ML052130286

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IR 05000237-05-008 & 05000249-05-008; on 04/01/2005 - 06/30/2005; for Exelon Generation Company, Dresden Nuclear Power Station, Units 2 and 3; Identification and Resolution of Problems, Event Follow-up, Routine Integrated Report
ML052130286
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 07/29/2005
From: Ring M
NRC/RGN-III
To: Crane C
Exelon Generation Co
References
FOIA/PA-2010-0209 IR-05-008
Download: ML052130286 (55)


See also: IR 05000237/2005008

Text

July 29, 2005

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3

NRC INTEGRATED INSPECTION REPORT 05000237/2005008;

05000249/2005008

Dear Mr. Crane:

On June 30, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at

your Dresden Nuclear Power Station, Units 2 and 3. The enclosed report presents the

inspection findings which were discussed with Mr. D. Bost and other members of your staff on

July 12, 2005.

The inspection examined activities conducted under your license as they relate to safety and to

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, four NRC identified findings of very low safety

significance were identified. Two of these findings involved a violation of NRC requirements.

However, because of their very low safety significance and because they have been entered

into your corrective action program, the NRC is treating these issues as Non-Cited Violations, in

accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest any Non-Cited Violation, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to

the Regional Administrator, Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352;

the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C.

20555-0001; and the NRC Resident Inspector at the Dresden Nuclear Power Station.

C. Crane -2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Enclosure: Inspection Report 05000237/2005008; 05000249/2005008

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Dresden Nuclear Power Station

Dresden Nuclear Power Station Plant Manager

Regulatory Assurance Manager - Dresden

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Dresden and Quad Cities

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

State Liaison Officer

Chairman, Illinois Commerce Commission

DOCUMENT NAME: G:\dres\ML052130286.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RIII E RIII RIII

NAME MRing

DATE 07/29/05

OFFICIAL RECORD COPY

C. Crane -3-

ADAMS Distribution:

GYS

MXB

RidsNrrDipmIipb

GEG

KGO

DRC1

CAA1

C. Pederson, DRS (hard copy - IRs only)

DRPIII

DRSIII

PLB1

JRK1

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-237; 50-249

License Nos: DPR-19; DPR-25

Report No: 05000237/2005008; 05000249/2005008

Licensee: Exelon Generation Company

Facility: Dresden Nuclear Power Station, Units 2 and 3

Location: 6500 North Dresden Road

Morris, IL 60450

Dates: April 1 through June 30, 2005

Inspectors: D. Smith, Senior Resident Inspector

M. Sheikh, Resident Inspector

C. Phillips, Senior Operations Engineer

W. Slawinski, Senior Radiation Specialist

R. Winter, Reactor Engineer

L. Ramadan, Inspector, Region III

D. Melendez-Colon, Inspector, Region III

D. Reeser, Reactor Engineer

M. Gryglak, Reactor Inspector, Decommissioning Branch

R. Schulz, Illinois Emergency Management Agency

Approved by: Mark Ring, Chief

Branch 1

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000237/2005008; IR 05000249/2005008; 04/01/2005 - 06/30/2005; Exelon Generation

Company, Dresden Nuclear Power Station, Units 2 and 3; Identification and Resolution of

Problems, Event Follow-up, routine integrated report.

This report covers a 3-month period of baseline resident inspection; announced baseline

inspections on radiation material processing and transportation, operator requalification

program, maintenance rule effectiveness, and independent spent fuel storage installation

activities. The inspection was conducted by Region III inspectors and the resident inspectors.

Four Green findings, two of which involved Non-Cited Violations, were identified. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for

which the SDP does not apply may be Green or be assigned severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3,

dated July 2000.

A. Inspector Identified Findings

Cornerstone: Barrier Integrity

  • Green. On February 8, 2005, a performance deficiency was identified by the inspectors.

The licensee failed to identify the failure of the refuel floor damper in the reactor building

ventilation system in a timely manner which resulted in the late discovery of a design

deficiency with the standby gas treatment system. The standby gas treatment system

used reactor building ventilation ductwork before directing air flow to the standby gas

treatment filters. The refuel floor damper would throttle down, per design, to ensure a

local negative differential pressure in the reactor water cleanup heat exchanger rooms

with respect to the refuel floor. As a result, air flow to the standby gas treatment system

was significantly restricted and affected the standby gas treatment recovery time for the

entire secondary containment. The damper failed prior to 2003, masking the design

deficiency, and was unnoticed until February 2005. Also, inadequate inspections of the

dampers in the reactor building ventilation system during operation of the standby gas

treatment system contributed to the late discovery of this design issue. The primary

cause of this finding was related to the cross-cutting issue of problem identification and

resolution.

The finding was greater than minor because, if left uncorrected, the failure to identify

deficient plant equipment would become a more significant safety concern because

important systems could be rendered inoperable and because it impacted the barrier

integrity cornerstone objective to provide reasonable assurance that physical design

barriers protect the public from radionuclide releases caused by accidents or events. In

addressing this issue, the licensee gagged each units refuel floor damper open to 80

percent to ensure adequate air flow to the standby gas treatment system. The finding

was of very low safety significance because the standby gas treatment system was

always able to restore secondary containment differential pressure within the Technical

Specifications allowed outage time of four hours. (Section 4OA2.3)

1 Enclosure

  • Green. On May 2, 2005, a performance deficiency was identified by the inspectors. The

licensee failed to identify that corrective actions were ineffective from a previous 2004

event, involving the failure to follow the clearance order process. Also, an instrument

maintenance technician failed to properly implement annual clearance order process

training. As a result, the instrument maintenance technician removed the 2D traversing

incore probe (TIP) drawer which had a clearance order danger tag attached to the

control switch. The primary cause of this finding was related to the cross-cutting issues

of human performance and problem identification and resolution.

The finding was more than minor because, if left uncorrected, the licensees failure to

ensure plant personnel adherence to the clearance order process would become a more

significant safety concern by resulting in significant personnel safety consequences, and

because it impacted the barrier integrity cornerstone objective to provide reasonable

assurance that physical design barriers protect the public from radionuclide releases

caused by accidents or events. The removal and re-installation of the 2D traversing

incore probe drawer did not adversely affect the ability to ensure containment isolation

using the ball check containment isolation valve. The licensee briefed all maintenance

personnel on this event and added more detailed discussion on the clearance order

process to the annual site training. Therefore, this finding screened as having very low

safety significance. (Section 4OA2.6)

Cornerstone: Mitigating Systems

  • Green. On December 11, 2004, a performance deficiency involving a Non-Cited

Violation of 10 CFR Part 50, Appendix B, Criterion XI and Criterion III was identified by

the inspectors. The licensee failed to perform post-modification testing and to assure

critical aspects of the core spray modification installation, which included obtaining gap

measurement for mechanical joints, verifying the capability of the tooling to produce the

required surface finishes on pre-fabricated components, and verifying that the pre-

fabricated components were properly machined, met the leakage analysis

specifications.

The finding was greater than minor because it affected the mitigating systems

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences, specifically the

design control attribute. The finding was of very low safety significance because the

licensee was able to demonstrate, with the assistance of General Electric, that there

was reasonable assurance that the modification was installed properly. The licensee

planned to revise CC-AA-107, Configuration Change Acceptance Testing Criteria,

and/or CC-AA-107-1001, Post Modification Acceptance Testing. The procedure

change would provide that the substitution for post modification testing would ensure

quality at least equivalent to that specified in the original design bases. In addition, the

licensee planned to confirm that the installed core spray modification had been installed

with a level of quality equivalent to the original design basis. (Section 4OA3.1)

  • Green. On September 29, 2004, a performance deficiency involving a Non-Cited

Violation of 10 CFR Part 50, Appendix B, Criterion XVI, was identified by the inspectors.

The licensee had implemented inadequate corrective actions for a deficient condition

2 Enclosure

that occurred on September 6, 1996, to prevent recurrence of a similar deficient

condition that occurred on September 29, 2004. Both events involved the failure of

safety related time delay relays to meet acceptance criteria due to the use of a

stopwatch as a tool for calibration of safety related equipment. The primary cause of

this finding was related to the cross-cutting issue of problem identification and

resolution.

The finding was greater than minor because it impacted the mitigating system

cornerstone objective to ensure availability, reliability, and capability of systems that

respond to initiating events and because it affected the reliability of a safety related

component. As a result of the 2004 event, the licensee initiated issue report 258172,

created an action item to review the root cause of the event, revised the isolation

condenser initiation time delay relay calibration procedure to require the use of a strip

chart recorder, and created an action item to evaluate the extent of condition. The

finding was of very low safety significance because the isolation condenser system did

not lose the ability to perform its safety function and all other mitigating systems were

available. (Section 4OA3.3)

B. Licensee Identified Findings

No findings of significance were identified.

3 Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 2 began the inspection period at 912 MWe (95 percent thermal power and 100 percent of

rated electrical capacity).

  • On May 28, 2005, the unit was taken off line for main generator hydrogen seal

maintenance. The unit returned to full power on June 2, 2005.

  • On June 3, 2005, the unit downpowered to 767 MWe for control rod pattern adjustment,

and returned to full power on the same day.

Unit 3 began the inspection period at 912 MWe (95 percent thermal power and 100 percent of

rated electrical capacity).

seal. The unit returned to full power on May 1, 2005.

  • On May 8, 2005, the unit downpowered to 773 MWe for control rod pattern adjustment,

and returned to full power on the same day.

  • On June 2, 2005, the unit downpowered to 150 MWe due to a electro-hydraulic control

system oil leak in the turbine front standard. The unit returned to full power on June

4, 2005.

  • On June 16, 2005, the unit downpowered to 815 MWe due to an unexpected isolation of

a feedwater heater string, and returned to full power on the same day.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment (71111.04Q and S)

.1 Partial System Walkdowns

a. Inspection Scope

The inspectors selected a redundant or backup system to an out-of-service or degraded

train, reviewed documents to determine correct system lineup, and verified critical

portions of the system configuration. Instrumentation valve configurations and

appropriate meter indications were also observed. The inspectors observed various

support system parameters to determine the operational status. Control room switch

positions for the systems were observed. Other conditions, such as adequacy of

housekeeping, the absence of ignition sources, and proper labeling were also

evaluated.

4 Enclosure

The inspectors performed partial equipment alignment walkdowns of the:

  • Unit 2 Division I direct current system and Unit 3 Division II direct current system;

and

This represented four inspection samples.

b. Findings

No findings of significance were identified.

.2 Complete Walkdown

a. Inspection Scope

The inspectors performed a complete semiannual walkdown of the Unit 3 containment

cooling service water system to verify proper alignment, component accessibility,

availability, and current condition. The inspectors reviewed selected system operating

procedures, surveillance procedures, mechanical and electrical lineups, drawings, and

the Updated Final Safety Analysis Report (UFSAR) to identify proper system alignment.

The inspectors reviewed outstanding work orders associated with the system to

determine whether there were any deficiencies that could affect the ability of the system

to perform its safety related function. The inspectors also reviewed selected licensee

condition reports (CR) and issue reports (IR) to verify the effectiveness of completed

corrective actions of past issues.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

a. Inspection Scope

The inspectors toured plant areas important to safety to assess the material condition,

operating lineup, and operational effectiveness of the fire protection system and

features. The review included control of transient combustibles and ignition sources, fire

suppression systems, manual fire fighting equipment and capability, passive fire

protection features, including fire doors, and compensatory measures. The following

areas were walked down:

corner room, Fire Zone 11.2.1;

5 Enclosure

  • Unit 2/3 emergency swing diesel generator building, elevation 517' of the

emergency diesel generator room, Fire Zone 9.0.C;

  • Unit 2/3 turbine building, elevation 534' switchgear area, Fire Zone 8.2.6.A;
  • Unit 2 reactor building, elevation 476' 6" torus basement, Fire Zone 1.1.1.1;
  • Unit 3 turbine building, elevation 517' switchgear area, Fire Zone 8.2.5.E;

Zone 9.0.A; and

  • Unit 2 turbine building, elevation 517' trackway, Fire Zone 8.2.5.A.

This represented seven inspection samples.

b. Findings

No findings of significance were identified.

1R06 Flooding (71111.06)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report (USFAR)

Section 3.4.1.2 for internal flood analysis and reviewed the licensees procedure for

internal flooding. The inspectors walked down the Unit 2/3 cribhouse to verify

compliance with the licensees UFSAR and reviewed the licensees previously

implemented corrective actions for deficiencies associated with internal flood protection.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11A and Q)

.1 Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of the annual operating examination

which consisted of Job Performance Measure operating tests, and simulator operating

tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee from

May 3 through June 1, 2005. In addition, the inspectors reviewed the overall pass/fail

results for the biennial written examination (also required to be given per 10 CFR

55.59(a)(2)) administered by the licensee from May 4 through June 10, 2005. The

overall results were compared with the significance determination process in

accordance with NRC Manual Chapter 0609, Operator Requalification Human

Performance Significance Determination Process.

This represented one inspection sample.

6 Enclosure

b. Findings

No findings of significance were identified.

