IR 05000289/1986005
ML20211C929 | |
Person / Time | |
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Site: | Three Mile Island |
Issue date: | 05/29/1986 |
From: | Blough A, Conte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
To: | |
Shared Package | |
ML20211C898 | List: |
References | |
50-289-86-05, 50-289-86-5, NUDOCS 8606120433 | |
Download: ML20211C929 (36) | |
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U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Report N /86-05 Docket N License N DPR-50 Priority -- Category C Licensee: GPU Nuclear Corporation Post Office Box 480 Middletown, Pennsylvania 17057 i Facility: Three Mile Island Nuclear Station, Unit 1 Inspection At: Middletown, Pennsylvania Inspection Conducted: March 7, 1986 - April 11, 1986 Inspectors: R. Conte, Senior Resident Inspector (TMI-1)
D. Johnson, Resident Inspector (TMI-1)
A. Krasopoulos, Reactor Engineer, Region I D. LeQuia, Radiation Specialist, Region I R. McBrearty, Reactor Engineer, Region I J. Rogers, Resident Inspector (TMI-1)
A. Weadock, Radiation Specialist, Region I F. Young, Resident Inspector (TMI-1), Region I Reporting Inspector: 8 T 2P-JC fr R. Conte,6enior Resident Inspector (TMI-1) Date Approved By: M M 7-8(,
A. Blouffi, Chief Date Reactor Projects Section No. lA Division of Reactor Projects Inspection Summary:
Resident and region-based NRC staff conducted routine safety inspections (440 1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />) of power operations, focusing on plant and personnel performance. Spe-cifically, items reviewed in detail in the operation and maintenance area were:
outage preparation and shutdown /cooldown; significant performance appraisal team findings; and local leakrate testing. Special focus occurred on: the ;
eddy current testing of steam generator tubes; feedwater nozzle weld cracking; and significant events of March 15, 22, and 24-25, 1986. Other review areas included: fire protection program -- fire brigade training; outage radiation protection; and licensee action on an emergency diesel generator 10 CFR 21 ;
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Inspection Results:
Overall, licensee management took many initiatives to prepare for and control outage work impact on control room personnel. Licensed. operators continued to exhibit overall professionalism and demonstrated detailed knowledge of plant design and outage work status. However, during the transition from operations to outage conditions, the degasification event pointed out the need for enhanced attentiveness by technicians and operators to special evolutions. Also, the licensee apparently failed to properly survey or evaluate conditions in the reactor building for the buildup of radioactive iodine; this failure was con-trary to regulatory requirements (paragraph 3.4.5.2). Contributing to that event were communication factors during the high pace of activities on March 24-25, 1986. Once the iodine problem was recognized, licensee corrective action and dose evaluation methodologies were quite goo ! .There was also a failure to properly post a radiation area (paragraph 6.2.2).
l The implementation of the licensee's radiation protection program was generally
- proper, except as noted abov Plant and personnel performance for the reactor trip event of March 15, 1986, was essentially as expected. The licensee properly performed post-trip evaluations and identified followup action ^
Steam generator tube eddy current testing was properly conducted and controlled with respect to oversight of vendor activitie Proper corrective actions were planned and implemented for the emergency feedwater nozzle weld crack problem.
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Licensee planned followup actions on the emergency diesel generator 10 CFR 21 report are appropriate to the circumstance I a
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DETAILS 1. Introduction and Overview 1.1 NRC Staff Activities The overall purpose of this inspection was to assess licensee activities for the transition from power operations to cold shut-down outage activities as they related to reactor safety, worker radiation protection, and fire protection. Within each area, the inspectors documented the specific purpose of the area under review, scope of inspection activities and findings, along with appropriate conclusions. The inspector made his assessments by reviewing infor-mation on a sampling basis through actual observation of licensee activities, interviews with licensee personnel, measurement of radiation levels, independent calculation, and selective review of applicable document .2 Licensee Activities From the beginning of the inspection period to March 21, 1986, the licensee operated TMI-1 at full power, except for the reactor trip of March 15, 1986 (sae paragraph 3.2). The primary licensee focus during that period was preparations for the eddy current outage testing which started over the weekend of March 22-23, 1986. The reactor trip was due to a secondary plant trip caused by a combination of procedural weaknesses and operator actions during the tran:fer of inservice coolers for the main lube oil syste The remainder of the period involved cold shutdown and reactor vessel drained down conditions to support eddy current testing (ECT) of a sampling of steam generator tubes. Initial bubble and drip test of all tubes showed very good results with no indication of leaking tubes. At the end of the inspection period, ECT data collection was essentially complete and licensee analysis was proceedin )
l Two events occurred during the initial stage of the outag There was a noble gas release during RCS degasification on March 22, 1986, l which resulted in the declaration of an unusual event (see paragraph j 3.3). Also, there was a buildup of radioactive iodine and lesser '
significant contaminatica incidents on or about March 24, 1986, with the RCS vented to the RB etmosphere (see paragraph 3.4). The iodine buildup was due, in part, to inadequate plannin l l
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2. Plant Operations 2.1 Scope of Review The NRC resident inspectors periodically inspected the facility to determine the licensee's compliance with the general operating requirements of Section 6 of the Technical Specifications (TS) in the following areas:
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review of selected plant parameters for abnormal trends;
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plant status from a maintenance / modification viewpoint, including plant housekeeping and fire protection measures;
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control of ongoing and special evolutions, including control room personnel awareness of these evolutions;
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control of documents, including logkeeping practices;
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implementation of radiological controls; and,
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implementation of the security plan, including access control, boundary integrity, and badging practice Enhanced resident office coverage at this facility enabled the inspectors to more fully assess the adequacy and effectiveness of performance of operating activities to determine that:
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operators are attentive and responsive to plant parameters and conditions;
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plant evolutions and testing are planned and properly authorized; ,
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procedures are used and followed as required by plant policy;
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equipment status changes are appropriately documented and communicated to appropriate shift personnel;
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the operating conditions uf plant equipment are effectively monitored and appropriate corrective action is initiated when !
required;
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backup instrumentation, measurement, and readings are used as appropriate when normal instrumentation is found to be defective or out of tolerance;
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logkeeping is timely, accurate, and adequately rsflects plant activities and status; l
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operators follow-good operating practices in conducting plant :
operations; and, '
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operator actions are consistent with performance-oriented trainin The inspectors focused their attention on the areas listed belo General / Operations
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Control room operations during regular and backshift hours, including frequent observation of activities in progress, and periodic reviews of selected sections of the shift foreman's log and control room operator's log and other control room daily logs
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Followup items on activities that could affect plant safety or impact on plant operations
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Areas outside the control room
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Selected licensee planning meeting Plant shutdown and cooldown t
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RCS degasification
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Instrument air walkdown on Emergency Feedwater (EF) flow control valves
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EF flow indication alignment (indicator to transmitter alignment)
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EF standby status I
Maintenance I
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Testing of motor-operated valves
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"A" battery bank cell replacement ;
Surveillance i
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Local leakrate testing of the Reactor Building penetrations
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EF surveillance testing
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Radiological Controls-
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Locked high' radiation doors
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Radiation Work Permitsposting i
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Weekly survey maps 2.2 Findings 2. General -
T J Licensee manag'ement continued their presence and involve-ment.,in da,ily activitie t Good preparation and preplanning was poted for operatiqnal aspects of the scheduled eddy current outag The work list and scope of work to be pepformedwasaggressivebutachievablewithinthetime limit established by the licensee. During the weekend i
prioito :the start of thg outage, work appeared orcanized
[ Equipment was staged and made ready
'and"well contro1]e fo'r entry ,into radiologically controlled areas. A separate control point wi.th two nealth physics computer terminals for reactor building (RB) entries was established in readiness for.the substantial Monday morning work force a rri val .
