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Category:INSPECTION REPORT
MONTHYEARIR 05000213/20240012024-08-27027 August 2024 Connecticut Yankee Atomic Power Company - Independent Spent Fuel Storage Installation NRC Inspection Report Nos. 07200039/2024001 and 05000213/2024001 IR 07200039/20224012022-10-0505 October 2022 Connecticut Yankee Atomic Power Company - NRC Independent Spent Fuel Storage Security Inspection Report No. 07200039/2022401 IR 05000213/20210012021-10-26026 October 2021 Connecticut Yankee Atomic Power Company - NRC Independent Spent Fuel Storage Installation Inspection Report Nos. 07200039/2021001 and 05000213/2021001 IR 07200039/20204012020-11-20020 November 2020 Connecticut Yankee Atomic Power Company - Independent Spent Fuel Storage Installation Security Inspection Report 07200039/2020401, Without Enclosure (Public - Cover Letter Only) IR 05000213/20180012018-05-31031 May 2018 NRC Independent Spent Fuel Storage Installation Inspection Report Nos. 07200039/2018001 and 05000213/2018001, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 07200039/20184012018-05-17017 May 2018 Connecticut Yankee Atomic Power Company Independent Spent Fuel Storage Security Inspection Report No. 07200039/2018401 - (Cover Letter Only) IR 05000213/20160022016-11-22022 November 2016 NRC Inspection Report No. 05000213/2016002 and 07200039/2016002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20160012016-05-18018 May 2016 IR 05000213-16-001 and 07200039-16-001 on 4/21/16, Connecticut Yankee Atomic Power Company, East Hampton, CT Site IR 07200039/20140012014-05-0606 May 2014 IR 07200039-14-001, on 04/17-18/14, Independent Spent Fuel Installation Inspection, Connecticut Yankee Atomic Power Company, East Hampton, CT IR 07200039/20100012010-12-22022 December 2010 IR 07200039-10-001, on 11/29/10, Connecticut Yankee Atomic Power Company, East Hampton, CT IR 05000213/20070012007-11-20020 November 2007 IR 05000213-07-001, on 04/23-26/07, 06/06-07/07, 07/17/07, 09/04/07, 10/29/07, 10/31/07, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut IR 05000213/20060032007-04-11011 April 2007 IR 05000213-06-003, on 10/01/2006 - 03/30/2007, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20060022006-09-19019 September 2006 IR 05000213-06-002, on 06/26-29/2006, 07/24-28/2006, and 08/21-25/2006, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20060012006-07-14014 July 2006 IR 05000213-06-001, on 01/27/06 - 06/15/2006, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20050032006-02-0707 February 2006 IR 05000213-05-003; Connecticut Yankee Atomic Power Company; on 10/01/2006 - 01/26/2006; Connecticut Yankee Atomic Power Company IR 05000213/20050022005-11-10010 November 2005 IR 05000213-05-002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20050012005-08-0505 August 2005 IR 05000213-05-001, on 01/01/2005 - 03/31/2005, Connecticut Yankee Atomic Power Company, Haddam Neck Plant, Office of Investigations Report No. 1-2004-032 and Notice of Violation IR 05000213/20040022005-02-0808 February 2005 IR 05000213-04-002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site and Notice of Violation IR 05000213/20040012004-09-20020 September 2004 IR 05000213-04-001, on 02/07/04 to 06/08/04, Connecticut Yankee Atomic Power Company IR 05000213/20030022004-01-0707 January 2004 IR 05000213-03-002, on 07/07/03 to 12/17/03, Connecticut Yankee Atomic Power Company IR 05000213/20030012003-07-0303 July 2003 IR 05000213-03-001 on 02/18/03 - 06/11/03 for Haddam Neck, Regarding Dismantlement and Decommissioning of Facility ML0320401272003-06-24024 June 2003 Powerpoint Presentation at Yankee Rowe Connecticut Yankee Management Meeting with the NRC, June 23, 2003 IR 05000213/19990021999-08-20020 August 1999 Insp Rept 50-213/99-02 on 990420-0719.No Violations Noted. Major Areas Inspected:Decommissioning Operations & Sf Safety Maint & Surveillance,Plant Support & Rediological Controls IR 05000213/19980061999-06-0909 June 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp 50-213/98-06 on 990226. Util Did Not Agree with Disposition of Issue Cited as Severity Level IV Violation.Violation Will Be Noncited IR 05000213/19990011999-05-21021 May 1999 Insp Rept 50-213/99-01 on 980119-990419.No Violations Noted. Major Areas Inspected:Aspects of Licensee Activities in Preparation for Dismantlement & Decommissioning of Facility IR 05000213/19980051998-12-21021 December 1998 Insp Rept 50-213/98-05 on 980720-1102.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000213/19980041998-11-27027 November 1998 Forwards Special Insp Rept 50-213/98-04 of Licensee Performance During Reactor Coolant Sys Chemical Decontamination ML20155F8511998-10-29029 October 1998 Insp Rept 50-213/98-04 on 980720-0911.Violations Noted. Major Areas Inspected:Aspects of Licensee Preparations, Planning & Implementation of RCS Chemical Decontamination, Operations,Engineering,Maint & Plant Support IR 05000213/19980031998-10-14014 October 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/98-03 Issued on 980821.Ack That Program Improvements for Violations That Occurred During Sys Decontamination,Still in Progress IR 05000213/19980011998-05-13013 May 1998 Insp Rept 50-213/98-01 on 980113-0413.Violations Noted.Major Areas Inspected:Decommissioning Support Activities,Spent Fuel Safety,Plant Support & Radiological Controls & Facility Mgt & Control IR 05000213/19980021998-05-0505 May 1998 Insp Rept 50-213/98-02 on 980316-20 & 25-27.No Violations Noted.Major Areas Inspected:Radiological Control Programs IR 05000213/19970091998-02-17017 February 1998 Insp Rept 50-213/97-09 on 971012-980112.Violations Noted. Major Areas Inspected:Decommissioning Operations & Planning & Included Aspects of Engineering,Maint & Plant Support IR 05000213/19970081998-01-29029 January 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/97-08 on 970703 & 0811-0919.Violation Involved Failure to Follow Radiation Protection Procedures IR 05000213/19970121998-01-15015 January 1998 Insp Rept 50-213/97-12 on 970812-13 & 1006-09.No Violations Noted.Major Areas Inspected:Status of Rp&C Facilities & Equipment IR 05000213/19970101998-01-14014 January 1998 Insp Rept 50-213/97-10 on 971008-1128.No Violations Noted. Major Areas Inspected:Plant Support IR 05000213/19970111997-12-29029 December 1997 Insp Rept 50-213/97-11 on 971006-09 & 1103-07.No Violations Noted.Major Areas Inspected:Programs for Radioactive Liquid Control IR 05000213/19970051997-11-26026 November 1997 Insp Rept 50-213/97-05 on 970708-1006.No Violations Noted. Major Areas Inspected:Plant Operations,Maint Engineering & Plant Support IR 05000213/19970031997-11-0707 November 1997 Corrected Pages for Insp Rept 50-213/97-03 on 970408-0707 & 0805 IR 05000213/19970071997-11-0707 November 1997 Corrected Page for Insp Rept 50-213/97-07 on 970715-30 ML20198N2821997-10-29029 October 1997 Insp Rept 50-213/97-08 on 970703,0811-0919.Violations Noted. Major Areas Inspected:Applied Radiological Controls Program, Contamination Control Program & Training of Personnel Relative to 49CFR172,subpart H IR 05000213/19970061997-08-12012 August 1997 Insp Rept 50-213/97-06 on 970616-0718.Violations Noted. Major Areas Inspected:Radiological Controls Program at Cyap Station,Haddam,Ct IR 05000213/19970011997-07-31031 July 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/97-01 ML20149D6211997-06-13013 June 1997 Mgt Meeting Rept 50-213/97-03 on 970528.Areas Discussed: Actions in Response to Findings Detailed in NRC Insp Repts 50-213/96-12.96-201 & 97-01.Deficiencies Involved Implementation of Radiation Protection Program IR 05000213/19970041997-06-0303 June 1997 Physical Security Insp Rept 50-213/97-04 on 970505-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Mgt Control,Pa Detection Aids,Alarm Stations & Communication,Testing,Maint & Compensatory Measures IR 05000213/19950271997-05-12012 May 1997 Discusses Insp Repts 50-213/95-27,50-213/96-06,50-213/96-07, 50-213/96-08,50-213/96-11,50-213/96-80 & 50-213/96-201 on 951121-961122 & Forwards NOV & Proposed Imposition of Civil Penalty in Amount of $650,000 ML20141F8301997-05-0808 May 1997 Insp Rept 50-213/97-01 on 970106-0407.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000213/19960071997-04-0909 April 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/96-07 IR 05000245/19960121997-03-27027 March 1997 Informs That Info Will Be Withheld from Public Disclosure Per Licensee 970303 Request.Licensee Re Exam Rept 50-245/96-12,dtd 970207 Also Discussed IR 05000213/19970021997-03-21021 March 1997 Insp Rept 50-213/97-02 on 970207-07 & 0224-26.Violation Noted.Major Area Inspected:Programs for Radioactive Liquid & Gaseous Effluent Control,Including Organization & Effectiveness of Program Implementation IR 05000213/19960111997-03-0707 March 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp 50-213/96-11.Exam of Actions Will Be Done During Future Insp 2024-08-27
[Table view] Category:NRC-GENERATED
MONTHYEARIR 05000213/19990021999-08-20020 August 1999 Insp Rept 50-213/99-02 on 990420-0719.No Violations Noted. Major Areas Inspected:Decommissioning Operations & Sf Safety Maint & Surveillance,Plant Support & Rediological Controls IR 05000213/19990011999-05-21021 May 1999 Insp Rept 50-213/99-01 on 980119-990419.No Violations Noted. Major Areas Inspected:Aspects of Licensee Activities in Preparation for Dismantlement & Decommissioning of Facility IR 05000213/19980051998-12-21021 December 1998 Insp Rept 50-213/98-05 on 980720-1102.