.2 Licensed Operator Requalification Program

a. Inspection Scope

The inspectors observed an evaluation of operating crew #3 on June 1, 2005. The

scenario consisted of a loss of instrument air (recoverable), loss of motor control

center 28-7/29-7, and a recirculation line break resulting in containment flooding. The

inspectors verified that the operators were able to complete the tasks in accordance with

applicable plant procedures. The inspectors observed the licensees evaluators to

ensure that no inappropriate cues were provided by the evaluators while assessing the

operators' performance. In addition, the inspectors verified that issue reports written

regarding licensed operator requalification training were entered into the licensees

corrective action program with the appropriate significance characterization.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness (71111.12B and Q)

.1 Periodic Evaluation

a. Inspection Scope

The inspectors examined the periodic evaluation report completed for the period of

October 1, 2002 through September 30, 2004. To evaluate the effectiveness of (a)(1)

and (a)(2) activities, the inspectors examined a sample of Dresden (a)(1) Action Plans,

performance criteria, functional failures, and issue reports. These same documents

were reviewed to verify that the threshold for identification of problems was at an

appropriate level and the associated corrective actions were appropriate. Also, the

inspectors reviewed the maintenance rule procedures and processes. The inspectors

focused the inspection on the following four systems (samples):

  • Direct current electric system;
  • High pressure core injection system (HPCI);
  • Hardened containment vent system.

The inspectors verified that the periodic evaluation was completed within the time

restraints defined in 10 CFR 50.65 (once per refueling cycle, not to exceed 24 months).

The inspectors also ensured that the licensee reviewed its goals, monitored structures,

systems, and components (SSCs) performance, reviewed industry operating

7 Enclosure

experience, and made appropriate adjustments to the maintenance rule program as a

result of the above activities;

The inspectors verified that the licensee balanced reliability and unavailability during the

previous refueling cycle, including a review of high safety significant SSCs;

The inspectors verified that (a)(1) goals were met, that corrective action was appropriate

to correct the defective condition, including the use of industry operating experience,

and that (a)(1) activities and related goals were adjusted as needed; and

The inspectors verified that the licensee has established (a)(2) performance criteria,

examined any SSCs that failed to meet their performance criteria, and reviewed any

SSCs that have suffered repeated maintenance preventable functional failures including

a verification that failed SSCs were considered for (a)(1).

In addition, the inspectors reviewed maintenance rule self-assessments that addressed

the maintenance rule program implementation.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Routine Inspection

a. Inspection Scope

The inspectors reviewed the licensee's handling of performance issues and the

associated implementation of the Maintenance Rule (10 CFR 50.65) to evaluate

maintenance effectiveness for the selected systems. The following systems were

selected based on being designated as risk significant under the Maintenance Rule,

being in the increased monitoring (Maintenance Rule category a(1)) group, or due to an

inspectors identified issue or problem that potentially impacted system work practices,

reliability, or common cause failures:

  • Unit 3 miscellaneous sumps and drains system.

The inspectors verified the licensee's categorization of specific issues, including

evaluation of the performance criteria, appropriate work practices, identification of

common cause errors, extent of condition, and trending of key parameters. Additionally,

the inspectors reviewed the licensee's implementation of the maintenance rule

requirements, including a review of scoping, goal-setting, performance monitoring,

short-term and long-term corrective actions, functional failure determinations associated

with the condition and issue reports reviewed, and current equipment performance

status.

This represented two inspection samples.

8 Enclosure

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors evaluated the effectiveness of the risk assessments performed before

maintenance activities were conducted on structures, systems, and components and

verified how the licensee managed the risk. The inspectors evaluated whether the

licensee had taken the necessary steps to plan and control emergent work activities.

The inspectors also verified that equipment necessary to complete planned contingency

actions was staged and available. The inspectors completed evaluations of

maintenance activities on the:

  • Unit 2 maximum combined flow limiter setting adjustment;
  • Unit 3 Division 1 core spray logic system functional testing;

system functional testing;

  • Unit 3 125 Vdc battery charger #3 removal from service; and
  • Unit 2 and Unit 3 concurrent performance of surveillances associated with the

core spray system, high pressure coolant injection system, and standby liquid

control system.

This represented five inspection samples.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a. Inspection Scope

The inspectors reviewed operability evaluations to ensure that operability was properly

justified and the component or system remained available, such that no unrecognized

increase in risk occurred. The review included issues involving the operability of:

differential pressure abnormally long (IR 320258); and

and 353273).

This represented three inspection samples.

9 Enclosure

b. Findings

No findings of significance were identified.

1R16 Operator Work-Around (71111.16)

Semi-annual Review of the Cumulative Effects of Operator Workarounds

a. Inspection Scope

The inspectors reviewed all operator workarounds and challenges to assess any

cumulative effect on the :

  • reliability, availability, and potential for misoperation of a system;
  • ability of operators to respond in a correct and timely manner to plant transients

and accidents.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed post-maintenance test results to confirm that the tests were

adequate for the scope of the maintenance completed and that the test data met the

acceptance criteria. The inspectors also reviewed the tests to determine if the systems

were restored to the operational readiness status consistent with the design and

licensing basis documents. The inspectors reviewed post-maintenance testing activities

associated with the following:

inspection;

flex house, replacement of 2/3 diesel generator coolant water pump with

stainless steel design; and

This represented four inspection samples.

10 Enclosure

b. Findings

.1 Inability to Trip the 2B Service Water Pump from the Control Room

Introduction: The inspectors identified an unresolved item regarding the adequacy of

installation of sixteen trip coil mechanisms for breakers on Unit 2 safety related 4KV

buses 23 and 24.

Description: On April 15, 2005, while swapping service water (SW) pumps, the onshift

operator started the 2A SW pump and then attempted to secure the 2B SW pump by

placing the control switch in the normal-after-trip position. However, the pump did not

trip as indicated by the motor amperage reading, and the light indication for the pump

did not illuminate. Subsequently, the onshift operator placed the control switch in the

pull-to-lock position, but the 2B SW pump continued to run. A non-licensed operator

was dispatched locally to bus 24 and tripped the pump with the local trip pushbutton on

the breaker.

On April 20, 2005, the licensee informed the residents that the tripping capability of the

2B SW water pump was lost due to the incorrect installation of the pumps trip coil

mechanism. Initially, the licensee considered this installation error to be generic in

nature and to have existed since 1995. The inability to trip the 2B SW pump was of

concern because bus 24 could be lost due to the inability to shed this load from the bus

during an accident. This bus was the power supply source for the Division II

containment cooling service water system pumps.

Subsequently, the licensee determined that the 2B SW pump was worked on

February 15, 2005, under Work Order (WO) 00727085-01. The work was to clean and

inspect the close latch reset mechanism on the breaker for hardened lubricant. The

WO included the appropriate information from the vendor manual on how to perform the

work; however, the electrician installed the trip coil incorrectly. The WO provided an

optional instructional step for post-maintenance testing, which specified verification of

the electrical operation of the breaker. Because this step was not required to be

performed, the post maintenance test did not identify that the 2B SW pump would not

trip from the control room after the incorrect installation of the trip coil mechanism. The

licensee proceeded with inspecting the installation of the trip coil mechanisms for all the

potentially affected breakers even though the licensee suspected that the inadequate

work on the 2B SW pump was an isolated case of poor human performance.

The licensee performed inspections of all the applicable Unit 3 breakers during the

April 2005 forced outage. The inspections confirmed that all trip coils had been properly

installed. Initially, the licensee was able to verify proper installation of the trip coils for

several breakers on Unit 2 that had their associated breaker opened since the

equipment was not in service. Four more breakers were inspected, with satisfactory

results, during the 2005 May maintenance outage. The remaining 16 breakers will be

inspected during the Fall 2005 refueling outage because the licensee was concerned

that the inspection activity, which involved the removal of the breaker cover, could

adversely impact plant operations. This issue will be an Unresolved Item (URI) pending

inspector review of the results of the inspections on the remaining breakers.

(URI 05000237/2005008-01)

11 Enclosure

1R20 Outage Activities (71111.20)

.1 Unit 3 Maintenance Outage

a. Inspection Scope

The licensee conducted a maintenance outage on Unit 3 from April 26-May 1, 2005.

During the outage the licensee replaced the 3B reactor recirculation pump seal, repaired

the 3B master trip solenoid valve, replaced the 3E electromatic relief valve, and

assessed the condition of the strain gauges on the main steam lines and made

appropriate repairs.

The inspectors verified that the licensee effectively conducted the shutdown, managed

elements of risk pertaining to reactivity control during and after the shutdown, and

implemented decay heat removal system procedure requirements as applicable. The

inspectors performed the following activities daily:

  • attended control room operator and outage management turnover meetings to

verify that the current shutdown risk status was well understood and

communicated;

  • performed walkdowns of containment to identify any indications of unidentified

leakage;

  • ensured that the control room operators adhered to the plants Technical

Specifications;

  • performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

  • reviewed selected issues that the licensee entered into the corrective action

program to verify that identified problems were being entered into the program

with the appropriate characterization and significance;

  • ensured that the licensee appropriately considered risk factors during the

development and execution of planned activities;

  • monitored licensees troubleshooting efforts for emergent plant equipment

issues;

  • performed plant walkdowns to observe ongoing work activities;
  • observed control rod withdrawals and initial transition to criticality;
  • performed walkdown of containment prior to closure to ensure that debris had

not been left that could affect the performance of the containment sumps; and

  • monitored Mode switch changes and observed portions of power ascension.

b. Findings

No findings of significance were identified.

.2 Unit 2 Maintenance Outage

a. Inspection Scope

On May 28, 2005, the licensee commenced a four day maintenance outage on Unit 2 to

replace the #10 main turbine generator seal. During the outage, the reactor remained

12 Enclosure

critical at approximately 20 percent power. The licensee replaced the 2A stator cooling

water pump, calibrated the bus duct temperature alarms, and repaired the turbine

generator thrust bearing wear detector.

The inspectors verified that the licensee effectively removed the turbine from service,

conducted the downpower, and managed elements of risk pertaining to reactivity control

during and after the downpower.

The inspectors performed the following activities daily:

  • attended control room operator and outage management turnover meetings to

verify that the current online risk status was well understood and communicated;

  • ensured that the control room operators adhered to the plants technical

specifications;

  • performed walkdowns of the main control room to observe the alignment of

systems important to shutdown risk;

  • reviewed selected issues that the licensee entered into the corrective action

program to verify that identified problems were being entered into the program

with the appropriate characterization and significance;

  • ensured that the licensee appropriately considered risk factors during the

development and execution of planned activities;

  • monitored licensee troubleshooting efforts for emergent plant equipment issues;

and

  • performed plant walkdowns to observe ongoing work activities.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed surveillance testing on risk-significant equipment and reviewed

test results. The inspectors assessed whether the selected plant equipment could

perform its intended safety function and satisfy the requirements contained in Technical

Specifications. Following the completion of each test, the inspectors determined that

the test equipment was removed and the equipment returned to a condition in which it

could perform its intended safety function.

The inspectors observed surveillance testing activities and/or reviewed completed

packages for the tests, listed below, related to systems in the initiating event, mitigating

systems, and barrier integrity cornerstones:

  • Dresden Operating Surveillance (DOS) 1600-29, Unit 2 and 3 Drywell

Temperature Surveillance, Revision 4

  • MA-DR-773-733, Unit 3 - Calibration and Functional Test of RPS MG Set and

RPS Reserve Power Supply EPAs, Revision 2;

13 Enclosure

  • Dresden Instrument Surveillance (DIS) 1400-05, Division 1 Core Spray System

Functional Test, Revision 26;

  • DIS 1400-05, Division 2 Core Spray System Functional Test, Revision 26;

Logic System Functional Test, Revision 5;

  • DOS 6620-07, Station Black Out 2 (3) Diesel Generator Surveillance Tests,

Revision 18.

This represented seven inspection samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Modification (71111.23)

a. Inspection Scope

The inspectors screened one active temporary modification and assessed the effect of

the temporary modification on safety-related systems. The inspectors also determined if

the installation was consistent with system design:

  • Temporary Change Configuration Package 354622, Install Temporary Jumper

at Electro Hydraulic Control System Card 2-5640-A37 (in Cabinet 2-0902-31) to

Bypass the Function of A Main Steam Pressure Regulator.

This represented one inspection sample.

b. Findings

No findings of significance were identified.

1EP6 Drill and Training Evaluation (71114.06)

.1 Evaluation of Operating Crew #6 Training Evolution

a. Inspection Scope

The inspectors evaluated the training evolution to assess the licensees performance

and to determine if the training was of the appropriate scope to be included in the

performance indicator statistics. The inspectors observed Crew #6 on May 11, 2005.

The scenario consisted of spurious isolation of high pressure coolant injection system,

control rod drive system leak and accumulator trouble, anticipated transient without

scram, and reactor building high radiation.

This represented one inspection sample.

14 Enclosure

b. Findings

No findings of significance were identified.

2. RADIATION SAFETY

Cornerstone: Public Radiation Safety

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems (71122.01)

.1 Inspection Planning

a. Inspection Scope

The inspectors reviewed the licensees current revision to the Offsite Dose Calculation

Manual (ODCM) and the licensees Radioactive Effluent Release Reports for calendar

years 2002, 2003, and 2004, along with selected radioactive effluent release data for

2005 through April 2005. The inspectors verified that technical evaluations were

completed for modifications to the ODCM since the last inspection of this program area

in 2003, and that effluent radiation monitor setpoints were changed accordingly since

completion of those modifications, as warranted. The inspectors also reviewed self-

assessments, audits, and licensee event reports that involved unanticipated offsite

releases of radioactive effluents, as applicable. The effluent reports, effluent data, and

licensee evaluations were reviewed to verify that the radioactive effluent control program

was implemented as required by the radiological effluent technical specifications (RETS)

and the ODCM, to verify that public dose limits from effluents were not exceeded, and to

ensure that any anomalies in effluent release data were adequately understood by the

licensee and were properly assessed and reported.

The inspectors reviewed the ODCM to identify the gaseous and liquid effluent radiation

monitoring systems and associated effluent flow paths including in-line flow

measurement devices, and reviewed the description of radioactive waste systems and

effluent pathways provided in the UFSAR in preparation for the onsite inspection.

