IR 05000341/2020004
ML21041A276 | |
Person / Time | |
---|---|
Site: | Fermi |
Issue date: | 02/10/2021 |
From: | Nestor Feliz-Adorno NRC/RGN-III |
To: | Peter Dietrich DTE Electric Company |
References | |
IR 2020004 | |
Download: ML21041A276 (25) | |
Text
February 10, 2021
SUBJECT:
FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2020004
Dear Mr. Dietrich:
On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On January 19, 2021, the NRC inspectors discussed the results of this inspection with Mr. E. Olson, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.
No findings or violations of more than minor significance were identified during this inspection.
This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Docket No. 05000341 License No. NPF-43
Enclosure:
As stated
Inspection Report
Docket Number: 05000341 License Number: NPF-43 Report Number: 05000341/2020004 Enterprise Identifier: I-2020-004-0062 Licensee: DTE Electric Company Facility: Fermi Power Plant, Unit 2 Location: Newport, MI Inspection Dates: October 01, 2020 to December 31, 2020 Inspectors: T. Briley, Senior Resident Inspector T. McGowan, Resident Inspector V. Myers, Senior Health Physicist R. Ng, Project Engineer T. Taylor, Resident Inspector Approved By: Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects Enclosure
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
List of Findings and Violations
No findings or violations of more than minor significance were identified.
Additional Tracking Items
None.
PLANT STATUS
Unit 2 began the inspection period at rated thermal power. On November 18, 2020, the unit was down powered to 94 percent rated thermal power for planned hydraulic control unit maintenance. The unit was returned to rated thermal power the following day. On November 20, 2020, the unit was down powered to 74 percent rated thermal power for a planned control rod pattern adjustment. The unit was returned to rated thermal power the following day. The unit remained at or near rated thermal power for the remainder of the inspection period.
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19),resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.
REACTOR SAFETY
71111.01 - Adverse Weather Protection Seasonal Extreme Weather Sample (IP Section 03.01)
- (1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of the cold weather winter months for the following systems:
- Plant heating steam, including secondary containment isolations
Impending Severe Weather Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe weather due to a high wind advisory on November 19, 2020
71111.04 - Equipment Alignment Partial Walkdown Sample (IP Section 03.01)
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Division 2 emergency diesel generators (EDG) 13 and 14 while EDG 11 was out of service for maintenance during the week ending October 10, 2020
- (2) Division 2 emergency equipment cooling water while the reactor core isolation cooling (RCIC) system was out of service for maintenance during the week ending November 7, 2020
- (3) Division 1 non-interruptible air system (NIAS) while Division 2 NIAS was out of service for maintenance during the week ending November 21, 2020
- (4) Division 2 emergency equipment service water (EESW) while Division 1 EESW was out of service for maintenance during the week ending December 5, 2020
Complete Walkdown Sample (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated system configurations during a complete walkdown of the Division 1 residual heat removal (RHR) system during the week ending October 31, 2020
71111.05 - Fire Protection Fire Area Walkdown and Inspection Sample (IP Section 03.01)
The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:
- (1) Auxiliary building first floor, Division 1 switchgear room during the week ending October 17, 2020
- (2) Auxiliary building basement, control rod drive pump room during the week ending October 17, 2020
- (3) Reactor building basement and sub-basement, north east quad during the week ending December 12, 2020
- (4) Circulating water pump house during the week ending December 12, 2020
71111.06 - Flood Protection Measures Inspection Activities - Internal Flooding (IP Section 03.01)
The inspectors evaluated internal flooding mitigation protections in the:
- (1) Relay room
- (2) Division 1 switchgear room
71111.07A - Heat Sink Performance Annual Review (IP Section 03.01)
The inspectors evaluated readiness and performance of:
- (1) EDG 13 lubricating oil, jacket water, and air coolant heat exchangers
71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance
Requalification Examination Results (IP Section 03.03) (1 Sample)
- (1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification program annual operating test administered between October 19 and November 20, 2020
71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance
Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)
- (1) The inspectors observed and evaluated a licensed operator requalification graded scenario in the control room simulator on October 8, 2020
71111.12 - Maintenance Effectiveness Maintenance Effectiveness (IP Section 03.01)
The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:
- (1) Reactor recirculation system during the week ending October 31, 2020
- (2) Reactor feedwater system during the week ending November 28, 2020
- (3) Safety relief valves during the week ending December 12, 2020
- (4) NIAS during the week ending December 5, 2020
- (6) Visual annunciator system during the week ending December 19, 2020
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)
The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:
- (1) Division 1 switchyard breaker GK and EDG 11 out of service for planned maintenance during the week ending October 10, 2020