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20155F8511998-10-29029 October 1998 Insp Rept 50-213/98-04 on 980720-0911.Violations Noted. Major Areas Inspected:Aspects of Licensee Preparations, Planning & Implementation of RCS Chemical Decontamination, Operations,Engineering,Maint & Plant Support IR 05000213/19980011998-05-13013 May 1998 Insp Rept 50-213/98-01 on 980113-0413.Violations Noted.Major Areas Inspected:Decommissioning Support Activities,Spent Fuel Safety,Plant Support & Radiological Controls & Facility Mgt & Control IR 05000213/19980021998-05-0505 May 1998 Insp Rept 50-213/98-02 on 980316-20 & 25-27.No Violations Noted.Major Areas Inspected:Radiological Control Programs IR 05000213/19970091998-02-17017 February 1998 Insp Rept 50-213/97-09 on 971012-980112.Violations Noted. Major Areas Inspected:Decommissioning Operations & Planning & Included Aspects of Engineering,Maint & Plant Support IR 05000213/19970121998-01-15015 January 1998 Insp Rept 50-213/97-12 on 970812-13 & 1006-09.No Violations Noted.Major Areas Inspected:Status of Rp&C Facilities & Equipment IR 05000213/19970101998-01-14014 January 1998 Insp Rept 50-213/97-10 on 971008-1128.No Violations Noted. Major Areas Inspected:Plant Support IR 05000213/19970111997-12-29029 December 1997 Insp Rept 50-213/97-11 on 971006-09 & 1103-07.No Violations Noted.Major Areas Inspected:Programs for Radioactive Liquid Control IR 05000213/19970051997-11-26026 November 1997 Insp Rept 50-213/97-05 on 970708-1006.No Violations Noted. Major Areas Inspected:Plant Operations,Maint Engineering & Plant Support IR 05000213/19970031997-11-0707 November 1997 Corrected Pages for Insp Rept 50-213/97-03 on 970408-0707 & 0805 IR 05000213/19970071997-11-0707 November 1997 Corrected Page for Insp Rept 50-213/97-07 on 970715-30 ML20198N2821997-10-29029 October 1997 Insp Rept 50-213/97-08 on 970703,0811-0919.Violations Noted. Major Areas Inspected:Applied Radiological Controls Program, Contamination Control Program & Training of Personnel Relative to 49CFR172,subpart H IR 05000213/19970061997-08-12012 August 1997 Insp Rept 50-213/97-06 on 970616-0718.Violations Noted. Major Areas Inspected:Radiological Controls Program at Cyap Station,Haddam,Ct ML20149D6211997-06-13013 June 1997 Mgt Meeting Rept 50-213/97-03 on 970528.Areas Discussed: Actions in Response to Findings Detailed in NRC Insp Repts 50-213/96-12.96-201 & 97-01.Deficiencies Involved Implementation of Radiation Protection Program IR 05000213/19970041997-06-0303 June 1997 Physical Security Insp Rept 50-213/97-04 on 970505-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Mgt Control,Pa Detection Aids,Alarm Stations & Communication,Testing,Maint & Compensatory Measures ML20141F8301997-05-0808 May 1997 Insp Rept 50-213/97-01 on 970106-0407.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000213/19970021997-03-21021 March 1997 Insp Rept 50-213/97-02 on 970207-07 & 0224-26.Violation Noted.Major Area Inspected:Programs for Radioactive Liquid & Gaseous Effluent Control,Including Organization & Effectiveness of Program Implementation IR 05000213/19960121997-02-25025 February 1997 Summary of Meeting Re Insp 50-213/96-12 on 970205 in King of Prussia,Pa to Discuss Findings Detailed in Insp Rept on 961102.Radiation Program Was Deficient in Several Areas That Resulted in Potential Exposure to Radiation ML20138J6751997-02-0404 February 1997 Insp Rept 50-213/96-13 on 961116-970105.Violations Noted. Major Areas Inspected:Plant Operations,Maintenance, Engineering & Plant Support ML20133A5031996-12-24024 December 1996 Insp Rept 50-213/96-11 on 960921-1115.Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support ML20132G6211996-12-19019 December 1996 Insp Rept 50-213/96-12 on 961102-27.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Review of Airborne Radioactivity Event That Occurred on 961102 IR 05000213/19960101996-11-0505 November 1996 Insp Rept 50-213/96-10 on 960811-0920.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support IR 05000213/19960801996-10-30030 October 1996 Insp Rept 50-213/96-80 on 960903-1002.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Mgt Oversight & Controls ML20129F4701996-10-23023 October 1996 Insp Rept 50/213-96-07 on 960813-16.No Violations Noted. Major Areas Inspected:Licensee Performance During Biennial Emergency Preparedness Exercise,Emergency Facility Staffing, Procedure Emplementation & Effectiveness of Mitigation IR 05000213/20030141995-06-0808 June 1995 Insp Rept 50-397/95-03 on 950213-0314.Violations Noted.Major Areas Inspected:Performance of Engineers on Basis of Quality of Engineering Work Products Basic Design Changes IR 05000213/19940011994-01-24024 January 1994 Insp Rept 50-213/94-01 on 940110-14.No Violations Noted. Major Areas Inspected:Projected Dose Calculation Capability from Radioactive Liquid & Gaseous Effluent Releases IR 05000213/19930211993-12-30030 December 1993 Insp Rept 50-213/93-21 on 931107-1211.Violations Noted. Major Areas Inspected:Plant Operations,Maintenance, Engineering & Technical Support & Plant Support Activities IR 05000213/19930231993-12-17017 December 1993 Insp Repts 50-213/93-23,50-245/93-30,50-336/93-25 & 50-423/93-27 on Stated Date.Violation Noted.Major Areas Inspected:Ffd Program,Policies & Procedures,Ffd Organization & Mgt Control,Training,Chemical Testing & FFD Audit IR 05000213/19930191993-11-23023 November 1993 Insp Rept 50-213/93-19 on 931003-1106.No Violations Noted. Major Areas Inspected:Plant Operations,Maintenance, Engineering & Technical Support & Plant Support Activities IR 05000213/19930181993-10-0707 October 1993 Insp Rept 50-213/93-18 on 930927-30.No Safety Concerns or Violations Noted.Major Areas Inspected:Remp,Including Mgt Controls,Qa Audits,Meteorological Monitoring Program & QC Program for Analytical Measurements IR 05000213/19930151993-10-0101 October 1993 Insp Rept 50-213/93-15 on Stated Dates.No Violations Noted.Major Areas Inspected:Generic Ltr 89-10 Program & Related Activities IR 05000213/19930161993-09-29029 September 1993 Insp Rept 50-213/93-16 on 930725-0828.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Technical Support,Plant Support Activities,Outage Assessment & Emergency Planning Drill IR 05000213/19930121993-08-18018 August 1993 Safety Insp Rept 50-213/93-12 on 930620-0724.Violations Noted.Major Areas Inspected:Plant Operations,Outage Activities,Event Response,Maint,Engineering & Technical Support & Plant Support Activities IR 05000213/19930141993-08-0303 August 1993 Insp Rept 50-213/93-14 on 930719-23.No Violations Noted. Major Areas Inspected:Determination of Whether Licensee Design,Installation & Mod of safety-related Dynamic Pipe Restraints & Static Pipe Supports Performed Correctly IR 05000213/19930081993-07-26026 July 1993 Insp Rept 50-213/93-08 on 930509-0619.Deviation Noted.Major Areas Inspected:Plant Operations,Refuel Outage Activities, Radiological Controls,Maint,Surveillance,Plant Mod,Licensee Event Repts & Periodic Repts IR 05000213/19930111993-07-16016 July 1993 Insp Rept 50-213/93-11 on 930621-25.No Violations Noted. Major Areas Inspected:Insp Was Conducted on Licensee Actions Re Feedwater Nozzle Cracking & Associated Insp & Repair Activities IR 05000213/19930091993-06-17017 June 1993 Insp Rept 50-213/93-09 on 930524-28.No Violations Noted. Major Areas Inspected:Licensee ISI Program & Related Activities,Sg Tube Eddy Current Insp Program Including Data Acquisition & Analysis IR 05000213/19930101993-06-0909 June 1993 Insp Rept 50-213/93-10 on 930601-04.No Violations Noted. Major Areas Inspected:Radiation Protection Program,Mgt Organization,Radiation Control During Refueling Outage, ALARA & Implementation of Programs IR 05000213/19930071993-06-0404 June 1993 Insp Rept 50-213/93-07 on 930510-14.No Violations Noted. Major Areas Inspected:Mgt Support,Security Program Plans & Security & FFD Audits,Protected Area Physical Barriers, Detection & Assessment Aids & Packages & Vehicles IR 05000213/19930061993-06-0303 June 1993 Insp Rept 50-213/93-06 on 930328-0508.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint,Surveillance,Ler & Periodic Repts ML20045B5301993-06-0101 June 1993 Insp of Acceptability of Performance Enhancement Program (Pep) on 920921-25,1026-30 & 1130-1202.PEP Provides Significant Resource Increases in Key Depts as Well as Efforts to Improve Organizational & Mgt Performance ML20035H5661993-04-27027 April 1993 Resident Safety Insp Rept 50-213/93-03 on 930221-0327. Operator Response to Rod Drive Sys Malfunction on 930323 Timely & Appropriate.Major Areas Inspected:Plant Operations, Radiological Controls,Outage Planning & Periodic Repts IR 05000213/19930021993-04-19019 April 1993 Emergency Preparedness Exercise Insp Rept 50-213/93-02 on 930326-29.Major Areas Inspected:Licensee Annual partial- Participation Emergency Preparedness Exercise IR 05000213/19930011993-03-22022 March 1993 Safety Insp Rept 50-213/93-01 on 930110-0220.No Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls,Maint,Surveillance,Emergency Preparedness,Lers, Quality Assurance Audits & Previously Identified Items IR 05000213/19920261993-02-25025 February 1993 Insp Rept 50-213/92-26 on 921213-930109.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint,Surveillance,Engineering & Technical Support, Licensee self-assessment & LERs IR 05000213/19920211993-01-15015 January 1993 Insp Rept 50-213/92-21 on 921115-1212.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls,Maint,Lers & Periodic Repts & Manual Operator Actions During Postulated Station Blackout IR 05000213/19920241992-12-30030 December 1992 Insp Rept 50-213/92-24 on 921130-1204.No Violations Noted. Major Areas Inspected:Function of Engineering & Technical Support Reviewed to Evaluate Staffing of Engineering Dept IR 05000213/19920251992-12-22022 December 1992 Insp Rept 50-213/92-25 on 921214-17.No Violations Noted. Major Areas Inspected:Mgt Organization,Training & Assurance of Quality 1999-08-20
[Table view] Category:INSPECTION REPORT
MONTHYEARIR 05000213/20240012024-08-27027 August 2024 Connecticut Yankee Atomic Power Company - Independent Spent Fuel Storage Installation NRC Inspection Report Nos. 07200039/2024001 and 05000213/2024001 IR 07200039/20224012022-10-0505 October 2022 Connecticut Yankee Atomic Power Company - NRC Independent Spent Fuel Storage Security Inspection Report No. 07200039/2022401 IR 05000213/20210012021-10-26026 October 2021 Connecticut Yankee Atomic Power Company - NRC Independent Spent Fuel Storage Installation Inspection Report Nos. 07200039/2021001 and 05000213/2021001 IR 07200039/20204012020-11-20020 November 2020 Connecticut Yankee Atomic Power Company - Independent Spent Fuel Storage Installation Security Inspection Report 07200039/2020401, Without Enclosure (Public - Cover Letter Only) IR 05000213/20180012018-05-31031 May 2018 NRC Independent Spent Fuel Storage Installation Inspection Report Nos. 07200039/2018001 and 05000213/2018001, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 07200039/20184012018-05-17017 May 2018 Connecticut Yankee Atomic Power Company Independent Spent Fuel Storage Security Inspection Report No. 07200039/2018401 - (Cover Letter Only) IR 05000213/20160022016-11-22022 November 2016 NRC Inspection Report No. 05000213/2016002 and 07200039/2016002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20160012016-05-18018 May 2016 IR 05000213-16-001 and 07200039-16-001 on 4/21/16, Connecticut Yankee Atomic Power Company, East Hampton, CT Site IR 07200039/20140012014-05-0606 May 2014 IR 07200039-14-001, on 04/17-18/14, Independent Spent Fuel Installation Inspection, Connecticut Yankee Atomic Power Company, East Hampton, CT IR 07200039/20100012010-12-22022 December 2010 IR 07200039-10-001, on 11/29/10, Connecticut Yankee Atomic Power Company, East Hampton, CT IR 05000213/20070012007-11-20020 November 2007 IR 05000213-07-001, on 04/23-26/07, 06/06-07/07, 07/17/07, 09/04/07, 10/29/07, 10/31/07, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut IR 