These reviews represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Onsite Inspection - Walkdown of Effluent Control Systems, System/Program

Modifications, and Instrument Calibrations

a. Inspection Scope

The inspectors walked down the readily accessible components of the gaseous and

liquid release systems (e.g., radiation and flow monitors, tanks, and vessels) and the

radwaste control room to observe current system configuration with respect to the

15 Enclosure

description in the UFSAR, to discuss ongoing activities with radwaste operations staff,

and to assess equipment material condition. Records of material condition surveillances

performed since 2004 for those tanks and vessels located in locked high radiation areas

were reviewed to determine the extent of any problems and the licensees corrective

actions.

The inspectors reviewed the technical justification for any changes made by the licensee

to the ODCM, as well as changes to the liquid or gaseous radioactive waste system

design or operation since the last inspection to determine whether these changes

affected the licensees ability to maintain effluents as low as reasonably achievable and

whether changes made to monitoring instrumentation resulted in non-representative

monitoring of effluents. Radioactive effluent release reports for the three years

preceding the inspection were evaluated for any significant changes (factor of 5) in

either the quantities or kinds of radioactive effluents and for any significant changes in

offsite dose which could be indicative of problems with the effluent control program. No

significant adverse changes were identified.

The inspectors reviewed records of the most recent instrument calibrations for each

point-of-discharge effluent radiation monitor and for selected effluent flow measurement

devices to determine if they had been calibrated consistent with industry standards and

in accordance with station procedures, technical specifications and the ODCM.

Specifically, the inspectors reviewed calibration records for the following effluent

radiation monitors and flow measuring devices:

  • Unit 2/3 reactor building vent (station particulate, iodine and noble gas (SPING))

monitor;

  • Unit 2/3 main chimney (backup) noble gas monitor;
  • Unit 2/3 main chimney SPING monitor;
  • Unit 2 and Unit 3 service water effluent gross activity monitors;
  • Unit 2/3 liquid radwaste effluent gross activity monitor;
  • Unit 2 and Unit 3 isolation condenser vent radiation monitors;
  • Unit 2/3 main chimney flow rate monitoring device; and
  • Unit 2/3 reactor building vent flow rate monitoring device.

The inspectors also reviewed effluent radiation monitor setpoint bases and alarm

setpoint values for these monitors to verify their technical adequacy and for compliance

with ODCM criteria. Additionally, the inspectors discussed with system engineering staff

the availability and performance of the above listed effluent monitors and discussed the

corrective actions underway to address historical problems with the service water

monitors.

The inspectors reviewed chemistry department quality control data for those

instrumentation systems used to quantify effluent releases. Specifically, the inspectors

reviewed the most recent efficiency calibration records and lower limit of detection

determinations for Chemistry Department gamma spectroscopy systems and for the

liquid scintillation counter.

These reviews represented three inspection samples.

16 Enclosure

b. Findings

No findings of significance were identified.

.3 Onsite Inspection - Effluent Release Packages, Abnormal Releases, Dose Calculations,

and Laboratory Analytical Quality Control

a. Inspection Scope

The inspectors selectively reviewed batch liquid effluent release packages and gaseous

effluent sampling data for selected periods in 2004 through April 2005, including results

of chemistry sample analyses, the application of vendor laboratory analysis results for

difficult to detect nuclides, and the licensees effluent release procedures and practices.

Additionally, the inspectors reviewed the methods for calculating the projected doses to

members of the public from these releases. These reviews were performed to verify

that the licensee adequately applied analysis results in its dose calculations consistent

with ODCM methodology, and to determine if effluents were released in accordance with

the RETS/ODCM and procedural requirements.

The inspectors accompanied chemistry staff to observe the routine weekly change-out

of the particulate and iodine samplers and the collection of a noble gas sample from the

Unit 2/3 main chimney to determine if sampling practices, sampler restoration and

analytical techniques were sound and consistent with procedure.

The inspectors reviewed records of abnormal/unmonitored releases that the licensee

identified and documented in its 2003 and 2004 annual effluent reports and discussed

the methods used to quantify these releases. The inspectors also reviewed the

licensees practices for compensatory sampling during periods of effluent monitor

inoperability to verify compliance with ODCM requirements.

The inspectors reviewed a selection of quarterly and annual dose calculations to ensure

that the licensee properly calculated the offsite dose from radiological effluent releases

and to determine if any annual RETS/ODCM (i.e., Appendix I to 10 CFR Part 50) design

objectives (limits) were exceeded.

The inspectors reviewed the results of the quarterly radiochemistry inter-laboratory

cross-check comparisons for the five calendar quarters preceding the inspection to

validate the licensees analyses capabilities. The inspectors reviewed the licensees

evaluation of any disparate inter-laboratory comparisons and the associated corrective

actions for any deficiencies identified, as applicable. In addition, the inspectors

reviewed the results of the licensees 2003 and 2004 quality assurance audits of the

RETS/ODCM program.

These reviews represented four inspection samples.

b. Findings

No findings of significance were identified.

17 Enclosure

.4 Air Cleaning System Surveillance Tests

a. Inspection Scope

The inspectors reviewed the most recent results for both trains of the Unit 2/3 standby

gas treatment (SBGT) system ventilation system filter testing to verify that test methods,

frequency, and test results met technical specification requirements. Specifically, the

inspectors reviewed the results of in-place high efficiency particulate air (HEPA) and

charcoal absorber penetration tests, laboratory tests of charcoal absorber methyl iodide

penetration and in-place tests of pressure differential across the combined HEPA

filters/charcoal absorbers for the SBGT.

These reviews represented one inspection sample.

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors reviewed licensee self-assessments, audits, and special reports related

to the radioactive effluent treatment and monitoring program since the last inspection to

determine if identified problems were entered into the corrective action program for

resolution. The inspectors also verified that the licensee's problem identification and

resolution program together with its audit and self-assessment program were capable of

identifying repetitive deficiencies or significant individual deficiencies in problem

identification and resolution.

The inspectors reviewed various corrective action reports related to the radioactive

effluent treatment and monitoring program generated since 2004, interviewed staff, and

reviewed documents to determine if the following activities were being conducted in an

effective and timely manner commensurate with their importance to safety and risk:

  • Initial problem identification, characterization, and tracking;
  • Disposition of operability/reportability issues;
  • Evaluation of safety significance/risk and priority for resolution;
  • Identification of repetitive problems;
  • Identification of contributing causes;
  • Identification and implementation of effective corrective actions; and
  • Implementation/consideration of risk significant operational experience feedback.

These reviews represented one inspection sample.

b. Findings

No findings of significance were identified.

18 Enclosure

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

Cornerstone: Public Radiation Safety

.1 Radiation Safety Strategic Area

a. Inspection Scope

The inspectors sampled the licensees submittals for the performance indicator (PI)

listed below for the period indicated. The inspectors used PI definitions and guidance

contained in Revision 2 of Nuclear Energy Institute Document 99-02, Regulatory

Assessment Performance Indicator Guideline, to verify the accuracy of the PI data.

The following PI was reviewed:

  • Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrence.

The inspectors reviewed the licensees CR database and selected CRs generated since

this indicator was last reviewed in June 2004, to identify any potential occurrences such

as unmonitored, uncontrolled, or improperly calculated effluent releases that may have

significantly impacted offsite dose. The inspectors reviewed gaseous and liquid effluent

summary data and the results of associated offsite dose calculations for 2004 to

determine if indicator results were accurately reported. Additionally, the inspectors

discussed with chemistry staff its methods for quantifying effluents and determining

effluent dose.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Quarterly Review

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action system at an appropriate threshold,

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Minor issues entered into the licensees

corrective action system as a result of inspectors observations are generally denoted in

the report. In addition, in order to help identify repetitive equipment failures or specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees corrective action program. This review was

19 Enclosure

accomplished by reviewing daily issue reports and attending daily issue report review

meetings.

b. Findings

No findings of significance were identified.

.2 Semiannual Review for Trends

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

the inspectors performed a review of the licensees corrective action program (CAP) and

associated documents to identify trends that could indicate the existence of a more

significant safety issue. The inspectors review consisted of a six month period from

January 2005 through June 2005, although some examples expanded beyond those

dates when the scope of the trend warranted. The inspectors reviewed multiple issue

reports generated during the time period of January through June 2005, in an attempt to

identify potential trends. The screening was accomplished as follows:

1. IRs dealing with company policies, administrative issues, and other minor issues

were eliminated as being outside the scope of this inspection;

2. The IRs were sorted into categories involving same equipment problems,

repetitive issues, reoccurring departmental problem/challenges and repeated

entries into technical specifications. The IRs were then screened for potential

common cause issues and considered for potential trends;

3. The inspectors removed groups of IRs that discussed strictly programmatic

problems because the inspection requirement was primarily for equipment

problems and human performance issues;

4. The inspectors removed groups of IRs that discussed security issues, those will

be reviewed and documented as necessary in a separate report during a future

inspection by a security specialist;

5. The inspectors also removed groups of IRs where their review indicated that

duplicate IRs had been written for the same event or failure;

6. The inspectors obtained a list of all licensee common cause investigations

initiated in the last six months. All IRs in which the title indicated a trend or

potential adverse trend were considered licensee-identified trends;

7. The remaining groups, considered potential unidentified trends, were provided to

the licensee for discussion in case there was extenuating information that the

inspectors were not aware of; and

8. Groups of IRs remaining after all of the above screening were considered trends

which the licensee had failed to identify.

20 Enclosure

9. The inspectors then were able to make an assessment by comparing the trends

identified by the licensee to those trends identified by the NRC.

In addition, the inspectors reviewed corrective action backlog lists and all of the nuclear

oversight assessments and audits conducted during January to June of 2005.

This represented one inspection sample.

b. Findings

There were no findings of significance identified. The inspectors determined that

licensee employees were writing issue reports at an appropriate threshold, and that

employees at all levels of the organization were writing IRs. The inspectors determined

that the licensee had identified the same specific trends as the inspectors. Overall, the

licensee identified issues adequately and entered them into their corrective action

program.

.3 Secondary Containment Differential Pressure (dP)

a. Inspection Scope

The inspectors reviewed issue reports associated with the loss of secondary

containment dP and the inability to maintain secondary containment dP at the required

Technical Specifications (TS) value of -0.25 inch dP when starting one train of the SBGT

system either automatically or manually.

This represented one inspection sample.

b. Findings

Introduction: A Green finding was identified by the inspectors involving the licensees

failure to identify the failure of a damper in the reactor building ventilation system in a

timely manner, and the licensee's failure to identify a design deficiency during operation

of the SBGT system. The licensee identified the damper failure on February 8, 2005.

However, the damper had been in a failed open condition since 2003. The failed open

damper allowed significant additional air flow and masked a design deficiency with air

flow to the SBGT system. The amount of air flow to the SBGT system was significantly

restricted when the failed damper was repaired, which delayed the ability of the SBGT

system to restore secondary containment dP to -0.25 inch.

Description: The inspectors reviewed the control room logs and determined that there

were eight occasions between January 14, 2005 and May 20, 2005, where there were

problems with the SBGT system maintaining secondary containment to -0.25 inch dP.

During the first six instances, one train of the SBGT system was able to restore

secondary containment dP to -0.25 inch within 5 to 15 minutes. Other variables which

contributed to the normal recovery times of 5 to 15 minutes included wind speed, and

the resultant 28 square foot opening in secondary containment that existed until the

reactor building ventilation isolation valves closed due to the delay time between

21 Enclosure

manually securing reactor building ventilation fans and closing the reactor building

ventilation isolation valves.

On April 1, 2005, the seventh occurrence, after manually starting one train of the SBGT

system and manually isolating the reactor building ventilation system, secondary

containment was not restored to -0.25 inch dP until 56 minutes later. On May 20, 2005,

the SBGT system automatically started when a refueling floor radiation monitor failed

high. Secondary containment was not recovered to -0.25 inch dP until 12 minutes and

had reached a positive value for approximately one minute. In addition to this

occurrence where secondary containment went positive, the licensee determined that

there were 51 other times when secondary containment went positive between July

26, 2001 and January 24, 2005.

As a result of the April 1, 2005 event, the inspectors challenged the acceptability of

reactor building ventilation and SBGT performance with respect to the time required to

restore secondary containment to -0.25 inch dP. The licensee conducted an

investigation into the April 1, 2005 event. The licensee documented in apparent cause

evaluation 320358 that the excessive 56 minute recovery time was due to an inadequate

design, which had existed since original plant operation, and inadequate inspections of

the reactor building ventilation system.

The SBGT system was designed to maintain Unit 2 and 3 secondary containment at

-0.25 inch dP by using reactor building ductwork and controls to ensure all radioactive

particles were processed through the SBGT system before releasing to the

environment. The reactor building ventilation system has a significantly higher flow rate

than the SBGT system. This flow rate difference between the systems was the reason

why the restricted air flow affected the SBGT system and not the reactor building

ventilation system. One dP controller, #2-5703-15, controlled 14 dampers, including the

refuel floor damper on each unit, #2/3-5772-58. The operation of the SBGT system was

adversely affected by the operation of this dP controller when the refuel floor damper

was operating correctly. The dP controller controlled area dP control dampers to ensure

the regenerative and non-regenerative heat exchanger rooms were maintained at a

negative pressure relative to the refuel floor. If a negative dP was not maintained

between these rooms and the refuel floor, dP controller #2-5703-15 would throttle down

all 14 area control dampers and force air to be drawn from these two heat exchanger

rooms. Since the SBGT system used the reactor building ventilation ductwork prior to

directing flow to the SBGT system, the throttling down response of the 14 area control

dampers restricted the air flow available to the SBGT system and delayed the systems

ability to restore the entire secondary containment to -0.25 inch dP.

