IR 05000346/2005006

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IR 05000346-05-006; 4/1/2005 - 5/13/2005; Davis-Besse Nuclear Power Station; Routine Integrated Inspection Report, Including Special Inspection Related to Confirmatory Order
ML051640125
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 06/10/2005
From: Reynolds S
NRC/RGN-III
To: Bezilla M
FirstEnergy Nuclear Operating Co
References
EA-03-214 IR-05-006
Download: ML051640125 (28)


Text

une 10, 2005

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION NRC INTEGRATED INSPECTION REPORT 05000346/2005006

Dear Mr. Bezilla:

On May 13, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Davis-Besse Nuclear Power Station. The enclosed inspection report documents the inspection findings which were discussed on May 19, 2005, with you and other members of your staff. Additionally, this inspection report documents special inspection activities to ensure your compliance with the March 8, 2004, Confirmatory Order (EA 03-214).

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

For the entire inspection period, Davis-Besse was under the Inspection Manual Chapter 0350 Process. The Davis-Besse Oversight Panel assessed inspection findings and other performance data to determine the required level and focus of followup inspection activities and any other appropriate regulatory actions. Even though the Reactor Oversight Process had been suspended at Davis-Besse, it was used as guidance for inspection activities and to assess findings.

Based on the results of this inspection, the NRC has determined that no violations of NRC requirements occurred. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Steven A. Reynolds Chairman Davis-Besse Oversight Panel Docket No. 50-346 License No. NPF-3

Enclosure:

Inspection Report 05000346/2005006 w/Attachment: Supplemental Information

REGION III==

Docket No: 50-346 License No: NPF-3 Report No: 05000346/2005006 Licensee: FirstEnergy Nuclear Operating Company (FENOC)

Facility: Davis-Besse Nuclear Power Station Location: 5501 North State Route 2 Oak Harbor, OH 43449-9760 Dates: April 1 through May 13, 2005 Inspectors: S. Thomas, Senior Resident Inspector J. Rutkowski, Resident Inspector M. Salter-Williams, Resident Inspector G. Wright, Project Engineer R. Landsman, Project Inspector, Decommissioning Branch M. Maymi, Reactor Inspector Region II J. Persensky, Office of Research M. Keefe, Office of Research J. Cai, NRR Approved by: C. Lipa, Chief Branch 4 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000346/2005006; 4/1/2005 - 5/13/2005; Davis-Besse Nuclear Power Station; Routine

Integrated Inspection Report, including special inspection related to Confirmatory Order.

This report covers a 6 week period of resident inspection, including special inspection related to the March 8 Confirmatory Order. The inspection was conducted by staff from NRR and Research, a Region II inspector, Region III inspectors, and resident inspectors. No findings of significance were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector-Identified and Self-Revealed Findings No findings of significance were identified.

B. Licensee-Identified Findings No findings of significance were identified.

REPORT DETAILS

Summary of Plant Status

At the beginning of the inspection period, the plant was operating at approximately 100 percent power. During this inspection period, brief planned power reductions of less than 10 percent occurred on two occasions (April 17th and May 8th) to support planned testing. On each occasion, the testing was completed and power was restored to approximately 100 percent.

The plant operated at approximately 100 percent power for the remainder of the inspection period.

For the entire inspection period, the Davis-Besse Nuclear Power Station was under the IMC 0350 Process.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors reviewed the licensees restoration of systems from cold weather preparations and the licensees preparations for hot weather operations. The inspectors reviewed the licensees procedural requirements and sampled equipment status for restoration from cold weather valve and ventilation alignments. Additionally, the inspectors, after reviewing the procedural status of preparations for hot weather operations, interviewed operations personnel on their progress towards completion of the preparations. This included questioning the time period assumed in the licensees procedure for completion of hot weather preparations.

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors reviewed equipment alignment to identify any discrepancies that would impact the function of system components. The inspectors also reviewed if the licensee had properly identified and resolved any equipment alignment problems that could cause an initiating event or impact the availability and functional capability of the mitigating system. Documentation reviewed to determine the correct system lineup included plant procedures, drawings, and the Updated Safety Analysis Report (USAR).

