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{{#Wiki_filter:TENNESSEE VALLEY AUTHORITY BROGANS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT BROWNS FERRY NUCLEAR PLANT SEPTEMBER 1980 Submitted By: Plant Manager-">>o;6 o5//  
{{#Wiki_filter:TENNESSEE VALLEY AUTHORITY BROGANS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT BROWNS FERRY NUCLEAR   PLANT SEPTEMBER 1980 Submitted By:
Plant Manager
-">>o;6 o5//


TABLE OF CONTENTS PART I Operations Summary Plant Operations Fuel Performance
TABLE OF CONTENTS PART I Operations Summary Plant Operations Fuel Performance       .
.Refueling Information.
Refueling Information.                                         10 Equipment Performance.                                         12 Change     in Procedures                                       16 Change     in Facility     Design.                             16 Surveillance Testing                                           17 Containment Leak Rate Tests.                                   18 Changes,     Tests, and Experiments Requiring Authorization from the         NRC Pursuant to 10 CFR 50 59  ~   (a)                   ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ o 18 Changes     in Plant Operating Organization.                 18 Reports to     NRC .                                         19 Changes,     Tests, and Experiments Not Requiring Authorization from the         NRC Pursuant to 10 CFR 50.59 (a)                                               20 Primary Coolant Chemistry.
10 Equipment Performance.
Source Tests       0 ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 22 Environmental Technical Specification Requirements             23 Calculation of       Usage   Factor.                           23 PART II Important Events.                                                     24 Vis i'to 1 s ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~
12 Change in Procedures 16 Change in Facility Design.16 Surveillance Testing 17 Containment Leak Rate Tests.18 Changes, Tests, and Experiments Requiring Authorization from the NRC Pursuant to 10 CFR 50~59 (a)~~~~~~~~~~o 18 Changes in Plant Operating Organization.
Safety and       First Aid.                                           27
18 Reports to NRC.19 Changes, Tests, and Experiments Not Requiring Authorization from the NRC Pursuant to 10 CFR 50.59 (a)20 Primary Coolant Chemistry.
 
Source Tests 0~~~~~~~~~~~~~~~~~~~22 Environmental Technical Specification Requirements 23 Calculation of Usage Factor.23 PART II Important Events.24 Vis i'to 1 s~~~~~~~~~~~~~~~Safety and First Aid.27 TABLE OF CONTENTS (Continued)
TABLE OF CONTENTS   (Continued)
PART II (Continued)
PART II (Continued)
Accidental'
Accidental'
~~~~o~~~27 Plant Personnel Listing.Personnel Changes-Annual Personnel Changes-Hourly.Significant Operational Events Plant Instruction Revisions.
                    ~ ~ ~ ~ o ~ ~ ~                   27 Plant Personnel Listing.                             28 Personnel Changes Annual                           31 Personnel Changes Hourly .                         37 Significant Operational Events                       40 Plant Instruction Revisions.                         45 Reportable Occurrences                               46 Primary Coolant Chemistry.                           49 Average Daily Gross Capacity Factor.                 51 Accumulated Average Daily Gross Factor       .     52 Radwaste Monthly Average Discharge       Rate/Total Activity Discharged.                                 57 Building   and Stack Monthly Release     Rates       58 Specification Comparison Building            'echnical and Stack Release     Rates                         59 Reactor Power Percent.                               60 Nuclear Plant Operating       Statistics             63 Unit Outage   and Availability                     64 Outage Summary .                                     67 Electrical   Maintenance Summary                     68 Electrical   Maintenance Summary Charts CSSC Equipment.                               70 Non-CSSC Equipment.                             73 Mechanical Maintenance Summary                       76
28 31 37 40 45 Reportable Occurrences 46 Primary Coolant Chemistry.
 
Average Daily Gross Capacity Factor.Accumulated Average Daily Gross Factor.49 51 52 Radwaste Monthly Average Discharge Activity Discharged.
I TABLE OF CONTENTS (Continued)
Rate/Total 57 Building and Stack Monthly Release Rates 58'echnical Specification Comparison and Stack Release Rates Building 59 Reactor Power Percent.60 Nuclear Plant Operating Statistics 63 Unit Outage and Availability 64 Outage Summary.67 Electrical Maintenance Summary Electrical Maintenance Summary Charts CSSC Equipment.
Non-CSSC Equipment.
68 70 73 Mechanical Maintenance Summary 76 I
TABLE OF CONTENTS (Continued)
PART II (Continued)
PART II (Continued)
Mechanical Maintenance Summary Charts CSSC Equipment Non-CSSC Equipment Instrument Maintenance Summary.77 80 82 CSSC Equipment 87 Radioactive Liquid Effluents.
Mechanical Maintenance Summary Charts CSSC Equipment                                 77 Non-CSSC Equipment                               80 Instrument Maintenance Summary.                       82 CSSC Equipment                                 87 Radioactive Liquid Effluents.                         88 Airborne Releases Solid Radioactive Waste                               96 Effluent   and Waste Disposal Monthly Report.       100 Resin Usage   .                                       101 Powdered Resins   % Total Usage .               ~ ~ 102 BFNP Filter Demineralizer Performance               103 Fuel Cladding Integrity Parameters.                 106 Waste Treatment System Volume Throughputs             108 Water Treatment Chemical Use.                         109 Total Plant Training   Summary.                     110
88 Airborne Releases Solid Radioactive Waste 96 Effluent and Waste Disposal Monthly Report.100 Resin Usage.101 Powdered Resins%Total Usage.~~102 BFNP Filter Demineralizer Performance 103 Fuel Cladding Integrity Parameters.
 
106 Waste Treatment System Volume Throughputs 108 Water Treatment Chemical Use.109 Total Plant Training Summary.110 PART I 0 erations Summar September 1980 Unft 1 Unit 1 was critical for 703.3 hours, produced 699,320 MWH (gross)with 3.07 percent station use, resulting'n a average hourly gross load of 1,003,012 Kw during the month.The average net heat rate for the month was 10,950 BTU/KWH.There are 192 full power days estimated remaining until the end of cycle 3 fuel.With a capacity factor of 85 percent the target EOC exposure would be reached on May 10, 1981.This includes 0 days of coastdown.
PART I 0 erations Summar September   1980 Unft 1 Unit   1 was critical for 703.3 hours, produced 699,320 MWH (gross) with 3.07 percent   station use, resulting'n a average hourly gross load of 1,003,012   Kw during the month. The average net heat rate for the month was 10,950 BTU/KWH. There are 192       full power   days estimated remaining     until the end of cycle     3 fuel. With   a capacity factor of   85 percent the target EOC exposure would be reached on May 10, 1981.         This includes   0 days of coastdown. The capacity factor for the month   was 88.4   percent.
The capacity factor for the month was 88.4 percent.There were two scrams on the unit during the month.On September 1, the reactor scrammed when water from the offgas cooler dripped onto the stator cooling cabinet causing a short in a pressure relay tripping the turbine.The reactor scrammed on September 24, when a short circuit occurred in the sudden pressure trip caosing the 500 KV circuit breakers to open which caus'ed a general load reject.There were seven power reductions during the month.On September 3, power was reduced because of maintenance to the"C" string high pressure heaters.Power was reduced on September 7, 20, and 27, for turbine control valve tests and Sl's.On September 16, power was reduced when"A" recirculating water pump was taken out-of-service to place the unit on cooling towers.Power was reduced on September 19, when the"B" reactor feedwater pump was taken out-of-service for maintenance for excessive vibration.
There were two scrams on the     unit during the   month. On September 1, the reactor   scrammed when   water from the offgas cooler dripped onto the stator cooling cabinet causing a short in     a pressure relay tripping the turbine.       The reactor   scrammed   on September 24, when a short   circuit occurred in the sudden pressure   trip caosing the 500   KV circuit breakers to open which caus'ed     a general load reject.
On September 29, power was reduced for condensate de-mineralizer backwash and precoat due to problems on three of the condensate demineralizers.
There were seven power reductions during the month.         On September   3, power was reduced   because of maintenance to the "C" string high pressure heaters.           Power was reduced   on September   7, 20, and 27,   for turbine control valve tests       and Sl's.
0 erations Summar (Continued)
On September   16, power was reduced when "A"     recirculating water     pump was   taken out-of-service to place the unit       on cooling towers. Power was reduced on September 19, when the "B" reactor feedwater pump was taken         out-of-service for maintenance for excessive vibration.       On September 29, power was reduced     for condensate   de-mineralizer backwash     and precoat due to problems on     three of the condensate demineralizers.
September 1980 Evaluation of Unit 1 cycle performance shows that the unit operated 10,620 BTU/KWH gross heat rate which is 0.88 percent higher than expected.Unit 2 Unit 2 was critical 118.78 hours, produced 113,120 NWH (gross)with 4.69 percent station use, resulting in an average hourly gross load of 952,349 kW during the month.The average net heat rate for the month was 10,850 BTU/KWH.The EOC 3 refueling outage for Unit 2 began on September 5, 1980.The capacity factor for the month was 14.3 percent.There was one scram on the unit during the month.On September 5, the reactor was manually scrammed in preparation for the beginning of the EOC-3 re-fueling outage.There was one power reduction during the month.From September 1, to'I September 5, power was reduced due to end of cycle coastdown to the EOC-3 refueling outage that began on September 5.Evaluation of the Unit 2 cycle performance shows that the unit operated 10,350 BTU/KWH gross heat rate which is 2.72 percent lower than expected.Unit 3 Unit 3 was critical for 654.2 hours, produced 625,700 MK (gross)with 2.98 percent station use, resulting in an average hourly gross load of 956,245 kW during the month.The average net heat rate for the month was 10,820 BTU/KWH.There are 31 full power days estimated until the end of.cycle 3 fuel.With a capacity factor of 85 percent the target EOC exposure would be reached on October 31, 1980.This includes 26 days of coastdown.
 
The capacity factor for the month was 79.1 percent.
0 erations   Summar     (Continued)
0 erations Summar (Continued)
September   1980 Evaluation of Unit       1 cycle performance     shows that the unit operated 10,620   BTU/KWH   gross heat rate which       is 0.88 percent higher than expected.
September 1980 There were two scrams on the unit during the month.On September 12, the reactor was manually scrammed to begin a short maintenance outage on the"B" inboard main steam isolation valve.The reactor scrammed on September 20, when a 480 V shutdown board failed to transfer from alternate to normal feed pro-ducing a loss of RPS MG set and the isolation of a SJAE which caused a main condenser low vacuum.There were seven power reductions during the month.On September 1, power was reduced when"A" recirculation pump tripped.Power was reduced on September 7 and 27, for turbine control valve tests and SI's.From September 7 to September 12, power was reduced when the closure time was found to be too fast on MSIV 1-26 and the valve was closed until a short maintenance outage on September 12.Power was reduced on September 23, for a control rod pattern adjustment.
Unit 2 Unit   2 was critical   118.78 hours, produced 113,120       NWH (gross) with 4.69 percent station use, resulting           in an average   hourly gross load of 952,349 kW during the month.       The average   net heat rate for the month     was 10,850 BTU/KWH.
On September 24, power was reduced due to loss of the computer while performing preconditioning to full power.Evaluation of the Unit 3 cycle performance shows that the unit operated at 10,550 BTU/KMH gross heat rate which is 1.42 percent lower than expected.
The EOC 3   refueling outage for Unit       2 began on September     5, 1980. The capacity factor for the     month was 14.3 percent.
0 erations Summar (Continued)
There was one scram on the         unit during the     month. On September 5, the reactor   was manually scrammed in preparation         for the beginning of the     EOC-3 re-fueling outage.
September 1980 Reliabilit and Availabilit The accumulated average daily gross (AADG)capacity factors, based upon midnight IÃH meter readings, for each unit is tabulated below for each month during the last calendar year.The second column compares this year'performance with last year.Unit No.1 Unit No.2 Unit No.3 1979 1980 1979 1980 1979 1980 Jan Feb Apr*17.4*7.6 (28)50.7*3.8 (29)59.2 2.9 (22)67.0 18.1 94.8 86.4 94.0 62.5 91.5 65.9*90.4 69.4 90.8 37.4 93.3 67.4 93'77.8 93.6 83.1 June 72.5 31.1*72.3 72.9 90.5 84.1 75.7 38.9 72.4 73.1 85.0 84.2'uly 78.0 44.9 75.2 73.3 85.0 7.94 Aug 79.9, 51.0 77.7 75.0*81.8 81.4 Sept Oct Nov Dec(')79.1 55.2 80.0 79.6 80.1 79.0*68.2 (25)80.6*81.5 79.5*72.7.81.1*65.5 Nc (39)*59'*58.7*Refuel Outage (Days of Month)Yearly Average (1)Unit 1 can achieve an AADG capacity factor of about 62.7%for CY'80 if it averages 85%CF (presently averaging 77.8%)for the remainder of the year, considering unit operating time (i.e.: not in refuel).Similarly, Units 2 and 3 can reach about 64.8%and 73.0%AADG capacity factors, re-spectively.
There was one power reduction during the month.               From September   1, to
Presently these units are averaging 75.0%and 81.1%, respectively.
                      'I September     5, power was reduced due to end of cycle coastdown to the EOC-3 refueling outage that began on September 5.
0 erations Summer (Continued)
Evaluation of the Unit       2 cycle performance     shows that the unit operated 10,350   BTU/KWH   gross heat rate which is 2.72 percent lower than expected.
September 1980 Reliabilit and Availabilit (Continued)
Unit 3 Unit   3 was critical for     654.2 hours, produced 625,700 MK (gross) with 2.98 percent station use, resulting           in an average   hourly gross load of 956,245   kW during the month.       The average   net heat rate for the month     was 10,820 BTU/KWH. There are 31           full power   days estimated   until the end of
The largest capacity factor loss (12%)this month was on Unit 3 due to an inoperable HSIV (1-26"B" inboard valve).This valve was closed and limited to 75%power for about 5.8 days.The next largest CF loss (Unit 1~4.9%, Unit 3=2.9%)involves automatic scrams caused by equipment malfunctions.
.cycle   3 fuel. With   a   capacity factor of     85 percent the target   EOC exposure would be reached on October 31, 1980.             This includes   26 days of coastdown.
A significant controllable CF loss involved control rod pattern limitations on unit 1 and 3 at 0.8%and 1.7%re-spectively.
The capacity factor for the month         was   79.1 percent.
These losses result from postponing rod pattern adjustment until weekends when more favorable system load requirements exist.
 
l, RELIABILITY AND AVAILABILITY (CONTINUED)
0 erations   Summar   (Continued)
CAPACITY FACTOR LOSSES September 1980 Unit 1 Unit 2 Unit Losses were caused by: 80.1%88.4 79.5%14.3 58.7%79.1 l.2.3.4.5.6.7.8.9.10.11.12.13.14.15.16.17.18.19.20.21.22.23.24.25.26.27.28.29.30.31.32.33.Refueling P CION End of cycle coastdown Feed piping failure Startup testing Administrative limitations Steam tunnel temperature switches Reactor feed pump maintenance High condenser backpressure Thermal limits Recirculation pump motor bearing problems Automatic scram Drywell air leakage Reduced thermal limits Turbine vibration and balancing Heater problems Hoisture separator high level Recirculation pump starting problems Feedwater control problems EHC and turbine valve problems THI related modifications Recirculation system vibration evaluation Hain steam valve maintenance Recirculation H-G set brush changes Rod sequence exchange TIP system CMf system hydrogen sensor failure Offgas system malfunction Power cable replacement Testable check valve maintenance Load following demonstration test Demineralizer problems Low pressure air line break 5.5 2.8 1.4 1.4 0.9 0.8 0.7 0.6 0.6 0.5 0.5 0.5 0.4 0.4 0.3 0.3 0.3 0.3 0.2 1.9;0.6 1.8 I>4.9 0.2 0.6 9.5 2.5 0.2 0.5 0.6 0.1 I.0.6 0.2 0.8 2.2 1.5 0.6 0.'3 0.3 0.2 0.2 83.6 2-.1 29.3 1.8 1.0 1.3 0.3 3.9 0.8.0.1 0.2 0.2 0'0.5 0.3 0.3 0.2 0.2 0.1 2.1 0.2 2.9 12;0 0.2 RELIABILITY AND AVAILABILITY (CONTINUED)
September   1980 There were two scrams on the       unit during the     month. On September 12, the reactor was manually scrammed to begin a short maintenance outage on the "B" inboard main steam isolation valve.         The   reactor   scrammed   on September   20, when a 480 V shutdown board     failed to transfer from alternate to normal             feed pro-ducing a loss of   RPS MG set and the isolation of       a SJAE   which caused a main condenser   low vacuum.
CAPACITY FACTOR LOSSES September 1980 Unit 1 Unit 2 Unit 3 80.1%88.4 79.5%14.3 58.7%79.1 Losses were caused by: 34.Rod pattern, full core flow 35.Surveillance instruction 36.Recirculation pump trip 37.Feedwater system leak 38.Control rod adjustment 0.8 0.1 1.7 0.1 0.4 0.9 0.2 0 erations Summar (Continued)
There were seven power reductions during the month.               On September 1, power was reduced when "A"       recirculation     pump tripped.     Power was reduced on September   7 and 27,   for turbine control valve tests         and SI's. From September 7 to September 12, power     was reduced when     the closure time was found to be too fast on MSIV 1-26 and the       valve was closed until   a short maintenance outage on September   12. Power was reduced on September         23,   for a control rod pattern adjustment. On September   24, power was reduced due to loss           of the computer while performing preconditioning to         full power.
September 1980 Common The radwaste system performed as designed.Approximately 7.58E+05 gallons of waste liquid were discharged containing approximately 1.36E+00 curies of activities.
Evaluation of the Unit     3 cycle performance     shows   that the unit operated at 10,550   BTU/KMH gross heat rate which       is 1.42 percent lower than expected.
Floor drain system through-put increased this month primarily because of decontamination activities associated with the unit two refueling outage.Radwaste shipments to Barnwell, S.C.were interrupted for approximately 8 days due to a delay in the receipt of the required state shipping permit.There were 14 shipments for an approximate total volume of 5,600 cubic feet.There were 399 (55 gallon)drums of radwaste generated during the month at an average rate of 13.3 drums per day.There were 33 boxes of trash and irradiated components generated during the month at an average rate of 1.1 boxes per day.
 
0 erations Summar (Continued)
0 erations Summar   (Continued)
September 1980 Fuel Performance Unit 1 The reactor was operated at a nominal maximum thermal power level of 99.2%of rated.Typical thermal limits for this condition include CMFLPD, 0.973;MAPRAT, 0.945 and CMFCP, 0.885.The reactor operated in control rod sequence"A" 12 days, and in sequence"B" the remainder of the month.Fuel preconditioning at the rate of 0.11 kw/ft/hr was conducted for approximately 1.4 days in sequence"A", and 3.1 days in sequence"B".Unit 2 The reactor was operated at a nominal maximum thermal power level of 90%of rated.Typical thermal limits for this condition included CMFLPD, 0.731;HAPRAT, 0.730;CMFCP, 0.810.The reactor operated in control rod sequence"B" for the entire month.Fuel preconditioning at the rate of 0.11 kw/ft/hr was conducted for approximately 0 days in sequence"B".Unit 3 The reactor was operated at a nominal maximum thermal power level of 99.2%of rated.Typical thermal limits for this condition CttFPLD, 0.850: MAPRAT, 0.827;and CMFCP, 0.965.The reactor operated in control rod sequence"A" for 14 days, and in sequence"B" the remainder of the month.Fuel preconditioning at the rate of 0.11 Kw/ft/hr was conducted for 1.5 days in sequence"A", and 3.5 days in sequence"B".
September   1980 Reliabilit   and Availabilit The accumulated   average   daily gross   (AADG)     capacity factors, based upon midnight IÃH meter readings,       for each   unit is tabulated         below for   each month during the   last calendar year. The second     column compares       this year' performance with   last year.
Unit No. 1       Unit No. 2       Unit   No. 3 1979   1980       1979   1980       1979     1980 Jan             *17.4
* 7.6       94.8  86.4        90.8      37.4 (28)
Feb              50.7
* 3.8       94.0  62.5        93.3      67.4 (29) 59.2     2.9     91.5  65.9        93 '      77.8 (22)
Apr              67. 0 18. 1    *90.4 69.4         93.6      83.1 72.5   31.1     *72.3   72.9       90.5     84.1 June            75.7   38.9       72.4   73.1       85.0 84.2'uly 78.0   44.9       75.2   73.3       85.0     7.94 Aug             79.9, 51.0       77.7   75.0     *81.8 81.4 Sept             79.1   55.2       79.0 *68.2       *72.7.      81.1 (25)
Oct              80. 0            80.6 *           *65. 5   Nc (39)
Nov              79.6              81.5            *59 '
Dec(')          80.1              79.5            *58.7
*Refuel Outage (Days of Month)
(1) Yearly Average Unit 1 can achieve an   AADG capacity factor of about           62.7% for CY   '80 if it averages   85% CF   (presently averaging     77.8%)   for the remainder of the year, considering unit operating time       (i.e.:   not in refuel).           Similarly, Units 2 and 3 can reach about 64.8% and 73.0%       AADG     capacity factors, re-spectively. Presently these units are averaging         75.0% and 81.1%,       respectively.
 
0 erations Summer   (Continued)
September 1980 Reliabilit   and Availabilit   (Continued)
The largest capacity factor loss     (12%) this month was on   Unit 3 due   to an inoperable HSIV (1-26 "B" inboard valve).       This valve was closed and limited to 75% power for about 5.8 days.
The next largest   CF loss (Unit 1 ~ 4.9%,   Unit 3 = 2.9%)   involves automatic scrams caused by equipment malfunctions.       A significant controllable     CF loss involved control rod pattern limitations on unit       1 and 3 at 0.8% and 1.7%   re-spectively. These losses result from postponing rod pattern adjustment until weekends when more   favorable system load requirements exist.
 
l, RELIABILITY AND AVAILABILITY(CONTINUED)
CAPACITY FACTOR LOSSES September     1980 Unit 1             Unit 2           Unit 80.1%   88.4   79.5%     14.3     58.7%   79.1 Losses were caused by:
: l. Refueling                                                      5.5              9.5         83. 6   29.3
: 2. P CION                                                        2.8         1.9 2.5                  1.8      2.1
: 3. End  of cycle coastdown                                        1.4              0.2          2-. 1
: 4. Feed piping failure                                            1.4
: 5. Startup testing                                                0.9              0.5                  1.0
: 6. Administrative limitations                                    0.8
: 7. Steam tunnel temperature switches                              0.7
: 8. Reactor feed pump maintenance                                  0.6      ;0.6  0.6                  1.3
: 9. High condenser backpressure                                    0.6        1.8  0.1                  0.3      0.2
: 10. Thermal limits                                                 0.5                  I
: 11. Recirculation pump motor bearing problems                     0.5      I 3.9
: 12. Automatic scram                                               0.5      >4.9  .0.6                  0.8.      2.9
: 13. Drywell air leakage                                            0.4
: 14. Reduced thermal limits                                        0.4
: 15. Turbine vibration and balancing                                0.3
: 16. Heater problems                                               0.3        0.2
: 17. Hoisture separator high level                                  0.3
: 18. Recirculation pump starting problems                          0.3              0.2
: 19. Feedwater control problems                                    0.2              0.8                  0.1
: 20. EHC and turbine valve problems                                                 2.2                 0.2
: 21. THI related modifications                                                      1.5
: 22. Recirculation system vibration evaluation                                      0.6
: 23. Hain steam valve maintenance                                                    0.'3                          12;0
: 24. Recirculation H-G set brush changes                                            0.3
: 25. Rod sequence exchange                                                      0.0.2                  0.2
: 26. TIP system                                                                      0.2                  0'        0.2
: 27. CMf system hydrogen sensor failure                                                                  0.5
: 28. Offgas system malfunction                                                                            0.3
: 29. Power cable replacement                                                                              0.3
: 30. Testable check valve maintenance                                                                    0.2
: 31. Load following demonstration test
: 32. Demineralizer problems                                                                              0.2
: 33. Low pressure air line break                                                                          0.1
 
RELIABILITY AND AVAILABILITY(CONTINUED)
CAPACITY FACTOR LOSSES September  1980 Unit 1          Unit 2          Unit 3 80.1%      88.4 79.5%      14.3 58.7%      79.1 Losses were caused by:
: 34. Rod pattern,  full core flow                                          0.8                             1.7
: 35. Surveillance instruction                                                0.1                            0.1
: 36. Recirculation pump trip                                                                                0.4
: 37. Feedwater system leak                                                                                  0.9
: 38. Control rod adjustment                                                                                  0.2
 
0 erations  Summar  (Continued)
September 1980 Common The radwaste  system performed as designed.     Approximately 7.58E+05 gallons of waste liquid were discharged containing approximately 1.36E+00 curies of activities.     Floor drain system through-put increased this month primarily  because  of decontamination activities associated with the unit two  refueling outage.
Radwaste shipments    to Barnwell, S. C. were   interrupted for approximately 8 days due  to  a delay in the receipt of the required state shipping permit.
There were 14 shipments    for  an approximate  total  volume of 5,600 cubic  feet.
There were 399 (55 gallon) drums of radwaste generated        during the month at an average  rate of 13.3  drums per day. There were 33 boxes of trash and irradiated  components  generated during the month at an average rate of 1.1 boxes per day.
 
0 erations   Summar     (Continued)
September     1980 Fuel Performance Unit  1 The reactor  was operated    at  a  nominal maximum thermal power      level of 99.2%  of rated. Typical thermal limits for this condition include            CMFLPD, 0.973;  MAPRAT, 0.945    and CMFCP, 0.885.       The  reactor operated in control rod sequence    "A" 12 days, and in sequence "B"          the remainder of the month.
Fuel preconditioning at the rate of 0.11          kw/ft/hr was  conducted    for approximately 1.4 days in sequence "A", and 3.1 days in sequence "B".
Unit  2 The reactor was operated   at a nominal maximum thermal power     level of 90% of rated. Typical thermal limits for this condition included            CMFLPD, 0.731;   HAPRAT, 0.730;  CMFCP,   0.810. The reactor operated in control rod sequence   "B" for the entire    month.
Fuel preconditioning at the rate of 0.11           kw/ft/hr was conducted   for approximately   0 days in sequence   "B".
Unit 3 The reactor was operated at a nominal maximum thermal power level of 99.2%   of rated. Typical thermal limits for this condition         CttFPLD, 0.850:
MAPRAT,   0.827; and  CMFCP,   0.965. The reactor operated in control rod sequence   "A" for 14 days, and    in  sequence    "B" the remainder of the month.
Fuel preconditioning at the rate of 0.11 Kw/ft/hr           was conducted   for 1.5 days in sequence "A", and 3.5 days in sequence "B".
 
10 Operations Summary (Continued)
10 Operations Summary (Continued)
September 1980 Refuelin Information Unit 1 Unit 1'is scheduled for its fourth refueling beginning on or about April 15, 1981, with a scheduled restart date of July 25, 1981.This re-fueling will involve loading additional 8 x 8 R (retrofit) fuel assemblies into the core, the final fix on, the sparger modification, power supply on LPCI modification, and torus modifications if all approvals are received.There are 764 fuel assemblies in the reactor vessel.The spent fuel storage pool presently contains 550 spent 7 x 7 fuel assemblies, five 8 x 8 fuel assemblies, and one 8 x 8 R fuel assembly.Because of modification work to increase spent fuel pool capacity to 3471 assemblies, present capacity is limited to 1152 assemblies.
September   1980 Refuelin   Information Unit 1 Unit   1 'is scheduled for   its fourth refueling               beginning on or about April 15,   1981,   with a scheduled   restart date of July               25, 1981. This re-fueling   will involve   loading additional       8 x 8 R     (retrofit) fuel       assemblies into the core, the final         fix on, the sparger modification, power supply on LPCI modification,     and   torus modifications       if all approvals           are received.
Unit 2 Unit 2 is presently in its EOC 3 refueling outage.Unit 2 is scheduled for its fourth refueling beginning on or about March 1, 1982, with a scheduled restart date of June 14, 1982.This refueling outage will involve completing relief valve modifications, torus modifications if all approvals are received,"A" low pressure turbine'inspection, and loading additional 8 x 8 R fuel assemblies into the core.There are 764 fuel assemblies in the reactor vessel.At the end of the H+'onth, there were 132 discharged cycle 1 fuel assemblies, 156 discharged cycle 2 fuel assemblies, and 352 discharged cycle 3 fuel assemblies in the spent storage pool.The present storage capacity of the spent fuel pool is 820 assemblies.
There are 764     fuel assemblies in the reactor vessel.                     The spent   fuel storage pool presently contains 550 spent             7 x 7 fuel assemblies, five           8 x 8 fuel assemblies,     and one 8 x 8 R     fuel assembly.               Because of modification work to increase spent       fuel pool capacity to         3471 assemblies,         present capacity is limited to     1152 assemblies.
