IR 05000341/2020004

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Integrated Inspection Report 05000341/2020004
ML21041A276
Person / Time
Site: Fermi 
Issue date: 02/10/2021
From: Nestor Feliz-Adorno
NRC/RGN-III
To: Peter Dietrich
DTE Electric Company
References
IR 2020004
Download: ML21041A276 (25)


Text

February 10, 2021

SUBJECT:

FERMI POWER PLANT, UNIT 2 - INTEGRATED INSPECTION REPORT 05000341/2020004

Dear Mr. Dietrich:

On December 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Fermi Power Plant, Unit 2. On January 19, 2021, the NRC inspectors discussed the results of this inspection with Mr. E. Olson, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Néstor J. Féliz Adorno, Chief Branch 4 Division of Reactor Projects

Docket No. 05000341 License No. NPF-43

Enclosure:

As stated

Inspection Report

Docket Number:

05000341

License Number:

NPF-43

Report Number:

05000341/2020004

Enterprise Identifier: I-2020-004-0062

Licensee:

DTE Electric Company

Facility:

Fermi Power Plant, Unit 2

Location:

Newport, MI

Inspection Dates:

October 01, 2020 to December 31, 2020

Inspectors:

T. Briley, Senior Resident Inspector

T. McGowan, Resident Inspector

V. Myers, Senior Health Physicist

R. Ng, Project Engineer

T. Taylor, Resident Inspector

Approved By:

Néstor J. Féliz Adorno, Chief

Branch 4

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Fermi Power Plant, Unit 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

None.

PLANT STATUS

Unit 2 began the inspection period at rated thermal power. On November 18, 2020, the unit was down powered to 94 percent rated thermal power for planned hydraulic control unit maintenance. The unit was returned to rated thermal power the following day. On November 20, 2020, the unit was down powered to 74 percent rated thermal power for a planned control rod pattern adjustment. The unit was returned to rated thermal power the following day. The unit remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President of the United States on the public health risks of the Coronavirus Disease 2019 (COVID-19),resident inspectors were directed to begin telework and to remotely access licensee information using available technology. During this time, the resident inspectors performed periodic site visits each week; conducted plant status activities as described in IMC 2515, Appendix D, Plant Status; observed risk-significant activities; and completed on-site portions of IPs. In addition, resident and regional baseline inspections were evaluated to determine if all or portions of the objectives and requirements stated in the IP could be performed remotely. If the inspections could be performed remotely, they were conducted per the applicable IP. In some cases, portions of an IP were completed remotely and on-site. The inspections documented below met the objectives and requirements for completion of the IP.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Seasonal Extreme Weather Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated readiness for seasonal extreme weather conditions prior to the onset of the cold weather winter months for the following systems:

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the adequacy of the overall preparations to protect risk-significant systems from impending severe weather due to a high wind advisory on November 19, 2020

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Division 2 emergency diesel generators (EDG) 13 and 14 while EDG 11 was out of service for maintenance during the week ending October 10, 2020
(2) Division 2 emergency equipment cooling water while the reactor core isolation cooling (RCIC) system was out of service for maintenance during the week ending November 7, 2020
(3) Division 1 non-interruptible air system (NIAS) while Division 2 NIAS was out of service for maintenance during the week ending November 21, 2020
(4) Division 2 emergency equipment service water (EESW) while Division 1 EESW was out of service for maintenance during the week ending December 5, 2020

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the Division 1 residual heat removal (RHR) system during the week ending October 31, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Auxiliary building first floor, Division 1 switchgear room during the week ending October 17, 2020
(2) Auxiliary building basement, control rod drive pump room during the week ending October 17, 2020
(3) Reactor building basement and sub-basement, north east quad during the week ending December 12, 2020
(4) Circulating water pump house during the week ending December 12, 2020

71111.06 - Flood Protection Measures

Inspection Activities - Internal Flooding (IP Section 03.01) (2 Samples)

The inspectors evaluated internal flooding mitigation protections in the:

(1) Relay room
(2) Division 1 switchgear room

71111.07A - Heat Sink Performance

Annual Review (IP Section 03.01) (1 Sample)

The inspectors evaluated readiness and performance of:

(1) EDG 13 lubricating oil, jacket water, and air coolant heat exchangers

71111.11A - Licensed Operator Requalification Program and Licensed Operator Performance

Requalification Examination Results (IP Section 03.03) (1 Sample)

(1) The inspectors reviewed and evaluated the licensed operator examination failure rates for the requalification program annual operating test administered between October 19 and November 20, 2020

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) The inspectors observed and evaluated a licensed operator requalification graded scenario in the control room simulator on October 8, 2020

