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Category:NRC TECHNICAL REPORT
MONTHYEARML20136C8391996-02-29029 February 1996 Plant Status Rept,Turkey Point ML20136E0251995-11-0303 November 1995 Morning Rept 2-95-0092:licensee Announced,Nov 2,layoffs of 25 Employees at Plants in Fort Pierce,Fl & Nov 1 of 40 Employees at Plants in Florida City,Fl & Corporate Headquarters ML20136E2551995-01-0505 January 1995 Morning Rept 2-95-0004:licensee President Frank Resigned on 950104 & J Broadhead Will Assume Frank Duties on Iterim Basis ML20136E2711994-08-0808 August 1994 Morning Rept 2-94-0073:plants Announced That Listed Orgainzation Changes Will Become Effective 940901 ML20136E2831993-10-0101 October 1993 Morning Rept 2-93-0106:licensee Continues W/Corporate Cost Reduction Program,Including Nuclear Div.Staffing Reductions Being Announced Effective 931001 ML20136E3071993-09-20020 September 1993 Morning Rept 2-93-0096:mgt Changes Have Been Announced Affecting Licensee Organization & Plant Site,Effective 931001 ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20058A3561990-10-16016 October 1990 AEOD/T90-14, Seal Problems in Boric Acid Transfer Pumps ML20248F0001989-09-29029 September 1989 Debris in Containment Recirculation Sumps, Technical Review Rept ML20245B6061988-08-31031 August 1988 Inadequate NPSH in HPSI Sys in Pwrs, Engineering Evaluation Rept ML20204J6141988-08-31031 August 1988 AEOD/E807, Pump Damage Due to Low Flow Cavitation ML20196G5251988-06-15015 June 1988 Technical Review Rept T809, Blocked Thimble Tubes/Stuck Incore Detector ML20245H9601988-04-15015 April 1988 BWR Overfill Events Resulting in Steam Line Flooding, AEOD Engineering Evaluation Rept ML20148D0671988-03-17017 March 1988 Headquarters Daily Rept for 880317 ML20148B3291988-03-14014 March 1988 Headquarters Daily Rept for 880314 ML20196H6351988-03-0808 March 1988 Headquarters Daily Rept for 880308 ML20196G8881988-03-0303 March 1988 Headquarters Daily Rept for 880303 ML20147E3961988-01-0606 January 1988 Rept of Interview W/Rg Lagrange on 841206 & 14 to Discuss Info Contained in B Hayes 841017 Memo Identifying Series of Submittals Received from Util Between 1980 & 1984 ML20147E3211988-01-0606 January 1988 Rept of Interview W/Rg Lagrange to Discuss Gpu 830520 & s Re Environ Qualification equipment.Marked-up 850409 Statement from H Hukill Also Encl ML20237L3001987-08-24024 August 1987 AEOD/E709 Engineering Evaluation Rept Re Auxiliary Feedwater Trips Caused by Low Suction Pressure.Draft Info Notice Encl ML20235C9311987-06-23023 June 1987 Rept to ACRS Re Humboldt Bay Unit 3 - Core II ML20212F6581986-12-31031 December 1986 Technical Review Rept, Degradation of Safety Sys Due to Component Misalignment &/Or Mispositioned Control/Selector Switches ML20212D9091986-12-23023 December 1986 Localized Rod Cluster Control Assembly (Rcca) Wear at PWR Plants, Engineering Evaluation Rept ML20212B0321986-12-17017 December 1986 Emergency Diesel Generator Component Failures Due to Vibration, Engineering Evaluation Rept ML20214R4851986-10-0909 October 1986 Initial OL Review Rept for Seabrook Station Unit 1 ML20212K6641986-08-0707 August 1986 Inadvertent Recirculation Actuation Signals at C-E Plants, Technical Review Rept ML20206H0871986-03-0303 March 1986 Allegation Review Data Sheet for Case 4-85-A-013 Re Const Activities.Addl Info Requested from Alleger.Case Closed Due to Lack of Response.Related Info Encl ML20206H0761986-01-21021 January 1986 Allegation Review Data Sheet for Case 4-84-A-085 Re Alteration of Personnel Records.Based on Resolution of Allegation 4-84-A-094,case Closed ML20137X6151986-01-0909 January 1986 Engineering Evaluation of Deficient Operator Actions Following Dual Function Valve Failures ML20234F5601985-12-17017 December 1985 Draft Hazards Analysis ML20234F4751985-12-17017 December 1985 Licensing of Power Reactors by Aec ML20214T2211985-11-25025 November 1985 Initial OL Review Rept:Millstone Point Unit 3 ML20206H0621985-10-15015 October 1985 Allegation Review Data Sheet for Case 4-85-A-045 Re Inadequate Handling/Installation Procedures for Equipment, Vendor Control Programs & Spare Parts.Based on Insp Rept 50-482/85-22,case Closed ML20206H0371985-10-0202 October 1985 