L-2003-148, May 2003 Monthly Operating Report for Turkey Point Units 3 & 4

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May 2003 Monthly Operating Report for Turkey Point Units 3 & 4
ML031700550
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 06/11/2003
From: Jones T
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-2003-148
Download: ML031700550 (3)


Text

JUN 1 1 2003 0 L-2003-148 FPL 10 CFR 50.36 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 Monthly Operating ReDort - May 2003 In accordance with the requirements of Turkey Point Units 3 and 4 Technical Specification 6.9.1.5, and the guidance of Generic Letter 97-02, attached are the May 2003 Operating Data Reports and Summaries of Operating Experience for Turkey Point Units 3 and 4.

Ve os, 11CW, 7v7 Jones e President Turkey Point Plant LDT Attachments NRC Regulatory Issue Summary 2001-05 waived the requirements that multiple copies of documents be submitted to the NRC.

an FPL Group company

DOCKET NO.: 50-250 UNIT: Turkey Point UnK 3 DATE: 6/3/2003 COMPLETED BY: Linda Tudor TELEPHONE: (305) 246-6408 Reporting Period May, 2003 OPERATING DATA REPORT Design Electrical Rating (MWe-Net) l__720 _

Maximum Dependable Capacity (MWe-Net) l 693 Month_ _ _ .~~~~~~~

No. of hours reactor was critical 4 707.0 4 No. of hours generator was on line (service hours) 698.7 4 Unit reserve shutdown hours 4 0 4 4.

Net Eiectrical Energy (MWH) 480597 4 4

.1 .1. &

UNIT SHUTDOWNS No. Date Type Duration Reason Method of Corrective Actlon/ Comments F=Forced (hours) (1) Shutting S=Scheduled _ _ Down (2) 20030015 52003 F 23.27 A 1 Manual reactor shutdown due to Shutdown Bank B not able to move on demand. Shutdown Bank B was repaired and the unit was returned to Mode 1 on

_ _ _ _ _ _ _ __ ___ __ _ __ _ __ __ _ _ _ _ __ __ __ __ _ __ __ _ _ _ _ __ _ _ _ _ _ __ 5 /2 1 /0 3.

(1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual Trip/Scram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4 - Continuation E - Operator Training&Lcense Examination 5 - Other (Explain)

F - Administrative G - Operational Error (Explain)

H - Other Summary Of Monthly Operating Experience Un 3 returned to power operation on 5/1/03 after repairs to CV-3-200B. Unit 3 remained at essentially 100% power until 5/20/03. On 5/20/03, Unit 3 performed a manual reactor shutdown to repair Rod Control Shutdown Bank B. Unit 3 returned to power operation on 5/21/03 and remained at essentially 100%

power for the remainder of the month of May 2003.

DOCKET NO.: 50-251 UNIT: Turkey Point Unit 4 DATE: 06103/03 COMPLETED BY: Linda Tudor TELEPHONE: (305) 246-6408 Reporting Period May, 2003 Design Electrical Rating (MWe-Net) _ _720 Maximum Dependable Capacity (MWe-Net) 693 Month Year-to-date Cumulative No. of hours reactor was critical 744 3623 194985.7 No. of hours generator was on line (service hours) 744 3623 190568.2 Unit reserve shutdown hours 0 0 577.2 Net Electrical Energy (MWH) 521823 2545090 125504180 UNIT SHUTDOWNS No. Date Type Duratlon Reason Method of Corrective Action/ Comments F=Forced (hours) (1) Shutting S=Scheduled Down (2)

NiA N/A NA N/A N/A N/A N/A (1) Reason (2) Method A - Equipment Failure (Explain) 1 - Manual B - Maintenance or Test 2 - Manual TripJScram C - Refueling 3 - Automatic Trip/Scram D - Regulatory Restriction 4- Continuation E - Operator Training'Lcense Examination 5 - Other (Explain)

F -Administrative G - Opertional Error (Explain)

H - Other Summary Of Monthly Operatina Experlence Unit 4 operated at essentially 100% power for the month of May 2003.