05000213/20060032007-04-11011 April 2007 IR 05000213-06-003, on 10/01/2006 - 03/30/2007, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20060022006-09-19019 September 2006 IR 05000213-06-002, on 06/26-29/2006, 07/24-28/2006, and 08/21-25/2006, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20060012006-07-14014 July 2006 IR 05000213-06-001, on 01/27/06 - 06/15/2006, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20050032006-02-0707 February 2006 IR 05000213-05-003; Connecticut Yankee Atomic Power Company; on 10/01/2006 - 01/26/2006; Connecticut Yankee Atomic Power Company IR 05000213/20050022005-11-10010 November 2005 IR 05000213-05-002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site IR 05000213/20050012005-08-0505 August 2005 IR 05000213-05-001, on 01/01/2005 - 03/31/2005, Connecticut Yankee Atomic Power Company, Haddam Neck Plant, Office of Investigations Report No. 1-2004-032 and Notice of Violation IR 05000213/20040022005-02-0808 February 2005 IR 05000213-04-002, Connecticut Yankee Atomic Power Company, East Hampton, Connecticut Site and Notice of Violation IR 05000213/20040012004-09-20020 September 2004 IR 05000213-04-001, on 02/07/04 to 06/08/04, Connecticut Yankee Atomic Power Company IR 05000213/20030022004-01-0707 January 2004 IR 05000213-03-002, on 07/07/03 to 12/17/03, Connecticut Yankee Atomic Power Company IR 05000213/20030012003-07-0303 July 2003 IR 05000213-03-001 on 02/18/03 - 06/11/03 for Haddam Neck, Regarding Dismantlement and Decommissioning of Facility ML0320401272003-06-24024 June 2003 Powerpoint Presentation at Yankee Rowe Connecticut Yankee Management Meeting with the NRC, June 23, 2003 IR 05000213/19990021999-08-20020 August 1999 Insp Rept 50-213/99-02 on 990420-0719.No Violations Noted. Major Areas Inspected:Decommissioning Operations & Sf Safety Maint & Surveillance,Plant Support & Rediological Controls IR 05000213/19980061999-06-0909 June 1999 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp 50-213/98-06 on 990226. Util Did Not Agree with Disposition of Issue Cited as Severity Level IV Violation.Violation Will Be Noncited IR 05000213/19990011999-05-21021 May 1999 Insp Rept 50-213/99-01 on 980119-990419.No Violations Noted. Major Areas Inspected:Aspects of Licensee Activities in Preparation for Dismantlement & Decommissioning of Facility IR 05000213/19980051998-12-21021 December 1998 Insp Rept 50-213/98-05 on 980720-1102.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000213/19980041998-11-27027 November 1998 Forwards Special Insp Rept 50-213/98-04 of Licensee Performance During Reactor Coolant Sys Chemical Decontamination ML20155F8511998-10-29029 October 1998 Insp Rept 50-213/98-04 on 980720-0911.Violations Noted. Major Areas Inspected:Aspects of Licensee Preparations, Planning & Implementation of RCS Chemical Decontamination, Operations,Engineering,Maint & Plant Support IR 05000213/19980031998-10-14014 October 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/98-03 Issued on 980821.Ack That Program Improvements for Violations That Occurred During Sys Decontamination,Still in Progress IR 05000213/19980011998-05-13013 May 1998 Insp Rept 50-213/98-01 on 980113-0413.Violations Noted.Major Areas Inspected:Decommissioning Support Activities,Spent Fuel Safety,Plant Support & Radiological Controls & Facility Mgt & Control IR 05000213/19980021998-05-0505 May 1998 Insp Rept 50-213/98-02 on 980316-20 & 25-27.No Violations Noted.Major Areas Inspected:Radiological Control Programs IR 05000213/19970091998-02-17017 February 1998 Insp Rept 50-213/97-09 on 971012-980112.Violations Noted. Major Areas Inspected:Decommissioning Operations & Planning & Included Aspects of Engineering,Maint & Plant Support IR 05000213/19970081998-01-29029 January 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/97-08 on 970703 & 0811-0919.Violation Involved Failure to Follow Radiation Protection Procedures IR 05000213/19970121998-01-15015 January 1998 Insp Rept 50-213/97-12 on 970812-13 & 1006-09.No Violations Noted.Major Areas Inspected:Status of Rp&C Facilities & Equipment IR 05000213/19970101998-01-14014 January 1998 Insp Rept 50-213/97-10 on 971008-1128.No Violations Noted. Major Areas Inspected:Plant Support IR 05000213/19970111997-12-29029 December 1997 Insp Rept 50-213/97-11 on 971006-09 & 1103-07.No Violations Noted.Major Areas Inspected:Programs for Radioactive Liquid Control IR 05000213/19970051997-11-26026 November 1997 Insp Rept 50-213/97-05 on 970708-1006.No Violations Noted. Major Areas Inspected:Plant Operations,Maint Engineering & Plant Support IR 05000213/19970031997-11-0707 November 1997 Corrected Pages for Insp Rept 50-213/97-03 on 970408-0707 & 0805 IR 05000213/19970071997-11-0707 November 1997 Corrected Page for Insp Rept 50-213/97-07 on 970715-30 ML20198N2821997-10-29029 October 1997 Insp Rept 50-213/97-08 on 970703,0811-0919.Violations Noted. Major Areas Inspected:Applied Radiological Controls Program, Contamination Control Program & Training of Personnel Relative to 49CFR172,subpart H IR 05000213/19970061997-08-12012 August 1997 Insp Rept 50-213/97-06 on 970616-0718.Violations Noted. Major Areas Inspected:Radiological Controls Program at Cyap Station,Haddam,Ct IR 05000213/19970011997-07-31031 July 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/97-01 ML20149D6211997-06-13013 June 1997 Mgt Meeting Rept 50-213/97-03 on 970528.Areas Discussed: Actions in Response to Findings Detailed in NRC Insp Repts 50-213/96-12.96-201 & 97-01.Deficiencies Involved Implementation of Radiation Protection Program IR 05000213/19970041997-06-0303 June 1997 Physical Security Insp Rept 50-213/97-04 on 970505-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Mgt Control,Pa Detection Aids,Alarm Stations & Communication,Testing,Maint & Compensatory Measures IR 05000213/19950271997-05-12012 May 1997 Discusses Insp Repts 50-213/95-27,50-213/96-06,50-213/96-07, 50-213/96-08,50-213/96-11,50-213/96-80 & 50-213/96-201 on 951121-961122 & Forwards NOV & Proposed Imposition of Civil Penalty in Amount of $650,000 ML20141F8301997-05-0808 May 1997 Insp Rept 50-213/97-01 on 970106-0407.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support IR 05000213/19960071997-04-0909 April 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-213/96-07 IR 05000245/19960121997-03-27027 March 1997 Informs That Info Will Be Withheld from Public Disclosure Per Licensee 970303 Request.Licensee Re Exam Rept 50-245/96-12,dtd 970207 Also Discussed IR 05000213/19970021997-03-21021 March 1997 Insp Rept 50-213/97-02 on 970207-07 & 0224-26.Violation Noted.Major Area Inspected:Programs for Radioactive Liquid & Gaseous Effluent Control,Including Organization & Effectiveness of Program Implementation IR 05000213/19960111997-03-0707 March 1997 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp 50-213/96-11.Exam of Actions Will Be Done During Future Insp 2024-08-27
[Table view] Category:UTILITY
MONTHYEARIR 05000213/19900831990-11-0505 November 1990 Insp Repts 50-213/90-83,50-245/90-82,50-336/90-82 & 50-423/90-83 on 900924-28.No Violations Noted.Major Areas Inspected:Licensee Timeliness for Reporting/Operability Determinations IR 05000213/19900821990-10-23023 October 1990 Insp Repts 50-213/90-82,50-245/90-81,50-336/90-81 & 50-423/90-82,on 901001-12.No Violations Noted.Major Areas Inspected:Licensee Occupational Radiation Protection Program Activities During Unit 1 Refueling Outage IR 05000213/19900131990-10-19019 October 1990 Safety Insp Rept 50-213/90-13 on 900801-0911.Good Radiological Controls Performance Noted.Major Areas Inspected:Plant Startup Following 1989/1990 Refueling Outage,Reactor Trips on 900813 & 0903 & Safeguards Problems IR 05000213/19900181990-10-10010 October 1990 Insp Rept 50-213/90-18 on 900926.No Violations Noted IR 05000213/19900121990-08-22022 August 1990 Safety Insp Rept 50-213/90-12 on 900621-0731.Major Areas Inspected:Review of Final Refueling Outage Activities, Preparations for Reactor Startup,Exams of safety-related Equipment Readiness & Review of Operational Events IR 05000213/19900081990-07-11011 July 1990 Insp Rept 50-213/90-08 on 900509-0620.Weaknesses Noted.Major Areas Inspected:Plant Operations,Reactor Fuel Reload Activities,Radiological Controls,Loss of Power Testing, Cleaning & Insp of RCS & Insp of Pressurizer Clad Cracks IR 05000213/19900051990-06-0606 June 1990 Safety Insp Rept 50-213/90-05 on 900328-0508.No Violations Noted.Major Areas Inspected:Plant Operations,Radiological Controls During Thermal Shield Shipping & Refueling Cavity Cleaning & Emergency Preparedness Training Exercise IR 05000213/19900091990-06-0404 June 1990 Emergency Preparedness Insp Rept 50-213/90-09 on 900518-20. Unresolved Item & Exercise Weaknesses Identified.Major Areas Inspected:Licensee full-participation Emergency Preparedness Exercise Conducted on 900519 IR 05000213/19900071990-05-18018 May 1990 Insp Rept 50-213/90-07 on 900402-05.No Violations Noted. Major Areas Inspected:Changes to Emergency Plan & Implementing Procedures,Emergency Response Facilities, Equipment & Organization & Mgt Control IR 05000213/19900041990-04-18018 April 1990 Safety Insp Rept 50-213/90-04 on 900216-0327.No Violations Noted.Major Areas Inspected:Plant Operations & Radiological Controls During Thermal Shield Cutting & Cleaning of Refueling Water Storage Tank IR 05000213/19900061990-04-13013 April 1990 Insp Rept 50-213/90-06 on 900314-16.No Violations Noted. Major Areas Inspected:Licensee Program to Ensure Adequate Quality of Fuel Oil for Emergency Diesel Generators to Meet Tech Spec Operational Requirements IR 05000213/19900021990-03-14014 March 1990 Insp Rept 50-213/90-02 on 900109-0215.No Violations Noted. Major Areas Inspected:Plant Operations,Radiological Controls During Thermal Shield Removal,Reactor Vessel Thermal Shield Removal & App R Svc Water Performance Testing & Security IR 05000213/19890231989-12-28028 December 1989 Insp Rept 50-213/89-23 on 891127-1201.No Violations or Deviations Noted.Major Areas Inspected:Pump & Valve Inservice Test Program Implementation & Licensee Corrective Action Program for Leakage Problem Evaluation & Correction IR 05000213/19890221989-12-12012 December 1989 Insp Rept 50-213/89-22 on 891113-17.Violation Noted.Major Areas Inspected:Radiological Controls Program,Including Training & Qualifications of Health Physics Staff,Auditing, Internal Exposure Control & New TLD Personnel Dosimetry IR 05000213/19890161989-11-0808 November 1989 Safety Insp Rept 50-213/89-16 on 890906-1017.No Unresolved Items Noted.Major Areas Inspected:Plant Operations,Events Occurring During Insp Period Including Elevated RCS Activity,Radiological Controls,Security & Maint IR 05000213/19890191989-11-0202 November 1989 Insp Rept 50-213/89-19 on 891016-20.No