Allegation Review Data Sheet for Case 4-85-A-044 Re Lack of Effective QA Programs & QC Insps.Based on Insp Rept 50-482/85-22,allegation Closed IR 05000482/19850191985-09-30030 September 1985 Allegation Review Data Sheet for Case 4-85-A-050 Re Mishandling of Document Control Program.Concerns Addressed in Insp Rept 50-482/85-19.Dept of Labor & Allegation Cases Closed ML20206H0131985-09-27027 September 1985 Allegation Review Data Sheet for Case 4-84-A-076 Re Vague Administrative Procedures,Calibr Program Not Working,Test Engineer Authority & Harassment.Based on Insp Rept 50-482/85-03,case Closed ML20137B1231985-09-16016 September 1985 HPCS Sys Relief Valve Failures, Engineering Evaluation Rept ML20206G8431985-09-0303 September 1985 Allegation Review Data Sheet for Case 4-84-A-013 Re Improper Termination of Employee Due to Refusal to Weld Laminated Pipe.Welding non-safety Related.Case Closed on 850827.W/ 840315 Telcon Record & Addl Info IR 05000482/19850311985-08-28028 August 1985 Allegation Review Data Sheet for Case 4-85-A-077 Re 6 Rem Exposure in Containment Bldg Due to Pipe Break.Allegation Investigated During Insp 50-482/85-31 on 850715-19 & Found Unsubstantiated ML20206G7781985-08-27027 August 1985 Allegation Review Data Sheet for Case 4-84-A-195 Re Quality First.Fuel Load Issue Resolved in Insp Rept 50-482/85-10. Technical Issues to Be Resolved Prior to Full Power Licensing.Case Closed w/850815 Memo to File ML20206G8051985-08-27027 August 1985 Allegation Review Data Sheet for Case 4-84-A-114 Re Drugs Planted at Plant.Evidence Destroyed in Testing.Based on Insp Rept 50-482/85-03 & Mullikin 850429 Memo,Case Closed ML20209G3051985-08-0909 August 1985 Closure of ECCS Min Flow Valves, Engineering Evaluation Rept.Recommends IE Issue Info Notice to Remind Licensees of Importance of Min Flow Bypass Capability as Essential Pump Protection Feature ML20206H0801985-07-30030 July 1985 Allegation Review Data Sheet for Case 4-84-A-007 Re Intimidation of QC Inspector.Forwards Documents Closing Allegation.W/O Encls ML20206H1021985-07-30030 July 1985 Allegation Review Data Sheet for Case 4-84-A-008 Re Improper Const Practices.Insp Rept 50-482/84-12 Issued on 841012 & Closeout Ltr Sent on 850405 ML20147E4401985-06-20020 June 1985 Rept of Interview W/Cw Smyth on 850510.Smyth Advised of Unfamiliarity W/Environ Qualification Program in Technical Sense & W/Documentation Needed to Qualify Individual components.Marked-up Lw Harding Statement Encl ML20199G0701985-05-0303 May 1985 Partially Withheld Statement of Decision Re Allegation AQ-38 Concerning Alleged Harassment of QC Inspectors Upon Observation of Weld Defects on vendor-inspected Restraints. Allegation Substantiated.Addl Allegation Repts Encl ML20147H0101985-04-16016 April 1985 Draft Summary Rept for Regional Evaluation of Texas Utils Electric Co,Comanche Peak Steam Electric Station ML20206G9151985-03-12012 March 1985 Allegation Review Data Sheet for Case 4-84-A-015 Re Harassment of Mechanical/Welding QC Inspector for Writing Nonconformance Rept Re Improper Welding Amperage by Superintendent.Util Rept Issued & Case Closed ML20147G9901985-01-31031 January 1985 Summary Rept for Regional Evaluation of Texas Utils Electric Co,Comanche Peak Steam Electric Station ML20205Q7691985-01-18018 January 1985 Status Rept Mechanical/Piping Area. Related Info Encl 1996-02-29
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program ML17355A4471999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With 991008 Ltr ML17355A4121999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With 990909 Ltr ML17355A3981999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 990809 Ltr ML17355A3891999-07-20020 July 1999 LER 99-001-00:on 990623,manual Rt from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With 990720 Ltr ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept. ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3841999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With 990713 Ltr ML17355A3511999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With 990609 Ltr ML17355A3331999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Turkey Point,Units 3 & 4.With 990511 Ltr ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18. ML17355A2911999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With 990414 Ltr ML17355A2551999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With 990315 Ltr ML17355A2261999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With 990211 Ltr ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept. ML20206P1501999-01-0505 January 1999 LER 98-S03-00:on 981207,security Officer Discovered Uncontrolled Safeguards Info Drawing.Caused by Failure to Follow Established Procedures & Policies.Drawing Was Controlled by Site Security.With ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML17355A1911998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With 990112 Ltr ML20198E6381998-12-17017 December 1998 LER 98-S02-00:on 981130,security Access Was Revoked Due to Falsification of Criminal Record.Individual Was Escorted from Protected Area & Unescorted Access Was Restricted. with ML18008A0461998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 981209 Ltr ML17354B1921998-11-18018 November 1998 LER 98-007-00:on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With 981118 Ltr ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2. ML17354B1901998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 981112 Ltr ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17. ML17354B1361998-10-16016 October 1998 LER 98-004-00:on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With 981016 Ltr ML20153G4601998-09-30030 September 1998 USI A-46 Seismic Evaluation Rept, Vols 1-2 ML17354B1311998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With 981012 Ltr ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML15261A4681998-09-0404 September 1998 Safety Evaluation Supporting Amends 232,232 & 231 to Licenses DPR-38,DPR-47 & DPR-55,respectively ML17354B0981998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With 980915 Ltr ML17354B0771998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4.W/980810 Ltr ML17354B0341998-07-15015 July 1998 LER 98-003-00:on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves ML17354B0241998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4.W/980709 Ltr ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire. ML17354A9841998-06-18018 June 1998 LER 97-007-01:on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps ML17354A9741998-06-0909 June 1998 LER 98-002-00:on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9711998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4. W/980611 Ltr ML17354A9231998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4.W/980511 Ltr ML17354A8821998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4.W/980409 Ltr ML17354A8511998-03-24024 March 1998 LER 97-009-01:on 971114,discovered That CR Console Switch for 3B Sgfp Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR ML17354A8441998-03-18018 March 1998 LER 98-001-00:on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be revised.W/980318 Ltr ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 ML17354A8311998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Turkey Point,Units 3 & 4.W/980311 Ltr ML17354A7871998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Turkey Point,Units 3 & 4.W/980209 Ltr ML20247L9041997-12-31031 December 1997 1997 Annual Rept for Duke Energy Corporation & Saluda River Electric Cooperative,Inc,Financial Statements as of Dec 1997 & 1996 Together W/Auditors Rept ML17354A7581997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Turkey Point,Unit 3 & 4.W/980112 Ltr ML17354A7361997-12-12012 December 1997 LER 97-009-01:on 971114,identified That CR Console Switch for 3B SG Feedwater Pump Was Not in Start Position.Caused by Inadequate Procedural Guidance.Procedures 3/4-OP-074,SGFP Were revised.W/971212 Ltr ML17354A7381997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Turkey Point,Units 3 & 4.W/971215 Ltr 1999-09-30
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AEOD/E803 ENGINEERING ' EVALUATION REPORT INADEQUATE NPSH IN HIGH PRESSURE SAFETY INJECTION SYSTEMS IN PWRs August, 1988 Prepared by: Sanford Israel Office for Analysis and Evaluation of Operational Data J U.S. Nuclear Regulatory Cornmission 8904260181 esogop PDR I
.ORG NEXD PDC '
t i .