- (2) RCIC system and offsite power Shoal line planned maintenance, and emergent work on combustion turbine generator (CTG) 11-1 with CTG 11-2 and 11-4 out of service during the week ending November 7, 2020
- (3) Emergent work on main turbine control system during the week ending December 31, 2020
71111.15 - Operability Determinations and Functionality Assessments
Operability Determination or Functionality Assessment (IP Section 03.01) (2 Samples)
The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:
- (1) Operability and functionality of RCIC following Division 1 high steam line flow master trip unit failure, as documented in condition assessment resolution document (CARD) 20-39104
- (2) Operability and functionality of EDG 11 following identification of a change in crankcase oil chemistry parameters, as documented in CARD 20-33238
71111.18 - Plant Modifications
Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)
(2 Samples)
The inspectors evaluated the following temporary or permanent modifications:
- (1) Condensate storage tank vortex suppressor installation (permanent)
- (2) Uninterruptible power supply 'B' logic and fuse sizing change (permanent)
71111.19 - Post-Maintenance Testing Post-Maintenance Test Sample (IP Section 03.01)
The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:
- (1) Reactor building outer railroad door testing following identification of a degraded seal during the week ending October 3, 2020
- (2) RCIC system testing following a planned maintenance outage during the week ending November 7, 2020
- (3) Reactor building ventilation radiation monitor testing following identification of spurious operation and trips during the week ending November 14, 2020
- (4) Division 2 NIAS system testing following planned maintenance during the week ending November 28, 2020
- (5) Recirculation pump 'B' differential pressure channel 'B' master trip unit (MTU) testing following planned MTU replacement during the week ending December 4, 2020
71111.22 - Surveillance Testing The inspectors evaluated the following surveillance tests:
Surveillance Tests (other) (IP Section 03.01) (1 Sample)
- (1) EDG 13 slow start surveillance testing during the week ending October 24, 2020
Inservice Testing (IP Section 03.01) (1 Sample)
- (1) Division 2 core spray auto actuation testing during the week ending
December 12, 2020 FLEX Testing (IP Section 03.02) (1 Sample)
- (1) N+1 Neptune pump testing during the week ending November 28, 2020
71114.04 - Emergency Action Level and Emergency Plan Changes Inspection Review (IP Section 02.01-02.03)
- (1) The inspectors completed an evaluation of submitted emergency action level and emergency plan changes on December 8, 2020. This evaluation does not constitute NRC approval.
71114.06 - Drill Evaluation Drill/Training Evolution Observation (IP Section 03.02)
The inspectors evaluated:
- (1) Emergency preparedness tabletop drill on October 8,
RADIATION SAFETY
71124.07 - Radiological Environmental Monitoring Program
Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)
- (1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples
Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)
- (1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program
GPI Implementation (IP Section 03.03) (1 Sample)
- (1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative program to identify incomplete or discontinued program elements
==71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage,
& Transportation==
Radioactive Material Storage (IP Section 03.01) (1 Sample)
- (1) Inspectors evaluated the licensees performance in controlling, labelling and securing radioactive materials
Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)
- (1) Inspectors walked down accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality
Waste Characterization and Classification (IP Section 03.03) (3 Samples)
The inspectors evaluated the licensees characterization and classification of the following radioactive waste shipments:
- (1) EF2-19-050, resin
- (2) EF2-20-040, torus paint chips
- (3) EF2-20-117, resin
Shipment Preparation (IP Section 03.04) (1 Sample)
The inspectors observed the preparation of the following radioactive material shipment:
- (1) EF2-20-120, resin shipped as Type B
Shipping Records (IP Section 03.05) (3 Samples)
- (1) EF2-19-050, resin shipped as LSA-II
- (2) EF2-20-040, torus paint chips shipped as LSA-II
- (3) EF2-20-117, resin shipped as Type B
OTHER ACTIVITIES - BASELINE
===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:
EP01: Drill/Exercise Performance (IP Section 02.12) ===
- (1) July 1, 2019 through September 30, 2020
EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)
- (1) July 1, 2019 through September 30, 2020
EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)
- (1) July 1, 2019 through September 30, 2020 BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
- (1) July 1, 2019 through September 30, 2020
OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)
- (1) July 1, 2019 through September 30, 2020 PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)
- (1) July 1, 2019 through September 30, 2020
71152 - Problem Identification and Resolution Semiannual Trend Review (IP Section 02.02)
- (1) The inspectors reviewed the licensees corrective action program for potential adverse trends that might be indicative of a more significant safety issue
Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) A sample of issues open in the corrective action program with operability being maintained via compensatory measure or pending some final action to update or change the design basis. The inspectors reviewed a partial modification to the condensate storage tank to address the potential for vortexing, a degraded valve in the lube oil system for EDG 14, and licensee follow up to an error in methodology regarding motor operated valve calculations that had been discovered during a prior NRC inspection.