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (6 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Reactor recirculation system during the week ending October 31, 2020
(2) Reactor feedwater system during the week ending November 28, 2020
(3) Safety relief valves during the week ending December 12, 2020
(4) NIAS during the week ending December 5, 2020
(5) RHR complex dampers during the week ending December 11, 2020
(6) Visual annunciator system during the week ending December 19, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Division 1 switchyard breaker GK and EDG 11 out of service for planned maintenance during the week ending October 10, 2020
(2) RCIC system and offsite power Shoal line planned maintenance, and emergent work on combustion turbine generator (CTG) 11-1 with CTG 11-2 and 11-4 out of service during the week ending November 7, 2020
(3) Emergent work on main turbine control system during the week ending December 31, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (2 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Operability and functionality of RCIC following Division 1 high steam line flow master trip unit failure, as documented in condition assessment resolution document (CARD) 20-39104
(2) Operability and functionality of EDG 11 following identification of a change in crankcase oil chemistry parameters, as documented in CARD 20-33238

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02) (2 Samples)

The inspectors evaluated the following temporary or permanent modifications:

(1) Condensate storage tank vortex suppressor installation (permanent)
(2) Uninterruptible power supply 'B' logic and fuse sizing change (permanent)

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post-maintenance test activities to verify system operability and functionality:

(1) Reactor building outer railroad door testing following identification of a degraded seal during the week ending October 3, 2020
(2) RCIC system testing following a planned maintenance outage during the week ending November 7, 2020
(3) Reactor building ventilation radiation monitor testing following identification of spurious operation and trips during the week ending November 14, 2020
(4) Division 2 NIAS system testing following planned maintenance during the week ending November 28, 2020
(5) Recirculation pump 'B' differential pressure channel 'B' master trip unit (MTU) testing following planned MTU replacement during the week ending December 4, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01)

(1) EDG 13 slow start surveillance testing during the week ending October 24, 2020

Inservice Testing (IP Section 03.01) (1 Sample)

(1) Division 2 core spray auto actuation testing during the week ending December 12, 2020

FLEX Testing (IP Section 03.02) (1 Sample)

(1) N+1 Neptune pump testing during the week ending November 28, 2020

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors completed an evaluation of submitted emergency action level and emergency plan changes on December 8, 2020. This evaluation does not constitute NRC approval.

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Emergency preparedness tabletop drill on October 8,

RADIATION SAFETY

71124.07 - Radiological Environmental Monitoring Program

Environmental Monitoring Equipment and Sampling (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated environmental monitoring equipment and observed collection of environmental samples

Radiological Environmental Monitoring Program (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated the implementation of the licensees radiological environmental monitoring program

GPI Implementation (IP Section 03.03) (1 Sample)

(1) The inspectors evaluated the licensees implementation of the Groundwater Protection Initiative program to identify incomplete or discontinued program elements

71124.08 - Radioactive Solid Waste Processing & Radioactive Material Handling, Storage,

& Transportation

Radioactive Material Storage (IP Section 03.01)

(1) Inspectors evaluated the licensees performance in controlling, labelling and securing radioactive materials

Radioactive Waste System Walkdown (IP Section 03.02) (1 Sample)

(1) Inspectors walked down accessible portions of the solid radioactive waste systems and evaluated system configuration and functionality

Waste Characterization and Classification (IP Section 03.03) (3 Samples)

The inspectors evaluated the licensees characterization and classification of the following radioactive waste shipments:

(1) EF2-19-050, resin
(2) EF2-20-040, torus paint chips
(3) EF2-20-117, resin

Shipment Preparation (IP Section 03.04) (1 Sample)

The inspectors observed the preparation of the following radioactive material shipment:

(1) EF2-20-120, resin shipped as Type B

Shipping Records (IP Section 03.05) (3 Samples)

(1) EF2-19-050, resin shipped as LSA-II
(2) EF2-20-040, torus paint chips shipped as LSA-II
(3) EF2-20-117, resin shipped as Type B

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (IP Section 02.12)===

(1) July 1, 2019 through September 30, 2020

EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)

(1) July 1, 2019 through September 30, 2020

EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

(1) July 1, 2019 through September 30, 2020 BI01: Reactor Coolant System (RCS) Specific Activity Sample (IP Section 02.10) (1 Sample)
(1) July 1, 2019 through September 30, 2020

OR01: Occupational Exposure Control Effectiveness Sample (IP Section 02.15) (1 Sample)

(1) July 1, 2019 through September 30, 2020

PR01: Radiological Effluent Technical Specifications/Offsite Dose Calculation Manual Radiological Effluent Occurrences (RETS/ODCM) Radiological Effluent Occurrences Sample (IP Section 02.16) (1 Sample)