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Licensea operators remained professional in performing
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.,their duties, especially in control room activitie The control room operators were knowledgeable of plant status
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from a work activities viewpoint in addition to being knowledgeable of detailed reactor plant conditions. Shift
foremen were additionally stressed by interfaces with the work force for equipment control measures, but they remained in overall control and those pressures were somewhat alle-viated by management: 'For instance, additional "off-shift"
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, shift supervisors _were. assigned to be coordinators of activities.in various locations; such as, the reactor building. Also, a standard set of cold shutdown " tag outs" were made ready prior to the start of the outage to avoid
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numerous case-by-case equipment control measures and hand-
- ling by the on-shift shift forema There were two events that occurred at the start of the j' 'utage. Details are addressed in' paragraphs 3.3 and o
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It appears that the licensee could have better anticipated (by calculation and/or survey) the quantities of iodine
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released from the reactor coolant system during their preparatory effort Further, personnel could have paid
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closer attention to detail during the degassing operation
, at the chemical sampling room to avoid the actuation of the relief valve and subsequent release of noble ga ?- .
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2. Performance Appraisal Team Significant Findings During this inspection period, the resident inspectors were also involved in and supported the Performance Appraisal Team (PAT) Inspection (No. 50-289/86-03). The primary functional areas followed by the resident inspectors were plant operations and the design change, engineering and modification areas. The below-listed PAT findings were considered significant in that more information would be needed in order to determine impact relative to safety related equipment operability for the upcoming startu There was a lack of documentation on the environmental equipment qualification for certain cables used in the emergency feedwater system.
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10 CFR 50.59 safety evaluations were not performed for lead shielding on certain piping, and technical evalu-ations did not consider the additional stress on piping during dynamic conditions in distinction to static condition The remote shutdown panel (RSDP) was apparently not electrically isolated from control room (CR) panel Accordingly, a fire in the CR could adversely affect the RSD With the battery room temperature kept below minimum design temperature during certain time periods, the effect on battery capacity was not fully evaluated by i
the license For these items, the licensee will be conducting an internal evaluation to determine the affect of these find-ings on safety-relatad equipment operability. Licensee action will be verified during the next NRC inspection (N /86-06).
Prior to the outage startup, the NRC resident office staff will follow up on the below-listed additional PAT findings !
for which the licensee was in the process of taking correc-tive action during outage work:
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proper adjustment of limit switch and torque switch settings for those valves in which motor operated
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valve testing will be complete;
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quality of the compressed air purchased for emergency l feedwater two-hour backup air system in meeting design specification; and, I
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completion of licensee established preventive mainte-nance for MU-V16C, High Pressure Injection Isolation Valve (verified complete by the inspector during this period).
These and all other PAT findings will be documented in detail in NRC Inspection Report No. 50-289/86-0 . Reactor Building Local Leak Rate Testing The inspector conducted a review of the local leak rate testing that was being accomplished as a result of a scheduler exemption that was granted to the licensee in a NRC letter, dated February 20, 1986. This letter allowed the licensee to postpone 10 CFR Part 50, Appendix J local leak rate testing that was to be accomplished by February 23, 1986, until the present o'utage. The leak rate testing was to be accomplished on seventy-one (71) valves which were required to be individually leak tested per the requirements of Appendix J,Section III. At the end of the inspection period, the licensee was in the process of completing the remaining leak tests. The licensee had chosen to test all ninety-four (94) valves and penetrations required by their procedure. This testing encompassed the seventy-one (71) valves that were required to be tested. At the end of the inspection period, seven-ty-nine (79) of the ninety-four (94) valves were complet The inspector discussed with licensee personnel involved in conducting the testing and reviewing the data, the requirements for this testing and general overall test conduc Licensee personnel were aware of the require-ments, and personnel conducting the tests were knowledge-i
able of test methodology. The inspector witnessed selected ,
test evolutions and observed that equipment was calibrated i
and testing was accomplished according to procedure Corrective action for discrepancies found during testing was' acceptable. The test procedure SP 1303-11.18 was re-viewed and found to be adequate. Review of final data and total leak rate will be reviewed in the next resident office inspection (No. 50-289/ 86-06). The inspector had no concerns on the licensee's action to dat .3 Conclusion Operators continued to conduct themselves in a professional manne In general operators were responsive to daily plant problems as they arose. Overall, procedures were properly implemente ,
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i Management took initiative to control outage work and alleviate undue pressures on control room personnel. Appropriate licensee action is being planned to address the significant PAT findings noted abov . Event Review
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3.1 Introduction and General Scope of NRC Staff Review
During this inspection period, there were three events that the NRC staff reviewed in detai They were: the reactor trip of March 15, 1986; the unusual event of March 22, 1986; and, the airborne radio-activity / contamination events of March 24-25, 1986. In general, the i following aspects were considered for each of these events:
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details regarding the cause of the event and event chronology;
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functioning of safety systems as required by plant conditions;
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consistency of licensee actions with license requirements, approved procedures, and the nature of the event;
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radiological consequences (on-site or off-site) and personnel exposure, if any;
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proposed licensee actions to correct the causes of the event;
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verification that plant and system performance are within the limits of analyses described in the Final Safety Analysis Report (FSAR); and,
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proper notification of the NRC was made in accordance with 10 CFR 50.7 For each of these events the inspector provided a chronological /
factual summary; specific scope of NRC staff review; licensee find-ings, both operational and radiological; and, NRC staff findings,-
both operational and radiological. An overall conclusion on licensee performance is provided in paragraph .2 Reactor Trip 3. Event Chronology and Background Information !
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Shortly before 10:00 a.m. on March 15, 1986, operators started to shift main lube oil coolers. A low pressure transient developed in the main lube oil system and pres-sure sensing instrumentation tripped the main turbine generator. A restart modification functioned properly (turbine-to-reactor trip) and it tr.ipped the reactor at 10:02 a.m. This resulted in the actuation of the steam
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generator safety valves causing both visible steam and loud noises for several minutes. This was noticeable from off site location The main lobe oil systems provides relatively cool lubri-
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cating oil for the main turbine generator journal bearings and thrust bearing. If this system were inoperable as sensed by pressure switches, significant damage could result to the main turbine generator shaft and bearing assembly. Accordingly, a secondary plant trip (turbine trip) it designed to occur when low pressure is sensed, which is what occurred on March 15, 1986. The turbine-to-reactor trip is an anticipatory function to minimize the pressure transient on the reactor coolant system upon a secondary plant load rejection (which occurs on a turbine trip). Shifting lube oil coolers is a weekly operation to rotate operating equipmen Being on site at the time, the senior resident inspector heard the steam generator safety valves actuate and he immediately responded to follow licensee post-trip activi-ties, including the post-trip revie Plant response was as expected and operators established stable hot shutdown conditions. The licensee post-trip review identified proximate sequential causes of the trip back to the main lube oil pressure transient; however, a root cause of the lube oil transient could not be established. It was sus-pected that either a valve malfunctioned or the transfer 1 valve was not properly operated. The licensee planned to continue to review this area during the eddy current outag The licensee restarted the plant Saturday night, March 15, 1986, and achieved full power by early Monday, March 17, 198 .2.2 Specific Scope of NRC Staff Review for the Reactor Trip Specific to the reactor trip event noted above, the i inspector verified the below listed items:
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initial proper response of the plant to the post-trip window on the pressure-temperature (P-T) plot;
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personnel properly implemented ATOG procedures and prudently acted on unusual conditions;
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identification of the^ sequential proximate causes for the trip along with a reasonable determination of the i root cause;
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post-trip review was conducted in accordance with Administrative Procedure AP 1063, Revision 6, " Reactor Trip Review Process;" and,
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No ur veriewed safety issues identified in post-trip review dat In addition to discussions with cognizant licensee person-nel, the inspector:
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made an independent assessment of post-trip. parameter response based on visible strip chart and indicators in the control room shortly after the event;
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attended the licensee's post-trip review;
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attended the independent safety review of abnormal t
response of the feedwater system;
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reviewed the' complete post-trip review package (N ); and,
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reviewed Administrative Procedure (AP) 1063, Revision 7, dated March 24, 1986, " Reactor Trip Review Process" for adequac .2.3 Licensee Findings 1 No unreviewed safety questions were identified. Prior to the startup, the licensee imposed a requirement to further investigate duplicating those conditions that caused the low pressure situation in the main lube oil syste ,
Licensee personnel were able to duplicate a low pressure transient in the lube oil system during a transfer to standby cooler operation. However, the results of that review were inconclusive in identifying a specific root caus The licensee became more convinced that either personnel error or a procedure weakness contributed to the pressure transient in the lube oil syste Subsequent to that startup.and during shutdown for the eddy current outage on March 21, 1986, the licensee conducted a cooler transfer with the main turbine at full speed but off the regional electrical gri Licensee personnel learned that the degree of opening the cooler fill valve affects
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how long it takes the standby cooler to fill, vent, and be pressurized. After five minutes, when personnel were satisfied that the standby cooler was filled, vented, and pressurized, personnel shifted the transfer valve. No turbine trip occurred and the licensee continued the plant shutdown.