With present capacity, the 1979 refueling was the last Operations Summary (Continued)
Unit 2 Unit   2   is presently in its     EOC 3   refueling outage.               Unit 2 is scheduled for its fourth refueling beginning           on or about March 1, 1982,               with a scheduled restart date of     June 14, 1982.     This refueling outage               will involve completing relief valve modifications, torus modifications                 if all approvals are received, "A" low pressure turbine 'inspection, and loading additional                       8 x 8 R   fuel assemblies     into the core.
September 1980 Refuelin Information Unit 2 (Continued) refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.However, new high density storage racks are being installed during the third refueling of Unit 2.Unit 3 Unit 3 is scheduled for its third refueling beginning on or about November 2, 1980, with a scheduled restart date of December 11, 1980.This EOC-3 refueling, involves loading additional 8 x 8 R (retrofit) assemblies into the core, and power supply on LPCI modification.
There are 764     fuel assemblies in the reactor vessel.                   At the end of the there were   132   discharged cycle     1   fuel assemblies, H+'onth, 156 discharged cycle   2 fuel assemblies,     and 352 discharged       cycle         3 fuel assemblies in the spent storage pool.       The present   storage capacity of the spent fuel pool is 820 assemblies.       With present capacity, the 1979 refueling was the                     last
There are 764 fuel assemblies presently in the reactor vessel.There are 144 discharged cycle 2 fuel assemblies, 208 discharged cycle 1 fuel assemblies, and 164 new P 8 x 8 R assemblies in the spent fuel storage pool.The present storage capacity of the spent fuel pool is 1528 assemblies.
 
With present capacity, the 1980 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.
Operations   Summary (Continued)
12 0 erations Summar (Continued)
September 1980 Refuelin   Information Unit 2 (Continued) refueling that could     be discharged   to the spent fuel pool without exceeding that capacity     and maintaining   full core discharge capability in the pool.
September 1980 E ui ment Performance On September 16, at approximately 1730 hours, localized flooding was ex-perienced in the yard in front of the radwaste and the unit 1 and 2 diesel building.The flooding began during an attempt to place Unit 1 on cooling towers.Gate lA1 was closed and the resulting back pressure forced open a cover-plate sealing the top of the CCW conduit.Opening gate 1Al halted the flow of water into the yard area.The cover-plate on the Unit 1 conduit has been securely refastened.
However, new high density storage racks are being           installed during the third refueling of Unit     2.
While performing leak checks on 2D RHR heat exchanger, it was discovered that a check valve in the raw service water charging connection to RHR service water was stuck open.This allowed a leak test on 2D RHR heat exchanger to be interpreted as positive indication of leakage because it placed 2D RHR heat ex-changer (RHR side)in communication with RHRSW through 2B RHR heat exchanger which was known to be leaking.The check valve was repaired and a satisfactory leak check of 2D RHR heat exchanger was performed.
Unit 3 Unit 3 is scheduled for its third refueling beginning       on or about November 2, 1980,     with a scheduled   restart date of     December 11, 1980. This EOC-3   refueling, involves loading additional       8 x 8 R (retrofit) assemblies into the core,     and power supply on LPCI   modification.
Unit 1 Reactor Building Equipment Drain Sump Heat Exchanger was determined to be providing inadequate cooling for the contents of the Reactor Building Equip-ment Drain Sump.This was indicated by steam rising through the sump pump support plate.Investigation thus far points to inadequate cooling water flow from RBCCW to the sump heat exchanger.
There are 764   fuel assemblies presently in the reactor vessel.           There are 144 discharged cycle     2 fuel assemblies,   208   discharged cycle 1 fuel assemblies,   and 164 new P 8 x 8 R assemblies       in the spent fuel storage pool. The present   storage capacity of the spent fuel pool is 1528 assemblies. With present capacity, the 1980 refueling would be the           last refueling that could     be discharged   to the spent fuel pool without exceeding that capacity     and maintaining   full core   discharge capability in the pool.
This investigation continues.
 
13 0 erations Summar (Continued)
12 0 erations   Summar   (Continued)
September 1980 E ui ment Performance (Continued)
September   1980 E ui ment Performance On September   16, at approximately 1730 hours,         localized flooding     was ex-perienced in the yard       in front of the radwaste       and the unit 1 and 2   diesel building. The flooding   began during   an attempt to place Unit     1 on   cooling towers. Gate lA1 was closed and the         resulting back pressure forced         open a cover-plate sealing the top of the         CCW   conduit. Opening gate 1Al halted the flow of water into the yard area.           The   cover-plate   on the Unit 1 conduit has been securely     refastened.
High vibration on 1B Reactor Feedwater Pump was noted during routine weekly vibration checks this month.Increased surveillance revealed a high axial vibration level initially.
While performing leak checks on         2D RHR   heat exchanger,   it was   discovered that a check   valve in the raw service water charging connection to               RHR service water was stuck open.       This allowed   a leak test on     2D RHR heat exchanger to be interpreted   as positive indication of leakage         because   it placed   2D RHR heat ex-changer (RHR side)     in   communication with     RHRSW   through 2B RHR heat exchanger which was known to be leaking.         The check     valve was repaired and   a satisfactory leak check of     2D RHR heat exchanger was performed.
This then shifted to high horizontal vib-ration at a frequency two times the pump run speed.As this is indicative of misalignment and the vibration levels continued to become more severe, the pump was removed from service and the coupling disassembled.
Unit 1 Reactor Building Equipment Drain         Sump   Heat Exchanger was determined to be providing inadequate cooling for the contents of the Reactor Building Equip-ment Drain Sump.       This   was indicated by steam rising through the         sump pump   support plate. Investigation thus far points to inadequate cooling water flow from                 RBCCW to the   sump heat exchanger.       This investigation continues.
It was found that all of the oil had been thrown out of the coupling.The oil was replaced and the pump returned to service without further problems.Prior to the beginning of Unit 2 refueling outage, performance checks on both spent fuel storage pool cooling pumps for Unit 2 determined both pumps to be performing at less than 85%of their design capacities.
 
Both pumps were rebuilt and subsequently performed at greater than design criteria.High differential pressures were experienced on 2B reactor water clean-up filter demineralizer.
13 0 erations   Summar     (Continued)
Investigation revealed that a failure of the stainless steel filter elements allowed precoat material to accumulate on the resin trap.The problem was corrected by replacement of the filter elements and associated resin trap.Resin traps on reactor water clean-up demineralizers 1A and 1B were removed I and examined to determine the cause of high differential pressure.An accumulation of rust was found on the traps.The source of the rust is still under investigation.
September   1980 E ui ment Performance     (Continued)
There was no indication of problems with filter element integrity.
High vibration   on 1B Reactor Feedwater         Pump was   noted during routine weekly   vibration   checks   this month. Increased surveillance revealed         a high axial vibration level       initially. This then shifted to high horizontal vib-ration at   a frequency two times the       pump   run speed.     As this is indicative of misalignment     and the vibration levels continued to become more severe,             the pump was removed     from service and the coupling disassembled.             It was   found that all   of the   oil had   been thrown out     of the coupling.       The oil was replaced and the   pump returned to service without further problems.
New resin traps were installed and the demineralizers were successfully returned to service.
Prior to the beginning of Unit         2 refueling outage, performance checks         on both spent fuel storage pool cooling pumps for Unit               2 determined both pumps to be performing at less than       85% of their design capacities.         Both pumps were rebuilt   and subsequently     performed at greater than design         criteria.
14 0 eration Summar (Continued)
High differential     pressures were experienced on         2B reactor water clean-up filter demineralizer.         Investigation revealed that       a   failure of   the stainless steel filter elements       allowed precoat material to accumulate on the resin trap.
September 1980 E ui ment Performance (Continued)
The problem was     corrected by replacement of the         filter elements     and associated resin trap.
Problems were experienced with the condensate demineralizers on Unit 1.Failure of the filter element on vessels J and E allowed resin to accumulate on the downstream resin traps.High differential pressure across the resin traps forced replacement of the traps along with the failed filter elements.The reason for unusually short service runs on vessel 1D was investigated.
Resin traps on reactor water clean-up demineralizers 1A and                 1B were removed I
The vessel's filter elements were found to be severely fouled with iron oxide.It is believed the fouling resulted from improper precoating techniques which failed to protect the element with an over-lay of resin.The fouled elements were re-placed and the vessel was satisfactorily returned to service.Precoating records are being reviewed to determine if additional corrective action is warranted.
and examined     to determine the cause of high         differential pressure.     An accumulation of rust   was found on   the traps.     The source     of the rust is   still under   investigation.
A visual inspection was made of the Unit 2 CCW tunnel on September 17, 1980.Algae growth covering approximately 10%of the wall surface (bottom and sides)of the tunnel was noted.The floor of the tunnel was covered with silt and mud that ranged from 1/2 inch to 2 inches in thickness.
There was no     indication of problems with       filter element integrity.       New resin traps were   installed   and the demineralizers were successfully returned to service.
At the intake butterfly valves, there was approximately 1.5 ft of clams accumulated in the discharge 3 from CCH pump B.At the inlet to the water boxes, there was approximately 0.5 ft 3 of clams scattered around the tunnel floor.TIP problems on Unit 3 affected the ability to establish full power rod patterns throughout the month of August.Problems with two of the five TIP machines resulted in fewer TIP sets being run than otherwise would have been run.Detector"A" was replaced on September 22, 1980, and a PORC approved PMR was completed to eliminate problems with"D" machine.At the end of the month, all five TIP machines were operational.
 
0 erations Summar (Continued)
14 0 eration   Summar     (Continued)
September 1980 E ui ment Performance (Continued)
September   1980 E ui ment Performance   (Continued)
The plant purchased a helium leak detection instrument to check the integrity of the main condensers.
Problems were experienced     with the condensate demineralizers         on Unit 1.
The instrument was not fully operational in time to check the Unit 2 condensers at the start of the refueling outage.A leak check on the Unit 2 condenser is planned prior to the end of the outage when condenser vacuum is re-established.
Failure of the   filter element   on vessels     J and E allowed resin to accumulate on the downstream     resin traps. High   differential   pressure across the resin traps forced replacement of the traps along with the failed               filter elements.
18 0 erations Summar (Continued)
The reason   for unusually short service runs       on vessel   1D was investigated. The vessel's   filter elements   were found to be severely fouled         with iron oxide.     It is believed the fouling resulted from improper precoating techniques which failed to protect the element with an over-lay of resin.             The fouled elements were re-placed and the vessel was     satisfactorily returned to service.           Precoating records are being reviewed to determine       if additional     corrective action is warranted.
September 1980 Containment Leak Rate Tests'rimary containment penetration leak rate tests were performed during the month.The results are within technical specification limits and are listed in the following table.Leaka e (scfm T e Test Unit 1 Unit 2 Unit 3 Type A (integrated containment)
A visual inspection   was made   of the Unit   2 CCW tunnel on September 17, 1980. Algae growth covering approximately         10% of the wall surface (bottom     and sides) of the tunnel was noted.         The floor of the tunnel     was covered with   silt   and mud   that ranged from 1/2 inch to     2 inches   in thickness. At the intake   butterfly valves, there   was approximately 1.5     ft3  of clams accumulated in the discharge from   CCH pump B. At the inlet to   the water boxes, there was approximately 0.5           ft3 of clams scattered around the tunnel floor.
Type B (Drywell/torus hatches)Personnel Air Lock (X2)Equipment hatches No Test No Test Incomplete No Test 0.0011 0.2119 Type C (Isolation valves)No Test Totals 0.0 Electrical Penetration (X107B)0.0173 0.3236 0.3420 No Test 0.2119 Chan es Test and E.eriments Re uirin Authorization From the NRC Pursuant to 10 CFR 50.59 a)There was one revision to the Unit 3 Technical Specification comprised of pages ix through xxxi-EPL 1 through 22, 156, 157, 170 and 171.Inoperable time was changed from 24 hours to 10 days on standby coolant supply capability.
TIP problems on   Unit 3 affected the ability to establish         full power   rod patterns throughout the month of August.           Problems   with two of the five TIP machines resulted     in fewer   TIP sets being run than otherwise would have been run.
Chan e in Plant Or anization There was one change to the plant staff for those positions designated as key supervisory personnel positions in the Technical Specifications.
Detector "A"   was replaced on September 22, 1980, and         a PORC approved PMR was completed to eliminate problems with "D" machine.             At the end of the month,     all five   TIP machines were operational.
A Plant Shift Engineer, M-4, was selected as Plant Assistant Operations Supervisor, M-4.
 
19 0 erations Summar (Continued)
0 erations   Summar     (Continued)
September 1980 Re orts to NRC There were 23 reportable occurrences, a revision to one of these, and 2 cancelled reportable occurrences were reported to the NRC during the month.
September   1980 E ui ment Performance     (Continued)
20 0 erations Summar (Continued)
The plant purchased     a   helium leak detection instrument to check the integrity of   the main condensers.       The   instrument was not fully operational in time to check the Unit     2 condensers   at the start of the refueling outage.
September 1980 Chan es Tests and Ex eriments Not Re uirin Authorization from the NRC Pursuant to 10 CFR 50.95 (a S ecial Test-186"Scram Discharge Volume (SDV)Drain Valve Closure Pressure on Loss of Control Air-Unit 2" This test was performed to determine the control air pressure at which the SDV drain valves would drift shut on a loss of control air.It was originated to aid in the evaluation of the potential for flooding the SDV as a result of a decrease in control air pressure.STEAR 80-20"I and C Bus A and B Load Current Determination" Test involved measuring current to various branch circuits feeding from I and C bus A and B.Data was submitted to EN DES to be used in their eval-uation of the voltage reliability analysis performed for these buses.This was in response to NRC inquiries.
A leak check on the Unit     2   condenser   is planned prior to the end of the outage when condenser   vacuum   is re-established.
Plant modifications will be submitted in the annual report.
 
21 0 erations Summar (Continued)
18 0 erations Summar     (Continued)
September 1980 Primar Coolant Chemistr Unit 1 The conductivity of the reactor coolant exceeded technical specification and fuel warranty limits for a total of 30.1 hours during the month.A rup-tured tube in Cl waterbox and transients associated with Scrams 135 and 136 were responsible for the conductivity increases.
September   1980 Containment Leak Rate Tests
Chloride concentrations and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month.This calendar year the technical specifications and fuel warranty limits has been exceeded for 140.9 hours.Unit 2 The" conductivity of the reactor coolant remained within technical speci-fication,and fuel warranty limits for the month.Chloride concentration and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month.This calendar year technical specification and fuel warranty conductivity limit has been exceeded for 71.3 hours.Unit 3 The conductivity of the reactor coolant remained within fuel warranty limits during the month.The conductivity of the reactor coolant remained within technical specifications of 2.0 pmhos during the month.Chloride concentration and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month.This calendar 22 0 erations Summar (Continued)
          'rimary     containment penetration leak rate tests were performed during the month.       The results are within technical specification limits and are   listed in the following table.
September 1980 Primar Coolant Chemistr year the fuel warranty conductivity limit has been exceeded for 27.55 hours, and technical specification limit has been exceeded for a total of 1 hour.Source Test None 23 0 erations Summar (Continued)
Leaka e (scfm T   e Test                             Unit 1             Unit 2       Unit 3 Type A   (integrated containment)                 No  Test            Incomplete    No  Test Type B   (Drywell/torus hatches)                 No  Test            0.0011 Personnel     Air Lock   (X2)                                               0.2119 Equipment hatches Electrical Penetration        (X107B)                          0.0173 Type C   (Isolation valves)                       No Test           0.3236        No Test Totals    0.0               0.3420       0.2119 Chan es     Test   and E. eriments Re     uirin Authorization From the   NRC Pursuant to 10     CFR 50.59     a)
September 1980 Environmental Technical S ecification Re uirement-The raw water chlorination system was not operated during the month of September.
There was one revision to the Unit           3 Technical Specification comprised of pages   ix through xxxi     EPL 1   through 22, 156, 157, 170 and 171.       Inoperable time was changed from       24 hours to 10 days on standby coolant supply capability.
Reservoir water temperatures exceeded technical specification limits on two different days during the month of September.
Chan e in Plant     Or anization There was one change to the plant           staff for   those positions designated as key supervisory personnel positions in the Technical Specifications.
On September 28th and 29th the temperature rise was 5.1'.The average intake water temp-erature for the month was 83.6'., The largest water temperature rise was 5.1', with an average downstream water temperature of 85.3'.Approximately 700,000 gallons of water was released from the unlined pond to the Tennessee River.The pH of the release was maintained within technical specification limits of 6.0 to 9.0.Calculation of Usa e'Factor The cumulative usage factors for the reactor vessel are as follows: Location Usa e Factor Shell at water line Feedwater nozzle Closure studs Unit 1 0.00487 0.23254 0.19566 Unit 2 0.00369 0.15822'.12899 Unit 3 0.00314 0.11570 0.09194 24 0 erations Summar (Continued)
A Plant Shift Engineer, M-4,         was   selected as Plant Assistant Operations Supervisor, M-4.
September 1980 Im ortant Events September The Plant Manager and the Plant Operations Supervisor attended a briefing on Division Plan to Compensate Nuclear Power Employees and an Operator Staffing Presentation in Chattanooga.
 
The Plant Manager attended the Bi-Weekly Plant Manager Meeting in Chattanooga.
19 0 erations Summar (Continued)
879 A Plant Outage Civil Engineer and a Plant Outage Electrical Engineer attended a meeting in Knoxville, on the Post-Accident Sampling Facility.15-19 The Plant Chemical Unit Supervisor taught a chemistry and radio-chemistry course at the Power Operation Training Center for the STA's.15-30 Two Plant Chemical Engineers attended an engineering training course at the Power Operation Training Center in Chattanooga.
September 1980 Re orts to NRC There were 23 reportable occurrences,   a revision to one of these, and 2 cancelled reportable occurrences were reported to the   NRC during the month.
The Plant Manager attended a meeting in Chattanooga on recommendations from Management Training Committee for M position profile plan.The Plant Acting Compliance Supervisor attended a meeting in Chattanooga on IE Bulletin 79-01B.19 The Plant Systems, Analyst attended a meeting in Huntsville, AL., with Chattanooga Central Office personnel and PIC Systems, Inc., to review the design of the PRIME/GE 4020 link.A meeting was held at the plant between EN DES-Knoxville, personnel, and the Plant Instrument Maintenance personnel to discuss power sources for the Feedwater Control System.The Plant Outage Director attended a meeting in Chattanooga on Instrumentation Sensing Lines.20 The Plant Acting Compliance Supervisor attended the NRC Region II, meeting in Atlanta on NUREG-0660 clarifications/TMI Action Plans.22 The Plant Manager and representatives from the plant Co-op group attended a"kick-off" for combined'Federal Campaign at the Marshall Space Flight Center in Huntsville, AL.
 
25 0 erations Summar (Continued)
20 0 erations Summar   (Continued)
September 1980 Im ortant Events September 22-25 The Plant Mechanical Results Unit Supervisor, the Plant Equipment Diagnostics Engineering Associate, and a Plant Mechanical Engineer attended a Vibration Training Class in Chattanooga.
September   1980 Chan es     Tests   and Ex eriments Not Re     uirin Authorization from the     NRC Pursuant to 10   CFR   50.95 (a S ecial Test     186 "Scram Discharge Volume (SDV) Drain Valve Closure Pressure           on Loss of Control Air Unit 2" This test   was performed   to determine the control     air pressure at which the SDV drain valves would     drift shut on a   loss of control air. It was originated to aid in the evaluation of the potential for flooding the             SDV as a result of a decrease   in control air pressure.
23-24 The Plant Manager attended a Nuclear power Quality Meeting in Chattanooga.
STEAR   80-20 "I and C Bus A and B Load   Current Determination" Test involved measuring current to various branch           circuits feeding from I and   C bus A and B. Data was submitted to     EN DES to be used in their eval-uation of the voltage     reliability analysis     performed   for these buses. This was in response   to NRC inquiries.
24 The Plant Outage Director attended a Division Meeting in Chattanooga.
Plant modifications     will be   submitted in the annual report.
25 The Plant Manager and representatives from the Plant Co-op group attended the-United May"Kick-off" dinner in Huntsville, AL.30 The Plant Quality Assurance Supervisor attended a QA Supervisor Meeting at the Power Operation Training Center.The Plant Manager, the Plant Electrical Maintenance Supervisor, a Plant Shift Engineer, and two Plant Outage Electrical Engineers attended a meeting in Knoxville on Browns Ferry Nuclear Plant Under-voltage Modifications.
 
The Plant Outage Refuel Floor Coordinator attended a meeting in Chattanooga on Multi-Stud Tensioners.
21 0   erations Summar   (Continued)
Visitors September Mr.Dale Nix, Plant Engineering Staff;Mr.Frank Kelly, Reactor Engineering Staff;and Mr.C.D.Evans, EN DES-Knoxville, met with the Plant Chemical Supervisor concerning PASF and revised design criteria.Mr.Tom Hall, London Nuclear Services, was onsite to meet with the Plant Assistant Outage Director and the Plant Outage Drywell Coor-dinator, concerning chemical decontamination of CRD scram headers.Mr.Barry Smith, General Electric Customer Service Plant and AMPS, met with various plant section supervisors.
September 1980 Primar   Coolant Chemistr Unit 1 The conductivity of the reactor coolant       exceeded technical specification and fuel warranty limits for     a total of 30.1 hours during the month.       A rup-tured tube in Cl waterbox and transients associated with Scrams 135 and 136 were responsible   for the conductivity increases.         Chloride concentrations and pH of the reactor coolant remained within technical specification           and fuel warranty   limits during the month.     This calendar year the technical specifications and fuel warranty limits has been     exceeded   for 140.9 hours.
Unit 2 The" conductivity of the reactor coolant remained within technical speci-fication,and fuel warranty limits for the month.           Chloride concentration and pH of the reactor coolant remained within technical specification           and fuel warranty   limits during   the month. This calendar year technical specification and fuel warranty conductivity limit has       been exceeded   for 71.3 hours.
Unit 3 The conductivity of the reactor coolant remained within fuel warranty limits during the   month. The conductivity of the reactor coolant remained within technical specifications of 2.0       pmhos   during the month. Chloride concentration   and pH of the reactor coolant remained within technical specification   and fuel warranty limits during the       month. This calendar
 
22 0 erations Summar   (Continued)
September   1980 Primar   Coolant Chemistr year the fuel warranty conductivity   limit has   been exceeded   for 27.55 hours, and technical specification   limit has been exceeded for a total of 1 hour.
Source Test None
 
23 0 erations   Summar     (Continued)
September   1980 Environmental Technical     S ecification   Re   uirement
    -
The raw water chlorination system       was   not operated during the month of September.
Reservoir water temperatures       exceeded     technical specification limits on two   different days during the month       of September.         On   September   28th and 29th   the temperature     rise was 5.1'.       The average       intake water temp-erature for the month     was 83.6'.,     The   largest water temperature rise was 5.1',   with an average downstream water temperature                 of 85.3'.
Approximately 700,000 gallons of water was released from the unlined pond   to the Tennessee River.       The pH   of the release     was     maintained within technical specification limits of 6.0 to 9.0.
Calculation of   Usa e 'Factor The cumulative usage factors for the reactor vessel are as follows:
Location                                               Usa e       Factor Unit  1          Unit      2            Unit  3 Shell at water line                 0.00487           0.00369                0.00314 Feedwater nozzle                    0.23254                                    0.11570 0.15822'.12899 Closure studs                      0.19566                                    0.09194
 
24 0 erations Summar   (Continued)
September 1980 Im ortant Events September The Plant Manager and the Plant Operations Supervisor attended a briefing on Division Plan to Compensate Nuclear Power Employees and an Operator Staffing Presentation in Chattanooga.
The Plant Manager attended the Bi-Weekly Plant Manager Meeting in Chattanooga.
879     A Plant Outage Civil Engineer and a Plant Outage Electrical Engineer attended   a meeting in Knoxville, on the Post-Accident Sampling Facility.
15-19   The Plant Chemical Unit Supervisor taught a chemistry and radio-chemistry course at the Power Operation Training Center for the STA's.
15-30   Two Plant Chemical Engineers attended an engineering training course at the Power Operation Training Center in Chattanooga.
The Plant Manager attended a meeting in Chattanooga on recommendations from Management Training Committee for M position profile plan.
The Plant Acting Compliance Supervisor attended     a meeting in Chattanooga on IE     Bulletin 79-01B.
19     The Plant Systems, Analyst attended a meeting in Huntsville, AL.,
with Chattanooga Central Office personnel and PIC Systems, Inc.,
to review the design of the PRIME/GE 4020 link.
A meeting was held at the plant between EN DES Knoxville, personnel, and the Plant Instrument Maintenance personnel to discuss power sources for the Feedwater Control System.
The Plant Outage Director attended     a meeting in Chattanooga on Instrumentation Sensing Lines.
20     The Plant Acting Compliance Supervisor attended the NRC Region II, meeting   in Atlanta on NUREG-0660 clarifications/TMI Action Plans.
22     The Plant Manager and representatives from the plant Co-op group attended a   "kick-off" for combined 'Federal Campaign at the Marshall Space Flight Center in Huntsville,     AL.
 
25 0 erations Summar   (Continued)
September 1980 Im ortant Events September 22-25   The Plant Mechanical Results Unit Supervisor, the Plant Equipment Diagnostics Engineering Associate, and a Plant Mechanical Engineer attended a Vibration Training Class in Chattanooga.
23-24   The Plant Manager attended   a Nuclear power Quality Meeting in Chattanooga.
24   The Plant Outage Director attended   a Division Meeting in Chattanooga.
25   The Plant Manager and representatives from the Plant Co-op group attended the- United May "Kick-off" dinner in Huntsville, AL.
30   The Plant Quality Assurance Supervisor attended a     QA Supervisor Meeting at the Power Operation Training Center.
The Plant Manager, the Plant Electrical Maintenance Supervisor, a Plant Shift Engineer, and two Plant Outage Electrical Engineers attended a meeting in Knoxville on Browns Ferry Nuclear Plant Under-voltage Modifications.
The Plant Outage Refuel Floor Coordinator attended a meeting   in Chattanooga on Multi-Stud Tensioners.
Visitors September Mr. Dale Nix, Plant Engineering Staff; Mr. Frank Kelly, Reactor Engineering Staff; and Mr. C. D. Evans, EN DES Knoxville, met with the Plant Chemical Supervisor concerning PASF and revised design criteria.
Mr. Tom Hall, London Nuclear Services, was onsite to meet with the Plant Assistant Outage Director and the Plant Outage Drywell Coor-dinator, concerning chemical decontamination of CRD scram headers.
Mr. Barry Smith, General Electric Customer Service Plant and AMPS, met with various plant section supervisors.
Representatives from the Hewlett-Packard Corporation met with the Plant Chemical Supervisor to demonstrate the HP 9845 for PASF.
Representatives from the Hewlett-Packard Corporation met with the Plant Chemical Supervisor to demonstrate the HP 9845 for PASF.
0 erations Summar (Continued)
September 1980 Visitors September Ms.Marilyn Taylor, Director of Personnel, was on site to meet with employees regarding various employee concerns.Her visit was a result fo Chairman Freeman's visit in July when questions regarding personnel were addressed to him.Job surveys were performed at nuclear plant positions by members of Ms.Taylor's staff and representatives of the Division of Nuclear Power personnel office.The results of these surveys will be compared to job surveys to be performed at a fossil plant.4-5 Messrs.Ralph Thompson, Charlie Howell, and Frank Garrett, Chattanooga Industrial Safety and Fire Protection Engineering Staff was onsite to conduct an air flow test-Unit 1 Reactor Building.8-11 Office of Power Quality Assurance auditors were onsite to audit special processes and maintenance activities.
10-12 General Electric representatives were onsite to meet with the Plant Manager concerning HPCI and RCIC performance.
A 5-man team from Occupational Health and Safety was onsite to audit the outage operation.
12 Mr.Ron Westbrook, IS and FPE Supervisor, CHattanooga, was onsite for a Safety Inspection Audit Exit Meeting.15 Two NRC licensing personnel were onsite to administer reactor operator and senior reactor operator licensing examinations to 10 Browns Ferry operators.
15-18 Three representatives from PLC (Professional Loss Control, Inc.)were onsite to perform an audit of the fire protection system as required by technical specifications.
16 An NRC inspector was onsite to audit the inservice program.22-25 Representatives from the Division of Occupational Health and Safety conducted a safety audit of outage work.23 Mr.Marvin Lane, Executive Vice Pr'esident of Graver Water Company, met with the Plant Results Section Supervisor and others on the problems of contaminated powdered resins.23-26 Office of Power Quality Assurance auditors were onsite to perform an audit of document control and technical specifications.
27 0 erations Summar (Continued)
September 1980 Safet and First Aid The regular weekly safety meetings of salary policy and trades and labor groups were held this month.Accidents There were 2 loss-of-time accidents during the month of September.