During the walkdown, the inspectors also evaluated the material condition of the equipment to identify if there were significant conditions not already in the licensees corrective action system. The following samples were selected:

  • April 14, 2005, high pressure injection system train 2 (while high pressure injection train 1 was inoperable and unavailable for scheduled maintenance activities);
  • April 21, 2005, decay heat system train 2 (while decay heat train 1 was inoperable and unavailable due to scheduled maintenance activities); and
  • May 3, 2005, high pressure injection system train 1 (while high pressure injection train 2 was inoperable and unavailable for scheduled maintenance activities).

This constitutes four samples.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted fire protection inspections focused on the availability, accessibility, and condition of fire fighting equipment, the control of transient combustibles, and the condition and status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events, and their potential to impact equipment which could initiate a plant transient. Inspectors checked that fire hoses and extinguishers were in their designated locations and available for immediate use, that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits, and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition.

The following areas were inspected:

  • Mechanical penetration room 4 (Fire Area A, Room 314);
  • Diesel generator 1-2 room (Fire Area J, Rooms 319 and 319A);
  • Auxiliary building elevation 545' and 555' passageway (Fire Area A, Rooms 110 and 110A);
  • Borated water storage tank pipe tunnel, (Fire Area B, Rooms 100 and 101); and
  • ECCS pump room 1-1, (Fire Area AB, Room 105).

This constitutes five samples.

b. Findings

No findings of significance were identified.

1R06 Flood Protection - External Flooding

a. Inspection Scope

The inspectors evaluated the potential for flooding from external factors by reviewing plant design parameters pertinent to controlling the potential for flooding from external means. The evaluation included a review to check for deviations from the descriptions provided in the USAR for features intended to mitigate the potential for flooding from external factors. As part of this evaluation, the inspectors reviewed the conditions of roof drains on the auxiliary building and checked for obstructions that could prevent draining and checked that the roofs did not contain obvious loose items that could clog drains in the event of heavy precipitation. Additionally, the inspectors walked down portions of accessible auxiliary building interior roof drain lines to observe if the pipes were intact.

The inspectors also reviewed the visible condition of sewer and culvert drains that surrounded the units power block.

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

a. Inspection Scope

On April 19, 2005, the inspectors observed operating crews during simulator annual requalification training associated with an emergency plan exercise and attended the post-session licensee controller critique. The inspectors reviewed crew performance in the areas of:

  • Clarity and formality of communications;
  • Ability to take timely action in a safe direction;
  • Ability to prioritize, interpret and respond to alarms;
  • Procedure use;
  • Oversight and direction from supervisors; and
  • Group dynamics.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in Davis-Besse operational and administrative procedures.

The operational scenario included a reactor coolant system small break with a subsequent loss of offsite power.

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 480 Volt AC System

a. Inspection Scope

The inspectors reviewed the licensees handling of performance issues associated with the 480 V AC system, specifically the failures of breakers BEF122, BE314, B25Q25, loss of buses F4 and F6, and manual de-energization of motor control center E21A. The inspection consisted of evaluating the following specific activities:

  • The licensees use of the condition report process in identifying deficiencies and issues with 480V AC system equipment;
  • Whether equipment performance issues were correctly categorized per the systems scoping sheet performance criteria for reliability;
  • Whether the licensee was effectively tracking key parameters and recognizing trends for 480V AC system condition monitoring failures;
  • Appropriateness of goals and corrective actions for the long-term reliability;
  • Whether the licensees corrective actions included extent of condition; and
  • Appropriateness of maintenance rule system status classification and current reclassification appeared appropriate for the equipments recent history.

This constitutes one sample.

b. Findings

No findings of significance were identified.

.2 345 kV Switchyard Components

a. Inspection Scope

The inspectors reviewed the licensees handling of material condition issues associated with the 345 kV switchyard, specifically the spalling and freeze cracking of concrete caissons, soil drainage, and an air brake misalignment. The inspection consisted of evaluating the following specific activities:

  • The licensees use of the condition report process and work order notification system in identifying deficiencies and issues with switchyard equipment;
  • Whether observed deficiencies were captured in either the condition report system or the work order system;
  • Appropriateness of short term corrective actions for deficiencies with potential for significant operator workarounds;
  • Whether equipment performance issues were correctly categorized per the systems scoping sheet performance criteria for reliability
  • Appropriateness of goals and corrective actions for the long-term reliability;
  • Whether the licensees corrective actions included extent of condition; and
  • Appropriateness of maintenance rule system status classification and current reclassification of equipments recent history; Additionally the inspectors performed a walkdown of the switchyard and discussed future corrective actions with the system engineer.

