ML20197A877

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SALP Rept 50-289/98-99 for Period 960805-980124
ML20197A877
Person / Time
Site: Crane Constellation icon.png
Issue date: 02/26/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20197A880 List:
References
50-289-98-99, NUDOCS 9803100017
Download: ML20197A877 (7)


See also: IR 05000289/1998099

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ENCLOSURE 1

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE (SALP)

THREE MILE ISLAND UNIT 1

Report No. 50 289/98 99

1.

BACKGROUND

The SALP Board convened on February 5,1998, to assess the nuclear safety performance

of Three Mile Island Unit 1 for the period from August 5,1996, through Jarsuary 24,1998.

The Board was conducted pursuant to NRC Management Directive (MD) 8.6 (see NRC

Administrative Letter 93 20). The Board members were Charles W. Hehl (Board

Chairman), Director, Division of Reactor Projects, Region I (RI), Larry E. Nicholson, Deputy

Director, Division of Reactor Safety, Bl, and Cecil O. Thomas Jr., Director, Projects

Directorate 1-3, Office of Nuclear Reactor Regulation. The Board developed this

assessment for the approval of the Region i Administrator.

The performance ratings and the functional areas used below are described in NRC MD

8,6, " Systematic Assessment of Licensee Performance (SALP)."

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PERFORMANCE ANALYSIS - OPERATIONS

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Overall Three Mile Island Unit 1 (TMI) plant operation was excellent over this period.

Operations management continued to provide extensiva oversight of control room

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activities, which iesulted in a very good level of safe'.y performance. The operations staff

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conduct of norma ~ r:tivities and response to the infrequent plant transients and equipment

problems were excellst GPU took effective actions to address previous issues with the

control of equipment and human errors. - However, on occasion the operators did not

rigorously fellow approved procedures. The licensed operator requalificatlan program

remained a strength. The standing review committees functioned well and the corrective

actions systems generally improved. However, improvements were needed in the conduct,

tracking, and oversight of the corrective action process (CAP).

Licensed operators performed routine activities very well and did not initiate any plant

transients. Shift management and operators displayed excellent control over plant

activities during unit shutdowns, startups, and planned on-line maintenance. The control

room annunciator panels were routinely maintained clear of alarm annunciators. The

operators' response to the reactor trip and loss of offsite power in June 1997 was

excellent. Effective corrective actions prevented recurrence of previously identified

problems such as the failure to enter Technical Specification (TS) limiting conditions for

operations when equipment problems occurred. Human errors were reduced, indicating the

effectiveness of severallicensee initiatives in this area. Operators' procedure use during

routine and planned evolutions was generally good. However, on occasion, when faced

with unfamiliar conditions, the shift crews did not follow procedures or used a procedure

that did nct meet the intent of the performed activity. Most noteworthy, during the

refueling outage a shift supervisor directed the use of a water flow path that was not

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authorized by operations management for the given plant conditions. This resulted in a

faster than desired reactor coolant system fill rate and the spilling of water from the control

rod drive mechanism vents.

Plant management continued extensive involvement with the operation of TMI. Routine

management meetings effectively evaluated equipment problems and established priorities.

The daily meetings focused on safe plant operation and kept the operating crews aware of

the risks of conducting on-line maintenance. The operating crews were provided risk

analysis for sensitive planned maintenance activities. However, on one occasion,

mcnagement did not demonstrate a good safety perspective by the decision to lower

reactor coolant water level to the mid loop condition, for an extended period, with only one

active means of decoy heat removal operable and available. This was in contrast to

management's normally conservative decisions regarding plant activities.

The licensed operator requalification program continued to be a strength. Management

involvement in the conduct of simulator activitiet was extensive and showed a

commitment to consistent crew performance.

The plant review group, the group offsite review board, and the other oversight

committees generally performed wellin the review and identification of possible plant and

personnel performance issues. The licensee corrective action process has generally

improved the identification and assessment of adverse conditions since its introduction in

March 1997. However, the increasing backlog of open issues combined with an

inconsistent tracking and escalation process warrant management's continued attention.

