IR 05000275/2011005
ML120450843 | |
Person / Time | |
---|---|
Site: | Diablo Canyon |
Issue date: | 02/14/2012 |
From: | O'Keefe N NRC/RGN-IV/DRP/RPB-B |
To: | Conway J Pacific Gas & Electric Co |
References | |
IR-11-005 | |
Download: ML120450843 (59) | |
Text
UNITED STATES NUCLEAR REGULATORY COMMISSION REGION I V 1600 EAST LAMAR BLVD ARLINGTON, TEXAS 76011-4511 February 14, 2012 John Senior Vice President and Chief Nuclear Officer Pacific Gas and Electric Company 77 Beale Street, B32 San Francisco, CA 94105 Subject: DIABLO CANYON POWER PLANT - NRC INTEGRATED INSPECTION REPORT 05000275/2011005 AND 05000323/2011005
Dear Mr. Conway:
On December 31, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Diablo Canyon Power Plant. The enclosed integrated inspection report documents the inspection findings, which were discussed on January 4, 2012, with Mr. James Becker, Site Vice President and other members of your staff.
The inspections examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
Two NRC identified findings of very low safety significance were identified during the inspection.
Both of the findings were determined to be in violation of NRC requirements.
Further, one licensee-identified violation, which was determined to be of very low safety significance, is listed in this report. The NRC is treating these findings as a non-cited violations, consistent with Section 2.3.2 of the NRC Enforcement Policy.
If you contest the violations or the significance of the non-cited violations, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 1600 E. Lamar Blvd, Arlington, Texas, 76011-4511; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Diablo Canyon Power Plant.
-1- Enclosure
If you disagree with a cross-cutting aspect assigned in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV, and the NRC Resident Inspector at the Diablo Canyon Power Plant.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response, if any, will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC Agencywide Document Access and Management System document system (ADAMS).
ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Neil OKeefe, Branch Chief Project Branch B Division of Reactor Projects Docket Nos.: 050000275, 050000323 License Nos.: DPR-80, DPR-82
Enclosure:
Inspection Report 05000275/2011005 and 05000323/2011005 w/Attachment A: Supplemental Information w/Attachment B: Items are requested for the O
REGION IV==
Docket: 05000275, 05000323 License: DPR-80, DPR-82 Report: 05000275/2011005 05000323/2011005 Licensee: Pacific Gas and Electric Company Facility: Diablo Canyon Power Plant, Units 1 and 2 Location: 7 1/2 miles NW of Avila Beach Avila Beach, California Dates: September 26 through December 31, 2011 Inspectors: M. Peck, Senior Resident Inspector L. Micewski, Resident Inspector M. Young, Reactor Inspector A. Fairbanks, Reactor Inspector D. Reinert, Reactor Inspector N. Makris, Project Engineer L. Ricketson, P.E., Senior Health Physicist C. Alldredge, Health Physicist E. Ruesch, Reactor Inspector G. Guerra, Emergency Planning Inspector Approved By: N. OKeefe, Chief, Project Branch B Division of Reactor Projects-4- Enclosure
SUMMARY OF FINDINGS
IR 05000275/2011005, 05000323/2011005; 9/26/2011 - 12/31/2011; Diablo Canyon Power
Plant, Integrated Resident and Regional Report; Operability Evaluations.
The report covered a 3-month period of inspection by resident inspectors and region-based inspectors. Two Green non-cited violations of significance were identified. The significance of most findings is indicated by their color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, Significance Determination Process. The cross-cutting aspect is determined using Inspection Manual Chapter 0310, Components Within the Crosscutting Areas. Findings for which the significance determination process does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
NRC-Identified Findings and Self-Revealing Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified a non-cited violation of 10 CFR Part 50,
Appendix B, Criteria V, Instructions, Procedures, and Drawings, after Pacific Gas and Electric failed to evaluate the affect of new seismic information on the operability of plant structures, systems and components. On January 7, 2011, the licensee completed and submitted to the NRC a report detailing the results of a deterministic reevaluation of the local seismology. This report concluded that an earthquake on three local faults could produce greater vibratory ground motion than the safe shutdown earthquake as described in the Final Safety Evaluation Report Update. Quality Procedure OM7.ID12, Operability Determinations, required plant operators to assess the impact of nonconforming conditions for the affect on plant structures, systems and components without delay. On June 22, 2011, the licensee entered the condition into the corrective action program as Notification 50410266 and completed an operability determination on June 24, 2011.
The inspectors determined that the licensees failure to promptly evaluate the new seismic information against the plant design and licensing bases was a performance deficiency. The finding was more than minor because the performance deficiency was associated with the Mitigating Systems Cornerstone initial design control attribute and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The senior reactor analyst evaluated the significance of the finding using a Phase 3 analysis because the inspectors were unable to confirm that the operability of plant systems was not impacted. The senior reactor analyst concluded that the finding was of very low risk significance (Green) because no significant change in overall core damage frequency resulted from the new seismic hazards. This finding had a cross-cutting aspect in the area of human performance associated with the decision-making component because the licensee used non-conservative assumptions in deciding not to evaluate the new seismic information against the current plant design and licensing bases [H.1.(b)] (Section 1R15.2).
Cornerstone: Barrier Integrity
- Green.
The inspectors identified a non-cited violation of 10 CFR Part 50,
Appendix B, Criteria V, Instructions, Procedures, and Drawings, after operations personnel failed to adequately evaluate the operability and extent of condition of a nonconforming control room habitability train. Beginning on August 30, 2011, the inspectors identified several nonconforming conditions associated with the habitability system, including disconnected ductwork, two 12-inch diameter openings in the control room envelope boundary, and less than adequate control room envelope pressurization and tracer gas surveillance tests. On November 7, 2011, the licensee re-performed the tracer gas test and observed significant unfiltered in-leakage into the control room envelope. Plant operators declared the habitability system inoperable. The licensee restored system operability after implementing compensatory measures. The licensee entered the finding into the corrective action program as Notification 50425114 and planned to restore the system to the current licensing basis condition.
The inspectors concluded that the failure of plant operators to adequately evaluate the operability and extent of a nonconforming condition was a performance deficiency. This finding was more than minor because the licensees operability evaluation created a reasonable doubt that the system was capable of performing the specified safety function, similar to Example 3.k in Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues. The inspectors concluded that the finding was of very low safety significance because only the radiological barrier function of the control room was affected. This finding had a cross-cutting aspect in the area of problem identification and resolution, associated with the corrective action program component, because the licensee did not thoroughly evaluate the degraded control room ventilation train for operability and extent of condition P.1(c) (Section 1R15.1).
Licensee-Identified Violations
A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking number (condition report numbers) are listed in Section 4OA7.
REPORT DETAILS
Summary of Plant Status
At the beginning of the inspection period, Pacific Gas and Electric Company was operating both units at full power. On October 10, 2011, plant operators reduced Unit 1 to 50 percent power following debris fouling in the condenser cooling system. On October 11, 2011, the licensee cleared the debris and returned the unit to full power. Both units remained at full power for the remainder of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
1R01 Adverse Weather Protection
Readiness for Seasonal Extreme Weather Conditions
a. Inspection Scope
The inspectors performed a review of the adverse weather procedures for winter storm season preparations. The inspectors verified that weather-related equipment deficiencies identified during the previous year were corrected prior to the onset of seasonal extremes, and evaluated the implementation of the adverse weather preparation procedures and compensatory measures for the affected conditions before the onset of, and during, the adverse weather conditions.
During the inspection, the inspectors focused on plant-specific design features and the procedures used by plant personnel to mitigate or respond to adverse weather conditions. Additionally, the inspectors reviewed the Final Safety Analysis Report Update (FSARU) and performance requirements for the systems selected for inspection, and verified that operator actions were appropriate as specified by plant-specific procedures. Specific documents reviewed during this inspection are listed in the attachment. The inspectors also reviewed corrective action program items to verify that plant personnel were identifying adverse weather issues at an appropriate threshold and entering them into the corrective action program in accordance with station corrective action procedures. The inspectors reviews focused specifically on the following plant systems:
- Units 1 and 2, Hillside auxiliary saltwater system piping
- Units 1 and 2, Breakwater at the intake structure These activities constitute completion of one readiness for seasonal adverse weather sample as defined in Inspection Procedure 71111.01-05.
b. Findings
No findings were identified.