- .0 INTP.000CTION i Two recent reports highlighted a potential problem of inadequate net positive l suction head (NPSH) for high pressure safety injection pumps during the recir-l- culation phase following a loss of ccolant accident. This problem is the same l
issue reported in Ref.1 on inadequate NPSP for low pressure safety systems in PWRs. An information notice (IN 87-63), published in December 1987, addressed the low pressure pump NPSH concern. The Sequence Coding and Search System was used in this present study, but did not provide any additional events beyond those found in the inspection reports.
2.0 ~ DESCRIPTION OF EVENTS
! The following events were reported as 10 CFR 50.72, immediate notification l
reports. '
Turkey Point, May 13, 1988 As part of an ongoing design basis reconstitution, the licensee discovered a condition of potential inadequate NPSH for the containment spray and high pressure safety injection pumps during the recirculation mode following a LOCA l
(Fef. 2). Under these conditions, the low head safety injection pump is providing coolant to the containment spray pumps and the high pressure safety ir.jection pumps. A throttle valve in the P.HR discharge line is normally throttled to 30 percent. This valve was opened completely while the licensee conducted an engineering analysis of the situation. Subsequent evaluation showed the original configuration to be acceptable.
Oconee, May 19, 1988 During the review of safety analysis calculation files, the licensee discovered S a set of conditions that could defeat the recirculation function following certain small break LOCAs (Ref. 3). Under these conditions, the low pressure ir.jection system provides suctica flow to the containment spray system and the high pressure injection pumps in a piggyback mode. With inadequate procedural guidance, the flow configuration may result in inadequate NPSH for the high pressure pumps and thus fail the system. The licensee is modifying appropriate emergency procedures to correct the problem.
3.0 ANALYSIS AND EVALUATION In many plants, the high pressure safety injection (HPSI) pumps and, in some ,
cases, the containment spray system is "piggybacked" on the discharge of the !
low head safety injection pumps during the recirculation phase following a small break LOCA. This situation occurs where the low head pumps can not '
provide core cooling directly because the reactor vessel has not depressurized sufficiently. The design discharge pressure for the low head pumps, which is on the order of 100 psi, should be sufficient to provide adequate NPSH for the high head pumps in the " piggyback" mode for reasonable installations. This apparently is not the case at all plants.
-2 A typical ECCS installation of interest is shown in the enclosed figure. A crossover line downstream of the decay heat coolers connects the discharge of the low head safety injection pumps to the containment spray pumps and the HPSI pur;ps . There may be a throttle valve located in this crossover line in some plant designs such as Turkey Point.
NPSH deficiencies may be incurred because of several different factors.
Running multiple pumps off the discharge of a single pump may increase the flow above design flow rate and consequently reduces the available pressure at the low head pump discharge because of the characteristic pump performance curve.
Another factor is the as-built cross connect piping between the low head pump and the high head pump which may have higher resistance than originally considered in the design calculations because of the length and size of the piping and any intervening partially closed throttle valves. Thus, the actual ;
attainable pressure at the high head pump inlet during recirculation conditions {
may be less than the design estimate.
Another aspect of this problem is that preoperational flow tests were not performed with the ECCS aligned in the recirculation mode. According to the updated FSARs, the recirculation tests are performed with the pumps blocked to evaluate system realignment, not functional capability. It would be difficult to run a full blown flow test that included the containment spray pumps as well.
Post-operational surveillance tests suffer from the same limitations. The extent to which the results of partial flow tests have been used to confirm the design basis conditions is unknown. Retrieval of archival documents related to these ,
calculations is fragmentary, so that their robustness may not be easily ascertained.