This constitutes one sample.

b. Findings

No findings of significance were identified.

.3 Control Room Emergency Ventilation System

a. Inspection Scope

The inspectors used an issue/problem oriented approach to identify performance problems associated with the control room normal chillers S12-1 and S12-2. The control room normal ventilation system provides a supporting function to the control room emergency ventilation system during a high radiation event. The normal ventilation system can be placed in recirculation mode to prevent the potential in leakage of toxic gases or a radiological release. On several occasions, the control room normal chillers S12-1 and S12-2 tripped during the spring and summer months resulting in increased temperatures in the control room. The inspectors reviewed performance history, work orders and corrective and preventive maintenance documents to independently assess the extent of condition and to determine to what extent the problems may affect other systems. The inspectors reviewed condition report and work orders to determine if observed deficiencies were captured in the condition report system or the work order system and whether goals and corrective actions for the long-term reliability were appropriate. In addition, the inspectors walked down the system and evaluated whether the maintenance rule system status classification and current reclassification appeared appropriate for the equipments recent history.

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the licensees response to risk significant activities. These activities were chosen based on their potential impact on increasing overall plant risk.

The inspections were conducted to determine whether the planning, control, and performance of the work were done in a manner to reduce overall plant risk and minimize the duration where practical, and that contingency plans were in place where appropriate. The licensees daily configuration risk assessments, observations of shift turnover meetings, observations of daily plant status meetings, and the documents listed at the end of this report were used by the inspectors to verify that the equipment configurations had been properly listed, that protected equipment had been identified and was being controlled where appropriate, and that significant aspects of plant risk were being communicated to the necessary personnel. The inspectors evaluated the following licensee activities:

  • The licensees initial response and long term corrective actions associated with the discovery of a misaligned headshaft sleeve on an operating service water pump, on March 4, 2005;
  • The licensees response to an unexplained increase (approximately 0.200 gallons per minute) in unidentified reactor coolant system leakage, on April 9, 2005;
  • The licensee experienced a test failure of the relays that sense the loss of a auxiliary feedwater sources to the pump and provide input signals to the control scheme for the steam supply valves to the auxiliary feedwater turbine during planned surveillance testing of auxiliary feedwater water system train 1, on April 19 and 20, 2005;
  • The licensee entered an Orange risk condition with train 1 emergency core cooling equipment inoperable due to stroking close decay heat valve 7B which isolated train 1 equipment from the borated water storage tank, on April 21, 2005;
  • The licensee response to cloudy oil samples taken from high pressure injection pump 2 and subsequent draining of the pumps lube oil system, on May 4, 2005; and
  • The licensee entered an Orange risk condition due to the unavailability of the motor driven feed pump while replacing breaker AD 210, on May 6, 2005.

This constitutes six samples.

b. Findings

No findings of significance were identified.

1R16 Operator Workarounds

a. Inspection Scope

The inspectors performed a review of all the existing operator workarounds and control room deficiencies to determine whether their cumulative affect had a significant impact on plant risk or on the operators ability to respond to a transient or an accident. This involved reviewing all documented operator workarounds, control room deficiencies, and shift turnover sheets. In addition, the inspectors interviewed operators and licensee staff to determine whether the licensee had appropriately classified the significance of the workarounds and deficiencies, that the workarounds were achievable, and whether the licensee had initiated the appropriate corrective actions, commensurate with the significance of the deficiency or workaround. The inspectors also reviewed the impact of licensees program being controlled in accordance with a guideline and not a procedure.

In addition to evaluating the individual impact of each operator workaround, the inspector evaluated the cumulative effect of all workarounds on plant safety.

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed post-maintenance testing activities to determine whether the testing adequately verified system operability and functional capability with consideration of the actual maintenance performed. The inspectors referenced the appropriate sections of the Technical Specifications (TSs), the USAR, as well as the documents listed at the end of this report, to evaluate the scope of the maintenance and see that the work control documents required sufficient post-maintenance testing to adequately demonstrate that the maintenance was successful and that operability was restored.