1R04 Equipment Alignments
Partial Walkdown
a. Inspection Scope
The inspectors performed partial system walkdowns of the following risk-significant systems:
- October 12, 2011, Unit 1, Safety Injection System Train A
- November 15, 2011, Unit 2, Component Cooling Water System Train A
- December 13, 2011, Unit 1, Emergency Diesel Generator 1-3 The inspectors selected these systems based on their risk significance relative to the reactor safety cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could affect the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, FSARU technical specification requirements, administrative technical specifications, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also inspected accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of three partial system walkdown samples as defined in Inspection Procedure 71111.04-05.
b. Findings
No findings were identified.
1R05 Fire Protection
Quarterly Fire Inspection Tours
a. Inspection Scope
The inspectors conducted fire protection walkdowns that were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
- October 3, 2011, Unit 1, 12kV Switchgear cable spreading room
- October 31, 2011, Unit 2, Fire Area 3-CC, 115 Containment penetration room
- November 10, 2011, Unit 1, Fire Area 3-BB, 85 Containment penetration room
- December 2, 2011, Unit 2, Fire Areas TB-10, TB-12 and TB-13, Essential 4 kV switchgear and cable spreading rooms The inspectors reviewed areas to assess if licensee personnel had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant; effectively maintained fire detection and suppression capability; maintained passive fire protection features in good material condition; and had implemented adequate compensatory measures for out of service, degraded or inoperable fire protection equipment, systems, or features, in accordance with the licensees fire plan.
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to affect equipment that could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees corrective action program.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of four quarterly fire-protection inspection samples as defined in Inspection Procedure 71111.05-05.
b. Findings
No findings were identified.
1R07 Heat Sink Performance
a. Inspection Scope
The inspectors reviewed licensee programs, verified performance against industry standards, and reviewed critical operating parameters and maintenance records for Component Cooling Water Heat Exchanger 2-2. The inspectors verified that performance tests were satisfactorily conducted for heat exchangers/heat sinks and reviewed for problems or errors; the licensee utilized the periodic maintenance method outlined in EPRI Report NP 7552, Heat Exchanger Performance Monitoring Guidelines; the licensee properly utilized biofouling controls; the licensees heat exchanger inspections adequately assessed the state of cleanliness of their tubes; and the heat exchanger was correctly categorized under 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one heat sink inspection sample as defined in Inspection Procedure 71111.07-05.
b. Findings
No findings were identified.
1R11 Licensed Operator Requalification Program
a. Inspection Scope
On November 8, 2011, the inspectors observed a crew of licensed operators in the plants simulator to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
- Licensed operator performance
- Crews clarity and formality of communications
- Crews ability to take timely actions in the conservative direction
- Crews prioritization, interpretation, and verification of annunciator alarms
- Crews correct use and implementation of abnormal and emergency procedures
- Control board manipulations
- Oversight and direction from supervisors
- Crews ability to identify and implement appropriate technical specification actions and emergency plan actions and notifications The inspectors compared the crews performance in these areas to preestablished operator action expectations and successful critical task completion requirements.
Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one quarterly licensed-operator requalification program sample as defined in Inspection Procedure 71111.11.
b. Findings
No findings were identified.
1R12 Maintenance Effectiveness
a. Inspection Scope
The inspectors evaluated degraded performance issues involving the following risk significant systems:
- Ineffective carbon dioxide system maintenance, Notification 50086255
- Ineffective emergency diesel generator maintenance, Notification 50419169
The inspectors reviewed events such as where ineffective equipment maintenance has resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following:
- Implementing appropriate work practices
- Identifying and addressing common cause failures
- Scoping of systems in accordance with 10 CFR 50.65(b)
- Characterizing system reliability issues for performance monitoring
- Charging unavailability for performance monitoring
- Trending key parameters for condition monitoring
- Ensuring proper classification in accordance with 10 CFR 50.65(a)(1) or (a)(2)
- Verifying appropriate performance criteria for structures, systems, and components classified as having an adequate demonstration of performance through preventive maintenance, as described in 10 CFR 50.65(a)(2), or as requiring the establishment of appropriate and adequate goals and corrective actions for systems classified as not having adequate performance, as described in 10 CFR 50.65(a)(1)
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the corrective action program with the appropriate significance characterization. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of two quarterly maintenance effectiveness samples as defined in Inspection Procedure 71111.12-05.
b. Findings
No findings were identified.
1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
The inspectors reviewed licensee personnel's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
- Risk Assessment 11-16, Revision 0, Assessment of Single Component Maintenance Outage Window Configuration with an Elevated Base Risk due to Fire Barriers Surveillance Requirement 0.3
- Risk Assessment 11-17, Revision 1, Fire Water Storage Tank 0-1 and Fire Protection Features Unavailable for Maintenance
- Maintenance risk assessment for Work Week 1150, Unit 2, December 19, 2011
- Maintenance risk assessment for Work Week 1152, Unit 2, December 26, 2011 The inspectors selected these activities based on potential risk significance relative to the reactor safety cornerstones. As applicable for each activity, the inspectors verified that licensee personnel performed risk assessments as required by 10 CFR 50.65(a)(4)and that the assessments were accurate and complete. When licensee personnel performed emergent work, the inspectors verified that the licensee personnel promptly assessed and managed plant risk. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed the technical specification requirements and inspected portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
These activities constitute completion of four maintenance risk assessment and emergent work control inspection samples as defined in Inspection Procedure 71111.13-05.
b. Findings
No findings were identified.
1R15 Operability Evaluations
a. Inspection Scope
The inspectors reviewed the following issues:
- Incorrect American Institute of Steel Construction Code edition used for the Unit 1 polar crane, Systems Applications Process Notification (SAPN) 50424629, September 6, 2011
- Incorrect damping value used for seismic analysis of the Unit 1 polar crane, SAPN 50424627, September 6, 2011
- Auxiliary salt water pump 2-1 high stator temperature, SAPN 50433056, October 12, 2011
- Component cooling water potential over-pressurization, SAPN 50428811, October 27, 2011
- Control room habitability system design vulnerability, SAPN 50438661, November 3, 2011
- Containment fan coolers 2-2 and 2-4 bearings degraded, SAPN 50405029, November 8, 2011
- Containment fan cooler wiring exceeded equipment qualification temperatures, SAPN 50443002, November 30, 2011
- Units 1 and 2 reactor protection system did not meet seismic qualification requirements, SAPN 50445580, December 7, 2011
- Auxiliary feedwater pump 2-2 recirculation line flow indication, SAPN 20432954, December 16, 2011
- Dual indication on flow control valves 679 and 681 CS, SAPN 50447696, December 19, 2011
- Emergency diesel generator 2-3 failed to meet generator frequency surveillance requirement, SAPN 50449027, December 22, 2011 The inspectors selected these potential operability issues based on the risk significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that technical specification operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the technical specifications and FSARU to the licensee personnels evaluations to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of eleven operability evaluations inspection samples as defined in Inspection Procedure 71111.15-04.
b. Findings
- (1) Less than Adequate Evaluations of a Degraded/Nonconforming Control Room Habitability Train
Introduction.
The inspectors identified a green non-cited violation of 10 CFR Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings, after plant operations personnel failed to adequately evaluate the operability and extent of condition of a nonconforming control room habitability train.
Description.
Technical Specification 3.7.10, Control Room Ventilation System, required the licensee to maintain two independent and redundant control room ventilation trains operable. In conjunction with an operable control room envelope, each train was required to limit operator dose to less than 5 Rem committed effective dose
equivalent (CEDE) for the duration of an accident. The basis for technical specification 3.7.10 stated that each ventilation train was operable when the associated ductwork was operable and air circulation could be maintained. The basis also stated that each ventilation train was required to pressurize the control room envelope to about 1/8-inch water gauge to prevent contaminated outside air from in-leaking into the envelope. The accident analysis demonstrated that the licensee met the General Design Criteria 19, Control Room, requirement to limit operator dose to less than 5 Rem CEDE. The accident analysis assumed that no unfiltered in-leakage would enter the control room envelope.
On August 30, 2011, the inspectors observed that the licensee had removed the ductwork connecting control room supply fan S-36 to the control room ventilation discharge header. The inspectors observed ventilation flow bypassing the control room discharge header and blowing into the mechanical equipment room from the open ductwork. The inspectors also identified two 12-inch diameter openings through the wall.
