IR 05000346/2022002

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Integrated Inspection Report 05000346/2022002
ML22221A255
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 08/11/2022
From: Eve E
NRC/RGN-III/DRP/B2
To: Tony Brown
Energy Harbor Nuclear Corp
References
IR 2022002
Download: ML22221A255 (29)


Text

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION - INTEGRATED INSPECTION REPORT 05000346/2022002

Dear Mr. Brown:

On June 30, 2022, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Davis-Besse Nuclear Power Station. On July 27, 2022, the NRC inspectors discussed the results of this inspection with you and other members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. One of these findings involved a violation of NRC requirements. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

A licensee-identified violation which was determined to be Severity Level IV is documented in this report. We are treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this inspection report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector at Davis-Besse Nuclear Power Station.

If you disagree with a cross-cutting aspect assignment or a finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region III; and the NRC Resident Inspector at Davis-Besse Nuclear Power Station.

August 11, 2022 This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Elise C. Eve, Acting Branch Chief Branch 2 Division of Reactor Projects Docket No. 05000346 License No. NPF-3

Enclosure:

As stated

Inspection Report

Docket Number:

05000346

License Number:

NPF-3

Report Number:

05000346/2022002

Enterprise Identifier:

I-2022-002-0043

Licensee:

Energy Harbor Nuclear Corp.

Facility:

Davis-Besse Nuclear Power Station

Location:

Oak Harbor, OH

Inspection Dates:

April 01, 2022 to June 30, 2022

Inspectors:

D. Mills, Senior Resident Inspector

K. Barclay, Reactor Inspector

R. Cassara, Resident Inspector

J. Cassidy, Senior Health Physicist

E. Fernandez, Reactor Inspector

M. Garza, Emergency Preparedness Inspector

T. Ospino, Resident Inspector

J. Reed, Health Physicist

Approved By:

Elise C. Eve, Acting Branch Chief

Branch 2

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Davis-Besse Nuclear Power Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A licensee-identified non-cited violation is documented in report section: 71114.0

List of Findings and Violations

Failure to Use Procedure during Loss of Letdown Event Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Event Green FIN 05000346/2022002-01 Open/Closed

[H.8] -

Procedure Adherence 71152A A self-revealed finding of very low safety significance (Green) was identified when the licensee failed to use procedures when responding to a loss of letdown. Specifically, the licensee failed to enter the annunciator response procedure, and isolated letdown with valve MU2B instead of valves MU6 and MU4 per procedure. The licensee also failed to utilize procedures while attempting to restore letdown during the initial response to the loss of letdown.

Failure to Provide Adequate Procedural Instructions when Swapping Purification Demineralizer Trains Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000346/2022002-02 Open/Closed

[H.2] - Field Presence 71152A A self-revealed finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Technical Specification (TS) 5.4.1(a) were identified for the licensees failure to establish and implement procedural guidance for performing a change of the on-service purification demineralizer. Specifically, the guidance in licensee procedure DB-OP-6006, "Makeup and Purification System," revision 53, for switching purification demineralizers did not provide instructions to ensure that the purification demineralizer being placed on-service was not manually isolated. This lack of procedural guidance resulted in control room operators inadvertently isolating letdown because they failed to un-isolate the manually closed outlet valve of purification demineralizer 1 prior to putting it on-service.

This resulted in high pressure in the letdown system, lifting of the relief valve MU-1890, and subsequent increase of pressurizer level to over 228 inches. This required the licensee to enter TS LCO 3.4.9 conditions A and B, resulting in a rapid reduction in power to roughly 15 percent.

Additional Tracking Items

Type Issue Number Title Report Section Status URI 05000346/2021050-06 Potential Adverse Changes During 2006 Emergency Diesel Generator Modifications 93812 Discussed

PLANT STATUS

The unit began the inspection period shut down for refueling outage. On April 18, the unit entered startup, and on April 21 the unit reached full power. On May 17, the unit was down powered to 64 percent to allow repair of a cracked small diameter instrument line on the secondary side. On May 19, the unit was returned to rated thermal power, and remained at or near rated thermal power for the remainder of the inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://ww.w.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance, and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Decay heat train 2 during the week ending April 30, 2022
(2) Containment spray train 1 during train 2 scheduled maintenance during the week ending June 30, 2022

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1) The inspectors evaluated system configurations during a complete walkdown of the control room emergency ventilation system through the week ending June 11, 2022.

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Containment closeout walkdown, fire areas D, AB, and A, during the week ending April 9, 2022
(2) Emergency core cooling system train 2 room 115, fire area A-04, during the week ending April 16, 2022
(3) Low voltage switchgear rooms E and F, fire areas X and Y, during the week ending May 7, 2022
(4) Radioactive waste exhaust equipment and main station exhaust fan room, fire area EE, during the week ending June 30, 2022

71111.08P - Inservice Inspection Activities (PWR) PWR Inservice Inspection Activities Sample (IP Section 03.01)

(1) The inspectors verified that the reactor coolant system boundary, steam generator tubes, reactor vessel internals, risk-significant piping system boundaries, and containment boundary are appropriately monitored for degradation, and that repairs and replacements were appropriately fabricated, examined and accepted by reviewing the following activities from March 7, 2022 to March 18, 2022:

03.01.a - Nondestructive Examination and Welding Activities

Ultrasonic examination (UT) of cold leg inlet nozzle to pipe weld, component ID RC-MK-B-59-1-FW-113B

Ultrasonic examination (UT) of hot leg outlet nozzle to shell weld, component ID RC-RPV-WR-13/14/72-Z

Liquid penetrant (PT) examination of fillet weld on RCTC CLNT 1-2-1 seal return line component ID DB-FTMU60A

Liquid penetrant (PT) examination of fillet weld on RCTC CLNT 1-2-1 seal return line component ID DB-FTMU60B

Visual examination (VT) of reactor vessel interior keyways

Visual examination (VT) of control rod guide tubes per MRP-227

Welding of 2 to 1 fillet weld on RCTC CLNT 1-2-1 seal return line component ID DB-FTMU60B (WO 200747521)03.01.b - Pressurized-Water Reactor Vessel Upper Head Penetration Examination Activities

Visual examinations of 69 penetrations on the reactor vessel closure head 03.01.c - Pressurized-Water Reactor Boric Acid Corrosion Control Activities

Condition Report (CR)-2020-05467 containment spray pump 1 pipe cap at CS32

CR-2021-07323 BWST SFAS channel 2 level transmitter

CR-2021-07401 decay heat pump casing vent

CR-2021-02688 makeup pump 2 outlet isolation 03.01.d - Pressurized-Water Reactor Steam Generator Tube Examination Activities

Eddy current (ET) testing of 15502 steam generator tubes in SG 2A

Eddy current (ET) testing of 15538 steam generator tubes in SG 1B

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated licensed operator performance in the control room during power ascension, including syncing main generator to grid, delta cold leg temperature adjustments, and starting of second main feed pump during the week ending April 23, 2022.