NUCLEAR PLANT PERSONNEL 28 Browns Ferry Nuclear PLANT Power Plant Superintendent~
M-8 Assistant Power Plant Superintendent M 6 TITLE End of Previous Month Changes End of Present Month Records Officer SA-2 eosIMst Mechanical En ineer SD-3 S ecification En ineer SD-3 En ineerin Aide SE-2 Safety Engineer SO 3 ngzneer ng i e Sa ety SE-Su ervisor, Mana ement Services Section M-5 Su ervisor Administrative Services hbck Unit H-4~fctttsttgtttofstetocMZ Su ervisor Document Control Unit H-~otaotctNsttgLeffttttxtnTgtrimst7BItsd Su ervisor Plt Services Unit H Secretar SB.4>tlaarttISmNcgtgtPtorILM-Editor SA-2 Clerk Typist SB 3 Clerk-Typist SB 2 zfftetsofrftsfcs88.8 Clerk SB-2 Payroll Clerk SB 5 Pa roll Clerle%8Q<
Payroll ClerleSBR SB-3 File Clerk SB.3 Supervisor Services H-4 Su ervisor Qualit Assurance Stalf M 5 Qualit Assurance En ineer SO 4 Quality Assurance Engineer SO-3 Quality Assurance Engineer SO 2 Engineering Aide (Quality Assurance)
SE 5 En ineerin Aide (Quality Assurance)
SE.4 n ineerin Aide ualit Assurance)
SE-3 lerk, SB-3 ail Clerk SB-2 Power Plant Results Supervisor M.5 Assistant Power Plant Results Supervisor M4 ower Plt Maintenance Supvr (Inst)H-5 Instrument Engineer SO 4 IfecuttttgtfrBI@tttmtcs88 Personnel Clerk SB-4 otttramstBBM S stems Anal st, SD-3 enior Instrument Mechanic-Instructor Irgtmtdge8agtsrtttt~".ItttL(saacsflsft Programming Technician SE-4 Engineering Aide SE 3 Senior Instrument Mechanic Foreman Senior Instrument Mechanic Instrument Mechanic Instrument Mechanic Ap rentice-'4th Pd.Instrument I'ftechanic Apprentice-3rd Pd.ctsrssrotttuntnhtacttmt(enectprzmfeme Pthc Nord Processor SB-4 sst.Power Plt.Maintenance Supervisor (Inst)M-4 Reactor En ineer SO 4 5U@tnBmjNI@SttgO7B Clerk SB-4 Engineering Aide (Nuclear)ZSA SE-5 TAMNQNSBrp;IftmttSGAz Supervisor, Mechanical Unit M-4 Mechanical En ineer SO 3 Engineerin Aide(Statistician)BRA SE-5 ttgfotroc'otg7rtfsfm(lamISr18ntaias)ISED Data Entry Clerk SB-2 15 44 22 10 15 16 43 27 Engineering Aide (Test Bt Studies)SE.3 TVA 7037 (PP-10.77) sheer 1 M mn,r September>>80 NUCLEAR PLANT PERSONNEL 29 Browns Ferr Nuclear PLA14T T IT t.s Mechanical En ineerin Associate SE 6 En ineerin Aide (Mechanical)
SE 4 En ineerir.Aide (Mechanical)
SE-3 En ineerin Aide (Instrument)
SE.En ineerin Coo Student (N)SE.3 Enoineerin
'Coo Student OQXZSZ (M)SE-3 Supervisor Chemical Unit if-4 Chemical En ineer SO 4 Chemical En ineer SO 3 Chemical Enoineerin Associate SE 6 Radiochelnical Laboratory Analyst SE 5 Radiochemical Laboratory Analyst SE 4 Chemical Laborator~
Anal st SE 3 Engineering Coop Student (C)SRR SE-4 En ineerinn Coo Student (C)SE.2 Radiochemical Laborato Anal st-Tr SE-3 Su ervisor Reactor Unit M-4 Power Plant Operations Supervisor M 5 Assistant Power Plant Operations Supervisor M.4 Clerk SB 3 Shift Engineer M-4 Assistant Shift Engineer M-3 Assistant Shift Engineer-SR L Unit Operator Unit Operator-RL Assistant Unit Operator Student Generating Plant Operator-th Pd.tu ent eneratxng ant perator-r Clerk SB-2 Supervisor Janitorial Services i'-3 Janitor SF 3 Janitor SF 2 Janitor SF.l End of Previous Month 16 15 55 Chonoes+1-1+17-4+27-20 Eno of PfeSenl Montn 15 15 20 17 62 Power Plant Maintenance Su ervisor E M-5 Power Plant Maintenance Supervisor M 5 Assistant Power Plant Klaintenance Supervisor (E)M 4 Assistant Power Plant Maintenance Supervisor (M)M 4 General Electrical Foreman M-4 Electrical Engineer SO 4 Electrical En.ineer SO 3 General Mechanical Foreman M-4 Mechanical Engineer SO.4 Mechanicaf En ineer SO 3&rJcttacthsgtt(:cttxftfzstutstnt)Ms'echanical Engineer SD-2 En ineerin Aide (41echanical)
SE 3 Engineering Coop Student (M)SE.Xmxnnmsmmm~unx!&SR En ineerin Aide Electrical SE-Electrician Foreman Electrician Electrician Apprentice-Pd.Electrician Apprentice-1st Pd.B Electrician Apprentice-1st Pd.A 10 46+.-2 10 10 TVA 7OS7 (PP tO 77)Sheet 2 September,(0 I'JUCLEAR PLANT PERSONNEL 30 PLANT Machinist Foreman Machinist Machinist Welder Machinist A orentice-4th Pd TITLE end or Previous Month ChangeS End or Present Month Machinist Apprentice-3rd Pd.Machinist Apprentice-2nd Pd.Hachinist A I7rentice-1st Pd.B Hachinist A rentice-1st Pd.A Boilermaker Foreman Boilermaker Boilermaker Welder Boilermaker Apprentice-Pd.Boilermaker Apprentice-Pd.Sheetmetal Worker A rentice-1st Pd.A Steamfitter Foreman Steamfitter Steamfitter Welder Steamfitter Ap rentice-5th Pd Steamfitter'Apprentice-1st Pd.A General Labor Foreman H-3 Car enter Foreman Asbestos Worker Foreman ainter Apprent3.ce
-st P.A Structural Ironworker Sheetmetal Worker Foreman Sheetmetal Worker Asbestos Worker Car enter Painter Foreman Painter Heavy Equipment Operator-Power Labor Foreman Nuclear Plant Laborer Truck Oriver I Sign Painter Total Annual Salary Policy Total ATL Operations Total ATL Maintenance 24 12 23 233 112+67-33+7-13 12 23 267 106 Total Plant 660+91-60 691 Hourly-List Titles Car enter 23 Car enter 1 Construction Laborer 71 Hortar Hixer 1 Boilermaker (10)Hach Wldr (1)Steamfitter 15 Hach 28 Bricklaver 1 Painter 13 Asbestos Worker 2 Crane 0 erator 2 Sheetmetal Worker 3 Truck Driver I 2 Total Hourly 63 20 152+12 26 TVA 7037 (PP.10.77)
Sheet 3 Month or 0 L 31 Se tember 1980 Personnel Chan es-Annual Name Title Effective Date Betty J.Grimes Billy J.Allen Kenneth E.Howard Richard L.Ingram William C.Jones, Jr.Arthur L.Littleton Jose I.Lozano Michael E.Maples Margaret L.Reach Larry D.Smith Jack W.Vinson Barbara L.Weigart Randall L.Keeton Dennis M.Castell Wayne E.Guthrie M.Neil Haraway Kenneth D.Sylvester Gary R.Cobb Janitor F01 Janitor F01 Janitor F01 Janitor FOl Janitor FOl Janitor FOl Janitor F01 Janitor F01 Janitor FOl Janitor F01 Janitor F01 Janitor F01 Janitor FOl Janitor F01 Janitor F01 Janitor F01 Janitor FOl Janitor F01 09 02 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 03 80 09 04 80 09 05 80 09 05 80 09 05 80 09 05 80 09 08 80 32 Se tember 1980 Personnel Chan es-Annual Name Title Effective Date Russell B.Huffman Willie M.Jenkins Robert L..Rice Nicholas L.Austin Thomas I.Vines Robert C.Murphy Charles Crawley James R.Hine Harlon L.Ramsey Janitor F01 Janitor F01 Janitor F01 Janitor F01 Janitor FOl Janitor F01 Janitor F01 Janitor FOl Janitor F01 09 08 80 09 08 80 09 08 80 09 09 80 09 09 80 09 10 80 09 11 80 09 15 80 09 17 80 B.Reclassifications Name Former Title New Title Effective Date Rickey E.Holtzclaw James C.Hall Danny L.Tuggle Wendell K.Holt Kenneth W.Brown Timothy D.Lane Linda G.Murphy SGPO-4th Pd SGPO-4t}1 Pd Inst Mech AP3 Elect APlA Elect APlA Inst Mech AP3 Elect APlA Asst Unit Op Asst Unit Op Inst Mech AP4 Elect AP1B Elect AP1B Inst Mech AP4 Elect AP1B 07 23 79 10 01 79 06 23 80 07 21 80 08 04 80 08 04 80 08 04 80 33 Se tember 1980 Personnel Chan es-Annual B.Reclassifications (Continued)
Name Elizabeth L.White Kenneth E.Davis Tony D.Hill Patricia F.Roland Lona C.Belue Roger D.Shireman Former Title Elect AP1A Elect AP1A Elect AP1A Inst Mech AP3 Clerk B03 Radiochem Lab Anal E04 New Title Elect AP1B Elect AP1B Elect APlB Inst Mech AP4 Effective Date 08 11 80 08 18 80 08 18 80 08 18 80 Radiochem Lab Anal E05 08 24 80 Word Processor B04 08 24 80 James A.Green Asst Shft Engr M03 James S.Watson Thomas M.Thompson Lardell Goodloe, Dan C.Barger Martha C.Barnett Nellarene P.Cobb Larry W.Cole Leonard A.Cole Michael W.Davis Helen J.Franklin William C.Freeman Elect (H)Elect (H)Elect (H)Janitor FOl Janitor F01 Janitor F01 Janitor F01 Janitor FOl Clerk B02 Janitor F01 Janitor F01 Robert E.Stone, Jr.Inst Mech AP3 Sup, Janitorial Servs M03 Inst Mech AP4 Elect Elect Elect Janitor F02 Janitor F02 Janitor F02 Janitor F02 Janitor F02 Clerk B03 Janitor F02 Janitor F02 08 31 80 09 01 80 09 01 80 09 03 80 09 04 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 34 Se tember 1980 Personnel Chan es-Annual B.Reclassifications (Continued)
Name Former Title New Title Effective Date James O.George Bobby F.Grizzard David S.Haney Robert L.Ingram Martin Johnson John W.Maynor, Jr.Morris W.Morell William L.Sandy Burl D.Stark Janitor F01 Janitor F02 Janitor F01 Janitor F02 Janitor F01 Janitor F01 Janitor F01 Janitor F01 Janitor F02 E.Jane Wilkerson Janitor FOl Thomas L.Williamson Janitor FOl Robert E.Woods Janitor FOl Garfield J.Taylor, Jr.Sr Inst Mech Inez H.Bedingfield Janitor F01 Austin L.,Burnette Shft Engr H04 Janitor F02 Janitor F03 Janitor F02 Janitor F03 Janitor F02 Janitor F02 Janitor F02 Janitor F02 Janitor F03 Janitor F02 Janitor F02 Janitor F02 Sr Inst Mech Fmn Janitor F02 Asst Pr Plt Op Sup M04 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 07 80 09 08 80 09 21 80 09 21 80 David T.Davis Herbert L.Johnson Inst Mech AP3 Qual Assurance Engr D02 Inst Mech AP4 Qual Assurance Engr D03 09 21 80 09 21 80 Donell King Richard W.Shultz Ardie R.Champion James C.Coz Janitor F01 Inst Mech AP3 Unit Op RL Unit Op RL Janitor F02 Inst Mech AP4 09 21 80 09 21 80 Asst Shft Engr M03 09 29 80 Asst Shft Engr M03 09 29 80.Willard B.Dawes, Jr.Asst Unit Op Unit Op 09 29 80 35 Se tember 1980 Personnel Chan es-Annual B.Reclassifications (Continued)
Name Former Title New Title Effective Date Johnny E.Duke Russell R.Eades Charles B.Fisher Steve R.Gray Charles G.McClain Marvin L.Meek Michael V.Hiller Asst Unit Op Asst Unit Op Asst Unit Op Asst Unit Op Unit Op RL Unit Op RL Unit Op RL Unit Op Unit Op Unit Op Unit Op 09 29 80 09 29 80 09 29 80 09 29 80 Asst Shft Engr M03 09 29 80 Asst Shft Engr H03 09 29 80 Asst Shft Engr M03 09 29 80 C.Transfers Out Name Former Title James L.Turner Radiochem Lab Anal E04 Jeannette Y.Johnson Clk B02 New Title Clk B02 Chemist-D01 Place TQ OCH&S Trng Ctr Effective Date 09 07 80 09 21 80 D.Transfers In Name George N.Veal David E.Newton Former Title Shmtl Qcr Elect New Title Shmtl Wkr Elect Place From W Creek Service Shops Effective Date 08 25 80 09 02 80 Michael N.Brown Radchm Lab Ana Tr E03 Radchm Lab Ana Trng Ctr Tr E03 09 21 80 James tJ.Burton III Chem Engr D02 Chem'Engr D03 Ctl&Test 09 21 80 B.Joan Chandler Clk B02 Data Engry Op B02 P&Svs 09 21 80 36 Personnel Chan es-Annual D.Transfers In (Continued)
Former Name Title Se tember 1980 New Title Place From Effective Date Edward J.Frederick Radchm Lab Ana Tr E03 Radchm Lab Ana Trng Ctr Tr E03 09 21 80 Aaron J.Goode Radchm Lab Ana Tr E03 Radchm Lab Ana Trng Ctr Tr E03 09 21 80 Albert M.Reynolds Radchm Lab Ana Radchm Lab Ana Trng Ctr 09 21 80 Tr E03 Tr E03 E.Return From LWOP Name Title Effective Date Brian E.Williams Engg Coop Student E03 (M)William B.Pendergrass Engg Coop Student E02 (C)Theresa M.Pickney Engg Coop Student E04 (C)09 02 80 09 08 80 09 08 80 F.Placed On LWOP Name David A.Robeson Title Engg Coop Student E02 (C)Effective Date 09 08 80 G.Terminations Name Fred Fraser Betty J.Grimes Harlon L.Ramsey Randall C.Arnold John D.Quigley Joe E.Rice Title Janitor F02 Janitor F01 Janitor F01 Elect Elect Unit Op RL Effective Date 09 02 80 09 09 80 09 10 80 09 15 80 09 15 80 09 19 80 37 Se tember 1980 Personnel Chan es-Houri Name J.R.Daniel Title Mach Robert W.Daniels Mach Jimmy D.Dean Jimmy W.Embry Billy J.Emmons William E.Griggs Harry F.Hacker Bennie D.Stults Thomas M.Thompson Harold F.Wilson Mach Stftr Stftr Mach Mach Mach Elect Stftr Jack D.Gaston Lardell Goodloe Stftr Elect Charles W.Warhurst Mach Bill C.Thornton Edwin R.Warren Morris G.Brown Earnest E.Cosby William H.Draper James P.Fields Leon Pope Stftr Mach Cons Lbr Cons Lbr Cons Lbr Cons Lbr Cons Lbr Willie T.Eggleston Stftr Effective Date 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 02 80 09 03 80 09 03 80 09 03 80 09 03 80 09 04 80 09 04 80 09 05 80 09 05 80 09 05 80 09 05 80 09 05 80 38 Se tember 1980 Personnel Chan es-Houri e Name Title Effective Date Loyd C.Canon James J.Cashion Jimmie 0.Garrett A.D.Jackson Cons Lbr Cons Lbr Cons Lbr Cons Lbr Kenneth R.Smith Esadore Meeks Albert S.Smith Mach Cr Op Mortar Mixer Thomas F.Schemeltz Cons Lbr James J.Smothermon Cons Lbr 09 05 80 09 05 80 09 08 80 09 08 80 09 08 80 09 09 80 09 15 80 09 17 80 09 30 80 B.Reclassifications Name James S.Watson Thomas M.Thompson Lardell Goodloe Former Title Elect Elect Elect New Title Elect (A)Elect (A)Elect (A)Effective Date 09 01 80 09 03 80 09 04 80 C.Transfers Out None D.Transfers En None 16 0 erations Summar (Continued)
September 1980 Chan e in Procedure There were 54 revisions to plant instructions during the month.47 instructions were changed primarily for corrections.
The remaining 7 revisions related to the safe operation of the plant.Chan e in Facilit Desi n All changes in facility design will be included in the unit outage summary report.
0 erations Summar (Continued)
September 1980 Surveillance Testin Unit 1 A total of 478 surveillance tests were completed on Unit 1 per 151 different test instructions.
Unit 2 A total of 205 surveillance tests were completed on Unit 2 per 95 different test instructions.
Unit 3 A total of 328 surveillance tests were completed on Unit 3 per 115 different test instructions.
39 Se tember 1980 Personnel Chan es-Houri E.Terminations Name Title Effective Date Gary D.Nichols Charlie E.Keener Lloyd W.Guthrie Johnny Norton Harty F.Hacker Hach Cons Lbr Carpenter Mortar Mixer Hach Leslie L.Abernathy Cons Lbr 07 15 80 08 27 80 09 04 80 09 16 80 09 22 80 09 29 80 40 Date Time 9/01/80 0001 1341 1736 2025 2230 2343 Si nificant 0 erational Events Unit 1 Event Reactor thermal power.at>99%, steady state control rod sequence"A".Reactor Scram No.135 from>99%on turbine stop valves closure, due to water causing a short in pressure relay 62-C1, which caused relay KT 303 to trip turbine.Commenced rod withdrawal.
Reactor Critical No.156.Rolled T/G.Synchronized generator, commenced power ascension.
9/02/80 1500 9/03/80 0040 1939 2030 Commenced PCIOHR from 82%thermal power.Reactor thermal power at 95%, holding due to"C" string high pressure heaters isolation due to relief valve flange leak."C" string high pressure heaters maintenance completed and heaters placed in service.Resumed PICOHR from 95%thermal power.9/05/80 1500 9/07/80 0015 0230 0705 0905 Reactor thermal power at 99%, maximum flow.Reduced thermal power from 99%to 85%for turbine C.V.tests and SI's.Turbine C.V.tests and SI's completed, commenced power ascension.
Commenced PCIOHR from 95%thermal power.Reactor thermal power at>99%, steady state.9/10/80 1500 9/12/80 2100 Reactor thermal power at>99%, steady state.Reduced thermal power from>99%to 50%for control rod sequence exchange from"A" to"B".9/13/80 0205 2130 Control rod sequence exchange from"A" to"B" completed, commenced power ascension.
Commenced PCIOHR from 82%thermal power.9/14/80 2300 9/16/80"1843 1905 2030 2300 Reactor thermal power was>99%, steady state.Reduced thermal power from>99%to 90%for removal of"A" circulating water pump to allow stop log lA1 to be lifted."A" circulating water pump placed in service, (mode to cooling towers would not operate due to stuck gate), commenced power ascension.
Commenced PCIOHR from 95%thermal power.Reactor thermal power at>99%, steady state.
41 Date Tillle Si nificant 0 erational Events Unit 1 Event 9/19/80 2230 Reduced thermal power from>99%to 77%for removal of"B" reactor feedwater pump for maintenance (excessive vibration).
9/20/80 0216 0315 1220 1225 2030 Reduced thermal power from 77%to 70%for turbine C.V.tests and SI's.Turbine C.V.tests and SI's completed, commenced power ascension.
Reduced thermal power from 77%to 50%due to loss of unit preferred power, when shutdown board power supply was trans-ferred.Commenced power ascension.
Commenced PCIOIR from 80%thermal power.9/21/80 1550 9/24/80 2222 Reactor thermal power at>99%, steady'state.
Reactor Scram No.136 from>99%thermal power on load re-(1)ject trip from negative ground on main transformer sudden pressure relay circuit.9/25/80 0530 0820 1038 1107 2110 Commenced rod withdrawal.
Reactor Critical No.157, sequence"B".Rolled T/G.Synchronized generator, commenced power ascension.
Commenced PCIOIK from 67%thermal power.9/27/80 0015 0125 1500 Reduced thermal power from 99%to 85%for turbine C.V.tests and SI's.Turbine C.V.tests and SI's completed, commenced PCIOMR.Reactor thermal power at>99%, steady state.9/28/80 1500 9/29/80 0115 Reactor thermal power at>99%, steady state.Reduced thermal power from>99%to 85%for backwash and precoat condensate demineralizers.
9/30/80 2400 Reactor thermal power at 85%, holding for condensate de-mineralizer problems.
42 Si nificant 0 erational Events Unit 2 Date Time Event 9/01/80 0001 1500 Reactor thermal power at 92%, EOC-3 coastdown control rod sequence"B".Reactor thermal power at 90%, EOC-3 coastdown.
9/04/80 1500 9/05/80 2130 2247 Reactor thermal power at 89%, EOC-3 coastdown.
Commenced reducing thermal power from 89%for refuel shut-down (EOC-3).Reactor Scram No.109 (manual)from 35%thermal power to accommodate refueling outage.9/12/80 1320 1650 Received permission for fuel movement operation, holding due to communication porblems.Communications restored, commenced fuel movement operation to accommodate LPRM maintenance.
9/19/80 1000 9/30/80 2400 Commenced core fuel shuffle operations.
Refueling operation in progress.
43 Date Time Si nificant 0 erational Events Unit 3 Event 9/01/80 0001 1455 1522 2055 2200 Reactor thermal power at>99%, steady state control rod sequence"A".Reduced thermal power from>99%to 63%due to"A" recir-culation pump trip from a spurious trip.Reduced thermal power from 63%to 54%due to"A" recircu-lation pump being out-of-service."A" recirculation pump maintenance completed and pump placed in service, commenced power ascension.
Commenced PCIOMR from 75%thermal power.9/03/80 1500 9/07/80 0230 0330 0430 1500 Reactor thermal power at>99%, steady state.Reduced thermal power from 99%to 75%for turbine C.V.tests and SI's.Reduced thermal power from 75%to 67%due to MSIV-1-26 closing too fast (~1.3 seconds).Turbine C.V.tests and SI's completed, holding at 67%due to MSIV 1-26 being left in closed position, awaiting maintenance.
Increased reactor thermal power from 67%to 75%, holding due to closure of MSIV 1-26.9/10/80 1500 Reactor thermal power at 75%, holding due to MSIV 1-26 being closed.9/12/80 2245 2355 Commenced reducing thermal power from 75%for shutdown for MSIV 1-26 mainte~y~ce.
Reactor Scram No.88 (manual)from 35%thermal power to accommodate maintenance to MSIV 1-26.9/14/80 0525 1009 1706 2233 2243 Maintenance to MSIV 1-26 completed, commenced rod with-drawal.Reactor Critical No.98.Reactor was made subcritical due to a feedwater valve (3-219A)leak.Repairs to feedwater valve 3-219A completed, commenced rod withdrawal.
Reactor Critical No.99.9/15/80 0155 0233 1600 Rolled T/G.Synchronized generator, commenced power ascension.
Commenced PCIOMR from 76%thermal power.
44 Si nificant 0 erational Events Unit 3 Date Time Event 9/16/80 2330 Reactor thermal power at 92%, maximum flow, awaiting rod,pattern adjustment load drop.9/17/80 2300 Reactor thermal power at 91%, maximum flow, awaiting rod pattern adjustment load drop, 9/18/80 0700 9/20/80 1358 2230 Reactor thermal power at 90%, maximum flow.Reactor Scram No.89 from 90%thermal power, on loss (1)of preferred power when"A" 480 volt shutdown board failed to transfer back to normal causing loss of"A" RPS MG set.Commenced rod withdrawal.
9/21/80 0104 0440 0500 1500 Reactor Critical No.100.Rolled T/G.Synchronized generator, commenced power ascension.
Commenced PCIOMR from 67%thermal power.9/22/80 2240 9/23/80 2145 2255 2300 Reactor thermal power at 90%, maximum flow.Reduced thermal power from 90%to 75%for control rod pattern adjustment.
Control rod pattern adjustment'ompleted, commenced power ascension.
Commenced PCIOMR from 82%thermal power.9/24/80 0725 2130 Reactor thermal power at 93%, holding due to computer malfunction.
Computer back in service, resumed PCIOMR from 93%thermal power.9/25/80 0200 1500 9/27/80 0130 0217 0300 1200 Reactor thermal power at 99%, maximum flow.Reactor thermal power at 98%, maximum flow.Reduced thermal power from 98%to 80%for turbine C.V.Tests and SI's.Turbine C.V.tests and SI's completed, commenced power ascension.
Commenced PCIOMR from 90%thermal power.Reactor thermal power at>99%, steady state.9/30/80 2400 Reactor thermal power at>99%, steady state.Equipment Malfunction (1) 45 Plant Instruction Revisions Cate or September 1980 Instruction Reason for Re uest Change in Facility Design EHI-46 Freeze Protection Program SI 4.2.A.6 Primary Containment and Reactor Building Isolation Instrumentation Low Pressure Main Steam Line To include heat tapes at cooling tower.Junction boxes have been added for test purposes.SIHI-3 System Instrument Maintenance Index 3-Instruction Reactor Feedwater System Density compensation removed per ECN P-0130, DCR 1533, workplan 9870 for Unit 2 only.SIMI-46 System Instrument Maintenance Index 46-Instruction Feedwater Control System Pressure compensation removed per ECN P-0129, DCR 1532, workplan 9838 for Unit 2 only.Change Required to Improve the Safety of Operation EMI-44 Reactor Protection System Scram Solenoid Relays EMI-80 Maintenance of Inboard and Outboard Drywell Leak Detection Isolation Valves To implement DPH N 80 Ml, which requires an inspection of the movable contacts for a possible binding problem.Recurrence control for LER 50-259/8040.'TI-23A Refueling Test Instruction 23A, Feedwater System When controlling in"A" water level sensor element in case of 250 VDC normal supply failure.
46 Re ortable Occurrences BFRO Occurrence Date Descri tion Unit 1 50-259/8060 8/14/80 While performing SI 4.2.B-60, thermostat TS-64-73 for"B" core spray pump area cooler fan was found set above the technical specification limit.50-259/8061 8/14/80 While performing SI 4.2.B-57, a thermal overload on the breaker for 1A RHR area cooler fan was found tripped.50-259/8063 8/20/80 While performing SI 4.8.B.4.2, CAM 1-RM-90-251 for the turbine building vent was removed from service for a period exceeding one hour.50-259/8064 8/20/80 While performing SI 4.8.B.4.2, CAM 1-RM-90-249 for the turbine building roof vents was removed from service for a period exceeding one hour.50-259/8065 8/28/80 Wind direction at elevation 887 M.S.I.failed.The LCO to restore the inoperable channel to operating status within 7 days was exceeded.50-259/8066 9/02/80 Operations personnel observed an annunciation on the torus hydrogen containment atmospheric monitoring.
50-'259/8068 9/01/80 Inspection of the fire protection system by a qualified fire consultant was not per-formed within the 3 year interval as required by Technical Specification 3.11.E.2.50-259/8069 9/02/80 While performing SI 4.2.A-17, channel B of"refueling zone isolation static pressure permissive and static pressure logic systems units 1, 2, and 3" modulating damper 0-PDC 64-8 failed to close.50-259/8070 9/19/80 During a review of Unit 1 core verification video tape bundle TY 582 at core location 11-06 was found to be 90'ut of proper orientation.
47 Re ortable Occurrences BFRO Occurrence Date Descri tion Unit 2 50-260/8033 8/15/80 50-260/8034 8/15/80 During routine test TI-36A an indicated leak was found on RHR heat exchanger 2B.During a routine test TI-36A RHR heat exchanger 2C was found leaking.50-260/8035 8/30/80 Test personnel detected an increase in pressure on the shell side of RHR heat exchanger 2D while performing TI-36A, RHR heat exchanger leak test.50-260/8036 8/29/80 During normal operation while performing SI 4.7.H, the H H-76-39 hydrogen monitor for the drywell would not calibrate.
50-260/8037 9/14/80 Fuel assemblies TZ 758 in core location 15-26 and TX 399 in core location 29-28 were found to be rotated 90'rom their correct orientation.
50-260/8038 9/11/80 With the unit in cold shutdown during a scheduled refueling outage, HPCI check valve 2-73-609 failed the local leak rate test.Unit 3 50-296/8031 8/09/80 During the performance of 1'RI 303 it was found that the EECW flow was below the minimum allowed flow on 3B RHR pump seal heat"exchanger.
50-296/8032 8/25/80 While performing RCIC steam line space high temperature SI 4.2.B-32, lead wires were accidently pulled out of the RCIC speed feedback magnetic pickup connector.
50-296/8033 8/15/80 During routine test TI-36A, a leak on RHR heat exchanger 2B was indicated.
50-296/8034
'/29/80 While investigating overload setting for RHR area cooler fans, the overload for 3A RHR pump area cooler fan was found to be set too high.When the overload was adjusted to the proper setting, the overload relay failed causing the fan to trip.50-296/8035 9/Ol/80.The"A" reactor recirculation pump tripped.The 24 hour LCO for one pump operation was initiated I,'Technical Specification 3.6.F.1).