On August 31, 2011, the Pacific Gas and Electric completed an evaluation of the disconnected ductwork (Notification 50424714). The licensee concluded that the control room ventilation system was not adversely affected because the bypassing airflow into the mechanical equipment room was still within the control room envelope. The inspectors concluded that Pacific Gas and Electrics evaluation was inadequate because they failed to evaluate the affect of the nonconforming condition on all design basis functions. The inspectors concluded that the bypassing flow from disconnected ductwork could affect the ventilation system flow balance and the capability to pressurize all areas of the control room envelope. The inspectors also concluded that the two 12-inch diameter wall openings provide a path for unfiltered outside air into the control room envelope because they failed to evaluate all design basis functions that were affected.
On September 12, 2011, the inspectors identified that the last control room envelope in-leakage tracer gas test results were greater than the limiting value used in the bounding accident analysis. The last test, Control Room Habitability Tracer Gas Leak Testing of the Diablo Canyon Power Plant, conducted in January 2005, measured up to 59 standard cubic feet per minute of unfiltered in-leakage into the control room envelope.
The licensee declared the control room envelope inoperable and implemented compensatory measures to protect control room operators.
Technical specification 5.5.19, Control Room Envelope Habitability Program, required the licensee to use the control room envelope testing methods specified in Sections C1 and C2 of Regulatory Guide 1.197, Demonstrating Control Room Envelope Integrity at Nuclear Power Reactors. Regulatory Guide 1.197, Section C2, required the licensee to perform testing in the configuration that would result in the greatest dose consequence to the operators. The inspectors verified that last control room envelope tracer gas in-leakage test did not include the disconnected ductwork as a test configuration.
On September 30, 2011, Pacific Gas and Electric performed a control room envelope pressurization test to demonstrate system operability with the removed ductwork. The licensee performed the test after the inspectors challenged the licensees previous operability conclusions. The licensee concluded that control room ventilation train was still capable of pressurizing the control room envelope with the ductwork removed. The
inspectors concluded that the licensees evaluation was inadequate because the licensee had performed the test with equipment from both ventilation trains in operation.
Technical specification basis 3.7.10 stated that each ventilation train was required to pressurize the control room envelope.
On November 7, 2011, Pacific Gas and Electric re-performed the control room envelope tracer gas in-leakage test as a result of the inspectors concerns. Plant technicians measured about 800 standard cubic feet per minute of unfiltered in-leakage into the control room envelope. Plant operators declared the habitability system inoperable as a result of the test results. The licensee was able to reduce the in-leakage to about 45 standard cubic feet per minute by operating a booster fan in the redundant train. The licensee concluded that the operator dose limits could be met by ensuring the redundant train equipment was in operation and by reducing the amount of primary containment bypass leakage. The licensee implemented these compensatory measures and restored system operability. The licensees corrective actions included restoring the habitability system to the design condition.
The inspectors determined that this finding did not impact the smoke mitigation function, and the system did not have a toxic gas mitigation function.
Analysis.
The inspectors concluded that the failure of plant operators to adequately evaluate the specified safety function and extent of condition of a nonconforming control room habitability train was a performance deficiency. This finding was more than minor because licensees operability evaluation created a reasonable doubt that the system was capable of performing the specified safety function similar to Example 3.k in Inspection Manual Chapter 0612, Appendix E, Examples of Minor Issues. The finding was associated with the Barrier Integrity Cornerstone. Using Inspection Manual Chapter 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, the inspectors concluded that the finding was of very low safety significance (Green) because only the radiological barrier function of the control room was affected.
This finding had a cross-cutting aspect in the area of problem identification and resolution associated with the corrective action program component because the licensee did not thoroughly evaluate the degraded control room ventilation train for
Enforcement.
Title 10 CFR Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings, required that activities affecting quality be accomplished in accordance with instructions or procedures. Quality Procedure OM7.ID12, Operability Determinations, Revision 22, Section 5, required plant operations personnel to evaluate the impact and extent of condition of potentially nonconforming plant equipment against each of the specified safety functions for that equipment. Contrary to the above, on August 31, 2011, plant operations personnel failed to perform an operability evaluation, an activity affecting quality, in accordance with instructions or procedures. Specifically, the licensee did not adequately evaluate the impact and extent of condition of nonconforming ductwork of the Unit 1 control room habitability train against each of the specified safety functions for that equipment. In particular, the licensee did not evaluate the potential impact of the disconnected ductwork on the ventilation system flow balance and the capability to pressurize all areas of the control room envelope. Because this finding is of very low safety significance and was entered into the corrective action program as Notification 50425114, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy:
NCV, 05000275; 323/2011005-01, Less than Adequate Evaluations of a Degraded/Nonconforming Control Room Habitability Train.
.2 (Closed) Unresolved Item 05000275; 323/2011002-03: Failure to perform an operability
evaluation following receipt of new seismic information.
Introduction.
The inspectors identified a green non-cited violation of 10 CFR Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings, after Pacific Gas and Electric failed to promptly evaluate the operability of plant structures, systems and components (SSCs) after completing a reevaluation of the local seismology.
Description.
In November 2008, Pacific Gas and Electric notified the NRC of a new seismic feature located about a kilometer offshore from the plant. This newly discovered feature became known as the Shoreline fault. In January 2011, Pacific Gas and Electric submitted Report on the Analysis of the Shoreline Fault Zone, Central Coast California to the NRC, (Agency Wide Documents Access and Management System, (ADAMS) ML110140400). This report concluded that the Shoreline, the Los Osos, and San Luis Bay faults were capable of producing about 70 percent greater vibratory ground motion than described in the double design earthquake FSARU safety analysis.
The double design earthquake was used to establish the initial seismic qualification requirements for plant structures, systems and components (SSCs) for the plant safe shutdown earthquake as required by General Design Criterion 2, Design Bases for Protection against Natural Phenomena; and 10 CFR 100, Appendix A, Seismic and Geologic Siting Criteria for Nuclear Power Plants.
In December 2010, the licensee concluded that plant licensing bases only required that new seismic information be evaluated against the Long Term Seismic Program (LTSP)deterministic margin analysis (Notification 50086062) and not the plant design bases.
The inspectors opened Unresolved Item 05000275; 323/2011002-03 to determine if the licensee was required to evaluate the new seismic information against the plant seismic design basis in addition to the LTSP.
In August 2011, the NRC completed a review of the Diablo Canyon license and design bases and issued Task Interface Agreement - Concurrence on Diablo Canyon Seismic Qualification Current Licensing and Design Basis, (ADAMS ML112130665). The NRC concluded that new seismic information developed by the licensee was required to be evaluated against each of the three design basis earthquakes used to establish the seismic qualification of plant SSCs, including the assumptions and acceptance criteria described in the supporting FSARU safety analyses. The NRC also concluded that comparison of the new information only to the Hosgri Event or LTSP was insufficient to ensure all plant SSCs were capable of performing their specified safety functions.
Based on this staff position, the inspectors concluded that the licensees evaluation of the impact of new potential seismic ground motion information was not evaluated against the design and licensing basis requirements.
Title 10 CFR 50.71, Maintenance of Records and Making Reports, required the licensee to update the FSARU to include the new seismic information. The new information resulted in existing FSARU Sections 2.5.2.9, Maximum Earthquake, and 3.7.1.1, Design Response Spectra, to be nonconforming with the requirements of General Design Criterion 2 and Appendix A to Part 100. Diablo Canyon Quality Procedure OM7.ID12, Operability Determinations, Section 5.1, Immediate
Determination of Operability, required plant operators to assess the impact of nonconforming conditions for the effect on plant SSCs without delay.
Pacific Gas and Electric completed an operability determination in June 2011 (Notification 50410266). The licensee concluded that plant SSCs would function because the new predicted ground motions were bounded by the ground motions assumed in the Hosgri safety analysis. In October 2011, the licensee revised the operability determination to add information justifying application of the Hosgri calculation methodology as an alternative methodology as described in the NRC Inspection Manual, Part 9900: Technical Guidance, Operability Determinations &
Functionality Assessments for Resolution of Degraded or Nonconforming Conditions Adverse to Quality or Safety (ADAMS ML073440103). The staff concluded that the revised operability determination provided an initial basis for concluding a reasonable assurance that plant equipment would withstand the potential effect of the new vibratory ground motion. In order to complete a comprehensive evaluation, the licensee needed NRC approval of the methodology to be used to complete this evaluation.