71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)
- (1) The inspectors evaluated a control rod drive hydraulic system transient and licensees performance on November 14,
INSPECTION RESULTS
Observation: Semi-Annual Corrective Action Program Trend Review 71152 The inspectors noted a trend in organizational and programmatic issues entered into the corrective action program that did not have sustainable corrective actions. Several examples included, but were not limited to, the following:
- In May 2019, following a planned safety system maintenance outage for EDG 14, Nuclear Quality Assurance (NQA) identified several tube clamps taped to the wall in the EDG 14 room that had not been reinstalled as intended. The primary cause listed in the organizational effectiveness analysis that followed was inadequate field oversight. Specifically, it concluded that one field supervisor was not sufficient to oversee multiple major-scope jobs occurring in parallel. However, none of the corrective actions taken addressed the primary cause or the organizational issues which led to the breakdown during the EDG outage. The missing clamps ultimately did not impact EDG 14 operability.
- In February 2020, the licensee initiated CARD 20-21195 for some organizational effectiveness issues associated with execution and implementation of a planned safety system maintenance outage for EDG 13. The licensee determined the work delays were caused by issues with how the schedule was prepared, communication challenges between day and night shift and between departments, and the operations department not being formally part of the outage control center (OCC) staff. The corrective action was to revise a post-outage critique form which added some organizational effectiveness questions. However, the inspectors noted this corrective action did not address issues associated with the execution and implementation of system outages because the post-outage critique form was used following the completion of safety system outages.
- During the most recent refueling outage (i.e., from March to August 2020), the inspectors identified foreign material issues (mainly small cleanliness issues) during their primary containment closeout inspection. Most of the material was fairly easy to find or was discovered in a location that was easily accessible. During the prior refueling outage, inspectors also noted a large amount of material during their closeout inspections. Given the prior issues, the inspectors questioned the process the licensee employed to validate primary containment cleanliness prior to final closeout. In response, the licensee added a list of drywell areas and a reference to operations department cleanliness standards to a work order used by decontamination personnel. However, these actions were similar to those documented for a similar issue captured in May 2018 as CARD 18-23959. The inspectors questioned the effectiveness of implementing corrective actions that were similar to actions that were already in place and demonstrated to not address the issue during the most recent refueling outage.
The inspectors discussed their observations with licensee staff, who subsequently generated CARD 21-20263 to capture the issues. Through the discussions with licensee personnel, the inspectors learned that licensee staff had recently noted similar (but separate) issues regarding sustainability of corrective actions as part of a self-assessment. The inspectors will continue to routinely monitor CAP performance via the baseline inspection program.
EXIT MEETINGS AND DEBRIEFS
The inspectors verified no proprietary information was retained or documented in this report.
- On January 19, 2021, the inspectors presented the integrated inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff.
- On October 22, 2020, the inspectors presented the radiation protection inspection results to Mr. R. LaBurn, Radiation Protection Manager, and other members of the licensee staff.
- On December 8, 2020, the inspectors presented the emergency action level and emergency plan changes inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff.
- On December 15, 2020, the inspectors presented the licensed operator requalification program annual operating test results inspection results to Mr. A. Spencer, Licensed Operator Requalification Program Lead, and other members of the licensee staff.