(1) July 1, 2019 through September 30, 2020

71152 - Problem Identification and Resolution

Semiannual Trend Review (IP Section 02.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program for potential adverse trends that might be indicative of a more significant safety issue

Annual Follow-up of Selected Issues (IP Section 02.03) (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) A sample of issues open in the corrective action program with operability being maintained via compensatory measure or pending some final action to update or change the design basis. The inspectors reviewed a partial modification to the condensate storage tank to address the potential for vortexing, a degraded valve in the lube oil system for EDG 14, and licensee follow up to an error in methodology regarding motor operated valve calculations that had been discovered during a prior NRC inspection.

71153 - Follow-up of Events and Notices of Enforcement Discretion Personnel Performance (IP Section 03.03)

(1) The inspectors evaluated a control rod drive hydraulic system transient and licensees performance on November 14,

INSPECTION RESULTS

Observation: Semi-Annual Corrective Action Program Trend Review 71152 The inspectors noted a trend in organizational and programmatic issues entered into the corrective action program that did not have sustainable corrective actions. Several examples included, but were not limited to, the following:

  • In May 2019, following a planned safety system maintenance outage for EDG 14, Nuclear Quality Assurance (NQA) identified several tube clamps taped to the wall in the EDG 14 room that had not been reinstalled as intended. The primary cause listed in the organizational effectiveness analysis that followed was inadequate field oversight. Specifically, it concluded that one field supervisor was not sufficient to oversee multiple major-scope jobs occurring in parallel. However, none of the corrective actions taken addressed the primary cause or the organizational issues which led to the breakdown during the EDG outage. The missing clamps ultimately did not impact EDG 14 operability.
  • In February 2020, the licensee initiated CARD 20-21195 for some organizational effectiveness issues associated with execution and implementation of a planned safety system maintenance outage for EDG 13. The licensee determined the work delays were caused by issues with how the schedule was prepared, communication challenges between day and night shift and between departments, and the operations department not being formally part of the outage control center (OCC) staff. The corrective action was to revise a post-outage critique form which added some organizational effectiveness questions. However, the inspectors noted this corrective action did not address issues associated with the execution and implementation of system outages because the post-outage critique form was used following the completion of safety system outages.
  • During the most recent refueling outage (i.e., from March to August 2020), the inspectors identified foreign material issues (mainly small cleanliness issues) during their primary containment closeout inspection. Most of the material was fairly easy to find or was discovered in a location that was easily accessible. During the prior refueling outage, inspectors also noted a large amount of material during their closeout inspections. Given the prior issues, the inspectors questioned the process the licensee employed to validate primary containment cleanliness prior to final closeout. In response, the licensee added a list of drywell areas and a reference to operations department cleanliness standards to a work order used by decontamination personnel. However, these actions were similar to those documented for a similar issue captured in May 2018 as CARD 18-23959. The inspectors questioned the effectiveness of implementing corrective actions that were similar to actions that were already in place and demonstrated to not address the issue during the most recent refueling outage.

The inspectors discussed their observations with licensee staff, who subsequently generated CARD 21-20263 to capture the issues. Through the discussions with licensee personnel, the inspectors learned that licensee staff had recently noted similar (but separate) issues regarding sustainability of corrective actions as part of a self-assessment. The inspectors will continue to routinely monitor CAP performance via the baseline inspection program.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 19, 2021, the inspectors presented the integrated inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff.
  • On October 22, 2020, the inspectors presented the radiation protection inspection results to Mr. R. LaBurn, Radiation Protection Manager, and other members of the licensee staff.
  • On December 8, 2020, the inspectors presented the emergency action level and emergency plan changes inspection results to Mr. E. Olson, Site Vice President, and other members of the licensee staff.
  • On December 15, 2020, the inspectors presented the licensed operator requalification program annual operating test results inspection results to Mr. A. Spencer, Licensed Operator Requalification Program Lead, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Corrective Action