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The licensee's internal trip review also identified that personnel physically forced the transfer valve during repositioning. Applicable procedures were not clear in
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assuming the standby cooler was filled, vented, and pressurized. Licensee operations management concluded that'
.the major (root) cause of the event was weak procedures and
, a minor (root) cause was personnel error. Procedure changes are planned.which are to include keeping the fill valve
, . opened. Operations engineers will continue to monitor lube oil cooler transfers and to identify potential valve
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malfunctioning.
- Two other post-startup items were identified for review by
the licensee's Technical Functions Divisio At the time of the trip, the saturation margin monitor (SMM) instruments responded by indicating 25-30 F sub-cooling margin. One computer channel alarmed (indica-ting'less than 25 F). Redundant subcooling instrumen-tation and the post-trip P-T plot indicated that saturation margin was above 50 F. Licensee personnel believe that the response of the SMMs was due to
resistance temperature detector (RTD) respons The plant did not get to the post-trip P-T window until about twelve minutes; whereas, the procedural guideline is 10 minutes. The post-trip review deter-mined that the cause of the problem was feedwater flow going to zero or the regulating valves going shu This was unanticipated for proper Integrated Control System (ICS) OTSG level contro I&C personnel were to work on the applicable controllers during the eddy current outag Total radioactivity (mostly Xe-133) released as a result of the steam generator safety valve actuation was 37 micro-curies which was well below technical specification limit .2.4 NRC Findings Operator response to the event was consistent with emer-gency procedures. Operators were conscious of, and oriented their action toward, decay heat removal. Plant response was essentially as expected, except as discussed belo The inspector independently confirmed the licensee's findings as noted above. The sequential proximate causes
' of the trip were reasonably-determined prior to startup and the licensee provided an extensive and thorough review to identify a root cause of the event. Although a specific root cause could not be identified, the trip could have i
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been avoided had personnel used better judgement by stand-ing back and further reviewing the situation, instead of forcing the transfer valve to repositio The post-trip review package was not distributed until
shortly before the post-review meeting. Consequentially, it appeared that certain plant engineering personnel were i reviewing and analyzing data during the conduct of the meeting. However, a majority of the meeting members were
knowledgeable of the data; and it was evident that they had ( analyzed and made conclusions prior to the meeting. The late distribution of the data package did not adversely affect the adequacy of the post-trip revie However, the inspector discussed with licensee management potential problems in certifying the AP 1063 requirement (paragraph 3.1)..." group... convene to review and concur with the
. conclusion of the post-trip review" with the untimely
distribution of a post-trip review packag Licensee management acknowledged the inspector's comments and reiterated the engineering personnel were adequately briefed and prepared for the meeting. The inspector had no i further comments on this matter.
i At the conclusion of the inspection, Technical Functions Division (TF) was still reviewing the post- startup items (SMM response, and feedwater response).and the licensee event report to the NRC was not received. Accordingly,
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this area is unresolved pending licensee submittal and Region I review of the applicable LER. Further, Region I will review TF disposition of the post-startup items noted __"
above (289/86-LO-06).
3.3 Inadvertent Release During Degassing Operations 3. Event Chronology At 1:50 a.m. on March 22, 1986, during degassing opera-tions, a first alarm (alert) was received on RM-A-6, Auxiliary Building gaseous effluent radiation monito This was followed at 3:01 a.m. by a similar alarm on RM-A-8, Auxiliary Building ventilation stack vent radiation monito The plant was in a cooldown mode at approximately 260 F in preparation for a five-week outage and the primary system was being degassed via the pressurizer steam space
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sample line to the make-up tan The licensee secured the degas flow path and at 3:05 the radiation monitor alarms had cleared. The release path was determined to be the inadvertent lifting of CA-RV-5, a relief valve in the degas flow pat >
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3.3.2. Specific Scope of NRC Staff
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The inspector conducted discussions with cognizant licensee personnel and reviewed the following documents:
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system flow diagrams; ,
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Operating Procedure (0P) 1102-12, " Hydrogen Addition and Degassification;" and,
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OP 1104-43, " Nuclear Plant Sampling."
3. Licensee Findings 1 The licensee determined that the lifting of CA-RV-5 was
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due to improper throttling of CA-V-10 as the cause of the release. When CA-RV-5 lifted, a flow path was set up to the Auxiliary Building sump which vented to the environment via the Auxiliary Building ventilation. system. Initial calculations showed that approximately 30 curies of noble gases, primarily Xenon-133, were released. This calcula-tion was subsequently changed to approximately 15 curies upon systematic evaluation of the strip chart recorders from RM-A-6 and RM-A- Calculation of dose at site boundary revealed a cumulative dose of 4.3 x 10 -4 mra .
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All releases and site boundary doses were far below the *
limits of 10 CFR Part 20 and the technical specification Although applicable procedures contained precautions about the potential lifting of CA-RV-5, the operating procedures
, are being revised to more clearly specify pressure limits to be used when degassing to preclude lifting of the relief
valv The licensee is also reviewing the entire degassing opera-tion; flow paths and methodology to determine if operating methods can be changed to preclude future degassing problec3. These recommendations will be reviewed by the Plant Review Group (PRG) in future meeting . NRC Staff Findings The licensee's initial actions in response to this event were timely and adequate to control the release. The inspector agreed with the licensee that the cause was improper throttling of CA-V-10, which caused CA-RV-5 to lift and discharge to the Auxiliary Buildin i
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The licensee acknowledged that, due to the process flow path liquid / gas / steam mixture coupled with the difficulty
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of pressure control, the potential exists to lift CA-RV-5 and release radioactivity to the Auxiliary Building spaces instead of to designed processing systems. The licensee has agreed to review this evolution oy referral to the Plant Review Group for possible long-term corrective actions. Present corrective actions to prevent recurrence consist of operating procedure changes to ensure more adequate control of the degassing evolution as presently conducte This area will remain will remain unresolved until Region I reviews the completion of licensee action as stated above (289/86-05-01).
3.4 Airborne Radioactivity and Persc....el Contamination Event of March 24-25, 1986 3. Sequence of Events On March 24, 1986, starting at approximately 9:00 a.m., the licensee removed the "A" and "B" once-through steam genera-tor (OTSG) handhole covers and commenced ventilation of the
"A" and "B" OTSGs to the Reactor Building (RB). Ventilation was effected by connecting the suction from a 500 cfm port-able HEPA unit directly to the handholes after cover removal. These filter units provided particulate cleanup only and exhausted directly to the RB. By 9:49 a.m., the licensee had collected air samples from the exhaust of the HEPA units as required by their Radiation Work Permit (RWP)
, and ALARA review for the job, but failed to analyze the
! iodine samples until 8:47 p.m. that evenin In addition, the "B" OTSG sample result, which showed
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3.8 MPC iodine, was not evaluated by the counting room technician or reviewed by the Group Radiological Control
Supervisor (GRCS) until the following day (March 25,1986).
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i of the worker breathing zone samples discussed below. Delay was due to a large sample backup in the counting room; the
licensee was concurrently concerned with noble gas levels t
inside the RB, and noble gas air samples were receiving l counting priority.
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The licensee continued to work on both OTSGs throughout the day (removing manways, etc.). The licensee indicated that although they discussed the potential for airborne radir-iodine in the RB, they dismissed it partly due to the
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[The inspector reviewed the applicable RWP and determined these samples could not be considered representative of general RB airborne iodine conditions since: they sampled the worker's breathing zone air on OTSG platform; and, a portable ventilation spot intake was positioned immediately adjacent to the handhole during removal and would, there-fore, be pulling any airborne iodine away from the worker.]
