ML20135B090

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Insp Rept 50-289/96-06 on 960804-0928.Violations Noted.Major Areas Inspected:Plant Operations,Engineering,Maint & Plant Support
ML20135B090
Person / Time
Site: Crane Constellation icon.png
Issue date: 11/14/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20135B071 List:
References
50-289-96-06, 50-289-96-6, NUDOCS 9612040162
Download: ML20135B090 (18)


See also: IR 05000289/1996006

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U. S. NUCLEAR REGULATORY COMMISSION

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REGION I

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- Docket No.

50-289

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License No.

DPR-50

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Report No.

96-06

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Licensee:

GPU Nuclear Corporation

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Facility:

Three Mile Island Station, Unit 1

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Location:

P.O. Box 480

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Middletown, PA 17057

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Dates:

August 4,1996 - September 28,1996

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inspectors:

Samuel L. Hansell, Senior Resident inspector

Dan E. Billings, Resident inspector

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Approved by:

Peter W. Eselgroth, Chief

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Reactor Projects Section No. 7

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9612040162 961114

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ADOCK 05000289

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EXECUTIVE SUMMARY

Three Mile Island Nuclear Power Station

Report No. 50-289/96-06

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 8 week period of resident inspection

for unit 1.

Plant Operations

An improvement was noted in the area of operability determinations. Senior reactor

operators (SROs) identified and properly dotamented a degradation of Auxiliary Building

and Fuel Handling Building Ventilation (ABFHV) system flow. The ABFHV flow dropped

below the Technical Specification minimum value during the routine purge of the Reactor

Building. The shift SRO entered the applicable TS Limiting Condition for Operation (LCO)

and initiated efforts to troubleshoot the problem (Section 01.3).

Plant operations performed and implemented multiple detailed on-line safety risk

assessments for planned safety related equipment outages. The applicable system

Technical Specification limiting conditions for operation were entered and exited correctly

for the equipment outage times (Section 01.3).

An area for improvement was noted for the senior reactor operator's lSROs) review and

understanding of a maintenance work activity and the associated impact on plant

operation. A Shift SRO authorized an emergency feedwater (EFW) controller pushbutton

module removal without a complete understanding of the module's impact on the controller

operation. The diligence of the system engineer ultimately resulted in the correct

understanding of the EFW module operation (Section 01.2).

Licensed operators were very knowledgeable about the decay heat pump generic minimum

flow concerns. The operators' had an excellent working knowledge of the small break loss

of coolant accident (SBLOCA) emergency operating procedure (EOP). The SBLOCA EOP

provided clear and concise written directions for the operators (Section E1.1).

Maintenance

The maintenance and surveillance test activities observed during this inspection were

performed satisfactorily and demonstrated that the associated systems could perform their

design safety functions (Section M1.1).

The weekly component vibration monitoring program, not required by the IST program,

was an example of an excellent maintenance initiative to detect and correct safety related

equipment problems before the component fails or becomes inoperable. The mechanical

maintenance workers' excellent attention tc, detail resulted in the replacement of the pump

without impacting the other safety related equipment in the river water screenhouse

(Section M1.1).

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Enaineerina

The TMl engineering response to the Crystal River decay heat pump minimum flow safety

issue was comprehensive, thorough, and demonstrated management's commitment and

perseverance to resolve the generic safety issue (Section E1.1).

Engineering management promptly addressed a potential design concern related to the

safety related decay river cooling water system. The immediate and long term system

operability concerns were addressed by a detailed plant review group evaluation and

subsequent engineering reviews (Section E1.2).

Plant Support

TMI identified a repeat problem related to the failure to control a posted high radiation

barrier. This issue is considered a violation of the Unit 1 Technical Specifications. The

immediate corrective actions were comprehensive (Section R2.1).

The site investigation team performed a detailed, thorough, and timely review of the high

radiation barrier incident. Plant Management support was meaningful and focused

significant resources on the incident to resolve the recent repeat work problems (Section

R 2.1 ).