Documents

20-29557

NQA-First Level Escalation-Repeat Deficiencies with

Seasonal Readiness Activities

08/24/2020

20-32239

Pri 4 Cold Weather Prep Work Order Not Scheduled

11/16/2020

Engineering

Changes

TM-16-0025

Install One Temp Boiler and Provide Spare Connections for

a Second Temp Boiler

11/08/2016

Miscellaneous

MOP01-200

Severe Weather Guidelines

Procedures

MWC16-100

Seasonal Readiness

Work Orders

51732374

Perform MWC16-100 Cold Weather System Readiness

Review Checklists

03/20/2020

71111.04

Calculations

DC-6356

Stress and Seismic Analysis of the Reactor/Auxiliary

Building CTI Nuclear Fan Coil Units

A

Corrective Action

Documents

20-31283

Damaged Labels - RBSB NW

10/15/2020

20-31377

Torus Room AZ 250

10/19/2020

20-31440

NRC Identified Condition, Insulation Repairs

10/20/2020

20-32269

NRC Identified Issue: The E1100F619A and E1100F619B

have Local Manual Positioners but are Not Tracked by

Valve Lineups

11/17/2020

20-32273

NRC Concern: Missing Label on P50R413A

11/17/2020

Drawings

6M721-2084

Diagram Residual Heat Removal (RHR) Division I

BQ

6M721-2084

Diagram Residual Heat Removal (RHR) Division I

BQ

6M721-5729-2

EECW Division II Functional Operating Sketch

BD

6M721-5734

Emergency Diesel Generator System Functional Operating

Sketch

BL

M-2015

Station and Control Air

CS

M-4615

Interruptible and Non-Interruptible Control Air

AH

M-5706-3

RHR Service Water Make-Up Decant and Overflow

Systems

AH

M-5729-2

Emergency Equipment Cooling Water Division II

BD

Miscellaneous

Operator Logs

Operations AUTOTOUR Logs - Reactor Building

Procedures

23.129

Station and Control Air

21

23.205

Division 1 RHR LPCI Standby Lineup Verification,

8A

147

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

23.208

RHR Complex Service Water Systems

29

71111.05

Fire Plans

FP-AB-2-9b

Auxiliary Building, Division 1 Switchgear Room, Zone 9, El.

613'6"

FP-AB-B-4b

Control Rod Drive Pump Room, Zone 4, El. 562'0"

FP-CWPH-1-32

Circulating Water Pumphouse Zone 32 Elevation 58'6"

FP-RB-B-5b

Reactor Building Basement Northeast Corner Room

Zone 5, Elevation 562'0"

71111.06

Engineering

Evaluations

EF2-PRA-011

Internal Flood Walkdown Summary Notebook

EF2-PRA-012

Fermi 2 Nuclear Power Station PRA Internal Flood Analysis

Notebook

71111.07A

Calculations

DC-5804

Diesel Generator Service Water Design Basis

Requirements Calculation

F

Miscellaneous

MES540001

EDG 11 Air Coolant Heat Exchanger Inspection Report

10/05/2020

MES54001

EDG 11 Jacket Cooling Heat Exchanger Inspection Report

10/05/2020

MES54001

EDG 11 Lube Oil Heat Exchanger Inspection Report

10/05/2020

71111.11A

Miscellaneous

Fermi 2020 LORT Annual Operating Test Summary Results

2/15/2020

71111.11Q Miscellaneous

SS-OP-904-2001

Evaluation Scenario

71111.12

Corrective Action

Documents

17-25639

Management Review Committee (MRC) Cognitive Trend -

SRVs

06/27/2017

18-20350

North Reactor Feed Pump Turbine Lube Oil Level High

01/16/2018

18-20351

N RFPT Turning Gear Engage Solenoid Valve (N21F111A)