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (3 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Replacement of station battery 2 during the week ending March 12, 2022
(2) Decay heat pump 2 bearing and oil seal replacement due to oil leak during the week ending April 16, 2022 (3)10-year overhaul of the YVB inverter static transfer switch channel 'B' during the week ending May 7, 2022

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Reactor power reduction and emergent work related to instrument line steam leak repairs from May 17 - 19, 2022

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (4 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the following operability determinations and functionality assessments:

(1) Main steam isolation valve 2 inoperable due to scaffold pole in path of MS100, CR 2022-01484, during the week ending April 9, 2022
(2) Decay heat pump 2 pump outboard constant level oiler empty, CR 2022-02550, during the week ending April 16, 2022
(3) Decay heat pump 1 inboard/outboard bearings constant level oilers were found empty, CR 2022-03669, during the week ending April 30, 2022
(4) RCP 1-2 seal leak / lower differential pressure, CR 2022-03463, and CR 2022-03482, during the week ending June 30, 2022

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the following post-maintenance testing activities to verify system operability and/or functionality:

(1) Containment air cooler 2 outlet temperature control valve SW1357 during the week ending May 14, 2022

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage 1R22 activities from March 4, 2022 through April 19, 2022

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance testing activities to verify system operability and/or functionality:

Surveillance Tests (other) (IP Section 03.01) (5 Samples)

(1) Steam feed rupture control system channel 2 integrated testing during the week ending April 9, 2022
(2) Physics testing during power ascension during the week ending April 23, 2022
(3) Emergency diesel generator 1 monthly test during the week ending April 30, 2022
(4) Steam feed rupture control system channel 1 differential pressure inputs surveillance on May 16, 2022
(5) Low pressure injection quarterly test during the week ending June 11, 2022

FLEX Testing (IP Section 03.02) (1 Sample)

(1) Annual run of FX-P1A alternate low pressure flex emergency feed water pump and FX-P2A flex emergency feed water storage tank replenishment and spent fuel pool spray N+1 pump during the week ending 30 June, 2022

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1) The inspectors evaluated the following maintenance and testing of the alert and notification system:

2020 annual siren preventive maintenance (PM) results

2021 annual siren PM results

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1) The inspectors evaluated the readiness of the emergency preparedness organization

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1) The inspectors evaluated the maintenance of the emergency preparedness program

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1) Integrated drill on May 24,

RADIATION SAFETY

71124.05 - Radiation Monitoring Instrumentation

Walkdowns and Observations (IP Section 03.01) (8 Samples)

The inspectors evaluated the following radiation detection instrumentation during plant walkdowns:

(1) ARGOS-5 number Li 2.12.112 at the main exit of the radiologically controlled area
(2) SAM-11 number Li 2.12.54 at the main exit of the radiologically controlled area
(3) GEM-5 number Li 2.12.115 at the main exit of the radiologically controlled area
(4) AMP-100 number Li 2.7.502 in the calibration facility
(5) Chronos-4 number Li 2.12.113 in the rad waste truck bay
(6) Telepole Li.2.7.337 ready for issuance in radiation protection counting room
(7) Area radiation monitor RE-8426 in the fuel handling building
(8) Area radiation monitor RE-1998 in the auxiliary building

Calibration and Testing Program (IP Section 03.02) (13 Samples)

The inspectors evaluated the calibration and testing of the following radiation detection instruments:

(1) ARGOS 5-AB number Li 2.12.112
(2) GEM-5 number Li 2.12.115
(3) SAM-11 number Li 2.12.54
(4) FUJI neutron detector number Li 2.7.682
(5) AMP-100 number Li 2.7.502
(6) Chronos-4 number Li 2.12.113
(7) Whole body counter number Li 2.12.42
(8) TopTrak air flow calibration standard number 65775
(9) Benchtop counter model L-177 number Li 2.7.545
(10) Benchtop counter model L-177 number Li 2.7.558
(11) Failed fuel monitor number RE-1998
(12) Control room normal air supply monitor number RE-4597
(13) Containment air normal monitor number RE-4597 Effluent Monitoring Calibration and Testing Program Sample (IP Sample 03.03) (2 Samples)

The inspectors evaluated the calibration and maintenance of the following radioactive effluent monitoring and measurement instrumentation:

(1) Batch tank liquid effluent monitor, RE-1878A
(2) Station vent accident range noble gas monitor, RE-4598AB

OTHER ACTIVITIES - BASELINE

===71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (DEP) Sample (IP Section 02.12)===

(1) January 1, 2021 through March 31, 2022 EP02: Emergency Response Organization (ERO) Drill Participation (IP Section 02.13) (1 Sample)
(1) January 1, 2021 through March 31, 2022 EP03: Alert And Notification System (ANS) Reliability Sample (IP Section 02.14) (1 Sample)
(1) January 1, 2021 through March 31, 2022

71152A - Annual Follow-Up Problem Identification and Resolution Annual Follow-Up of Selected Issues (Section 03.03)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) February 5, 2022, forced downpower due to loss of letdown

71153 - Follow-Up of Events and Notices of Enforcement Discretion Event Follow-Up (IP Section 03.01)

(1) The inspectors evaluated forced downpower and licensees response on February 5,

INSPECTION RESULTS

Licensee-Identified Non-Cited Violation 71114.02 This violation of very low safety significance was identified by the licensee and has been entered into the licensee corrective action program and is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

Violation:

On July 19, 2020, Ottawa County, Ohio notified the licensee that a single emergency siren sounded spuriously. On July 20, 2020, the licensee notified the Ottawa County Dispatch that the affected siren was out of service for repair. Title 10 CFR 50.72(b)(2)(xi) requires the licensee to report within four hours, any event related to the health and safety of the public for which notification to other government agencies has been made. Initially on July 19, the licensee concluded that the siren actuation was not reportable because less than 25 percent of the local population was affected. On July 20, the licensee reviewed the circumstances surrounding the siren, and concluded that 10 CFR 50.72(b)(2)(xi) applied and a four-hour report should have been made. NUREG-1022 includes as an example that an emergency notification is needed if county governments are informed of an actuation by concerned members of the public. The licensee made the notification at 1636 on July 20, 2020. The inspectors concluded that the failure to make the required four-hour notification in timely fashion was a performance deficiency. Because the violation impacted the regulatory process, in that the licensee failed to make a required report on time, the inspectors assessed the performance deficiency using traditional enforcement. The licensee entered the condition into the corrective action process as Condition Report 2020-05859. Corrective actions included clarifications to licensee procedures to prevent similar occurrences.