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TABLE OF CONTENTS

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EX EC UTI VE S U M M A RY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

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TABLE O F CO NT EN T S . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iv

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l. Operations

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Conduct of Operations (71707)

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01.1 General Comments

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01.2 Operability of Emergency Feedwater Equipment / Systems

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01.3 Operability of Auxiliary Building Ventilation Equipment / Systems . . 2

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11. Maintenance

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Conduct of Maintenance (62707,61726)

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M 1.1 General Comments

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Ill . Engine ering . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

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Conduct of Engineering (37551) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

E1.1

TMI Response to the Crystal River Decay Heat Pump Minimum

Flow issue (37 5 51 ) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

E1.2 Operability of the Decay River Water System (37551)

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IV. Plant Support

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R2

Status of RP&C Facilities and Equipment . . . . . . . . . . . . . . . . . . . . . . . 6

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R2.1

(Opened VIO, 50-289/96-06-01) Loss of Controls For a High

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Radiation Area (92904)

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P3.1

Emergency Plan Procedures and Documentation (71750)

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M a nage m e nt Me eting s . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

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Exit Meeting Summary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

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PARTIAL LIST OF PERSONS CONTACTED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 11

ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 12

LIST OF ACRO NYMS U SED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

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Report Details

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Summarv of Plant Status

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Unit 1 remained at 100% power throughout the inspection period.

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l. Operations

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Conduct of Operations (71707)'

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01.1 General Comments

Using Inspection Procedure 71707, " Plant Operations," the inspectors conducted frequent

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reviews of ongoing plant operations. In general, the conduct of operations was

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professional and safety-conscious; specific events and noteworthy observations are

detailed in the section below. Improved Technical Specification (TS) operability

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determinations and documentation by the shift senior reactor operators (SROs), were noted

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for the emergency feedwater (EFW) and Auxiliary Building ventilation work activities.

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The operations department performed and implemented multiple detailed on-line safety risk

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assessments for planned safety related equipment outages. The applicable system

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Technical Specification limiting conditions for operation were entered and exited correctly

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for the equipment outage times.

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O 1.2 Operability of Emeraencv Feedwater Eauioment/ Systems

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Inspection Scope

An area for improvement was noted during the SRO review of the EFW control module, EF-

V-30A, work package. The flow control module was removed from the main control panel

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to allow the instrumentation and control (l&C) technicians to perform a routine cleaning

and inspection of the controller pushbutton and spring assembly, in the past two years,

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the controllers had experienced intermittent problems when the operators swapped the

controllers from the automatic to manual mode of operation.

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Observations and Findinos

The shift SRO authorized the work activity without a complete understanding of the

operational impact of the I&C work in relation to the EFW module. It was not clear to the

SRO if the controller would swap from the normal automatic mode to a manual mode of

operation when the l&C technician removed the pushbutton assembly. The SRO contacted

the system engineer to determine the correct controller operation with the pushbutton

assembly removed from the controller.

' Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized

reactor inspection report outline. Individual reports are not expected to address all outline

topics.

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After a review of the EFW logic prints and associated technical documents, the system

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engineer informed the shift SRO that the EFW controller would remain in the automatic

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mode if the pushbutton assembly was removed. However, to verify the correct EFW

response the system engineer contacted Foxboro, the flow controller vendor. The vendor

informed the engineer that the EFW flow controller could switch from automatic to the

manual control mode when removing and installing the pushbutton assembly. The updated

information was provided to the control room personnel. The diligence of the system

engineer ultimately resulted in the correct understanding of the EFW flow control module

operation,

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Conclusions

An area for improvement was noted for the senior reactor operator's review and

understanding of a maintenance work activity and the associated impact on plant

operation. One example was noted when a shift SRO authorized an emergency feedwater

controller pushbutton module removal without a complete understanding of the module's

impact on the controller operation. The diligence of the system engineer ultimately

resulted in the correct understanding of the EFW module operation

01.3 Operability of Auxiliary Buildina Ventilation Eauioment/ Systems

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Insoection Scoce

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An improvement was noted in the area of the SROs' Technical Specification equipment

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operability determinations. The SROs identified and properly documented a degradation of

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Auxiliary Building and Fuel Handling Building Ventilation (ABFHV) system flow. The

ABFHV flow dropped below the TS minimum value during the routine purge of the Reactor

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Building.