Violations or Deviations Noted.Major Areas Inspected:Inservice Insp,Steam Generator Eddy Current & Erosion/Corrosion Programs & Status of Debris in Fuel Bundles IR 05000213/19890171989-11-0101 November 1989 Insp Rept 50-213/89-17 on 891002-06.No Violations Noted. Major Areas Inspected:Radiological Control Activities During Refueling Outage & Radiological Controls Program Onsite IR 05000213/19890181989-10-24024 October 1989 Insp Rept 50-213/89-18 on 891010-13.No Violations Noted. Major Areas Inspected:Operational Radiological Environ Monitoring Program,Including Mgt Organization,Sample Collection & Control of Contractor Activities IR 05000213/19890151989-10-12012 October 1989 Insp Rept 50-213/89-15 on 890911-15.No Violations Noted. Major Areas Inspected:Previously Identified Open Items & Adequacy of Resolution IR 05000213/19890121989-09-29029 September 1989 Insp Rept 50-213/89-12 on 890726-0905.No Violations Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Fire Protection,Security,Maint,Surveillance Testing,Licensee Events,Open Items & Opening of New Security Access Point IR 05000213/19890141989-09-21021 September 1989 Insp Rept 50-213/89-14 on 890911-15.No Violations or Deviations Noted.Major Areas Inspected:Solid Radwaste Sys, Transportation,Liquid & Gaseous Effluents Programs, Including Mgt Controls,Audits & QA IR 05000213/19890131989-09-15015 September 1989 Insp Rept 50-213/89-13 on 890814-18.No Violations Noted. Major Areas Inspected:Const Activities of New Switchgear Bldg Constructed to Comply W/App R Requirements & Review of Adequacy & Implementation of Fire Protection Program IR 05000213/19890111989-08-24024 August 1989 Safety Insp Rept 50-213/89-11 on 890731-0804.No Violations Noted.Major Areas Inspected:Changes to Emergency Preparedness Program,Emergency Facilities,Equipment, Instrumentation,Supplies & Organization & Mgt Control IR 05000213/19890101989-08-18018 August 1989 Safety Insp Rept 50-213/89-10 on 890614-0725.No Violations & No New Unresolved Items Noted.Major Areas Inspected:Plant Operations,Radiation Protection,Fire Protection,Security, Maint,Surveillance Testing,Open Items & Safety Sys Lineups IR 05000213/19890091989-08-0303 August 1989 Partially Withheld Physical Security Insp Rept 50-213/89-09 on 890626-30 (Ref 10CFR73.21 & 2.790(a)).No Violations Noted.Major Areas Inspected:Mgt Support,Program Plans, Audits & Protected & Vital Area Physical Barriers IR 05000213/19890071989-07-11011 July 1989 Insp Rept 50-213/89-07 on 890503-0613.Violations Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Fire Protection,Security,Maint,Surveillance Testing,Licensee Events & Open Items from Previous Insps IR 05000213/19890081989-07-0707 July 1989 Insp Rept 50-213/89-08 on 890614-16.No Violations Noted. Major Areas Inspected:Radiological Controls Program on Site, Including Changes in Organization,Personnel,Procedures & Review of Preparations for Refueling Outage ML20247J2391989-05-19019 May 1989 Insp Rept 50-213/89-200 on 890130-0210.Weaknesses Noted Re Installation of commercial-grade Items.Major Areas Inspected:Implementation of Vendor Interface Program & Program for Procurement of Items in safety-related Sys IR 05000213/19890051989-05-17017 May 1989 Safety Insp Rept 50-213/89-05 on 890329-0502.Violation Noted.Major Areas Inspected:Plant Operations,Radiation Protection,Fire Protection,Security,Maint,Surveillance Testing & Licensee Events IR 05000213/19890041989-05-12012 May 1989 Insp Rept 50-213/89-04 on 890421-22.No Violations Noted. Major Areas Inspected:Emergency Preparedness & Observation of Licensee partial-participation,emergency Preparedness Exercise Conducted on 890422 IR 05000213/19890021989-05-0303 May 1989 Safety Insp Rept 50-213/89-02 on 890222-0328.No Violations Noted.Major Areas Inspected:Plant Operations,Radiation Protection,Fire Protection,Security,Maint,Surveillance Testing,Events Occurring During Insp & Open Items IR 05000213/19890011989-03-10010 March 1989 Insp Rept 50-213/89-01 on 890104-0221.No Violations Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Fire Protection,Security,Maint,Surveillance Testing,Noble Gas Source Investigation & Reactor Containment Temp IR 05000213/19880191988-12-0101 December 1988 Insp Rept 50-213/88-19 on 880928-1115.No Violations Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Fire Protection,Security,Maint,Surveillance Testing,Licensee Events & Containment Integrated Leak Rate Test Rept IR 05000213/19880211988-11-15015 November 1988 Physical Security Insp Repts 50-213/88-21,50-245/88-22, 50-336/88-25 & 50-423/88-21 on 881017-21.No Noncompliance Noted.Major Areas Inspected:Safeguards Info Program - Corporate Ofcs IR 05000213/19880201988-11-0808 November 1988 Insp Rept 50-213/88-20 on 881014-16.No Violations,Deviations or Unresolved Items Noted.Major Areas Inspected:Emergency Preparedness Exercise Conducted on 881014-16 IR 05000213/19880161988-11-0404 November 1988 Insp Rept 50-213/88-16 on 880830-31 & 0901.No Violations or Deviations Noted.Major Areas Inspected:Emergency Preparedness Program IR 05000213/19880181988-10-14014 October 1988 Insp Rept 50-213/88-18 on 880906-09.No Violations Noted. Major Areas Inspected:Radiological Controls Program, Including Radiation Surveys,Respirator Issue & Maint,Air Sampling Equipment Calibr & Counting Room Operations IR 05000213/19880151988-10-12012 October 1988 Safety Insp Rept 50-213/88-15 on 880801-0912.No Violations Noted.Major Areas Inspected:Plant Operations,Radiation Protection,Fire Protection,Security,Maint,Surveillance Testing,Licensee Events & Open Items from Previous Insps IR 05000213/19880131988-10-0606 October 1988 Insp Rept 50-213/88-13 on 880822-26.No Violations Noted. Major Areas Inspected:Radiochemical Measurements Program, Including Confirmatory Measurements,Program for Qa/Qc of Radiological Measurements & Mgt Controls IR 05000213/19880171988-09-26026 September 1988 Insp Rept 50-213/88-17 on 880822-26.No Violations Noted. Major Areas Inspected:Inservice Insp Program Per ASME Code & Regulatory Requirements IR 05000213/19880141988-08-16016 August 1988 Insp Rept 50-213/88-14 on 880719-22.No Violations Noted. Major Areas Inspected:Concrete Work & Records,Structural Steel Work & Records for New Switchgear Bldg IR 05000213/19880111988-07-31031 July 1988 Insp Rept 50-213/88-11 on 880517-0731.No Violations Noted. Major Areas Inspected:Plant Operations,Radiation & Fire Protection,Security Maint,Surveillance Testing,Switchgear Bldg Const & Open Items from Previous Insps IR 05000213/19880091988-07-22022 July 1988 Insp Rept 50-213/88-09 on 880516-20.No Violations or Deviations Noted.Major Areas Inspected:Steam Generator Inservice Insp,Secondary Water Chemistry Control,Radiation Protection Results & Insp of Other Secondary HXs IR 05000213/19880101988-06-21021 June 1988 Insp Rept 50-213/88-10 on 880523-27.No Violations Noted. Major Areas Inspected:Operational Radiological Environ Monitoring Program,Including Mgt Organization,Environ Sample Collection & Meteorological Monitoring IR 05000213/19880081988-05-27027 May 1988 Safety Insp Rept 50-213/88-08 on 880405-0516.No Violations Noted.Major Areas Inspected:Plant Operations,Radiation Protection,Fire Protection,Security,Maint,Surveillance Testing & Generic Ltrs 87-12 & 81-21 IR 05000213/19880061988-04-21021 April 1988 Insp Rept 50-213/88-06 on 880307-11.No Violations Noted. Major Areas Inspected:Assurance of Readiness for Mode Changes Leading to Power Operation Based on Review of Operations,Mods,Preoperational/Startup & Low Physics Tests IR 05000213/19880031988-04-20020 April 1988 Insp Rept 50-213/88-03 on 880301-0404.No Violations Noted. Major Areas Inspected:Plant Operations,Radiation Protection, Fire Protection,Security,Maint,Surveillance Testing,Licensee Events & Open Items from Previous Insps IR 05000213/19880071988-04-0101 April 1988 Insp Rept 50-213/88-07 on 880314-17.No Violations Noted. Major Areas Inspected:Plan & Implementing Procedures, Organization,Program Audit,Records & Repts,Testing & Maint, Physical Barriers,Protected & Vital Areas & Lighting ML20151C1791988-03-29029 March 1988 Insp Rept 50-213/87-28 on 871116-20.Violations Noted. Major Areas Inspected:Licensee Implementation of Environ Qualification Program & Verification of Implementation Per 10CFR50.49 Requirements IR 05000213/19880021988-03-11011 March 1988 Safety Insp Repts 50-213/88-02 on 880113-0229.No Violations Noted.Major Areas Inspected:Outage Activities,Radiation Protection,Fire Protection,Security,Maint,Surveillance Testing & Events Occurring During Insp Period 1990-08-22
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARPNO-I-99-039, on 990831,Haddam Neck Plant CR Was Notified by Transportation Contractor,Hittman Transportation Svcs,That Driver of Truck,Left Plant Earlier in Day Noticed Water Leakage from from sea-land Container He Was Transporting1999-09-0101 September 1999 PNO-I-99-039:on 990831,Haddam Neck Plant CR Was Notified by Transportation Contractor,Hittman Transportation Svcs,That Driver of Truck,Left Plant Earlier in Day Noticed Water Leakage from from sea-land Container He Was Transporting IR 05000213/19990021999-08-20020 August 1999 Insp Rept 50-213/99-02 on 990420-0719.No Violations Noted. Major Areas Inspected:Decommissioning Operations & Sf Safety Maint & Surveillance,Plant Support & Rediological Controls IR 05000213/19990011999-05-21021 May 1999 Insp Rept 50-213/99-01 on 980119-990419.No Violations Noted. Major Areas Inspected:Aspects of Licensee Activities in Preparation for Dismantlement & Decommissioning of Facility ML20206R7391999-05-12012 May 1999 Notice of Violation from Investigation on 970616-0718. Violations Noted:On 961209 & 10,J Foley Deliberately Caused Util to Be in Violation of 10CFR50.9 & TS 6.11 & in June 1997 Provided Inaccurate Info to NRC Inspector ML20206R7141999-05-12012 May 1999 Notice of Violation from Investigation on 970314-0722. Violation Noted:M Thomas Engaged in Deliberate Misconduct on 970227,that But for Detection,Would Have Caused Licensee to Be in Violation of 10CFR20.1802 ML20205J8031999-04-0505 April 1999 Notice of Violation from Insp on 961102-27.Violation Noted:Licensee Failed to Adequately Instruct Workers & Failed to Perform Adequate Radiological Surveys in Reactor Cavity & Fuel Transfer Cavity ML20206B3801999-03-29029 March 1999 EN-99-015:informs Commission That Staff Intends to Exercise Discretion Pursuant to Section VII.B.6 of Enforcement Policy & Not Propose Civil Penalty for Severity Level III Problem That Occurred in Nov 1996,prior to Licensee Decision ML20207B7041999-02-26026 February 1999 Notice of Violation from Insp on 981103-990118.Violations Noted:Two Different Locked High Radiation Area Doors in Containment Builiding Found Unlocked & Unattended IR 05000213/19980051998-12-21021 December 1998 Insp Rept 50-213/98-05 on 980720-1102.No Violations Noted. Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20155F8511998-10-29029 October 1998 Insp Rept 50-213/98-04 on 980720-0911.Violations Noted. Major Areas Inspected:Aspects of Licensee Preparations, Planning & Implementation of RCS Chemical Decontamination, Operations,Engineering,Maint & Plant Support ML20237D4071998-08-21021 August 1998 Notice of Violations from Insp on 980414-0803 & 13. Violations Noted:Licensee Failed to Declare Unusual Event Re 980620 Release of About 800 Gallons of Water Containing Approx 2200 Uci Radioactivity from a Waste Test Tank PNO-I-98-033, on 980728,licensee Identified Leak of Approximately 1,000 Gallons of Demineralized Water & Chemical Agents Used for Decontamination of Plant Sys.Region I Radiation Specialist Will Be Onsite to Review Licensee1998-07-28028 July 1998 PNO-I-98-033:on 980728,licensee Identified Leak of Approximately 1,000 Gallons of Demineralized Water & Chemical Agents Used for Decontamination of Plant Sys.Region I Radiation Specialist Will Be Onsite to Review Licensee IR 05000213/19980011998-05-13013 May 1998 Insp Rept 50-213/98-01 on 980113-0413.Violations Noted.Major Areas Inspected:Decommissioning Support Activities,Spent Fuel Safety,Plant Support & Radiological Controls & Facility Mgt & Control IR 05000213/19980021998-05-0505 May 1998 Insp Rept 50-213/98-02 on 980316-20 & 25-27.No Violations Noted.Major Areas Inspected:Radiological Control Programs ML20203E6771998-02-17017 February 1998 Notice of Violation from Insp on 971012-980112.Violation Noted:Licensee Did Not Provide for Verifying or Checking Adequacy of Design for Listed Sys & Components IR 05000213/19970091998-02-17017 February 1998 Insp Rept 50-213/97-09 on 971012-980112.Violations Noted. Major Areas Inspected:Decommissioning Operations & Planning & Included Aspects of Engineering,Maint & Plant Support IR 05000213/19970121998-01-15015 January 1998 Insp Rept 50-213/97-12 on 970812-13 & 1006-09.No Violations Noted.Major Areas Inspected:Status of Rp&C Facilities & Equipment IR 05000213/19970101998-01-14014 January 1998 Insp Rept 50-213/97-10 on 971008-1128.No Violations Noted. Major Areas Inspected:Plant Support IR 05000213/19970111997-12-29029 December 1997 Insp Rept 50-213/97-11 on 971006-09 & 1103-07.No Violations Noted.Major Areas Inspected:Programs for Radioactive Liquid Control PNO-I-97-073A, on 971210,update of Offsite Surveys for Contaminated Blocks Made.Total of 114 Blocks Out of 3032 Indicated Radioactive Contamination at Greater than Two Times Background Levels.Licensee Plans to Return to Sites1997-12-11011 December 1997 PNO-I-97-073A:on 971210,update of Offsite Surveys for Contaminated Blocks Made.Total of 114 Blocks Out of 3032 Indicated Radioactive Contamination at Greater than Two Times Background Levels.Licensee Plans to Return to Sites PNO-I-97-074, on 971203,licensee Announced Senior Mgt Restructuring,Which Included Naming New Chairman,President, Chief Executive Officer,Chief Financial Officer & Promotion of Director of Site Operations1997-12-0404 December 1997 PNO-I-97-074:on 971203,licensee Announced Senior Mgt Restructuring,Which Included Naming New Chairman,President, Chief Executive Officer,Chief Financial Officer & Promotion of Director of Site Operations PNO-I-97-073, survey Identified Former Cask Wash Down Area Needing Further Characterization & Remediation within Licensee Control Area.Concrete Blocks Used for Temporary Shield Wall Was Used by 15 Households as of 9711301997-12-0101 December 1997 PNO-I-97-073:survey Identified Former Cask Wash Down Area Needing Further Characterization & Remediation within Licensee Control Area.Concrete Blocks Used for Temporary Shield Wall Was Used by 15 Households as of 971130 IR 05000213/19970051997-11-26026 November 1997 Insp Rept 50-213/97-05 on 970708-1006.No Violations Noted. Major Areas Inspected:Plant Operations,Maint Engineering & Plant Support IR 05000213/19970071997-11-0707 November 1997 Corrected Page for Insp Rept 50-213/97-07 on 970715-30 IR 05000213/19970031997-11-0707 November 1997 Corrected Pages for Insp Rept 50-213/97-03 on 970408-0707 & 0805 ML20198N2761997-10-29029 October 1997 Notice of Violation from Insp on 970703,0811-0919.Violation Noted:On 950222,individual Working on Radiation Work Permit (RWP) 1950603,received Facial Contamination & Not Sent to Be whole-body-counted ML20198N2821997-10-29029 October 1997 Insp Rept 50-213/97-08 on 970703,0811-0919.Violations Noted. Major Areas Inspected:Applied Radiological Controls Program, Contamination Control Program & Training of Personnel Relative to 49CFR172,subpart H ML20217J3981997-10-0909 October 1997 Notice of Violation from Insp on 970408-0805.Violations Noted:From 960814-970311,licensee Did Not Assure That Significant Condition Adverse to Quality Was Promptly Corrected ML20199B5731997-10-0202 October 1997 EN-97-095:on 971009,staff Intends to Issue Notice of Violation for Two Severity Level III Violations of App B, Criterion Xvi, Corrective Actions. Violations Involved Discovery of Old Plant Design Discrepancy in SWS ML20210P0101997-08-12012 August 1997 Notice of Violation from Insp on 970616-0718.Violation noted:post-dive Diver Tritium Bioassay Sample for 961108 Dive Was Not Shipped as Expeditiously as Possible for Analysis & No Preservative Was Added IR 05000213/19970061997-08-12012 August 1997 Insp Rept 50-213/97-06 on 970616-0718.Violations Noted. Major Areas Inspected:Radiological Controls Program at Cyap Station,Haddam,Ct PNO-I-97-049, on 970807,inadvertent Actuation of Halon Sys Occurred Affecting CR & Adjacent Central Alarm Station. Personnel Took Photographs of Panel of Halon Actuation Panel,Prior to Actuation.Root Cause of Actuation Evaluated1997-08-0808 August 1997 PNO-I-97-049:on 970807,inadvertent Actuation of Halon Sys Occurred Affecting CR & Adjacent Central Alarm Station. Personnel Took Photographs of Panel of Halon Actuation Panel,Prior to Actuation.Root Cause of Actuation Evaluated ML20149D6211997-06-13013 June 1997 Mgt Meeting Rept 50-213/97-03 on 970528.Areas Discussed: Actions in Response to Findings Detailed in NRC Insp Repts 50-213/96-12.96-201 & 97-01.Deficiencies Involved Implementation of Radiation Protection Program IR 05000213/19970041997-06-0303 June 1997 Physical Security Insp Rept 50-213/97-04 on 970505-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Mgt Control,Pa Detection Aids,Alarm Stations & Communication,Testing,Maint & Compensatory Measures ML20141D2621997-05-12012 May 1997 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $650,000.Violation Noted:Licensee Did Not Assure That Applicable Regulatory Requirements & Design Basis Were Correctly Translated Into Specifications ML20140G4491997-05-12012 May 1997 EN-97-035:on 970512,notice of Proposed Imposition of Civil Penalty in Amount of $650,000 Issued to Licensee.Action Based on Three Severity Level II Problems Consisting of Multiple Individual Violations ML20141F8301997-05-0808 May 1997 Insp Rept 50-213/97-01 on 970106-0407.Violations Noted.Major Areas Inspected:Licensee Operations,Engineering,Maint & Plant Support ML20141F8181997-05-0808 May 1997 Notice of Violation from Insp on 970106-0407.Violation Noted:No RCS Chemistry Samples Were Taken from 961115-970206 IR 05000213/19970021997-03-21021 March 1997 Insp Rept 50-213/97-02 on 970207-07 & 0224-26.Violation Noted.Major Area Inspected:Programs for Radioactive Liquid & Gaseous Effluent Control,Including Organization & Effectiveness of Program Implementation PNO-I-97-014, on 970227,retrieval of Contaminated Matl at Vendor Facility Made.Licensee Dispatched Survey Team, Consisting of HP Supervisor,Hp Technician & Radioactive Matl Handler to Vendor Facility to Survey & Retrieve Matl1997-02-28028 February 1997 PNO-I-97-014:on 970227,retrieval of Contaminated Matl at Vendor Facility Made.Licensee Dispatched Survey Team, Consisting of HP Supervisor,Hp Technician & Radioactive Matl Handler to Vendor Facility to Survey & Retrieve Matl IR 05000213/19960121997-02-25025 February 1997 Summary of Meeting Re Insp 50-213/96-12 on 970205 in King of Prussia,Pa to Discuss Findings Detailed in Insp Rept on 961102.Radiation Program Was Deficient in Several Areas That Resulted in Potential Exposure to Radiation ML20138J6721997-02-0404 February 1997 Notice of Violation from Insp on 961116-970105.Violation Noted:On 961127,during Preparations to Test EG2B After Jacking Engine,Operator Failed to Remove Crank Over Tool Per Step 6.2.10 Prior to Running Diesel for One Hour Test ML20138J6751997-02-0404 February 1997 Insp Rept 50-213/96-13 on 961116-970105.Violations Noted. Major Areas Inspected:Plant Operations,Maintenance, Engineering & Plant Support ML20133A5031996-12-24024 December 1996 Insp Rept 50-213/96-11 on 960921-1115.Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support ML20133A4911996-12-24024 December 1996 Notice of Violation from Insp on 960921-1115.Violation Noted:On 960924,B Residual Heat Removal Pump Failed Due to Inherent Manufacturing Defects & Marginal Design Tolerance ML20132G6211996-12-19019 December 1996 Insp Rept 50-213/96-12 on 961102-27.Apparent Violations Being Considered for Escalated Enforcement Action.Major Areas Inspected:Review of Airborne Radioactivity Event That Occurred on 961102 PNO-I-96-085, on 961204,board of Directors of Connecticut Yankee Atomic Power Co Voted to Retire Haddam Neck Nuclear Power Generating Station,After Nearly 29 Yrs of Svc.Nrc Responding to Media Inquires & Present at Press Conference1996-12-0505 December 1996 PNO-I-96-085:on 961204,board of Directors of Connecticut Yankee Atomic Power Co Voted to Retire Haddam Neck Nuclear Power Generating Station,After Nearly 29 Yrs of Svc.Nrc Responding to Media Inquires & Present at Press Conference PNO-I-96-080, on 961102,two Radiation Workers Entered Reactor Cavity & Fuel Transfer Canal Area to Inspect & Collect Debris in Preparation for Flooding Cavity to Accomplish Defueling Operation Causing Airborne Contamination1996-11-0808 November 1996 PNO-I-96-080:on 961102,two Radiation Workers Entered Reactor Cavity & Fuel Transfer Canal Area to Inspect & Collect Debris in Preparation for Flooding Cavity to Accomplish Defueling Operation Causing Airborne Contamination IR 05000213/19960101996-11-0505 November 1996 Insp Rept 50-213/96-10 on 960811-0920.No Violations Noted. Major Areas Inspected:Plant Operations,Maint,Engineering & Plant Support IR 05000213/19960801996-10-30030 October 1996 Insp Rept 50-213/96-80 on 960903-1002.Violation Noted. Major Areas Inspected:Operations,Maint,Engineering & Mgt Oversight & Controls 1999-09-01
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report No.