Significance/Severity: Severity Level IV. The inspectors concluded that the finding was a Severity Level IV violation in accordance with the Enforcement Policy, which includes a failure to make a report required by 10 CFR 50.72 as an example of a SL IV violation.

Because the licensee self-identified the condition, entered the condition in the corrective action program, and took action to address the causes, the inspectors concluded that the issue could be addressed as a licensee-identified non-cited violation.

Corrective Action References: CR 2020-05859 Failure to Use Procedure during Loss of Letdown Event Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Event Green FIN 05000346/2022002-01 Open/Closed

[H.8] -

Procedure Adherence 71152A A self-revealed finding of very low safety significance (Green) was identified when the licensee failed to use procedures when responding to a loss of letdown. Specifically, the licensee failed to enter the annunciator response procedure and isolated letdown with valve MU2B instead of valves MU6 and MU4 per procedure. The licensee also failed to utilize procedures while attempting to restore letdown during the initial response to the loss of letdown.

Description:

On February 5, 2022, a switching of on-service purification demineralizers was performed.

During operator performance of this evolution, letdown was inadvertently isolated. Letdown pressure raised above 150psig, sounding annunciator alarm 2-2-A, "Letdown Pressure High,"

and letdown system pressure relief valve MU-1890 lifted. The annunciator response procedure corresponding to annunciator 2-2-A, "Letdown Pressure High," was not entered.

Entering the correct annunciator response procedure is required by NOP-OP-1002 "Conduct of Operations" revision 16. The annunciator response procedure, DB-OP-02002, 2-2-A, step 3.1 states, verify MU-4, pressure reducing valve closed, and step 3.2 states verify MU-6 letdown flow control valve closed. Operators did not reference a procedure but instead used their system knowledge and isolated letdown by closing letdown isolation valve MU-2B.

Operators attempted to restore letdown by closing MU10A (1 purification demineralizer inlet),opening MU10B (2 purification demineralizer inlet), and then opened MU-2B. Makeup system pressure increased to 145psig, and indications of rising reactor coolant drain tank (RCDT)level again caused operators to isolate letdown with MU2B again. Operators then entered abnormal procedure DB-OP-02512 Makeup and Purification System Malfunctions, section 4.3 Loss of letdown flow path." Following the loss of letdown, the level in the pressurizer increased. When pressurizer level reached 228 inches, operators entered LCO 3.4.9 condition A restore level to within limit within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. Operators attempted to restore letdown again by opening MU104 purification demineralizer bypass and closing MU10B before opening MU2A and slowly raising letdown flow through MU6. Operators correctly diagnosed that letdown relief valve MU1890 failed to reseat based on indications of increasing RCDT level, and operators isolated letdown by closing MU6 and MU4. Operators again attempted to restore letdown through MU104 to allow mechanical agitation of MU1890 to seat the relief valve, but continuing indications of increasing RCDT level indicated MU1890 did not reseat.

Operators then entered DB-OP-02504, "Rapid Shutdown," and commenced a power reduction at 10 percent per minute. Operators did not restore pressurizer level to within limit and entered LCO 3.4.9. condition B be in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and be in mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Letdown was isolated by closing MU4 and MU6, and MU1890 was manually cycled and reseated. Letdown was then restored with a stable level in the RCDT. Pressurizer level was restored to within limits and LCO 3.4.9 was exited with reactor power at approximately 15 percent.

Corrective Actions: Corrective actions included the removal of operators from duty for training remediation including simulator training specific to alarm response and procedural adherence, revisions to operating procedures, and improved control board markings.

Corrective Action References: CR 2022-00879, Abnormal procedure entries for loss of letdown flow path

Performance Assessment:

Performance Deficiency: The inspectors reviewed this finding using the guidance contained in IMC 0612, "Issue Screening," Appendix B, "Issue Screening Directions," dated July 23, 2021.

The inspectors determined that the licensees failure to use procedures during the initial response to the loss of letdown constituted a performance deficiency that was reasonably within the licensees ability to foresee and correct and should have been prevented.

Specifically, the licensee failed to enter the annunciator response procedure for letdown pressure high requiring isolation with valve MU6 and valve MU4 but operators isolated letdown with valve MU2B by memory without procedural guidance.

Screening: The performance deficiency was more than minor in accordance with IMC 0612, "Issue Screening," Appendix B, "Issue Screening Directions," dated July 23, 2021, because, if left uncorrected the performance deficiency had the potential to lead to a more significant safety concern. Specifically, by not performing activities affecting quality in accordance with a procedure, the operators could improperly manipulate plant equipment and challenge plant safety by causing unexpected transients or impact safety-related equipment.

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding to be of very low safety significance (Green) since it did not cause a reactor trip and the loss of mitigation equipment relied upon to transition the plant from the onset of the trip to a stable shutdown condition.

Cross-Cutting Aspect: H.8 - Procedure Adherence: Individuals follow processes, procedures, and work instructions. Specifically, the licensee failed to enter the annunciator response procedure for letdown pressure high during the initial response to loss of letdown.

Enforcement:

Inspectors did not identify a violation of regulatory requirements associated with this finding.

Failure to Provide Adequate Procedural Instructions when Swapping Purification Demineralizer Trains Cornerstone Significance Cross-Cutting Aspect Report Section Initiating Events Green NCV 05000346/2022002-02 Open/Closed

[H.2] - Field Presence 71152A A self-revealed finding of very low safety significance (Green) and an associated non-cited violation (NCV) of Technical Specification (TS) 5.4.1(a) were identified for the licensees failure to establish and implement procedural guidance for performing a change of the on-service purification demineralizer. Specifically, the guidance in licensee procedure DB-OP-6006, "Makeup and Purification System," revision 53, for switching purification demineralizers did not provide instructions to ensure that the purification demineralizer being placed on-service was not manually isolated. This lack of procedural guidance resulted in control room operators inadvertently isolating letdown because they failed to un-isolate the manually closed outlet valve of purification demineralizer 1 prior to putting it on-service. This resulted in high pressure in the letdown system, lifting of the relief valve MU-1890, and subsequent increase of pressurizer level to over 228 inches. This required the licensee to enter TS LCO 3.4.9 conditions A and B, resulting in a rapid reduction in power to roughly 15 percent.