48 Re ortable Occurrences BFRO Occurrence Date Descri tion Unit 3 50-296/8036 9/04/80 While running SI 4.9.A.l.a after SEMI-18 had been performed, it was found that diesel generator 3A would not trip to idle speed from a loaded condition.
50-296/8037 9/09/80 50-296/8038 9/07/80 During normal operation, while performing SI 4.7.H, H2M-76-39 would not calibrate.
While running SI 4.7.D.l.b.2 with unit at 99%steady state power, main steam isolation valve FCV 3-1-26 closed too fast.
Primar Coolant Chemistr Parameter 1.Gross Radioactivit September 1980 Unit 1 Unit 2 Unit 3 a.Crud on 0.45 millipore filter (uCi/ml)High Low Average b.Filtrate (uCi/ml)High Low Average 2.Sus ended Solids 3.98E-03 5.00E-04 1.22E-03 4.01E-01 1.13E-01 1.79E-Ol 8.68E-03 3.60E-05 1.47E-03 1.56E-01 1.60E-03 3.29E-02 5.32E-03 4.64E-04 1.12E-03 2.36E-01 6.47E-02 1.26E-01 Stained 0.45 milli ore filter (b High Low Average 3.Gross Tritium 25<10<10<10<25 10<10<10 (uCi/ml)High Low Average 1.44E-03 1.14E-03 1.27E-03 1.17E-03 9.88E-04 1.04E-03 2.18E-03 1.53E-03 1.81E-03 4.Iodine-131
~(uC i/ml High Low Average 1.02E-03 1.89E-04 6.88E-04 1.92E-03 3.43E-05 5.01E-04 7.64E-03 2.07E-05 1.75E-03 (1)Unit down 50 Primar Coolant Chemistr (Continued)
September 1980 Parameter (Continued) 5.Ratio of Unit 1 Unit 2 Unit 3 Todine-131 to iodine-133 6.Chloride (ppb)Limit 100 High Low Average 4.33E-01 1.02E-01 2.13E-01 1.72E+02 3.45E-01 4.93E+Ol 1.32E+01 3.33E-01 2.64E+00 High Low<50<50<50<50<50 Average<50<50<50 Limit 5.6 or 8.6 High Low 6.7 6.0 6.7 5.7 7.0 5.8 Average 8.Conductivit (umho/cm 8 25'eratin Limit 1.0 umho/cm Shutdown Limit 10.0 umho/cm High Low 6.4 C.)8 25'.)8 25'C.2 8(1).36 6.3 2 4(l).38 6.2 2 4(l).15 Average.72.81.53 Unit down (1) l<V IIII R<.t<<<n<~I I I~n y n I<~<~<~II~I I vs~4~L<~ww we<nv<<n<<<.,~~vv<<w GX:~J'::~%II~Ag PIII I<0 III II~.L CRAPII I*PC R 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 IO 0 0 0 I 00 rn<O H o H.CII M<<r 0: 0.-a--C H O" H--<<r 0: H 0-M 45-D=-O W-A-0 0 A.=0-H H H--ps A-0 a CA W H O H.gl-0-C"-W 0 0."~P OC CII+MW 04 PI1 CI$CO H W CII Cll CQ xa-am O CII CI1--o O=H lcl=0 O CII O 0'=0=a: H'O Pn On io ln A g 0 8 CII A H A o~\, M 0 rn 4 5 6 7 8 9 10 11 12 13 11 15 16 17 13 19 20 21 22 23 24 25 26 27 28 29 30 31 tv1ONTH OF September 19 80 13hSl:.1)111'ON NTDNI'Cll'I'lll Hl';1'1'.8 ill:hl)l'NCS
~V, I F F~~~~~(c'Coi@j+CIIAPII PAPUA tIIIIIO IA II,J,A I 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 AC UHU ATE ER GE cf:19 f 80.F-AC UMV D-ER GE.C'/K9 0=55-I 2 3 4 5 6 7 8 9 10 I I 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 i V i4I L~I~L Alai~~i 1 A~(.CX 1: till IEO Ii Il,S,i, Ct<At'N pAVCll 2 3 4 5 6 7 8 9 10 11 12 13 14 I 5 16 17 19 19 20 21 22 23 24 25 26 27 28 29 30 31 n 0-=IK n 0 0 I V.OQ 2 3 4 5 6 7 8 9 IO 11 12 13 14 19 16 17 1 il 19 20 21 22 2 3 24 25 26 27 28 29 s0 31 MONTH QF September igloo BASED UPON kfIDNIGllT NW HETER READINGS tw alE I\~I Hvl IN U1 tkh14~Iw@tIIIaly (cCoQd~>s"~
Cll*PI~PAPEA ICI~IID III II, C,J 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 AC LAT'D.GE VERA c/y 191 79.5)U.-ACC LAT VERA'D.A GE c-/--19 80-68.2)-C ft'LA 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 4 I I<<a 8 f 4 dC EC C<<I~~Unit 3 AVERAGE DAILY GROSS CAPACITY FACTOR 4 C CI I~4411!~}!hj~~~>>afja il i jj>>'I}j}a'~I h!jt}<ll i!, l jhft~hfdf If I''!),hj LIMITED>>FLO OD'ENEI I.l ND SI'S jl!I S AA I 4 TEST TURB!,'l It l" I h I~l jlh}at f" jfr h~W(OD~~f i~h'lf hi>>I}'i ft I, MPi,FL I'i af k L'IIif TED k,~I I ER II!'h UT I E!TO CO If<<I'ICE ERV PCI'HO DINGf,D N AIJUS ak~I}'>>h jt 4 ROL, ROD*PATTER fE I CO/>>I}lh~I IOIhfR':Dl I~l l I I 0ER ASCE I I 4 I'I'I h NS ION 4 3561 HOU*~ll h h i I SCIM k~tljl" Ill!>>l'.I h",Ij~I f!hi<<alt I~~f l WIi I~I L'IIh P NEE OW l(ROQ DED fETED OAD IMUEEI'L DRO~hh', ,, 1!!I<<I fR}''PCIO~'j'!l}POWER NSION ASC , ath'II l'lf fjt;hh~i f, rjj(jf}fi j>>I~~..if.i:~,~~MAINTENANCE TO MSIV 1 h'.'f I I!f,~~I'l SCRAM AT 2'355 HOURS 14~fk",,,'C fl.'i I i 4 I I 4 hfll I I I h~'.C j'It I 4 I-I II.Ikf Il:;II}~i i!1>>MSIV 1>26 OUT'0R , h I I IW I,I~!MAIN TEN TURBIN)CVITESflS'A i'i$J~-A~QUX WQ~j l I!vljl ND'I'a I~TC INXXNANC;i''.,'i i.a~l ill.I>>ki li 4 IMU~if FLOW (ROD LIMITE D)PCIOlhfR~I If~'I 4 f NCE T FOR HAINTENAA I I AI'E'CIRCULATION PUMP 0~~I I days unit on cooling tower (helper mode)<<Indicates 4 ,h RS~~I}~f f ,-hk I Qh CC n k<<I f'=o 00 Gh (c='hf I g fhf 4J tWte fhh cn A 0}-y 0 Ch 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 ED.AVE G SO'.(SJ CUE.A ED AV iAG i~C y-l 79 (-5=7.SO A O A 2 3 4 5 6 7 8 9 10 I'I 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 MQNTH QF Se tember]g SO C' 35/7 RRDHRSTE tIONTIILY AVERAGE DISCIIAR RATE/T RL ACTIVITY DISCtlRRSED FLOH RATE}II EH~RK.G BYE~IB.H LQH~2.2 I8/2 RCT I V ITY BCT I V ITY 2.e BVG~H.B LQH~H.I 7.8 RRDHASTE SYSTEH THROUGHPUT CEALLOIIS~HG)
HRSTE 5065YSTEII RHETT HIGH~7.6 RVG~K.H LOH<2.I.8 FLOOR DRAI 8 F FLOOR DRRIh'IGH>>
2.8 BVG~I.H LOW~H.H l.8.8 a.a l8.8 T RRDHRSTE-tlat<<P~
RRTIIIG COSTC$<<E43)T HASTE 7 tiONTII R 0 III TOTRL COST T TOTAL HlEH~63.ll BVG~W.H LGH~KI.3 5!RSTE H I EI<~IK.7 BVG~2K.H LGH>>3.2 FLOOR DHRIN BIEII~39.8 BVG~IB,H LOW~G.S HUILDINE RND STRCI MONTHLY RELERSE RRTES SEPTEMBER IBHI/I SEPTEtlHER ISOH PREVIOUS II IIISTAttTAttEOUS PLOT AttCE/Stt I f'T 20L'20 BUILD lltG A ISO!4 AUILDltlS AVG=GUILDIIIG LQII 4 STACK tl!GI!4 STACK AVG=STACK LOII~!SAI.CH'l33.99 7l.00 IS!7I.CH 3HSH.S3 S20.00 2'Vtl.20 B!.GO Gl.GH 23232.00 3!l2.3fl l32.30 I SHOO AICROCURIES SEC/I!HO ADDED TO ALL OUILDltlG VALUES~~~4~4 4 4 4~4~"'4 F 4>4~4 4~~g g 4 4+1 4 4~4 4 I-4-4-1 4-4-4-4-4-r4-)-4-r4 4-4 4 4~4444!IAllll 4 Si I 4~4 4 IC I 4 i'I C IH IS 20 2S 3 el l I 4 TECHNICRL 5PECIF ICRTIGN CGHPRRI5GN HUILDINE RND STRCK RELER5E BHTE5 5EPTEI"IHER IBEIB I ttSTfitITBIIEOUS PLOT ONCET'SII II T SEPTEtlGER IBQH PI!EVIOOS I I t!I I.G lll GH~I.'I7 at.78 BVG a>>!I.SII'OM~S.I2.II 2 I.al O.'I I!I JI, a...a...a.-.a.a.a a=a~~a I-DIIYS I!>>l I~I!II I~I~L~I LI If>>L~I l I~~>>a~


rs cnemis les cn 0 teselIO Im Is~S.A I 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 10 A o 9 0 9 50 2 e 3~6.'-7 0-l-Re cto zan f~l-pP s tI'-11 a':1iP ue'Iles e co te'I binI.Ie pro~l~.ec:.V: Tu 01 Fu I IAI c t ra a te tur.in go tao an:lie te s tea ts ne equ ain'e n ang=SI 3 s ll tao eju uti>p HlP nc 11.B at'<<p U OU Dg eed t~PU CC 5 po pre-'H 0 ra r.e r-a man p3=n ca 0 r-o i.t oa n++ro n)=.f se of.se b 11 0 j ec eke 2 3 4 5 6 7 8 9 10 I I'12 13 14 15'16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 MQNTH Qg September Ig 80 C N 4 f'i i I'A I'L'il 1 2 3 4 5 6 7 8 9'10 11'12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 IO-2-;4-:Co e act e n:Rqf u esca-B a'co'ce'in re eo std:--sh era..OU e-E wn td taj 1g, el: wn.=(e sh f or-OC=-Er EH-re ma)-..uel ng oui).=.Cy APP le" Eered-C=Eu it)-LP e'pPs ce len 70 A o/0 Q 20 2 3 4 5 6 7 8 9 10 11 12 13 14 15.16 17 18'19 20 21 22 23 24 25 26 27 28 29 30 31 MONTH O SeP tember 19 80
0 erations    Summar  (Continued)
<<A':5 A'I ONA 0>~0A m<01~55<5150 lm U,c, 5, 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 6 27 28 29 30 31<0 1.0~0 50 50 0 O H 50 50:l'2=3-Tj uel b ur ecz;pr ne rcupL CQI es s-a ori.pum em'IIm.on'j:.l.A-00"-5:1 SIV 1-.6=1 sL'.1 SU I.I.:.6':.I-RR=T'ld amm eac ue1 ng OV pr.du dM V:1 26.(ma 88.1ng+Scr GO I PN-~tO,-dit on.be.V.ua7 US ng: Jg o ed.i.n ce----.J.O-l'l-=l2 axi eac ont lunl or ol-s44p r.od m-.pa tel nL omp lte 5.-0--S rvi I 2 3 4 5 6 7 8 9 10 11-12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 MONTH OF~Sptkmmer 10 80  
September  1980 Visitors September Ms. Marilyn Taylor, Director of Personnel, was on site to meet with employees regarding various employee concerns. Her visit was a result fo Chairman Freeman's visit in July when questions regarding personnel were addressed to him. Job surveys were performed at nuclear plant positions by members of Ms. Taylor's staff and representatives of the Division of Nuclear Power personnel office. The results of these surveys will be compared to job surveys to be performed at a fossil plant.
4-5    Messrs. Ralph Thompson, Charlie Howell, and Frank Garrett, Chattanooga Industrial Safety and Fire Protection Engineering Staff was onsite to conduct an air flow test  Unit 1 Reactor Building.
8-11   Office of Power Quality Assurance auditors were onsite to audit special processes and maintenance activities.
10-12   General Electric representatives were onsite to meet        with the Plant Manager concerning HPCI and RCIC performance.
A 5-man team    from Occupational Health and Safety was onsite to audit the outage operation.
12    Mr. Ron Westbrook, IS and FPE Supervisor,      CHattanooga,  was  onsite for  a Safety Inspection Audit Exit Meeting.
15    Two NRC  licensing personnel were onsite to administer reactor operator  and senior reactor operator licensing examinations to 10 Browns  Ferry operators.
15-18  Three representatives from PLC (Professional Loss Control, Inc.)
were onsite to perform an audit of the fire protection system as required by technical specifications.
16    An NRC  inspector    was  onsite to audit the inservice program.
22-25  Representatives    from the Division of Occupational Health and Safety conducted a safety audit of outage work.
23    Mr. Marvin Lane, Executive Vice Pr'esident of Graver Water Company, met with the Plant Results Section Supervisor and others on the problems of contaminated powdered resins.
23-26  Office of Power Quality Assurance auditors were onsite to perform an audit of document control and technical specifications.
 
27 0  erations  Summar  (Continued)
September 1980 Safet  and First Aid The regular weekly safety meetings of salary policy and trades    and labor groups were held  this  month.
Accidents There were 2  loss-of-time accidents during the    month of September.
 
28 NUCLEAR PLANT PERSONNEL                                            Browns Ferry Nuclear                      PLANT End of                End of Previous              Present TITLE                              Month      Changes  Month Power Plant Superintendent~ M-8 Assistant Power Plant Superintendent M 6 Records          Officer      SA-2 eosIMst  Mechanical          En ineer  SD-3 S    ecification            En    ineer    SD-3 En      ineerin Aide              SE-2 Safety Engineer SO 3 ngzneer ng              i  e Sa ety SE-Su      ervisor,        Mana ement Services            Section M-5 Su ervisor Administrative Services      hbck  Unit H-4
~fctttsttgtttofstetocMZ Su              ervisor Document Control Unit H-
~otaotctNsttgLeffttttxtnTgtrimst7BItsd Su        ervisor Plt Services Unit H Secretar SB.4
>tlaarttISmNcgtgtPtorILM-    Editor      SA-2 Clerk Typist SB 3                                                                                        15 Clerk-Typist SB 2 zfftetsofrftsfcs88.8     Clerk SB-2 Payroll Clerk SB 5 Pa    roll Clerle%8Q<
Payroll ClerleSBR          SB-3 File Clerk SB.3 Supervisor Services H-4 Su ervisor Qualit Assurance        Stalf M 5 Qualit Assurance En ineer SO 4 Quality Assurance Engineer SO-3 Quality Assurance Engineer SO 2 Engineering Aide (Quality Assurance) SE 5 En ineerin Aide (Quality Assurance) SE.4 n    ineerin Aide                  ualit      Assurance)    SE-3 lerk,        SB-3 ail      Clerk SB-2 Power Plant Results Supervisor M.5 Assistant Power Plant Results Supervisor      M4 ower      Plt    Maintenance Supvr              (Inst) H-5 Instrument Engineer SO 4 IfecuttttgtfrBI@tttmtcs88      Personnel Clerk SB-4 otttramstBBM S    stems Anal st, SD-3 enior Instrument Mechanic                        Instructor Irgtmtdge8agtsrtttt~".ItttL(saacsflsft    Programming Technician SE-4 Engineering Aide SE 3 Senior Instrument Mechanic Foreman                                                15                     16 Senior Instrument Mechanic                                                        44                    43 Instrument Mechanic Instrument Mechanic Ap rentice-        '4th  Pd.                                22                     27 Instrument I'ftechanic Apprentice-      3rd  Pd.                                10 ctsrssrotttuntnhtacttmt(enectprzmfeme          Pthc Nord Processor  SB-4 sst.        Power      Plt. Maintenance Supervisor (Inst) M-4 Reactor En ineer SO 4 5U@tnBmjNI@SttgO7B        Clerk SB-4 Engineering Aide (Nuclear)    ZSA SE-5 TAMNQNSBrp;IftmttSGAz              Supervisor, Mechanical Unit M-4 Mechanical En ineer SO 3 Engineerin Aide(Statistician)BRA SE-5 ttgfotroc'otg7rtfsfm(lamISr18ntaias)ISED Data      Entry Clerk SB-2 Engineering Aide (Test    Bt Studies) SE.3 TVA 7037 (PP-10.77) sheer        1                                                  M  mn,r September >>80
 
29 NUCLEAR PLANT PERSONNEL                                              Browns Ferr    Nuclear                PLA14T End of                  Eno of Previous                PfeSenl T IT t.s                                  Month        Chonoes    Montn Mechanical En ineerin Associate SE 6 En ineerin Aide (Mechanical) SE 4 En ineerir. Aide (Mechanical) SE-3 En ineerin  Aide (Instrument) SE.
En ineerin Coo Student (N) SE.3 Enoineerin 'Coo Student OQXZSZ (M)            SE-3 Supervisor Chemical Unit if-4 Chemical En ineer SO 4 Chemical En ineer SO 3 Chemical Enoineerin Associate SE 6 Radiochelnical Laboratory Analyst SE 5 Radiochemical Laboratory Analyst SE 4 Chemical Laborator~ Anal st SE 3 Engineering Coop Student (C) SRR      SE-4 En ineerinn Coo Student (C) SE.2                                                           +1        -1 Radiochemical Laborato                      Anal st  Tr  SE-3 Su ervisor Reactor Unit M-4 Power Plant Operations Supervisor M 5 Assistant Power Plant Operations Supervisor M.4 Clerk SB 3 Shift Engineer M-4                                                                16                     15 Assistant Shift Engineer M-3 Assistant Shift Engineer-SR L                                                    15                      15 Unit Operator Unit Operator-RL                                                                                          20 Assistant Unit Operator Student Generating Plant Operator-      th Pd.
tu ent eneratxng                  ant perator  r Clerk SB-2 Supervisor Janitorial Services i'-3 Janitor SF 3 Janitor SF 2                                                                               +17      -4   17 Janitor SF.l                                                                      55      +27    -20   62 Power      Plant Maintenance              Su  ervisor  E  M-5 Power Plant Maintenance Supervisor M 5 Assistant Power Plant Klaintenance Supervisor (E) M 4 Assistant Power Plant Maintenance Supervisor (M) M 4 General        Electrical        Foreman M-4 Electrical Engineer SO 4 Electrical En. ineer SO 3 General Mechanical Foreman M-4 Mechanical Engineer SO.4 Mechanicaf En ineer SO 3
&rJcttacthsgtt(:cttxftfzstutstnt)Ms'echanical          Engineer SD-2 En ineerin  Aide (41echanical) SE 3 Engineering Coop Student (M) SE.
Xmxnnmsmmm~unx!&SR En                      ineerin Aide Electrical        SE-Electrician Foreman                                                              10                      10 Electrician                                                                      46      +    .  -2 Electrician Apprentice-         Pd.
Electrician Apprentice-  1st    Pd. B                                                                  10 Electrician Apprentice-  1st    Pd. A TVA 7OS7 (PP tO 77) Sheet    2                                                                September,(0
 
30 I'JUCLEAR PLANT PERSONNEL                                                                                    PLANT end or                End or Previous                Present TITLE                                  Month        ChangeS  Month Machinist Foreman Machinist Machinist Welder Machinist A orentice-   4th  Pd Machinist Apprentice-   3rd  Pd.
Machinist Apprentice-   2nd  Pd.
Hachinist        A  I7rentice        1st Pd. B Hachinist        A    rentice        1st Pd. A Boilermaker Foreman Boilermaker Boilermaker Welder Boilermaker Apprentice-          Pd.
Boilermaker Apprentice-          Pd.
Sheetmetal Worker            A    rentice      1st Pd.     A Steamfitter Foreman Steamfitter                                                                      24 Steamfitter Welder Steamfitter Ap rentice- 5th    Pd Steamfitter'Apprentice-  1st    Pd. A                                          12                    12 General Labor Foreman H-3 Car    enter Foreman Asbestos Worker Foreman ainter Apprent3.ce  st                  P  . A Structural Ironworker Sheetmetal Worker Foreman Sheetmetal Worker Asbestos Worker Car enter Painter Foreman Painter Heavy Equipment Operator-Power Labor Foreman Nuclear Plant Laborer                                                          23                      23 Truck Oriver  I Sign Painter Total Annual Salary Policy 233          +67    -33 267 Total ATL Operations      112          +  7  -13 106 Total ATL Maintenance Total Plant                660          +91    -60 691 Hourly-List Titles Car    enter 23 Car enter 1 Construction Laborer 71 Hortar Hixer 1                                            63          +12 Boilermaker (10) Hach Wldr (1) Steamfitter                            15        20                      26 Hach      28    Bricklaver          1 Painter        13    Asbestos Worker 2 Crane 0      erator      2    Sheetmetal Worker            3 Truck Driver I            2 Total Hourly                  152 TVA 7037 (PP.10.77) Sheet  3                                                        Month or
 
L 0
 
31 Se tember 1980 Personnel Chan es  Annual Name                        Title      Effective Date Betty J. Grimes            Janitor F01 09 02 80 Billy J. Allen              Janitor F01 09 03 80 Kenneth E. Howard          Janitor F01 09 03 80 Richard L. Ingram          Janitor FOl 09 03 80 William C. Jones, Jr.       Janitor FOl 09 03 80 Arthur L. Littleton        Janitor FOl 09 03 80 Jose  I. Lozano            Janitor F01 09 03 80 Michael E. Maples          Janitor F01 09 03 80 Margaret L. Reach          Janitor FOl 09 03 80 Larry  D. Smith            Janitor F01 09 03 80 Jack  W. Vinson            Janitor F01 09 03 80 Barbara L. Weigart          Janitor F01 09 03 80 Randall L. Keeton          Janitor FOl 09 04 80 Dennis M. Castell          Janitor F01 09 05 80 Wayne E. Guthrie          Janitor F01 09 05 80 M. Neil Haraway            Janitor F01 09 05 80 Kenneth D. Sylvester        Janitor FOl 09 05 80 Gary R. Cobb                Janitor F01 09 08 80
 
32 Se tember 1980 Personnel Chan es  Annual Name                                Title                      Effective  Date Russell  B. Huffman                Janitor F01                09 08 80 Willie M. Jenkins                    Janitor F01                09 08 80 Robert L..Rice                      Janitor F01                09 08 80 Nicholas L. Austin                  Janitor F01                09 09 80 Thomas  I. Vines                  Janitor FOl                09 09 80 Robert C. Murphy                    Janitor F01                09 10 80 Charles Crawley                      Janitor F01                09 11 80 James  R. Hine                      Janitor FOl                09 15 80 Harlon L. Ramsey                  Janitor F01                09 17 80 B. Reclassifications Effective Name                  Former Title              New  Title              Date Rickey E. Holtzclaw    SGPO 4th Pd              Asst Unit  Op          07 23 79 James  C. Hall        SGPO 4t}1 Pd            Asst Unit  Op          10 01 79 Danny L. Tuggle        Inst Mech AP3            Inst  Mech AP4          06 23 80 Wendell K. Holt        Elect APlA                Elect  AP1B            07 21 80 Kenneth  W. Brown    Elect APlA                Elect  AP1B            08 04 80 Timothy D. Lane        Inst Mech AP3            Inst  Mech AP4          08 04 80 Linda  G. Murphy      Elect APlA                Elect  AP1B            08 04 80
 
33 Se  tember 1980 Personnel Chan es    Annual B. Reclassifications      (Continued)
Effective Name                        Former  Title            New  Title          Date Elizabeth L. White          Elect  AP1A              Elect  AP1B        08 11 80 Kenneth E. Davis            Elect  AP1A              Elect  AP1B        08 18 80 Tony D. Hill              Elect  AP1A              Elect APlB          08 18 80 Patricia  F. Roland        Inst  Mech AP3          Inst  Mech AP4      08 18 80 Lona C. Belue              Clerk  B03              Word  Processor B04 08 24 80 Roger D. Shireman          Radiochem Lab            Radiochem Lab      08 24 80 Anal  E04                Anal E05 James A. Green            Asst Shft Engr    M03    Sup,  Janitorial    08 31 80 Servs M03 Robert E. Stone,    Jr. Inst  Mech AP3          Inst  Mech AP4      09 01 80 James  S. Watson            Elect (H)                Elect              09 01 80 Thomas M. Thompson          Elect  (H)              Elect              09 03 80 Lardell Goodloe,            Elect (H)                Elect              09 04 80 Dan C. Barger            Janitor    FOl            Janitor  F02        09 07 80 Martha C. Barnett          Janitor    F01            Janitor  F02        09 07 80 Nellarene P. Cobb      Janitor    F01            Janitor  F02        09 07 80 Larry  W. Cole            Janitor    F01            Janitor  F02        09 07 80 Leonard A. Cole            Janitor    FOl            Janitor  F02        09 07 80 Michael  W. Davis          Clerk  B02              Clerk  B03          09 07 80 Helen J. Franklin          Janitor    F01            Janitor  F02        09 07 80 William  C. Freeman      Janitor    F01            Janitor  F02        09 07 80
 
34 Se tember 1980 Personnel Chan es      Annual B. Reclassifications (Continued)
Effective Name                      Former  Title          New  Title          Date James  O. George          Janitor  F01            Janitor  F02        09 07 80 Bobby F. Grizzard      Janitor  F02            Janitor  F03        09 07 80 David S. Haney            Janitor  F01            Janitor  F02        09 07 80 Robert L. Ingram          Janitor  F02            Janitor  F03        09 07 80 Martin Johnson            Janitor  F01            Janitor  F02        09 07 80 John  W. Maynor,  Jr. Janitor  F01            Janitor  F02        09 07 80 Morris    W. Morell      Janitor  F01            Janitor  F02        09 07 80 William L. Sandy      Janitor  F01            Janitor  F02        09 07 80 Burl  D. Stark          Janitor  F02            Janitor  F03        09 07 80 E. Jane Wilkerson          Janitor  FOl            Janitor  F02        09 07 80 Thomas    L. Williamson    Janitor  FOl            Janitor  F02        09 07 80 Robert E. Woods        Janitor  FOl            Janitor  F02        09 07 80 Garfield J. Taylor, Jr.      Sr Inst  Mech        Sr  Inst Mech Fmn  09 08 80 Inez H. Bedingfield      Janitor  F01            Janitor  F02        09 21 80 Austin L.,Burnette        Shft Engr  H04          Asst Pr  Plt Op    09 21 80 Sup M04 David T. Davis            Inst Mech AP3          Inst  Mech AP4      09 21 80 Herbert L. Johnson        Qual Assurance Engr D02 Qual Assurance      09 21 80 Engr D03 Donell King              Janitor  F01            Janitor  F02        09 21 80 Richard  W. Shultz      Inst Mech AP3          Inst  Mech AP4      09 21 80 Ardie  R. Champion        Unit Op RL              Asst Shft Engr  M03 09 29 80 James  C. Coz            Unit Op RL              Asst Shft Engr  M03 09 29 80 .