50-213/86-20 Docket No.
50-213 License No.
DPR-61 Licensee:
Connecticut Yankee Atomic Power Company P. O. Box 270 Hartford, CT 06101 Facility:
Haddam Neck Plant, Haddam, Connecticut Inspection at: Haddam Neck Plant Inspection conducted:
July 8 through August 14, 1986 Inspectors:
Stephen Pindale, Resident Inspector Paul D. Swetland, Senior Resident Inspector A. G. Krasopoulos, Reactor Engineer Approved by:
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Or~1e.
Pl25EC E. C. McCabe, Chief, Reactor Projects Section 3B Date Summary:
Areas Inspected:This was a routine resident inspection (141.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />) of the fol-lowing areas:
plant operations, radiation protection, physical security, fire protection, maintenance, surveillance testing and licensee events.
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Results: Two violations were identified for unauthorized operation of containment isolation valves for surveillance testing (Detail 4.3) and failure to inspect port-able fire extinguishers in the switchgear room (Detail 2.4).
An unresolved item was identified concerning the adequacy of licensee review of the safety implica-tions of installation of a heavy, unrestrained, breathing air bottle cart in the control room (Detail 2.3).
Another unresolved item was identified regarding the adequacy of reactor coolant system 3-loop flow (Detail 4.4).
Continued plant operation with equipment not fully operational was identified when operators did not take timely follow-up on indication of erratic charging pump operation (Detail 4.2).
Also, repairs to the nuclear instrumentation system resulted in indication of excessive axial flux offset at 100% power.
In this case, it appears that the positioning of the flux sensors should have been assessed before 100% power was achieved (Detail 4.8).
8609100101 860829 PDR ADOCK 05000213 G
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TABLE OF CONTENTS Page 1.
Summary of Facility Activities.......................................
2.
Review of Plant Operations...........................................
3.
Observation of Maintenance and Surveillance Testing..................
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Followup on Events Occurring During the Inspection...................
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Review of Periodic and Special Reports...............................
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Unresolved Items.....................................................
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Exit Interview.......................................................
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DETAILS 1.
Summary of Facility Activities At the beginning of the inspection period on July 8, 1986, the plant was operating at 100% power. On July 11, a load reduction was initiated due to oscillation (pressure and amperage) of the "A" charging pump.
The Technical Specification Limiting Condition for Operation for the charging pump could not be met and the unit was placed in a hot shutdown condition (mode 4) for pump. repair. On July 15, the licensee placed the unit in a cold shutdown (mode 5) to accomplish steam generator (SG) tube repairs.
The resulting 3-week unplanned shutdown came about as a result of evaluation of SG eddy cur-rent' test data (performed during the 1986 refueling outage).
On July 23, during the outage, an above limit radiation exposure of a contractor SG worker occurred. The worker received about 10% more quarterly exposure than NRC regulations permit.
(NRC Region I Specialist Inspection Report 50-213/86-22 addresses this item.) On July 26, the outage was completed.
Full power was achieved on August 6.
A subsequent load reduction to 80% power was initiated to perform in-core flux mapping to resolve a discrepancy in axial offset (AO)
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indications.
The unit returned to 100% power on August 9 and remained at 100%
power through the end of the inspection period.
2.
Review of Plant Operations The inspector observed plant operation during regular tours of the following plant areas:
Control Room Security Building
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Primary Auxiliary Building Fence Line (Protected Area)
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Vital Switchgear Room Yard Areas
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Diesel Generator Rooms Turbine Building
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Control Point Intake Structure and Pump
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Containment Building Building Control room instruments were observed for correlation between channels and for conformance with Technical Specification requirements.
The inspector observed varicus alarm conditions which had been received and acknowledged.
Operator awareness and response to these conditions were reviewed.
Control room and shift manning were compared to regulatory requirements.
Posting and control of radiation and high radiation areas was inspected.
Compliance with Radiation Work Permits and use of appropriate personnel monitoring devices were checked.
Plant housekeeping controls were observed, including control and storage of flammable material and other potential safety hazards.
The inspector also examined the condition of various fire protection systems.
During plant tours, logs and records were reviewed to determine if entries were properly made and communicated equipment status / deficiencies.
These records included operating logs, turnover sheets, tagout and jumper logs, process computer printouts, and Plant Information Reports.
The inspector observed selected aspects of plant security including access control, physical barriers, and personnel monitorin.
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2.1 The inspector reviewed the status of constantly annunciated control room alarms.
Previously identified alarms (NRC inspection report 50-213/86-16)
which remain annunciated are the pressurizer relief tank temperature and several electrical distribution system high bus voltage alarms.
During this inspection period, there were two additional continuous alarms an-nunciated in the control room: reactor coolant pump seal water high tem-perature at seal and high loop differential temperature.
The reactor coolant pump (RCP) seal water high temperature alarm was constantly an-nunciated due to an instrumentation problem with the No.3 RCP lower bearing water temperature monitoring channel.
The alarm was previously annunciated before the steam generator tube plugging outage, when the resistance temperature detector (RTD) for the No.3 RCP lower bearing water temperature was replaced.
However, this alarm came in again.
In-strument maintenance is continuing to troubleshoot the channel.
Reactor coolant pump seal water return flow and seal differential pressure are being monitored to v3rify that the high reading is due to instrumentation error as opposed to being a bona fide indication. On August 12, the an-
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nunciator was bypassed to eliminate the possibility of masking actual or new plant conditions.
No unacceptable conditions were identified by inspector review of this alarm.
The inspector questioned the presence of the high loop differential tem-perature (delta-T) alarm. While operators knew the alarm setpoint and the current delta-T readings, the reason for the high delta-T annunciator was not known.
The licensee stated that the delta-T alarm setpoints were raised for cycle 14, due to the new reactor coolant system (RCS) RTOs, to 50(+0,-2) degrees F.
Delta-T readings indicated approximately 48-49 degrees F.
There is no Technical Specification upper limit on loop delta-T.
The variable low pressure scram (VLPS) uses Tave and delta-T inputs to calculate an RCS pressure at which a reactor trip will occur (to prevent departure from nucleate boiling).
The purpose of the high delta-T alarm is to warn operators that, while significant margin exists to the VLPS reactor trip, the cause of the high delta-T should be inves-tigated.
The inspector questioned whether the delta-T alarm was related to the additional steam generator tube plugging performed since the delta-T alarm was not annunciated during operation prior to the shutdown.
The licensee indi ated that this was not the case, and that the delta-T indicator configuration was the cause.
However, the licensee performed a four loop flow test (SUR 5.3-45) on August 12 to determine RCS flow following the SG tube repair and to aid in troubleshooting this problem.
No unacceptable conditions were identified by the licensee or by the inspector's review of this alarm condition.
This matter is further ad-dressed in Detail 4.4 of this report, and the status of unnecessary alarms will continue to be reviewed during routine inspections.
2.2 The inspector attended a Plant Operations Review Committee (PORC) meeting on July 31, 1986.
Technical specification 6.5 requirements for required member attendance were met.
The meeting agenda included procedural changes, proposed changes to the Technical Specifications, and field changes to design change packages.
The meeting was characterized by
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frank discussions and questioning of the proposed changes.
In particular, PORC consideration was given to assure clarity and consistency among procedures.
Items for which adequate review time was not available were postponed to allow committee members time to review and comment.
Dis-senting opinions were encouraged.
The inspector had no further comments.
2.3 During an NRC team inspection of the licensee's fire protection program in June 1986, the inspector observed a cart with breathing air bottles (compressed gas cylinders) within the control room confines. The cart is made with swivel wheels, weighs more than 1500 pounds and was found unrestrained behind the emergency diesel generator control cabinets.
This installation is of concern because the unconstrained mass of the cart and bottles are a potential hazard to control room equipment and personnel.
The inspector asked the licensee for the safety evaluation performed in accordance with 10 CFR 50.59, and the licensee stated that no such analysis was performed.
There was no available written safety evaluation documenting why this installation does not pose an unreviewed safety question.
The licensee subsequently moved the breathing air bottles to a remote location, within the confines of the control room, and the cart was provided with curved wooden blocks at the wheels to restrict motion.
This item is unresolved pending further NRC and licen-see assessment of safety implications of this case (UNR 213/86-20-01).
2.4 On August 8,1986, while performing a routine plant walkthrough, the in-spector observed that several portable fire extinguishers (PFEs) were not inspected in accordance with PMP 9.5-120 (Portable Fire Extinguisher Inspection).
PMP 9.5-120 requires that all station PFEs be inspected monthly. All PFEs located in the switchgear room were last inspected, as logged on the PFE monthly inspection status tag, on June 26, 1986.
Failure to inspect the switchgear room PFEs in July 1986 in accordance with PMP 9.5-120 is a violation (VIO 213/86-20-02).
2.5 The monthly inspection status of the PFEs in the control room indicated that the last three PFE inspections were performed on 5/27/86, 6/5/86, and 7/24/86.
Westinghouse Standard TSs allow a 25% maximum extension of any surveillance interval, and define monthly as at least once per 31 days.
However, Haddam Neck TS 1.21 (Frequency), defines monthly as
"At least once per month".
Nonetheless, performance of inspections at the end of one month and again at the beginning of the next month does not appear to meet the intent of the monthly inspection frequency.
From the three dates on the monthly inpection status tags on the control room PFEs, well over 30 days passed between the June and July inspections.
The inspector brought this discrepancy to licensee management attention.
Licensee action on this matter will be reviewed by NRC during a subse-quent routine inspection.
3.
Observation of Maintenance and Surveillance Testing The inspector observed various maintenance and problem investigation activi-ties for compliance with requirements and applicable codes and standards, QA/QC involvement, safety tags, equipment alignment and use of jumpers, per-
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sonnel qualifications, radiological controls, fire protection, retest, and reportability. Also, the inspector witnessed selected surveillance tests to determine whether properly approved procedures were in use, test instrumenta-tion was properly calibrated and used, technical specifications were satisfied, testing was performed by qualified personnel, procedure details were adequate, and test results satisfied acceptance criteria or were properly dispositioned.
The following activities were reviewed:
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Maintenance of P-18-1A, P-18-1B Charging Pump (CMP 8.5-141)
Component Cooling Water to Neutron Shield Tank Cooler, P-60 (SUR 5.7-93)
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Operation of the Flux Map System (ENG 1.7-28)
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Steam Generator Tube Repair (VP-200)
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NIS Coaxial Extension Cable Replacement (PMP 9.2-9)
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Four Loop Reactor Coolant Flow Measurement (SUR 5.3-45)
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3.1 During the 1986 refueling outage, component cooling water (CCW) system containment isolation check valves failed their respective type C leak rate tests due to silt build-up in the CCW system.
Following installa-tion of a slip-stream filter in the CCW system and a subsequent system realignment which allowed silt accumulation in the CCW system, the valves again failed the test.
The valves involved are CC-CV-885 (CCW supply to neutron shield tank heat exchanger-SUR 5.7-93) and CC-CV-721 (CCW supply to reactor coolant pump seal thermal barrier-SUR 5.7-51).
Fol-lowing cleaning of the valves, both met their respective acceptance cri-teria.
To assure that the CCW valves remained operable throughout the operating cycle, the licensee committed to test these valves during plant shutdowns.
During the outage in July 1986, the licensee performed the committed leakrate tests. On July 19, 1986, the licensee performed leakrate testing on CH-RV-332 (SUR 5.7-60) in addition to CC-CV-721 and CC-CV-885.