Description:

On February 5, 2022, a switching of on-service purification demineralizers was performed. A turnover for the command senior reactor operator and the balance of plant reactor operator was conducted so they could participate in a concurrent fire brigade drill. A pre-job brief for swapping to purification demineralizer 1 was conducted in the control room. The brief did not include a discussion of the caution tagged purification demineralizer outlet isolation valve MU139 that was closed due to leak-by of purification demineralizer 1 inlet isolation valve MU10A. A pre-job brief form was not used as required by procedure. The demineralizer swap was performed per DB-OP-6006, "Makeup and Purification System," revision 53.

DB-OP-6006 does not have a step to address the plant conditions encountered, namely that MU139 purification demineralizer 1 outlet had been manually isolated for an extended period due to leak-by of purification demineralizer 1 inlet, MU10A. The procedure does have such a step applying to purification demineralizer 3 outlet, for similar leak-by conditions. Operators inadvertently isolated letdown when taking purification demineralizer 2 off service because the purification demineralizer 1 lineup was not complete due to MU139 being closed. Letdown pressure increased above 150 psig, resulting in annunciator alarm 2-2-A, "letdown pressure high." Operators attempted to restore letdown but were unsuccessful. Following the loss of letdown, the level in the pressurizer rose. When pressurizer level reached 228 inches, the operators appropriately entered LCO 3.4.9 condition A restore level to within limit within one hour. Operators did not restore pressurizer level to within limit and entered LCO 3.4.9 condition B, be in mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and be in mode 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Operators entered DB-OP-02504, "Rapid Shutdown," and commenced a power reduction at 10 percent per minute. During the rapid shutdown, letdown was reestablished, and pressurizer level was restored to within limits, allowing operators to exit LCO 3.4.9 conditions A and B. Reactor power was reduced to approximately 15 percent before the restoration of letdown and proper pressurizer level.

Corrective Actions: Corrective actions included the removal of operators from duty for training remediation, issuance of standing order 22-001 for crew engagement in briefs and observations of evolutions, revision of the system procedure (DB-OP-6006, "Makeup and Purification System," revision 55) to address manipulation of each purification demineralizer outlet valve as required if there is known leak-by of the inlet valve, control room crew reorganization and assessment, and senior crew mentor implementation.

Corrective Action References: CR 2022-00879, "Abnormal procedure entries for loss of letdown flow path"

Performance Assessment:

Performance Deficiency: The inspectors reviewed this finding using the guidance contained in IMC 0612, "Issue Screening," Appendix B, "Issue Screening Directions," dated July 23, 2021.

The inspectors determined that the licensees failure to provide adequate procedural instructions to plant operators for performing a change of the on-service purification demineralizer constituted a performance deficiency that was reasonably within the licensees ability to foresee and correct and should have been prevented. Specifically, the licensee failed to provide procedural instructions to open purification demineralizer 1 outlet, MU 139, if it had been isolated due to leak-by of the purification demineralizer 1 inlet, MU 10A. However, the procedure has a step for purification demineralizer 3.

Screening: The inspectors determined the performance deficiency was more than minor in accordance with IMC 0612, "Issue Screening," Appendix B, "Issue Screening Directions,"

dated July 23, 2021, because it was associated with the configuration control (or human performance) attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. This issue is similar to example 4.b from IMC 0612 Appendix E, "Examples of Minor Issues."

Significance: The inspectors assessed the significance of the finding using IMC 0609 Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The inspectors determined the finding had resulted in a transient initiator for the Initiating Events cornerstone and using, "Exhibit 1 - Initiating Events Screening Questions," determined that the finding was of very low safety significance (Green). Specifically, because the finding did result in a turbine trip, and not a reactor trip, the finding screened directly to Green without the need for a detailed risk evaluation.

Cross-Cutting Aspect: H.2 - Field Presence: Leaders are commonly seen in the work areas of the plant observing, coaching, and reinforcing standards and expectations. Deviations from standards and expectations are corrected promptly. Senior managers ensure supervisory and management oversight of work activities, including contractors and supplemental personnel.

Specifically:

A procedural change order was in progress to address procedural inadequacies in DB-OP-6006 but was not yet implemented at the time of the event.

The reactivity manipulation pre-job brief that occurred in the control room prior to the evolution did not accurately review the activity, or potential consequences, and supervision did not identify or correct the deviation from the standards and expectations.

Concurrent fire drill and relief turnover distractions occurred that impacted the brief, peer checks, and supervisory oversight of the reactivity manipulation for changing purification demineralizers with no intervention of supervision to mitigate the distractions.

Enforcement:

Violation: Technical Specification Section 5.4.1.a requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. NRC Regulatory Guide 1.33, Revision 2, Appendix A, Section 3 addresses Procedures for Startup, Operation, and Shutdown of Safety-Related PWR Systems, Instructions for energizing, filling, venting, draining, startup, shutdown, and changing modes of operation should be prepared, as appropriate, for the following systems, Section 3.n, addresses Chemical and Volume Control System (including Letdown/Purification System). The licensee established procedure DB-OP-6006, Makeup and Purification System, revision 53, to provide instructions for operating the makeup and purification system.

Contrary to the above, between September 2, 2020 and February 7, 2022, the licensee failed to maintain a written procedure for the chemical and volume control system (including letdown/purification system). Specifically, the licensee failed to maintain procedure DB-OP-6006, Makeup and Purification System, such that it accurately directed operations personnel to un-isolate purification demineralizer 1 if it was manually isolated by MU-139 outlet for purification demineralizer 1.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy.

URI (Discussed)

Potential Adverse Changes During 2006 Emergency Diesel Generator Modifications URI 05000346/2021050-06 93812

Description:

The NRC continues to evaluate an unresolved item documented in inspection report 2021050-06 (ADAMS Accession Number ML21348A767). Generally, the staff is assessing the adequacy of the sites modification associated with the installation of the emergency diesel generator field flash selector switches.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On July 27, 2022, the inspectors presented the integrated inspection results to Mr. T. Brown, Site Vice President, and other members of the licensee staff.

On March 18, 2022, the inspectors presented the ISI Exit Meeting inspection results to Mr. T. Brown, Site Vice President, and other members of the licensee staff.

On May 16, 2022, the inspectors presented the radiation protection baseline inspection results to Mr. T. Brown, Site Vice President, and other members of the licensee staff.