DOCUMENTS REVIEWED
Inspection Type Designation Description or Title Revision or
Procedure Date
71111.01 Corrective Action 20-29557 NQA-First Level Escalation-Repeat Deficiencies with 08/24/2020
Documents Seasonal Readiness Activities
20-32239 Pri 4 Cold Weather Prep Work Order Not Scheduled 11/16/2020
Engineering TM-16-0025 Install One Temp Boiler and Provide Spare Connections for 11/08/2016
Changes a Second Temp Boiler
Miscellaneous MOP01-200 Severe Weather Guidelines 3
Procedures MWC16-100 Seasonal Readiness 1
Work Orders 51732374 Perform MWC16-100 Cold Weather System Readiness 03/20/2020
Review Checklists
71111.04 Calculations DC-6356 Stress and Seismic Analysis of the Reactor/Auxiliary A
Building CTI Nuclear Fan Coil Units
Corrective Action 20-31283 Damaged Labels - RBSB NW 10/15/2020
Documents 20-31377 Torus Room AZ 250 10/19/2020
20-31440 NRC Identified Condition, Insulation Repairs 10/20/2020
20-32269 NRC Identified Issue: The E1100F619A and E1100F619B 11/17/2020
have Local Manual Positioners but are Not Tracked by
Valve Lineups
20-32273 NRC Concern: Missing Label on P50R413A 11/17/2020
Drawings 6M721-2084 Diagram Residual Heat Removal (RHR) Division I BQ
6M721-2084 Diagram Residual Heat Removal (RHR) Division I BQ
6M721-5729-2 EECW Division II Functional Operating Sketch BD
6M721-5734 Emergency Diesel Generator System Functional Operating BL
Sketch
M-2015 Station and Control Air CS
M-4615 Interruptible and Non-Interruptible Control Air AH
M-5706-3 RHR Service Water Make-Up Decant and Overflow AH
Systems
M-5729-2 Emergency Equipment Cooling Water Division II BD
Miscellaneous Operator Logs Operations AUTOTOUR Logs - Reactor Building 0
Procedures 23.129 Station and Control Air 121
23.205 Division 1 RHR LPCI Standby Lineup Verification, 147
8A
Inspection Type Designation Description or Title Revision or
Procedure Date
23.208 RHR Complex Service Water Systems 129
71111.05 Fire Plans FP-AB-2-9b Auxiliary Building, Division 1 Switchgear Room, Zone 9, El. 3
613'6"
FP-AB-B-4b Control Rod Drive Pump Room, Zone 4, El. 562'0" 4
FP-CWPH-1-32 Circulating Water Pumphouse Zone 32 Elevation 58'6" 6
FP-RB-B-5b Reactor Building Basement Northeast Corner Room 4
Zone 5, Elevation 562'0"
71111.06 Engineering EF2-PRA-011 Internal Flood Walkdown Summary Notebook 0
Evaluations EF2-PRA-012 Fermi 2 Nuclear Power Station PRA Internal Flood Analysis 3
Notebook
71111.07A Calculations DC-5804 Diesel Generator Service Water Design Basis F
Requirements Calculation
Miscellaneous MES540001 EDG 11 Air Coolant Heat Exchanger Inspection Report 10/05/2020
MES54001 EDG 11 Jacket Cooling Heat Exchanger Inspection Report 10/05/2020
MES54001 EDG 11 Lube Oil Heat Exchanger Inspection Report 10/05/2020
71111.11A Miscellaneous Fermi 2020 LORT Annual Operating Test Summary Results 12/15/2020
71111.11Q Miscellaneous SS-OP-904-2001 Evaluation Scenario 2
71111.12 Corrective Action 17-25639 Management Review Committee (MRC) Cognitive Trend - 06/27/2017
Documents SRVs
18-20350 North Reactor Feed Pump Turbine Lube Oil Level High 01/16/2018
18-20351 N RFPT Turning Gear Engage Solenoid Valve (N21F111A) 04/30/2018
is Blowing By
18-23923 Received 5D28 South RFP/RFPT Shaft Trouble While 05/17/2018
Taking the N RFP Out of Service
19-20000 Unexpected Alarm During Startup of NRFPT 01/01/2019
19-20309 SRV 'A' (B2104F013A) Tail Pipe Temperature Elevated to 01/14/2019
~205F
19-20660 SRV 'J' Tail Pipe Temperature Elevated to ~212F 01/30/2019
19-21751 Need RF20 WO to Perform a Body Off Inspection of 03/06/2019
SRV 'A' due to Elevated Tailpipe Temperatures per CARD
19-20309
19-23939 2019 DBAI: MRFF Action Needed for Previously Closed 05/22/2019
CARD 17-23452
19-24545 Oil Surrounding Mechanical Seal on RRMG LO 06/17/2019
Inspection Type Designation Description or Title Revision or
Procedure Date
B3103C001D
19-28069 Excessive Carbon on Brushes and Intake 10/23/2019
20-00023 Bushing Broken on N2100-F006B SRFPT OTBD Seal 03/23/2020