is Blowing By

04/30/2018

18-23923

Received 5D28 South RFP/RFPT Shaft Trouble While

Taking the N RFP Out of Service

05/17/2018

19-20000

Unexpected Alarm During Startup of NRFPT

01/01/2019

19-20309

SRV 'A' (B2104F013A) Tail Pipe Temperature Elevated to

~205F

01/14/2019

19-20660

SRV 'J' Tail Pipe Temperature Elevated to ~212F

01/30/2019

19-21751

Need RF20 WO to Perform a Body Off Inspection of

SRV 'A' due to Elevated Tailpipe Temperatures per CARD

19-20309

03/06/2019

19-23939

2019 DBAI: MRFF Action Needed for Previously Closed

CARD 17-23452

05/22/2019

19-24545

Oil Surrounding Mechanical Seal on RRMG LO

06/17/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

B3103C001D

19-28069

Excessive Carbon on Brushes and Intake

10/23/2019

20-00023

Bushing Broken on N2100-F006B SRFPT OTBD Seal

Water TCV Outlet Isolation Valve

03/23/2020

20-20091

Division 1 RHR Pump Room Dampers

01/06/2020

20-20099

Abnormal Noise/Indications from P50-F516A Solenoid

01/06/2020

20-21585

Time Delay Relay P50M832 Failed as Found Testing

2/12/2020

20-21602

Division 2 Control Air Compressor Failed PMT

2/13/2020

20-21659

Control Air Compressor PMT

2/14/2020

20-21688

Online Work Orders for Vendor Inspection of Recirc MG Set

Brushes and Potential Stoning

2/14/2020

20-21708

As-Found Condition of Division II NIAS Dryer

2/16/2020

20-21840

Division 2 Control Air Compressor Will Not Load

2/11/2020

20-21936

X4103F128 Excessive Scoring on Hydra Motor Shaft

2/20/2020

20-23975

Received 3D19 Annunciator System Trouble

2/16/2020

20-24502

VAS Total System Failure

04/14/2020

20-24779

VAS Multiplexor C Time Errors

04/19/2020

20-25054

Potential Common Cause Failure of VAS

04/23/2020

20-25856

Discharge Pressure is High Out of Spec for N RRMG Set

Lube Oil Pump (B103C001A)

05/17/2020

20-25881

B3103C001D PMT Unsatisfactory due to Vibration Level

05/18/2020

20-26161

Stopped and Backed Out of 27.129.04

05/27/2020

20-26271

Findings from Division 1 NIAS Air Dryer Troubleshooting

05/29/2020

20-26312

VAS Clock Signal Distortion Cause and Remediation

05/30/2020

20-26672

RRMG Set Lube Oil Level Challenges in Refuel Requires

Add and Removal of Oil

06/08/2020

20-26692

P603 VAS Alarm Check Malfunction and System Battery

Low Voltage Warning

06/08/2020

20-26723

Dual Indication for Open Damper X4103F115

06/10/2020

20-26772

Dual Indication for Open Damper X4103F103

06/10/2020

20-27423

Two of Four North and South RFPT Speed Indications in

IPCS Erroneous

06/29/2020

20-28723

UNSAT SRV Inspection

07/28/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20-29013

SRV 'A' Tailpipe Temperature Elevated Following RF-20

Startup

08/06/2020

20-29165

SRV 'M' Tailpipe Temperature Elevated Following RF-20

Startup

08/10/2020

20-30180

Abnormal Speed Changes on South RFPT

09/13/2020

20-30351

Learnings from Industry Responses for 20-30180, SRFPT

Speed Anomaly

09/17/2020

20-30443

Abnormal Speed Differential Between North and South

RFPTs

09/21/2020

20-30554

Three SRVs Removed in RF-20 Found Outside of

As-Found Set-Point Tolerance

09/24/2020

20-30779

Oil Leak

09/30/2020

20-32479

Trend CARD - B2104F013A Tailpipe Temperature Increase

11/25/2020

20-32730

Broken Insulation in Hydra Motor Electrical Housing

2/08/2020

Engineering

Evaluations

Monthly Maintenance Rule Evaluation Report - Safety Relief

Valve - September 2020

10/09/2020

Miscellaneous

RHR Complex Ventilation (X4103) System Performance

Monitoring Plan

09/20/2020

P5002 (NIAS) System Monitoring Plan

03/15/2019

ACMP 20-007

SRV 'A' & 'M' Weeping

MMR 02

Maintenance Rule Program Description

6A

MMR 10

Maintenance Rule, Monitoring

18A

MMR APP E

Maintenance Rule Conduct Manual, Appendix E,

Maintenance Rule SSC Specific Functions

MMR Appendix B

Maintenance Rule Conduct Manual, Terms and Definitions

MMR Appendix D

Maintenance Rule Conduct Manual, Guidelines for

Determining Functional Failures and Maintenance

Preventable Function Failures

MMR Appendix E

Maintenance Rule Conduct Manual, Maintenance Rule SSC

Specific Functions

MMR Appendix F

Maintenance Rule Conduct Manual, Maintenance Rule

Performance Criteria

Monthly M-Rule

Evaluation Report

Tracking Group: N2100

July -

September,

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20

Plant Health

Report

Reactor Feedwater (System N2100)

2019, Quarter

and 2

Plant Health

Report

Condensate and Heater Feed Pumps (System N2000 and

N2003)

2019, Quarter

Plant Health

Report

Reactor Feedwater (System N2100)

2019, Quarter

Plant Health

Report

Reactor Feedwater (System N2100)