Willard  B. Dawes,  Jr. Asst Unit  Op          Unit  Op            09 29 80
 
35 Se  tember 1980 Personnel Chan es      Annual B. Reclassifications      (Continued)
Effective Name                      Former  Title                  New  Title            Date Johnny E. Duke            Asst Unit    Op                  Unit  Op              09 29 80 Russell    R. Eades      Asst Unit    Op                  Unit  Op              09 29 80 Charles B. Fisher          Asst Unit    Op                  Unit  Op              09 29 80 Steve R. Gray              Asst Unit    Op                  Unit  Op              09 29 80 Charles    G. McClain    Unit  Op RL                      Asst Shft Engr    M03 09 29 80 Marvin L. Meek            Unit  Op RL                      Asst Shft Engr H03    09 29 80 Michael V. Hiller      Unit  Op RL                      Asst Shft Engr    M03 09 29 80 C. Transfers Out Former                New                Place        Effective Name                      Title                Title              TQ          Date Jeannette Y. Johnson      Clk B02              Clk  B02            OCH&S        09 07 80 James L. Turner        Radiochem Lab        Chemist-D01        Trng Ctr    09 21 80 Anal E04 D. Transfers In Former                New                Place        Effective Name                      Title                Title              From        Date George N. Veal            Shmtl Qcr            Shmtl Wkr          W  Creek    08 25 80 David E. Newton            Elect                Elect              Service      09 02 80 Shops Michael    N. Brown      Radchm Lab Ana        Radchm Lab Ana      Trng Ctr    09 21 80 Tr  E03              Tr  E03 James  tJ. Burton  III  Chem  Engr D02        Chem  'Engr D03    Ctl  & Test  09 21 80 B. Joan Chandler          Clk  B02              Data Engry  Op    P&Svs        09 21 80 B02
 
36 Se  tember 1980 Personnel Chan es    Annual D. Transfers In (Continued)
Former              New            Place        Effective Name                    Title                Title          From        Date Edward  J. Frederick    Radchm Lab Ana      Radchm Lab Ana Trng Ctr    09 21 80 Tr E03              Tr  E03 Aaron J. Goode          Radchm Lab Ana      Radchm Lab Ana Trng Ctr      09 21 80 Tr E03              Tr  E03 Albert  M. Reynolds    Radchm Lab Ana      Radchm Lab Ana Trng Ctr    09 21 80 Tr E03              Tr  E03 E. Return From  LWOP Name                    Title                              Effective Date Brian E. Williams        Engg Coop Student E03 (M)          09 02 80 William B. Pendergrass    Engg Coop Student E02 (C)        09 08 80 Theresa  M. Pickney    Engg Coop Student E04 (C)          09 08 80 F. Placed  On LWOP Name                    Title                              Effective Date David A. Robeson        Engg Coop Student E02 (C)          09 08 80 G. Terminations Name                    Title                              Effective Date Fred Fraser              Janitor  F02                        09 02 80 Betty J. Grimes          Janitor  F01                        09 09 80 Harlon L. Ramsey        Janitor  F01                        09 10 80 Randall  C. Arnold      Elect                              09 15 80 John D. Quigley          Elect                              09 15 80 Joe E. Rice            Unit  Op RL                        09 19 80
 
37 Se tember 1980 Personnel Chan es    Houri Name                    Title                    Effective Date J. R. Daniel            Mach                    09 02 80 Robert  W. Daniels    Mach                    09 02 80 Jimmy D. Dean            Mach                    09 02 80 Jimmy  W. Embry        Stftr                    09 02 80 Billy J. Emmons        Stftr                    09 02 80 William  E. Griggs      Mach                    09 02 80 Harry F. Hacker          Mach                    09 02 80 Bennie D. Stults      Mach                    09 02 80 Thomas M. Thompson      Elect                    09 02 80 Harold F. Wilson        Stftr                    09 02 80 Willie T. Eggleston      Stftr                    09 03 80 Jack D. Gaston          Stftr                    09 03 80 Lardell  Goodloe        Elect                    09 03 80 Charles  W. Warhurst  Mach                    09 03 80 Bill C. Thornton      Stftr                    09 04 80 Edwin R. Warren          Mach                    09 04 80 Morris  G. Brown        Cons  Lbr                09 05 80 Earnest E. Cosby        Cons  Lbr                09 05 80 William H. Draper        Cons  Lbr                09 05 80 James  P. Fields        Cons  Lbr                09 05 80 Leon Pope                Cons  Lbr                09 05 80
 
38 Se tember 1980 Personnel Chan es  Houri e
Name                  Title                          Effective Date Thomas F. Schemeltz  Cons  Lbr                      09 05 80 James  J. Smothermon Cons  Lbr                      09 05 80 Loyd C. Canon        Cons  Lbr                      09 08 80 James  J. Cashion    Cons  Lbr                      09 08 80 Jimmie 0. Garrett    Cons  Lbr                      09 08 80 A. D. Jackson        Cons  Lbr                      09 09 80 Kenneth R. Smith      Mach                          09 15 80 Esadore Meeks        Cr Op                          09 17 80 Albert  S. Smith      Mortar Mixer                  09 30 80 B. Reclassifications Former              New Name                  Title                Title    Effective Date James  S. Watson      Elect                Elect (A) 09 01 80 Thomas M. Thompson    Elect                Elect (A) 09 03 80 Lardell  Goodloe    Elect                Elect (A) 09 04 80 C. Transfers Out None D. Transfers  En None
 
16 0  erations  Summar    (Continued)
September  1980 Chan e  in Procedure There were 54 revisions to plant    instructions during the month. 47 instructions  were changed  primarily for corrections. The remaining  7 revisions related to the safe operation of the plant.
Chan e  in Facilit Desi  n All changes in facility design will be included in    the unit  outage summary  report.
 
0 erations  Summar  (Continued)
September 1980 Surveillance Testin Unit 1 A  total of 478 surveillance tests  were completed on Unit 1 per 151 different test instructions.
Unit 2 A  total of 205 surveillance tests were completed  on Unit 2 per 95 different test instructions.
Unit 3 A  total of 328 surveillance tests  were completed on Unit 3 per 115 different test instructions.
 
39 Se tember 1980 Personnel Chan es  Houri E. Terminations Name                  Title                  Effective Date Leslie L. Abernathy    Cons Lbr                07 15 80 Gary D. Nichols        Hach                    08 27 80 Charlie  E. Keener    Cons Lbr                09 04 80 Lloyd W. Guthrie      Carpenter              09 16 80 Johnny Norton          Mortar Mixer            09 22 80 Harty F. Hacker        Hach                    09 29 80
 
40 Si nificant  0  erational Events Unit  1 Date    Time                              Event 9/01/80  0001 Reactor thermal power. at >99%, steady state control rod sequence  "A".
1341 Reactor Scram No. 135        from >99% on turbine stop valves closure, due to water causing a short in pressure relay 62-C1, which caused relay KT 303 to trip turbine.
1736 Commenced rod withdrawal.
2025 Reactor Critical No. 156.
2230 Rolled T/G.
2343 Synchronized generator, commenced power ascension.
9/02/80  1500 Commenced  PCIOHR  from 82%  thermal power.
9/03/80  0040 Reactor thermal power at 95%, holding due to "C" string high pressure heaters isolation due to relief valve flange leak.
1939 "C"  string high pressure heaters maintenance completed and heaters placed in service.
2030 Resumed PICOHR from 95% thermal power.
9/05/80  1500 Reactor thermal power at    99%, maximum  flow.
9/07/80  0015 Reduced thermal power from 99% to 85% for turbine C. V.
tests and SI's.
0230 Turbine C. V. tests and SI's completed, commenced power ascension.
0705 Commenced PCIOHR from 95% thermal power.
0905 Reactor thermal power at >99%, steady state.
9/10/80  1500 Reactor thermal power at >99%, steady state.
9/12/80  2100 Reduced thermal power from >99% to 50%      for control rod sequence exchange from "A" to "B".
9/13/80  0205 Control rod sequence exchange from "A" to "B" completed, commenced  power ascension.
2130 Commenced  PCIOHR  from 82%  thermal power.
9/14/80  2300 Reactor thermal power was >99%, steady state.
9/16/80 "1843 Reduced  thermal power from >99% to 90% for removal of "A" circulating water pump to allow stop log lA1 to be lifted.
1905 "A"  circulating water  pump  placed  in service, (mode  to cooling towers would not operate      due to stuck gate),
commenced  power ascension.
2030 Commenced  PCIOHR  from 95% thermal power.
2300 Reactor thermal power at >99%, steady state.
 
41 Si  nificant  0  erational Events Unit  1 Date    Tillle                              Event 9/19/80 2230  Reduced  thermal power from >99% to 77% for removal of "B" reactor feedwater pump for maintenance (excessive vibration).
9/20/80 0216  Reduced thermal power from 77% to 70% for turbine C. V.          tests and SI's.
0315  Turbine C. V. tests and SI's completed, commenced power ascension.
1220  Reduced thermal power from      77% to 50% due to loss of unit preferred power,    when shutdown board power supply was trans-ferred.
1225  Commenced  power ascension.
2030  Commenced  PCIOIR from 80% thermal power.
9/21/80 1550  Reactor thermal power at >99%, steady'state.
9/24/80 2222  Reactor Scram No. 136 (1) from >99% thermal power on load        re-ject trip from negative ground on main transformer sudden pressure relay circuit.
9/25/80 0530  Commenced  rod withdrawal.
0820  Reactor  Critical  No. 157, sequence "B".
1038  Rolled T/G.
1107  Synchronized generator, commenced power ascension.
2110  Commenced PCIOIK from 67% thermal power.
9/27/80 0015  Reduced thermal power from 99% to 85% for turbine C. V.
tests and SI's.
0125  Turbine C. V. tests and SI's completed, commenced PCIOMR.
1500  Reactor thermal power at >99%, steady state.
9/28/80 1500  Reactor thermal power at >99%, steady state.
9/29/80 0115  Reduced  thermal power from    >99%  to 85%  for  backwash and precoat    condensate    demineralizers.
9/30/80 2400  Reactor thermal power at 85%, holding        for  condensate de-mineralizer problems.
 
42 Si  nificant  0  erational Events Unit  2 Date    Time                            Event 9/01/80 0001 Reactor thermal power at    92%, EOC-3  coastdown  control rod sequence "B" .
1500 Reactor thermal power at    90%, EOC-3  coastdown.
9/04/80 1500 Reactor thermal power at    89%, EOC-3  coastdown.
9/05/80 2130 Commenced  reducing thermal power from    89%  for refuel shut-down (EOC-3).
2247 Reactor Scram No. 109 (manual)    from 35%  thermal power to accommodate  refueling outage.
9/12/80 1320 Received permission for fuel movement    operation, holding due to communication porblems.
1650 Communications restored, commenced    fuel  movement operation to accommodate LPRM maintenance.
9/19/80 1000 Commenced  core fuel shuffle operations.
9/30/80 2400 Refueling operation in progress.
 
43 Si nificant  0  erational Events Unit  3 Date    Time                              Event 9/01/80 0001 Reactor thermal power at >99%, steady state control rod sequence "A".
1455 Reduced thermal power from >99% to 63% due to "A" recir-culation pump trip from a spurious trip.
1522 Reduced thermal power from 63% to 54% due to "A" recircu-lation pump being out-of-service.
2055 "A" recirculation pump maintenance completed      and pump placed in service, commenced power ascension.
2200 Commenced  PCIOMR  from 75%  thermal power.
9/03/80 1500 Reactor thermal power at >99%, steady state.
9/07/80 0230 Reduced thermal power from 99% to 75% for      turbine  C. V.
tests and SI's.
0330 Reduced thermal power from 75% to 67% due      to MSIV-1-26 closing too fast (~1.3 seconds).
0430 Turbine C. V. tests and SI's completed, holding at 67%
due to MSIV 1-26 being left in closed position, awaiting maintenance.
1500 Increased reactor thermal power from      67% to  75%,  holding due to closure of MSIV 1-26.
9/10/80 1500 Reactor thermal power at    75%,  holding due to  MSIV 1-26 being closed.
9/12/80 2245 Commenced reducing thermal power from 75%      for  shutdown for MSIV 1-26 mainte~y~ce.
2355 Reactor Scram No. 88        (manual) from 35%  thermal power to accommodate maintenance to MSIV 1-26.
9/14/80 0525 Maintenance to MSIV 1-26 completed,      commenced rod with-drawal.
1009 Reactor Critical No. 98.
1706 Reactor was made subcritical due to a feedwater valve (3-219A) leak.
2233 Repairs to feedwater valve 3-219A completed, commenced rod withdrawal.
2243 Reactor Critical No. 99.
9/15/80 0155 Rolled T/G.
0233 Synchronized generator, commenced power ascension.
1600 Commenced  PCIOMR from 76% thermal power.
 
44 Si nificant  0  erational Events Unit  3 Date      Time                                    Event 9/16/80    2330      Reactor thermal power at 92%, maximum flow, awaiting rod,pattern adjustment load drop.
9/17/80    2300      Reactor thermal power at 91%, maximum flow, awaiting rod pattern adjustment load drop, 9/18/80    0700      Reactor thermal power at 90%, maximum flow.
9/20/80    1358      Reactor Scram No. 89 (1) from 90% thermal power, on loss of preferred power when "A" 480 volt shutdown board failed to transfer back to normal causing loss of "A" RPS MG set.
2230      Commenced rod withdrawal.
9/21/80    0104      Reactor  Critical  No. 100.
0440      Rolled T/G.
0500      Synchronized generator, commenced power ascension.
1500      Commenced  PCIOMR from 67% thermal power.
9/22/80    2240      Reactor thermal power at      90%, maximum  flow.
9/23/80    2145      Reduced  thermal power from    90%  to 75% for control rod pattern adjustment.
2255      Control rod pattern adjustment'ompleted,        commenced power ascension.
2300      Commenced  PCIOMR  from 82%  thermal power.
9/24/80    0725      Reactor thermal power at      93%,  holding due to computer malfunction.
2130      Computer back    in service,  resumed PCIOMR from 93%
thermal power.
9/25/80    0200      Reactor thermal power at      99%, maximum  flow.
1500      Reactor thermal power at      98%, maximum  flow.
9/27/80    0130      Reduced thermal power from 98% to 80%      for turbine  C. V.
Tests and SI's.
0217      Turbine C.V. tests and SI's completed,      commenced  power ascension.
0300      Commenced  PCIOMR from 90% thermal power.
1200      Reactor thermal power at >99%, steady state.
9/30/80    2400      Reactor thermal power at >99%, steady state.
(1) Equipment Malfunction
 
45 Plant Instruction Revisions September  1980 Cate or                      Instruction              Reason                for Re uest Change in  EHI-46                                  To                include heat tapes at Facility    Freeze Protection Program                cooling tower.
Design SI 4.2.A.6                              Junction boxes have been Primary Containment and                  added                for test purposes.
Reactor Building Isolation Instrumentation Low Pressure Main Steam Line SIHI-3                                  Density compensation removed System Instrument Maintenance          per ECN P-0130, DCR 1533, Index 3- Instruction Reactor          workplan 9870 for Unit 2 only.
Feedwater System SIMI-46                                Pressure compensation removed System Instrument Maintenance          per ECN P-0129, DCR 1532, Index 46  Instruction Feedwater      workplan 9838 for Unit 2 only.
Control System Change      EMI-44                                To implement DPH N 80 Ml, which Required to Reactor Protection System              requires an inspection of the Improve the Scram Solenoid Relays                  movable contacts for a possible Safety of                                          binding problem.
Operation EMI-80                                Recurrence control                  for LER Maintenance of Inboard and Outboard Drywell Leak Detection Isolation Valves 50-259/8040.'TI-23A When                  controlling in "A" water Refueling Test Instruction            level sensor element in case 23A, Feedwater  System                of                  250 VDC normal supply failure.
 
46 Re ortable Occurrences Occurrence BFRO            Date                  Descri tion Unit  1 50-259/8060  8/14/80            While performing SI 4.2.B-60, thermostat TS-64-73 for "B" core spray pump area cooler fan was found set above the technical specification limit.
50-259/8061  8/14/80            While performing SI 4.2.B-57, a thermal overload on the breaker for 1A RHR area cooler fan was found tripped.
50-259/8063  8/20/80            While performing SI 4.8.B.4.2, CAM 1-RM-90-251 for the turbine building vent was removed from service for a period exceeding one hour.
50-259/8064  8/20/80            While performing SI 4.8.B.4.2, CAM 1-RM-90-249 for the turbine building roof vents was removed from service for a period exceeding one hour.
50-259/8065  8/28/80            Wind  direction at elevation 887 M.S.I.
failed. The LCO to restore the inoperable channel to operating status within 7 days was exceeded.
50-259/8066  9/02/80            Operations personnel observed an annunciation on the torus hydrogen containment atmospheric monitoring.
50-'259/8068  9/01/80            Inspection of the  fire protection system by a qualified fire consultant was not per-formed within the 3 year interval as required by Technical Specification 3.11.E.2.
50-259/8069  9/02/80            While performing SI 4.2.A-17, channel B of "refueling zone isolation static pressure permissive and static pressure logic systems units 1, 2, and 3" modulating damper 0-PDC 64-8 failed to close.
50-259/8070  9/19/80            During a review of Unit 1 core verification video tape bundle TY 582 at core location 11-06 was found to be 90'ut of proper orientation.
 
47 Re ortable Occurrences Occurrence BFRO            Date                    Descri tion Unit  2 50-260/8033    8/15/80              During routine test TI-36A an indicated leak was found on RHR  heat exchanger 2B.
50-260/8034    8/15/80              During a routine test TI-36A    RHR heat exchanger 2C was found leaking.
50-260/8035    8/30/80              Test personnel detected an increase in pressure on the shell side of RHR heat exchanger 2D while performing TI-36A, RHR heat exchanger leak test.
50-260/8036    8/29/80              During normal operation while performing SI 4.7.H, the H H-76-39 hydrogen monitor for the drywell would not calibrate.
50-260/8037    9/14/80              Fuel assemblies  TZ 758 in core location 15-26 and TX 399 in core location 29-28 were found to be rotated 90'rom their correct orientation.
50-260/8038    9/11/80              With the unit in cold shutdown during a scheduled refueling outage, HPCI check valve 2-73-609 failed the local leak rate test.
Unit  3 50-296/8031    8/09/80              During the performance of 1'RI 303    it  was found that the EECW flow was below the minimum allowed flow on 3B RHR pump seal heat"exchanger.
50-296/8032    8/25/80              While performing RCIC steam line space high temperature SI 4.2.B-32, lead wires were accidently pulled out of the RCIC speed feedback magnetic pickup connector.
50-296/8033    8/15/80              During routine test TI-36A,    a  leak on  RHR heat exchanger  2B was  indicated.
50-296/8034 '/29/80                  While investigating overload setting for RHR area cooler fans, the overload for 3A RHR pump area cooler fan was found to be set too high.
When the overload was adjusted to the proper setting, the overload relay failed causing the fan to trip.
50-296/8035    9/Ol/80            . The "A" reactor  recirculation pump tripped.
The 24 hour LCO  for one pump operation was initiated I,'Technical Specification 3.6.F.1).
 
48 Re ortable Occurrences Occurrence BFRO          Date                  Descri tion Unit  3 50-296/8036  9/04/80            While running SI 4.9.A.l.a after SEMI-18 had been performed,  it was found that diesel generator 3A would not trip to idle speed from a loaded condition.
50-296/8037  9/09/80            During normal operation, while performing SI 4.7.H, H2M-76-39 would not calibrate.
50-296/8038  9/07/80            While running SI 4.7.D.l.b.2 with unit at 99%
steady state power, main steam isolation valve FCV 3-1-26 closed too fast.
 
Primar  Coolant Chemistr September  1980 Parameter                                Unit 1        Unit  2 Unit  3
: 1. Gross  Radioactivit
: a. Crud on 0.45  millipore filter (uCi/ml)
High                    3.98E-03    8. 68E-03  5.32E-03 Low                      5.00E-04    3.60E-05    4.64E-04 Average                  1.22E-03    1.47E-03    1.12E-03
: b. Filtrate (uCi/ml)
High                    4.01E-01    1.56E-01    2.36E-01 Low                      1.13E-01    1.60E-03    6.47E-02 Average                  1.79E-Ol    3.29E-02    1.26E-01
: 2. Sus ended    Solids Stained 0.45    milli ore filter    (  b High                      25                      10 Low                      <10          <10        <10 Average                  <10          <25        <10
: 3. Gross    Tritium (uCi/ml)
High                    1.44E-03    1.17E-03    2.18E-03 Low                      1.14E-03    9.88E-04    1.53E-03 Average                  1.27E-03    1.04E-03    1.81E-03
: 4. Iodine-131
    ~(uC i/ml High                    1.02E-03    1.92E-03    7.64E-03 Low                      1.89E-04    3.43E-05    2.07E-05 Average                  6.88E-04    5.01E-04    1.75E-03 (1) Unit down
 
50 Primar    Coolant Chemistr    (Continued)
September  1980 Parameter  (Continued)                Unit  1            Unit  2 Unit  3
: 5. Ratio of Todine-131 to iodine-133 High              4.33E-01        1.72E+02  1.32E+01 Low              1.02E-01        3. 45E-01  3.33E-01 Average          2.13E-01        4.93E+Ol    2.64E+00
: 6. Chloride (ppb)
Limit  100 High              <50                        <50 Low              <50            <50        <50 Average          <50            <50        <50 Limit 5.6 or 8.6 High              6.7              6.7        7.0 Low              6.0            5.7        5.8 Average          6.4              6.3        6.2
: 8. Conductivit    (umho/cm 8 25' C.)
eratin Limit 1.0    umho/cm 8  25'.)
Shutdown Limit 10.0    umho/cm 8 25'C.
High              2 8(1)          2 4(l)    2  4(l)
Low              .36              .38        .15 Average          .72              .81        .53 (1) Unit down
 
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                                                                        ~
AVERAGE DAILY GROSS Unit
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                                              ,,                                                                      ~
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                                                                                                                      ,
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                                                                                                                                                      }POWER ASC NSION
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I
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hk tWte fhh cn A
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                                                          '        .'
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                                                                                                                      ~                            TO MSIV 1
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                              ~    ~
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2 3 4 5 6 7 8 9 10 11  12 13 14 15 16  17  18  19  20  21  22  23  24    25    26 27 28 29 30 31 ED. AVE  G            SO'.(SJ CUE  .A ED AV iAG i ~  C  y -l 79    (-5    =7.
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2 3 4 5 6 7 8 9 10 I 'I 12 13 14 15 16  17  18  19  20  21  22  23  24    25    26 27 28 29 30 31 MQNTH QF    Se  tember]g      SO C'
 
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                                                                                        }IIEH~ RK.G BYE~ IB.H LQH~    2.2 BCT I V ITY 2.e BVG~ H.B I8/  2                                                                                LQH~ H. I RCT I V ITY RRDHASTE SYSTEH THROUGHPUT CEALLOIIS~HG)
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.8 FLOOR FLOOR DRAI      8                                                DRRIh'IGH>>
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  .8                                                                                  LGH>>    3.2 HASTE a.a                                                                              7    FLOOR DHRIN BIEII~ 39.8 0    III      BVG~ IB,H l8.8 LOW~ G.S tiONTII R
 
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o 0 9 50 9
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:.V: tea      ts ang=SI          s l~~
Ie                              3 11 01  pro                      ll                              ++ro n            0 6 .'-    Fu            .ec            tao    11.B        eju nc                )=.
7 I IAI                        Dg      at '<<p uti>p          U      f se ct          eed        t  ~PU HlP      OU      of .se pre            CC po 0                              ra    -'H 0          5            ra 0 r- oa              j ec l                      a  te        man      r- a                r. e o  i.t    n    b eke 2 3      4        5    6        7    8      9      10  II    '12      13    14    15  '16  17      18    19    20  21 22 23  24    25        26 27 28 29 30 31 MQNTH Qg                    September          Ig 80
 
C N 4 f'ii I'AI'L'il 1 2 3 4 5 6 7 8 9 '10 11    '12  13    14    15  16    17      18      19      20  21  22 23  24  25  26  27 28  29  30  31 IO
                                          'co std wn                                                                                  70
                        ;  :Co      e 'ce :--sh    td            f wn. or- -re            uel ng oui APP      C=                              A act          era                          ma        ).=.Cy le"      Eu                              o/0 4:Rqf u e 'in ..OU taj =(                  OC=      )-..
re        1g, e -Er                                  Eered-    it) -LP    e'pPs ce len            Q
                              -B escaa n eo e-E el: sh EH 20 2 3 4 5 6 7 8 9 10  11    12  13    14    15 .
16    17      18      '19    20  21  22 23  24  25    26  27 28    29  30  31 MONTH O              SeP tember              19      80
 
                                                                                                  <<A':5 A'I ONA 0> ~ 0A m<01 ~            55<5150 lm U,c, 5, 2    3      4      5      6    7      8  9    10  11    12    13 14    15  16 17    18      19  20 21 22 23  24      25        6 27 28 29 30 31
<0 1.0
                                                                                                                                                                  ~0 50                                                                                                                                                                50 0
O H 50                                                                                                                                                                50
:l'2                ecz    rcupL        ori. pum em'IIm                                                                                                                      00
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12    13 14    15  16 17    18      19  20 21 22 23  24      25      26  27 28 29 30 31 MONTH OF~Sptkmmer                  10 80
 
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63 TVA 7382'PP.l          1 78)
NUCLEAR PLANT OPERATING STATISTICS Browns    Ferr  Nuclear          plant Period    I lours                                                                                  Month    Sen tember    19 80 Item No.                        Unit No.
Average Hourly Gross Load, kW Maximum Hour Net Generation, MWh 3        Core Thermal Energy Gen., GWD(t)                  90.660        14.3365      80.1247 Gross Electrical Gen., MIVh                      699 320        113 120      625 700        1  438    4 Station Use. MWh                                  21 477            302      18 Net Electrical Gen., MWh                          677 843        107 818      607 023        1      2    4 7      Station Use. Percent                              3.07          4.69        2. 8 8        Accum. Core Exposure MWD/Ton                    12 610        16 028      1      27      42 9        CTEG This Month, 10 6TU                          7,425,276      1  170 328 6 570 852 15 166 456 10        Hours Reactor Was Critical                        703.30        118.78      669.05          14  1.13 Unit Use, Hours.Min.                            697:13        118:47      654:20          1  470:2 12        Capacit    Factor. Percent                        88.4          14.3        79.1            60". 6 13        Turbine Avail. Factor, Percent                    99. 5        19. 0        100            72. 8 Generator Avail. Factor. Percent                100            19.0        100 Turbocen. Avail. Factor. Percent                99.5          19.0        100 16        Reactor Avail. Factor, Percent                  100            16. 5        100            72. 2 17        Unit Avail. F ctor, Percent                      98.5          16.5          4.0 18        Turbine Startups                                                0 19        Peactor Cold Startups                            0              0            0 20 21        Gross Heat Rate, Btu/kWh                        10,620        10 350      10 500          10 550 22        Net Heat Rate, Btu/kWh                          10,950        10,850      10 820          10 890 Cl lJ  23 24 25 26        Throttle Pressure, psig                          950            913            38 27        Throttle Temperature, F                          539            534 28        Exhaust Pressure, InH Abs.                      3.12          3.33 29        Intake Water Temp.,    F                        82.9          87.0        83.8 30 31 32 33        Reactor Feedwater, M Ib/hr                      12.4          11.8        11.7            12e 34        Makeup, Percent 36 37        Full Pr. Days to End of Cycle (E)      (3)      192                        31 38        Oil Fired for Generation, Gallons                                                            2 39        Oil Heatin Value. Btu/Gal.                                                                  137 60 40        Diesel Generation, MWh                                                                      29.4 Max. Hour I'let Gen.              Max. Day Net Gen.        Load MWh          Time        Date        MWh          Date      Factor, %
43        2,972            0600        9-5-80        72, 284    9-4-80      65. 1 Pemarks 1 ~    Informa tion unavailable.
: 2. Unit 2 refuel outage (EOC-3) began at                    2247 hours on    9-5-80.
Based on 5% capacity tactor.
D t 5 bmitted                                      Date Revised Plant Superintendent
 
TVA  4'C Irn-3 1st UNIT OUTAGE AND AVAILABILITY Brouns Parr                    Nuclear Plant      l licensed Aeactor Power          3293 MIVRh)                                                    Unit No.