On July 1, 2022, the inspectors presented the emergency preparedness program inspection results to Mr. T. Brown, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.04

Corrective Action

Documents

22-03619

BACC: Boric Acid Leak from DH154 Pipe Cap

04/26/2022

71111.04

Corrective Action

Documents

22-03714

Maintenance Rule Reviews for CREVS System

04/29/2022

71111.04

Corrective Action

Documents

22-03879

CREVS Refrigerant Line Insulation and Support Degradation

05/05/2022

71111.04

Procedures

DB-OP-06012

Decay Heat and Low-Pressure Injection System Operating

Procedure

71111.04

Procedures

DB-OP-06013

Containment Spray System

71111.04

Procedures

DB-OP-06505

Control Room Emergency Ventilation System Procedure

71111.05

Fire Plans

PFP-AB-115

ECCS Pump Room 1-2, Rooms 115, Fire Area A-04

71111.05

Fire Plans

PFP-AB-428

Low Voltage Switchgear Room F - Bus, Room 428,

Fire Area X

71111.05

Fire Plans

PFP-AB-429

Low Voltage Switchgear Room E - Bus, Room 429,

Fire Area Y

71111.05

Fire Plans

PFP-AB-500

Radwaste and Fuel Handling Areas Air Supply Equipment

Area, Room 500, Fire Area EE

71111.05

Fire Plans

PFP-AB-501

Radwaste Exhaust Equipment and Main Station Exhaust Fan

Room, Rooms 501 and 501DC, Fire Area EE

71111.05

Fire Plans

PFP-AB-515

Purge Exhaust Equipment Room, Room 515, Fire Area EE

71111.05

Fire Plans

PFP-CB-214

Core Flooding Tank Area, Room 214, Fire Area D

71111.05

Fire Plans

PFP-CB-215

Let Down Coolers Area, Room 215, Fire Area D

71111.05

Fire Plans

PFP-CB-216

Steam Generator West D Ring Area, Room 216, Fire Area D

71111.05

Fire Plans

PFP-CB-218

Steam Generator East D Ring Area, Room 218, Fire Area D

71111.05

Fire Plans

PFP-CB-317

Containment Air Cooler Area, Room 317 and 317A,

Fire Area D

71111.05

Fire Plans

PFP-CB-410

East Elevation 603' and Valve Room Elevation 636', Rooms

410 and 508, Fire Area D

71111.05

Fire Plans

PFP-CB-A208

Southwest Penetration Area of Annulus Space Elevations

585' and 603', Partial Room 127W, Fire Area AB

71111.05

Fire Plans

PFP-CB-A236H

East and Southwest Penetration Areas at Elevations 585'