In October 2011, Pacific Gas and Electric submitted License Amendment Request 11-05, Evaluation of Process for New Seismic Information and Clarifying the Diablo Canyon Power Plant Safe Shutdown Earthquake, ADAMS ML113112A166. The licensee requested that the NRC approve the Hosgri earthquake as the Diablo Canyon safe shutdown earthquake. The licensee also requested NRC approval for a methodology to be used for evaluating the impact of new seismic information on the plant.
Analysis.
The inspectors determined that the failure to evaluate the nonconforming condition against the plant design and licensing bases was a performance deficiency.
This performance deficiency was more than minor because it was associated with the Mitigating Systems Cornerstone initial design control attribute and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding represented a design and qualification deficiency. The senior reactor analyst evaluated the significance of the finding using a Phase 3 analysis because the inspectors were unable to confirm operability was not impacted. Using updated seismic annual exceedance frequencies from Geosciences Report GEO.DCPP.10.05, Development of the Probabilistic Hazard Curves Incorporating the Shoreline Fault, January 3, 2011, and the seismic equipment fragilities included in the Diablo Canyon Individual Plant Examination for External Events, the senior reactor analyst concluded that the overall core damage frequency for seismic events was 2.1 x 10-5 per year. The increases in plant risk from the Shoreline, Los Osos, and San Luis Bay Fault higher predicted ground motions were offset by the decrease in risk from the licensees re-evaluation of the Hosgri Fault. As a result no significant change in conditional core damage probability occurred as a result of the new seismic information. The senior reactor analyst concluded that the finding was of very low risk significance (Green) based on no significant change in overall core damage frequency. This finding had a cross-cutting aspect in the area of human performance, associated with the decision-making component, because the licensees cause assessment concluded that they had used a non-conservative assumption to only evaluate the new seismic information against the LTSP and not the plant design basis [H.1.(b)].
Enforcement.
Title 10 CFR Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings, required that activities affecting quality be accomplished in accordance with instructions or procedures. Quality Procedure OM7.ID12, Section 5.1, Immediate Determination of Operability, required plant operators to assess the impact of nonconforming conditions for the effect on plant SSCs without delay. Contrary to the above, between January 7 and June 22, 2011, the licensee failed to evaluate the operability, and activity affecting quality, in accordance with instructions or procedures.
Specifically, plant operators failed to assess the impact of a nonconforming condition for the effect on plant SSCs without delay. On January 7, 2011, Pacific Gas and Electric completed a reevaluation of the local seismology. This new information rendered FSARU Sections 2.5.2.9 and 3.7.1.1 nonconforming with General Design Criteria 2 and Appendix A to Part 100, but operators failed to evaluate operability until June 22, 2011.
Because this finding is of very low safety significance and was entered into the corrective action program as Notification 50410266, this violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the NRC Enforcement Policy:
NCV, 05000275; 323/2011005-02, Failure to Perform an Operability Determination for New Seismic Information.
1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant
Modifications (71111.17)
.1 Evaluations of Changes, Tests, or Experiments
a. Inspection Scope
The inspectors reviewed nine evaluations to determine whether the changes to the facility or procedures, as described in the FSARU, had been reviewed and documented in accordance with 10 CFR 50.59 requirements. The inspectors verified that, when changes, tests, or experiments were made, evaluations were performed in accordance with 10 CFR 50.59 and licensee personnel had appropriately concluded that the change, test or experiment could be accomplished without obtaining a license amendment. The inspectors also verified that safety issues related to the changes, tests, or experiments were resolved. The team compared the safety evaluations and supporting documents to the guidance and methods provided in Nuclear Energy Institute (NEI) 96-07, "Guidelines for 10 CFR 50.59 Implementation," as endorsed by NRC Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments," to determine the adequacy of the safety evaluations.
The inspectors reviewed 19 samples of changes, tests, and experiments that licensee personnel determined did not require evaluations and verified that the licensee personnels conclusions were correct and consistent with 10 CFR 50.59.
The inspectors also verified that calculations, analyses, design change documentation, procedures, the FSARU, the Technical Specifications, and plant drawings used to support the changes were accurate after the changes had been made. Documents reviewed are listed in the attachment.
These activities constitute completion of nine samples of evaluations and 19 samples of changes, tests, and experiments that were screened out by licensee personnel as defined in Inspection Procedure 71111.17-04.
b. Findings
No findings were identified.
.2 Permanent Plant Modifications
a. Inspection Scope
The inspectors verified that calculations, analyses, design change documentation, procedures, the FSARU, the technical specifications, and plant drawings used to support the modifications were accurate after the modifications had been made. The inspectors verified that modifications were consistent with the plants licensing and design bases.
The inspectors confirmed that revised calculations and analyses demonstrated that the modifications did not adversely impact plant safety. Additionally, the inspectors interviewed design and system engineers to assess the adequacy of the modifications.
The inspectors reviewed nine permanent plant modifications, and specific documents reviewed during this inspection are listed in the attachment.
.2.1 Unit 1 Centrifugal Charging Pump Discharge Trimming Orifice
The inspectors reviewed a modification (DCP 1000000175) that installed a trimming orifice at the discharge of each of the centrifugal charging pumps. The rotating element in each Unit 1 centrifugal charging pump was replaced during 1R15. The hydraulic performance attributes of the new rotating elements were somewhat different from the required performance characteristics of the centrifugal charging pumps. A trimming orifice was added at the discharge of each pump to adjust its hydraulic performance to match the emergency core cooling system analysis assumptions. The effects of this modification were evaluated for vital bus loading from the centrifugal charging pump motors, emergency diesel generator fuel oil inventory requirements, air condition cooling demand in the auxiliary building, and environmental conditions in the centrifugal charging pump room.
.2.2 Removal of the Cask Pit Rack and Installation of the Transfer Cask Restraint Cup
The inspectors reviewed a modification (DCP 1000000126) that removed the existing spent fuel temporary high density cask pit rack and installed a spent fuel pool transfer cask restraint cup within the cask letdown area of the spent fuel pool. One phase of the transfer evolution was to lower the used fuel transfer cask into the spent fuel pool for the loading of used fuel from the spent fuel pool. While the used fuel transfer cask is being stored in the cask letdown area of the spent fuel pool, the cask is required to be laterally restrained to prevent damage or overturning in a seismic event. The restraint cup was mounted to the existing cask letdown area platform assembly. Installation of the restraint cup was required to allow transfer of the used fuel to the independent spent fuel storage installation for storage. The restraint cup enabled the plant to continue to refuel by freeing up space in the spent fuel pool.
.2.3 Abandonment of the Diesel Fuel Oil Storage Tank Cathodic Protection
The inspectors reviewed a modification (DCP 1000000205) that abandoned the diesel fuel oil storage tank cathodic protection system. The diesel fuel oil storage tank cathodic
protection system was degraded and was no longer providing protection to the tanks.
The anode currents had dropped to zero as measured during monthly maintenance tests. The wires associated with the anodes were disconnected from the terminal strips.
The storage tanks were made with double wall steel and an external fiberglass reinforced plastic clad shell on the secondary tank. The fiberglass shell had an air gap between the outer metal tank and the shell which limited the effectiveness of a cathodic protection system. Sufficient protection was provided for the diesel fuel oil storage tanks by means of the double walled tank and the fiberglass reinforced plastic cladding.
Diablo Canyon conducts a test every 36 months that draws a vacuum between the first and second wall of the tanks to check for leaks. Additionally, Diablo Canyon checks diesel fuel oil storage tank inventory and checks for water in the tanks every 31 days.
.2.4 Replacement of Existing Reinforced Concrete Reactor Coolant Drain Tank 3-Segment
Hatch Cover with 3-Segment Grating and Metal Plate Hatch Cover The inspectors reviewed a modification on Unit 1 (DCP 1000000397) that replaced the reinforced concrete reactor coolant drain tank 3-segment hatch cover with a 3-segment grating and metal plate hatch cover. For a postulated pipe break inside the biological shield wall, the licensees analysis credited upflow through a hatch in the concrete floor at the 91-foot elevation. Contrary to this assumption, the licensee identified that the hatch was covered with a multilayered steel radiation shield/barrier, which effectively prevented the upflow of water through the hatch. Therefore, the fluid flow into the recirculation sump could have been reduced, potentially impacting the net positive suction head for the residual heat removal pumps and/or causing vortexing in the sump.
The replacement of the concrete hatch cover with a metal plate hatch cover provided a fluid-flow path between the reactor cavity and the area above.