20, Quarter

1, 2, and 3

VMR1-46

Target Rock Model 7567F Safety Relief Valves Vendor

Manual

J

Procedures

23.420

RHR Complex Heating and Ventilation

23.621

Main Control Room Annunciator and Sequence Recorder

24.129.04

Control Air Valve Operability/Position Verification/Isolation

Integrity Test

49.419.002

RHR Damper Blocking

VAS USER

Visual Annunciator System (VAS) User Manual

Work Orders

54506175

North Recirc MG Set Slip Ring Measurement

04/09/2020

54506203

South Recirc MG Set Slip Ring Measurement

04/08/2020

71111.13

Corrective Action

Documents

15-21424

Number 2 HPSV went Closed and Then Open to 22 Percent

Multiple Times

2/21/2015

20-30925

Radka Air Compressor Air Leak

10/05/2020

20-31945

CTG 11-1 Not Ratcheting

11/04/2020

20-32152

Shoal Line Maintenance Risk Evaluation

11/11/2020

20-32176

Operations Performance Gap in Risk Management and

Identification of Risk

2/02/2020

20-33180

4D91 Electric Governor Trouble Number 1 HP Stop Valve

CC2 HW

2/23/2020

Corrective Action

Documents

Resulting from

Inspection

20-33113

Update ARP Action for Ratchet Trouble

2/21/2020

Miscellaneous

EF2-PRA-005.33

Combustion Turbine Generators (CTGs)

MMR APP H

Maintenance Rule Conduct Manual, Appendix H - On-Line

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Core Damage Risk Management Guidelines

Procedures

11D50

CTG 11 Unit 1 Trouble Alarm Response Procedure

ARP 4D91

Electric Governor Trouble

MMR12

Equipment Out of Service Risk Management

20A

MOP05-100

Protected Equipment

2C

MWC15

Elevated Risk Management

71111.15

Corrective Action

Documents

20-31904

MTU Failed During 44.020.234

11/03/2020

20-33238

EDG 11 Crankcase Oil Exhibits Increased Fuel Oil in the

Crankcase Oil

11/29/2020

Procedures

44.020.234

NSSSS-RCIC Steam Line Flow, Trip System B

Calibration/Functional

Work Orders

54136747

Perform 44.020.234 NS4 RCIC Steam Line Flow, Trip

System B, Calibration/Functional

11/03/2020

71111.18

Corrective Action

Documents

19-23227

Recommend Review of Site Response to Open

CARD 07-23630

04/26/2019

20-23661

UPS Battery Feed to UPS-B Fuse Found Blown

04/21/2020

20-26704

3071-128-EJ Spec R3100S027 Fuse Discrepancy

07/03/2020

20-27546

UPS B Appears to Have Repeat Failure of Battery Fuse

07/02/2020

20-27855

UPS A and B Fuse Ratings

07/09/2020

20-31438

Material Found at Bottom of Condensate Storage Tank

10/20/2020

20-31468

18-inch Pipe Clamp Bolt Length Issue

10/21/2020

20-31488

Threaded Rod Set Screw Too Short

10/21/2020

Drawings

M-5715-3

EDP-80127-018

M-5721-1

EDP-80127-006

M-Y-2000

EDP-80127

A

Engineering

Changes

80127

ECCS Pump CST Vortex Suppression Device

B

DEC 70303

UPS A/B DC Circuit Fuses and Cables

A

DEC 70304

UPS B Parallel Operation Software Change

EDP 70042

UPS A and B Replacement

C

Miscellaneous

Risk Management

Plan

CST Vortex Suppression

10/19/2020

71111.19

Corrective Action

Documents

20-30561

Received 3D6, Division 1/2 Reactor Building Vent Exhaust

Rad Monitor Upscale Trip, RBHVAC Trip, and D1 SGTS

09/24/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20-30756

While Replacing Seals on RR Car Interlock Door, 4 Bolts

Failed While Removing Bolts

09/30/2020

20-30824

East and West Airlock Door Seal Long Term

Recommendations

10/01/2020

20-32018

RCIC Turbine Exhaust Rupture Disc Leak

11/06/2020

20-32205

NRC Identified: IST Program Testing Methodology for

E5100F011

11/13/2020

Drawings

6I721-2611

Reactor Building Main Control Room A/C Mode Selection

Division 1

AA

6I721-2611-10

Reactor Building Secondary Containment Isolation Signals

Division 1

T

6M721-2034

Core Spray System CSS Reactor Building

AS

6M721-2035

High Pressure Coolant Injection System Reactor Building

BP

6M721-2044

Reactor Core Isolation Cooling System

BE

6M721-2045

Reactor Core Isolation Cooling System Barometric

Condenser

AT

Miscellaneous

2A1354AR

Reactor Core Isolation Cooling System

Clearance:

D1100-000138

Jumper Out High High Trip of Division 1 Rad Monitor

11/13/2020

ERE 54575

Evaluate Suitability of Replacement Garlock 3400 Sheet

Gasket

VMR4-15

Continental Disc Corp

A

Procedures

23.206

Reactor Core Isolation Cooling System

104

24.206.01

RCIC System Pump and Valve Operability Test

44.030.073

ECCS - Reactor Recirculation Pump B DP, Division 1,

Channel B Calibration/Functional

46.206.001

RCIC Turbine Governor Control System Calibration

45A

Work Orders

231076

Replace MTU B31N614A - Tin Whisker Susceptible

Rosemont 710DY MTU

11/30/2020

2386240

Replace and Calibrate RCIC Speed Controller (EG-M)