1152 MW(e)                                                                                                                        MonthiYear    Septcnber 1980 Generator Rata)g Design Gross Electrical Rating            1098 4      MW                                                                                                  Period Hours Vail                                      METHOD OF      UN I T      CORRECTIVE ACTION T)dne  Vn)l Available                  Time NOt Ava))able                                                                SHUTTING    STATUS Time      T)me            OUTAGE CAUSE                                    TAKEN TO PAEVENT Vn) I      O)dt        In                                    DOsvN    DURING            REPETITION Total                    Nol V)ed  Tw bine            Reactor REACTOR    OUTAGE sids  radn  )S)S  rdbn ~lr) s Mn Nds M)n  H)$ Mdn  I srs  Min lbs M)n I id) Mdn
                      ~58            06    07  ~0)    55                      03  r  55  13 41 23 43          Turbine  trl  due  to sto    Scrub  liat Standby 24 00 5
IO 12 13 15 18 P.t S~
          "4 22 22 00      24 100 22 t22                                                0~138        22l  22            ~l,d
* d                Scran  Oot Standby
                                                                                                    ~tt        on natn  transforner sudden 25  J 8~0        L22 )3 ~01          37                              05 130                        07
~r)                  ~41                                                                                        ressure rota 27 29 30              gC      0 31 1 'tat  1~08  57    )79    13      11    44  03 I 55                    11      03  >C OC


TVA 7382'PP.l 1 78)63'Period I lours Item No.Unit No.NUCLEAR PLANT OPERATING STATISTICS Browns Ferr Nuclear plant Month Sen tember 19 80 Average Hourly Gross Load, kW Maximum Hour Net Generation, MWh 3 Core Thermal Energy Gen., GWD(t)90.660 14.3365 80.1247 Gross Electrical Gen., MIVh Station Use.MWh Net Electrical Gen., MWh 699 320 113 120 625 700 18 21 477 302 677 843 107 818 607 023 1 438 4 1 2 4 7 Station Use.Percent 3.07 4.69 2.8 8 Accum.Core Exposure MWD/Ton 12 610 16 028 1 27 42 9 CTEG This Month, 10 6TU 10 Hours Reactor Was Critical 7,425,276 1 170 328 6 570 852 118.78 703.30 669.05 15 166 456 14 1.13 Unit Use, Hours.Min.
t, UNIT OUTAGE ANO AVAILABILITY Nuclear Plant Licensed Reactor Power             3293 MW(lh)                                                   Urut No Generator Rating~252               MW(e)                                                                                                   Month/Year    Se cenbee  1980 Design Gross Oectricat          Rating~~84            Mw                                                                                  Period Hours  720 Vnil METIIOO OF  UNIT        CORALCTIVE AC1ION time Vml Avaelbre                     Time eeet AVasrabre Time      Time                  SIIUTTING  STATUS      TAI<EN 10 PREVENT OUTAGE CAUSE 1 nrar     ~
12 Capacit Factor.Percent 697:13 88.4 118:47 14.3 654:20 79.1 1 470:2 60".6 13 16 17 Turbine Avail.Factor, Percent Generator Avail.Factor.Percent Turbocen.Avail.Factor.Percent Reactor Avail.Factor, Percent Unit Avail.F ctor, Percent 99.5 100 99.5 100 98.5 19.0 19.0 19.0 16.5 16.5 100 100 100 100 4.0 72.8 72.2 18 Turbine Startups 0 19 20 Peactor Cold Startups 0 0 0 Cl lJ 21 Gross Heat Rate, Btu/kWh 22 Net Heat Rate, Btu/kWh 23 24 25 10,620 10,950 10 350 10 500 10,850 10 820 10 550 10 890 26 Throttle Pressure, psig 950 913 38 27 Throttle Temperature, F 539 534 28 Exhaust Pressure, InH Abs.3.12 3.33 29 30 31 32 33 34 Intake Water Temp., F Reactor Feedwater, M Ib/hr Makeup, Percent 82.9 12.4 87.0 11.8 83.8 11.7 12e 36 37 Full Pr.Days to End of Cycle (E)(3)38 Oil Fired for Generation, Gallons 39 Oil Heatin Value.Btu/Gal.192 31 2 137 60 40 Diesel Generation, MWh 29.4 Max.Hour I'let Gen.MWh Time Date 43 2,972 0600 9-5-80 Pemarks Load Factor,%Max.Day Net Gen.MWh Date 72, 284 9-4-80 65.1 1~Inf orma tion unavailable.
Cen.     llOl Vied Tw bine               Aeactor      Vml        Ovt        In                      DOWN    DURING          ACPLT ITION nay   I lis   4'I n I lis   l.bn lbs rvbn ~lus. Msn lbl Mm     ~S4S ItlIn l 4S   Msn lb s Min llis   Mm                 REACTOR   OUTAGE I   24 I 00         24    00 2
2.Unit 2 refuel outage (EOC-3)began at 2247 hours on 9-5-80.Based on 5%capacity tactor.D t 5 bmitted Date Revised Plant Superintendent TVA 4'C Irn-3 1st UNIT OUTAGE AND AVAILABILITY licensed Aeactor Power 3293 MIVRh)Generator Rata)g 1152 MW(e)Design Gross Electrical Rating 1098 4 MW Brouns Parr Unit No.Nuclear Plant l MonthiYear Septcnber 1980 Period Hours Total sids radn~58 24 00)S)S rdbn 06 07 T)dne Vn)l Available Nol V)ed Time NOt Ava))able Reactor H)$Mdn Tw bine~lr)s M n Nds M)n~0)55 Vn)I I srs Min 03 r 55 Time O)dt Vail T)me In I id)Mdn 23 43 lbs M)n 13 41 OUTAGE CAUSE Turbine trl due to sto METHOD OF SHUTTING DOsvN REACTOR Scrub UN I T STATUS DURING OUTAGE liat Standby CORRECTIVE ACTION TAKEN TO PAEVENT REPETITION 5 IO 12 13 15 18 P.t 25~r)27 S~"4 00 22 22 J 8~0 24 100 22 t22 L22)3~41~01 37 0~138 05 130 22l 22~tt 07~l,d*d on natn transforner sudden ressure rota Scran Oot Standby 29 30 31 1'tat 1~08 57 gC 0)79 13 11 44 03 I 55 1 1 03>C OC t, UNIT OUTAGE ANO AVAILABILITY Licensed Reactor Power 3293 MW(lh)Generator Rating~252 MW(e)time Vml Avaelbre 1 nrar~Cen.llOl Vied Tw bine nay I lis 4'I n I lis l.bn lbs rvbn~lus.Msn Design Gross Oectricat Rating~~84 Mw Vml lbl Mm~S4S ItlIn l 4S Msn Time eeet AVasrabre Aeactor Urut No Vnil Time Ovt Time In lb s Min llis Mm Nuclear Plant OUTAGE CAUSE METIIOO OF SIIUTTING DOWN REACTOR UNIT STATUS DURING OUTAGE CORALCTIVE AC1ION TAI<EN 10 PREVENT ACPLT ITION Month/Year Se cenbee 1980 Period Hours 720 I 2 24 I 00 24 00~24 00 22 I 47~24 00 22 lC7 06 54 06 i 54 24 00 24 00 0LLL3&1~24'00 24L 00 I 12 13 15 22 I 25 2Ci 27 I I I I I 29 drs L" Intel 118 47 18 47~24 582 I 54 82 54~-'is i UNIT OUTAGE ANO AVAILABILITY Licensed Rcatlnr Power 3293 hIW(th)Gcncialnr Rating 1152 I.IW(c)Design Gioss Electrical Rating 1090~4 MSV Srovns Petr Nuclear Plant U is N.~hlonih/Year Se tenbec 19SO Period Hours 720 Toter trst Mn 24 i00 Gcn, t ris c.lsn 24 00 Nol Vscii Cist htsn Tinsc Unit AvaiNbte Tsss bine~trit lain Time Not Available Reactor leS Min~its r Min Vnil~His M so Vnsl Time In Time Ovl lrsr htin tlii Min OUTAGE CAUSE METHOD OF SHUT TING DOWN REACTOR UNIT STATUS DURING OUTAGE CORRECTIVE ACTION TAKEN TO PREVENT REPETITION c c sJ IO II 12 13~4 l5)fi l7 18 lg 0?I?7~7?l?6 27 24 IOO 13~08 2it I00 jk I28 2'K I 24~00 I 21.IQL+4 I 0 1'9i 00 24 00 c I 0~05 00 c 00 l05 24 00 08 I32~23 55 13 5S 02 33 05 00 Maintenance to MSIY 1-26 and feedvater valve 3-219A lass of nAn RPS MG Sct Manual Stean llot Stan b Ilot Standb 29 30 2~4 3l Trit.tt 676 31 t c 24 00 I 654 20 22 11 I 43 9 67 OUTAGE  
        ~24 00 ~24               00 22 I 47 22           lC7 06   54 06 i 54 0LLL3 24 '00
                                                                                  &1~
24L 00 24   00 24 00                       I 12 13 15 22         I I           I I
25 2Ci                        I           I 27 29 drs                                           ~24 L"
Intel 118       47       18     47             582 I 54 82   54
                                                                                                                                                                          ~ 'is i
 
Licensed Rcatlnr Power 3293 Gcncialnr Rating       1152 Design Gioss Electrical Rating I.IW(c) hIW(th) 1090 ~ 4           MSV U is N   .~
UNIT OUTAGE ANO AVAILABILITY Srovns Petr            Nuclear Plant hlonih/Year Period Hours Se 720 tenbec 19SO Vnsl Tinsc Unit AvaiNbte                            Time Not Available METHOD OF      UNIT        CORRECTIVE ACTION Time      Time                                SHUT TING    STATUS        TAKEN TO PREVENT OUTAGE CAUSE Toter         Gcn,      Nol Vscii    Tsss  bine                Reactor    Vnil        Ovl        In                                    DOWN      DURING REPETITION trst   Mn   t ris c.lsn   Cist   htsn ~trit lain   leS Min   ~its r Min ~His   Mso  lrsr htin tlii Min                                 REACTOR     OUTAGE 24    i00      24 00 c
c sJ IO II   24    IOO      24 ~00 12                                                                                 00  l05  ~23    55              Maintenance to MSIY 1-26 and  Manual  llot Stan  b 13                                     c                                            24    00                        feedvater valve 3-219A I
  ~4   13~08 l5  2it I00       21.IQL                                                                                   02    33
  )fi l7 18 lg                +4     I 0 0  jk                                I   0                                       08 I32   13     5S             lass of nAn RPS MG   Sct   Stean   Ilot Standb
  ?I
  ?7 2'K  I28 24 1'9i 00 ~05 00 00                                                              05    00
~7            I
  ?l c
  ?6 27 29                         t c
30   2~4             24    00                                                          I 3l                         I Trit.tt 676 31       654       20   22     11                                       43     9
 
67 OUTAGE  


==SUMMARY==
==SUMMARY==
September 1980 The unit two reactor shutdown sequence was conducted in an orderly process on September 5, 1980, for refueling activities and routine maintenance to plant equipment.
 
The refuel activities involve disassembly of Unit 2 reactor for refueling operation with reactor startup scheduled for October 26, 1980.The routine maintenance involves inspection and repairs to major components and safety systems within the plant.The initial containment entry was conducted at 1:05 P.H.on September 6, 1980.The planned duration for the Unit 2 cylce 3 refuel outage is 49 days.The pre-planned schedule shows that turbine inspection and maintenance work sequence as the critical work path, a fix'st at Browns Ferry Nuclear Plant.In order to prevent the outage duration from exceeding the 49 day schedule, non-curcial modifications are being minimized, however, major modifications intended to meet safety requirements are being performed.
September 1980 The unit two reactor shutdown sequence     was conducted   in an orderly process on September   5, 1980,   for refueling activities     and routine maintenance to plant equipment. The refuel activities involve disassembly of Unit         2 reactor for refueling operation with reactor startup       scheduled   for October 26, 1980.
68 ELECTRICAL MAINTENANCE
The routine maintenance involves inspection       and repairs to major components   and safety systems within the plant.       The initial containment entry was conducted   at 1:05 P.H. on September   6, 1980.
The planned   duration for the Unit   2 cylce 3 refuel outage is   49 days. The pre-planned schedule shows that turbine inspection and maintenance work sequence as the     critical work path, a   fix'st at Browns Ferry Nuclear Plant. In order to prevent the outage duration from exceeding the         49 day schedule,   non-curcial modifications are being minimized, however, major modifications intended to     meet safety requirements are being performed.
 
68 ELECTRICAL MAINTENANCE  


==SUMMARY==
==SUMMARY==
September 1980 Unit 1 There were no major maintenance on CSSC or non-CSSC equipment during the month.Unit 1 tripped when a ground in the wiring to the sudden~pressure relay caused a transformer trip.The ground was cleared and the unit returned to service.A summary of non-CSSC and CSSC maintenance activities is given in the following electrical maintenance summary.Unit 2 Major activities include major maintenance inspections to PCB's 5244 and 5248, inspection of 2A 500 kV transfoxmer, and inspection and repair of leaks on 2B and 2C main transformers.
 
At the close of the month, work is 90%complete on PCB 5248 and 25%complete on PCB 5244.The inspection of 2A main transformer is complete and final testing in progress.Work continues on 2B main transformer.
September     1980 Unit 1 There were no major maintenance           on CSSC   or non-CSSC equipment during the month. Unit 1 tripped   when a ground     in the wiring to the     sudden
The 2B condenser circulating water pump motor failed on September 2.After testing, the motor was sent to the service shop for repairs.The motor is due back in early October.Routine refueling outage activities are in progress.A summary of other non-CSSC and CSSC maintenance activities are given in the following elec-trical maintenance summary.Unit 3 A scram occurred on Unit 3 when returning 480 volt shutdown board 3A to service following changing the tap setting on transformer TS3A.The tap setting was also changed on transformer TS3B and TS3E.There was no 69 ELECTRICAL MAINTENANCE
~
pressure relay caused     a transformer     trip. The ground was cleared and the unit returned to service.           A summary   of non-CSSC and CSSC maintenance activities is given in the following electrical               maintenance   summary.
Unit 2 Major activities include     major maintenance       inspections to PCB's   5244 and 5248,   inspection of     2A 500 kV     transfoxmer, and inspection and repair of leaks   on 2B and 2C main     transformers.       At the close of the month, work is 90% complete on   PCB   5248 and 25% complete on PCB 5244.           The   inspection of 2A main transformer is complete and         final testing in     progress. Work continues on   2B main transformer.         The 2B condenser     circulating water pump motor failed   on September     2. After testing, the motor       was sent to the service shop   for repairs.       The motor   is due back   in early October.
Routine refueling outage       activities are in progress.         A summary   of other non-CSSC and CSSC     maintenance activities are given in           the following elec-trical maintenance summary.
Unit 3 A scram   occurred on Unit     3 when   returning   480 volt shutdown board 3A to service following changing the tap setting on transformer TS3A.                   The tap setting was also changed on transformer             TS3B and TS3E. There was no
 
69 ELECTRICAL MAINTENANCE  


==SUMMARY==
==SUMMARY==
(Continued)
(Continued)
September 1980 Unit 3 (Continued) major maintenance on CSSC and non-CSSC equipment.
September 1980 Unit 3 (Continued) major maintenance on   CSSC and non-CSSC equipment. A summary of other non-CSSC and CSSC maintenance   act'ivities is given in the following elec-trical maintenance summary.
A summary of other non-CSSC and CSSC maintenance act'ivities is given in the following elec-trical maintenance summary.Common NONE DROWNS PEit1;YiilUCLHtll PLAIT UHIT 1 ELECTRICAL HAINTENANCE SRBfhRY 1'or the Honth of 0,".te 9/2/8 System Neutron Honitor in Component RBH Bypass Switch Nature of Haintenance RBH Bypass Switch on panel 9-5 needs repair-ing E ect on Sa c Operation of The Reactor NONE Cause of Halfunction RBH Switch Bad Results of Halfunction Switch would not go in bypass Action Taken To Preclude Recurrence Replaced RBH switch.Checked switch for proper operation.
Common NONE
Switch functioned okay.TR8 179518 9/23/80 RNR ECV-74-71 RHR valve 1.-74-71 won'run Unit in limiting condition for operation (TS.3.5.8.7)
 
Hotor burned up Valve inoperable.
DROWNS   PEit1;YiilUCLHtll PLAIT UHIT 1 ELECTRICAL HAINTENANCE SRBfhRY 1'or the Honth     of E  ect  on Sa c                                                Action Taken 0,". te   System    Component    Nature of    Operation of            Cause of          Results of          To Preclude Haintenance    The Reactor          Halfunction        Halfunction          Recurrence 9/2/8   Neutron   RBH Bypass RBH Bypass         NONE             RBH Switch Bad Switch would not go Replaced RBH switch.
Performed EHI 71.Replaced old motor.Performed EHI 18.Valve now functioning properly.TR8 165755 LER No.BPRO 50-259/8072 o URU!'UR"URRT UUCUElS PXRUT UUXT 2 IQ,XNTENANCE SUtkfARY For the Honth of September]9 80 D.".te System Component Nature of Haintenance E ectonSae Operation of The Reactor Cause of Halfunction Results of~Rfal f tmc tion Action Taken To Preclude Recurrence 9/21/80 RBCCH 2B RBCCH Pump 2B RBCCH pump motor trips out.Sparks reported com-ing from the motor.NONE tutor failed.i Loss of 2B RBCCH pump motor.Hotor repaired at'ervice shop, then returned to service.TlU/178647, 160689 9/22/80 RHR FCV-74-24 Valve will not cycle.NONE Hire loose in alve would not cycle motor starter>overload assembly Tightened loose wire on overload assembly in motor starter.Valve operated okay.TRt 1'78632  
Honitor in Switch      Switch on                                              in bypass          Checked switch for panel 9-5                                                                  proper operation.
~~I~~~~~~~~~~~~I~~~~~~I ol I~~I I~ol~~~~~~~~~~I I I~~~~~~~~~~I l I<<I'l o~~~~ol~~~o~~~~~~~~~I I~~~~~~~~~~'/l~~~~~I~~I~l'~~~o~~~~~I~o~I~~o~I o~~~~~~~~~~~I I o~~~
needs  repair-                                                            Switch functioned ing                                                                        okay. TR8 179518 9/23/80 RNR       ECV-74-71   RHR valve     Unit in limiting Hotor burned      up Valve inoperable. Performed EHI 71.
NON-CSSC E UIPMENT URONNS PERRY NUCLEAR PLRNT UNIT ELECTRICAL MAINTENANCE
1.-74-71 won'   condition for                                             Replaced old motor.
run            operation                                                 Performed EHI 18.
(TS.3.5.8.7)                                               Valve now functioning properly. TR8 165755 LER No. BPRO 50-259/
8072 o
 
URU!'UR "URRT UUCUElS PXRUT UUXT       2 IQ,XNTENANCE SUtkfARY For the Honth of September       ]9 80 E  ectonSae                                                        Action Taken Nature of    Operation of        Cause of              Results of            To  Preclude D.". te   System   Component ftmc tion        Recurrence Haintenance   The Reactor       Halfunction           ~Rfal 2B                                                                          i 9/21/80 RBCCH   RBCCH Pump 2B RBCCH pump       NONE         tutor failed.     Loss   of   2B RBCCH Hotor repaired motor  trips                                        pump   motor.                   shop, then at'ervice out. Sparks                                                                returned to service.
reported com-                                                              TlU/ 178647,   160689 ing from the motor.
9/22/80 RHR     FCV-74-24   Valve will         NONE         Hire loose in       alve would not cycle Tightened loose wire not cycle  .                      motor starter>                           on overload assembly overload assembly                         in motor starter.
Valve operated okay. TRt 1'78632
 
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URONNS PERRY NUCLEAR PLRNT       UNIT ELECTRICAL MAINTENANCE  


==SUMMARY==
==SUMMARY==
Pot tbe Noetb oP SePtelnber IP SO DaLe 9/13@0 RWCU System Com onent 2A RMCU demin.Nature of Maintenance 2A RWCU demin.F valve will not open during precoat step.Cause of Malfunction or Maintenance Action Step switch not working properly.Corrective Action Adjusted step switch.Checked okay.TR8 169260 9/17/80 Reactor water cleanup.2B reactor water clean-up.pump motor 2B RMCU pump'motor locked up Motor bad.Replaced with rebuilt motor.Checked okay, Tlg 180452 9/19/80 Main steam FCV-1-59 Valve will not operate.Motor burned up and torque switch bad.Replaced motor an'd torque switch.Performed EMI 18.Checked okay,-TR8 160644 9/21/80 FCV-69-8 RMCU demin, bypass valve will only, open and close.Broken limit switches in valve FCV-2-69-8.
 
Replaced broken limit switches.Performed EMI 16 and 18.Checked okay.T1UI 169299 UROIINS PERRY NUCLEAR PLAN'1'NLT NON-CSSC E UZPlmNT ELK'CTRXCAL ifAXHTENANCH SUiQlARY pot tha Hooth of RapteaIbet 19 80 l)a te 9/25/80 RWCU System Com onent 3A RMCU demin.stepping switch Nature of Haintenance 3A RMCU demin.stepping switch needs to be cleaned and checked.Cause of Halfunction or Haintenance hction Switch.contacts dirty.-" Corrective Action 1 Inspeated switches and cleaned contacts.Checked okay.Tip 179.318 76 MECHANICAL MAINTENANCE SALARY September 1980 Unit 1 On September 19, 1980, the 1B RFP was experiencing high vibration problems.The RFP coupling was inspected and was found to be low in lub-ricant.The RFP coupling was disassembled, cleaned, and filled with new lubricant.
NON-CSSC E UIPMENT Pot tbe Noetb oP SePtelnber   IP SO Nature of          Cause  of Malfunction or onent    Maintenance          Maintenance Action                    Corrective Action DaLe           System    Com 9/13@0   RWCU         2A RMCU       2A RWCU demin. F       Step switch not working     Adjusted step switch. Checked demin.        valve  will not      properly.                    okay. TR8 169260 open  during precoat step.
This corrected the vibration problem.The mechanical controls on all RFP turbines were inspected for proper lubrication and cleanliness.
9/17/80   Reactor water 2B reactor   2B RMCU pump           Motor bad.                   Replaced with rebuilt motor.
Unit 2 Twenty-three of the CRD scram pilot solonoid valves were rebuilt during the month.A number of valves throughout the turbine and reactor building were worked on for packing leaks, broken diaphragms and o-rings.Some of the small hand control valves were replaced due to steam cuts around bonnet gasket surfaces.The 2A RCW booster pump discharge check valve was replaced because the old discharge check valve was stuck in the open position and beyond repair.The 2B reactor water cleanup demineralizer resin trap was replaced on'September 6, 1980.2A RCW pump isolation valves were dis-assemble, cleaned and reassembled.
cleanup.      water clean- 'motor locked  up                                  Checked okay,   Tlg 180452 up.pump motor 9/19/80   Main steam   FCV-1-59     Valve will not         Motor burned up and         Replaced motor an'd torque switch.
The RCIC turbine and pump were inspected during the last week of September and all outage work was completed September 30, 1980.The Unit 2 HPCI work is behind schedule due to delayed shipment of the new pedestal.The disassembly work has begun on the removal of the temporarily repaired pedestal performed earlier this year due to water hammer damage.The RHR and recirculation system valves graffoil packing was adjusted during the month.
operate.              torque switch bad.          Performed EMI 18. Checked okay,
77 MECHANICAL MAINTENANCE
                                                                                        -
TR8 160644 9/21/80                 FCV-69-8     RMCU   demin, bypass   Broken  limit switches in  Replaced broken limit switches.
valve   will only,     valve FCV-2-69-8.           Performed EMI 16 and 18. Checked open and  close.                                  okay. T1UI 169299
 
UROIINS PERRY NUCLEAR     PLAN'1'NLT NON-CSSC E UZPlmNT                       ELK'CTRXCAL ifAXHTENANCH SUiQlARY pot tha Hooth of RapteaIbet       19 80 Nature of          Cause  of Halfunction or l)a te         System    Com onent    Haintenance          Haintenance hction                    Corrective Action 1
9/25/80     RWCU         3A RMCU     3A RMCU demin.           Switch .contacts   dirty. - "
Inspeated switches and cleaned demin.      stepping switch                                        contacts. Checked okay. Tip stepping    needs  to be                                          179.318 switch      cleaned and checked.
 
76 MECHANICAL MAINTENANCE SALARY September   1980 Unit 1 On September   19, 1980, the 1B     RFP was   experiencing high vibration problems. The RFP   coupling   was inspected and     was found   to be low in lub-ricant. The RFP   coupling   was disassembled,     cleaned,   and filled with new lubricant. This corrected the vibration problem.           The mechanical   controls on all RFP turbines were inspected for proper lubrication and cleanliness.
Unit 2 Twenty-three of the     CRD scram   pilot solonoid   valves were   rebuilt during the month.     A number   of valves throughout the turbine         and reactor building   were worked on   for packing leaks, broken       diaphragms and     o-rings.
Some of the small   hand control valves were replaced         due to steam cuts around bonnet gasket surfaces.       The 2A   RCW booster   pump discharge check valve     was replaced because the old discharge check valve was stuck               in the   open position and beyond   repair. The 2B reactor water cleanup demineralizer resin trap was replaced on 'September 6, 1980.         2A RCW pump   isolation valves     were dis-assemble,   cleaned and reassembled.       The RCIC   turbine and pump were inspected during the last week of September and           all outage work was completed September 30, 1980. The Unit 2 HPCI work   is behind schedule due to delayed shipment of the   new pedestal. The disassembly     work has begun on the removal of the temporarily repaired pedestal performed earlier this year due to water hammer damage.     The RHR and   recirculation system valves graffoil packing was adjusted during the month.
 
77 MECHANICAL MAINTENANCE  


==SUMMARY==
==SUMMARY==
(Continued)
(Continued)
September 1980 Unit'3 Unit 3 ran essentially all month with only minor repair work with the exception of repair work to 3B MSIV.The MSIV had closed too fast during a routine surveillance instruction test.The unit was removed from service September 13, 1980, for inspection and repair to the MSIV.The valve operator was found to be approximately three quarts low of oil.Oil was added to the operator and the valve functioned properly.No sign of oil was evident on the floor or around the valve at the initial inspection.
September   1980 Unit'3 Unit 3 ran essentially   all month   with only minor repair work with the exception of repair work to     3B MSIV. The MSIV had closed too   fast during   a routine surveillance instruction test.         The unit was removed from service September 13, 1980, for inspection and repair to the MSIV.
3B CRD filter required replacing on September 25, 1980.The Unit 3 RCIC had to have three quarts of oil added on'September 8, 1980.The outboard packing on 3A fuel pool cooling pump required tightening on September 22, 1980.Common Scheduled maintenance of all service air compressors were performed September 24, 1980.No significant problems were found.The raw cooling water.lines to the CRD pump bearing were cleaned during the first part of the month.The 1B RHRSW pump vibration reading was above the acceptable limits on September 25, 1980, and the pump was pulled and disassembled during'the last few days in September.
The valve operator   was found   to be approximately three quarts low of       oil.
CSSC E UXP:kk;I!T 2'I IKCIU.NXCAL HAXNTENAN"F.
Oil was added   to the operator and the valve functioned properly.           No sign of oil was   evident on the floor or around the valve at the         initial inspection.
SUIQ4<RY DATE 9/22/80 SYSTP~I RCTC CC~!PONENT Turbine exhaus rupture disk NATUIIK OP E'i1.Vi TENAi ICE Ruptured disk EFFECT ON SEVE OE'EBATXO:I OF TIIE-RI~CTOR none CAUSE OP I!.'iLPUNCTXON old disk ruptured RESULTS OF I'ALFUNCTXON Ruptured disk ACZXON TAI'EN'19 PRECLUDE RECURRENCF.
3B CRD   filter required   replacing on September 25, 1980.       The Unit 3 RCIC had to have three quarts of     oil added   on 'September 8, 1980. The outboard packing on   3A fuel pool cooling   pump   required tightening on September 22, 1980.
Replaced disk with new one TR 103732 CSSC EOUXPH 2!T HECHAKXCAL KXINTENANCE SUGARY 3 BATE SYSTBf CGiaiPONEN T iB.'L'URE OF KXXNTENAN CE EFFECT ON SAFE OPERATXO:i'F 1dE REACTOR CAUSE OF Y~LFUNCTION RESULTS OF NALFUNCTXGN ACTION TAl:i;N'10 PRECLUDE RECURRENCE 9/17/80 Fuel pool coolin 3A FPC pump Outboard pack-None in Packing leak Packing leak Adjusted packing TR 178817 1 I.'02-CSSC~EUIPl KHT lKCHANICAI, MLU"HA11CE SLMQRY For the ltoeth of September tp 80 Date S stem Com nnent Nature of?faintenance Cause of 14alfu>>ction or llaintenance Action Corrective Action 9/12/80 Radwaste FSV-77-19 Bad solenoid valve Bad solenoid valve Replaced solenoid valve TR 182079 9/19/80 Reacotr Feed-um 1B RFP High vibration Lube oil dried out in cou lin Cleaned coupling and put new oil TR 103114 t''0:4-CSSC~F.
Common Scheduled maintenance     of all service air compressors were performed September   24, 1980. No significant   problems were found.     The raw cooling water. lines to the   CRD pump   bearing were cleaned during the       first part of the month. The 1B RHRSW pump   vibration reading     was above   the acceptable limits on September   25, 1980, and the pump was pulled and disassembled during 'the last few days in September.
UIPl KHT>?EC?>AHICgZ.
 
HAP?T"HAHCE SEQfAPY For the?fonth of September 19 80 Date S stem Com onent Nature of?fai.n tenance Cause of Malfunction or llaintenance Action Corrective Action 9/80 RCW 2A RCM pump isolation valves Isolation valve 2-24-516 A,B,&C ,2-24-520 A,B,&C would not close Isolation valve out of adjustment S Removed, cleaned, and a'djusted, and reinstalled TR 119083, 119085, 119086.9/28/80 Hain Steam PCV 1-167 Valve binding Valve binding Cleaned, lubricated, and adjusted valve TR 166667 9/24/80 9/25/80 Heater drains and vents LCV-6-73B Heater drains LCV-6-73A and vents Bad o-rings and diaphragm Bad o-rings and diaphragm Bad o-rings and diaphragm Bad o-rings and diaphragm Replaced o-rings, diaphragm.
2
Adjusted packing and lubricated ste TR 166658 Replaced o-rings, diaphragm.