.2.5 MS-1-5166 and MS-1-5167 Check Valve Replacement
The inspectors reviewed a modification on Unit 1 (DCP 1000000282) that replaced check valves MS-1-5166 and MS-1-5167, which were used to isolate flow between the two steam supply lines to the turbine driven auxiliary feedwater pump, in the event of a steam line break. Fluctuations in the pressure downstream of the replaced check valves had led to excessive wear of the valve discs and bodies. The check valves were replaced with normally-open nozzle check valves to reduce the inspection and maintenance requirements of the valves.
.2.6 Relocation of Emergency Diesel Generator Turbo Air Compressor and Both Starting Air
Compressor Hydraulic Unloader Sensing Lines The inspectors reviewed a modification on Unit 1 (DCP 1000000385) that rerouted the inlet of the emergency diesel generator turbo/starting air compressor hydraulic unloader sensing tubing from the seismic Category 1 air receiver tanks to the non-seismic Category 2 section of the compressor discharge. The tubing senses turbo/starting air receiver tank pressure for the operation of the compressors unloader valves. The tubing up to the unloader valves was Category 1, but the unloader valve itself, which was connected to the compressor, was not. Moving the inlet upstream of the code break check valve located it in the Category 2 portion of the compressor discharge line. Doing so made the tubing, unloader valves and associated compressors all Category 2, eliminating the need to qualify the compressor and sensing tubing as seismic Category 1.
.2.7 Replacement of Water-Seated Pressurizer Safety Valves with Steam-Seated Valves
The inspectors reviewed a modification on Unit 2 (DCP 1000000165) that replaced the water-seated pressurizer safety valves with steam-seated pressurizer safety valves.
This conversion allowed for the loop seal to be continuously drained, and no longer relied upon during operation to ensure the safety valve is seated properly. There was a drain added to the loop seal which connects directly to a nozzle on the pressurizer.
Previously, the temperature of the water was maintained in an established band to ensure the operability of the safety valve. Since the water-filled loop seal was no longer needed, this eliminated the need to maintain the water in the loop at a prescribed temperature. Therefore, this modification reduced the amount of thermal cycling of the pressurizer safety valves and decreased operator time inside containment.
.2.8 Replacement of Safety Injection Check Valves
The inspectors reviewed a modification on Unit 2 (DCP 1000000154) that replaced two inch safety injection Rockwell Edwards lift check valves with two inch Flowserve type 1878 piston check valves. The check valves were located in the safety injection pumps discharge header and prevent the over-pressurization of the safety injection system.
Previously, the leakage from the lift check valves produced a higher than normal pressure in the safety injection discharge header. The replacement decreased the leakage seen at the check valves and prevented the discharge header from over-pressurization. The pressure sealed bonnets on the new check valves had a pressure rating in excess of the safety injection system.
.2.9 Replacement of a Chemical Volume and Control System Check Valve Spring
The inspectors reviewed a modification on Unit 1 (DCP 1000000247) that replaced the existing spring on check valve CVCS-1-8109 with a stiffer spring. This check valve was designed to relieve the thermal pressure between two isolation valves during a postulated main steam line break or loss of coolant accident. The reason for the change was that this check valve had an unsatisfactory back flow leak test during the
1R15 outage. The new stiffer spring allowed the check valve to pass the back flow leak
test by providing a tighter closure on the seat. The stiffer spring had a slightly larger cracking pressure, but there was sufficient margin in the maximum allowable working pressure for containment isolation valves. The spring was tested and verified acceptable during the replacement part evaluation done by the licensee.
These activities constitute completion of nine samples of permanent plant modifications as defined in Inspection Procedure 71111.17-04.
b. Findings
No findings were identified.
1R19 Postmaintenance Testing
a. Inspection Scope
The inspectors reviewed the following postmaintenance activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
- Corrective maintenance of spare pressurizer heater group 1-3 Breaker, Unit 1, November 15, 2011
- Preventive maintenance of diesel fuel oil transfer pump 0-2, Units 1 and 2, December 12, 2011
- Preventive maintenance of containment spray pump 2-1, Unit 2, December 13, 2011
- Preventive maintenance of centrifugal charging pump 1-2, Unit 1, December 15, 2011
- Preventive maintenance of battery charger 2-2, Unit 2, December 15, 2011
- Preventive maintenance of auxiliary building supply fan S-33, Unit 2, December 16, 2011
- Corrective maintenance of emergency diesel generator 2-3 motor operated potentiometer, Unit 2, December 23, 2011 The inspectors selected these activities based upon the SSCs ability to affect risk. The inspectors evaluated these activities for the following (as applicable):
- The effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed
- Acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate The inspectors evaluated the activities against the technical specifications, the FSARU, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with postmaintenance tests to determine whether the licensee was identifying problems and entering them in the corrective action program and that the problems were being corrected commensurate with their importance to safety. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of seven postmaintenance testing inspection samples as defined in Inspection Procedure 71111.19-05.
b. Findings
No findings were identified.
1R22 Surveillance Testing
a. Inspection Scope
The inspectors reviewed the FSARU, procedure requirements, and technical specifications to ensure that the surveillance activities listed below demonstrated that the systems, structures, and/or components tested were capable of performing their intended safety functions. The inspectors either witnessed or reviewed test data to verify that the significant surveillance test attributes were adequate to address the following:
- Preconditioning
- Evaluation of testing impact on the plant
- Acceptance criteria
- Test equipment
- Procedures
- Jumper/lifted lead controls
- Test data
- Testing frequency and method demonstrated technical specification operability
- Test equipment removal
- Restoration of plant systems
- Fulfillment of ASME Code requirements
- Updating of performance indicator data
- Engineering evaluations, root causes, and bases for returning tested systems, structures, and components not meeting the test acceptance criteria were correct
- Reference setting data
- Annunciators and alarms setpoints The inspectors also verified that licensee personnel identified and implemented any needed corrective actions associated with the surveillance testing.
- Routine surveillance test of the Unit 1turbine-driven auxiliary feedwater pump 1-1, October 4, 2011
- Routine surveillance test of the Unit 2 control room ventilation system flow and differential pressure, October 22, 2011
- Routine surveillance test of the Unit 1 control room ventilation system tracer gas in-leakage, November 2, 2011
- Routine surveillance test of Unit 1 pressurizer pressure channel November 15, 2011
- Inservice test of Unit 1, safety injection pump, November 25, 2011
- Inservice test of Unit 1, safety injection pump 1-1 Suction Valve 8923A, November 28, 2011
- Units 1 and 2 Routine reactor coolant system leak rate surveillance tests, December 10, 2011,
- Routine Unit 1 emergency diesel generator 1-2 engine analysis test, December 13, 2011
- Routine Unit 2, emergency diesel 2-3 surveillance test,December 21, 2011 Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of nine total samples as defined in Inspection Procedure 71111.22-05.
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP4 Emergency Action Level and Emergency Plan Changes
a. Inspection Scope
The inspector performed an in-Office review of the Diablo Canyon Power Plant Emergency Plan Section 7, Emergency Facilities and Equipment, Revision 4, Change 15, submitted by letter dated July 26, 2011. This plan change implemented the dose assessment method described in Diablo Canyon Design Change Package (DDP)1000000351, Upgrade the Meteorological Instrumentation and Dose Assessment System (MIDAS). This change implemented a multiple regional meteorology tower input wind field dispersion model dose assessment system vice a terrain specific dispersion model. Included in this change was the addition of a seventh regional meteorological tower and a thirteenth pressurized ion chamber monitoring instrument.
This revision was compared to its previous revision, to the criteria of NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, and to the standards in 10 CFR 50.47(b) to determine if the revision adequately implemented the requirements of 10 CFR 50.54(q). This review was not documented in a safety evaluation report and did not constitute approval of licensee-generated changes; therefore, this revision is subject to future inspection. Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of one sample as defined in Inspection Procedure 71114.04-05.
b. Findings
No findings were identified.
1EP6 Drill Evaluation
.1 Training Observations
a. Inspection Scope
The inspectors observed a simulator training evolution for licensed operators on November 15, 2011, which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the postevolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the corrective action program. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the attachment.
These activities constitute completion of one sample as defined in Inspection Procedure 71114.06-05.
b. Findings
No findings were identified.