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Observations and Findinas

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On August 7,1996, control room operators' responded to a plant computer ABFHBV low

flow alarm. The ventilation low flow alarm was received after the initiation of the Reactor

Building (RB) purge system in preparation for a routine tour and maintenance activities.

The ABFHBV exhaust low flow alarm was received when total flow dropped to 99,160

cubic feet per minute (CFM). The shift SROs declared the system inoperable and entered

TS # 3.15.3.3b. An event or near miss capture form (ENMCF) was initiated to document

the problem and initiate a root cause evaluation for the event.

The inspectors reviewed the ABFHBV control room flow recorder, SRO log, RB purge

procedure and associated TSs. The shift SRO entered the applicable TS Limiting Condition

for Operation (LCO) when flow dropped below 100,580 CFM. The SRO log included the

same ABFHBV out of service time when compared to the flow recorder strip chart

readings. The SRO promptly documented the abnormal occurrence with an ENMCF to

ensure the problem was evaluated to determine the reason for the flow change. The

ventilation flow returned to normal after the RB purge system was secured.

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Conclusion

An improvement was noted in the area of operability determinations. SROs identified and

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properly documented a degradation of the ABFHBV system flow. The flow dropped below

the Technical Specification minimum value during the routine purge of the Reactor Building.

The shift SRO entered the applicable TS Limiting Condition for Operation (LCO) and

initiated efforts to troubleshoot the problem.

11. Maintenanc_gt

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Conduct of Maintenance (62707,61726)

M 1.1 General Comments

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Insoection Scoce

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The inspectors observed all or portions of the following maintenance and surveillance work

activities:

Job Order No. 121455, " Clean and Inspect EF-V-30A Hand Auto Controller."

Job Order No. 126097, " Troubleshoot the Main Condenser Offgas Radiation

Monitor RM-A 15."

Job Order No. 123250, " Lubricate the Feedwater Control Valves FW-V-

17A/B."

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Job Order Nos. 126111 and 126112, " Nuclear River Water Pump NR-P-1C

Pump High Vibration and Overhaul."

Electrical Maintenance Procedure E-1, " Vibration Monitoring for the River

Water Pumps."

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Surveillance Procedure 1303-3.1, " Control Rod Movement."

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Surveillance Procedure 1303-5.1, " Reactor Building Emergency Cooling and

Isolation System Logic Channel and Component Test."

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Observations and Findinos

The electrical maintenance routine vibration monitoring of safety related equipment resulted

in the early detection of a problem related to the nuclear river (NR) water pump, NR-P-1C.

The component vibration readings, not required by the inservice test (IST) program, were

an example of an excellent initiative by the maintenance department to detect and correct

equipment problems before the component fails or becomes inoperable.

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The inspector observed a significant portion of the mechanical maintenance pump repair

activities. The pump shaft and impeller were removed and replaced with new parts. The

location of the pump resulted in very limited work space for the maintenance mechanics to

remove the long pump column and shaft sections. The workers excellent attention to

detail resulted in the replacement of the pump without impacting the other safety related

equipment in the river water screenhone.

The emergent pump work was prioritized appropriately based on the significance of the

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safety related cooling water pump with respect to the previously planned work activities.

The plant risk associated with the out of service pump was low due to the fact that the

degraded pump was not required to be operable by Technical Specifications.

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Conclusions

The maintenance and surveillance test activities observed during this inspection were

performed satisfactorily and demonstrated that the associated systems could perform their

design safety functions.

The extra component vibration readings, not required by the IST program, were an example

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of an excellent initiative by the maintenance department to detect and correct equipment

problems before the component fails or becomes inoperable. The mechanical maintenance

workers' excellent attention to detail resulted in the replacement of the pump without

impacting the other safety related equipment in the river water screenhouse.