By 6:46 p.m. on the evening of March 24, 1986, a RB general area air sample fr)m the 346-foot elevation indicated MPC iodine. Additionally, a worker who had been contamin-ated during the day received a whole body count (WBC) at 5:50 p.m., which indicated I-131. The licensee indicated this data was recognized as indicators of an iodine problem by a member of the Radiological Controls Field Operations dayshift staff; however, this information was not effec-tively communicated to the relieving shift and no actions were taken. During this time the licensee also failed to notice a 6000 cpm increase on RMA-2, the RB airborne monitor iodine channel, which increased from 10,000 cpm at 3:00 p.m. to 16,000 cpm by 8:00 At approximately 9:00 p.m., two OTSG jumpers exiting the RB were found to be contaminated. They were showered and sent for a whole body count (WBC). WBC results at approximately 11:00 p.m. indicated that 'aese individuals had internal /
external contamination levels of Iodine-131 up to 340 nanocuries (nc).
The WBC technician notified the GRCS of the iodine result About this same time (11:00 p.m.), another set of OTSG HEPA exhaust samples were counted, showing 3.6 MPC and 1.5 MPC from the "A" and "B" 0TSG, respectively. The licensee also collected a " grab" sample from RMA-2 at 11:10 p.m., which subsequently showed 0.48 MPC in the RB recirculating ai At that point, approximately fourteen (14) hours after the start of the iodine event, the licensee first became aware of radioactive iodine concentrations in the RB. Shortly after this identification was made (approximately 1:00 on March 25,1986), the licensee restricted access to the R As a result of this failure to assess airborne radioactivity concentrations in a timely manner, one hundred and twenty-four (124) personnel were sent for whole body counting with seventy-seven(77) showing positive indication of unplanned iodine intakes up to 120 nC .
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3. Scope of NRC Review The inspectors assessed the licensee's identification and followup actions to the airborne radiciodine event on March 24, 1986, by the following methods:
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review of licensee air sample log sheets for March 24-25, 1986;
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review of the HP log book for March 24-25, 1986;
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review of RWP 31641, " Remove' Insulation and Manways
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and Handholes from "A" and "B" OTSG"
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review of associated ALARA Review No. 86-03-06;
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discussion with cognizant licensee personne review of OP 1102-12, " Plant Shutdown;" and,
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review of applicable maintenance and surveillance procedures, i
- 3. Licensee Findings - Radiological Licensee identification of airborne radiciodine in the RB i occurred at approximately 11
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WBC results from two individuals contaminated while
working in the OTSGs (see paragraph 6.0 of this report);
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air samples taken at the exhaust of HEPA units venti-lating OTSGs, showing 3.6 and 1.5 MPC, respectively; and,
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grap air sample result showing 0.48 MPC in RB general
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collecting and evaluating additional samples; scheduling individuals present in RB on March 24, j
1986,(124) for whole body countings for dose
- assessment;
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limiting access to the RB on March 25, 1986, until j airborne levels were reduced;
--__________._____.m__
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,
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shortening iodine charcoal filter count times from 1000 to 500 seconds to expedite sample processing; and,
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purchasing charcoal filter units to attach directly in line with the 500 cfm HEPA units to provide iodine cleanup capability. These units were purchased and on site by March 27, 198 The licensee had not performed a formal investigation or critique into the causes of the airborne event as of April
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2, 1986; the last day of NRC radiation specialist review of this event. However, informal discussion between the inspectors and cognizant radiological control personnel indicated the following factors contributed to a failure to identify airborne radioiodine levels in a timely manner:
--
reliance on two unrepresentative breathing zone air samples as indicators that no iodine problem existed;
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long delay in sample processing, compounded by a prioritizing of noble gas samples over iodine samples;
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failure to note the gradual increase in RMA-2 monitor readings; and,
,
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lack of communication among shift personnel and licensee division Licensee followup included whole body counting of 124 personnel present in the RB Nrch 24, 1986. Seventy-seven people were found *o external / internal contam-ination, predominantly Iod :-131. The highest WBC indicated 340 nCi of I-131; however, this individual had been externally contaminated while working in the OTS Selective shielding of body areas and recounting of this individual indicated the majority of this activity was t
located on the hands, approximately 80 nCi of I-131
! activity is being assigned as an intake. The highest intake value, discounting skin contamination contributions, ;
is 120 nCi of I-131. With respect to radiological release for the period March 25 to April 7, 1986, the licensee reported the release of 194 Ci of noble gases from reactor building purging. Also released were approximately 3.156 ;
E-5 Ci Particulate, Tritium, and Iodine, predominantly
'
Iodine 13 The value is based on ventilation filter effi-ciency calculations, since release rates were below detect-
' able limits of effluent iodine monitors. The potential release converts to an integrated dose at the site boundary i i
of 4.94 E-3 mrad, gamma, and 2.16 E-2 mrad, beta, which is l well within technical specification limits.
i l
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3. Licensee Findings - Operational A review of this event from an operational perspective was performed by the licensee to see if the methodology used in the operation of the plant contributed significantly to the event. A review of plant procedures and the order that plant evolutions were performed was conducted. The review did not identify any design problems that would directly contribute to the root cause of the even . NRC Findings - Radiological 3.4.5.1 Once the iodine buildup in the RB was identified, licensee response actions were appropriate and oriented toward worker radiation protectio Intake dose calculations were con-servative and confirmed by state-of-the-art equipmen Reasonable efforts were made to distinguish skin contamin-ation versus actual radioactive material intake based on whole body counting results. No overexposure were identifie However, the unplanned exposures could have been prevented as noted belo The inspector verified the licensee's. list of individuals identified as having intakes based on the preliminary WBC and that these res/ ts are being followed and recounted by
the licensee. The licensee appears to have adequate tech-nical expertise in this are .4.5.2 Requirements of 10 CFR 20.201 are that each licensee make such surveys as may be necessary to comply with all sections of Part 20. Requireraents of 10 CFR 20.103(a)(3), in part, are that "... the licensee shall use suitable measurements of concentrations of radioactive materials in air for detecting and evaluating airborne radioactivity ... as may be necessary for timely detection and assessment of indi-vidual intakes of radioactivity by exposed individuals ..."
The inspector considered that the licensee's failure to provide a timely detection and assessment of airborne radiciodine conditions in the RB on March 24, 1986, was i an apparent violation of 10 CFR 20.201. As a result of I an approximate 14-hour delay prior to detection of the l airborne radiofodine, 124 people present in the RB were 1 exposed to then unknown concentrations of airborne radiotodine. Seventy- seven individuals were later found to have unplanned uptakes of radiciodin Licensee radiological control personnel indicated that iodine had been surveyed for, in that samples of iodine had been taken starting at 9:49 a.m. and had continued through- !
out the day. The inspector stated that these samples had
o .
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been collected but not counted or analyzed and, therefore, they could not be considered "an evaluation of the radiation hazards" as defined in 10 CFR 20.201(a). The licensee also indicated that they had anticipated an iodine problem from the OTSGs,-as evidenced by their ALARA review requirement to sample at the HEPA unit exhaust. However, actual iodine levels turned out to be greater than those anticipate ,
As indicated above, the apparent failure to survey for airborne radioactivity is contrary to 10 CFR 20.201 and 20.203(a)(3) (289/86-05-02).