RADIATION SAFETY
Cornerstone: Occupational and Public Radiation Safety
2RS0 4 Occupational Dose Assessment
a. Inspection Scope
This area was inspected to:
- (1) determine the accuracy and operability of personal monitoring equipment;
- (2) determine the accuracy and effectiveness of the licensees methods for determining total effective dose equivalent; and
- (3) ensure occupational dose is appropriately monitored. The inspectors used the requirements in
10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance. During the inspection, the inspectors interviewed licensee personnel, performed walkdowns of various portions of the plant, and reviewed the following items:
- External dosimetry accreditation, storage, issue, use, and processing of active and passive dosimeters
- The technical competency and adequacy of the licensees internal dosimetry program
- Adequacy of the dosimetry program for special dosimetry situations such as declared pregnant workers, multiple dosimetry placement, and neutron dose assessment
- Audits, self-assessments, and corrective action documents related to dose assessment since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.04-05.
b. Findings
No findings were identified.
2RS0 5 Radiation Monitoring Instrumentation
a. Inspection Scope
This area was inspected to verify the licensee is assuring the accuracy and operability of radiation monitoring instruments that are used to:
- (1) monitor areas, materials, and workers to ensure a radiologically safe work environment; and
- (2) detect and quantify radioactive process streams and effluent releases. The inspectors used the requirements in 10 CFR Part 20, the technical specifications, and the licensees procedures required by technical specifications as criteria for determining compliance.
During the inspection, the inspectors interviewed licensee personnel, performed walkdowns of various portions of the plant, and reviewed the following items:
- Selected plant configurations and alignments of process, post accident, and effluent monitors with descriptions in the FSARU and the offsite dose calculation manual
- Selected instrumentation, including effluent monitoring instrument, portable survey instruments, area radiation monitors, continuous air monitors, personnel contamination monitors, portal monitors, and small article monitors to examine their configurations and source checks
- Calibration and testing of process and effluent monitors, laboratory instrumentation, whole body counters, post accident monitoring instrumentation, portal monitors, personnel contamination monitors, small article monitors, portable survey instruments, area radiation monitors, electronic dosimetry, air samplers, continuous air monitors
- Audits, self-assessments, and corrective action documents related to radiation monitoring instrumentation since the last inspection Specific documents reviewed during this inspection are listed in the attachment.
These activities constitute completion of the one required sample as defined in Inspection Procedure 71124.05-05.
b. Findings
No findings were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator Verification
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
.1 Data Submission Issue
a. Inspection Scope
The inspectors performed a review of the data submitted by the licensee for the third quarter 2011 performance indicators for any obvious inconsistencies prior to its public release in accordance with Inspection Manual Chapter 0608, Performance Indicator Program.
This review was performed as part of the inspectors normal plant status activities and, as such, did not constitute a separate inspection sample.
b. Findings
No findings were identified.
.2 Reactor Coolant System Specific Activity (BI01)
a. Inspection Scope
The inspectors sampled licensee submittals for the reactor coolant system specific activity performance indicator for Units 1 and 2 for the period from the fourth quarter 2010 through the third quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees reactor coolant system chemistry samples, technical specification requirements, issue reports, event
reports, and NRC integrated inspection reports for the period of October 2010 through September 2011 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of two reactor coolant system specific activity samples as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
.3 Reactor Coolant System Leakage (BI02)
a. Inspection Scope
The inspectors sampled licensee submittals for the reactor coolant system leakage performance indicator for Units 1 and 2 for the period from the fourth quarter 2010 through the third quarter 2011. To determine the accuracy of the performance indicator data reported during those periods, the inspectors used definitions and guidance contained in NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6. The inspectors reviewed the licensees operator logs, reactor coolant system leakage tracking data, issue reports, event reports, and NRC integrated inspection reports for the period of October 2010 through September 2011 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the performance indicator data collected or transmitted for this indicator and none were identified.
Specific documents reviewed are described in the attachment to this report.
These activities constitute completion of two reactor coolant system leakage samples as defined in Inspection Procedure 71151-05.
b. Findings
No findings were identified.
4OA2 Identification and Resolution of Problems
.1 Routine Review of Identification and Resolution of Problems
a. Inspection Scope
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. The inspectors reviewed attributes that included: the complete and accurate identification of the problem; the timely correction, commensurate with the
safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and previous occurrences reviews; and the classification, prioritization, focus, and timeliness of corrective actions. Minor issues entered into the licensees corrective action program because of the inspectors observations are included in the attached list of documents reviewed.
These routine reviews for the identification and resolution of problems did not constitute any additional inspection samples. Instead, by procedure, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
b. Findings
No findings were identified.
.2 Daily Corrective Action Program Reviews
a. Inspection Scope
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. The inspectors accomplished this through review of the stations daily corrective action documents.
The inspectors performed these daily reviews as part of their daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
b. Findings
No findings were identified.
.3 Semi-Annual Trend Review
a. Inspection Scope
The inspectors performed a review of the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors focused their review on repetitive equipment issues, but also considered the results of daily corrective action item screening discussed in Section 4OA2.2 above, licensee trending efforts, and licensee human performance results. The inspectors nominally considered the 6-month period of July 2011 through December 2011 although some examples expanded beyond those dates where the scope of the trend warranted.
The inspectors also included issues documented outside the normal corrective action program in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self-assessment reports, and Maintenance Rule assessments.
The inspectors compared and contrasted their results with the results contained in the licensees corrective action program trending reports.
Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
These activities constitute completion of a single semi-annual trend inspection sample as defined in Inspection Procedure 71152-05.
b. Observations and Findings
Adverse Trend in Missed Technical Specification Required Surveillances The inspectors identified an adverse trend related to the failure of the licensee to implement technical specification required surveillance tests. This trend included:
- SAPN 50222280, Failure to perform a power range nuclear instrumentation calibration during a reactor startup, March 24, 2009
- SAPN 50284723, Containment temperature surveillance test not performed, November 16, 2009
- SAPN 50323184, Inadequate emergency diesel generator power factor tests, April 9, 2010
- SAPN 50310054, Failure to perform containment concrete inspections, April 14, 2010
- SAPN 50328653, Inadequate remote shutdown equipment surveillance testing, July 13, 2010
- SAPN 50337146, Failure to adequately perform reactor coolant system leak rate surveillance due to calculation error, August 24, 2010
- SAPN 50044703, Inadequate engineering safety feature pump vibration testing, September 8, 2010
- SAPN 50368931, Failure to meet emergency diesel generator load rejection testing requirements due to a non-conservative Technical Specification, January 5, 2011
- SAPN 50371073, Failure to perform reactor protection system testing within the required frequency, January 20, 2011
- SAPN 50388482, Failure to perform reactor protection system turbine stop valve test, April 11, 2011
- SAPN 50416026, Less than adequate power operated pressurizer relief valve test, July 21, 2011 The licensee completed a common cause evaluation of the adverse trend on October 5, 2010. The licensee updated this evaluation in April 2011. The independent assessment organization also evaluated the adverse trend as part of the Technical
Specification Audit in October 2011. The licensee concluded that the trend was the result of various factors, including problems with:
- Screening and use of operating experience,
- Maintaining configuration control,
- Latent errors associated with the integration of licensing requirements into test procedures,
- Human performance errors, including poor communication between work groups,
- Inadequate oversight and awareness of the Surveillance Test Program, and
- Ineffective test coordinators.
The inspectors concluded that the licensees common cause evaluation was effective in identifying the underlying causes contributing to the adverse trend. The licensees corrective actions included the long term Licensing Basis Verification Project to address latent problems with the plant design and licensing basis documentation as well as reinforcing expectations and establishing accountability for an effective Technical Specification Surveillance Program. The inspectors will continue to monitor the licensees actions to address the adverse trend.
Adverse Trend in Problem Evaluation The inspectors concluded that licensee corrective actions were effective to reduce the adverse trend in problem evaluation. The inspectors first identified the adverse trend in September 2008 (described in Section 4OA2 of Inspection Report 05000275; 05000323/2008005). The NRC subsequently identified a substantive cross-cutting issue associated with this theme in the 2009 annual assessment. This theme continued through the 2011 NRC Mid-Cycle Assessment.
During the summer of 2011, inspectors completed a focused review of Pacific Gas and Electrics actions to address the substantive cross-cutting issue. The inspectors concluded that the licensees recovery plan addressed the actions needed to improve performance. However, many of the licensees initiatives had not been in place for an adequate time to allow the inspectors to assess the overall effectiveness of the recovery plan. The inspectors also identified a gap between the licensees corrective actions and the supporting root cause analysis. The corrective action plan did not include specific actions to address deficiencies with the extended leadership team demonstrating or reinforcing behaviors among the staff.
