliance Manual

7A

Procedures

MRP26

Process Control Program

4B

NPRP-22-0044

Quick Hit Self-Assessment: Radioactive Solid Waste

Processing and Radioactive Material, Handling, Storage,

and Transportation

05/24/2022

Self-

Assessments

Quick Hit Self-

Assessment Report

- Part 37 Security

Plan

10CFR37 Self-Assessment

09/23/2021

EF2-22-018

Radioactive Waste Shipment of Dry Active Waste in a

General Design Package

03/11/2022

EF2-21-006

Radioactive Waste Shipment, EF2-21-006, of Waste Class

'A' Bead Resin in a Type 'A' Package

06/16/2021

71124.08

Shipping Records

EF2-22-034

Radioactive Waste Shipment Documents for Bead Resin

04/29/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

in a General Design Package

EF2-22-047

Bead Resin Waste Shipment: UN2916 Shipment in a Type

'B' Package

05/26/2022

Corrective Action

Documents

21-27287

23.206 Procedure Enhancement and Clarification

08/18/2021

Miscellaneous

MSPI

Fermi 2 MSPI Basis Document

71151

Procedures

44.020.231

NSSSS - RCIC Steam Line Flow, Trip System 'A'

Functional Test

19-20003

SOP 23.107 Correction Required

01/01/2019

20-29211

Safety of Personnel Barring the Main Turbine

08/11/2020

21-21815

RIN Superintendent Continues to Disregard Traits of a

Healthy Nuclear Safety Culture

2/25/2021

2-23605

Union Safety Concern - MTG Barring Device Needs

Improvement

03/14/2022

2-25476

Operations Management Committed to Production

04/21/2022

2-25798

Illusion of Safety

04/28/2022

2-25884

Reactor Engineering Needs to Know if Scram Time

Testing is Required on Various Control Rods

05/01/2022

2-26246

Reactivity Management SRO Not Stationed

05/12/2022

2-27456

Ground Fault on Y-Phase on Output from Main Unit

Transformer to CM and CF Output Breakers

06/27/2022

2-27473

Procedure Revision for Mayfly Infestation Preparation Plan

27.322

06/27/2022

2-27499

Add Circuits to 27.322 Mayfly Infestation

06/28/2022

Corrective Action

Documents

2-27633

NSRG 22-01-15; Safety Oversight Subcommittee Action -

Develop Comprehensive Strategy to Address Potential

SCWE Issue

07/01/2022

2-26236

NRC Identified - Question on Use of WO to Document

Scram Time Testing

05/11/2022

Corrective Action

Documents

Resulting from

Inspection

2-28815

NRC Identified - Observations Related to Incomplete

Written CARD Responses to Employee Concerns

08/17/2022

ANSI N18.7-1976

Administrative Controls and Quality Assurance for the

Operational Phase of Nuclear Power Plants

1976

71152A

Miscellaneous

Event Notification

Main Turbine Trip

06/24/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

2-003

Memorandum to

Pete Dietrich from

Eric Olson

First Trimester 2022 Nuclear Safety Culture Report

06/28/2022

Organizational

Effectiveness Cause

Evaluation CARD

20-27403

Turbine Trip Resulting in Reactor Scram

06/24/2022

Organizational

Effectiveness Cause

Evaluation CARD

20-27545

Loss of 345kv Due to Mayfly Infestation

07/02/2020

Root Cause

Evaluation Report

2-21157, Reactor SCRAM on Loss of Feed

SS-OP-202-22013

RF-21 Shutdown JITT

2.000.03

Power Operation 25% to 100% to 25%

107

23.107

Reactor Feedwater and Condensate Systems

71, 89, 90,

155

27.322

Mayfly Infestation Preparation Plan

17, 23

Procedures

MOP19

Reactivity Management

27