and 603', Partial Rooms 127W and 127W, Fire Area A and

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

AB

71111.05

Fire Plans

PFP-CB-A236L

East Penetration Area of Annulus Space Elevations 585' and

603', Partial Room 127E, Fire Area A

71111.05

Fire Plans

PFP-CB-EL565

North Area 565' Elevation, Rooms 213, 217 and Normal

Sump Area, Fire Area D

71111.05

Fire Plans

PFP-CB-EL603

Fuel Transfer Pool and North and West 603' Elevation,

Rooms 219, 407 and 410A, Fire Area D

71111.08P

Corrective Action

Documents

22-02047

Foreign Material Found During Control Rod Guide Tube

MRP-227-A Exam

04/08/2022

71111.08P

Engineering

Evaluations

INR-DB1R22-001

Reactor Vessel - RPV Interior - Keys Examination

03/14/2022

71111.08P

Procedures

54-IISI-400-024

Multi-Frequency Eddy Current Examination of Tubing

2/07/2020

71111.08P

Procedures

54-ISI-808-000

Automated Phased Array Ultrasonic Examination of PPWR

Vessel Shell Welds

03/24/2020

71111.08P

Procedures

54-ISI-809-000

Automated Phased Array Ultrasonic Examination of PWR

Vessel Nozzle to Shell Welds from Nozzle Bore

03/24/2020

71111.08P

Procedures

NA-QC-00191

Liquid Penetrant Examination

71111.08P

Procedures

NOP-CC-5763

Appendix VIII Procedure for Ultrasonic Examination of

Austenitic Pipe Welds

71111.08P

Procedures

NOP-CC-5765

Appendix VIII Procedure for Straight Beam Ultrasonic

Examination of Bolts and Studs

71111.08P

Procedures

NOP-ET-2001

Boric Acid Corrosion Control Program

71111.08P

Procedures

WPS A8-2-1

Gas Tungsten (GTAW) of Stainless Steel (P8), Groove with

or Without Backing

71111.12

Corrective Action

Documents

2015-15566

Document NA of Step in DB-ME-09205 During YVA PM

11/15/2015

71111.12

Corrective Action

Documents

22-03731

Decay Heat Pump Problem Solving

04/29/2022

71111.12

Corrective Action

Documents

22-03860

X2 Replacement Board for YVB Found Bad

05/05/2022

71111.12

Corrective Action

Documents

22-03869

Document NA of Step in DB-ME-09205 During YVB PM

05/05/2022

71111.12

Corrective Action

Documents

22-04131

P42-2, 2 Decay Heat Oil Pump 2, Pump O/B Bearing Level

Low

05/15/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.12

Corrective Action

Documents

22-04174

Turbine Building Ventilation Concerns

05/17/2022

71111.12

Corrective Action

Documents

22-04175

Annunciator 5-1-B Delayed During SFAS CH 1 Monthly

Functional

05/17/2022

71111.12

Corrective Action

Documents

22-04452

YVB Normal Operations Light is Out

05/26/2022

71111.12

Corrective Action

Documents

22-04722

DH Pump 2 Pump O/B Oil Leak

06/09/2022

71111.12

Miscellaneous

80-9230400-90 Oscillator Board Technical Description

71111.12

Procedures

DB-ME-09202

Maintenance of Essential SC1 UPS

71111.12

Procedures

DB-ME-09205

Maintenance of Inverters YVA and YVB

71111.13

Corrective Action

Documents

22 -04032

Main Feed Pump 2 Recirculation Valve FW438 Packing Leak 05/12/2022

71111.13

Drawings

OS-012A SH 1

Main Feedwater System

71111.13

Miscellaneous

IR22 Shutdown Defense In-Depth Report

71111.13

Procedures

NOP-OP-1007

Risk Management

71111.15

Corrective Action

Documents

20-01652

1R21 BACC: Boric Acid Crystals and Oil Underneath West

Fuel Transfer Tube Flange

03/01/2020

71111.15

Corrective Action

Documents

20-01664

1R21 BACC: Fuel Transfer Tube 1-2 Flange

03/02/2020

71111.15

Corrective Action

Documents

22-03169

1R22 BACC: Active Leak in Refueling Canal/ Deep End

04/11/2022

71111.15

Corrective Action

Documents

22-03435

Main Feed Pump 2 Recirculation Valve FW438 Packing Leak

05/19/2022

71111.15

Corrective Action

Documents

22-03566

Minor Cooling Water Leak on Decay Heat Pump 2

04/24/2022

71111.15

Corrective Action

Documents

22-03570

AFPT 1 Steam Admission Valve Leak-By

04/24/2022

71111.15

Corrective Action

Documents

22-03614

Periodic Verification Testing of MS106, MS107 and MS107A

Missed Frequency

04/26/2022

71111.15

Corrective Action

Documents

22-03669

Decay Heat Pump 1 IB/OB Bearings Constant Level Oilers

Were Found Empty

04/28/2022

71111.15

Corrective Action

Documents

22-03704

RCP 1-2 Motor Lower Bearing High Oil Level Alarm

04/29/2022

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.15

Corrective Action

Documents

22-03879

CREVS Refrigerant Line Insulation and Support Degradation

05/05/2022

71111.15

Corrective Action

Documents

22-04128

RCP 1-2 Seal Leakage Increased Following CAC Swap/CAC

Monthly Testing

05/15/2022

71111.15

Corrective Action

Documents

22-04380

RCP 2-2 Seal Return TIRC17A2 Failed to Mid-Scale

(Approx. 214 F)

05/24/2022

71111.15

Corrective Action

Documents

22-04523

Reactor Coolant Pump 1-2 Leakage Missed 1R22 Learning

Opportunity

05/31/2022

71111.15

Corrective Action

Documents

22-04535

Main Steam Line 1 MS131 Leaks by the Closed Seat

06/01/2022

71111.15

Corrective Action

Documents

22-04574

Found CCW Train 1 Ventilation Damper Open with Fan Off

06/01/2022

71111.15

Corrective Action

Documents

22-04651

Component Cooling Water Pump 1 Outboard Bearing Oil

Leak

06/06/2022

71111.15

Corrective Action

Documents

22-04668

Potentiometer Dead Spots Found While Cycling SBODG

MOC

06/07/2022

71111.15

Corrective Action

Documents

22-04688

SBODG Overfilled with Lube Oil

06/07/2022

71111.15

Corrective Action

Documents

22-04691

DH Pump 2 Outboard Bearing Oil Leak

06/07/2022

71111.15

Corrective Action

Documents

22-04695

Foreign Material Identified in New Hoses for Replacement on

SBODG

06/08/2022

71111.15

Corrective Action

Documents

22-04722

DH Pump 2 Pump O/B Oil Leak

06/09/2022

71111.15

Corrective Action

Documents

22-04759

Potential FME Falling into Cooling Tower Basin

06/09/2022

71111.15

Corrective Action

Documents

22-04788

Station Blackout Diesel Generator Water Jacket Specific

Gravity High Out of Specification

06/10/2022

71111.15

Corrective Action

Documents

22-04789

Unexpected Alarm Received for Control Valve 4 Output

Current Voting Mismatch

06/10/2022

71111.15

Corrective Action

Documents

22-04807

Entered DB-OP-02515 Reactor Coolant Pump And Motor

Abnormal Operation Due to RCP 1-2 Third Stage Seal

Pressure Lowering and Bringing in Computer Point P814

06/12/2022

71111.15

Miscellaneous

ODMI 22-02

Operation with Reactor Coolant Pump 1-2 Indications of

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Degraded Seal Performance

71111.19

Corrective Action

Documents

22-03912

Service Water SW1357 Failed to Stroke Open

05/07/2022

71111.19

Corrective Action

Documents

22-04063

SW1357 Open Stroke Time Exceeded Maximum Time

05/13/2022

71111.19

Corrective Action

Documents

22-04101

Service Water SW1357 Nitrogen Supply Box Shield has

Stripped, Broken Fasteners

05/13/2022

71111.19

Procedures

DB-PF-03027

Service Water Train 2 Valve Test

71111.20

Procedures

DB-MI-05253

Nuclear Instrumentation NI 06 (RPS Channel 1) Power

Range Adjustment

71111.20

Procedures

DB-MI-05254

Nuclear Instrumentation NI 05 (RPS Channel 2) Power

Range Adjustment

71111.20

Procedures

DB-MI-05255

Nuclear Instrumentation NI 08 (RPS Channel 3) Power

Range Adjustment

71111.20

Procedures

DB-MI-05256

Nuclear Instrumentation NI 07 (RPS Channel 4) Power

Range Adjustment

71111.20

Procedures

DB-NE-03212

Zero Power Physics Testing

71111.22

Corrective Action

Documents

22-04169

PDS-2686B Preconditioned During Performance of

DB-MI-03203

05/16/2022

71111.22

Corrective Action

Documents

22-04169

PDS-2686B Preconditioned During Performance of

DB-MI-03203

05/16/2022

71111.22

Procedures

DB-MI-03203

Channel Functional Test and Calibration of SFRCS Actuation

Channel 1, Steam Generator Differential Pressure Inputs

PDS-2686A, PDS-2686B, PDS-2685C AND PDS-2685D

71111.22

Procedures

DB-PF-03001

Main Steam Safety Valve Setpoint Test

71111.22

Work Orders

200821891

RT 11915 DB-FX-P1A Operational Inspection

05/04/2020

71111.22

Work Orders

200821891

RT 11915 DB-FX-P1A Operational Inspection

05/04/2020

71111.22

Work Orders

200822483

SFRCS Channel 2 Integrated Test

03/06/2022

71111.22

Work Orders

200825784

Decay Heat Train 2 Pump and Valve Test (Mode 1-3)

06/06/2022

71111.22

Work Orders

200842476

MI3203-001 08.000 CH1 SFRCS ACH1

05/16/2022

71111.22

Work Orders

200842476

MI3203-001 08.000 Channel 1 SFRCS ACH1

05/16/2022

71111.22

Work Orders

200860045

PM 5554 SP17A1 Test MSSVs

2/27/2022

71114.02

Corrective Action

Documents

20-03003

Communication Failure on Siren 803 and Battery Failures on

Sirens 402&507

04/08/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71114.02

Corrective Action

Documents

20-05101

Siren Computer Remote Access Phone Lines Issues

06/16/2020

71114.02

Corrective Action

Documents

20-05859

Late 10 CFR 50.72 Notification of Siren Activation

08/20/2020

71114.02

Corrective Action

Documents

20-06246

DB Sirens 309 and 504 Reported False Failures

09/04/2020

71114.02

Corrective Action

Documents

21-00752

DB EPZ Sirens Indicated Chopper Motor Current Fail After

the 02/05/2021 One Minute Audible Siren

2/05/2021

71114.02

Corrective Action

Documents

21-03470

Trending of Alert and Notification System (Sirens)