The inspectors identified three new examples of less than adequate problem evaluation during the current semiannual trend:
- An inadequate extent of condition review of Fire Protection Program implementation issues during the third quarter 2011 (NCV 05000323/2011004-04, Failure to Perform Surveillances on Fire Barriers).
- Several inadequate evaluations and extent of condition reviews associated with the control room habitability system during the third and fourth quarters 2011(NCV 05000323/2011005-01, Less than Adequate Evaluations of a Degraded/Nonconforming Control Room Habitability Train).
- An inadequate diesel generator operability evaluation on December 22, 2011 (Notification 50449149). This issue was determined to be minor because testing demonstrated that the diesel generator was fully operable despite the unexpected indication from test equipment.
The inspectors also identified three examples of thorough problem evaluation of complex issues. The inspectors observed the extended leadership team was highly engaged and effectively reinforcing behaviors among the staff during in each evaluation:
- Prompt operability determination of the control room habitability system, November 3, 2011 (SAPN 50438661)
- Containment fan cooler wiring exceeded equipment qualification temperatures, November 30, 2011 (SAPN 50443002)
- Operability determination following identification of unqualified reactor coolant pump under frequency and under voltage reactor protection system inputs on December 7, 2011 (SAPN 50445580)
In December 2011, inspectors completed a second focused review of Pacific Gas and Electrics corrective actions. The results of this inspection are documented in Section 4OA2.4.
.4 Focused Review of the Substantive Cross-cutting Issue in Problem Identification and
Resolution In its March 4, 2009, Annual Assessment Letter (ML090630794) for Diablo Canyon, the NRC identified a cross-cutting theme in the thoroughness of problem evaluation aspect of the problem identification and resolution cross-cutting area P.1(c). In its March 3, 2010, Annual Assessment Letter (ML100620897), the NRC opened a substantive cross-cutting issue based on this theme. This theme has continued, and the substantive cross-cutting issue has remained open, through the most recent assessment period, as discussed in the 2011 Mid-cycle Assessment Letter dated September 1, 2011 (ML112440169).
In July 2011, inspectors performed a focused inspection of the licensees root cause evaluation and of the resulting corrective actions developed to address this substantive cross-cutting issue. During the inspection, the inspectors noted that the licensee had performed a comprehensive and thorough root cause analysis and had developed a plan to address the deficiencies which led to the substantive cross-cutting issue. However, the inspectors concluded that many of the process improvements initiated through this plan had not been in place for a sufficient length of time to provide assurance that the intended goals would be met. Further, the inspectors identified a weakness in the corrective actions taken by the licensee to address one of the causes identified in its root cause analysis: a failure of the extended leadership team to effectively demonstrate and reinforce positive behaviors among the licensee staff.
The results of this inspection were further discussed in Inspection Report 05000275 and 05000323/2011004 (ML113220067).
a. Inspection Scope
On December 19 and 20, 2011, the NRC performed a follow-up focused inspection of the licensees corrective actions implemented to correct the portion of its root cause statement regarding the role of management and supervision in demonstrating and reinforcing behaviors which led to thorough and complete problem evaluations. The inspectors noted that the majority of the recent NRC findings which led to the continuing cross-cutting theme were the result of weak or inadequate determinations of operability for safety-related equipment. Therefore, this inspection focused on the quality of these evaluations and on managements demonstration and reinforcement of behaviors which tended to support quality operability determinations.
The inspectors reviewed the revisions made to the licensees root cause evaluation and the additional corrective actions to prevent recurrence (CAPRs) that were implemented following the July 2011 inspection. The inspectors evaluated the licensees progress in implementing these CAPRs and reviewed the licensees metrics and measures used to track their effectiveness. The inspectors reviewed changes to plant program procedures that were implemented as part of these CAPRs or as a part of other corrective actions initiated through the root cause evaluation. The inspectors reviewed communications from management to site personnel regarding quality of evaluations. Finally, the inspectors interviewed 13 operations and engineering personnel who were routinely involved in the development and documentation of operability determinations and a number of management and supervisory personnel who were responsible for oversight of operability determinations.
These activities constitute completion of one in-depth problem identification and resolution sample as defined in Inspection Procedure 71152-01.05.
b. Observations and Findings
The inspectors determined that the licensee had made significant changes to its programs, processes, and procedures which, if continued, will likely result in improvement in the quality of evaluation products. Further, the inspectors noted that there was evidence that the licensee continued to periodically review the status of these changes and to adjust them as necessary to ensure continued improvement.
During interviews, the inspectors noted that there appeared to be recognition at all levels of the organization of the changes the licensee was implementing to improve the quality of its evaluations. Particularly, both engineers and operators expressed positive feedback on the level of management support for the development of high quality evaluation products and on the resources provided (including training) to ensure evaluations of operability were completed in a high quality manner, according to communicated management expectations.
The inspectors noted an overall positive performance trend in the licensees implementation or revision of programs, processes, and procedures designed to ensure complete, thorough, and accurate evaluations. However, the inspectors noted three areas of continued concern:
- Licensee staff do not fully understand the requirements of the new or revised procedures. Though the inspectors identified only a minor instance in which these procedures might fail to adequately provide for quality evaluations
- (see SAPN 50448164), several of the personnel interviewed did not have a thorough understanding of the requirements of the operability evaluation process.
- The licensees new qualification program for performing prompt operability assessments was a one-time qualification, with no requalification required. The licensee entered this into the corrective action program as SAPN 50448197.
Prior to the inspection, the licensees training committee had made a recommendation to implement a requalification process.
- The inspectors determined that the Evaluation Work Product Quality metric (used to trend the quality of prompt operability assessments and other engineering evaluation products) was based on data that were too variable to provide meaningful trend information. The Engineering Work Product Review Teams that grade the evaluations and other work products were of varied composition, the mix of work product types reviewed by the teams varied significantly from period to period, and the grading system employed by the teams was subjective. The inspectors noted that these subjective, non-normalized criteria may not provide a consistent measure for monitoring performance trends in evaluation quality. The licensee entered this observation into the corrective action program as SAPN 50448495.
No findings were identified.
.5 Selected Issue Follow-up Inspection
a. Inspection Scope
During a review of items entered in the licensees corrective action program, the inspectors recognized a corrective action item documenting:
- SAPN 5042678, Self-declaration of fatigue per fitness for duty rule, September 7, 2011
- SAPN 50443002, Containment fan cooler wiring exceeded equipment qualification temperatures, November 30, 2011 These activities constitute completion of two in-depth problem identification and resolution samples as defined in Inspection Procedure 71152-05.
b. Findings
No findings were identified.
.6 In-depth Review of Operator Workarounds
a. Inspection Scope
The inspectors conducted a cumulative review of operator workarounds on November 21, 2011, for Units 1 and 2, and assessed the effectiveness of the operator workaround program to verify that the licensee was:
- (1) identifying operator workaround problems at an appropriate threshold;
- (2) entering them into the corrective action program; and
- (3) identifying and implementing appropriate corrective actions. The review included walkdowns of the control room panels, interviews with licensed operators and reviews of the control room discrepancies list, the lit annunciators list, the operator burden list, and the operator workaround list.
These activities constitute completion of one review of operator workarounds sample as defined in IP 71152-05.
b. Findings
No findings were identified.
4OA3 Event Follow-up
.1 (Closed) Licensee Event Report 05000275/2011-002-01: Diablo Canyon Power Plant
Units 1 and 2 Auxiliary Building Ventilation System Single Failure Vulnerability and Loss of Unit 2 Auxiliary Building Ventilation System On January 11, 2011, Pacific Gas and Electric identified a condition prohibited by Technical Specification 3.7.12, Auxiliary Building Ventilation System, after both ventilation trains became inoperable following a single failure. This design vulnerability existed as part of the original plant design for both units. The licensee had an opportunity to identify and correct the problem when the ventilation control system was replaced in November 2010. The failure of the licensee to ensure the auxiliary building ventilation system met the single failure design basis was previously dispositioned as NCV 05000275/2011002-04 and 05000323/2011002-04, Inadequate Design Control for the Auxiliary Building Ventilation System Control Panel Modification.