Refuel floor damper #2-5772-58, had failed full open and remained in this position

from 2003 until February 8, 2005 and masked the air flow restriction problem to the

SBGT system. As a result of this damper failing open, when dP controller #2-5703-15

sent signals to all 14 dampers to throttle down, the SGBT system was able to draw a

significant amount of flow through this damper from the refueling floor and restore

secondary containment to -0.25 inch dP much sooner. After damper #2-5772-58 was

repaired on March 14, 2005, and capable of throttling down, the SBGT system would

experience excessive recovery times in restoring secondary containment based on the

severely restricted air flow to the SBGT system. The overall result was that the ability of

22 Enclosure

the SBGT system to restore total secondary containment was negatively impacted

based on the design of dP controller #2-5703-15. The inspectors determined and the

licensee agreed that there was a lack of sensitivity toward the loss of secondary

containment as supported by the 52 times that secondary containment went positive.

The licensee addressed this design deficiency by gagging the refuel floor damper on

each unit open by 80 percent. This action ensured adequate air flow to the SBGT

system and thus would allow timely restoration of secondary containment.

Analysis: The inspectors determined that the licensees failure to identify the failure of

refuel floor damper #2-5772-58 in a timely manner, which delayed the licensees

discovery of a design deficiency with the SBGT system, was a performance deficiency

warranting a significance evaluation. The inspectors concluded that the finding was

greater than minor in accordance with Inspection Manual Chapter (IMC) 0612, Power

Reactor Inspection Reports, Appendix B, Issue Screening, issued on May 19, 2005.

The inspectors concluded that the finding, if left uncorrected, would become a more

significant safety concern by potentially rendering safety related equipment inoperable

and because it impacted the barrier integrity cornerstone objective to provide reasonable

assurance that physical design barriers protect the public from radionuclide releases

caused by accidents or events. The flow to the SBGT system was significantly

restricted when damper #2-5772-58 operated as designed. The restricted air flow

delayed the ability of the SBGT system to restore secondary containment to -0.25 inch

dP. Although the SGBT system was adversely impacted by the refuel floor damper, the

SBGT system always restored secondary containment within the four hour TS allowed

outage time. The primary cause of this finding was related to the cross-cutting issue of

problem identification and resolution.

The inspectors completed a Phase 1 significance determination of this issue using

IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated

December 1, 2004. The inspectors concluded that the finding impacted the barrier

integrity cornerstone. The inspectors answered Yes to question 1 under the

containment barrier cornerstone column, in that, the finding only affected the SBGT and

reactor building ventilation systems. Therefore, this finding is of very low safety

significance (Green).

Enforcement: No violations of NRC requirements occurred because the finding involved

the reactor building ventilation system which is a non-safety related system. The

licensee entered this issue into the stations corrective action program as IR 320258.

The licensee implemented several corrective actions which included immediately

gagging open the refuel floor damper on each unit. The licensee subsequently changed

the set point of the differential pressure controller which would throttle the 14 dampers

less and thus ensure the restoration of secondary containment in a more timely manner.

(Finding (FIN)05000237/2005008-02; 05000249/2005008-02)

.4 Unit 2/3 Cribhouse Sump Pump Failure

The inspectors reviewed IR 331423. On May 3, 2005, the licensee entered Dresden

Operating Abnormal Procedure (DOA) 40-02, Localized flooding in plant, Revision 15,

due to the accumulation of 6 - 8" of water in the 2/3 cribhouse. The flooding occurred

due to the failure of the sump pumps limit switches which prevented the sump pumps

23 Enclosure

from starting on a high water level condition in the sump. The inspectors identified that

the licensee failed to repair the 2/3 cribhouse sump pumps level switches, in

accordance with the work control process, when the switches failed in February 2005.

This represented one inspection sample.

a. Effectiveness of Problem Identification

(1) Inspection Scope

The inspectors reviewed IR 331423 and the associated investigation report to verify that

the licensees identification of the problems were complete, accurate, and timely, and

that the consideration of extent of condition review, generic implications, and common

cause was adequate.

(2) Issues

There were no issues in the area of Effectiveness of Problem Identification.

b. Prioritization and Evaluation of Issues

(1) Inspection Scope

The inspectors reviewed IR 331423 and the associated investigation report. The

inspectors considered the licensees evaluation and disposition of performance issues,

and application of risk insights for prioritization of issues.

(2) Issues

The inspectors interviewed station personnel and reviewed the appropriate WO for the

issue. The inspectors noted that in February 2005, the 2/3 cribhouse sump was about

to overflow due to the failure of the sump pumps level switches. A facility type WO was

initiated in February to repair the level switches and was prioritized as a B3 ticket. Per

work control procedure WC-AA-106, Work screening and processing, Revision 2, B3

type work was supposed to be performed within five weeks.

The WO was initially on hold due to a request for parts; however, the work was not

completed even after the part arrived on March 1, 2005. The inspectors questioned the

lack of timely corrective actions for repairing the level switches, which were not

completed until May 2005. The licensee indicated that the untimely repair of the level

switches was because the work was assigned to the Fix It Now team. Due to emergent

work and maintenance outages which added to the teams backlog, the Fix It Now team

did not work this WO within the five week period. As a result of the licensees failure to

resolve the deficiency with the sump pumps level switches in February 2005, the

switches failed again and flooded the 2/3 cribhouse in May 2005. At that time, the

licensee initiated aggressive actions to repair the level switches. If the licensee had

repaired the switches in a more timely manner, reccurrence of the sump pumps failure

to run would not have occurred and caused the flooding in the cribhouse. The licensee

initiated IR 337135 to address the inspectors concerns. In addition, the licensee

24 Enclosure

implemented actions to address weaknesses in prioritizing the Fix It Now teams WO

backlog.

c. Effectiveness of Corrective Actions

(1) Inspection Scope

The inspectors reviewed the corrective actions which resulted from the investigation

report associated with IR 331423 to determine if the issue report addressed generic

implications and that corrective actions were appropriately focused to correct the

problem.

(2) Issues

There were no issues in the area of Effectiveness of Corrective Actions.

.5 Corrective Action Program

Introduction

The inspectors identified several examples where the licensee failed to properly

implement the various aspects of the stations CAP during this period. During the first

quarter 2005 and the fourth quarter of 2004, the licensee experienced problems with

writing issue reports. Initially, the inspectors planned to document this problem in the

first quarter inspection report; but, instead discussed this problem as an observation

during the quarterly exit meeting on April 15, 2005.

Additional examples of this problem ,as well as other deficient implementation aspects

of the stations CAP, continued to occur and included the lack of appropriate challenge

of documented information in issue reports, inappropriate closure of issue reports by the

site ownership committee (SOC) and management review committee(MRC), and the

failure of shift managers to document the operability basis when issue reports

documented known deficient plant conditions.

a. Effectiveness of Problem Identification

(1) Inspection Scope

The inspectors reviewed all the IRs and the associated immediate followup actions to

verify that the licensees identification of the problems was complete and accurate, and

that the consideration of extent of condition review, generic implications, and common

cause was adequate.

(2) Issues

Generally, the licensee identified deficient plant conditions but did not always enter the

items into the stations CAP. The licensee failed to generate five issue reports, until

prompted the inspectors. The issues were minor in nature. The licensee subsequently

generated the following Irs: 321457(Delay in Reset of TIP Group 2 Isolation from Partial

25 Enclosure

Group 2 Isolation), 333251(Ultrasonic Flow Meter for U2 Hydrogen Seal Oil Flow),

325867 (PPE Exemption Form not Properly Displayed), 345612 (Unit 2 SW Rad Monitor

Spike), and 338026 (Received Unexpected H2 Area Trouble Alarm).

b. Prioritization and Evaluation of Issues

(1) Inspection Scope

The inspectors considered the licensees evaluation and disposition of performance

issues, and application of risk insights for prioritization of issues.

(2) Issues

Generally the license prioritized and evaluated the issues. However, there were several

examples where either the shift manager failed to document the basis for operability for

deficient plant equipment or the site ownership and management review committees did

not challenge the absence of operability information or other information which ensured

effectiveness of the corrective action process. The oversight by the (CAP) committees

and the shift managers did not result in the inoperability of any equipment. The licensee

subsequently generated IRs 343019 (Operator Struck in Head by Falling Light Diffuser),

333408 (NRC Identifies Valve Locking Chain on Cable Tray Support), and 327336 (NRC

Questions Actions Taken in SOC and MRC Closure of IRs).

c. Effectiveness of Corrective Actions

(1) Inspection Scope

The inspectors reviewed the corrective actions for the associated IRs to determine if the

issue reports addressed generic implications and that corrective actions were

appropriately focused to correct the problem.

(2) Issues

The licensee continued to experience problems with initiating IRs without being

prompted by the inspectors. The site ownership and management review committees

had several instances where both groups were not effective in ensuring the appropriate

actions were taken by the station for documented plant deficiencies. Also, the shift

managers had not been consistently documenting the basis for why equipment

remained operable when deficiencies were identified with equipment.

This represented one inspection sample.

26 Enclosure

.6 Removal of the 2D Traversing Incore Probe Drawer While Clearance Order Danger Tag

Was Attached to Equipment

a. Inspection Scope

The inspectors reviewed the licensees followup actions to a clearance order event on

May 2, 2005. The inspectors interviewed several maintenance supervisors and

reviewed associated documentation for this event.

This represented one inspection sample.

b. Findings

Introduction: A Green finding was identified by the inspectors. The licensee failed to

identify that corrective actions were ineffective from a previous 2004 event involving the

failure to follow the clearance order process. Also, an instrument maintenance

technician failed to properly implement annual clearance order process training. As a

result, the instrument maintenance technician removed the 2D TIP drawer while it was

tagged out-of-service with a danger tag.

Description: On May 2, 2005, instrument maintenance (IM) technicians were assigned

to perform WO 692871-01 which was a two year preventive maintenance task on the 2D

TIP drawer. Operations personnel had placed clearance order #35879 to allow the

performance of other work associated with the system; a clearance order danger tag

was placed on the control switch of the 2D TIP drawer. During the pre-job brief, the IM

technicians did not discuss clearance order tags for WO 692871-01 because a

clearance order was not required for this type of work. After obtaining approval from the

on shift operations crew, the IM technician noted the clearance order danger tag on the

control switch of the 2D TIP drawer. Although the IM technicians pre-job briefing did

not discuss the 2D TIP drawer having a clearance order tag, the lead IM technician did

not question this information. Instead, the IM technician removed the drawer with the

clearance order tag and placed the tag inside the WO.

After the lead IM technician completed the work and was returning the 2D TIP drawer to

the control room on May 3, 2005, the Unit 2 unit supervisor noted the clearance order

danger tag inside the WO. The licensee re-installed the 2D TIP drawer, re-hung the

clearance order tag, and initiated a quick human performance investigation (QHPI). The

licensees investigation determined that of the two IM technicians conducting the work;

only the lead IM technician had been aware of the clearance order danger tag. The

second IM technician, who was responsible for only performing a verification that the

correct drawer was identified for removal, did not notice the danger tag. The lead IM

technician was not aware of the requirements specified in Clearance and Tagging

Procedure, OP-MW-109-101, Revision 3, which prohibited the removal of a component

from a system when the component had a danger tag attached to it. The IM lead

technician assumed that the system was in a safer condition by removing the drawer. In

addressing this issue, the licensee briefed this event to all maintenance personnel and

added more detailed training on the clearance order process to the annual Nuclear-

General Employee Training.

27 Enclosure

After the inspectors became aware of this issue, the inspectors informed the licensee

that this potentially significant personnel safety event did not receive the appropriate

level of concern and communication from the senior plant management. This issue was

not discussed at the operations shift turnover or the plan-of-the-day meetings. Also,

after the inspectors review of the QHPI, the inspectors determined that this event was a

repeat occurrence of an event on Unit 3 during the October 2004 refueling outage. The

QHPI failed to identify that this was a repeat event and that the corrective actions were

ineffective in preventing the recurrence of the May 2005 clearance order error. During

the previous event on November 4, 2004, an electrician removed the 3B drywell cooler

breaker which had been tagged out-of-service with a danger tag attached and in the

racked to test position. The licensee had also conducted a QHPI for this event and

implemented corrective actions which were limited to briefing electrical maintenance

personnel on the event. Since the second QHPI failed to identify ineffective corrective

actions from the first QHPI which also involved a clearance order error and both could

have had significant personnel safety consequences, the inspectors questioned the

appropriateness of conducting a QHPI for this type of event. Also, the inspectors were

concerned that the boilerplate QHPI did not contain the required information to ensure

previous events were reviewed while performing the QHPI. This was a concern to the

inspectors because no other actions were planned by the licensee other than the

performance of the QHPI, which would result in not discovering previous ineffective

corrective actions. The licensee generated IR 346783, as a result of the inspectors

comments on the deficient aspects of the QHPI. In addition, the licensee briefed this

event to all maintenance personnel and will conduct more detailed training on the

clearance order process during annual site training.

Analysis: The inspectors determined that the licensees failure to implement effective

corrective actions from the November 2004 event and an IM technicians failure to apply

annual clearance order training resulting in the repeat occurrence in May 2005

constituted a performance deficiency warranting a significance evaluation. The

inspectors concluded that the finding was greater than minor in accordance with

IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, issued

on May 19, 2005. The inspectors concluded that the finding, if left uncorrected, would

become a more significant safety concern by resulting in significant personnel safety

consequences, and because it impacted the barrier integrity cornerstone objective to

provide reasonable assurance that physical design barriers protect the public from

radionuclide releases caused by accidents or events. The primary cause of this finding

was related to the cross-cutting areas of problem identification and resolution as well as

human performance.