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E1

Conduct of Engineering (37551)

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TMI Response to the Crvstal River Decay Heat Pumo Minimum Flow issue (37551)

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Inspection Scope

A generic issue was raised at the Crystal River (CR) nuclear power plant related to the

decay heat (DH) pump design minimum flow capabilities. Based on the most recent

concerns TMI and CR have initiated a DHP minimum flow test with at an independent test

facility. The spare TMI DH pump was selected to perform a simulated minimum flow test

that would be representative of the post small break loss of coolant accident (SBLOCA)

conditions. As of October 21,1996, the pump had run for twelve days without any

unexpected problems.

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Observations and Findinas

TMl's two low pressure injection pumps are manufactured by Worthington and are similar

to the CR design. A difference is the minimum flow: at TMI the flow is 125 gallons per

minute (GPM) compared to the 80 GPM at CR. The pumps are single stage centrifugal

pumps rated at 3000 GPM at 151 pounds per square inch (psig). According to the TMI

updated final safety analysis (UFSAR) Chapter 6.1-4, the pumps can operate indefinitely at

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shutoff head with the 125 GPM minimum flowrate. Also, in response to Bulletin No.

88-04, TMl noted that the operation of the pumps in the low flow mode would last no

more than six hours under actual ECCS operation. TMI engineering is currently involved

with this issue through the Babcock and Wilcox owners group and have attended the

recent meetings in NRC Headquarters about the Bulletin No. 88-04 issue.

The inspectors reviewed the decay heat system section of the UFSAR, emergency

operating procedures (EOPs), and the plant review group (PRG) evaluation of the issue.

The TMl DH pumps start on_ low reactor coolant system (RCS) pressure at 1600 psig and

again at 500 psig, and a RB pressure of 4 psig. The TMl EOPs have the operators secure

the DH pumps if they started at 1600 psig RCS pressure OR 4 psig RB pressure and the

event is a SBLOCA that results in sufficient high pressure injection (HPI) flow and a slow

drop in RCS pressure. The pumps would receive an automatic signal to start when RCS

pressure dropped to 500 psig and begin injecting at approximately 250 psig.

All control room operators were familiar with the CR issue and understood how the TMI DH

pumps were designed. The operators' were very knowledgeable about the DH pump

automatic start signals and the expected system response to a SBLOCA. They had an

excellent working knowledge of the SBLOCA EOPs and understood the operational

limitations for the DH pumps. The EOPs provided clear direction for the operators about

the DH pump starting and stopping requirements.

The PRG evaluation of the fr:,ue concluded that the DH pumps were operable. The

determination was based upon the past operating history of the pumps and the fact that

the TMI pumps have been maintained in very good condition. The TMI pumps do have an

intermittent vibration condition that Engineering is trying to resolve. The PRG also

proposed four alternative flowpaths to maximize the DH system flow if the plant

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experienced a SBLOCA and the RCS suction path was unavailable for long term decay heat

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removal operation. Management's decision to perform the pump minimum flow test

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showed their willingness to completely resolve this potential safety issue.

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Conclusions

The TMI engineering response to the Crystal River decay heat pump minimum flow concern

was comprehensive, thorough, and demonstrated management's commitment and

perseverance to resolve the generic safety issue.

Licensed operators were very knowledgeable about the decay heat pump generic minimum

flow concerns. The operators' had an excellent working knowledge of the small break loss

of coolant accident emergency operating procedure. The SBLOCA EOP provided clear and

concise written directions for the operators.

E1.2 Operability of the Decav River Water System (37551)

A potential safety concern was raised by engineering related to the decay river (DR)

cooling water flow measurement. The decay heat river water flow data could be

unconservative due to the location of the annubar flow instrument near a pipe elbow, if

the DR system flow indicated higher than actual flow, then the measured flow could be

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less than the Technical Specification requirement. Increasing flow above current levels

raises issues with emergency diesel loading. Engineering management recognized the

potential safety significance of the concern and convened a plant review group (PRG)

meeting to evaluate the system operability and if the issue met the reportability criteria in

administrative procedure AP-1044. A material nonconformance report (MNCR) was

submitted to document the potential safety concern and track the recommended corrective

actions.