Water TCV Outlet Isolation Valve
20-20091 Division 1 RHR Pump Room Dampers 01/06/2020
20-20099 Abnormal Noise/Indications from P50-F516A Solenoid 01/06/2020
20-21585 Time Delay Relay P50M832 Failed as Found Testing 02/12/2020
20-21602 Division 2 Control Air Compressor Failed PMT 02/13/2020
20-21659 Control Air Compressor PMT 02/14/2020
20-21688 Online Work Orders for Vendor Inspection of Recirc MG Set 02/14/2020
Brushes and Potential Stoning
20-21708 As-Found Condition of Division II NIAS Dryer 02/16/2020
20-21840 Division 2 Control Air Compressor Will Not Load 02/11/2020
20-21936 X4103F128 Excessive Scoring on Hydra Motor Shaft 02/20/2020
20-23975 Received 3D19 Annunciator System Trouble 12/16/2020
20-24502 VAS Total System Failure 04/14/2020
20-24779 VAS Multiplexor C Time Errors 04/19/2020
20-25054 Potential Common Cause Failure of VAS 04/23/2020
20-25856 Discharge Pressure is High Out of Spec for N RRMG Set 05/17/2020
Lube Oil Pump (B103C001A)
20-25881 B3103C001D PMT Unsatisfactory due to Vibration Level 05/18/2020
20-26161 Stopped and Backed Out of 27.129.04 05/27/2020
20-26271 Findings from Division 1 NIAS Air Dryer Troubleshooting 05/29/2020
20-26312 VAS Clock Signal Distortion Cause and Remediation 05/30/2020
20-26672 RRMG Set Lube Oil Level Challenges in Refuel Requires 06/08/2020
Add and Removal of Oil
20-26692 P603 VAS Alarm Check Malfunction and System Battery 06/08/2020
Low Voltage Warning
20-26723 Dual Indication for Open Damper X4103F115 06/10/2020
20-26772 Dual Indication for Open Damper X4103F103 06/10/2020
20-27423 Two of Four North and South RFPT Speed Indications in 06/29/2020
IPCS Erroneous
20-28723 UNSAT SRV Inspection 07/28/2020
Inspection Type Designation Description or Title Revision or
Procedure Date
20-29013 SRV 'A' Tailpipe Temperature Elevated Following RF-20 08/06/2020
Startup
20-29165 SRV 'M' Tailpipe Temperature Elevated Following RF-20 08/10/2020
Startup
20-30180 Abnormal Speed Changes on South RFPT 09/13/2020
20-30351 Learnings from Industry Responses for 20-30180, SRFPT 09/17/2020
Speed Anomaly
20-30443 Abnormal Speed Differential Between North and South 09/21/2020
20-30554 Three SRVs Removed in RF-20 Found Outside of 09/24/2020
As-Found Set-Point Tolerance
20-30779 Oil Leak 09/30/2020
20-32479 Trend CARD - B2104F013A Tailpipe Temperature Increase 11/25/2020
20-32730 Broken Insulation in Hydra Motor Electrical Housing 12/08/2020
Engineering Monthly Maintenance Rule Evaluation Report - Safety Relief 10/09/2020
Evaluations Valve - September 2020
Miscellaneous RHR Complex Ventilation (X4103) System Performance 09/20/2020
Monitoring Plan
P5002 (NIAS) System Monitoring Plan 03/15/2019
ACMP 20-007 SRV 'A' & 'M' Weeping 1
MMR 02 Maintenance Rule Program Description 6A
MMR 10 Maintenance Rule, Monitoring 18A
MMR APP E Maintenance Rule Conduct Manual, Appendix E, 27
Maintenance Rule SSC Specific Functions
MMR Appendix B Maintenance Rule Conduct Manual, Terms and Definitions 7
MMR Appendix D Maintenance Rule Conduct Manual, Guidelines for 20
Determining Functional Failures and Maintenance
Preventable Function Failures
MMR Appendix E Maintenance Rule Conduct Manual, Maintenance Rule SSC 27
Specific Functions
MMR Appendix F Maintenance Rule Conduct Manual, Maintenance Rule 26
Performance Criteria
Monthly M-Rule Tracking Group: N2100 July -
Evaluation Report September,
Inspection Type Designation Description or Title Revision or
Procedure Date
20
Plant Health Reactor Feedwater (System N2100) 2019, Quarter
Report 1 and 2
Plant Health Condensate and Heater Feed Pumps (System N2000 and 2019, Quarter
Report N2003) 3
Plant Health Reactor Feedwater (System N2100) 2019, Quarter
Report 4
Plant Health Reactor Feedwater (System N2100) 2020, Quarter
Report 1, 2, and 3
VMR1-46 Target Rock Model 7567F Safety Relief Valves Vendor J
Manual
Procedures 23.420 RHR Complex Heating and Ventilation 41