The inspectors completed a Phase 1 significance determination of this issue using

IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated

December 1, 2004. The inspectors concluded that the finding impacted the barrier

integrity cornerstone. Removal and re-installation of the 2D TIP drawer did not

adversely affect the ability to ensure containment isolation using the ball check

containment isolation valve. The inspectors answered Yes to question 1 under the B

containment barrier cornerstone column, in that, the finding ultimately did not adversely

affect containment isolation ability; and concluded that this issue was of very low safety

significance (Green).

28 Enclosure

Enforcement: No violations of NRC requirements occurred because the finding involved

non-safety related equipment. The licensee entered this issue into their corrective

program as IR 346783. The licensee briefed this issue to all three maintenance shops

and revised the annual Nuclear General Employee Training to include more detailed

discussions on the clearance order process. (FIN 05000237/2005008-03)

4OA3 Event Follow-up (71153)

.1 (Closed) URI 05000249/2005003-01: Install U3 Core Spray Lower Sectional

Replacement

b. Findings

Introduction: A Green finding involving a Non-Cited Violation of 10 CFR 50, Appendix B,

Criterion XI, Test Control, and Criterion III, Design Control., was identified by the

inspectors. The licensee failed to perform post-modification testing and to assure

critical aspects of the core spray modification installation, which included obtaining gap

measurement for mechanical joints, verifying the capability of the tooling to produce the

required surface finishes on pre-fabricated components, and verifying that the pre-

fabricated components were properly machined, met the leakage analysis

specifications.

Description: During the Fall 2004 Unit 3 refueling outage, the licensee implemented

engineering change 6602 for the replacement of the lower sectional piping of the core

spray system. The modification was intended to replace piping inside the reactor vessel

annulus that was susceptible to intergranular stress corrosion cracking (IGSCC) due to

the environment and original welded materials (Type 304 stainless steel). The IGSCC

could result in leakage from the piping into the annulus rendering the core spray system

inoperable. The lower sectional replacement was designed by General Electric (GE)

using IGSCC resistant materials with mechanical connections in lieu of eight previously

welded connections to further mitigate susceptibility to IGSCC.

The modification consisted of cutting the core spray piping in the annulus at two points.

The first, on a vertical section of pipe referred to as the downcomer area, and the

second after the piping turned horizontal at the point where the piping enters the core

shroud. This section, once cut out, would be replaced with an L shaped pre-fabricated

piece of piping made of IGSCC resistant materials previously mentioned. The

downcomer piping would be joined to the pre-fabricated piping using a compression

fitting. After being cut, the downcomer was made up to a pre-fabricated ring such that

there was a flat surface to surface contact. The bottom of the ring was rounded and

mated with the flanged area of the pre-fabricated piping. The other end of the pre-

fabricated piping was bolted to the core shroud.

General Electric performed GENE-0000-0021-4342-04, Dresden Nuclear Power

Station, Unit 3 Core Spray Line Lower Sectional Replacement Leakage Analysis,

Revision 0. This analysis calculated the maximum gap sizes where mechanical

components were joined together that would result in excess leakage outside the core

shroud. Potential leakage pathways were between the downcomer pipe and the ring,

between the ring and the flange, and between the pre-fabricated piping and the core

29 Enclosure

shroud. An important component to the leakage analysis was the surface finishes of the

cut piping and the pre-fabricated ring and flange. Exceeding the maximum gap size,

described in the leakage analysis, could render one or more trains of the core spray

system inoperable. Although these finishes were critical parameters in the modification,

the licensee did not verify that the modification was bounded by the leakage analysis

through the verification of maximum gap sizes or through post modification testing.

Since the licensee did not obtain these gap measurements, the inspectors requested

the licensee to demonstrate how they ensured that the maximum gaps were not

exceeded. The licensee was unable to provide documentation of compliance; however,

the licensee along with GE demonstrated how the design of the mating surfaces

between the pre-fabricated piping and the core shroud would ensure that the gap at that

location would not be exceeded.

The licensee requested documentation from GE showing that the tooling used to make

the piping cuts inside the reactor vessel annulus on the downcomer was capable of

producing the surface finish specified in the GE leakage analysis. General Electric did

not have any documentation that could demonstrate this capability at the time of the

request. General Electric sent two coupons, that had been cut by the tooling used at

Dresden, out for independent measurement. One of the two coupons did not meet the

surface finish specification requirements and was due to dropping of the coupon after it

had been cut at the site in San Jose, California. This action marred its finish and

caused it to fail the test. The inspectors concurred with GEs conclusion of why the

coupon failed after reviewing the applicable documentation.

The licensee requested that GE provide documentation to show that the pre-fabricated

components were machined to the specifications described in the leakage analysis.

Although documents were located, GE determined that the pre-fabricated ring did not

meet the leakage analysis specifications. Subsequently, GE determined that the

leakage analysis was still bounded by the new surface of the ring under GENE-0000-

0021-4342-04, Dresden Nuclear Power Station, Unit 3 Core Spray Line Lower Sectional

Replacement, Revision 3.

Although the licensee failed to perform a post modification test or obtain gap

measurements of the mechanical joints to ensure the modification was bounded by the

leakage analysis, the licensee was able to demonstrate, with the assistance of GE that

there was reasonable assurance that the modification was installed properly and that the

maximum leakage specifications were not exceeded.

One of the station procedures that implemented Exelon Quality Assurance Manual,

Topical Report, Revision 75, Chapter 11, was CC-AA-107-1001, Post Modification

Acceptance Testing, Revision 0. Step 4.2.3.5 of CC-AA-107-1001, stated that, there

are times when portions of the modification will not be tested or are unable to be tested.

Justification for not testing at the site needs to be provided. The licensee stated that

justification for not testing was never completed. The inspectors pointed out that

CC-AA-107-1001 allowed for not testing modifications; however, the Exelon Quality

Assurance Manual Topical Report did not. The inspectors determined by review of

IR 343848, and through discussions with licensee management that the licensee

planned to revise CC-AA-107, Configuration Change Acceptance Testing Criteria,

30 Enclosure

and/or CC-AA-107-1001. The procedure change would provide that the substitution for

post modification testing would ensure quality at least equivalent to that specified in the

original design bases. In addition, the licensee planned to confirm that the installed core

spray modification had been installed with a level of quality equivalent to the original

design basis.

Analysis: The licensee failed to perform post-modification testing and to assure critical

aspects of the core spray modification installation, which included obtaining gap

measurement for mechanical joints, verifying the capability of the tooling to produce the

required surface finishes on pre-fabricated components, and verifying that the pre-

fabricated components were properly machined, met the leakage analysis specifications

was a performance deficiency warranting a significance evaluation. The inspectors

concluded that the finding was greater than minor in accordance with IMC 0612, Power

Reactor Inspection Reports, Appendix B, Issue Screening, issued on May 19, 2005

because it affected the mitigating systems cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences, specifically the design control attribute. The

licensee, with assistance from GE was able to demonstrate proper installation of the

core spray system piping modification inspite of the licensees failure to ensure gap

measurements for mechanical joints, verify the capability of the tooling, determine that

the pre-fabricated components were properly machined, and conduct post modification

testing to ensure the leakage analysis remained valid for these various aspects.

The inspectors completed a Phase 1 significance determination of this issue using

IMC 0609, Significance Determination Process, Appendix A, dated December 1, 2004.

The inspectors determined that this finding impacted the mitigating system cornerstone.

The inspectors entered the mitigating systems cornerstone column of the Phase I SDP

sheet and answered No to all five questions. Therefore, the inspectors concluded that

the finding was of very low safety significance (Green).

Enforcement: Title 10 of the Code of Federal Regulations Part 50, Appendix B,

Criterion XI, states, a test program shall be established to assure that all testing

required to demonstrate that structures, systems, and components will perform

satisfactorily in service is identified and performed in accordance with written test

procedures which incorporate the requirements and acceptance limits contained in

applicable design documents. The test program shall include ... operational tests during

nuclear power plant operation, of structures, systems, and components.

The Exelon Quality Assurance Manual, Topical Report, Revision 75, Chapter 11, Test

Control implements Title 10 of the Code of Federal Regulations Part 50, Appendix B,

Criterion XI. The Exelon Quality Assurance Manual, Topical Report, Revision 75, states

in Chapter 11, Test Control, Section 2.1.1, that the test program covers all required tests

including the demonstration of satisfactory performance following plant maintenance or

modifications. Section 2.7 states, in part, The Company performs testing following

plant modification or significant changes in operating procedures to confirm that the

modification or changes produces the expected results.

Title 10 of the Code of Federal Regulations Part 50, Appendix B, Criterion III, Design

Control, states in part, that measures shall be established to assure that applicable

31 Enclosure

regulatory requirements and the design basis, as defined in § 50.2 and as specified in

the license application, for those structures, systems, and components to which this

appendix applies are correctly translated into specifications, drawings, procedures, and

instructions. These measures shall include provisions to assure that appropriate quality

standards are specified and included in design documents and that deviations from such

standards are controlled.

Contrary to the above, from October 26, 2004, to December 11, 2004, the licensee

installed Modification EC 6602, Core Spray Lower Sectional Replacement, without

performing post modification testing or assuring that appropriate quality standards were

specified in installation procedures and instructions to ensure obtaining gap

measurement for mechanical joints, verifying the capability of the tooling to produce the

required surface finishes on pre-fabricated components, and verifying that the pre-

fabricated components were properly machined in order to meet the leakage analysis

specifications. Because this violation was of very low safety significance and because

the issue was entered into the licensees corrective action program (IR 303093,

IR 325097, and IR 325133), the issue is being treated as a NCV, consistent with Section

VI.A.1 of the NRC Enforcement Policy. (NCV 05000249/2005008-04)

.2 (Closed) Licensee Event Report (LER) 50-237/2005-002-00: Unit 2 Group 1 Isolation

and Resulting Scram

On March 24, 2005, with Unit 2 at full power, an automatic scram occurred due to the

malfunction of the A electro-hydraulic control system pressure regulator. All systems

responded as expected to the scram. Initial investigation and troubleshooting activities

by the licensee focused on the pressure regulator circuitry and card connections that

could have caused the transient. However, no abnormalities were identified. In

addition, the licensee sent the A45", C46", and A54" cards from the A electro-

hydraulic control pressure regulator circuitry to an offsite lab for failure analysis. No

abnormalities or failed components were found.

A root cause investigation to determine the cause of the failure was initiated and

concluded that the apparent cause of the failure was indeterminate. The licensee

determined that the most probable cause of this event was attributed to an increase in

electrical resistance between electrical pins 13 and 22 on card A54." Also, calculations

identified that an increase in electrical resistance of approximately 220 ohms for pin 22

or 2000 ohms for pin 13 could have caused the event. Corrective actions completed

and planned by the licensee included the replacement of the A45", A54", and C46"

cards prior to startup; replacement of the A54" card backplane connector; and rework

of the remaining connectors to card A54" during the Fall 2005 refueling outage. This

LER was reviewed by the inspectors and no findings were identified. This LER is

closed.

.3 (Closed) LER 50-249/2004-005-00: Unit 3 Isolation Condenser Time Delay Relays

Exceed Technical Specification Allowable Value

32 Enclosure

b. Findings

Introduction: A Green finding involving a Non-Cited Violation of 10 CFR Part 50,

Appendix B, Criterion XVI, was identified by the inspectors. The licensee failed to

implement adequate corrective actions to prevent recurrence of a deficient condition that

occurred on September 6, 1996, which involved surveillance testing of the anticipated

transient without scram (ATWS) time delay relays. This failure caused the Unit 3

isolation condenser (IC) time delay relays to exceed their TS allowable values due to the

continued usage of the stopwatch as a calibration tool.

Description: On September 29, 2004, the licensee conducted DIS 1300-08, Sustained

High Reactor Pressure Time Delay Relay Calibration, Revision 2. Three of the four

reactor high pressure IC initiation time delay relays were found out-of-tolerance and in

non-compliance with TS requirements. The IC will initiate on a sustained high reactor

pressure in a one-out-of-two twice logic. The purpose of the time delay was to avoid

spurious initiations of the IC system by allowing time for the spurious pressure spike,

caused by a main steam isolation or stop valve closure, to decay. The maximum time

delay allowed per TS surveillance requirement 3.3.5.2.3 was 15 seconds. The as-found

time delay relay setting values for high pressure switches 2-263-53A, 53B and 53C were

15.2, 15.8 and 15.1 seconds, respectively. IR 258172 was issued on

September 29, 2004, to document this issue.

The inspectors had previously closed LER 50-249/96012-00, which discussed the out of

tolerance of ATWS time delay relays, due to inadequate calibration check methodology.

Three of the four low-low reactor water level ATWS time delay relays were found

outside of the TS tolerance. The licensee determined that the initial failures were

attributable to human error in using a stopwatch. In addressing this issue, the licensee

switched to the use of a chart recorder to enhance time delay measurements. The

licensee indicated that the testing methodology, that utilized the chart recorder, would

produce more reliable and accurate results by eliminating human errors and reducing

test equipment response time errors.

One of the corrective actions associated with the 1996 event was to revise safety related

surveillance procedures to either increase the available margin to the TS allowable value

and/or require the use of a measurement technique that was not affected by errors

inherent in the use of stopwatches. A stopwatch was determined to be insensitive to

calibration checks on components with limited margin. However, the IC time delay

relays were not identified as affected components; therefore, the procedure was not

revised.