The Operations area was rated Category 1.

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111.

PERFORMANCE ANAL.YSIS - MAINTENANCE

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Excellent plant material condition, very few equipment failures ud consistently good

squipment response were noted this period. GPU appropriately applied resources to

resolve several important issues. The control of work activities both during operation and

shutdown was very good. Management and supervision continued to have a strong field

presence. However. a relatively small number of rework problems resulted in the increases

in shutdown and operational risk. The TMI staff conducted surveillance activities very well,

including inservice inspection activities. However, there were a few missed surveillances

due to inservice test program problems.

The excellent plant condition resulted from good management coordination and

implementation of the maintenance program. There was only one automatic reactor trip,

few challenges to safety systems, no indicated fuelleaks, and essentially zero primary to

secondary leakage. When the infrequent plant upset conditions occurred, the equipment

responded as designed and did not complicate the operators' restoration. An example was

the excellent equipment response to the June 1997, reactor trip and loss of offsite power.

Management continued to provide the resources needed to ensure a high level of plant

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equipment performance. Examples noted were the control rod drive thermal barrier

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replacement, main generator stator bar replacement / rewind, 'B' decay heat removal pump

replacement, high pressure injection thermal sleeve crack repair, and the 100% steam

generator tube eddy current testing.

Management and supervision involvement and oversight c,f maintenance activities,

including the refueling activities, continued as a program strength. Proper management of

non-outage work requests and control room deficiencies led to low backlogs. On-line

maintenance equipment outages were well-planned, coordinated, and controlled. Excellent

human performance during these work activities resulted in no challenges to plant

operation. For potentially challenging activities, a detailed written risk evaluation and

prescribed manual actions were prepared to minimize risk,

The experienced work force and good maintenance procedure use resulted in few rework

items. However, maintenance related difficulties in the 'A' decay heat removal pump seal

replacement impacted the plant shutdown risk during the 1997 refueling outage and the

improperly wired power operated relief valve (PORV) affected operational risk during the

19951997 operating cycle. The PORV wiring problem, which occurred in 1995,

highlighted some problems in the post-maintenance testing process, workers' questioning

attitude, and self checking. The liceme did a thorough rcot cause analysis which

generated comprehensive corrective , 4 o :o address these issues.

The licensee's Nuclear Safety Assessment Group completed a comprehensive post-

maintenance testing review prior to the re-start from the 1997 refueling outage. The

quality verification group continued to perform objective assessments of maintenance

activities that resulted in personnel performance and program improvements.

Good surveillance test performance contributed to the safe and reliable operation of plant

equipment. There were no significant errors during the performance of surveillance testing

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or adverse plant responses. A more consistent use of self checking practices was noted

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during field observations. Outage inservice inspection was well planned and accomplished.

The Maintenance area was rated Category 1.

IV.

PERFORMANCE ANALYSIS - ENGINEERING

Performance in the engineering area was mixed. Significant problems were identified in a

number of engineering program areas. Examples included problems with the Inservice

Testing (IST) and Motor Operated Valve (MOV) programs, the Quality Classification List

(OCL) Process, and Technical Support. Adverse findings associated with engineering

performance, which were previously identified by the licensee's oversight groups, were not

addressed effectively, and did not resolve the programmatic conclusions eventually found

by the NRC. In contrast, system engineering provided generally good support to address

emergent issues. The procurement engineering program was excellent and had good

management oversight.

A lack of effective management involvement and oversight contributed to numerous

problems with engineering programs. Important check valves were omitted from the IST

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program, the MOV program was not adequately completed within the required time, and

significant errors were made in the OCL process that resulted in the improper downgrading

of safety related equipment. Some key engineering procedures were nnt in the safety

review process nor were they followed during the downgrading of safety related

components. Management failed to effectively establish, communicate, and enforce

adequate engineering standards and provided poor oversight to correcting problems

identified through Quality Assurance audito. As a result of the problems noted above, GPU

conducted a thorough Engineering Corrective Action Program Assessment Team (ECAPAT)

review, which confirmed inadequate management involvement as an underlying root cause.