23.621 Main Control Room Annunciator and Sequence Recorder 89
24.129.04 Control Air Valve Operability/Position Verification/Isolation 52
Integrity Test
49.419.002 RHR Damper Blocking 7
VAS USER Visual Annunciator System (VAS) User Manual 0
Work Orders 54506175 North Recirc MG Set Slip Ring Measurement 04/09/2020
54506203 South Recirc MG Set Slip Ring Measurement 04/08/2020
71111.13 Corrective Action 15-21424 Number 2 HPSV went Closed and Then Open to 22 Percent 02/21/2015
Documents Multiple Times
20-30925 Radka Air Compressor Air Leak 10/05/2020
20-31945 CTG 11-1 Not Ratcheting 11/04/2020
20-32152 Shoal Line Maintenance Risk Evaluation 11/11/2020
20-32176 Operations Performance Gap in Risk Management and 12/02/2020
Identification of Risk
20-33180 4D91 Electric Governor Trouble Number 1 HP Stop Valve 12/23/2020
CC2 HW
Corrective Action 20-33113 Update ARP Action for Ratchet Trouble 12/21/2020
Documents
Resulting from
Inspection
Miscellaneous EF2-PRA-005.33 Combustion Turbine Generators (CTGs) 1
MMR APP H Maintenance Rule Conduct Manual, Appendix H - On-Line 15
Inspection Type Designation Description or Title Revision or
Procedure Date
Core Damage Risk Management Guidelines
Procedures 11D50 CTG 11 Unit 1 Trouble Alarm Response Procedure 15
ARP 4D91 Electric Governor Trouble 19
MMR12 Equipment Out of Service Risk Management 20A
MOP05-100 Protected Equipment 2C
MWC15 Elevated Risk Management 20
71111.15 Corrective Action 20-31904 MTU Failed During 44.020.234 11/03/2020
Documents 20-33238 EDG 11 Crankcase Oil Exhibits Increased Fuel Oil in the 11/29/2020
Crankcase Oil
Procedures 44.020.234 NSSSS-RCIC Steam Line Flow, Trip System B 41
Calibration/Functional
Work Orders 54136747 Perform 44.020.234 NS4 RCIC Steam Line Flow, Trip 11/03/2020
System B, Calibration/Functional
71111.18 Corrective Action 19-23227 Recommend Review of Site Response to Open 04/26/2019
Documents CARD 07-23630
20-23661 UPS Battery Feed to UPS-B Fuse Found Blown 04/21/2020
20-26704 3071-128-EJ Spec R3100S027 Fuse Discrepancy 07/03/2020
20-27546 UPS B Appears to Have Repeat Failure of Battery Fuse 07/02/2020
20-27855 UPS A and B Fuse Ratings 07/09/2020
20-31438 Material Found at Bottom of Condensate Storage Tank 10/20/2020
20-31468 18-inch Pipe Clamp Bolt Length Issue 10/21/2020
20-31488 Threaded Rod Set Screw Too Short 10/21/2020
Drawings M-5715-3 EDP-80127-018 0
M-5721-1 EDP-80127-006 0
M-Y-2000 EDP-80127 A
Engineering 80127 ECCS Pump CST Vortex Suppression Device B
Changes DEC 70303 UPS A/B DC Circuit Fuses and Cables A
DEC 70304 UPS B Parallel Operation Software Change 0
EDP 70042 UPS A and B Replacement C
Miscellaneous Risk Management CST Vortex Suppression 10/19/2020
Plan
71111.19 Corrective Action 20-30561 Received 3D6, Division 1/2 Reactor Building Vent Exhaust 09/24/2020
Documents Rad Monitor Upscale Trip, RBHVAC Trip, and D1 SGTS
Inspection Type Designation Description or Title Revision or
Procedure Date
20-30756 While Replacing Seals on RR Car Interlock Door, 4 Bolts 09/30/2020
Failed While Removing Bolts
20-30824 East and West Airlock Door Seal Long Term 10/01/2020
Recommendations
20-32018 RCIC Turbine Exhaust Rupture Disc Leak 11/06/2020
20-32205 NRC Identified: IST Program Testing Methodology for 11/13/2020
E5100F011
Drawings 6I721-2611 Reactor Building Main Control Room A/C Mode Selection AA
Division 1
6I721-2611-10 Reactor Building Secondary Containment Isolation Signals T
Division 1
6M721-2034 Core Spray System CSS Reactor Building AS
6M721-2035 High Pressure Coolant Injection System Reactor Building BP
6M721-2044 Reactor Core Isolation Cooling System BE
6M721-2045 Reactor Core Isolation Cooling System Barometric AT
Condenser
Miscellaneous 22A1354AR Reactor Core Isolation Cooling System 13
Clearance: Jumper Out High High Trip of Division 1 Rad Monitor 11/13/2020
D1100-000138
ERE 54575 Evaluate Suitability of Replacement Garlock 3400 Sheet 0
VMR4-15 Continental Disc Corp A