The three relays that were outside the TS allowable value were last tested on

June 16, 2002, using DIS 1300-01, Sustained High Reactor Pressure Time Delay Relay

Calibration, Revision 15. The relays were left within the as-left setting tolerance using a

stopwatch. As a result, when the relays were tested on September 29, 2004, the

as-found values for three of the relays were outside the TS limit which was a violation of

the TS.

Analysis: The inspectors determined that the failure to have adequate corrective actions

associated with repetitive failures of safety-related instruments was a performance

33 Enclosure

deficiency warranting a significance evaluation. The inspectors concluded that the

finding was greater than minor in accordance with IMC 0612, Power Reactor Inspection

Reports, Appendix B, Issue Screening, issued on May 19, 2005, because it impacted

the mitigating system cornerstone objective to ensure availability, reliability, and

capability of systems that respond to initiating events and because it affected the

reliability of a safety related component. The failure to utilize appropriate tools while

performing instrument calibrations can result in equipment being outside of the TS

allowable limits over the surveillance period and hence inadequate performance of

safety related equipment. However, the IC system did not lose the ability to perform its

safety function and all other mitigating systems were available. Therefore, this finding

was considered to be of very low safety significance. The licensee was able to

demonstrate, with the assistance of outside vendors, that during the period since the

last calibration of the time delay relays, the IC system would have initiated at a time

sooner than that assumed in the loss of feedwater transient analysis which was the

most bounding analysis. The primary cause of this finding was related to the cross-

cutting issue of problem identification and resolution.

The inspectors completed a Phase 1 significance determination of this issue using

IMC 0609, Significance Determination Process, Appendix A, Attachment 1, dated

December 1, 2004. The inspectors concluded that the finding impacted the mitigating

system cornerstone. The inspectors answered No to all five questions under the

mitigating system cornerstone column, and the issue screened as having very low safety

significance (Green).

Enforcement: Appendix B, Criterion XVI of 10 CFR Part 50, required, in part, that

measures shall be established to assure that conditions adverse to quality, such as

failures, malfunctions, deficiencies, deviations, defective material and equipment, and

non-conformances are promptly identified and corrected. In the case of significant

conditions adverse to quality, the measures shall assure that the cause of the condition

is determined and corrective actions taken to preclude repetition. Contrary to the above,

the licensee implemented ineffective corrective actions to prevent recurrence of the

1996 event, involving out-of-tolerances of ATWS relays. This failure allowed the usage

of stopwatches in the performance of safety related surveillances. As a result three

relays were outside TS requirements after performing DIS 1300-01, Revision 15. As a

result of the 2004 event, the licensee initiated IR 258172, created an action item to

review the root cause of the event, revised the IC initiation time delay relay calibration

procedure to require the use of a strip chart recorder, and created an action item to

evaluate the extent of condition. Because this violation was of very low safety

significance and it was entered into the licensees corrective action program

(IR 258172), this violation is being treated as an NCV, consistent with Section VI.A of

the NRC Enforcement Policy. (NCV 05000249/2005008-05)

4OA4 Cross-Cutting Findings

.1 A finding described in Section 4OA2.3(1) of this report had, as its primary cause, a

problem identification and resolution issue, in that, the licensee was slow in identifying a

failed damper in the reactor building ventilation system. As a result, a design deficiency

with the standby gas treatment system, that caused a delay in the systems ability to

restore secondary containment to the required -0.25 inch differential pressure, continued

34 Enclosure

to exist. The design deficiency had existed since original construction and remained

masked by the damper failure until 2005.

.2 A finding described in 4OA2.3(4) of this report had, as its primary cause, problem

identification and resolution as well as human performance, in that, the licensee failed to

implement effective corrective actions for a November 2004 event involving the removal

of equipment with a clearance order danger tag. As a result, a repeat event involving

an instrument maintenance technician removing equipment with a clearance order

danger tag occurred in May 2005. The instrument maintenance technician had received

training on the clearance order process and should have been aware of the requirement

that prohibited the removal of equipment when tagged in this manner.

.3 A finding described in Section 4OA3.3 of this report had, as its primary cause, problem

identification and resolution. The licensee failed to implement adequate corrective

actions to prevent recurrence of a deficient condition that occurred on

September 6, 1996, which involved surveillance testing of ATWS time delay relays.

This failure caused the Unit 3 isolation condenser time delay relays to exceed the TS

allowable values due to the continued usage of a stopwatch as a calibration tool.

4OA5 Other Activities

.1 Operational Readiness of Offsite Power (Temporary Instruction (TI) 2515/163)

The objective of TI 2515/163, "Operational Readiness of Offsite Power," was to confirm,

through inspections and interviews, the operational readiness of offsite power (OSP)

systems in accordance with NRC requirements. On May 22-25, 2005, the inspectors

reviewed licensee procedures and discuss the attributes identified in TI 2515/163 with

licensee personnel. In accordance with the requirements of TI 2515/163, inspectors

evaluated licensee procedures against the attributes discussed below.

The operating procedures that the control room operator uses to assure the operability

of the OSP have the following attributes:

1. Identify the required control room operator actions to take when notified by the

transmission system operator (TSO) that post-trip voltage of the OSP at the

nuclear power plant will not be acceptable to assure the continued operation of

the safety-related loads without transferring to the onsite power supply.

2. Identify the compensatory actions the control room operator is required to

perform if the TSO is not able to predict the post-trip voltage at the nuclear

power plant for the current grid conditions.

3. Identify the notifications required by 10 CFR 50.72 for an inoperable offsite

power system when the nuclear station is either informed by its TSO or when an

actual degraded voltage condition is identified.

The procedures to ensure compliance with 10 CFR 50.65(a)(4) have the following

attributes:

35 Enclosure

1. Direct the plant staff to perform grid reliability evaluations as part of the required

maintenance risk assessment before taking a risk-significant piece of equipment

out-of-service to do maintenance activities.

2. Direct the plant staff to ensure that the current status of the OSP system has

been included in the risk management actions and compensatory actions to

reduce the risk when performing risk-significant maintenance activities or when

loss of offsite power or station blackout mitigating equipment are taken

out-of-service.

3. Direct the control room staff to address degrading grid conditions that may

emerge during a maintenance activity.

4. Direct the plant staff to notify the TSO of risk changes that emerge during

ongoing maintenance at the nuclear power plant.

The procedures to ensure compliance with 10 CFR 50.63 have the following attribute:

1. Direct the control room operators on the steps to be taken to try to recover offsite

power within the station blackout coping time.

The results of the inspectors' review were forwarded to office of Nuclear Reactor

Regulation for further review and evaluation. "

.2 Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

a. Inspection Scope

The inspectors evaluated the licensees response to the failure of the cask transfer

facility (CTF) while the CTF was lifting a cask loaded with fuel. The inspectors reviewed

the prompt investigation report, a condition report, and an engineering evaluation

associated with the incident. The inspectors also reviewed the certificate of compliance

(CoC), the technical specifications, the Safety Evaluation Report, Revision 1, the Final

Safety Analysis Report (FSAR), Revision 2, and the Calculation Package On Hitran-140,

Revision 2. The purpose of the review was to verify that the cask configuration had

been analyzed to withstand natural phenomena such as tornados, earthquake, tornado

missile strike, and a vertical drop, and that the radiation dose rates contained in the

technical specifications were not exceeded. The inspectors also reviewed the

10 CFR 72.48 safety screening/evaluation and the special procedure, Hi-Track setdown

at the CTF (Action Tracking Item (ATI) 340904-14), to verify that the use of an

alternative lifting device with four hydraulic lifting boom systems conformed with

conditions of the CoC , the technical specifications, and the FSAR.

b. Findings

No findings of significance were identified

36 Enclosure

4OA6 Meetings

.1 Interim Exit Meeting

Interim exit meetings were conducted for:

  • Maintenance Effectiveness Periodic Evaluation with D. Bost, Site Vice President

on April 15, 2005;

  • Radiation Protection (RETS/ODCM) inspection with Mr. D. Bost and other

licensee staff on April 29, 2005;

  • Licensed Operator Requalification 71111.11 with Mr. M. Otten, Operations

Requalification Training Supervisor on June 16, 2005, via telephone; and

  • Independent Spent Fuel Storage Installation with Mr. M. Mikota, Dry Cask

Project Manager, via telephone, on June 21, 2005.

ATTACHMENT: SUPPLEMENTAL INFORMATION

37 Enclosure

KEY POINTS OF CONTACT

Licensee

D. Bost, Site Vice President

D. Wozniak, Plant Manager

S. Bell, Shipping Specialist

H. Bush, Radiological Engineering Manager

R. Conklin, Radiation Protection Supervisor

J. Fox, Design Engineer

R. Gadbois, Operations Director

D. Galanis, Design Engineering Manager

V. Gengler, Dresden Site Security Director

J. Griffin, Regulatory Assurance - NRC Coordinator

P. Salas, Regulatory Assurance Manager

J. Kalb, Environmental/ODCM Chemist

A. Khanifar, Nuclear Oversight Director

S. Kroma, Reactor Services Project Manager

T. Loch, Supervisor, Design Engineering

M. McGivern, System Engineer

M. Mikota, Dry Cask Project Manager, Dresden

D. Moore, Dry Cask Project Manager, Quad Cities

D. Nestle, Radiation Protection Technical Manager

M. Otten, Operations Requalification Training Supervisor

M. Overstreet, Radiation Protection Supervisor

R. Quick, Security Manager

N. Spooner, Site Maintenance Rule Coordinator

J. Strmec, Chemistry Manager

B. Surges, Operations Requalification Training Supervisor

G. Bockholdt, Maintenance Director

S. Taylor, Radiation Protection Director

NRC

M. Ring, Chief, Division of Reactor Projects, Branch 1

IEMA

R. Zuffa, Resident Inspector Section Head, Illinois Emergency Management Agency

R. Schulz, Illinois Emergency Management Agency

1 Attachment

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000237/2005008-01 URI Inability to Trip the 2B Service Water Pump from the

Control Room

05000237/2005008-02 FIN Failure of the Refuel Floor Damper & Design Deficiency

05000249/2005008-02 with the Standby Gas Treatment System

05000237/2005008-03 FIN Removal of the 2D Traversing Incore Probe Drawer With

Clearance Order Danger Tag Attached

05000249/2005008-04 NCV Modification to the Unit 3 Core Spray Piping

05000249/2005008-05 NCV Isolation Condenser Time Delay Relays Exceed TS Value

Closed

05000237/2005008-02 FIN Failure of the Refuel Floor Damper & Design Deficiency

05000249/2005008-02 with the Standby Gas Treatment System

05000237/2005008-03 FIN Removal of the 2D Traversing Incore Probe Drawer With

Clearance Order Danger Tag Attached

05000249/2005008-04 NCV Modification to the Unit 3 Core Spray Piping

05000249/2005008-05 NCV Isolation Condenser Time Delay Relays Exceed TS Value

(4OA3.4)05000249/2005003-01 URI Install U3 Core Spray Lower Sectional Replacement

50-249/2004-005-00 LER Unit 3 Isolation Condenser Time Delay Relays Exceed

Technical Specification Allowable Value

50-237/2005-002-00 LER Unit 2 Group 1 Isolation and Resulting Scram

Discussed

None

2 Attachment

LIST OF DOCUMENTS REVIEWED

The following is a list of documents reviewed during the inspection. Inclusion on this list does

not imply that the NRC inspectors reviewed the documents in their entirety but rather that

selected sections of portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R04 Equipment Alignment

-DOP 6900-E4; Revision 11; Unit 2 Electrical Systems Checklist

-DOP 6900-E1; Revision 07; Unit 3 Electrical Systems Checklist

-DOP 7500-M1/E1; Revision 06; Unit 2/3 Standby Gas Treatment

-OP-MW-109-101; Revision 2, Attachment 14; Worker Tagout Form Part 1: Hang/Lift

Section; Tagout # 2005-3131

-DOP 1400-M1; Revision 20; Unit 3 Core Spray System

-DOP 1400-E1; Revision 03; Unit 2 Core Spray Electrical

-DOP 1400-M1/E1; Revision 17; Unit 3 Core Spray System

-DOP 0900-E1; Revision 20; Unit 2(3) Control Room Panels

-DOP 1500-E1; Revision 13; Unit 3 LPCI and CCSW Electrical

-DOP 1500-M1; Revision 29; Unit 3 LPCI and Containment Cooling Valve Checklist

-DOP 1500-01; Revision 13; Preparation of Low Pressure Coolant Injection for

Automatic Start

-DOP 1500-02; Revision 50; Torus Water Cooling Mode of Low Pressure Coolant

Injection System

-DOP 1500-03; Revision 29; Containment Spray Cooling Mode of Low Pressure Coolant

Injection System

-DOP 1500-05; Revision 14; LPCI System Operation and/or Shutdown After Automatic

Initiation

-IR 344388; LPCI Thermal Performance Calculations Delayed; June 9, 2005

-IR 342659; Flow Transmitter Found Out of Tolerance During Calibration; June 9, 2005

-IR 314046; CCSW Pump Vibration in the Alert Range; March 17, 2005

-IR 295277/295464; Unit 3 CCSW Flow Instrumentation Piping Improperly Supported;

January 28, 2005

-IR 293713; Pipe Degradation of 2C & 2D CCSW Pump Discharge Elbows;