Although CC-CV-885 passed as witnessed by the inspector, both CH-RV-332 and CC-CV-721 failed to meet their respective inservice in-spection (ISI) acceptance criteria.
Together, they exceeded the Techni-cal Specification 4.4 (Containment Testing) limit for containment pene-tration isolation valve leakage.
The licensee made the necessary NRC notification via ENS.
Subsequent investigation revealed that the cause of both test failures was backflow through test boundary valves.
Upon ensuring that all test boundary valves were fully closed, the valves were retested satisfactorily without any valve rework.
The licensee has again committed to perform leakage rate testing of CC-CV-721 and CC-CV-885 during the next cold shutdown, thereby assuring valve operability and slip-stream filter effectiveness.
These valves, and others as deemed appropriate by the licensee, will be placed on the plant shutdown work list.
The conduct and results of these tests will be followed by the resident inspectors during a subsequent routine inspection and for re-solution of unresolved item UNR 213/86-06-0.
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4.
Followup on Events Occurring During the Inspection 4.1 ~ Licensee Event Reports (LERs)
The following LERs were reviewed for clarity, accuracy of the description of cause, and adequacy of corrective action.
The inspector determined whether further information was required and whether there were generic implications. The inspector also verified that the reporting require-ments of 10 CFR 50.73 and Station Administrative and Operating Procedures had been met, that appropriate corrective action had been taken, and that the continued operation of the facility was conducted within Technical Specification Limits.
86-31 -- Failure of the Safety Injection Recirculation Isolation Valve to the RWST (Detailed in NRC Inspection Report 50-213/86-16)
86-32 -- Drift of Dropped Rod Load Runback Setpoint of Nuclear Instru-mentation 86-34 -- Three Loop Flowrate Measurement (Detail 4.4)
86-35 -- Steam Generator Tube Eddy Current Testing Undefined Signals (Detail 4.5)
86-36 -- 1A Charging Pump Shaft Fallare (Detail 4.2)
4.2 On July 7, 1986, the plant was operating at 100% power when the operating charging pump (A) pressure and amperage indications became erratic, but remained within specification.
At 4:00 p.m., the "A" charging pump was secured and the "B" charging pump was started.
Charging flow and related system parameters returned to normal and plant operations were stabilized.
Concurrent with shifting the charging pumps, the positive displacement metering pump relief valve was isolated at 4:15 p.m., as leakage past that valve was evident.
It was initially suspected that leakage past the metering pump relief valve may have caused the erratic "A" charging pump indications; the metering pump relief valve is connected to the chemical and volume control system (CVCS) common discharge piping.
At 6:30 p.m.,
test operation of the "A" charging pump again revealed pres-sure and amperage surges.
The metering pump was subsequently isolated for maintenance on the relief valve.
Inspection of the "A" charging pump was planned for the following morning, with both the "A" and "B" charging pumps considered operable since indications were within specification.
On July 8,1986, at approximately 11:10 a.m., "A" pump inspection re-vealed that the pump shaft had sheared just outside the pump casing.
While the pump would still run and charge water to the system, it was declared inoperabl.-.
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Technical Specification (TS) 3.5, related to CVCS, requires either two charging pumps or one metering pump and one charging pump to be operable while the reactor is critical.
Therefore, with only one charging pump operable, the plant immediately initiated a controlled load reduction as required by 10 CFR 50.36.
The investigation of the metering pump relief valve leakage determined
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that the leakage past the valve was within limits, but the relief valve
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setting was noted to be incorrect.
The improper relief valve setting was corrected before the metering pump and relief valve were returned
to service. Maintenance on the metering pump relief valve was completed at 12:00 noon.
With the metering pump and associated piping operable,
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the load reduction was terminated at approximately 90% power.
The unit was then returned to 100% power.
Administrative TS 3.6.(Core Cooling Systems) requires that two charging l
pumps be operable in modes.1-3. The action statement for the associated i
limiting condition for operation allows continued operation for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> i
with one charging pump operable.
On July 11, 1986, it was evident that the "A" charging pump could not be repaired within the time allotted;
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therefore, a controlled plant shutdown was initiated at 3:00 a.m. on July 11, and the necessary notifications were made to NRC and the state.
The
"B" charging pump remained operable throughout the event, with the metering pump also operable approximately one hour after the "A" charging pump problem was declared inoperable. After reaching hot shutdown, a
corporate decision was made on July 15, 1986, to place the unit in a cold
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shutdown condition for steam generator tube repair (Detail 4.5).
The inspector questioned the licensee why the metering pump was tagged out of service on July 7 at 6:53 p.m., while maintenance was not planned until the following day.
This question included concerns about tagging out a second pump (metering) when the operability of the first pump ("A" i
charging) may have been questionable.
The licensee stated that they be-lieved the "A" charging to be operable at the time because cf attribution-of the oscillations to the metering pump relief valve.
However, the "A"
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charging pump was test run at 6:30 p.m., after the relief valve isolation, and erratic operation still occurred.
Further, no oscillations occurred with the "B" pump operating and the "A" pump secured.
The suspect "A" charging pump was not further addressed for approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />.
Prompt investigation could have identified the problem earlier. The in-spector also questioned whether the metering pump should have been tagged out of service when erratic "A" charging pump indications existed.
Previous charging pump failures of a similar nature have occurred.
On May 1, 1985, a charging pump shaft failure occurred at a point on the i
shaft on the threaded portion on which a locking nut is installed to i
compress the 13 stages of the pump.
The July 8, 1986 failure was also
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in the threaded portion, with the fracture point on a different thread along the shaft.
Causal indications of both failures, upon inspection,
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were of high cyclic fatigue.
Inspector concerns on this matter include identification of the root cause of.the failures and establishment of measures to prevent-further recurrence.
A representative from the pump manufacturer ( acific) was sent to the site to assist the plant staff in identification of the cause of the
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event and to establish measures to be taken;during assembly and instal-o lation of the repaired pump.
The licensee had a spare pump shaft and
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impellers readily available on site.
No significant damage was incurred to the 13 stage pump.
The licensee and company representative formulated s
additional precautionary steps in the pump assembly and installation'
procedure. These included dye penetrant testing of the diffusers and wear rings, blue checks on the threaded portion of-the threaded section of the shaft (to ensure proper-locknut seating),1 hand-fitting of.all mating surfaces which transmit forces through the. shaft (to reduce the-likelihood of inducing high stress regions along the shaft), revised balancing processes for rotating components, and greater attention to detail throughout the reassembly process.
During a torque test of the shaft and locking nut, galling of the rotating element and locking nut occurred and the locking nut was' cut off.
Blue checks were again per-
formed as was a revised torque test.
The pump was satisfactorily re-
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paired and tested on July 27, 1986.
Additional measures taken by the licensee include submittal of a project assignment (PA) request to investigate the pump design as-applicable to its. intended use and to evaluate the history of the pump's previous operational data.
The licensee hopes to gain information on whether the
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processes used for the charging pump reassembly and installation were adequate to prevent recurrence.
The PA request also includes a proposal
to investigate whether sufficient margin exists in the current pump de-sign.
With respect to the improper relief valve setpoint, licensee' review of the procedure used to set the relief valve indicated that the procedure
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did not require a setpoint verification with the-setpoint control log.-
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The specific procedure (PMP 9.5-114) is to be changed'to address this
concern.
Additionally, to address whether this is a generic concern, all safety-related relief valve setpoints will be verified.
The comple-
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tion of this review, the PA, and in plant evaluation'results will be reviewed under the routine inspection program.
4.3 On July 8, 1986, the licensee identified that, during surveillance test SUR 5.1-4, four manual containment isolation valves were opened for the i
l test-(SI-V-863 A/B/C/D). These four 1/2" manual loop' recirculation valves are normally locked closed during power operation, and are located i
outside containment.
They serve as the second. isolation boundary in the containment isolation system.
The licensee's~ investigation was to de-
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termine the reasons for opening the HPSI system common recirculation valve (SI-HCV-1881) whose failure led to the loss of both HPSI trains, I
and was addressed in NRC inspection report 50-213/86-16.
Upon discovery
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of the opening of.the four isolation valves, it was determined that the valves have been opened monthly for this surveillance test since 1966.
The primary reason for opening the valves is to equalize boron concen-tration and prevent boron stratification in the HPSI discharge piping.
The cpening of SI-863A/B/C/D violates Containment Integrity (Technical-Specification 3.11) as defined in TS 1.8.
Immediate corrective actions-include providing administrative controls to maintain SI-V-863 A/B/C/D valves locked closed until procedural. changes have been made to comply-with TS. The inspector questioned whether administratively locking 3'
a closed the valves had any impact on HPSI system design bases.
On a steam line break accident,_the integrated Emergency Core Cooling System pro-vides water with specified. concentrations of boric acid in solution to
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the reactor coolant system. The licensee stated that, above 32 degrees
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F, the boric acid would not precipitate out of solution.
The licensee t
also stated that the design of the HPSI system is such that all outside piping is insulated and electrically heat traced, further reducing the likelihood of borated water delivery problems.
Similar TS violations have occurred previously on other containment
isolation valves: operation of manual isolation valve SA-V-413 was iden-
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tified in NRC inspection report 50-213/86-08; and post-accident sampling system (PASS) valve operations were identified in NRC inspection report
50-213/84-14.
As indicated by the repetitive nature of the violations, l
the individual corrective actions have not resulted in correction of the i
underlying cause(s).
This concern was discussed with licensee management on August 8, 1986.
The licensee included, in the long term corrective
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' Y to be manipulated. The current Haddam Neck TSs do not allow for manipu-lation of these containment isolation valves when the reactor is critical.
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As indicated by the final corrective action for the PASS valve problem, I
where good cause is shown, TS amendments can be granted to allow manipu-E 1ation of' containment isolation valves under administrative control.
B The inspector will review the licensee's corrective action plan and its implementation'at a later date.
The licensee's failure to adhere to current TS limits regarding SI-V-863A/S/C/D constitutes a violation (VIO 213/86-20-03).
i 4.4 On July 11, 1986, while in Mode 3, the licensee identified problems with
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the 3-loop reactor coolant system (RCS) flow test (ENG 1.7-48) which was performed on June 24, 1986.
The current safety analyses assume a minimum
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f 3-loop flow rate of 207,000 gpm.
The minimum flow measured during the
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test was 202,520 gpm, about 2.4 percent less than the safety analysis minimum.
Upon evaluation of the test results, the licensee made the
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g necessary notification to NRC and the State.
Currently, there are no Technical Specifications (TS) for the required 3-loop flow rate.
For the short term, the licensee prohibited 3-loop operation in Mode 1 via temporary procedure changes86-471 and 86-472.
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The licensee also performed a 4-loop flow test (SUR 5.3-45) on May 29, 1986.
These 3-loop and 4-loop RCS flow rate tests were the first actual flow tests performed since initial startup testing.
The acceptance cri-
-terion for RCS. flow rate, based upon mode 1 steady state operation with-four reactor coolant loops operating, is 257,000 gpm. 'TS 3.20 (RCS Flow, Temperature:and Pressure) specifies this minimum 4-loop RCS flow rate for mode 1.
The minimum 4-loop flow rate, as measured in SUR 5.3-45, was 267,067 gpm.
This value was reduced to 259,154 gpm when a 2.963 percent uncertainty factor was incorporated.
That yields a margin of 2154 gpm or 0.8 percent of the TS 3.20 limit.
The present licensee established routine frequency for RCS flow testing is once each refueling.
Since 126 Steam Generator (SG) tubes were
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plugged during the July 1986 outage, the licensee performed an additional 4-loop flow test on August 12, 1986 after plant startup from the tube-plugging outage.