                                                                    'I CSSC E UXP:kk;I!T                               IKCIU.NXCAL HAXNTENAN"F. SUIQ4<RY EFFECT  ON SEVE                                          ACZXON TAI'EN DATE SYSTP~I       CC~!PONENT   NATUIIK OP         OE'EBATXO:I OF         CAUSE OP            RESULTS OF    '19 PRECLUDE E'i1.ViTENAi ICE  TIIE -RI~CTOR     I!.'iLPUNCTXON         I'ALFUNCTXON   RECURRENCF.
Adjusted packing and lubricated sten TR 166659 9/25/80 Heater drains and vents 9/25/80 Heater drains and vents 9/10/80 Feedwater LCV-6-62A LCV-6-62B HCV-3-211A Bad o-rings and diaphragm Bad o-rings and diaphragm Bad seat in valve Bad o-rings and diaphragm Bad o-rings and diaphragm Bad seal in valve Replaced o-rings, diaphragm.
9/22/80 RCTC        Turbine exhaus Ruptured          none              old disk            Ruptured disk    Replaced disk with rupture disk  disk                                  ruptured                              new one TR 103732
Adjusted packing and lubricated ste TR 166661 Replaced o-rings, diaphragm.
 
Adjusted packing and lubricated stem TR 166662 Replaced valve TR 180437 9/9/80 Heater drains and vents HCV-6-418A Bad seat in valve Valve seat worn Replaced valve TR 180438 82 INSTRUMENT MAINTENANCE SALARY September 1980 Unit 1 There were no major instrument maintenance or modification activities on Unit 1 this month.Unit 2 Extensive time and effort has been expended this month on refueling outage related routine calibration, maintenance and modification activities.
3 CSSC EOUXPH 2!T                             HECHAKXCAL KXINTENANCE SUGARY EFFECT ON SAFE                                      ACTION TAl:i;N BATE SYSTBf       CGiaiPONEN T   iB.'L'URE OF OPERATXO:i'F       CAUSE OF           RESULTS OF   '10 PRECLUDE KXXNTENANCE    1dE REACTOR      Y~LFUNCTION        NALFUNCTXGN    RECURRENCE 9/17/80 Fuel pool   3A FPC pump   Outboard pack- None             Packing leak     Packing leak coolin                                                                                        Adjusted packing in                                                                  TR 178817
Major areas include: Installed the Hays-Republic oxygen and hydrogen analyzer system, including writing of new surveillance instructions, maintenance procedures, and initial calibrations.
 
Implemented DCR 1937 by work plan 6617.This modification replaces six mercoid pressure switches in the condensate system.Implemented DCR 1892 by work plant 9818.This modification prevents feed-water control loops from reading downscale upon meter failure.Replaced twelve LPRM detector assemblies due to end of life criteria.An additional LPRM assembly had to be replaced due to being irreparably damaged during preliminary LPRM activities.
1 I.'02-CSSC~EUIPl KHT                       lKCHANICAI, MLU"HA11CE SLMQRY For the ltoeth of September     tp 80 Nature of         Cause of 14alfu>>ction or Date            S stem    Com nnent    ?faintenance        llaintenance Action               Corrective Action 9/12/80   Radwaste       FSV-77-19   Bad solenoid valve   Bad solenoid valve       Replaced solenoid valve TR 182079 9/19/80     Reacotr Feed- 1B RFP       High vibration       Lube oil dried out in   Cleaned coupling and put new oil um                                              cou lin                      TR 103114
All thirteen assemblies are of the GE NA-200 breeder types.Representatives from the General Electric Company in conjunction with Instrument Maintenance personnel conducted extensive testing on the EHC system to resolve the tubing vibration and servo valve''a'ilure problems.Realignment and modifications include: increase the dampening on the fluid pressure sensors, changed the valve movement operating point to the second slope of the Diode Function Generator and attached the sensing line to the wall at four foot intervals.
 
83 INSTRIRKNT MAINTENANCE
t''0:4-CSSC~F. UIPl KHT                       >?EC?>AHICgZ. HAP?T"HAHCE SEQfAPY For the ?fonth of     September   19 80 Nature of          Cause of Malfunction or Date               S stem     Com onent     ? fai.n tenance       llaintenance Action                   Corrective Action S
9/80         RCW           2A RCM pump   Isolation valve          Isolation valve out of      Removed,  cleaned, and a'djusted, and isolation      2-24-516 A,B,&C         adjustment                  reinstalled valves        ,2-24-520 A,B,&C                                         TR 119083, 119085, 119086 would not close
.9/28/80       Hain Steam   PCV 1-167     Valve binding           Valve binding               Cleaned, lubricated,   and adjusted valve TR 166667 9/24/80       Heater drains LCV-6-73A     Bad o-rings     and     Bad o-rings and diaphragm Replaced o-rings, diaphragm.
and vents                    diaphragm                                            Adjusted packing and lubricated ste TR 166658 9/25/80        Heater drains LCV-6-73B      Bad  o-rings    and    Bad  o-rings  and diaphragm Replaced o-rings, diaphragm.
and vents                  diaphragm                                            Adjusted packing and lubricated sten TR 166659 9/25/80       Heater drains LCV-6-62A     Bad   o-rings     and     Bad o-rings and diaphragm Replaced  o-rings, diaphragm.
and vents                  diaphragm                                             Adjusted packing and lubricated ste TR 166661 9/25/80        Heater drains LCV-6-62B      Bad o-rings     and     Bad o-rings and diaphragm Replaced o-rings, diaphragm.
and vents                  diaphragm                                            Adjusted packing and lubricated stem TR 166662 9/10/80        Feedwater    HCV-3-211A    Bad  seat in valve      Bad  seal in valve          Replaced valve TR 180437 9/9/80         Heater drains HCV-6-418A   Bad   seat in valve       Valve seat worn             Replaced valve and vents                                                                            TR 180438
 
82 INSTRUMENT MAINTENANCE SALARY September   1980 Unit 1 There were no major instrument maintenance       or modification   activities   on Unit 1 this month.
Unit 2 Extensive time and     effort has been expended   this month on   refueling outage related routine calibration, maintenance         and modification activities.       Major areas include:
Installed the Hays-Republic       oxygen and hydrogen analyzer system,     including writing of   new surveillance instructions, maintenance procedures,         and initial calibrations.
Implemented   DCR 1937   by work plan 6617. This modification replaces six mercoid pressure switches     in the condensate system.
Implemented   DCR   1892 by work   plant 9818. This modification prevents feed-water control loops from reading downscale upon meter         failure.
Replaced twelve     LPRM detector assemblies due to     end of life criteria.     An additional   LPRM assembly had to be replaced due to being       irreparably   damaged during preliminary     LPRM activities. All thirteen     assemblies   are of the   GE NA-200 breeder   types.
Representatives     from the General   Electric Company in conjunction with Instrument Maintenance personnel conducted extensive testing on the             EHC system to resolve the tubing vibration and servo valve''a'ilure problems.           Realignment and modifications include:     increase the dampening on the     fluid   pressure sensors, changed the valve movement operating point to the second slope of the Diode Function Generator and attached the sensing       line to the wall at four foot intervals.
 
83 INSTRIRKNT MAINTENANCE  


==SUMMARY==
==SUMMARY==
(Continued)
(Continued)
September 1980 Unit 3 N There were no major instrumentation maintenance or modification activities on Unit 3 this month.Common DCR's were initiated this month concerning the following modifications:
September   1980 Unit 3 N
-1.Replacement of FE-66-111 in the off-gas system, due to the flow element not being reliable and spare parts not available.
There were no major instrumentation maintenance or modification           activities on Unit 3 this month.
2.Enclose and air condition the off-gas hydrogen analyzer area.This modification will imporve the environment of the electronics and therefore improve the reliability of the system.3.Incorporate additional HPCI and RCIC testing parameters'into the Real-time evaluation, monitoring and analysis system.4.Replacement of the freestanding E-Field mounted on the face of pilars at the intake pumping station with a microwave transmitter and receiver system.5.Extending the E-Field in sectors 4 and 5 along the wingwalls of the intake to the waterline.
Common DCR's were   initiated this month concerning the       following modifications:
6.Installation of additional standby batteries in the PERIM-ALERT and Wells Fargo system to sustain operation for at least 24 hours following a power failure.This modification is due to NRC specification WA-00450B.
    -1. Replacement   of FE-66-111 in the off-gas system,       due to the flow element not being   reliable and spare   parts not available.
INSTR12KNT MAINTENANCE SUKfARY (Continued)
: 2. Enclose and   air condition the off-gas hydrogen analyzer area.       This modification   will imporve the environment of the electronics       and therefore   improve the reliability of the system.
September 1980 Com uter S stem System availability for the units 1 and 2, and unit 3 process computer was 98.47%and 99.86%respectively.
: 3. Incorporate additional   HPCI and RCIC     testing parameters'into the Real-time evaluation, monitoring and analysis system.
Downtime was due to analog scanner problems which was resolved by replacing 25 leaking diodes.System availability for the PRIME computer was 100%with only routine mainte-nance being performed.
: 4. Replacement   of the freestanding E-Field mounted on the face of pilars at the intake   pumping   station with   a microwave transmitter and receiver system.
System availabiltiy for the RRRMS PDP 1134 computer was 99.93%.Downtime was due to high temperature in the computer room (1/2 hour).The Instrument Maintenance section in conjunction with the Controls&Test Section has installed two NOVA 1200 computers in the secondary alarm station to monitor the RUSCO MAC S40.This system will allow report generating and up-to-'date cross reference of all coded data form the cardkey system.Securit S stems RUSCO Card Access S stem-On September 2, we experienced another system malfunction due to power transfer.As of this date, we still have not received the recommendations from Chattanooga or Knoxville for an uninterruptable power supply to help stabilize our power source.CCTV-Browns Ferry now has 18 CCTV cameras in operation.
: 5. Extending the E-Field in sectors     4 and 5   along the wingwalls of the intake to the waterline.
These cameras and associated monitors are requiring daily maintenance for adjustment and re-location for security and fuel pool activities.
: 6. Installation of additional   standby batteries     in the PERIM-ALERT and Wells Fargo system to sustain operation for at least         24 hours following a power   failure. This modification is     due to   NRC specification   WA-00450B.
Intrusion Detection Hells Far o-Performed routine maintenance and repair on MP2 modules, AS24 boards, and Cu-3 boards.Failure rates on these components are much higher than expected.
 
85 INSTRUMENT MAINTENANCE St&MARY The following instrument Maintenance Summary tabulates man-hours expended on instrument maintenance, calibration, loop checks, and work plans for various plant systems.Svs tern Main Steam Unit Total 3 M-H 30 2.3.5.6.12.18.23.24.25.26.27.28.31.32.33.34.35.37.39.40.43.44.46.47.53.56.58.63.65.66'7.68.69.70.71.73.74.75.Condensa te Ho 0 Reactor Feedwater Extraction Steam Heater Drain and Vent Auziliarv Boiler Fuel Oil RHR Service Water Raw Coolin Water Raw Service Water High-Pressure Fire Protection Condenser Circulatin Water Water Treatment Air Condition Coolin and Heatin Control Air Service Air Vacuum Primin Generator H dro en Coolin Gland Seal Water COo Station Draina e Sam lin and Water Oualitv Buildin Heatin Feedwater Control Turbo enerator Control Demineralizer Backwash Air Temo rature Monitorin Biothermal Research Standbv Li uid Control Prima~Con tainmen t Standbv Gas Treatm nt Off-Gas Eeer enc E nionen~ttoolin
INSTR12KNT MAINTENANCE SUKfARY       (Continued)
!Pater Reactor Water Recirculation Reactor Water Cleanup Reactor Buildin Closed Coolin Hater Reactor Core Isolation Coolin Hi~h-Pressure Coolin In ection Residual Heat Removal Core Sorav Isolation Coolin 39 40 21 21 10 51 157 35 43 32 515 320 51 36 10 45 181 102 55 237 12 304 147 49 72 74 51 10 45 71 28 12 28 10 62 94 207 173 10 134 468 32 340 187 55 125 34 32 86 INSTRUMENT MAINTENANCE S'CHARY (Continued)
September 1980 Com uter S stem System   availability for     the units 1 and 2, and   unit 3 process computer was 98.47% and 99.86%   respectively.       Downtime was due to analog scanner     problems which was resolved by replacing 25 leaking diodes.
S stem Unit Total M-H 76.77.78.80.82.84.85.90.92.Containment Inertin Radvaste Fuel Pool Coolin and Demineralizin Prima Containment Coolin Standb Diesel Generator Containment Air Dilution Control Rod Drive H draulic Radiation Monitorin Neutron Monitorin 308 1 0 550 228 1086 96.99.Travelin In-Core Probe TIP Recirculation Floe Control Reactor Protection RPIS EHC 26 330 245 24 50 335 259 SI IMI Comouter 4020 Prime RRK 1S 129 313 743 151 1075 504 781 2599 427 1211 313 Pere herials Card Ke intrusion Detection Closed Circuit T.V.Portal Monitors Standards Coolin Towers 321 203 304 256 16 331 49 319 49 319 321 203 304 256 98 654 331 General Instrument Pork Instrument Repair Recorder Maintenance 443 179 32 223 139 761 32 223 General Employee Trainin ADDrentice Trainin H P.Trainin B'.JR Instrumentation)
System   availability for     the PRIME computer was   100%   with only routine mainte-nance being performed.
Trainin"C" Zone Dressout Radiochem 1ab H P Lab TR's Received/Completed Dual Rate Foremen Outa e Sup ort Hand and Foot Monitors X Rav 65 262 100 255 45 45 96 86 17 177 308 12 211 260 33 27 62 25 47 61 204 8 127 260 125 111 20 307 774 39 438 520 255 299/269 93 47 17 I.D.Camera Overtime Seismic Monitors'2 292 239 30 5003 42 441 5975 30 CSSC E UIPlfENT BROWS l FERkY'UCLEAR PLANT UNIT 1,2,3 INSTRUI'IENT MAINTENANCE SUI MARY I FOR THE HONTII OF September 19 80 DATE SYSTEH Unit 1 COMPONENT NATURE OF MAINTENANCE EFFECT ON SAFE OPERATION OF THE REACTOR CAUSE OF MALFUNCTION RESULTS OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE 9-2 Containment Inerting H A-76-37 2 Replace None Faulty Heter Alarm would not reset None 9-24 Unit 2 P rimary Containment Reactor Building Closed Cool-ing Hater PDT-64-138 TI-70-56 Calibrate Replace None None Zero'Shif t Did Not Indicate with Redundant Broken Indicator Did Not Indicate None None 9-23 lligh Press-ure Fire Protection PS-26-78J Calibrate None Instrument Drif t Setpoint Incorrect None Unie 3 9-25 Emergency Equipment Cooling Mater RllR Service Hater FI-67-9A-12A PT-23-11 FH-23-42 FH-23-48 Calibrate Calibrate Calibrate Calibrate None None None None Zero Shif t Zero Shift Zero Shift Zero Shift Indicated Low Flow Indicated Low Pressur Indicated Low Flow Indicated Low Flow None None None None 88 Radioactive Li uid Effluents September 1980 1.Gross Radioactivit a)Total Release (1)b)Average Diluted Concentration Released c)Maximum Concentration Released d)Percent of Applicable Limit (20 Ci/quarter)
System   availabiltiy for     the RRRMS PDP 1134 computer was 99.93%.     Downtime was due   to high temperature in the computer room (1/2 hour).
Units Curies uCi/ml uCi/ml 1.36E+00 3.16E-08 1.91E-07 6.80E+00 2.Tritium a)Total Release b)Average Diluted Concentration Released c)Percent of Applicable Limit (3E-03 uCi/ml)3.Dissolved Noble Gases (2)Curies uCi/ml 1.93E+00 4.49E-08 1.50E-03 a)Total Release b)Average c)Percent of Applicable Limit (6E-06 uCi/ml)Curies uCi/ml<3.07E-02<7.12E-10<1.19E-02 4.Gross Al ha Radioactivit a)Total Release b)Average Diluted Concentration Released 5.Volume of Li uid Waste to Dischar e Canal 6.Volume of Dilution Water 7.Isoto es Released Curies uCi/ml Liters Liters Ci 3.96E-05 9.19E-13 2.87E+06 4.33E+10 Ba/La-140 Co-58<5.15E-04<1.85E-03 (1)Based on pre-release analyses which are not decay corrected (2)includes Xe-133, Xe-135, and others (3)Released on basis of MPC 89 Radioactive Li uid Effluents (Continued)
The Instrument Maintenance section in conjunction with the Controls             & Test Section has installed two       NOVA   1200 computers in the   secondary alarm station to monitor the   RUSCO MAC   S40. This system will allow   report generating   and up-to-
September 1980 Isoto es Released (Continued)
                                    '
Units Co-60 Cr-51 Cs-134 Cs-137 Fe-59 I-131 Mn-54 Mo-Tc-99m Na-24 Nb-95 Sr-89 Sr-90 Zn-65 Zr-95<1.31E-02<1.56E-02<2.64E-02<3,20E-02<8.01E-04<6.94E-03<2.58E-03<8.39E-04 2.71E-02<1.17E-03 2.98E-03 4.07E-04<1.51E-02<1.25E-03 Others F-18 Cs-136 Cu-64 I-133 7.94E-04<9.02E-04<9.62E-03<2.04E-03 90 Radioactive Liquid Effluents (Continued)
date cross reference of       all coded data form the cardkey system.
Others (Continued)
Securit   S stems RUSCO Card Access   S stem On September   2, we experienced   another system malfunction due to power transfer.         As of this date,   we still have not received the recommendations     from Chattanooga or Knoxville       for an uninterruptable   power supply to help stabilize our power source.
September 1980 Uni ts Mn-56 Sb-122 Sb-124 Xe-133 Xe-135 I-135 Br-82 As-76 Ag-110m Sb-125 As-74 Ci<1.47E-04<3.53E-03<7.03E-04<1.51E-02<1.17E-02<6.82E-03<1.07E-03<3.78E-03<2.02E-03<7.39E-04<7.39E-04 NOTE: Symbol<indicates sums of nuclide activity influenced by values representing threshold limit of analytical sensitivity.
CCTV Browns   Ferry   now has 18 CCTV cameras     in operation. These cameras and associated   monitors are requiring daily maintenance for adjustment and re-location for security     and   fuel pool activities.
Thus, re-ported values are conservatively higher than actual release.
Intrusion Detection Hells Far       o Performed   routine maintenance   and repair on MP2 modules,   AS24 boards, and Cu-3 boards.       Failure rates   on these components are much higher than expected.
91 Airborne Releases (1)Summation of All Releases September 1980 Unit This Month A.Fission and Activation Gases 1.Total Release 2.Average release rate for period 3.Percent of Technical Specification limit Ci uCi/sec.<1.43E+04<4.73E+03 9.46E+00 B.Iodines 1.Total Iodine-131 2.Average release rate for period 3.Percent of Technical Specification limit Ci uCi/sec.7.50E-03 2.48E-03 6.21E-01 C.Par ticulates 1.Particulates with half-lives
 
-8 days 2.Average release rate for period 3.Percent of Technical Specification limit 4.Gross Alpha radioactivity uCi/sec.Ci<3.29E-03<1.09E-03 2.7E-01<1.43E-09 D.Tritium 1.Total release 2.Average release rate for period 3.Percent of Technical Specification limit 4.Ground Level Release 5.Elevated Release Ci uCi/sec.Ci 7.07E+00 2.34E+00 1.87E+00 6.74E+00 3.31E-01 (1)Reporting period-35 days 92 Elevated Releases Airborne Releases (Continued)
85 INSTRUMENT MAINTENANCE St&MARY The   following instrument Maintenance     Summary   tabulates man-hours expended on instrument maintenance,           calibration, loop checks,   and work plans for various plant systems.
September 1980 A.Fission Gases 1.Krypton-85 2.Krypton-85m 3.Krypton-87 4.Krypton-88 5.Xenon-133 6.Xenon-135 7.Xenon-135m 8.Xenon-138 Unit Ci Ci Ci Ci This Ifonth 7.73E+00 2.05E+03<8.19E+02<3.18E+03 6.28E+03<1.88E+02<8.17E+01<4.60E+02 Others (specify)9.Argon-41 Unidentified Total for Period Ci Ci Ci<3.13E001 NA<1.31E+04 B.Iodines l.Iodine-131 2.Iodine-133 3.Iodine-135 Total for Period Ci 5.18E-03<4.45E-03<3.99E-03<1.36E-02 93 Airborne Releases (Continued)
Unit Total Svs     tern                                                             3       M-H Main Steam                                                      30
September 1980 Elevated Releases C.Particulates l.Strontium-89 2.Strontium-90 3.Cesium-134 4.Cesium-137 5.Barium-140 6.Zirconium-95 7.Niobium-95 8.Cobalt-58 9.Ifanganese-54 10.Zinc-65 11.Tron-59 12.Cobalt-60 Other (speci f y)N/A 13.Lanthanum-140 D.Tritium Total for Period Unit Ci Ci Ci Ci Ci Ci Ci This Month 4.61E-06 3.82E-07<1.03E-05<1.01E-05<6.55E-05<2.19E-05<9.79E-06<1.02E-05<8.85E-06 3.78E-05<2.25E-05 1.73E-05<6.70E-05<2.86E-04 3.31E-01 94 Airborne Releases (Continued)
: 2.       Condensa te  Ho 0                            39    515      74    62
September 1980 Ground Level Releases A.Fission Gases Unit This Month 1.Krypton-85 2.Krypton-85m 3.Krypton-87 4.Krypton-88 5.Xenon-133 6.Xenon-135 7.Xenon-135m 8.Xenon-138 Others (specify)9.Argon-41 Unidentified Ci Ci<3.69E-03<2.78E+01<6.80E+Ol<9.11E+01<1.22E+02<1.85E+02<1.86E+02<4.89E+02<4.14E+01 Total for Period<1.21E+03 B.Iodines l.Iodine-131 2.Iodine-133 3.Iodine-135 Total for Period Ci Ci 2.32E-03<1.79E-03<9.94E-03<1.41E-02 95 Airborne Releases (Continued)
: 3.       Reactor Feedwater
September 1980 Ground Level Releases C.Particulates Unit This Month 1.Strontium-89 2.S trontium-90 3.Cesium-134 4.Cesium-137 5.Barium-140 6.Zirconium-95 7.Niobium-95 8.Cobalt-58 9.Manganese-54 10.Zinc-65 11.Iron-59 12.Cobalt-60 Others (specify)N/A 13.Lanthanum-140 D.Tritium Total for Period Ci Ci Ci Ci 1.93E-06 1.79E-06<1.35E-04 1.30E-04<4.87E-04<2.69E-04<1.21E-04<1.18E-04<1.20E-04<4.98E-04 2.88E-04 4.32E-04<3.94E-04<3.00E-03 6.74E+00 96 Solid Radioactive Waste (1)September 1980 Low Level Shi, ments Approximate Volume of Sludge Shipped 42.1 Cu.M.(1486 Cu.Ft.)Total Curies Shipped Principal isotopes 9/08/80 9/10/80 9/12/80 9/16/80 9/18/80 9/21/80 9/23/80 9/30/80 195.2 MAP, MCP (Dewatered Resins)Dis osal Facilit Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Hi h Level Shi ments Approximate Volume of Sludge Shipped 17.7 Cu.M.(624 Cu.Ft.)Total Curies Shipped Principal isotopes 282.6 MAP, MCP (Dewatered Resins)Dis osal Facilit 9/09/80 9/15/80 9/19/80 9/24/80 Barnwell, SC Barnwell, SC Barnwell, SC Barnwell, SC Footnotes on next page.
: 5.       Extraction    Steam
: 6.       Heater Drain and Vent                          40      320
: 12.       Auziliarv Boiler
: 18.       Fuel Oil
: 23.       RHR Service Water                                      51      51
: 24.        Raw Coolin Water
: 25.       Raw Service Water
: 26.       High-Pressure Fire Protection
: 27.       Condenser Circulatin Water                              36
: 28.       Water Treatment
: 31.       Air Condition Coolin and Heatin                        10      10
: 32.       Control Air                                    21
: 33.       Service Air
: 34.       Vacuum Primin
: 35.       Generator  H  dro en Coolin
: 37.       Gland Seal Water
: 39.       COo
: 40.       Station Draina    e
: 43.       Sam  lin  and Water    Oualitv                          45      45      94
: 44.       Buildin Heatin
: 46.       Feedwater Control
: 47.       Turbo enerator Control                        21      181            207
: 53.       Demineralizer Backwash Air
: 56.       Temo rature Monitorin                                  102      71    173
: 58.       Biothermal Research                            10                      10
: 63.       Standbv Li uid Control Prima ~ Con tainmen t                          51      55      28    134
: 65.       Standbv Gas Treatm nt 66         Off-Gas                                      157      237            468
      '7.
Eeer enc E nionen~ttoolin !Pater                        12      12      32
: 68.       Reactor Water Recirculation                            304      28    340
: 69.       Reactor Water Cleanup                          35    147            187
: 70.       Reactor Buildin Closed Coolin Hater                    49              55
: 71.       Reactor Core Isolation Coolin
: 73.       Hi~h-Pressure Coolin In ection                  43      72      10      125
: 74.       Residual Heat Removal                                                    34
: 75.       Core Sorav Isolation Coolin                     32                      32
 
86 INSTRUMENT MAINTENANCE S'CHARY (Continued)
Unit Total S stem                                                                  M-H
: 76. Containment Inertin
: 77. Radvaste                                            1 0
: 78. Fuel Pool Coolin and Demineralizin
: 80. Prima      Containment Coolin
: 82. Standb Diesel Generator
: 84. Containment Air Dilution
: 85. Control Rod Drive H draulic
: 90. Radiation Monitorin                            308  550    228    1086
: 92. Neutron Monitorin Travelin In-Core Probe TIP                          26    24      50
: 96. Recirculation Floe Control
: 99. Reactor Protection RPIS                                              330            335 EHC                                                245            259 SI                                            743  1075    781    2599 IMI                                  129      151  504    427    1211 Comouter 4020                      313                            313 Prime RRK 1S Pere  herials              321                            321 Card Ke                            203                            203 intrusion Detection                304                            304 Closed Circuit T.V.                256                            256 Portal Monitors                                    49      49      98 Standards                                      16  319    319    654 Coolin Towers                                331                  331 General Instrument Pork                      443  179    139    761 Instrument Repair                                  32              32 Recorder Maintenance                              223            223 General Employee Trainin                      65  177      61    307 ADDrentice Trainin                            262  308    204    774 H   P. Trainin                                      12      8      39 B'.JR  Instrumentation) Trainin "C" Zone Dressout                            100  211    127    438 Radiochem 1ab                                      260    260    520 H P    Lab                                    255                  255 TR's Received/Completed          45 45    96 86 33 27 125 111 299/269 Dual Rate Foremen                                  62      20      93 Outa e Sup ort                                      25 Hand and Foot Monitors                              47              47 X Rav                                17                            17 I.D. Camera                                                        42 Overtime Seismic    Monitors'2              292      239 30 5003    441    5975 30
 
BROWS l FERkY'UCLEAR  PLANT    UNIT  1,2,3 INSTRUI'IENT MAINTENANCE SUI MARY I
CSSC E UIPlfENT                          FOR THE HONTII OF  September      19 80 NATURE      EFFECT ON SAFE          CAUSE                                  ACTION TAKEN DATE    SYSTEH        COMPONENT    OF        OPERATION OF            OF                  RESULTS OF      TO PRECLUDE MAINTENANCE    THE REACTOR        MALFUNCTION            MALFUNCTION        RECURRENCE Unit 1 9-2    Containment  H 2
A-76-37  Replace            None          Faulty Heter          Alarm would not        None Inerting                                                                          reset P rimary    PDT-64-138    Calibrate          None          Zero 'Shif t          Did Not Indicate        None Containment                                                                        with  Redundant 9-24    Reactor      TI-70-56      Replace            None          Broken  Indicator    Did Not Indicate        None Building Closed Cool-ing Hater Unit 2 9-23    lligh Press- PS-26-78J      Calibrate        None          Instrument  Drift    Setpoint Incorrect      None ure Fire Protection Unie 3 9-25    Emergency    FI-67-9A      Calibrate        None          Zero Shif t          Indicated  Low Flow    None Equipment          -12A Cooling Mater RllR Service PT-23-11      Calibrate        None          Zero  Shift        Indicated  Low Pressur    None Hater       FH-23-42      Calibrate          None          Zero  Shift        Indicated  Low Flow        None FH-23-48      Calibrate         None           Zero Shift        Indicated  Low Flow        None
 
88 Radioactive Li uid Effluents September    1980
: 1. Gross  Radioactivit                                Units a)  Total Release (1)                              Curies    1.36E+00 b)  Average Diluted Concentration Released        uCi/ml    3.16E-08 c)  Maximum  Concentration Released              uCi/ml    1.91E-07 d)  Percent of Applicable Limit (20 Ci/quarter)              6.80E+00
: 2. Tritium a)  Total Release                                  Curies    1. 93E+00 b)  Average Diluted Concentration Released        uCi/ml    4.49E-08 c)  Percent of Applicable Limit (3E-03 uCi/ml)                1.50E-03
: 3. Dissolved Noble Gases (2) a)   Total Release                                 Curies    <3.07E-02 b)   Average                                       uCi/ml    <7.12E-10 c)   Percent of Applicable Limit (6E-06 uCi/ml)              <1.19E-02
: 4. Gross  Al ha  Radioactivit a)   Total Release                                 Curies    3.96E-05 b)   Average Diluted Concentration Released         uCi/ml     9.19E-13
: 5. Volume  of Li uid  Waste to Dischar e Canal        Liters    2.87E+06
: 6. Volume  of Dilution Water                            Liters    4.33E+10
: 7. Isoto  es Released                                    Ci Ba/La-140                                                    <5.15E-04 Co-58                                                        <1.85E-03 (1) Based on  pre-release analyses which are not decay corrected (2) includes Xe-133, Xe-135, and others (3)  Released   on  basis of MPC
 
89 Radioactive  Li uid Effluents (Continued)
September  1980 Isoto es Released (Continued)                          Units Co-60                                              <1.31E-02 Cr-51                                              <1.56E-02 Cs-134                                            <2.64E-02 Cs-137                                            <3,20E-02 Fe-59                                              <8.01E-04 I-131                                              <6.94E-03 Mn-54                                              <2.58E-03 Mo-Tc-99m                                         <8.39E-04 Na-24                                               2.71E-02 Nb-95                                             <1.17E-03 Sr-89                                               2.98E-03 Sr-90                                               4.07E-04 Zn-65                                             <1.51E-02 Zr-95                                              <1.25E-03 Others F-18                                                7.94E-04 Cs-136                                            <9.02E-04 Cu-64                                              <9.62E-03 I-133                                              <2.04E-03
 
90 Radioactive Liquid Effluents (Continued)
September  1980 Others (Continued)                                          Uni ts Ci Mn-56                                                  <1.47E-04 Sb-122                                                <3.53E-03 Sb-124                                                <7.03E-04 Xe-133                                                <1.51E-02 Xe-135                                                <1.17E-02 I-135                                                  <6.82E-03 Br-82                                                  <1.07E-03 As-76                                                  <3.78E-03 Ag-110m                                                <2.02E-03 Sb-125                                                <7.39E-04 As-74                                                  <7.39E-04 NOTE: Symbol <  indicates  sums  of nuclide activity influenced by values representing threshold    limit of analytical sensitivity. Thus, re-ported values are conservatively higher than actual release.