January 24, 2005

-DWG M-355; Diagram of Service Water Piping; Revision RP

-DWG M-360; Sheet 1; Diagram of L.P. Coolant Injection Piping; Revision VK

-DWG M-360; Sheet 2; Diagram of L.P. Coolant Injection Piping; Revision AV

1R05 Fire Protection

-Dresden Fire Pre-Plan U2TB-43; Revision 05

-Dresden Fire Pre-Plan U2TB-45; Revision 05

-Dresden Fire Pre-Plan U2TB-51; Revision 05

-Dresden Fire Pre-Plan U3TB-76; Revision 05

3 Attachment

-Dresden Fire Pre-Plan U2/3DG-105; Revision 05

-IR 328975; Low Water Level in Ssd Light Batteries; May 2, 2005

-IR 333918; Bell Alarm for 3 Detectors Only Buzzes; May 10, 2005

-IR 334382; Green Normal Power Light Is out Wih No Trouble or Alarm LIG;

May 12, 2005

-IR 336018; 1-4199-H-TV Leaks by the Seat; May 17, 2005

-IR 336146; 3-7902-396, BOP EM Light 396 Has Solid Fast Charge Light on;

May 18, 2005

-IR 336779; 2-7902-285, SSD Light Battery Requires Replacement; May 19, 2005

-IR 337075; Two NLOs Do Not Indicate Qualified in PQD; May 20, 2005

-IR 337139; Two NLSs Respirator Mask Med. Qualifications Were Not Met;

May 20, 2005

-IR 337503; Weaknesses for 2nd Quarter Fire Drill; May 23, 2005

-IR 338671; Dresden Fire Protection Report; May 26, 2005

1R06 Flooding

-IR 302902; 2/3 Cribhouse Sump Failure; February 18, 2005

-IR 331158; U2 west side ECCS Corner Room Watertight Door 1/2" Ajar; May 2, 2005

-IR 331423; 2/3 Cribhouse (UHS) Sump Pump Failure; May 3, 2005

-IR 331583; LS-3-4941-8 May Be Impacted by Temporary Staged Equipment;

May 3, 2005

-IR 333678; Shift Manager Fails to Generate PINV Assignment for Prompt; May 10,

2005

-IR 337100; NRC Questions Timeliness of 2/3 Cribhouse Sump Repairs; May 17, 2005

-IR 337105; Troubleshooting WO Documentation Incomplete; May 20, 2005

-IR 337135; NRC IDs FIN Backlog Issue; May 16, 2005

-IR 338392; SOC Enters Incorrect Information in IR; May 25, 2005

-WO 784571; 2/3 Cribhouse Sump Failure; February 23, 2005

-DOA 0040-02; Localized Flooding in Plant; Revision 15

-NRC Information Notice 2005-11; Internal Flooding / Spray-down of Safety Related

Equipment Due to Unsealed Equipment Hatch Floor Plugs and/or Blocked Floor Drains;

May 6, 2005

-WC-AA-106; Revision 2

1R07 Heat Sink

-IR 331949; Corrosion of Channel Head on RBCCW Heat Exchanger; May 4, 2005

-IR 332102; 2A TBCCW Heat Exchanger End Covers Are Degraded; May 5, 2005

-IR 332659; Maintenance Rule Database Incorrect; May 6, 2005

1R11 Operator Requalification

-IR 326406; Breaker Inspection Finds Trip Coil Incorrectly Mounted; April 19, 2005

-IR 330042; The Results of the FASA on LORT Exam Readiness - 4 Recom.;

April 29, 2005

-IR 334912; NOS Identifies Minor Exam Security Issue; May 13, 2005

4 Attachment

1R12 Maintenance Effectiveness

-IR 181118; Floor drains backed up in U2 HPCI contaminated floor space;

October 14, 2005

-IR 198770; HPCI Inoperable on Unit 2; February 1, 2004

-IR 198824; RBEDT pump down rate clos; February 1, 2004

-IR 201799; Failed Surveillance on U1 Battery Charger Swap; February 13, 2004

-IR 219445; CCSW Piping Degradation Exceeds Code Minimum; May 6, 2004

-IR 268340; Corporate PE FASA Procurement Engineering Assessment Plan;

February 24, 2005

-IR 270869; Received Alarm (923-4) D-1, 3B/D RBFD Sump PP Trip/Isol;

November 5, 2004

-IR 308487; Maintenance Rule Quarterly Evals Not Performed for Iso Cond.;

March 3, 2005

-IR 325977; Risk Tool Does Not Model RAT Breaker to Bus 34; April 18, 2005

-IR 327965; U2 CRD P-4 PMT Failed Due to Seat Leakage - Repeat Issue;

May 13, 2005

-IR 333736; Maint. Rule Database Support Documentation Needs Update;

May 10, 2005

-IR 334228; Maintenance Rule Functional Failure Criteria Needs to Be Eval;

May 11, 2005

-IR 336506; Maintenance Rule Evaluations Not Completed as Required; May 17, 2005

-ER-AA-310-1001; Maintenance Rule - Scoping; Revision 1

IR12 Maintenance Effectivenss (71111.12B)

-Maintenance Rule Periodic Assessment #5; October 1, 2002 - September 30, 2004;

dated December 2004

-Shutdown Cooling (a)(1) Action Plan; dated January 9, 2003

-Reactor Coolant Pressure Boundary (a)(1) Action Plan; dated December 18, 2003

-Secondary Containment (a)(1) Action Plan; dated May 22, 2003

-CCSW Supply to CR HVAC (a)(1) Action Plan; dated January 31, 2002

-Instrument Air (a)(1) Action Plan; dated January 20, 2005

-Augmented Primary Containment Vent (a)(1) Action Plan; dated July 16, 2004

-Feedwater Unit 2 (a)(1) Action Plan; dated January 22, 2004

-Service Water Standby Coolant Supply (a)(1) Action Plan; dated December 18, 2003

-List of Maintenance Rule Equipment Monitored for Unavailability; dated March, 2005

-List of Functional Failures for Assessment Period from October 1, 2002 -

September 30, 2004; dated October 2004

-Expert Panel Meeting Minutes; dated January 31, 2003

-Expert Panel Meeting Minutes; dated June 24, 2003

-Expert Panel Meeting Minutes; dated September 11, 2003

-Expert Panel Meeting Minutes; dated February 12, 2004

-Expert Panel Meeting Minutes; dated May 21, 2004

-Expert Panel Meeting Minutes; dated August 5, 2004

-HPCI System Health Overview Report; December 2004

-125 VDC System Health Overview Report; December 2004

-CCSW Quarterly Ship System Report; December 2004

-Primary Containment System Health Overview Report; December 2004

5 Attachment

-ER-AA-310; Implementation of the Maintenance Rule; Revision 3

-ER-AA-310-1003; Maintenance Rule - Performance Criteria Selection; Revision 2

-ER-AA-310-1004; Maintenance Rule - Performance Monitoring; Revision 2

-ER-AA-310-1005; Maintenance Rule - Dispositioning Between (a)(1) and (a)(2);

Revision 2

-ER-AA-310-1007; Maintenance Rule - Periodic (a)(3) Assessment; Revision 3

-MA-AA-716-210; Performance Centered Maintenance (PCM) Process; Revision 3

-MA-AS-716-210-1001; Performance Centered Maintenance Templates; dated

July 26, 2004

-SA-1126; Probability Risk Assessment Basis for Dresden Maintenance Rule

Availability, Performance Criteria and Revisions to Reliability Performance Criteria;

Revision 0

-Focused Area Self-assessment - Dresden Maintenance Rule Program (ATI

178673-01); dated October 1, 2003

1R13 Maintenance Risk Assessments and Emergent Work Control

-IR 333497; Inadequate Preparation Causes Schedule Delay; May 10, 2005

-IR 333822; HLAS Generated Within the Execution Week Without and IR; May 10, 2005

-IR 336144; Unit 3 125 Vdc Battery Discharge Test Stopped Prematurely; May 18, 2005

1R15 Operability Evaluations

-IR 324995; 2B Service Water Pump Breaker Failed to Trip from C/S; April 15, 2005

-IR 328459; Pipe Support for Line 2-3711-21/2" L is Damaged; April 25, 2005

-IR 328461; Feedwater Sparger End Bracket Pin Stops Are Loosening; April 25, 2005

-IR 329880; Ineffective CA Taken 3B Recirc Seal Hydro Failure in D3R18; April 28, 2005

-IR 333831; NOS Identifies OPS Not Following Guidance in LS-AA-120; May 10, 2005

-IR 336707; NRC & IEMA Req. For Additional Clarification for 50.50 Eval; May 19, 2005

-Operability Evaluation No.04-015

-EC No. 352592; Operability Evaluation for Isolation Condenser Steam Supply Vent

Lines 2-1309-3/4"- A, 2-1308-3/4"- A, and 2-1307-3/4"- A

-EC No. 353273; Modify U2 IsCo Steam Supply Vent Line Supports

-NES-MS-03.2; Revision 5; Evaluation of Discrepant Piping and Support Systems

-Specification K-4080; Revision 12; General Work Specification,

Maintenance/Modification Work

-USA Standard Code for Pressure Piping B31.1.0, Power Piping; 1967

-American Society of Mechanical Engineers Code,Section III, Division I; 1976

-Dresden UFSAR Sections 3.9.3.1.3.1.1 (Acceptance Criteria) and 5.4.6 (Isolation

Condenser)

1R16 Operator Work-Around

-OP-AA-102-103; Operator Work-Around Program; Revision 1

1R17 Permanent Plant Modification

-IR 303093; IEMA [Illinois Emergency Management Agency] Inspector Questions PMT

[Post Modification Testing] for Core Spray Modification; February 18, 2005

6 Attachment

-IR 325133; NRC Questions QATR [Quality Assurance Topical Report] Consistency

With CC [Configuration Change] Procedure; April 15, 2005

-IR 325097; EC [Engineering Change] 6602 Lacks Documented Justification for No PMT

[Post-Modification Testing]; April 15, 2005

-IR 330762; PMT for 2-1901-40 U2 FPC Filt Demin Byp AOV Mod Failed; May 24, 2005

-WO 97010448-06; Install Lower Sectional Replacement Piping as Required

-GENE-0000-0021-4342-04; Dresden Nuclear Power Station, Unit 3 Core Spray Line

Lower Sectional Replacement; Revision 0

-GENE-0000-0021-4342-04; Dresden Nuclear Power Station, Unit 3 Core Spray Line

Lower Sectional Replacement; Revision 1

-GENE-0000-0021-4342-04; Dresden Nuclear Power Station, Unit 3 Core Spray Line

Lower Sectional Replacement; Revision 3

-Field Deviation Disposition Request RMCN05077; Revision 0; dated October 8, 2004

-Terminal Manufacturing Company, Mechanical Measurements Inspection Report; Job

Number 11007- 1 & 2; dated April 1, 2005;

1R19 Post Maintenance Testing

-DOS 4400-01; Containment Cooling Service Water Vault Floor Drain; Revision 08

-DIS 3900-05; Diesel Generator Cooling Water Flow Indication Calibration; Revision 04

-DOS 6600-08; Diesel Generator Cooling Water Pump Quarterly and

Comprehensive/Progressive Test for Operational Readiness and In-Service Test (IST)

Program; Revision 32

-WO Package 00777955-01; D2/3 QTS TS D/G Cooling Water Pump Test for IST

Program Surveillance

-IR 324995; 2B Service Water Pump Breaker Failed to Trip from C/S; April 15, 2005

-IR 325097; EC 6602 Lacks Documented Justification for No PMT; May 5, 2005

-IR 329020; Perform and Document Extent of Condition Reviews 4KV BKR;

April 28, 2005

-IR 330004; D3M11 Forced Outage Due to 3B Rx. Recirc. Pp.seal Failure;

April 29, 2005

-IR 335891; RC EOC Discovered Another Recirc Seal Reverse Press Event;

May 17, 2005

-IR 329888; Initiate Root Cause for 3b Recirc Pump Seal Degradation; April 28, 2005

1R20 Outage Activities

-IR 324800; TR 29 Outage During D2R19 Requires Unit 3 Shutdown; April 14, 2005

-IR 329242; D3M11: Found Loose Hardware on 3E ERV Microswitch; May 24, 2005

-IR 329541; D3M11 Post-job Critique (OPS-Nightshift); April 28, 2005

-IR 330355; Equipment Status Tags Log Entry Report; May 11, 2005

-IR 331080; Limit Switch #1 for IRM#14 Drive Circuit Not Working; May 2, 2005

-IR 333410; Data Recorded in Incorrect ROWS on NF-AB-715 Attachment 2;

April 29, 2005

-IR 333418; Delays During U3 Startup Following D3M11; May 9, 2005

-IR 330503; NRC Identified Items During U3 Drywell Close Out, D3M11; April 30, 2005

-IR 330547; D3M11 Drywell Closeout Discrepancies; April 30, 2005

7 Attachment

1R22 Surveillance Testing

-IR 324377; Increase in U2 DW under Vessel Temp Points 24, 25, and 26;

April 15, 2005

-IR 324858; IR Not Written to Revise DIS 0263-01; April 14, 2005

-IR 329649; 2 of 8 MSIVs Timed Unsat During Surveillance; April 28, 2005

-IR 329880; Ineffective CA Taken 3B Recirc Seal Hydro Failure in D3R18; April 28, 2005

-IR 329904; Potential Error Occurred During D3R18 3B RR Motor Work; April 28, 2005

-IR 330844; 2-1349-B Iso. Condenser High Flow Ind/switch Out of Spec; May 2, 2005

-IR 332046; 3-1705-16B Fuel Ppol CH B Out of Tolerance; May 5, 2005

-IR 333412; No Feedback Ever Given on Negative Scorecards; May 9, 2005

-IR 335633; D2 Core Flow Found Outside Procedural Tolerance During CAL;