3. NRC Findings - Operational The resident inspector reviewed the event to verify that the licensee was performing the plant operations associated with this event per applicable station procedures. A review of the shutdown and degassing event was performed. This review determined that the evolutions were performed in accordance with applicable procedure. The plant had been degassed down to below 5 cc/kg of hydrogen in the reactor coolant system. However, the pace of operational activities on March 24, 1986, appears to have been a factor in the even Licensee orientation that day was to establish access to both steam generators so that contractors could start the eddy current test process. It appears that pace was too fast in contrast to activities over the previous two days for support personnel; namely, Radiological Con-trols Division, to keep up with activities in radiological areas. On the other hand, if the Radiological Controls Division was severely taxed, it could have stopped work for support activities to catch u The inspector concluded that both the operation and radiological controls personnel failed to effectively
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communicate, which was contributory to the unplanned exposure .5 Conclusion j For the reactor trip event, operator response was in accordance with applicable emergency procedures and consistent with their performance-oriented training. The licensee's post-trip review was thorough and a substantial effort was made to identify the root caus For the degasification event, operators could have been more attentive to prevent the relief valve lift. Further review is warranted on the viability of the licensee's degasification methodolog I
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For the RB iodine event, certain NRC requirements on properly evalua- r ting' radiological conditions.were apparently violate Contributing to the root cause was poor licensee personnel communication with re-spect to the pace of activities surrounding the event. Post-event review and dose evaluation methodologies were adequate and conservativ . Fire Protection Program 4.1 Periodic Inspections and Quality Assurance Audits 4. Annual Audits The inspector reviewed the licensee's 1985 annual audit report, Audit No. 0-TMI-85-03, Fire Protection. The scope of review was to ascertain that the audit was conducted in accordance with the Technical Specification 6.5.3.2.a and audit findings were being resolved in a timely and satis-factory manner. No unacceptable conditions were identifie . Biennial Audit The inspector reviewed the licensee's last biennial audit, Audit Report No. S-TMI-84-03, TMI 1 and 2 Fire Protection Program. The scope of review was to ascertain that the audit was conducted in accordance with TS 6.5.3.1.g and audit findings were being resolved in a timely and satis-factory manner. The inspector also reviewed the licensee's effort to complete Audit No. S-TMI-86-03 being performed to satisfy the above mentioned TS requirement for the current perio The auditers performing this audit have placed an increased emphasis on fire brigade training since it was previously identified by NRC as an area of potential weakness. No unacceptable conditions were identifie . Triennial Audit The inspector reviewed the licensee's triennial audit, Audit Report No. 0.TMI-84-05, Fire Protection. The scope of review was to ascertain that the audit was conducted in i'
accordance with TS 6.5.3.2.a and audit findings were being resolved in a timely and satisfactory manner. No unaccept-able conditions were identifie .2 Facility Tour The inspector examined fire protection water systems, including fire pumps, fire water piping and distribution systems, post- indicator valves, hydrants, and contents of hose houses. The inspector toured accessible vital and non-vital plant areas and examined fire detection and alarm systems, automatic and manual fixed suppression systems, interior hose stations, fire barrier penetration seals, and fire l
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. _ _ __ _ _ _-_______
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door The inspector observed general plant housekeeping conditions and randomly checked tags of portable extinguishers for evidence of periodic inspection No deterioration of equipment was noted. The inspection tags attached to extinguishers indicated that monthly inspections were performe During a tour of the control room, the inspector observed that about six 5 gallon plastic jugs full of water were on the floor by the water cooler. The inspector pointed out to the licensee that a water spill in the area of electrical panels is undesirabl The licensee agreed and the excess water bottles were remove .3 Fire Brigade Training The inspector reviewed the training records of the fire brigade members to ascertain that they had attended the required quarterly training, participated in a quarterly drill, and received the annual hands-on fire extinguishment practice. No unacceptable conditions were identified, except as noted belo .4 Fire Drills The inspector reviewed fire drill records and noted that, in some instances, 12 to 20 fire fighters responded to a dril The inspec-tor indicated to the licensee that a drill cannot be realistic and provide meaningful training for 20 individual Further, the licensee does not have enough fire fighting equipment to supply this number of personnel. Plant management initially agreed with the inspector that drills under these conditions could be ineffective and committed to review the method by which drills were conducted. Depending on the results of that review, the licensee also agreed to submit a plan for improvement. Subsequently, the licensee informed the inspector that the method by which drills were conducted was adequate and in accor-dance with the accepted progra In light of the licensee's position on this matter, NRC Region I will refer the adequacy of training relatively large numbers of personnel on a per drill basis to the Office of Nuclear Reactor Regulation (NRR). This is an unresolved item pending further NRC review of the licensee's training methodology (289/86-05-03).
4.5 Clarification Requirement for Unannounced and Backshift Drills The inspector reauested to review fire drill records to determir com-pliance with the requirement to annually perform unannounced ant'
backshift fire drills for each shift fire brigad The licensee's records indicate that drills for each shift fire brigade were performed. Because of the licensee's fire brigade membership size (approximately 130-150 fire fighters), the inspector wanted to know how many fire fighters had participated in unannounced
.
.-
and backshift drills. The licensee stated that they are not required to maintain this type of records. Given the size of the shift fire brigade of 5 fire fighters, it is possible that only 10 to 15 fire fighters participate in these type of drills. The licensee agreed that this is possible, but it is not the cas !
NRC Region I will also refer this matter to NRR for review on the acceptability of not having records to distinguish unannounced and backshift fire drill participation and the issue will be included in the unresolved item noted above (289/86-05-03).
4.6 Fire Drills in Adverse Weather The National Fire Protection Association (NFPA) Standard No. 17 requires that fire drills be held occasionally under adverse weather conditions. The inspector reviewed reports of this type of drill and
!
the licensee produced the records of 3 drills that were held under j adverse weather conditions. The drills were held on February 14,
'
1985, August 8,1985, and September 4,1985. A check with the '
- National Weather Service identified'that for the dates indicated the temperatures were 30 F, 87 F, and 91 F with clear skie The inspector asked NFPA representatives for clarification as to i
what constitutes adverse weather. NFPA response was that heavy rain,
, snowfall, freezing conditions, and extreme heat would qualify. The conditions under which the above drills were held do not meet the requirement Licensee mana'gement acknowledged the conflict and i
agreed to review the matter. This is unresolved pending further review of the licensee and NRC Region I (289/86-05-04).
5. Steam Generator Tube Eddy Current Testing and Emergency Feedwater Nozzle Cracking
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5.1 Allegation on Vendor Use of Controlled Substance
5. Background
,
On or about March 11, 1986, licensee representatives i reported to the NRC's TMI-1 Resident Office that an indi-vidual employed at another nuclear facility made allegations to the cognizant NRC regional office and/or cognizant Atomic Safety and Licensing Board on certain vendor representatives who were to perform eddy current testing on TMI-1 steam generator tubes. The allegation dea'.t with the misuse of
, controlled substances (drugs) at that other facility. As yet the allegations were not substantiated, but cognizant NRC staff are conducting a followup revie i i
! !
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l
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e
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For TMI-1,' licensee management became concerned and insti-tuted action to enhance random inspections and vendor personnel screening during the eddy current outage. During the period from March 18 to 24, 1986, the licensee reported i that they had the contract with the vendor revised to speci-fically exclude the use of controlled substances by vendor representatives and to require that vendor equipment, facilities, and persons be subject-to random inspection and/or testing, as applicabl When the vendor arrived on site, the licensee reported that they conducted a thorough search of the vendor's facilities and equipment taken into the protected area in accordance with the licensee's security pla No controlled substances were found. Also 18 vendor personnel were tested with one having positive results, possibly indicating the recent use of a controlled substance. The vendor management acknowl-edged this finding and asked the licensee to terminate the individual's access to TMI-1. The individual was not allowed to participate in eddy current testin . Scope of NRC Staff Review In addition to receiving periodic status reports from the licensee on this problem, the inspector verified the follow-ing item The licensee contract with the eddy current test vendor of equipment / facilities reflected the agreement for licensee inspection and test of personnel for con-trolled substance Vendor personnel were not in possession of or using controlled substance The licensee's contract with the vendor reflected ,
appropriate regulations; such as on the reporting of '
deficiencies (10 CFR 21), on employee discrimination '
for expressing safety concerns (10 CFR 50.7) and
- having a quality assurance program (10 CFR 50,
.
Appendix B).