04/29/2021

71114.02

Corrective Action

Documents

21-04458

Trending of Alert and Notification System Sirens - Siren 504

06/04/2021

71114.02

Corrective Action

Documents

22-04213

DB Siren 2 Failure

05/18/2022

71114.03

Corrective Action

Documents

20-06204

Missed ERO 3rd Quarter Tabletop Drill

07/30/2020

71114.03

Corrective Action

Documents

20-06317

On Duty ERO Member Did Not Respond Appropriately

08/10/2020

71114.03

Corrective Action

Documents

21-03367

Emergency Response Organization Not Notified When

Individual Assigned to On-Call Position Went on Short Term

Leave

04/27/2021

71114.03

Corrective Action

Documents

21-03667

CANS Weekly Test Phone Call Issue

05/05/2021

71114.03

Corrective Action

Documents

21-03929

Individual Did Not Complete All Required Requalification

Training to Support SCBA Quals

05/13/2021

71114.03

Corrective Action

Documents

21-04224

Strategic Engineer Call-Tree Individual Did Not Respond to

Augmented Call-In Drill in a Timely Manner

05/25/2021

71114.03

Corrective Action

Documents

21-04233

RP Call-Tree Individual Did Not Respond to the Augmented

Call-In Drill in a Timely Manner

05/25/2021

71114.03

Corrective Action

Documents

21-04271

Chemistry Call-Tree Individual Failed to Respond to

Augmented Call-In Drill

05/26/2021

71114.03

Corrective Action

Documents

21-06935

Ops Advisor Call-Tree Position Individual Did Not Respond

to the ERO Call-In Drill

09/15/2021

71114.03

Corrective Action

21-09314

ERO Call-Tree Position Individual Did Not Respond to CANS

2/08/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Documents

Call-In Drill

71114.03

Corrective Action

Documents

22-01665

Effective Review for ERO Call-In Response Did Not Meet

Success Metrics

03/03/2022

71114.03

Corrective Action

Documents

ATA-2021-13077

4th Quarter 2021 Unannounced Call-In Drill

10/14/2021

71114.03

Miscellaneous

ATA-2020-12191

3rd Quarter 2020 Unannounced Call-In Drill

11/06/2020

71114.03

Miscellaneous

ATA-2020-15528

4th Quarter 2020 Unannounced Call-In Drill

2/19/2020

71114.03

Miscellaneous

ATA-2021-13075

2nd Quarter 2021 Unannounced Call-In Drill

04/12/2021

71114.03

Miscellaneous

ATA-2021-13076

3rd Quarter 2021 Unannounced Call-In Drill

07/01/2021

71114.03

Miscellaneous

ATA-2021-4521

1st Quarter 2021 Unannounced Call-In Drill

03/26/2021

71114.05

Corrective Action

Documents

21-01242

EP Drill: Drill Objective C.7 Not Met Due to Failing to

Communicate Entire PAR

2/24/2021

71114.05

Corrective Action

Documents

21-01253

EP Drill: EOF Controller Interject For State and County

Communication

2/24/2021

71114.05

Corrective Action

Documents

21-06491

EP Drill: CTRM Simulate Initial Notification Objective C.1 Met

with Comments

08/27/2021

71114.05

Corrective Action

Documents

21-06496

EP Drill: Drill Objective F.6 Not Met for DA due to Controller

Inject

08/27/2021

71114.05

Miscellaneous

DBNPS Emergency Plan

71114.05

Miscellaneous

ATA-2020-13695

20 Medical Emergency Drill

11/06/2020

71114.05

Miscellaneous

ATA-2021-5276

EP Integrated Drill Evaluation

04/07/2021

71114.05

Miscellaneous

ATA-2021-5372

Evaluate 1st Quarter 2021 ERO Proficiency Table Top Drills

04/09/2021

71114.05

Miscellaneous

ATA-2022-10418

Evaluation the Performance of the ERO During the

August 24, 2021 EP Integrated Drill

06/07/2022

71114.05

Miscellaneous

ATA-2022-10737

3rd Quarter 2021 ERO Proficiency Tabletop Drill Summary

06/11/2022

71114.05

Miscellaneous

ATA-2022-9175

Assess the Performance During the 2021 Post-Accident

Sample Drills

05/15/2022

71114.05

Miscellaneous

ATA-2022-9176

Evaluated Performance During October 15, 2021, Ops DA

Focus Area Drill

05/15/2022

71114.05

Miscellaneous

CA-SA-DB-2020-

0005

20 RMT Environmental Sample Drill Results

10/13/2020

71114.05

Miscellaneous

DBRM-EMER-

1500A

Davis-Besse Emergency Action Level Basis Document

71114.05

Miscellaneous

RA-EP-01500

Davis-Besse Nuclear Power Station Emergency Plan

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Implementing Procedure

71114.06

Corrective Action

Documents

22-04375

Simulator Malfunction Could Not be Removed During an

Evaluated Scenario

05/24/2022

71114.06

Corrective Action

Documents

22-04396

EP Drill 5/24/22 Integrated Drill UE Classification

06/24/2022

71114.06

Corrective Action

Documents

22-04403

EP Drill Simulator Computer Point Did Not Display Correctly

06/24/2022

71114.06

Corrective Action

Documents

22-04413

05/24/22 EP Integrated Drill Started 1 Hour Late Due to

Phone Issues in Simulator

05/25/2022

71114.06

Corrective Action

Documents

22-04415

EP Drill - Incorrect Release Path Analyzed Caused Missed

Drill Objective F.13

05/25/2022

71114.06

Miscellaneous

Davis-Besse Nuclear Power Station Drill/Exercise

May 24, 2022

05/24/2022

71124.05

Calculations

Library 105

Gamma Spectroscopy Nuclide Library

71124.05

Calibration

Records

LI 2.12.112

ARGOS-5 Calibration Record

2/31/2020

71124.05

Calibration

Records

LI 2.12.112

ARGOS-5 Calibration Record - Partial Calibration

Completed for Detector Replacement

03/05/2021

71124.05

Calibration

Records

LI 2.12.112

ARGOS-5 Calibration Record

01/19/2022

71124.05

Calibration

Records

LI 2.12.113

Chronos-4 Calibration Record

10/08/2020

71124.05

Calibration

Records

LI 2.12.113

Chronos-4 Calibration Record

10/19/2021

71124.05

Calibration

Records

LI 2.12.115

GEM-5 Calibration Record

2/04/2021

71124.05

Calibration

Records

LI 2.12.115

GEM-5 Calibration Record

2/11/2022

71124.05

Calibration

Records

LI 2.12.42

Whole Body Counter Calibration Record

11/03/2021

71124.05

Calibration

Records

LI 2.12.42

Whole Body Counter Calibration Record