11/02/2020

2386240

Replace and Calibrate RCIC Speed Controller (EG-M)

01/14/2015

43954320

Replace NIAS Isolation Valve P5000F403 Solenoid Valve

11/17/2020

43954342

Replace Time Delay Relays in P50P402B, D2 NIAS Dryer

Control Cabinet

11/17/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

53421010

Calibrate Pressure Switch RCIC Pump Suction Low

Pressure Trip

11/03/2020

54136663

Perform 24.206.01 RCIC System Pump Operability and

Valve Test at 1000 PSIG

11/05/2020

268801

Replace Division 2 S Control Air Compressor Unloading

Cylinder Solenoid Valve

11/17/2020

58734795

Troubleshoot/Replace Relay T41M80 in H21P296C

Causing 3D36 and RBHVAC Trip

11/02/2020

E967190100

Replace Secondary Containment Railroad SE Airlock Door

Inflatable Seal NE-6.6-EQMS.122

09/28/2020

E967190100

Replace Secondary Containment Railroad SE Airlock Door

Inflatable Seal

09/28/2020

T363180100

License Renewal Required Replace Secondary

Containment Railroad South Airlock Door Inflatable Seal

09/29/2020

71111.22

Corrective Action

Documents

20-32994

Procedure Enhancement to 24.203.02 and 24.203.03

Division 1 / 2 Core Spray Operability Test

2/16/2020

Drawings

6M721-2034

Diagram Core Spray System CSS Reactor Building

AS

Work Orders

53934688

Perform 24.307.16 Sec 5.1 EDG 13 Start and Load

Test-Slow Start

10/19/2020

54370155

Perform Quarterly Testing of N+1 Train Neptune Diesel

11/28/2020

54514769

Perform 24.203.03 Sec-5.2 Division 2 CSS Simulated

Automatic Actuation Test

2/16/2020

71114.04

Corrective Action

Documents

CARD 19-25318

Review EP-101 Revisions Using ACR Process to Determine

10CFR50.54(q) Applicability

07/15/2019

CARD 19-27058

Changes Needed to Improve EP-101

09/19/2019

CARD 19-28389

Error Made While Revising EP-101

11/04/2019

Miscellaneous

10CFR50.54(q) Screen Number 2019-69S

10/18/2019

10CFR50.54(q) Screen Number 2019-71S

10/17/2019

10CFR50.54(q) Screen Number 2019-72S

10/18/2019

10CFR50.54(q) Screen Number 2019-73S

10/18/2019

10CFR50.54(q) Screen Number 2019-74S

10/18/2019

10CFR50.54(q) Screen Number 2019-75S

10/18/2019

10CFR50.54(q) Screen Number 2019-76S

10/18/2019

10CFR50.54(q) Screen Number 2019-82S

10/18/2019

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

10CFR50.54(q) Screen Number 2019-87S

10/23/2019

10CFR50.54(q) Evaluation Number 2019-11E

10/18/2019

10CFR50.54(q) Screen Number 2019-88S

10/23/2019

10CFR50.54(q) Screen Number 2019-89S

10/23/2019

10CFR50.54(q) Screen Number 2019-90S

10/23/2019

10CFR50.54(q) Screen Number 2019-91S

11/01/2019

10CFR50.54(q) Evaluation Number 2019-15E

10/23/2019

Procedures

EP-101

Classification of Emergencies

2C

EP-101

Classification of Emergencies

EP-101

Classification of Emergencies

43A

EP-590

10CFR50.54(q) Screens and Evaluation

LP-ER-874-0001

CFR 50.54Q Compliance Reviews Training Lesson Plan

RERP

Fermi 2 Radiological Emergency Response Preparedness

Plan

Fermi 2

Radiological

Emergency

Response

Preparedness

Plan;