The test results indicated a 0.5 increase in flow rate during preliminary licensee review.
The licensee committed to re-analyze 3-loop flow to determine if suffi-cient margin exists in the safety analyses to justify 3-loop operation.
Also, the 4-loop flow test final evaluation is to include a determination of the cause of the high differential temperature _(delta-T) alarm which was annunciated following plant startup from the outage (Detail 2.1).
This item remains unresolved pending these actions (UNR 213/86-20-04).
4.5 During the 1986 refueling outage, the licensee performed eddy current testing (ECT) of all Steam Generator (SG) tubes, except for 4 tubes in SG #4.
ECT data identified many tubes (575) with undefined signals (UDSs)
in the tube sheet-area.
A SG U-tube was removed from SG #2 for destruc-tive testing to aid in characterization of the SG tube UDSs. The de-structive test indicated that the UDSs were multiple tube cracks initi-ated inside the tube.
The cause was attributed to primary side stress corrosion.
There were a total of 575 SG tubes with UDS indications, with the crack indications ranging from 20-100% through wall.
The licensee notified the resident inspectors and NRC Licensing of the preliminary findings on June 19, 1986.
The licensee submitted a letter to NRC, dated June 20, 1986, which documented the safety basis for continued operation, concluding that the potential flaws did not represent an undue risk to the public health and safety.
A June 26, 1986 NRC safety evaluation report (SER) concurred with the licensee's position on maintenance of tube structural integrity.
The SER~ established a corrective action plan submittal date of September 30, 1986.
During further licensee review and evaluation of the preliminary ECT findings, 35 of the 575 tubes were assessed as acceptable.
Therefore, 540 SG tubes remained with UDSs ranging from 20-100% through wall.
The licensee performed analyses from which interim SG tube structural ac-ceptance criteria were established.
The analyses assumed that the flaws were in the rolled region of the tubes.
The analyses showed that one inch of sound tube-to-tubesheet roll provides the frictional resistance
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required to withstand normal operating, test, and postulated accident loads.
Further analysis demonstrated that, with no defect in the uppermost one inch of the rolled region, any crack below the one-inch point would result in a leakage well below the Technical Specification (TS) limits and structural integrity would be maintained. Therefore, the licensee's proposed interim structural acceptance criteria were 1) no UDSs in the uppermost one inch of hard roll; and 2) any size UDS defect is acceptable below the uppermost one inch of hard roll.
Based upon this information and review of the ECT results, the licensee developed a list of 119 SG tubes that did not satisfy the criteria.
On July 15, 1986, licensee corporate management decided to place the unit in cold shutdown to plug these 119 tubes.
Three of four SGs were affected (SG #2,#3,#4).
The NRC was informed verbally of this action.
Formal notification was made by letter dated July 24, 1986.
The licensee also decided to plug one SG #2 tube with a 55% through wall defect that was inadvertantly left unplugged during the 1986 refueling outage.
The licensee also examined previous ECT results of the four SG #4 tubes which were not inspected during the 1986 refueling outage.
Review and evaluation of previous ECT results indicated that there were no UDSs present.
The licensee has determined that UDSs do not readily propagate and therefore decided not to plug these 4 tubes.
The final plugging list included 120 tubes.
The tubes were plugged in accordance with VP-200.
System hydrostatic tests were then performed to verify the adequacy and leak tightness of the mechanical tube plugs.
The option existed to remove the mechanical plugs and install welded plugs if tube leakage occurred following initial tube repair.
No welded plugs were required.
Six tubes not on the plugging list were also plugged.
Two tubes were inadvertently plugged in SG #4 due to vendor error.
Another two tubes, in SG #2, were plugged because of measurable leakage during the hydrostatic test.
A third SG
- 2 tube were plugged because of boric acid deposits around and within the tube end.
(Additional ECT on these three tubes indicated tube cracks in the roll transition region of one tube.
The other two tubes did not show any crack indications.) A fourth tube in SG #2 was plugged because special additional ECT during the 1986 refueling outage indicated a flaw in the roll transition zone.
Other 1986 Refueling Outage ECT results were sampled.
No further discrepancies were found.
All SG tube repairs and testing were completed on July 26, 1986.
The NRC reviewed the information and analyses provided in the licensee's
July 24,1986 submittal in support of the interim acceptance criteria.
The NRC subsequently issued a safety evaluation report (SER), dated July 30, 1986, which concluded that there was reasonable assurance that the potential flaws in the rolled region of the 540 SG tubes would not result i
in catastrophic failure in the near term and that any propagation of l
existing flaws will be revealed by an increased primary-to-secondary leakage rate, which is limited by TS.
(As of the end of the inspection l
period, daily measurements indicated no primary to secondary system
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leakage.) The SER further specified that the licensee complete the UDS et decion to specify final acceptance criteria by the previously speci-
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fied September 30, 1986 submittal date, and that a license amendment for the appropriate final acceptance criteria be submitted by October 31, 1986.
4.6 On July 17, 1986, the inspector was notified of a potential problem with the power operated relief valves (PORVs). The PORVs are air-operated and function to limit reactor coolant system (RCS) pressure transients and limit actuation of the pressurizer code safety valves.
The automatic lift setpoint of the two air-operated PORVs is 2270 psig.
A high pres-surizer pressure reactor trip occurs at 2300 psig, and the three pres-surizer code safety valves lift at 2485, 2535, and 2585 psig, respec-tively.
In 1977, the PORVs were replaced with new valves as a result of seat leakage and operability problems.
The new PORVs were initially procured for Millstone Point Unit 3 and have approximately three times more relieving capacity than the original PORVs.
The 2270 psig setpoint did not change with the PORV replacement.
The associated plant design change request (PDCR), No. 248, included a safety evaluation which de-termined that the change could be safely implemented without adversely affecting plant design bases.
On July 17, 1986, the licensee issued a plant information report which identified that, during a loss of load (LOL) transient, the current PORV setpoint may allow liquid to be discharged from the pressurizer code safety valves.
The current LOL transient analysis assumes a high pres-surizer pressure reactor trip to occur within 7 seconds of the transient, with credit taken for the operabiljgy o( thg N ig; g M d g;jg, The inspector expressed concern about using the 2270 psig setpoint with the higher capacity PORVs.
Doing so may delay the high pressurizer pressure reactor trip, reducing the margin to departure from nucleate boiling (DNB).
In response, the licensee and NRC conducte'd'a conference call regarding the setpoint.
NRC questioned why the setpoint should not be changed prior to plant startup, since the higher capacity PORVs, when used with the original setpoint, seem to invalidate the facility de-scription and safety analysis (FDSA) chapter 10 assumptions.
The licensee acknowledged that the PORV setpoints may need to be raised to a value greater than the 2300 psig reactor trip but did not consider it necessary to change them before plant startup.
They further stated that the problem was discovered during the FDSA Chapter 10 reanalysis, during the 1986 refueling outage, and that additional time was required to establish, through analysis, the appropriate setpoint.
They presented arguments to justify postponing the setpoint change, including: 1) the operating moderator temperature coefficient as defined in the cycle 14 reload package is more negative than that assumed in the FDSA (this represents an increase in DNB margin), and 2) the plant normally operates with the PORV block valves closed.
Since the block valves receive the same signal to open as do the PORVs (2270 psig) and require approximately 15 seconds to fully cpen, the reactor would have reached the 2300 psig reactor trip before the PORVs (1.5 second opening time) would have been
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able to delay the' trip.
The licensee then committed to perform an in-ternal safety evaluation for justification of continued operation.
The safety evaluation was reviewed and accepted by PORC on July 31, 1986.
The licensee implemented administrative controls to assure that the block valves remain closed during operation.
The analysis for the setpoint change _is anticipated to be completed by approximately August 19, 1986.
The inspector will follow the implementation of the setpoint change under the routine inspection program.
4.7 On July 25, 1986, it was discovered that the licensee's emergency noti-fication system (ENS) was out of service.
ENS provides communication channels among the control room, technical support center, NRC resident office and NRC Emergency Operations Centers.
All necessary notifications were made.
On July 29, 1986, following troubleshooting of the ENS by the local telephone company, voices could faintly be heard on the system.
The telephone company is currently investigating the problem. While ENS remains out of service, daily functional checks are performed on the commercial telephone service to the NRC Operations Center in lieu of performing the daily ENS phone checks.
This will continue until ENS service is restored.
The inspector will follow the daily commercial phone checks and ENS repair status during routine inspection.
4.8 On August 6, 1986, after reaching 100% power from the steam generator tube plugging outage, the licensee discovered that the electrical cur-rents associated with three of four nuclear instrumentation system (NIS)
axial offset (AO) channels were inconsistent.
The fourth channel was out of service as permitted by plant technical specifications (TS).
The three A0 channels were investigated because the NIS channel No. 32 A0 channel was in an alarmed condition (negative A0).
Prior to the inves-tigation, the licensee suspected that, during excore detector cable re-placement and sleeving, the detectors were not reinserted in their exact position, creating different nuclear flux readings.
Following the main-tenance, the excore detectors were inserted into their respective hori-l zontal chambers.
Since the detectors monitor a limited area of neutron l
flux (due to horizontal vice vertical alignment), a small offset in their l
placement can cause a change in the flux reading currents.
The unit reduced power to 80% to perform in-core flux mapping to determine whether
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A0 conditions actually did exist in the core and to generate updated i
correlations between incore and excore readings.
The licensee completed
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the incore flux map and associated evaluations and adjustments subse-quently achieved 100% power on August 9.
The incore flux map indicated that the linear heat generation rate were well within acceptable limits.
i In-core flux maps were performed to verify the new correlations at 100%
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No additional problems were encountered.
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TS 3.18, Power Distribution monitoring and Control, specifies that ex-
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core-incore correlation be checked after a major change in excore in-l strumentation using results of incore flux measurements.
As the excore l
detector cable replacement was not viewed as a major change in the system, the checks were not performed.
To prevent recurrence, the licensee com-
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mitted, for all maintenance procedures which affect excore instrumenta-tion, to incorporate a notification to reactor engineering (RE) before any maintenance.is performed.
Therefore, RE can make a determination-as to the effects of the maintenance on the incore-excore correlations.
.The inspector had no further questions.
Implementation of the procedural changes will be reviewed during subsequent-routine inspection.
4.9 On August 8, during a severe electrical storm,.the licensee's security computer system experienced lightning induced problems.
The problems included minor loss of system functions for a short period of time.
Im-mediate corrective actions satisfactorily compensated for this loss.
Normal functioning was restored within nine minutes.
The NRC resident inspector was. informed at the tima of the event.
The event was input
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to the Security log system, and was not immediately reportable to NRC.
The inspector had no further questions.
5.
Review of Periodic and Special Reports Upon receipt, periodic and special reports submitted pursuant to Technical Specification 6.9 were reviewed.
This review verified that the reported in-formation was valid and included the NRC required data; that test results and supporting information were consistent with design predictions and performance specifications; and that planned corrective actions were adequate for resolu-tion of the problem.
The inspector also ascertained whether any reported in-formation should be classified as an abnormal occurrence.
The following periodic reports were reviewed:
-- Monthly Operating Report 86-06, plant operations from June 1-30, 1986.
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No unacceptable conditions were identified.
6.
Unresolved Items Unresolved items are matters about which more information is required in or. der
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to determine whether they are acceptable.
Unresolved items identified during
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this inspection are discussed in Paragraphs 2.3 and 4.4.
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7.
Exit Interview
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During this inspection, meetings were held with plant management to discuss the findings.
No proprietary information related to this inspection was identified.
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