The PRG evaluated the issue on August 20,1996, and determined that a concern may

exist under the worst case conditions assumed in the updated final safety analysis report

(UFSAR). The "as found" DR system data that was presented to the PRG showed that the

heat exchanger fouling, strainer differential pressure (DP), river water level and river water

temperature did not exceed the design limits. Considering the above, the PRG determined

that the decay river system was operable and the issue was not reportable. The Shift

Engineer (SE) was instructed to monitor and log the DR plant conditions to assure that the

system does not approach the safety analysis assumptions.

The inspectors verified that the SEs understood the DR safety concern and that the DR

data was properly monitored and logged. In addition, the associated DR parameter

computer alarm setpoints were adjusted to alert the control room personnel before the

system deigri limits were exceeded. The PRG meeting conducted a detailed review of the

potential safety concern and recommended appropriate actions to ensure the DR system

operability would be considered if a key design parameter exceeds a value used for the

safety analysis calculations. The PRG also assigned engineering an action item to

determine the proper flow alignment during the routine system flow test.

In summary, engineering management promptly addressed a potential design concern

related to the safety related decay river cooling water system. The immediate and long

term system operability concerns were addressed by a detailed plant review group and

engineering evaluation.

IV. Plant Support

R2

Status of RP&C Facilities and Equipment

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R2.1

(Opened VIO. 50-289/96-06-01) Loss of Controls For a Hiqh Radiation Area

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(92904)

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Inspection Scoce

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The inspectors reviewed a licensee-identified incident that occurred on August 7,1996,

involving a barrier to a posted high radiation area (HRA) in the Auxiliary Building (AB) to

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determine the effectiveness of the licensee's root cause investigation and proposed

corrective actions. Postings on the barrier were appropriate and cautioned workers that

the barrier was required by TS. Actual dose rates in the area varied from 300 to 500

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millirem per hour on contact and 90 mrem at 30 centimeters. The barrier was estimated

out of position for approximately three hours. The highest radiation dose received by a

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plant worker was approximately 6 millirem on the day of the moved barrier.

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b.

Observations and Findinos

The HRA and contamination postings around the AB 'B' emergency safeguards vault area

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were changed on dayshift to support the plant preservation activities. The activities

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included the floor scabbling and painting work in the 'B' decay heat removal and building

spray vault areas. The radiological controls technician requested that the contaminated

area and high radiation area postings be extended to the boundary of the entire area to be

scabbled. The expanded boundaries provided a more convenient working area for the

preservation activities. The group radiological control supervisor (GRCS) approved the

posting change in the 'B' emergency safeguards vault area. After completion of the floor

scabbling work activities at approximately 2:30 p.m., the preservation crew left for the day

with the high radiation area gate in the proper position.

At approximately 5:00 p.m. a second dayshift GRCS inspected the expanded postings

surrounding the 'B' emergency safeguards vault area. The GRCS specifically remembered

looking at the two high radiation area swing gates around the work area access points sr.d

determined that the posting and gates were properly positioned. At approximately 8:00

p.m., the high radiation area swing gate at the west access point step off pad was found

to be moved 180 degrees and did not provide a barrier to the area, as required by the TMl

Technical Specification 6.12.1.a. An Auxiliary Operator (AO) noticed the gate open and

inforrned the in plant shift foreman (SF). The SF immediately notified the duty GRCS of the

situation. The GRCS and SF photographed the HRA gate in the as found condition, the

gate was returned to its proper position, and a second photograph was taken to capture

the HRA barrier condition. TMI management was informed of the incident, a radiation

survey was performed of the AB area, and an event near miss and capture form was

initiated to document the problem.

On August 8,1996, TMl initiated an investigation to determine the cause of the incident.

The investigative team consisted of a representative from nuclear safety assessment

(NSA), security, operations, maintenance, and radiological controls departments. Based on

the GRCS verification and AO recognition of the HRA barrier, the Team determined that the

high radiation barrier was prGpped open between 5:00 p.m. and 8:00 p.m. on August 7th.

Computer printouts were obtained that listed all of the personnel signed on an RWP (18

workers) and all of the personnel that key carded through the AB vital area doors (43

workers) between the hours of 5:00 p.m. and 8:00 p.m. The investigation team

conducted individual interviews with the personnel that accessed the AB. Ir* addition,

plant walkdowns of the 'B' emergency safeguards vault area were performed with the

GRCS that inspected the area at 5:00 p.m. and the AO and SF that found the gate propped

open at 8:00 p.m. Nobody that was in the AB on August 7th admitted to moving or

knowing who moved the HRA gate during the three hour time period.