A program to expand the evaluation scope and implement corrective actions was ongoing

as the period ended.

Design control weaknesses were identified with calculations. Nonconservative inputs and

assumptions were used in the analysis to support Emergency Core Cooling System (ECCS)

switchover to the reactor building sump under post accident conditions. As a result, the

ECCS was found to be inoperable. Calculations were informally addressed in docume'its

such as memoranda, technical data reports, ano plant / engineering evaluations that did not

comply with established engineering procedures. Circuit breaker testing (IEEE standards)

for certain molded case circuit breakers was not performed, and there were numerous

discrepancies noted in the Final Safety Analysis Report (FSAR), drawings, design basis

documents, and procedures. In additicn, a previously identified unreviewed safety

question regarding the net positive suction head for decay heat removal and building spray

pumps was not addressed in a timely manner. The quality of engineering / licensing

packages submitted to the NRC was mixed. While the submittals were generally timely,

they usually required additional information and were sometimes technically weak.

In contrast, strengths were observed in system engineering and with the procurement

program. System engineers addressed emergent issuer well, including providing prompt

support for operability determinations. Equipment was maintained well, with prompt

attention to resolve identified safety issues. Identification of improperly wired PORV issue

was the result of diligent review and questioning by an engineer. The procurement

engineering documents provided clear descriptions of each procurement item.

The engineering area is rated Category 3

V.

PERFORMANCE ANALYSIS PLANT SUPPORT

Performance in the plant support functional area resulted in a good level of safety

performance. Overall performance in iadiological controls was effective; however, !ssues

regarding high radiation area controls and contamination control persisted. Emergency

preparedness exercise performance results continued to be mixed. Overall performance in

the security program improved, especially in the area of problem identification and

resolution.

Overall performance in radiological controls was effectiva. Activities involving ALARA,

radioactive waste management and transportation, radiological effluents, and

environmental monitoring were implemented well, especially ALARA planning for high dose

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evolutions. However, some performance problems occurred, especially during the refueling

outage. inadequate procedural guidance and supervisory involvement, coupled 19f1 an

unanticipated contamination level environment, contributed to a significant hot particle skin

contamination.- High radiation area control issues arose early and late in this cycle, and

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were repetitive from the last cycle. Weaknesses in the establishment and maintenance of

containinated areas and in the radiological survey program were identified.

Performance in the emergency preparedness program area was mixed. Although good

program content was noted, implementation in the March 1997 exercise was poor.

Exercise performance weaknesses included a failure to recognize and classify a General

Emergency condition. Ineffective management attention and involvement to the EP area

contributed to this poor exercise performance. A remedial emergency preparedness (EP)

exercise was required. Improvement was noted in performance during the remedial

exercise.

The security program was effectively implemented with continued strong management

support as evidenced by upgrades and enhancements to the program. The controls for

identifying, resolving, and preventing security program problems were effective.

An effective fire protection and prevention program continued to be implemented as

evidenced by routine observations by inspectors. The problems with emergency lighting,

identified during the previous cycle, were corrected.

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Housekeeping was generally good. However, a period of poor housekeeping occurred

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during the refueling outage, involving miscellaneous debris on the floors in the reactor

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building. There was improvement near the end of this cycle.

The Plant Support area was rated a Category 2.

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Enclosure 2

THREE MILE ISLAND SALP 12 MONTH

INSPECTION PLAN

INSPECTION

TITLE / PROGRAM AREA

PLANNED

TYPE INSPECTION

DATES

COMMENTS

IP 86750

Solid Radioactive Waste Management and

4/20/98

Core Inspection

Transportation of Radioactive Materials

IP 62706

Maintenance Rule Inspection

5/18/98

Core inspection

IP 81700

Physical Security Program

6/15/98

Core Inspection

IP 92903

Engineering Followup

6/15/98

Regional Initiative

Legend:

IP - Inspection Procedure

T1 - Temporary Instruction

Core Inspection

- Minimum NRC Inspection Program (mandatory at all plants)

RegionalInitiative - Additional Inspection Effort Planned by Region i

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