05000364/LER-1982-028

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LER 82-028/01T-0:on 820609,markings for Trains a & B Svc Water Cooling Valves Found Reversed.Caused by Personnel Error in Installing Permanent Labels.Labeling Error Corrected
ML20054K120
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 06/24/1982
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20054K115 List:
References
LER-82-028-01T, LER-82-28-1T, NUDOCS 8207010100
Download: ML20054K120 (1)


LER-2082-028,
Event date:
Report date:
3642082028R00 - NRC Website

text

, LICENSEE EVENT REPORT

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[Hij l At 2200 on 6-9-82, it was determined that "A" train _ and "B" train __Seryice_. water _ cooling ]

g j q [ valves associated with the swing charging pump were mislabeled i.e. "A" train marked as_j g g ["B" train and vice versa. As a result, the swing charging pump may have failed under I gjg [certain postulated accidents as described in the FSAR. An extensive investigation _j

[ g l revealed that since initial operation of Unit 2, the swing charging pump was designated j as one of two operable charging pumps only during the period from 5-1-81 through 5-18-81.

[1B LDur_in_g the yeriod from 5-1-81 to 5-13-81uthe unit did not exceed five percent reactor __J g[g l power. Health / safety of the public was not affected. J SvSl f fM C AI JSL C At l,( CGW. VALVE CODE COOL SinCOt r E CO*.*F O'.r f.T COUL SUb CO DE SUiCCDE ELBn LaLel69 LAlO LBJ@ L2LzLzLzt2! J@ lz l@ Lz_j i t' D

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g-g gand #2. The labeling error has been corrected. l 7 b 9 83 GI All L PGl.lfi ()1 Hl H Si A T US 1 f DISCOVE HY t' '" cmp TION IEEl IJJ@ LIL 0_LOJ8!_ NA I LAl@! oper_a_tional Event  !

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