The inspectors observed and evaluated test activities associated with the following sample:

This constitutes one sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed the surveillance test or evaluated test data to determine whether the equipment tested met TSs, Updated Safety Analysis Report, and licensee procedural requirements, and also demonstrated that the equipment was capable of performing its intended safety functions. The inspectors used the documents listed at the end of this report to determine whether the test met the TS frequency requirements; the test was conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; the test acceptance criteria were met; and the results of the test were properly reviewed and recorded. The following surveillances were evaluated:

C DB-SC-03071, Emergency Diesel Generator 2 Monthly Test, Revision 07, on April 7, 2005; and C DB-ME-03046; D1 Bus Under Voltage Units Monthly Functional Test, Revision 06, on April 8, 2005.

This constitutes two samples.

b Findings No findings of significance were identified.

EP6 Drill Evaluation

a. Inspection Scope

The inspectors monitored the licensees emergency preparedness exercise conducted on April 19, 2005, from various locations and perspectives. The observations included licensee preparations, evaluation of drill conduct, review of the drill critiques, and the identification of weaknesses and deficiencies. The inspectors reviewed the licensees scenario and preparations to determine if the drill evolution was of appropriate scope to be included in the performance indicator statistics. The inspectors observed drill activities and personnel performance in the simulator control room, the technical support center, and the emergency operating facility. The inspectors evaluated the effectiveness of the licensees communications, the accuracy of situation evaluations, and the timeliness of required reporting (simulated) of event related information to the appropriate agencies. Finally, the inspectors reviewed the licensees drill critique to determine whether weaknesses and deficiencies were acknowledged and appropriate corrective actions identified.

This constitutes one sample.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA2 Identification and Resolution of Problems

.1 Daily Review

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and in order to help identify any repetitive equipment deficiencies or specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees corrective action program. This screening was accomplished by reviewing documents entered into the licensee corrective action program and review of document packages prepared for the licensees daily Management Alignment and Ownership Meetings.

b. Findings

No findings of significance were identified.

.2 Small Bore Piping Condition Report - Annual Sample

a. Inspection Scope

The inspectors chose for review condition report CR 05-00750 (Incorrect Pipe Support Installation) and performed a detailed review of an issue involving small bore piping supports. Various support configurations had been installed using a simplified design methodology. The inspectors reviewed the extent of issue identification through review of condition reports, extent of condition evaluations, operating experience, and operability evaluations. The inspectors also reviewed specified corrective actions for appropriateness, completeness, and if identified issues were addressed in a timely manner.

b. Findings and Observations

The issue was initially identified when it was observed that a pipe support on the reactor coolant pump seal injection line was different than that shown on the drawing. The licensee initiated a condition report (CR 05-00750) which eventually led to an extent of condition investigation and generation of an operability evaluation to address the conditions found. The extent of condition review found other conditions that needed to be reviewed. Overall, the licensee concluded that some discrepancies in construction and some assumptions used in the original design of small bore piping, while not sufficient to cause loss of function in the reviewed piping, could result in potential or actual over-stress condition under maximum thermal load conditions.

The licensees original design criteria stated that small bore piping systems that have service conditions less than 500F (low carbon and low alloy systems) or 400F (stainless steel), did not need to have a rigorous computer analysis but could be analyzed with a less rigorous approach that was assumed to be conservative for seismic loading. This original methodology has been replaced, in current design efforts, by a more rigorous approach.

The original identified issue was resolved with physical changes to the supports on the reactor coolant pump seal injection lines. The licensee completed an operability evaluation for the other conditions, identified by the extent of condition review, where potential overstress conditions might develop. The operability evaluation was initially reviewed in IR 05000346/2005002. The licensee initiated corrective actions to perform reviews of existing calculations for some piping and perform pipe stress analysis for others where a thermal stress issue may exist. These actions were scheduled to be completed by July 13, 2005.

The licensees corrective actions are adequate to address the issue and no findings of significance were identified during the evaluation of this issue.

.3 Elevated Reactor Coolant System (RCS) Unidentified Leakage - Annual Sample

a. Inspection Scope

The inspectors chose to review Condition Report 05-02165, RCS Unidentified Leakage Rise from Approximately 0.024 to 0.26 gpm, and the licensees response to the identified condition. The inspectors reviewed the licensees program documents governing RCS leakage rate monitoring and the responses to increased leakage and compared the licensees actions to their program requirements. This included the licensees criteria for entering and exiting the licensees defined action levels associated with unidentified RCS leakage. Additionally, the inspectors reviewed the licensees condition report system for recent condition reports describing conditions that might affect RCS leakage rate or the leakage rate program.

b. Findings and Observations

The condition was initially identified on April 9, 2005, when control room personnel noted an increase in containment sump pump-out rate. Subsequent to that observation, the control room operators, using existing procedures, determined that the RCS unidentified leakrate had increased, in about one day, from approximately 0.024 gpm to 0.26 gpm.