In addition to discussions with the Director of TMI-1 and plant security personnel, the inspector conducted random inspections of licensee / vendor facilities and equipmen Selected sections of the following documents were reviewe Vendor letter to GPUN, dated April 3, 1986, on indi-
vidual termination
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Contract File No. 017519, original, dated October 16, 1984, through Change No. 7, d ted March 11, 1986
,
)
.y- .-
p-
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Various attachments to above contract changes includ-ing GPUN specification GED-CS-36, Revision 1, dated February 29, 1980, and GPUN Contract General Terms and Conditions, Revision 2, dated January 2,1985 5. NRC Staff Findings In general, the inspector verified the accuracy of the reports made to the NRC's TMI-1 Resident Office. No con-trolled substances were observed to be in place or in use at the data collection facility on site and at the analysis facility in Hershey, Pennsylvani The contract reflected provisions for the licensee to con-duct random inspections and testing of vendor personnel for controlled substances. The licensee reported that they implemented that option with negative findings, except as noted above. The contract also invoked applicable federal regulation As noted below, NRC staff independently observed and con-firmed selected vendor / licensee eddy current results for the steam generator tubes. The results of the NRC staff's technical review of the area are addressed belo .2 Eddy Current Examination of Steam Generator Tubes The inspector reviewed data, observed examinations in progress, and interviewed eddy current examination personnel to ascertain that the examinations and the data interpretation were done in accordance with regulatory requirements and ASME Code requirements. The inspector's observations included the examination of tube 107, row 41, in the "A" steam generator. This was a re-examination to assure that complete-and legible data were obtained for interpretation and evaluation purposes. Additionally, the inspector observed the interpretation of data including tube 68, row 30, in the "B" generator, and tube 27, row 104, and tube 1, row 73, in the "A" generator, and discussed the interpretation with cognizant vendor Level III personne A 46?; throughwall flaw was identified in "B" generator tube 65, row 30, which was not identified during the 1982 examination of the tub A review of the 1982 data, using the equipment available for the 1986 interpretation, indicated that the flaw was present in 1982. The low voltage associated with the indication, the size of the indication displayed on the screen, and the presence of non-relevant indications in the display resulted in misinterpretation of the indication in 198 Currently available improved equipment, including computer enhancement capability, allowed the data evaluator to recognize the indication as a 46?4 throughwall flaw. Additional 1982 data were
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reviewed by the licensee to assure that additional flaws were not missed. The inspector reviewed the 1982 and the 1986 data and dis-
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cussed the two data sets with the Level III individual who was responsible for the 1986 data interpretation. The inspector con-
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cluded that no change in signal characteristics sere discernible in the two data sets and that no change in throughwall dimension had occurred since the 1982 examination. This conclusion was stated to NRR during a telephone conversation from the site on April 11, 198 At the exit meeting, the licensee stated that an anticipated revised technical specification will change the tube plugging limit from 40%
to 50% throughwall; and, based on this, the tubes which contain flaws less than 50% throughwall would not be plugged at this tim The inspector found that the data collection and interpretation was done by qualified personnel and that code and regulatory requirements were me !
l No violations were identified. Licensee repair and test activities
, will be reviewed in the next inspection period (NRC Inspection Report
- No. 50-289/86-06).
5.3 Emergency Feedsater Nozzles Each of the six active nozzles on each steam generator contains a
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thermal sleeve held in place by a collar which is fillet welded to the sleeve. Cracks in the fillet welds have been found at other plants and were evaluated by B& The welds were scheduled by the licensee for inspection during the December 1986 refueling outag Because of maintenance on the emergency feedwater spray ring, one of the six active nozzles was required to be removed from the "A" steam generator and the thermal sleeve / collar fillet weld was liquid i penetrant examine Cracks were detected which resulted in two 1 additional nozzles being removed from the "A" generator for i examination. The additional welds displayed cracks; and, at this point, the licensee decided to remove the remaining nozzles from the
"A" generator and the nozzles from the "B" generator for liquid penetrant examination. The cracked welds were repaired by welding
- and re-examinatian by the liquid penetrant method was done to ascer-tain that the repair was properly mad The inspector observed the examination of repaired welds on nozzles A-1 and A-2 and the initial examination of welds on nozzles B-1 and B- The examinations were done in accordance with procedure 6110-QAP-7209.02, Revision 0-01, using the visible dye solvent remov-able technique. Indications which were identified were evaluated and dispositioned in accordance with acceptance standards as defined by
. the procedure.
.
_ _ _ _ _ _ _ _ _ . _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ _ . _ _ _ _ . _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _ . _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _
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' The licensee reported that B&W has changed the nozzle thermal sleeve design to correct the cracking problem and that the new design will be installed by TMI-1 at some later date. At the time of this inspection, the licensee had not decided when the sleeves will be replaced.
The cracking at TMI-1 was attributed by the licensee to fatigue, but the specific kind of fatigue was not identifie The item is con-sidered unresolved pending the availability of documentation to confirm that the failures at TMI-1 resulted from the failure mechanism which was evaluated by B&W regarding the earlier cracking at other
'
facilities (289/86-05-05). No violations were identified. Licensee repair and testing activities will be reviewed during the next in-spection period (NRC Inspection Report No. 50-289/86-06)
5.4 Conclusion With respect to alleged use of controlled substances by vendor per-sonnel at another facility, the inspector concluded that the licensee is taking adequate preventive and surveillance measure Except as noted in above paragraphs, no unresolved issues exist on the process and collection of required eddy current testing dat The inspector concluded that the personnel involved in obtaining and
'
analyzing the data were knowledgeable and were very familiar with the eddy current indications expected and found at TMI- Review of feedwater nozzles and repairs determined that the repairs were performed in accordance with applicable codes. Interviews and
, discussions with different licensee line organizations indicated that
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qualified people were used and positive control and direction were i
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given to this project by licensee management. Independent visual review of the weld repairs by the inspector determined adequate weld repairs were performed. In general, the inspector concluded the
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licensee was proceeding in a safe manner and adequate quality assur-ance was being implemented on the repair proces .0 Outage Radiation Protection 6.1 Introduction The inspector reviewed the licensee's radiological controls imple-mented in support of the OTSG outag The inspector's effort was
.
focused in two areas:
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0TSG work activities; and,
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licensee posting and labeling of controlled area l Within the scope of this review, one violation, a failure to con-l spicuously post a radiation area, was identifie !
e
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6.2 Postir.g and Labeling of Controlled Areas
, 6. The inspector reviewed the licensee's program for the !
'
posting and labeling of radioactive material and radio- '
logical areas against criteria contained in 10 CFR 20.202 and 10 CFR 20.203. This review included:
--
discussion with health physics technician and super-visory personnel;
--
inspection of the Reactor and Auxiliary Buildings; and,
-
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review of procedure 9100-ADM-4110.01, " Establishing and Posting Areas."
l 6. In general, applicable NRC regulations were properly implemented. However, on April 1,1986, at approximately 3:00 p.m., the inspector conducted a tour of the Auxiliary Building; and, it was noted that the equipment access double
,
doors to the " hot" machine shop on the 305-foot elevation i had been left fully open to support equipment removal and i' no radiological posting at the access to the shop was visibl Posting for this area is placed on the doors to the shop; with both doors fully opened, this posting was totally obscured. Two workers, who had been involved in
'
removal of equipment from the machine shop, were standing in the nearby area; however, these workers gave no warning or did not otherwise act to prevent inadvertent entry to the hot machine sho The inspector remained in the
.i immediate area an additional ten minutes until the health l physics technician supporting the equipment removal process returned. After surveys of the area and on the removed
,
equipment, the access doors were secure l The definition of 10 CFR 20.202(b)(2) for " radiation area" is any area accessible to personnel where a major portion 1 of the body could receive a dose in excess of 5 millirem in one hou Requirements for 10 CFR 20.203(6) are that radiation areas be conspicuously posted with a sign bearing the words " Caution - Radiation Area."