Revision 48

RERP

Fermi 2 Radiological Emergency Response Preparedness

Plan

71114.06

Procedures

EP-101

Classification of Emergencies

43A

71124.07

Calibration

Records

Radeco Model AVS-28A Calibration Form for Serial Number

6980

01/03/2020

Radeco Model AVS-28A Calibration Form for Serial Number

7570

01/03/2020

Radeco Model AVS-28A Calibration Form for Serial Number

7571

01/03/2020

Corrective Action

Documents

Resulting from

Inspection

20-31431

NRC Identified - Vegetation Sampling in ODCM Not

Consistent with Annual Report and Surveillances

10/20/2020

Miscellaneous

Offsite Dose Calculation Manual

Offsite Dose Calculation Manual

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

NRC-20-0027

Annual Radioactive Effluent Release Report and

Radiological Environmental Operating Report

04/29/2020

71124.08

Miscellaneous

NPRP-20-0044

Scaling Factor Report for Torus Debris

05/27/2020

Procedures

67.000.505

Survey and Movement of Waste Liners in the OSSF

1C

MRP15

Controlling Radioactive Material Outside the Plant

Radiologically Controlled Area

Shipping Records EF2-19-050

Resin Characterization and Shipping Package

08/28/2019

EF2-20-040

Torus Paint Chips Characterization and Shipment

04/21/2020

EF2-20-117

Resin Characterization and Shipping Package

09/30/2020

71151

Miscellaneous

Alert and Notification System Reliability Performance

Indicator Records

07/01/2019 -

09/30/2020

Emergency Response Organization Drill Participation

Performance Indicator Records

07/01/2019 -

09/30/2020

Drill and Exercise Performance - Performance Indicator

Records

07/01/2019 -

09/30/2020

71152

Corrective Action

Documents

07-23630

CDBI: UFSAR Anti-Vortex Methodology Non-Conservative

06/28/2007

18-28666

NRC Concern: Foreign Material Left in Drywell

10/23/2018

19-21822

NQA - EDG 14 Tubing Not Secured Per Design

03/08/2019

19-23328

NQA - Failure of Multiple Groups to Adequately Evaluate

the EDG 14 Clamp Issue and Associated Contributors

05/01/2019

19-23915

2019 DBAI: Methodology Error Found in MOV Torque

Calculation

05/21/2019

19-23915

2019 DBAI: Methodology Error Found in MV Torque

Calculation

05/21/2019

20-20867

Received 10D21 Division II EDG 14 Lube Oil Tank D Level

High/Low in MCR

01/24/2020

20-20876

Clarification of Design Basis Document R40-00 Needed

Regarding EDG Lube Oil Requirements

01/25/2020

20-21195

OCC Effectiveness Challenged During EDG 13 SSO

2/03/2020

20-21597

EDG 14 LO Sump Level High

2/12/2020

20-27717

EDG 14 Oil Sump Level HOOS

07/07/2020

20-28726

Emerging Trend in CAP Performance Gaps

07/28/2020

20-28753

Results of Drywell Closeout Walkdown

07/28/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

20-29742

Request a Revision to Planners Template: FO18

08/28/2020

20-29776

Revision to the RFO Plant Restoration Checklist

08/31/2020

20-31928

EDG Lube Oil Tank Low Level Alarm Less than Required

for 7-Day Run Time

11/03/2020

20-32446

NQA Audit 02-0112 Finding - Identified Gap Between Fermi

Corrective Action Program Performance and Standards

11/24/2020

20-32817

ODMI 20-007 has Incorrect LCO Completion Time

2/10/2020

Corrective Action

Documents

Resulting from

Inspection

20-31385

NRC Identified: CARD 20-28850 Closed Without Issue

Resolution

10/19/2020

20-32182

NRC Identified-Meeting Effectiveness

11/12/2020

20-32858

NRC Identified - NRC Question on CARD 20-28753

2/11/2020

21-20263

NRC Identified - NRC Semiannual PI&R Trend Review

Observations

01/08/2021

Miscellaneous

Fermi 2 Refuel

Outage 20

Plan of the Day

07/06/2020

MOP05

Operations Conduct Manual, Chapter 5 - Control of

Equipment

MQA11-200

Quality Assurance Conduct Manual Implementing

Procedure, Condition Initiation

1B

MWC13

Outage Nuclear Safety

Operations

Department

Expectation ODE-

Operator Challenges

Procedures

24.000.02

Shiftly, Daily, and Weekly Required Surveillances

159

71153

Corrective Action

Documents

20-31731

CRD Pump Suction Press Control Valve Issues

10/29/2020

20-31732

Received CRD Accumulator Trouble for HCU 22-15 due to

High Water Level

10/29/2020

Fire Plans

Troubleshooting

Plan

CARD 20-31731, WO 59092486, Component C1106C001B

Miscellaneous

Day Recharge

Report

CRD Accumulator Recharge Report

November

20

ARP 3D1

CRD Pump A/B Suction Pressure Low

ARP 3D13

CRD Hydraulic Temperature High

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operator Log

10/29/2020

SOER Log Report

11/06/2020

Procedures

20.106.01

CRD Hydraulic System Failure

21