2/28/2022

71124.05

Calibration

Records

LI 2.12.54

SAM-11 Calibration Record

07/21/2021

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.05

Calibration

Records

LI 2.7.233

ASP-1 with Neutron Radiation Detector Calibration Record

04/14/2021

71124.05

Calibration

Records

LI 2.7.233

ASP-1 with Neutron Radiation Detector Calibration Record

07/08/2021

71124.05

Calibration

Records

LI 2.7.502

Amp-100 Calibration Record

03/01/2022

71124.05

Calibration

Records

LI 2.7.502

AMP-100 Calibration Record

03/01/2021

71124.05

Calibration

Records

LI 2.7.545

Model L-177 Stationary Frisker Calibration Record

01/04/2021

71124.05

Calibration

Records

LI 2.7.545

Model L-177 Stationary Frisker Calibration Record

01/03/2022

71124.05

Calibration

Records

LI 2.7.558

Model L-177 Stationary Frisker Calibration Record

2/22/2021

71124.05

Calibration

Records

LI 2.7.558

Model L-177 Stationary Frisker Calibration Record

2/11/2022

71124.05

Calibration

Records

LI 2.7.682

FUJI Electric Model NSN3 Calibration Record

11/08/2021

71124.05

Calibration

Records

M&TE FAF0047

Calibration of Mass Thermal Flowmeter

09/21/2022

71124.05

Corrective Action

Documents

20-07352

RE5328A Will Not Calibrate

09/21/2020

71124.05

Corrective Action

Documents

20-07798

Station Vent Flow Computer Point F885 Step Change

10/08/2020

71124.05

Corrective Action

Documents

20-07980

20 D-B Mid-Cycle Assessment Observation - Radiation

Element Belt Guards

10/14/2020

71124.05

Corrective Action

Documents

20-08509

RE4597A Flow Reg Valve is >60 Percent Open

11/02/2020

71124.05

Corrective Action

Documents

20-09062

RP Section Gamma-Spec Failed Daily QC Check

11/25/2020

71124.05

Corrective Action

Documents

20-09113

Gamma-Spec Failed Daily QC Check

11/29/2020

71124.05

Corrective Action

Documents

20-09482

451B 2.7.525 Failed Source Check

2/15/2020

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.05

Corrective Action

Documents

20-09645

HPGe 3 (Radiation Protection) Failed Daily Source Check

2/22/2020

71124.05

Corrective Action

Documents

21-00174

Gamma-Spec Failed Daily Quality Control Check

01/10/2021

71124.05

Corrective Action

Documents

21-00727

J.L. Shepherd Model 89 Gamma Irradiator Safety Lock

Failure

2/04/2021

71124.05

Corrective Action

Documents

21-01230

RE4597BA Flow Regulating Valve is >60 Percent Open

2/24/2021

71124.05

Corrective Action

Documents

21-08786

IPA Quarterly Trending - Radiation Monitoring Equipment

11/17/2021

71124.05

Corrective Action

Documents

Resulting from

Inspection

22-04055

NRC Identified: Full Standardization of the Model 89

Calibrator

05/12/2022

71124.05

Corrective Action

Documents

Resulting from

Inspection

22-04146

NRC Identified: DB-HP-04029 Inconsistencies

05/16/2022

71124.05

Corrective Action

Documents

Resulting from

Inspection

22-04147

NRC Identified: Documentation of Dose Study for Measuring

RE4598 Grab Samples

05/16/2022

71124.05

Miscellaneous

DB-0395-2

Model 89 Standardization Check

01/13/2022

71124.05

Miscellaneous

DB-0395-2

Model 89 Standardization Check

01/15/2021

71124.05

Miscellaneous

Interlab Cross

Check Program

Results of Radiochemistry Cross Check Program

01/01/2020 -

2/31/2021

71124.05

Miscellaneous

NOP-OP-3201-06

20 and 2021 Interlaboratory Testing Program Results

01/01/2020 -

2/31/2021

71124.05

Procedures

DB-0500-0

Instrument Evaluation Form

71124.05

Procedures

DB-HP-00010

Radiation Measuring and Test Equipment Calibration and

Control Program

71124.05

Procedures

DB-HP-01103

Use of Portable Radiation, Contamination, and Airborne

Survey Equipment

71124.05

Procedures

DB-HP-01407

Calibration and Use of the J.L. Shepherd Model 89

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71124.05

Procedures

DB-HP-01458

Ludlum Model 2000 Portable Scaler Operation and

Calibration

71124.05

Procedures

DB-HP-1407

Calibration and Use of the J.L. Shepherd Model 89

71124.05

Procedures

DB-MI-04559

Channel Calibration if RE-1998 (Failed Fuel)

71124.05

Procedures

DBBP-RP-1007

Meter Source and Response Testing

71124.05

Procedures

NOP-OP-4416

ARGOS-5 Personnel Contamination Monitor Calibration and

Use

71124.05

Work Orders

200761572

DB-HP4029-001 Review Rad Monitor Setpoints

2/30/2020

71151

Miscellaneous

NRC Performance Indicator Data; Emergency Preparedness

Drill/Exercise Performance

01/01/2021 -

03/30/2022

71151

Miscellaneous

NRC Performance Indicator Data; Emergency Preparedness:

ERO Participation Drill

01/01/2021 -

03/30/2022

71151

Miscellaneous

NRC Performance Indicator Data; Emergency Preparedness:

Alert and Notification System

01/01/2021 -

03/30/2022

71152A

Corrective Action

Documents

22-00879

Abnormal Procedure Entries for Loss of Letdown Flow Path

2/05/2022

71152A

Corrective Action

Documents

22-00879

Abnormal Procedure Entries for Loss of Letdown Flow Path

2/05/2022

71152A

Procedures

DB-OP-01003

Operations Procedure Use Instructions

71152A

Procedures

DB-OP-02002

Letdown/Makeup Alarm Panel 2 Annunciators

71152A

Procedures

DB-OP-02512

Makeup and Purification System Malfunctions

71152A

Procedures

DB-OP-06006

Makeup and Purification System

71152A

Procedures

DBBP-DCU-0109

Processing Engineering Change Packages

71152A

Procedures

NOBP-OP-0012

Operator Work-Arounds, Burdens, Control Room

Deficiencies and Operations Aggregate Assessment

71152A

Procedures

NOBP-SS-4001

Change Management

71152A

Procedures

NOP-LP-2601

Procedure/Work Instruction Use and Adherence

71152A

Procedures

NOP-OP-1001

Clearance/Tagging Program

71152A

Procedures

NOP-OP-1002

Conduct of Operations

& 17

71152A

Procedures

NOP-OP-1014

Plant Status Control

08