Procedures 23.206 Reactor Core Isolation Cooling System 104
24.206.01 RCIC System Pump and Valve Operability Test 87
44.030.073 ECCS - Reactor Recirculation Pump B DP, Division 1, 36
Channel B Calibration/Functional
46.206.001 RCIC Turbine Governor Control System Calibration 45A
Work Orders 24231076 Replace MTU B31N614A - Tin Whisker Susceptible 11/30/2020
Rosemont 710DY MTU
2386240 Replace and Calibrate RCIC Speed Controller (EG-M) 11/02/2020
2386240 Replace and Calibrate RCIC Speed Controller (EG-M) 01/14/2015
43954320 Replace NIAS Isolation Valve P5000F403 Solenoid Valve 11/17/2020
43954342 Replace Time Delay Relays in P50P402B, D2 NIAS Dryer 11/17/2020
Control Cabinet
Inspection Type Designation Description or Title Revision or
Procedure Date
53421010 Calibrate Pressure Switch RCIC Pump Suction Low 11/03/2020
Pressure Trip
54136663 Perform 24.206.01 RCIC System Pump Operability and 11/05/2020
Valve Test at 1000 PSIG
268801 Replace Division 2 S Control Air Compressor Unloading 11/17/2020
Cylinder Solenoid Valve
58734795 Troubleshoot/Replace Relay T41M80 in H21P296C 11/02/2020
Causing 3D36 and RBHVAC Trip
E967190100 Replace Secondary Containment Railroad SE Airlock Door 09/28/2020
Inflatable Seal NE-6.6-EQMS.122
E967190100 Replace Secondary Containment Railroad SE Airlock Door 09/28/2020
Inflatable Seal
T363180100 License Renewal Required Replace Secondary 09/29/2020
Containment Railroad South Airlock Door Inflatable Seal
71111.22 Corrective Action 20-32994 Procedure Enhancement to 24.203.02 and 24.203.03 12/16/2020
Documents Division 1 / 2 Core Spray Operability Test
Drawings 6M721-2034 Diagram Core Spray System CSS Reactor Building AS
Work Orders 53934688 Perform 24.307.16 Sec 5.1 EDG 13 Start and Load 10/19/2020
Test-Slow Start
54370155 Perform Quarterly Testing of N+1 Train Neptune Diesel 11/28/2020
54514769 Perform 24.203.03 Sec-5.2 Division 2 CSS Simulated 12/16/2020
Automatic Actuation Test
71114.04 Corrective Action CARD 19-25318 Review EP-101 Revisions Using ACR Process to Determine 07/15/2019
Documents 10CFR50.54(q) Applicability
CARD 19-27058 Changes Needed to Improve EP-101 09/19/2019
CARD 19-28389 Error Made While Revising EP-101 11/04/2019
Miscellaneous 10CFR50.54(q) Screen Number 2019-69S 10/18/2019
10CFR50.54(q) Screen Number 2019-71S 10/17/2019
10CFR50.54(q) Screen Number 2019-72S 10/18/2019
10CFR50.54(q) Screen Number 2019-73S 10/18/2019
10CFR50.54(q) Screen Number 2019-74S 10/18/2019
10CFR50.54(q) Screen Number 2019-75S 10/18/2019
10CFR50.54(q) Screen Number 2019-76S 10/18/2019
10CFR50.54(q) Screen Number 2019-82S 10/18/2019
Inspection Type Designation Description or Title Revision or
Procedure Date
10CFR50.54(q) Screen Number 2019-87S 10/23/2019
10CFR50.54(q) Evaluation Number 2019-11E 10/18/2019
10CFR50.54(q) Screen Number 2019-88S 10/23/2019
10CFR50.54(q) Screen Number 2019-89S 10/23/2019
10CFR50.54(q) Screen Number 2019-90S 10/23/2019
10CFR50.54(q) Screen Number 2019-91S 11/01/2019
10CFR50.54(q) Evaluation Number 2019-15E 10/23/2019
Procedures EP-101 Classification of Emergencies 42C
EP-101 Classification of Emergencies 43
EP-101 Classification of Emergencies 43A
EP-590 10CFR50.54(q) Screens and Evaluation 0
LP-ER-874-0001 10 CFR 50.54Q Compliance Reviews Training Lesson Plan 0
RERP Fermi 2 Radiological Emergency Response Preparedness Fermi 2
Plan Radiological
Emergency
Response
Preparedness
Plan;
Revision 48
RERP Fermi 2 Radiological Emergency Response Preparedness 49
Plan
71114.06 Procedures EP-101 Classification of Emergencies 43A
71124.07 Calibration Radeco Model AVS-28A Calibration Form for Serial Number 01/03/2020
Records 6980
Radeco Model AVS-28A Calibration Form for Serial Number 01/03/2020
7570
Radeco Model AVS-28A Calibration Form for Serial Number 01/03/2020
7571
Corrective Action 20-31431 NRC Identified - Vegetation Sampling in ODCM Not 10/20/2020
Documents Consistent with Annual Report and Surveillances
Resulting from