This supplemental Licensee Event Report provided additional information related to the cause of the condition and corrective actions taken. The licensee determined that the design change process was deficient because the failure modes and effects analyses did not include a check for legacy issues. Corrective actions included system modifications to ensure the design basis criteria were met and provide for manual operation if automatic actuation is unavailable.
No additional findings of significance were identified during this review.
.2 (Closed) Licensee Event Report 05000275/2011-002-02: Diablo Canyon Power Plant
Units 1 and 2 Auxiliary Building Ventilation System Single Failure Vulnerability and Loss of Unit 2 Auxiliary Building Ventilation System On January 11, 2011, Pacific Gas and Electric identified a condition prohibited by Technical Specification 3.7.12, Auxiliary Building Ventilation System, after both ventilation trains became inoperable following a single failure. This design vulnerability
existed as part of the original plant design for both units. The licensee had an opportunity to identify and correct the problem when the ventilation control system was replaced in November 2010. The failure of the licensee to ensure the auxiliary building ventilation system met the single failure design basis was dispositioned as NCV 05000275/2011002-04 and 05000323/2011002-04, Inadequate Design Control for the Auxiliary Building Ventilation System Control Panel Modification.
This supplemental Licensee Event Report clarified that only Unit 2 experienced an event that could have prevented fulfillment of its safety function.
No additional findings of significance were identified during this review.
.3 (Closed) Licensee Event Report 05000275/2011-004-01: Emergency Diesel Generators
Actuated Upon 230 kV Isolation Due to Maintenance Activities on Relay Panel. On May 17, 2011, Unit 1 lost the preferred source of offsite power source due to inappropriate modification activities on energized equipment. All three emergency diesel generators automatically started as expected following the loss of offsite power. The loss of offsite power occurred as a technician was cutting an opening on the startup bus using a reciprocating saw. Mechanical vibration from the saw caused an electrical protective relay to actuate and separate the startup bus from preferred offsite power. The licensees failure to adequately evaluate the impact of cutting activity in the vicinity of energized plant equipment was dispositioned as FIN 05000275/2011003-02, Unplanned Loss of Preferred Offsite Power Due to Less than Adequate Work Planning.
This supplemental Licensee Event Report provided additional information related to the licensees root cause evaluation and corrective actions. The licensee concluded that plant personnel failed to perform an adequate risk assessment during the planning stage of the modification. While evaluating the work to be performed on the panel, personnel overlooked the possible effects of mechanical agitation to the protective relays. The licensees corrective actions included revising station procedures to require a risk assessment and provide additional protective steps for work being performed in panels that can potentially impact both units.
No additional findings of significance were identified during this review.
.4 (Closed) Licensee Event Report 05000275/2011-005-01: Emergency Diesel Generator
Actuations Upon Loss of 230 kV Startup Due to Electrical Maintenance Testing Activities On May 26, and May 27, 2011, 230 kV preferred offsite power supply was lost to Unit 1.
All three emergency diesel generators automatically started as expected. The loss of offsite resulted from personnel error during the installation of post modification test equipment on the Unit 2 startup bus The failure of plant technicians to follow post-modification testing work instructions was previously dispositioned as FIN 05000275/2011003-03; Unplanned Loss of Preferred Offsite Power Due to the Failure to Follow Work Instructions.
This supplemental Licensee Event Report provided additional information related to the licensees root cause evaluation and corrective actions. The licensee concluded that the events were the result of human error and inconsistent reinforcement of human performance. An inadequate post modification procedure contributed to the event. The licensees corrective actions included strengthening expectations for correct component
identification during maintenance activities, uses of robust barriers on adjacent components, and developing maintenance supervisor coaching.
No additional findings of significance were identified during this review.
4OA6 Meetings
Exit Meeting Summary
On September 29, 2011, the inspectors presented the preliminary inspection results on evaluations of changes, tests, or experiments and permanent plant modifications to Mr. K. Peters, Vice President of Engineering and Projects, and other members of the licensees staff. The licensee acknowledged the results as presented. While some proprietary information was reviewed during this inspection, no proprietary information was included in this report.
On December 8, 2011, the inspectors presented the results of the radiation safety inspections to Mr. J. Welsh, Station Director, and other members of the licensee staff.
The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary.
No proprietary information was identified.
On December 20, 2011, the inspectors presented the problem identification and resolution focused baseline inspection results to Mr. J. Becker, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented.
The licensee confirmed that no proprietary information was reviewed during the inspection or retained by the inspectors.
On December 23, 2011, the inspector discussed the results of the in-office review of emergency preparedness plan changes with Ms. P. Grefen, Director, Operations, and other members of the licensees staff. The licensee acknowledged the issues presented.
The inspector asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
On January 4, 2012, the inspectors presented the inspection results to Mr. J. Becker, Site Vice President, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. All proprietary information provided during the inspection was clearly identified.
4OA7 Licensee-Identified Violations
The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which meet the criteria of Section 2.3.2 of the NRC Enforcement Policy for being dispositioned as non-cited violations.
Failure to Evaluate the Cumulative Effect of Operator Work Arounds Title 10 CFR, Part 50, Appendix B, Criteria V, Instructions, Procedures, and Drawings, required the licensee to perform activities affecting quality in accordance with procedures appropriate to the circumstances. Quality Procedure OP1.DC40, Operations Equipment Deficiency Tracking, Revision 5, required the shift manager or designee to identify and evaluate operator work arounds for the cumulative effect on the capability of plant operators to implement compensatory actions during plant transients.
On November 21, 2011, the licensee identified that neither the shift manager nor designee had identified or evaluated the cumulative effect of operator work arounds.
The finding was more than minor because the performance deficiency was associated with the Mitigating Systems Cornerstone human performance attribute and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events. The inspectors concluded that the finding was of very low safety significance, Green, because the performance deficiency was not a design or qualification deficiency, did not result in the loss of operability or functionality of Technical Specification equipment, or potentially risk significant due to a seismic, flooding, or severe weather initiating event. Pacific Gas and Electric entered the issue into the corrective action program as Notification 50441633.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
- J. Becker, Site Vice President
- J. Welsch, Station Director
- K. Peters, Senior Director, Engineering Services
- J. Nimick, Director, Operations Services
- S. David, Director, Site Services
- L. Walter, Director Learning Services
- L. Hopson, Acting Director Site Services
- W. Guldemond, Special Assistant to the Site Vice President
- T. Baldwin, Manager, Regulatory Services
- N. Jahangir, Manager Engineering
- P. Gerfen, Manager, Operations
- T. Irving, Manager, Radiation Protection
- L. Hopson, Manager, Site Services
- J. Summy, Director, Engineering Services
- M. Zawalick, Senior Advising Coordinator, Emergency Preparedness
- M. Barnby, Engineer, Radiation Protection
- T. Irving, Manager, Radiation Protection
- J. Knemeyer, Effluents Engineer, Chemistry
- K. ONeil, System Engineer, Engineering Services
- L. Sewell, Engineering Leader, Radiation Protection
- D. Shippey, ALARA Team Leader, Radiation Protection
- S. Stoffel, Dosimetry Laboratory and Office Supervisor, Radiation Protection
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened and Closed
- 05000275; NCV Less than Adequate Evaluations of a
- 05000323/-2011005-01 Degraded/Nonconforming Control Room Habitability Train (Section 1R15.1)
- 05000275; NCV Failure to Perform an Operability Determination for New
- 05000323/-2011005-02 Seismic Information (Section 1R15.2)
Closed
- 05000275; URI Failure to Perform an Operability Evaluation Following 23/2011002-03 Receipt of New Seismic Information (Section 1R15.2)
- 05000275/2011-002-01 LER Diablo Canyon Power Plant Units 1 and 2 Auxiliary Building Ventilation System Single Failure Vulnerability and Loss of Unit 2 Auxiliary Building Ventilation System (Section 4OA3.1)
- 05000275/2011-002-02 LER Diablo Canyon Power Plant Units 1 and 2 Auxiliary Building Ventilation System Single Failure Vulnerability and Loss of Unit 2 Auxiliary Building Ventilation System (Section 4OA3)
Attachment
- 05000275/2011-004-01 LER Emergency Diesel Generators Actuated Upon 230 kV Isolation Due to Maintenance Activities on Relay Panel (Section 4OA3.2)
- 05000275/2011-005-01 LER Emergency Diesel Generator Actuations Upon Loss of 230 kV Startup Due to Electrical Maintenance Testing Activities (Section 4OA3.3)