The licensees Technical Specification limit for unidentified leakage is 1.0 gpm. The licensees leakage rate measurement program has significantly lower limits that trigger investigations and other actions designed to determine the source of the leakage.

The licensee formed a problem solving team that gathered the known facts and developed a problem solving plan. That plan included listing potential leak sources and locations and implementing followup activities which included actions that were specified in NG-EN-00327 (RCS Integrated Leakage Program). Procedure NG-EN-00327 specifies 3 Action Levels, in addition to normal operation, that are triggered by sustained step changes in leak rate, specified rate of changes in leak rate, or by cumulative leakage. The observed change in leak rate was sufficient to trigger the licensees highest action level, Action Level three.

In addition to reviewing potential leakage paths outside of the reactor containment, the problem solving plan included a containment entry at power. The data from that entry, combined with the results from inspections external to containment, led the licensee to conclude that the increase in leakage was due to leakage through one or more sets of RCS manually operated drain valves. These drain valves are hard-piped to a drain header, which can be aligned to a drain tank outside containment. The physical location of the drain valves within containment precludes operating them during full power operation.

The licensee, through discussions with the valve vendor and other utilities, found that there is industry experience showing that RCS drain valves, if checked closed at RCS temperatures lower than normal RCS operating temperature, have developed seat leakage as the valve heats up and expands. The licensee had procedure requirements to verify several drain isolation valves closed when RCS temperature exceeded 355 degrees F. They initiated a condition report to change the closure verification to be when RCS temperature was at or above 500 degrees F.

Since the licensee believed they had identified the source of the leakage, that the leakage was being collected in a closed system, and that the leakage could be measured, the licensee, using existing procedures, developed the documents necessary under their program, to reclassify the measured leakage through the drain valves as identified instead of unidentified. The licensees technical specification limit for identified leakage is 10 gpm. The licensee stated that they were reclassifying this leakage as identified leakage, as allowed by their procedures, to maintain sensitivity to new changes in unidentified leakage.

Throughout the event, the licensee demonstrated actions consistent with their procedural requirements and with an appropriate sensitivity to unidentified RCS leakage.

The licensees program provides for action level entries at unidentified leakage rates significantly below technical specification limits and the licensee took action when trigger levels were exceeded. The licensees program permitted the exit from action levels if leakage rates did not show a continuing upward trend.

There were no findings of significance identified during the evaluation of this issue.

4OA5 Other Activities

.1 Operation of an Independent Spent Fuel Storage Installation (ISFSI) (60855.1)

a. Inspection Scope

The inspectors evaluated the licensees monitoring of dry fuel storage to verify that the concrete temperatures remained within long-term storage limits. The inspectors verified that the monitoring (visual inspection that the vent screens are clear and thermocouple readings) was performed as specified in the site surveillance test procedure, DB-NE-03400, Horizontal Storage Module (HSM) Monitoring. The inspectors also reviewed data for the three HSMs, and compared it to the requirements specified in the Certificate of Compliance, the TSs, and the Safety Analysis Report.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

Following restart authorization, Inspection Procedure 93812 remained in effect to facilitate the inspection and documentation of issues that were not specifically covered by existing procedures, but were important to the evaluation of the licensees performance post-restart. This inspection procedure remains in effect as part of the integrated resident inspection report until a time to be determined by the Davis-Besse Oversight Panel.

.1 Review Submitted Calendar Year 2005 Independent Assessment Plan for the Corrective

Action Program

a. Inspection Scope

As part of the inspection activities performed to verify the licensees compliance with the requirements for independent assessments, as described in the March 8, 2004, Confirmatory Order Modifying License No. NPF-3 (EA-03-214), the inspectors verified that the licensee had submitted the required inspection plan for the year 2005 corrective action program independent assessment 90 days prior to the performance of the assessment, currently scheduled for July 11-22, 2005. The licensee submitted its plan in a letter to the NRC, dated April 12, 2005 (ML051030011). The inspectors reviewed the licensees letter describing the assessment plans and evaluated the scope and depth of the plans, including the credentials, experience, objectivity, and independence of the designated assessors.

b. Observations and Findings

The inspectors verified that the individuals designated to perform the assessment were independent from FENOC and that they had the credentials, experience, and objectivity necessary to accomplish the assessment. The inspectors determined that the assessment plan as described in the April 12, 2005, letter should provide a comprehensive review of the Davis-Besse corrective action program and its implementation.