The licensee conducted an investigation and critique of this event and determined that one

root cause that had contributed to this event was a lack of attention to detail by personnel

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working in the room. Since the time of this event, the licensee has further investigated

and analyzed the failures and implemented some corrective actions. These actions

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included providing a review of the event to all operations personnel, reviewing the

corrective actiors taken as a result of previous similar incidents, evaluating all HRA

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postings and barriers for " user friendliness", and coordination of feedback from employees

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on the condition and ease of use for HRA barriers.

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The inspectors interviewed plant workers independently to determine the facts about the

incident. The inspectors determined that the employees understood their responsibilities

for ensuring that radiological controls and barriers were in place when they entered and

exited a radiological area. Similar to the GPUN investigation, nobody admitted that they

moved or knew who moved the HRA gate on August 7,1996. It appears that there were

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three probable reasons for the moved barrier: 1) the barrier made it difficult to remove

protective clothing at the contaminated and HRA boundary; 2) a plant worker moved the

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barrier to transport equipmant into or out of the contaminated /HRA: and 3) an unknown

person intentionally opened the HRA swing gate.

The inspectors also reviewed the maintenance activities performcd in the AB on August

7th. The maintenance tasks that were performed in the AB did not require the workers to

pass through the HRA boundary on the 281 foot elevation. A review of the personnel

exposure on the day of the moved the barrier revealed that the maximum individual dose

was 6 millirem.

The site investigation team performed a detailed and thorough review of the incident. The

Team was assembled promptly after the facts about the issue were known Management

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recognized the significance of the repeat HRA barrier problems and assigned the most

knowledgeab!e personnel onsite to perform the root cause investigation. The investigation

was initiated immediately after the Team was formed in an attempt to increase the

probability that the person and reason for the moved barrier would be determined. As part

of the interview process, personnel were asked for suggestions and recommendations to

improve the TMl radiological controls program with respect to high radiation area posting

and control. The following is a summary of the comments:

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The vast majority of suggestions by both radiological controls and non-

radiological controls personnel were to eliminate where possible, or reduce to

a minimum, overly conservative high radiation area postings within TMI. The

incident described in the event capture form involved a high radiation area

posting that was in a 2 mr/hr radiation field.

Use of " turnstiles", instead of swing gates, for high radiation area barriers

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would ensure that a physical barricade is in place at all times.

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Installation of devices similar to limit switches on the swing gates that would

cause a light or buzzer to energize when the gate was open.

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Placement of video cameras at high radiation area gate locations.

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Increase TMl worker sensitivity to company and regulatory concerns with

repeated high radiation area barrier violations, through short training

discussions, videotapes, or shop meetings.

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c.

Conclusions

The immediate corrective actions were comprehensive. Because of the repeat problem,s

related to the control of high radiation barriers, this latest example is considered a violation

of the TMI Unit 1 TS 6.12.1.a. (VIO 50-289/96-06-01).

The site investigation team performed a detai!ed and thorough review of the incident. The

team was assembled promptly after the facts about the issue were known. Plant

Management support was meaningful and focused significant resources on the incident to

resolve the recent repeat work problems.

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P3.1

Emeraency Plan Procedures and Documentation (71750)

The Region i emergency preparedness inspector performed an in-office review of the

revisions to the TMI emergency plan irnplementing procedures. Based on your

determinations that the changes did not decrease the overall effectiveness of your

emergency plan, and that it continues to meet the standards of 10 CFR 50.47(b) and the

requirements of Appendix E to Part 50, NRC approval is not required. Our initial review of

these changes indicates them to be in accordance with 10 CFR 50.54(q). Implementation

of these changes will be subject to inspection to confirm that they have not decreased the

overall effectiveness of your emergency plan. A list of the specific revisions that were

reviewed is included below. The inspector concluded that the revisions did not reduce the

effectiveness of the E-Plan and were acceptable.