May 16, 2005

-IR 335776; Timing on Relay Was Found to Be out of Tolerance; May 17, 2005

-IR 335900; Unit 3 #14-51 Accum Pressure Switch Out-of-Tolerance; May 17, 2005

-IR 336123; D3 HCU Pressure Switch 30-19 Out of Tolerance; May 17, 2005

-IR 337554; Reset Operations Team Event Clock; May 23, 2005

-IR 338564; U1 125 VDC Battery Float Voltage Out of Tolerance; May 26, 2005

-IR 348496; U2 SBO Panel 2202-105 Alarm Tiles Not Functioning; June 29, 2005

-WO 00570002; D2 24M TS Div 1 LPCI Cont Cooling System Functional Test;

March 24, 2005

-DOS 6600-01; Diesel Generator Surveillance Tests; Revision 88

-DOS 6620-07; SBO 2 (3) Diesel Generator Surveillance Tests; Revision 18

-WO Package 00547472

-WO Package 00810022

-WO Package 00788502

-WO Package 00788507

-Unit NSO Daily Surveillance Log; Unit 2(3), Appendix A, Revision 98

1R23 Temporary Plant Modifications

-OP-AA-106-101-1006; Revision 1; Operational and Technical Decision Making Process

-CC-MW-112-1001; Training and Reference Material for Temporary Configuration

Changes

-Dresden FSAR 15.1.3; Increase in Steam Flow

-Dresden FSAR 15.1.3.2; Sequence of Events and System Operation

-Dresden FSAR 15.2; Decrease in Heat Removal by the Reactor Coolant System

-Dresden FSAR 15.2.1; Steam Pressure Regulator Malfunction

-Dresden FSAR 15.2.2.1; Load Rejection Without Bypass

-Dresden FSAR 15.2.3.1; Turbine Trip Without Bypass

-Drawing 12E-2910S; Schematic Diagram Electro-Hydraulic Control System Pressure

Control Unit; Revision B

-IR 330827; Temporary power cord usage; May 2, 2005

-IR 333103; LD has control of U2 output CB through SCADA; May 27, 2005

-IR 333454; DIS 0600-05 reactor narrow range level calibration; May 10, 2005

-IR 333797; Inappropriate revision to WO during D3M11; May 10, 2005

8 Attachment

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

-Offsite Dose Calculation Manual; Chapters 2, 4, and Appendix A (Revision 2),

Chapter 10 (Revision 4), Chapter 12 (Revision 5), and Appendix F (Revision 2)

-Dresden Nuclear Power Station Radioactive Effluent Release Reports for Calendar

Years 2002, 2003, and the 2004 Draft Report; dated April 30, 2003, April 30, 2004 and

Undated 2004 Draft Report, respectively

-CY-DR-170-2020/2030; Abnormal/Unmonitored Radiological Release; Revision 0

-Dresden Computation for Mn-54 Identified in Service Water Sample (DAR-2002-04);

dated April 7, 2003

-Radiation Protection Memorandum 99-001; Unit 1 Main Turbine Floor Effluents; dated

January 4, 1999

-DCP 3207-01; Gamma Isotopic Analysis; Revision 19

-DCP 2000-28; River Discharge; Revision 17

-CY-DR-120-600; Liquid Radwaste Scaling Factors; Revision 1

-CY-DR-170-210; Main Chimney Sampling; Revision 0

-Annual/Semi-Annual Surveillance Records of Unit 2/3 Radwaste High Radiation Area

Room Material Condition Inspections; 2004 through March 2005

-IR 00250661; Floor Drain and Waste Collector Tank Room Has Leaks;

September 7, 2004

-DIS-1700-14; Unit 2/3 Reactor Building Vent Stack SPING Calibration;

December 12, 2003

-DRS 5821-56; SPING Effluent Monitor Calibration; dated December 15, 2003

-DIS-1700-14; Unit 2/3 Main Chimney SPING Calibration; dated January 16, 2004

-DRS 5821-56; Main Chimney Radiation Monitor SPING Calibration; dated

January 22, 2004

-DIS 3900-01; Unit 2 Service Water Effluent Radiation Monitor Calibration; dated

June 4, 2003

-DIS 3900-01; Unit 3 Service Water Effluent Radiation Monitor Calibration; dated

April 16, 2004

-DRS 5830-01; Unit 3 Service Water Monitor Calibration; dated November 6, 2004

-DRS 5830-01; Unit 2/3 Liquid Radwaste Discharge Monitor Calibration; dated

March 26, 2004

-DIS 1300-04; Unit 2 Isolation Condenser Vent Radiation Monitor Calibration; dated

February 10, 2005

-DIS 1300-04; Unit 3 Isolation Condenser Vent Radiation Monitor Calibration; dated

February 11, 2005

-DIS 5700-03; Unit 2/3 Chimney Flow Monitor Calibration; dated July 21, 2003

-DIS 5700-02; Unit 2/3 Reactor Building Vent Stack Flow Calibration; dated

June 14, 2004

-Results of Analytics Radiochemistry Cross-Check Program for Dresden Nuclear

Power Station; Quarterly Results for 1st Quarter 2004 - 1st Quarter 2005

-Efficiency Calibrations and Lower Limit of Detection Determinations for Gamma

Spectroscopy Systems (6 detectors with multiple geometries); dated various periods

between January 2000 and April 2005

-Liquid Scintillation Counter (serial number 402097) Calibration and Lower Limit of

Detection Determination; dated January 25, 2005

-DTS 7500-13; Standby Gas Treatment System Visual Inspection (Train A and Train B);

dated May 26, 2004 and May 25, 2004, respectively

9 Attachment

-DTS 7500-07; Standby Gas Treatment System Charcoal Absorber Leak Test (Train A

and Train B); dated May 26, 2004 and May 25, 2004, respectively

-NCS Corporation Radioiodine Retention/Penetration/Efficiency Test Report; dated

June 9, 2004 (Train A - East and West Banks); dated May 28, 2004 (Train B - East

Bank)

-IR 00311151 and 00311622; Activity Detected in Unit 3 and Unit 2 Service Water

Effluent Samples; March 10 and 11, 2005

-IR 00315849; Increased Tritium in Well T-1; March 22, 2005

-IR 00317313; Service Water Sampling Requirements per ODCM; March 25, 2005

-IR 00326931; Unit 2/3 Chimney SPING Data Indication Flush Mode; April 20, 2005

-Audit NOSA-DRE-03-08; Radiological Environmental Monitoring Program, ODCM, Non-

Radiological Effluent Monitoring Audit Report; dated November 19, 2003

-Focus Area Self-Assessment Report; Radiological Effluent Control; dated

March 14, 2005

-Audit NOSA-DRE-04-04; Chemistry, Radwaste and Process Control Program; dated

May 25, 2004

-IR 00289411; Sludge Found During High Radiation Room Inspection;

January 10, 2005

-DTS 7500-11; DOP Testing of Unit 2/3 Standby Gas Treatment System HEPA Filters

(Train A and Train B); dated May 25 and May 26, 2004

-DOS 7500-02; Standby Gas Treatment System Surveillance and IST Test; dated

April 2, 2005

4OA1 Performance Indicator Verification

-Summary of Quarterly Dose Calculations from Liquid and Gaseous Effluents for 2004

through March 2005

4OA2 Identification and Resolution of Problems (71152)

-IR 239066; Negative Safety Trend Identified Within Security Department; April 26, 2005

-IR 324732; Operator Aid #159 Turnover Checklists; April 14, 2005

-IR 324902; NRC Identified Concerns; April 14, 2005

-IR 326630; U3 DW Hi Temp Alarm Setpoint Non-conservative vs. DEOP; April 20, 2005

-IR 327295; NOS Audit NOSA-DRE-05-01 (AR 287372) - Deficiency #1; May 11, 2005

-IR 327336; NRC Questions Actions Taken in SOC and MRC Closure of IRS;

April 21, 2005

-IR 329017; Generator H2 Pressure Dropped During Unit Shutdown; May 13, 2005

-IR 329045; Cracked Weld on U2 EDG Air Box Mount; May 24, 2005

-IR 329698; Large Quantity of Air Entrained in U3 Turbine Lube Oil; April 28, 2005

-IR 330004; D3M11 Forced Outage Due to 3b Rx. Recirc. PP.Seal Failure;

April 29, 2005

-IR 330030; Aggregate Reviews / Status of HCU PM 2005 Implementation;

April 29, 2005

-IR 330591; 3A MSDT Level Transmitter Calibration Drift; April 30, 2005

-IR 331420; Unplanned DOA 6500-12, Low Switchyard Voltage Entry; May 3, 2005

-IR 331430; Entered DOA 6500-11 for High Voltage on Bus 24-1; May 3, 2005

-IR 331875; M&TE Unable to Locate; May 4, 2005

-IR 331968; IEMA Representative Questions ECR for IR 326630; May 4, 2005

10 Attachment

-IR 332047; Unplanned Tech Spec Entry; May 5, 2005

-IR 332346; High Temperature (197 Deg F) on A Phase Bkr Supply Cable; May 5, 2005

-IR 332358; High Temperature (180 Deg F) on B Phase Bkr Supply Cable; May 5, 2005

-IR 332363; High Temperature (150 Deg F) on Hot Clg Twr MCC 2/3-7856-2B2;

May 5, 2005

-IR 333057; DGA-12 Hard Card Revised but Not the Procedure Section; May 9, 2005

-IR 333892; Inadequate Corrective Action Documentation in ATI 310957-02;

May 10, 2005

-IR 334295; Adverse Trend - Rising Water Level in Unit 3 Torus; May 11, 2005

-IR 334413; U3 125 Vdc Battery Cell 23 Sample Tube; May 12, 2005

-IR 335710; RB DP Low Condition for about 30 Seconds; May 16, 2005

-IR 335752; Experienced Difficulties Contacting BOC Gas; May 17, 2005

-IR 336040; NOS IDs Unidentified Cables/hoses; May 17, 2005

-IR 336506; Maintenance Rule Evaluations Not Completed as Required; May 18, 2005

-IR 337285; Fuel Pool Channel A Rad Hi Alarm; May 20, 2005

-IR 337403; Enter TS 3.3.6.2 Because of Failed Refuel FLR Rad Monitor; May 22, 2005

-IR 338273; NOS Ids Commitment Management Deficiency; May 25, 2005

-IR 338300; U2 SWRM Declared Inoperable; May 25, 2005

-IR 346783; Corrective Actions Not Effective ATI 270871; June 23, 2005

4OA3 Event Follow-up (71153)

-IR 325097; EC 6602 Lacks Documented Justification for no PMT; April 15, 2005

4OA5 Other Activities

TI 2515/163 Operation Readiness of Offsite Power

-IR 326685; Enter DOA 6500-12 and TS 3.8.1; May 11, 2005

-IR 333057; DGA-12 Hard Card Revised but Not the Procedure Section; May 9, 2005

-IR 333697; DOA 6500-12 Entered for Low Post Trip Red Bus Voltage; May 10, 2005

Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

-Certificate of Compliance (CoC) and the Technical Specifications; Revision 1

-Safety Evaluation Report; Revision 1

-Final Safety Analysis Report (FSAR); Revision 2

-Calculation Package On Hitran-140; Revision 2

-Prompt Investigation Report, No. 340904; Cask Transfer Facility (CTF) Lift Stopped

With Loaded Cask

-Engineering Evaluation, EC Eval 355831; Evaluation of Suspended Hi-Trac Storage

Unit in Cask Transfer Facility; Revision 0

-WO 817345-01; Troubleshooting and Repair of the CTF Instructions

-Maintenance Logs; dated April 7, 2005

-Condition Report; CTF Failure; dated June 6, 2005

-DAP 10-14A; Hi-Track Setdown at the CTF (ATI 340904-14) & Structural Qualification

of Hi-Track Recovery from DNPS CTF Drive Failure (AR340904);

72.48 Screening/Evaluation

-Special Procedure SP 05-05-006; Hi-Track Setdown at the CTF (ATI 340904-14);

Revision 0

11 Attachment

LIST OF ACRONYMS USED

ADAMS Agencywide Documents Access and Management System

ATI Action Tracking Item

ATWS Anticipated Transient Without Scram

CAP Corrective Action Program

CCSW Containment Cooling Service Water System

CoC Certificate of Compliance

CFR Code of Federal Regulations

CR Condition Report

CTF Cask Transfer Facility

DIS Dresden Instrument Surveillance

DOA Dresden Operating Abnormal Procedure

DOS Dresden Operating Surveillance

dP Differential Pressure

DRP Division of Reactor Projects

DRS Division of Reactor Safety

FIN Finding

FSAR Final Safety Analysis Report

GE General Electric

HEPA High Efficiency Particulate Air

HPCI High Pressure Core Injection System

IC Isolation Condenser

IGSCC Intergranular Stress Corrosion Cracking

IM Instrument Maintenance

IEMA Illinois Emergency Management Agency

IMC Inspection Manual Chapter

IR Issue Report

LER Licensee Event Report

MRC Management Review Committee

MWe megawatts electrical

NCV Non-Cited Violation

NRC Nuclear Regulatory Commission

ODCM Offsite Dose Calculation Manual

OSP Offsite Power

PARS Publicly Available Records

PI Performance Indicator

QHPI Quick Human Performance Investigation

RETS Radiological Effluent Technical Specifications

SBGT Standby Gas Treatment System

SDP Significance Determination Process

SOC Site Ownership Committee

SPING Station Particulate, Iodine and Noble Gas Monitor

SSC Structures, Systems, and Components

SW Service Water

TI Temporary Instruction

TIP Traversing Incore Probe

12 Attachment

TS Technical Specification

TSO Transmission System Operator

UFSAR Updated Final Safety Analysis Report

URI Unresolved Item

WO Work Order 13 Attachment