.2 Review of Cycle 14 Operational Improvement Plan Commitments

As part of the licensees Return to Service Plan, the licensee developed a Cycle 14 Operational Improvement Plan. This plan was developed to focus on key improvement initiatives and safety barriers to ensure continued improvements and sustained performance in nuclear safety and plant operations. During this inspection period, the inspectors performed a basic review of the following Cycle 14 completed operational improvement plan initiatives:

C Implement Risk Management Process to Improve Station Knowledge and Awareness (Initiative 5.1.d);

C Provide Apparent Cause Training to Managers (Initiative 9.5);

  • Directors and Managers to Attend a Leadership Academy to Improve Management Skills (Initiative 1.3);
  • Provide Face-to-Face Communications Training to All Site Supervisors and Above (Initiative 1.7);
  • Monitor Safety Culture on a Monthly Basis (Initiative 7.1);
  • Provide Refresher Training on SCWE and Safety Culture to Davis-Besse Supervisors and Above (Initiative 7.5);
  • Perform an Effectiveness Assessment of the Corrective Actions Taken in Response to the November 2003 SCWE Survey Results (Initiative 7.8)

[Additional information on this initiative can be found in inspection report 05000346/2004015];

  • Supplement Management Oversight With Off-Site Assistance to Improve Objectivity and Ensure Assessments are Sufficiently Critical (Initiative 10.2);
  • Conduct an External Assessment to Evaluate the Progress of Organizational Improvements in the Areas of Critical Self-Assessments and Performance Observations (Initiative 10.5); and
  • Utilize INPO Assist Visits to Assess the Effectiveness of Improvement Initiatives (Initiative 10.6)

Overall the inspectors concluded that the referenced Operating Cycle 14 commitments had been adequately implemented.

.3 Evaluation of the Independent Safety Culture/Safety Conscious Work Environment

Assessment Report

a. Inspection Scope

As part of the inspection activities performed to verify the licensees compliance with the requirements for independent assessments, as described in the March 8, 2004, Confirmatory Order Modifying License No. NPF-3, the inspectors reviewed the Confirmatory Order Safety Culture/Safety Conscious Work Environment Assessment for the Davis-Besse Nuclear Power Station, dated February 4, 2005. The inspectors reviewed the report to ensure that the report provided an overall assessment of Safety Culture and Safety Conscious Work Environment, the assessment activities supported the reports conclusions, and the licensee documented specific action plans to address areas for improvement identified in the report.

In addition to the external assessment, the inspectors performed a detailed review of the following Cycle 14 completed Operational Improvement Plan initiatives regarding the area of safety culture and safety conscious work environment:

  • Assess Safety Culture Using the FENOC Guidance (Initiative 7.2)
  • Perform a Safety Culture Assessment Utilizing an Independent Outside Organization (Initiative 7.3)
  • NQA to Perform a Safety Culture Assessment in 2004 (Initiative 7.6(04))
  • Employee Concerns Program Group to Perform a Survey of the Safety Conscious Work Environment in 2004 (Initiative 7.7(04))

b. Observations and Findings

The independent assessment and associated action plan submitted by the licensee was consistent with the requirements of the Confirmatory Order. The inspection team found the assessment team members to be appropriately qualified, methodologies used were valid, and conclusions were consistent with other assessments conducted by the licensee.

The external assessment concluded that overall safety culture and safety conscious work environment had not significantly changed since the February 2003 independent assessment. The assessment and internal surveys revealed that a number of organizations exhibited a continuation of the negative trend from the March 2003 results.

The continued negative trend indicated that the licensees corrective actions have not been fully effective. The teams evaluation of the assessment results indicated that previous corrective actions have not always been aggressively and broadly implemented.

The assessment identified six areas for improvement and four cross cutting issues (not related to NRC cross-cutting issues), to be considered in developing the action plan. The areas for improvement were entered into the licensees Corrective Action Program (CAP) as condition report 04-07262 and broadly discussed in the action plan. The licensees list of corrective actions addressed all of the areas identified for improvement.