At the time of this incident, licensee posting on the " hot" machine shop identified it as a'"High Radiation Area" and a
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" Contaminated Area." The inspector reviewed surveys of the area and determined that the licensee had over posted the area; general area dose rates were less than 100 millirem /
.
hour and did not support posting the area as a high radia- l tion area. The inspector noted, however, that general area l dose rates exceeded 5 millirem / hour, and ranged to a !
maximum value of 20 millirem / hou '
[
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__.________.__.____m_ _ . _ _ _ _ _ _ _ _ _ . _ _ _ _ _ - . . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . _ _ _ - . _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ . . . _ - . _ _ _ _ _ _ _ _ . - . _ _ . _ _ _ _ _ . _ _ . _ _ . _ . _ ______._ ____._ ___ m__ ______.__________
a
,
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Consequently, failure to conspicuously post the access to the " hot" machine shop is in apparent violation.of 10 CFR 20.203(b) (289/86-05-06).
The inspector noted that, although not technically meeting the criteria for a high radiation area, the hot machine shop was considered as such by the licensee and was posted and controlled accordingly. Two recent additienal problems in the posting and control of high radiation areas are described in NRC Inspection Report 50-289/85-3 In one of the instances, posting for a high radiation area was left on the ground after a worker exited from the area. Sub-sequently, another individual inadvertently entered the area. In the second instance, the licensee did not adequately post a high radiation area due to non-uniform radiation fields in the area. While the licensee's posting and boundary were adequately placed while dose rates were measured at waist level, dose rates greater than 100 mrem /
hour could be measured outside the high radiation boundary at the head leve The licensee indicated that the HP technician supporting equipment removal from the " hot" machina shop on April 1, 1986, was, in effect, acting at posting for the area while the doors were open and should cave continually romained in the area until the doors were secured. The licentee went on to state that the failure to conspicuously post the shop was therefore a personnel problem since the HP technician left his pos The inspector agreed that had the HP tech-nician remained in the area and issued appropriate verbal warnings this would have constituted appropriate " posting;"
however, since no one was present, the violation remains a failure to conspicuously post the area. The licensee's response to this violation should also address the implica-tions of recent high radiation area posting problem .2.3 In a related matter, licensee's letter (Serial No.85-301),
dated October 14, 1985, indicated that the licensee adopted a practice of identifying and controlling high radiation areas based on dose rate measured at one foot from the radiation source. The licensee's proposed change has been reviewed by NRC regional staff and was found to be in accordance with the applicable regulations in 10 CFR 2 The inspector reviewed the following procedures and veri-fied appropriate revisions reflecting the change have been incorporated:
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9100-ADM-4000.08, " Definitions Used in Radiological Control Procedures;"
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9100-ADM-4110.01, " Establishing and Posting Areas;"
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9200-ADM-4110-06, " Control of Locked High Radiation 4 Areas;" and, i' ,
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3000-IMP-4400.01, " Radioactive Material Identification and Handling."
! No unacceptable conditions were identifie '
! 6.3 Steam Generator Work Activity l
l 6. The inspector reviewed licensee performance of several
! work activities in the "A" and "B" once- through steam
! generators (OTSGs), including the performance of the bubble test and template installation. This review included:
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review of RWPs covering the above activities (Nos, l 31660 and 31652);
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review of associated ALARA reviews;
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review of OTSG and personnel contamination surveys;
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review of meeting minutes of critique held after l
] personnel contamination on March 24, 1986; i
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discussion with HP personnel;
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attendance at the pre-job briefing prior to template
- installation on March 25, 1986; .tnd, i
! --
observation of "A" 0TSG template installation activ-l ities on March 25, 198 ;
J
) Within the scope of the above review, no violations were identifie '
"
6. The inspector noted that during the licensee OTSG entries i on March 25, 1986, adequate health physics personnel were
!
i present at the work site to control the work activity, OTSG jumpers were equipped with breathing zone air samples and headset communication equipment to assess and control
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personnel exposure. However, the following deficiencies ;
were noted during the "A" upper channel head jump i
- activitie i i
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A OTSG manway diaphragm, removed from the OTSG on l j March 24, 1986, was noted in the general area of 1
} worker access to the "A" OTSG platform. Surveys )
j indicated 2.5 R/hr. on contact, 800 mR/hr, at 12 i
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_ _ ._ . _ _ _ _ _ _ _ ._ _ _ , _ _
a
e
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I inches from the diaphragm. Yet, it did not appear i that ALARA principles were used to minimize worker
] exposure.
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During jump activities on March 25, 1986, face shields j were required by licensee RWP for general access to j the Reactor Building (RB) due to high noble gas con-
! centrations. The inspector noted several personnel i
involved in the template jump preparation in the RB were not yearing face shields as required.
,
l The above deficiencies were corrected by the licensee after
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identification by the inspector. Face shields were provided f
to all workers inside the RB; the manway diaphragm was j turned over to reduce dose rates emanating from the contam-
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inated side and later moved to a lower. traffic area. The i licensae provided the following explanation concerning the j above item ,
Individuals not wearing face shields in the RB were
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OTSG jumpers, who would be wearing bubble hoods during i jump activitie It was not anticipated jumpers would j be waiting one-half to I hour in the RB prior to jump
- activities and would thereby require face shields.
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The manway diaphragm had not been transported out of-
due to access restrictions described in paragraph 3.4.1
) of this report.
j The inspector noted that the manway diaphragms were i
originally removed during the afternoon of March 24, 1986,
and access to the RB was not restricted until midnight on the same day. Additionally, no efforts such as shielding j the manways or removing them to a lower. traffic area had j been taken at the time of removal.
I
- The inspector had.no further comments on this area, l
6. On March 24, 1986, at approximately 8:00 p.m., workers were in the upper channel heads of the "A" and "B" OTSGs to '
perform a bubble test and install "bungee" cord markers for j later phatography of the tubesheet. During these activ-
- ities, the water level in the OTSGs was 8-12 inches above l the tubesheet. The RWP and associated ALARA review required i
fireman's boots, wet suits, and double rubber gloves'for
} these activities. The gloves worn were standarc plant
- issue, approximately nine inches in length. All seams were
! taped, using masking tape, during the cord inst 411ation to l the tubesheet. Both workers, one in each OTSG, had to reach
! into the standing primary coolant water that was deeper I
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f than 9 inches in water. The seams allowed water to leak in; and, consequently, both workers were contaminated on each forearm and hand. Skin decontamination efforts were
- not completely successful; both workers left site with detectable levels of contamination remaining on the skin, but affected areas were bagged to prevent contamination sprea ; Within the scope'of the above review, no violations were identifie Skin contamination resulting from this event did not have the potential for exceeding regulatory skin dose limits, The inspector noted, however, that the appli-s care RWP (No. 31652) and associated ALARA review were not completely adequate in that appropriate protective clothing
'
, was not provided for the arm extremities in anticipation of the work activit Leakage hazards inherent to working in the standing primary coolant levels were obviously recog-nized and resulted in the prescription of high-top boot However, it apparently was not recognized that the work performed would require immersion of the hands past the glove seal level.
- Additional concerns involved in this contamination incident include the followin '
, ,
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No direct method of measuring water level above the tubesheet was used prior to personnel entry;
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The workers in the' steam generators did not make~any communication during the work activity concerning the immersion of their hands past the glove seam leve Communications to the HP personnel providing coverage concerning the potential for contamination would have
- been appropriate.
The licensee held a critique on March 24, 1986, after the personnel contamination problem was identified. At this time, it was decided a Radiological Investigation Report (RIR) would be generated to identify the causes and cor-rective actions of this incident. This is unresolved pending NRC Region I review of the scope and findings of
1 the licensee's RIR during a subsequent inspection (289/86-05-07).
6.4 Conclusion In general, the implementation of the licensee's radiation protection program was oriented toward worker radiation protectio The licensee continued to exhibit difficulties in completely adhering to posting
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regulations.
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The events of March 24-25, 1986, were caused by some inattention to basic ALARA principles and in adhering completely to RWP requirement The contamination event did not result in a significant exposure, but communication and RWP adequacy problems were note The inspec-tor did not consider these problem reflective of a programmatic proble . 10 CFR Part 21 Review: Emergency Diesel Generator Scavenging Air Blower 7.1 Background In accordance with 10 CFR 21.21(b), on February 24, 1986, Philadel-phia Electric Company (PECo) reported to the NRC Region I recent failure of the scavenging air blower on Colt Industries, Fairbanks Morse Diesel Generator installed at the Peach Bottom Atomic Power Station (PBAPS). Colt Industries' letter to the NRC, dated February 25, 1986, identified TMI Unit 1 as having similar emergency diesel generators (EDGs) with the same scavenging air blower system as at PBAPS (Fairbanks Morse Diesel Model No. 3800 TD 8-1/8).