EMERGENCY PLAN AND IMPLEMENTING PROCEDURES REVIEWED

Document

Document Title

Revision

EPIP-TMI .01 Emergency Classification and Basis

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EPIP-TMf .07 Activation of the RAC

2

EPIP-TMI .16 Contaminated injuries

4

EPIP-TMI .27 Emergency Operations Facility

7

EPIP-TMI .28 Activation of the TSC

6

TEP-ADM-1300.02 Emergency Preparedness Training

1

TEP-ADM-1300.04 Administration of the TMl Initial

Response and Emergency Support

Organization Duty Roster

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Manaaement Meetinas

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Exit Meeting Summary

At the conclusion of the reporting period, the resident inspector staff conducted an exit

meeting with TMl management on October 15,1996, summarizing Unit 1 inspection

activities and findings for this report period. TMl staff comments concerning the issues in

this report were documented in the applicable report section. No proprietary information

was identified as being included in the report.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Knubel, Vice President, TMI

  • M. Ross, Director, Operations and Maintenance

L. Noll, Plant Operations Director

R. Maag, Plant Maintenance Director

D. Etheridge, Radiological Controls / Occupational Safety Director

J. Schork, Regulatory Affairs

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J. Wetmore, Manager, Regulatory Affairs

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D. Hosking, NSA Manager

G. Skillman, Technical Functions Site Director

P. Walsh, Engineering Director

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R. Hess, Training Manager

  • senior licensee manager present at exit meeting on October 15,1996.

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NRC

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J. Norris, TMl Project Manager, NRR

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INSPECTION PROCEDURES USED

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IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 37551:

Onsite Engineering

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lP 71750:

Plant Support Activities

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IP 92904:

Followup - Plant Support

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ITEMS OPENED, CLOSED, AND DISCUSSED

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Ooened

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50-289/96-06-01, " Loss of Controls For a High Radiation Area" (VIO).

Closed

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None

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Updated

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LIST OF ACRONYMS USED

AB

Auxiliary Building

AEOF

Annex to the Emergency Operations Facility

ALARA

As low As Reasonably Achievable

ASME

American Society of Mechanical Engineers

CDF

Core Damage Frequency

CEDE

Committed Effective Dose Equivalent

CR

Control Room

CFR

Code of Federal Regulations

DBD

Design Basis Documents

ECCS

Emergency Core Cooling System

ED

Emergency Director

EDG

Emergency Diesel Generator

EFW

Emergency Feedwater

EOF

Emergency Operations Facility

ENMCF

Event or Near Miss Capture Form

EPIP

Emergency Plan and implementing Procedure

ESF

Engineered Safety Feature

HEPA

High Efficiency Particulate

HRA

High Radiation Area

IFl

Inspection Followup Item

IPE

Individual Plant Evaluation

IR

inspection Report

IST

Inservice Testing Program

JO

Job Order

JPM

Job Performance Measure

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LCO

Limiting Condition of Operation

LER

Licensee Event Report

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MNCR

Material Nonconformance Report

MSA

Mine Safety Appliance

NCV

Non-Cited Violation

NI

Nuclear Instrument

NRC

Nuclear Regulatory Commission

NSA

Nuclear Safety Assessment

NVLAP

Nuclear Voluntary Laboratory Accreditation Program

ODCM

Offsite Dose Calculation Manua!

OSC

' Operations Support Center

PAS

Post Accident Sample

PCR

Procedure Change Request-

PPB

Part per Billion

PPM

Part per Million

PRA

Probabilistic Risk Assessment

PRG

Plant Review Group

QV

Quality Verification

RAC

Radiological Assessment Coordinator

RCA

Radiological Control Area

RCS

Reactor Coolant System

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RP

Radiation Protection

RSP

Remote Shutdown Panel

RWP

Radiation Work Permits

SALP

Systematic Assessment of Licensee Performance

SF

Shift Foreman

SRO

Senior Reactor Operator

SS

Shift Supervisor

Tl

Temporary Instruction

TLD

Thermoluminescent Dosimeter

TS

Technical Specification

TSC

Technical Support Center

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved item

VIO

Violation

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