The licensee planned to assess SC and SCWE monitoring and assessment tools to identify opportunities to enhance their effectiveness. The inspection team will monitor the licensees efforts in assessing the SC and SCWE tools to ensure the tools can accurately reflect the status of SC and SCWE at the site and allow for effective comparisons and trending with previous results.

The licensee reported that the results of a survey conducted following its mid-cycle outage (January 17, 2005 through February 9, 2005) were fairly positive. The interviews conducted by the inspection team with senior managers indicated the same and provided some examples to illustrate improvements in the work environment. The inspection team did not interview any staff level individuals, therefore the team did not obtain independent information on plant staff views regarding the outage. Further, the inspection team did not evaluate the effectiveness of the licensees corrective actions because not all actions had been implemented and not enough time had passed for them to have had an effect. For example, part of the licensees action plan relies on the Teamwork-Ownership-Pride (TOP) Team to address all the areas for improvement.

However, the inspection team received mixed information on the TOP team and it was not evident that the TOP Team had a clear picture of its mission, responsibilities, or activities. The licensee indicated that the TOP Team charter was being revised and that members will receive training on SCWE. The NRC Inspection Team will assess the effectiveness of the actions assigned to the TOP team at a later date.

The licensee indicated it had received several comments from its staff regarding the lack of consistency in understanding the wording of questions on the survey instruments. The comments indicated that some questions appeared to have been interpreted differently by groups of individuals. For example, the term management appeared to be unclear.

Some individuals may have interpreted the word management to mean the upper echelon of corporate management for Davis-Besse and FENOC. Others may have interpreted the word management to mean their immediate shift supervisors and section management. Plant management is aware of the issues regarding misinterpretation of the questions on the survey instruments and plans to take this issue into consideration when assessing the results of subsequent surveys.

c. Conclusion Based on its review of the assessments and interviews with licensee management, the inspection team concluded that:

1) the external assessment and associated action plan were consistent with the Confirmatory Order; 2) the safety culture and safety conscious work environment at Davis-Besse continues to be acceptable for plant operation; 3) the external and internal SC/SCWE evaluations were reasonably consistent in their identification of areas for improvement at Davis-Besse; 4) the action plan contains appropriate actions to address the areas for improvement identified by the assessments; and 5) the licensees implementation of previous corrective actions, in the SC/SCWE arena, has not been sufficiently aggressive or broadly applied to ensure their effectiveness.

.4 Company Nuclear Review Board Meeting

The inspectors attended the meeting of the Davis-Besse Company Nuclear Review Board meeting which was held on April 7, 2005. The inspectors attended presentations given by the Chairmen for the following subcommittees; Operate the Plant/Training, Configuration Control/Equipment Reliability, Work Management, Loss Prevention, 10 CFR 50.59 Evaluation Review, and License Amendment Requests. The inspectors determined that the depth of evaluation and the material selected for review by each subcommittee was appropriate and that the Board was sufficiently challenging in their evaluation of the licensee.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. M. Bezilla, and other members of licensee management on May 19, 2005. The licensee acknowledged the findings presented. No proprietary information was identified.

.2 Interim Exit Meetings

Interim exit meetings were conducted for:

  • Independent Spent Fuel Storage Installation with the Dry Cask Project Manager, D. Dibert on April 13, 2005; and
  • Inspection of SC/SCWE Independent Assessment and review of several Cycle 14 initiatives with M. Bezilla, on April 14, 2005.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

B. Allen, Director, Plant Operation
J. Amidon, ECP Coordinator
M. Bezilla, Site Vice President
B. Boles, Manager, Plant Engineering
D. Dibert, Dry Cask Project Manager
J. Grabnar, Manager, Design Engineering
L. Harder, Manager, Radiation Protection
D. Haskins, Manager, Leadership & Organizational Development
R. Hovland, Manager, Technical Services
R. Hruby, Manager, Nuclear Oversight
G. Kendrick, Acting Manager, Site Maintenance
D. Kline, Manager, Security
S. Loehlein, Director, Station Engineering
P. McClosky, Manager, Site Chemistry & TOP Team Manager Sponsor
L. Myers, Chief Operating Officer, FENOC
D. Noble, Radiation Protection Supervisor
K. Ostrowski, Manager, Plant Operations
C. Price, Manager, Regulatory Compliance
R. Schrauder, Director, Performance Improvement
M. Trump, Manager, Training

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

None Attachment

LIST OF DOCUMENTS REVIEWED