The discovery of the potential deficiency in NPSH at Turkey Point and Oconee was the cutcome of post-operational programs to reconstitute design calculations.
In one instance, the effort was prompted by comments in an NRC inspection report on a totally unrelated fluid system. The utility took the initiative to explore similar deficiencies in other systems. It is doubtful that these deficiencies would have been uncovered without these specific investigations by the utilities.
Inadecuate NPSH causes cavitation which ultimately results in pump failure. The high pressure safety injection system is essential for mitigating small break LOCAs and at some plants, it is used for hot leg recirculation even for large LOCAs. Thus, loss of this system in the recirculation mode would represent a significant reduction in safety margin.
i 4.0 FINDINGS AND CONCLUSIONS l l
- 1. Two utilities have discovered that their high pressure safety injection )
system may have inadequate NPSH during the recirculation phase following ]
a LOCA. j l
i
- 2. Plant specific piping arrangements and the presence of throttling valves between the low head pumps and the high head pumps contribute to the deficiencies in NPSH.
- 3. Potential deficiencies in NPSH for high head pumps will go undetected because the surveillance tests, including preoperational tests, do not test the complete ECCS in the recirculation mode. i
)
_ _ _ _ _ - . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - . _ _ _ _ _ _ . _ . - - - - - _ _ . . _ _ _ _ - . . _ . _ _ _ _ _ _ _ _ _ _ - . . . - - - - _ _ _ - . _ .J
5.0 REFERENCES
- 1. Memorandum from T. Novak (AE00) to C.E. Rossi (NRR), " Inadequate NPSH in L Low Pressure Safety systems in FWRs", AE00/710, dated October 7, 1988.
- 2. Immediate Notification 50.72 Report No.12278, Turkey Point plants, dated May 13, 1988.
- 3. Immediate Notification 50.72 Report No. 12326, Oconee plants, dated May 19, 1988.
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UNITED STATES j NUCLEAR REGULATORY COMMISSION 0FFICE OF NUCLEAR REACTOR REGULATION.
WASHINGTON, O. C. 220555 August , 1988 INFORMATION NOTICE NO. 87-63, SUPPLEMENT 1: INADEQUATE NET POSITIVE SUCTION j HEAD IN LOW PRESSURE SAFETY SYSTEMS 1
)
' Addressees.
All pressurized water reactors holding an operating license or a construction j pennit. ;
Purpose:
Ir. formation Notice 87-63 provided information to the addressees about inadequate NPSH in low pressure safety systems because of. deficiencies in design, installa-tion, or operation of these systems. This supplement extends this concern to high pressure safety injection systems in certain PWRs which " piggyback" the HFSI pumps off the low head pumps in the recirculation phase following a LOCA.
Fecipients are expected to review the information provided for applicability to their facilities and consider actions, if appropriate, to preclude similar occurrences at their plants. However, suggestions contained in this information netice do not constitute NPC requirements; therefore, no specific action or written response is required.
Discussion: -
Recently, two different utilities reported potential deficiencies in the NPSH fer HPSI pumps when operating in the recirculation mode following a LOCA. In bcth instances, the HPSI would be "piggybacked" off the low pressure pumps dLring the recirculation phase. Although the low head pumps provide relatively high discharge pressure, the intervening cross-connect piping between the HPSI ar.d the low head pumps and partially closed throttle valves provide sufficient hydraulic resistance to cause potential problems at the HPSI pump inlets.
Corrections include opening partially closed throttle valves and procedure modifications to improve the hydraulic characteristics of the ECCS in the recirculation mode. This is a significant safety concern because of the reliance on HPSI for mitigating small LOCAs and in some cases, they are used fer hot leg recirculation even for large LOCAs. No specific action or written response is required by this information notice. If you have any questions about this matter, please contact the technical contact listed below or the Regional Administrator of the appropriate regional office.
Charles E. Rossi, Director Division of Operational Events Assessment Office of Nuclear Reactor Regulation Technical
Contact:
S. Israel, AE0D 301 492-4437