The PBAPS and TMI-1 EDGs are equipped with a turbo-blower parallel scavenging air system. The scavenging air blower supplies atmospheric air under pressure to the cylinders for starting and low load conditions. The blower discharges compressed air to the suction side of the two turbo chargers where the air is further compressed if the engine load is approximately 50% or greater. The turbo chargers are driven by engine exhaust. As the engine load increases, the increase in exhaust gases increases the speed of the turbo chargers creating a suction at the turbo charger air inle The pressure imbalance opens the turbo charger inlet air check valve allowing suction directly from the atmosphere. At that point, the scavenging air blower becomes " unloaded" so that at 100% load the blower is "windmilling."
The scavenging air blower is a positive displacement lobe-type blower. This blower consists of two three-lobe spiral aluminum impellers with approximately 30 mil (.0030 inches) clearance between lobes and the aluminum casin Both impeller shafts are attached to a flexible drive gear, which is driven by the EDG upper crank shaf At no load conditions, the blower supplies all of the combustion air to the diesel. During no or low loads, the loss of the blower causes the diesel to stop due to insufficient air suppl The PBAPS blower failure was caused by seizure and fragmentation of the aluminum lobes of the scavenging air blower and the diesel sub- i
, sequently stopped due to lack of ai The cause of the contact
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between moving parts was believed to be thermal deformation of the air blower internals and stationary parts due to operation at no load and low load conditions. (Prior to the PBAPS DG failure, the engine had been running continuously for fif ty one hours at 20% or low load.)
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' A similar EDG scavenging air blower failure occurred at the Duane
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Arnold BWR in June 1984. Colt Industries failure analysis indicated that the cause could either be thermal creep of the aluminum impel-1ers or elastic thermal expansion of the impellers due to higher than normal blower operating temperatures. Either cause could lead to inneller lobe expansion and reduction of clearance ;
Fairbanks Morse Engine Division Service Information Letter (SIL),
dated November 15, 1984,'for Diesel Model No. 3800 TD 8-1/8, suggests that the following blower clearances be checked annually since recent blower failures were due to contact of blower impeller lobes and the blower casing: rotor to rqtor; . rotor to housing; rotor to inner end plate; rotor to outer end plate; and rotor to rotor trailing edge.
- < The rotor to rotor, rotor to housing, and rotor to inner and outer i '
cnd plate tolerances require removal of the air blower suction and
', discharge lines. The rotor to rotor trailing edge clearances can be taken through inspection plug holes on t,he blowe The SIL states that the most likely cause of the Duane Arnold blower failure is the deformation of the aluminum housing due to localized heating while running at no load condi,tions for extended periods of time.' The SIL further cautions against running at no load conditions longer than five minutes since the differential pressure across the blower ischigher due to the turbo charger inlet impeller restriction
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which may lead to excess temperature in the blower. In 1985, Fairbanks Morse increased the clearances between the blower lobes and casing for new blowers. '
FairbanksMorseVSII,.datedAugust 13,'1985, cautioned against running the air blower'at no load conditions during engine break-in after rebuilt or major repairs. The SIL also suggests that the air temper-ature be monitored at the suction and discharge of tha blower to avoid exceeding a temperature differential of 100 F to limit thermal expan-
sion of the blower aluminum lobes. (Neither of the two'TMI-1 EDGs i have blower suction and discharge temperature gauges.)
7.2 Scope of NRC Staff Review j
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The inspector reviewed the above noted 10 CFR 21 report and vendor ;
service information letters to ascertain the nature of the problems l (deficiencies) as related to TMI-1. Subsequently, he reviewed j licensee corrective actions to ascertain if the licensee received i
complete and appropriate information from the applicable vendor and if licensee corrective actions were adequate to resolve the deficiency consistent with vendor recommendation In addition to discussions with cognizant. licensee personnel, selected sections of the following documents were reviewed:
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Colt Industries' Service Information Letters (SILs), dated November 15, 1984, and August 13, 1985, for Diesel Model N TD 8-1/8;
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Abnormal Transient Procedure (ATP) 1210-6, Revision 5, dated March 8, 1985, "Small Break LOCA Cooldown;"
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Surveillance Procedure (SP) 1303-4.16, Revision 35, dated December 9, 1985, " Emergency Power System;"
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SP 1301-8.2, Revision 27, dated December 9, 1985, " Diesel Generator Inspection and Data for 1984 and 198E "
7.3 NRC Staff Findings i
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7. If a loss of coolant accident (LOCA) should occur with available offsiteLpower, the TMI-1 EDGs would start and remain unloaded. That ATP 1210-6 states that, if after twenty minutes the EDGs are not required (offsite power is available), the EDGs should be secured by bypassing the emergency start (ES) signal and then placing the DGs in ES standby. The bypassing of the ES signal and securing the EDG requires that the control room operator push both the engine stop and the diesel generator emergency shutdown pushbuttons on the control room consol (To place the EDG back into ES standby requires that an auxiliary operator push the reset button at the LOCA panel and the control room operator place the diesel start switch in automatic standby.) The inspector had no further comments in this area.
- 7. The licensee received the November 1984 SIL after the 1984
Annual Emergency Diesel Generator Inspection. After review-ing the SIL, the licensee determined that the intent of the e
SIL concerning blower clearance checks had been met since a j vendor representative was on site and observed the EDG
- inspections. The 1985 EDG inspections were also performed with a vendor representative presen The inspector determined that the licensee had not received
, the August 1985 SIL. By the end of the inspection period,
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the licensee had distributed copies of both SILs and the
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PBAPS 10 CFR 21 Report to TMI-1 engineering personne The licensee is in the process of reviewing both SILs and the Part 21 Report for applicability to maintenance and opera- '
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tion procedure revision During review of the completed ;984 and 1985 EDG inspection packages (SP 1301-8.2), the inspector observed that scarring and scratching were indicated for the lobes of both EDGs scavenging air blowers. Scarring can be an early indication
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of blower clearance problems. All clearance checks during the annual inspections appeared to be within the tolerances specified in the November 1984 SIL. The licensee is recon-sidering the cause of the lobe scarring as it pertains to possible blower failure. This problem needs further evalu-ation by the license .4 Conclusion
, At TMI-1, the time restriction on no load operation, along with the licensee's inspection program, appears to be adequate corrective action to prevent the type of air blower failure described in the PBAPS 10 CFR 21 Repor The licensee's investigation into the lobe scarring and appropriate procedure revisions will be reviewed in a future inspection report (289/86-PT-01). Generic implication of this j problem is being reviewed by NRC staf . Exit Interview l
The inspector conducted interim exit interviews on March 27, 1986, in the area of fire protection and on April 2, 1986, in the area of outage radiation protection. The inspectors discussed the inspection scope and findings for the entire period with the licensee management at a final
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exit interview conducted April 11, 1986. The following key licensee management personnel attended the final exit meeting: ,
J. Colitz, Plant Engineering Director, TMI-1 H. Hukill, Director, TMI-1 G. Tomb, TMI-I Communications M. Ross, Operations Director, TMI-1 C. Smyth, TMI-1 Licensing Manager, TF R. Toole, Operations and Maintenance Director, TMI-1 L. Wickas, Operation Quality Assurance Manager, Nuclear Assurance A representative from the Commonwealth of Pennsylvania, Mr. William Dornsife, also attended the final exit meeting. A member of Region I management, Mr. W. Johnston, Deputy Director, Division of Reactor Safety, also attended the final exit meetin T5e inspection results, as discussed at the meeting are summarized in the
- cover page of the inspection report. Licensee representatives indicated that none of the subjects discussed contained proprietary of safeguards informatio Unresolved Items are matters about which information is required in order to ascertain whether they are acceptable items, violations, or deviation Unresolved item (s) discussed during the exit meeting are documented in paragraphs 3.3.4, 4.4, 4.5, 4.6, and 6.3.3.
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