Inspection
Miscellaneous Offsite Dose Calculation Manual 22
Offsite Dose Calculation Manual 23
Inspection Type Designation Description or Title Revision or
Procedure Date
NRC-20-0027 Annual Radioactive Effluent Release Report and 04/29/2020
Radiological Environmental Operating Report
71124.08 Miscellaneous NPRP-20-0044 Scaling Factor Report for Torus Debris 05/27/2020
Procedures 67.000.505 Survey and Movement of Waste Liners in the OSSF 1C
MRP15 Controlling Radioactive Material Outside the Plant 14
Radiologically Controlled Area
Shipping Records EF2-19-050 Resin Characterization and Shipping Package 08/28/2019
EF2-20-040 Torus Paint Chips Characterization and Shipment 04/21/2020
EF2-20-117 Resin Characterization and Shipping Package 09/30/2020
71151 Miscellaneous Alert and Notification System Reliability Performance 07/01/2019 -
Indicator Records 09/30/2020
Emergency Response Organization Drill Participation 07/01/2019 -
Performance Indicator Records 09/30/2020
Drill and Exercise Performance - Performance Indicator 07/01/2019 -
Records 09/30/2020
71152 Corrective Action 07-23630 CDBI: UFSAR Anti-Vortex Methodology Non-Conservative 06/28/2007
Documents 18-28666 NRC Concern: Foreign Material Left in Drywell 10/23/2018
19-21822 NQA - EDG 14 Tubing Not Secured Per Design 03/08/2019
19-23328 NQA - Failure of Multiple Groups to Adequately Evaluate 05/01/2019
the EDG 14 Clamp Issue and Associated Contributors
19-23915 2019 DBAI: Methodology Error Found in MOV Torque 05/21/2019
Calculation
19-23915 2019 DBAI: Methodology Error Found in MV Torque 05/21/2019
Calculation
20-20867 Received 10D21 Division II EDG 14 Lube Oil Tank D Level 01/24/2020
High/Low in MCR
20-20876 Clarification of Design Basis Document R40-00 Needed 01/25/2020
Regarding EDG Lube Oil Requirements
20-21195 OCC Effectiveness Challenged During EDG 13 SSO 02/03/2020
20-21597 EDG 14 LO Sump Level High 02/12/2020
20-27717 EDG 14 Oil Sump Level HOOS 07/07/2020
20-28726 Emerging Trend in CAP Performance Gaps 07/28/2020
20-28753 Results of Drywell Closeout Walkdown 07/28/2020
Inspection Type Designation Description or Title Revision or
Procedure Date
20-29742 Request a Revision to Planners Template: FO18 08/28/2020
20-29776 Revision to the RFO Plant Restoration Checklist 08/31/2020
20-31928 EDG Lube Oil Tank Low Level Alarm Less than Required 11/03/2020
for 7-Day Run Time
20-32446 NQA Audit 02-0112 Finding - Identified Gap Between Fermi 11/24/2020
Corrective Action Program Performance and Standards
20-32817 ODMI 20-007 has Incorrect LCO Completion Time 12/10/2020
Corrective Action 20-31385 NRC Identified: CARD 20-28850 Closed Without Issue 10/19/2020
Documents Resolution
Resulting from 20-32182 NRC Identified- Meeting Effectiveness 11/12/2020
Inspection 20-32858 NRC Identified - NRC Question on CARD 20-28753 12/11/2020
21-20263 NRC Identified - NRC Semiannual PI&R Trend Review 01/08/2021
Observations
Miscellaneous Fermi 2 Refuel Plan of the Day 07/06/2020
Outage 20
MOP05 Operations Conduct Manual, Chapter 5 - Control of 57
Equipment
MQA11-200 Quality Assurance Conduct Manual Implementing 1B
Procedure, Condition Initiation
MWC13 Outage Nuclear Safety 22
Operations Operator Challenges 18
Department
Expectation ODE-
Procedures 24.000.02 Shiftly, Daily, and Weekly Required Surveillances 159
71153 Corrective Action 20-31731 CRD Pump Suction Press Control Valve Issues 10/29/2020
Documents 20-31732 Received CRD Accumulator Trouble for HCU 22-15 due to 10/29/2020
High Water Level
Fire Plans Troubleshooting CARD 20-31731, WO 59092486, Component C1106C001B 0
Plan
Miscellaneous 30 Day Recharge CRD Accumulator Recharge Report November
Report 2020
ARP 3D1 CRD Pump A/B Suction Pressure Low 10
ARP 3D13 CRD Hydraulic Temperature High 20
Inspection Type Designation Description or Title Revision or
Procedure Date
Operator Log 10/29/2020
SOER Log Report 11/06/2020
Procedures 20.106.01 CRD Hydraulic System Failure 21
23