 
91 Airborne Releases (1)
September  1980 Summation  of  All Releases                                Unit  This Month A. Fission  and Activation  Gases
: 1. Total Release                                      Ci  <1.43E+04
: 2. Average release rate    for period            uCi/sec. <4.73E+03
: 3. Percent of Technical Specification      limit          9.46E+00 B. Iodines
: 1. Total Iodine-131                                  Ci    7.50E-03
: 2. Average release rate    for period            uCi/sec. 2.48E-03
: 3. Percent of Technical Specification    limit            6.21E-01 C. Par ticulates
: 1. Particulates with half-lives      8 days              <3.29E-03
: 2. Average release rate    for period            uCi/sec. <1.09E-03
: 3. Percent of Technical Specification    limit             2.7E-01
: 4. Gross Alpha  radioactivity                        Ci  <1.43E-09 D. Tritium
: 1. Total release                                      Ci    7. 07E+00
: 2. Average release   rate for period             uCi/sec. 2.34E+00
: 3. Percent of Technical Specification     limit             1.87E+00
: 4. Ground Level Release                              Ci    6.74E+00
: 5. Elevated Release                                        3.31E-01 (1)  Reporting period   35 days
 
92 Airborne Releases  (Continued)
September  1980 Elevated Releases A. Fission  Gases                              Unit This Ifonth
: 1. Krypton-85                                Ci 7.73E+00
: 2. Krypton-85m                                  2.05E+03
: 3. Krypton-87                                  <8.19E+02
: 4. Krypton-88                                Ci <3.18E+03
: 5. Xenon-133                                    6.28E+03
: 6. Xenon-135                                    <1.88E+02
: 7. Xenon-135m                                Ci <8.17E+01
: 8. Xenon-138                                Ci <4.60E+02 Others (specify)
: 9. Argon-41                                  Ci <3.13E001 Unidentified                                  Ci NA Total for Period            Ci <1. 31E+04 B. Iodines
: l. Iodine-131                                Ci  5.18E-03
: 2. Iodine-133                                  <4.45E-03
: 3. Iodine-135                                  <3.99E-03 Total for Period              <1.36E-02
 
93 Airborne Releases (Continued)
September 1980 Elevated Releases C. Particulates                                    Unit This Month
: l. Strontium-89                                Ci  4.61E-06
: 2. Strontium-90                                    3.82E-07
: 3. Cesium-134                                    <1.03E-05
: 4. Cesium-137                                  Ci <1.01E-05
: 5. Barium-140                                    <6.55E-05
: 6. Zirconium-95                                Ci <2.19E-05
: 7. Niobium-95                                    <9.79E-06
: 8. Cobalt-58                                  Ci  <1.02E-05
: 9. Ifanganese-54                                  <8.85E-06
: 10. Zinc-65                                    Ci  3.78E-05
: 11. Tron-59                                        <2.25E-05
: 12. Cobalt-60                                      1.73E-05 Other (speci fy)
N/A
: 13. Lanthanum-140                                  <6.70E-05 Total for Period          Ci  <2.86E-04 D. Tritium                                          Ci  3.31E-01
 
94 Airborne Releases  (Continued)
September  1980 Ground Level Releases A. Fission  Gases                                Unit This Month
: 1. Krypton-85                                  <3.69E-03
: 2. Krypton-85m                                  <2.78E+01
: 3. Krypton-87                                Ci <6.80E+Ol
: 4. Krypton-88                                  <9.11E+01
: 5. Xenon-133                                    <1.22E+02
: 6. Xenon-135                                    <1.85E+02
: 7. Xenon-135m                                  <1.86E+02
: 8. Xenon-138                                Ci <4.89E+02 Others (specify)
: 9. Argon-41                                    <4.14E+01 Unidentified Total for Period              <1.21E+03 B. Iodines
: l. Iodine-131                                Ci  2.32E-03
: 2. Iodine-133                                  <1.79E-03
: 3. Iodine-135                                Ci <9.94E-03 Total for Period              <1.41E-02
 
95 Airborne Releases (Continued)
September 1980 Ground Level Releases C. Particulates                                    Unit This Month
: 1. Strontium-89                                Ci  1.93E-06
: 2. S trontium-90                                  1.79E-06
: 3. Cesium-134                                    <1.35E-04
: 4. Cesium-137                                  Ci  1.30E-04
: 5. Barium-140                                  Ci <4.87E-04
: 6. Zirconium-95                                  <2.69E-04
: 7. Niobium-95                                    <1.21E-04
: 8. Cobalt-58                                      <1.18E-04
: 9. Manganese-54                                  <1.20E-04
: 10. Zinc-65                                        <4.98E-04
: 11. Iron-59                                        2.88E-04
: 12. Cobalt-60                                      4.32E-04 Others (specify)
N/A
: 13. Lanthanum-140                              Ci  <3.94E-04 Total for Period              <3.00E-03 D. Tritium                                              6.74E+00
 
96 Solid Radioactive Waste (1)
September 1980 Low Level Shi, ments Approximate Volume of Sludge Shipped 42.1 Cu. M. (1486 Cu. Ft.)
Total Curies Shipped                                195.2 Principal isotopes                      MAP, MCP  (Dewatered Resins)
Dis osal  Facilit 9/08/80                                        Barnwell,  SC 9/10/80                                        Barnwell,  SC 9/12/80                                        Barnwell,  SC 9/16/80                                        Barnwell,  SC 9/18/80                                        Barnwell,  SC 9/21/80                                        Barnwell,  SC 9/23/80                                        Barnwell,  SC 9/30/80                                        Barnwell,  SC Hi h Level Shi ments Approximate Volume of Sludge Shipped 17.7 Cu. M. (624 Cu. Ft.)
Total Curies Shipped                                282.6 Principal isotopes                      MAP, MCP  (Dewatered Resins)
Dis osal  Facilit 9/09/80                                        Barnwell,  SC 9/15/80                                        Barnwell,   SC 9/19/80                                       Barnwell,  SC 9/24/80                                       Barnwell,   SC Footnotes on next page.
 
97 Solid Radioactive Waste (Continued)
97 Solid Radioactive Waste (Continued)
September 1980 Slud e Inventor Condensate and Waste Phase Separator Sludge on Hand Cleanup Phase Separator Sludge on Hand 34.0 CU.M.(1199 CU.Ft.)5.7 Cu.M.(200 Cu.Ft.)Drummed Shi ments (2)Total Number of Drums Total Curies Shipped Principal Isotopes Date Shi ed 233 18.2 CR5 1~CS 1 37~ZN65 j C060~MN54~SR90 Dis osal Facilit 9/17/80 9/19/80 Barnwell, SC Barnwell, SC 98 Solid Radioactive Waste (Continued)
September   1980 Slud e Inventor Condensate and Waste Phase Separator Sludge on Hand                                       34.0   CU. M. (1199 CU. Ft.)
September 1980 Boxed Shi ments (2)Total Number of Boxes Total Curies Shipped Principal Isotopes 9/11/80 9/17/80 22 0.1 CR51,CS137,ZN65,C060,i$
Cleanup Phase Separator Sludge on Hand                                          5.7 Cu. M. ( 200 Cu. Ft.)
54,SR90 Dis osal Facilit Barnwell, SC Barnwell, SC (1)All shipments by Sole-use truck.(2)Combination box/drum shipments on these dates.
Drummed Shi ments (2)
Total Number of Drums                               233 Total Curies Shipped                                 18. 2 Principal Isotopes                        CR5 1 ~ CS 1 37 ~ ZN65 j C060 ~ MN54 ~ SR90 Date Shi  ed                                Dis osal     Facilit 9/17/80                                               Barnwell,    SC 9/19/80                                               Barnwell,     SC
 
98 Solid Radioactive Waste (Continued)
September   1980 Boxed Shi ments (2)
Total Number of Boxes                                   22 Total Curies Shipped                                       0.1 Principal Isotopes                          CR51,CS137,ZN65,C060,i$ 54,SR90 Dis osal Facilit 9/11/80                                          Barnwell, SC 9/17/80                                          Barnwell, SC (1) All shipments   by Sole-use truck.
(2) Combination box/drum shipments on these dates.
 
99 Solid Radioactive Waste (Continued)
99 Solid Radioactive Waste (Continued)
September 1980~scmaac Drums Boxes Resin Shipped to Barnwell 1747.5 ft 2292 ft 2110 6149.5 ft Stored Onsite 1650 ft 3100 ft 4750 ft Allotted~sac e 6149.5 ft 6149.5 ft 100 Effluent and Waste Dis osal Monthl Re ort September 1980 Su lemental Information 1.Batch Releases-Li uid Units a)Number of batch release b)Total time period for batch releases c)Maximum time period for a batch release d)Average time period for batch release e)Minimum time period for a batch release Each 32 Minutes 10883 Minutes 783 Minutes 340.1 Minutes 180 2.Batch Releases-Gaseous None 3.Abnormal Releases-Liquid None 4.Abnormal Releases-Gaseous None 101 Resin Usage for September 1980 Resin-Cu.Ft.Powdered Volume Bead Resins Radwaste Floor Drain Filter Waste Demineralizer Waste Filter (1)Fuel Pool Demineralizers 516.0 192.0 16.0 130.0 516.0 192.0 16.0 Reactor Water Cleanu Unit 1 Unit 2 Unit 3 120.0 56.0 12.0 120.0 56.0 12.0 Condensate Demineralizers U it 1 Unit 2 Uni 827.0 198.0 376.0 827.0 198.0 376.0 Totals 2313.0 130.0 2313.0 (1)Total Resin Volume includes 16.0 cu.ft.of Overlay Haterial.(2)Total Resin Volume includes 63.0 cu.ft.of Overlay Haterial.(3)Total Resin Volume includes 20.0 cu.ft.of Overlay Haterial.(4)Total Resin Volume includes 17.0 cu.ft.of Overlay Haterial.
September   1980
102-Powdered Resins%Total Usa e September 1980 Radwaste Usa e Total Floor Drain Filter Waste Filter Reactor Water Cleanu 516.0/2313.0 22.3 192.0/2313.0 8.3 Unit 1 Unit 2 Unit 3 120.0/2313.0 56.0/2313.0 12.0/2313.0 5.2 2.4 0.5 Condensate Demineralizers U it 1 U.it 2"'.it 3 (4)827.0/2313.0 35.8 198.0/2313.0 8.6 376.0/2313.0 16.3 Fuel Pool Demineralizers (1)ALL UNITS 16.0/2313.0 0.7 (1)Total Resin Volume includes 16.0 cu.ft.of Overlay Material.(2)Total Resin Volume includes 63.0 cu.-.ft.of Overlay Material.(3)Total Resin Volume includes 20.0 cu.ft.of Overlay Material.(4)Total Resin Volume includes 17.0 cu.ft.of Overlay Material.
                        ~scmaac Shipped to           Stored        Allotted Barnwell             Onsite        ~sac e Drums 1747.5 ft           1650  ft     6149.5 ft Boxes 2292    ft           3100 ft Resin 2110 6149.5 ft           4750  ft      6149.5 ft
HI=flP f.I LTER I)EH I IIERL I ZER PERFORHfINCE I.INI 7 ONE PEP fEI'IIJER I IHH I I" 1 I.!Vfririftr I!f!5 0 T I'I I I I S C"'1'" I~r I t I I I I I I l 1 I I~I I I I P.IS 28 2S 30<Ot!DEIISHTE DENII!fRHLI/ER PEFF'ORI!IltlCE HYG IIOI!RS gOHJI(P~P-PI-PI-I-IBII.BB IN BERYICE Ciili Of'IIST Olt!IILHTIYF:.
 
EIIEt!ftll CI!Ll!IGE.
100 Effluent and Waste Dis   osal Monthl Re ort September   1980 Su   lemental Information
IS3.'Pl'I/22/HB 6 f liS 7I.........-.-P r Pr--"-Pi---'-I 36.'IB IGS.SO 50.3$97.6I BIZ Pt-I'c I-Pt-P-Pf-Pr: p-p--si'=Iir--I'--" l--.-l'r-Fl---Pr---." rP--"r-Pr P-" I""I Bi I''.P r..I'I...P I I'P I-Pr'r"r'I--" I-Pr-P-.SB'lS 3!1.36 I 06.23 3!1.7 I 9 I.HS PI-P~.P~P P-.Bi.17 IIB.'I'I IH2.29 IIG.I3'I I.20 I I I.I 0 II-el-Pt-I'P r------.'I
: 1. Batch Releases   Li uid                                 Units a) Number   of batch release                           Each    32 b) Total time period for batch releases                 Minutes 10883 c) Maximum   time period for a batch release           Minutes 783 d) Average time period   for batch release             Minutes 340.1 e) Minimum time   period for   a batch release         Minutes 180
--"I-PI-"I'I--PI-P-PI-PI-" I'r PFilCTOR ItilTER Ct.frlltt"I!P PERF'f!RI!HtlCE 7/0/HL'l/10/Bf!9/29/HL'/29/79 3/I/79 II/IP/'10'I/I6/00 9/3l!/Bil it f I.I~r{!P f IIIT.C F-!-'-I'F-F-!'F--F-P I-c r-F---.-.-F----"F-'-F-F--F--.F--F c I-.F--.flB.I, I'I!Ill.DfllltlfRill.t/f:0 VERt ORI!HIICf.
: 2. Batch Releases   Gaseous None
72B.QB 39I.2'I 0/IB/73 P/l3/73 II/IS/I'I IB DflYSi 2S LEGf t!D C-NIGII COIIDIICTIYITY 5-)ll!Bt Sll l<H P"II I Gll VESSiEL N'-I'iltlilr til!tl<E T"NIGII RESIN THile DP 0-OTI!t::-:
: 3. Abnormal Releases   Liquid None
<EXPLHtiHTlON)
: 4. Abnormal Releases   Gaseous None
...YlSSEL Otl STHt!D-BY HITII BLD FRECL'ill i Vf SSCL r"r i-r i r ra 8 5 IIR5 I l t I t r 1 r I 1 I C r I l 1 1~I I IH IS 28 2S 3H<AIIDEHSAIC DEHltlERALIZER PERf'ORHAIKE AYG HOURS 0 P P P P IBB.IB Itl 5CRVICC DiAIE Of'AS'I CllttlllATJVC f.'Lft!El Ji LHAtlftf, I'l7.SS 2/221 7B E C Pi 9l.F~P~...-.P 6.P r?3.Pr P=P r P I I I.I'!.....P 13 fi~.Pf P REACTOR HATER CLEAII-UP PERfARHAHK I'I'I SH IS'l.77 3I.33 I89.37 3I'I.HH ISO.'IH 20.88 l28.9'I 7II.HH I I G.IIH 2IIH.SH 28'l.77 I88.88 l76.91 70.fi7.127.26!2/IIV 10 S/91 08 l2/9/70 21 27/70 6/IO/19 I/I3/79 9/ZG/79 9/IS/70----F-F-F-F-F-F-F-f'UEL FOOL DEtllt!EEL I ZER!'ERC!Il!I!lltlCE
 
'l7.68 l38.92 IIB.OH IO'4.I7 6/3/79 0/3H/08 728.88 S92.93 I2/3/73 DAY5 8 S IH IS 28 2S I J J I I I I I I I LCGEtlD C-HI Gll CAtlDUCT I V IIV 5-Ill cil SlLI<ft P-Hl GII VESSEL DF II"IG!IHTEIIAII<C I"HIGH RCSltl TARP DF 0"OTHER (EXFLAHATIOH)
101 Resin Usage for September   1980 Resin Cu. Ft.
...YC55CL ON 5TIIHD-HY I!IIII OI.D I'PE<OAT 0-UNIT 5HVTDDt JM I~I HI=NP I=I I..I Fl'>I..H I IIEI'L.I ZEC<PERI=flf'tlCINI"E I.IN I 1'l IRI:.E 5EP I EHY~EC)I"188 t EBI5f I fl 0 I O'I I I't 1 PH llR!i I f I S'I T 3'I I l~I~l IH IS 20 (ORDEtlSRTC DCIIIIICRflLI ZER PCRF'ORltRtl<E 30 RVG l!OIIR5 YOttTII P I-26BI.PV Itl SCRYI<E (Ut!ULIIT I VE I60.92 DATE OF'RST CLQ!CttT g!R'IGC l2/29/79 6 L3.P II~I'l P ,Bl 0 2!Il i~B.P!-0 4 IH 0 0 I.O'I 2I..IB~P~P B.r I..P I 3!I~P!P~P I'7$P!IB~RGB<TOP.IIRTER<Lf:Atl-llP PEhVORrfltt<E FIICI, rf!OL Df Hltlf Rtll.I7f R I'ffBJ ORttlttt(C PF IBl3.76 I 06.67 237.3 I S2.56.ISH.I2 I 9 I.50 2'13.39 P 2I G.00 2 IS.'Ll PP IBB.BB ISI.BB f90.2S 27'I.BIS I 0'I.50 2QS.SH I33.2S$3'I.00 I'l7.9i P I~~70.29'll I'l'79 2/7/QH 6/l3/t9 2/IG/QH I/IS/00 IH/2'I/l0 3/S/00 II/9/70 3/S/7'I 7/3l/7PI 720.l!0 li!19.0I 12/3/73 IH DflY5 IS LEGI7ID C-Illfill (OtlDlt(TIVITY 5-IIBGII 5ILI(fl P-lllGII VC55CL Dfi r.-l:BIIOTEt:OR(C T-IIIG)l RE5lll TfibP DP 0-UTI!ER (EX!BLRtiRTIOtt)
Powdered Volume       Bead       Resins Radwaste Floor Drain   Filter                       516.0                  516.0 Waste Demineralizer                                     130.0 Waste   Filter                               192.0                 192.0 Fuel Pool Demineralizers (1)                  16.0                 16.0 Reactor Water Cleanu Unit 1                                       120.0                 120.0 Unit  2                                        56.0                 56.0 Unit  3                                        12.0                 12.0 Condensate   Demineralizers U it 1                                       827.0                827. 0 Unit  2                                      198.0                 198.0 Uni                                          376.0                 376.0 Totals                         2313.0       130.0   2313.0 (1) Total Resin   Volume includes   16.0 cu. ft. of Overlay Haterial.
...VE55CL litt GTItttD-BY It!Tll IILD PRC(URT 0-LM R.OW 106 Fuel Claddin Inte rit Parameters Unit 1 September 1980 Reactor Water Iodines (uCi/sec.)
(2) Total Resin   Volume includes   63.0 cu. ft. of Overlay Haterial.
Date I-131 I-132 I-133 I-134 I-135 9-04-80 9-22-80 2.97E+00 1.68E+01 l.92E+01 3.15E+02 6.86E+00 1.08E+02 3.77E+02 1.82E+02 3.71E+Ol 1.24E+01 Fission Gases at Dischar e of SJAE (uCi/sec.)
(3) Total Resin   Volume includes 20.0 cu. ft. of Overlay Haterial.
Date 9-02-80 Xe-138 1.33E+03 Kr-87 Kr-88 Kr-85m 4.43E+02 2.87E+02 1.47E+02 Xe-135 1.21E+03 Xe-133 3.10E+03 Off-gas flow rate 13 scfm 0>&#xc3;t 9-23-80 4.72K+04 1.76E+04 8.87E+03 6.44E+03 2.62E+04 1.45E+04 Off-gas flow rate 50 scfm 3265 11Wt Unit 2 Reactor Water Iodines uCi/sec.)Date 9-04-80 9-22-80 I-131 I-132 I-133 3.36E+00 1.74E+01 6.40E+00 (Unit Outage)I-134 2.25E+01 I-135 1.04E+01 Fission Gases at Dischar e of SJAE uCi/sec.)Date 9-02-80 Xe-138 Kr-87 9.52E+03 1.42E+03 Kr-88 Kr-85m 8.16E+02 6.06E+02 Xe-135 Xe-133 2.08E+03 6.97E+02 Off-gas flow rate 120 scfm 2985 Mit 9-23-80 (Unit Outage)Off-gas flow rate 0 scfm 0 M<t 107 Fuel Claddin Inte rit parameters (Continued)
(4) Total Resin   Volume includes 17.0 cu. ft. of Overlay Haterial.
September 1980 Unit 3 Reactor Water Iodines (uCi/sec.)
 
Date 9-04-80 9-22-80 I-131 3.28E+01 6.67E+00 I-132 2.26E+02 l.22E+01 I-133 5.49E+01 7.04E+00 I-134 1.79E+02 2.94E+Ol I-135 9.23E+01 9.64E+00 Fission Gases at Dischar e of SJAE (uCi/sec.)
102-Powdered Resins   % Total   Usa e September   1980 Radwaste                                             Usa e     Total Floor Drain   Filter                           516.0   / 2313.0     22.3 Waste  Filter                                  192.0   / 2313.0       8.3 Reactor Water Cleanu Unit 1                                         120.0   / 2313.0       5.2 Unit  2                                            56.0 / 2313.0       2.4 Unit  3                                            12.0 / 2313.0       0.5 Condensate   Demineralizers U it 1                                         827.0   / 2313.0     35.8 U.it  2                                          198.0   / 2313.0       8.6 (4)
Date Xe-138 Kr-87 Kr-88 Kr-85m Xe-135 Xe-133 9-02-80 3.27E+03 3.29E+02 1.62E+02<4.86E+00.
              "'.it 3                                          376.0   / 2313.0     16.3 Fuel Pool Demineralizers     (1)
4.62E+02 3.03E+02 Off-gas flow rate 42 scfm 2497 HWt 9-23-80 5.48E+03 6.83E+02 3.48E+02 2.09E+02 8.04E+02 2.24E+02 Off-gas flow rate 80 scfm 3018 MWt j w r WASTE TREATMENT SYSTEM VOLUME THROUGHPUTS (1).1980 Year (2)September Month 9.47E+04 d[2.84E+06]FLOOR DRAIN COLLECTOR TANK FLOOR DRAIN FILTER 3 756 FLOOR DRAIN'RPLE TANK 1.40E+04 gpd[4.19E+05]TO CANAL--2.53E+04 d gpd[7.58E+05][2.42E+06][2.84E+06]LAUNDRY DRAIN TANK 7~27 E+0[2.18E+05]~pd[0'2.00E+06 EVAPORATOR DISTILLATE TANK 0'pd 0 gpf WASTE COLLECTOR TANK WASTE FILTER (4)308[6.42E+06]WASTE DEMINERALIZE 130 ft (9-17-80)WASTE SAMPLE TANK 4,03E+03 gpd[1.21K+05]~2.14K+05 pd 2.10E+05 gpd[6.42E+06][6.30K+06][0]CONDENSATE STORAGE TANK (1))Represents 30 days 3 Values accurate to two (2)(p)240 Ft3 of powdered resins 116 Ft of powdered resins gpd evetage gallons pet day signifjcant figures[]total gallons 516 Ft of mixed resin/filter media 192'Ft of mixed resin/filter media 3  
ALL UNITS                                         16.0 / 2313.0       0.7 (1) Total Resin Volume includes       16.0 cu. ft. of Overlay Material.
'P 109 WATER TREADKNT CHEMICAL USE Browns Ferr Nuclear Plant Month September Year 198,0 CHEMICALS REQUIRED DESCRIPTION AMOUNT Grade, concentration
(2) Total Resin   Volume includes   63.0   cu.-. ft. of Overlay Material.
%, Pounds, Gallons, Cuft, etc.Anh drous etc.This Month/Year To Date BOILER WATER MAKEUP TREATifENT Aluminum Sulfate Anthracite (filter media)Coagulant aid, Polyelectrolyte (Wisprofloc 20)Sodium hydroxide Sulfuric acid, demineralizer Coagulant-liquid polymer (Magnifloc 575-C)2700 lbs 8700 lbs 11.9 tons 65.8 tons 8.2 tons 65.9 tons 1000 lbs BOILER WATER SECONDARY TREATMENT Ammonium hydroxide Hydrazine, hydrate Powdex, PAO (Wet)Powdex, PCH (Wet)Resins, bead type (stator cooling)Celite, Supergel HSC Epicor PD-1 anion (Dry)Epicor PD-3 cation (Dry)Epicor AC-31 Mixed Bed (Gravex-Mixed Bed)1 gal 1 gal 20,790 lbs 51,650 lbs 19 Cu Ft 1,200 lbs 192 Cu Ft 216 CU Ft 196 Cu Ft 13 gal 12 gal 111,870 lbs 272,650 lbs 28 CU Ft 19,900 lbs 4,056 Cu Ft 5,496 Cu Ft 2,112 Cu Ft Epifloc-Waste Filter Graver Ecocote-condensate Graver Ecodex-Fuel Pool&Waste Filter 1,044 Cu Ft 1,088 Cu Ft 3,788 Cu Ft MISCELLANEOUS WATER TREATMENT (Includes sample and bearing cooling water systems, ash pond treatment, and other water systems, i.e., radwaste systems and fuel pool cleanup systems at nuclear plants requiring treatment.)
(3) Total Resin   Volume includes   20.0   cu. ft. of Overlay Material.
Sodium Nitrite (RBCCW and and Off Gas chiller)450 lbs SEWAGE TREATMENT Sodium Hypochlorite Soda Ash 620 gal 1,575 gal 5,500 lbs Se tember Nonth 1980 Year Total Pla>>nt Training Summary 0 4J (>>>>>>0 pl 0 cI (>>(>>(>>>>>>0 (t>(>>U 0 0 Cg 0~~'u (4 X C4 6 I>SecLion OI>eraLor Traini>>g II.P.Ra(Iiological)Iygiene Trai>>ing (8 hours)II.P.Retraining (3 hours)Chemical Laboratory
(4) Total Resin Volume includes       17.0   cu. ft. of Overlay Material.
'ualification Training Fire Training N.E.Training I.H.Training U (>>4J 0 I>>>W'0 0 Cl I>>>>>0 U t>>(J>4J (>>(>(lI (>>Cl llea 1 th~Vh sic>>I:.lee t ri ca 1 II;I i>>tenance.Plcch;>ni c;>1 ll>>l I.l>LC>>>>l>>ce 14 10 OI>el>>>Liolls II>>:I I I Ly>1ssllr>>lllc('0 22 IIes>>l ts h(lm>>s Lr tv I>>>>Lr C(>>>t r(>I.s I'ub I ic.S>>JII cL'y I o(J('."L(>rc'.:
 
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                                                                                                                              ... VE55CL litt GTItttD-BY It!Tll IILD PRC(URT DflY5                                                                              0-LM R.OW IH                        IS
 
106 Fuel Claddin     Inte rit   Parameters September    1980 Unit 1 Reactor Water Iodines (uCi/sec.)
Date         I-131         I-132             I-133           I-134         I-135 9-04-80     2. 97E+00     1. 68E+01           6.86E+00        3.71E+Ol    1.24E+01 9-22-80      l. 92E+01     3. 15E+02           1.08E+02       3.77E+02     1.82E+02 Fission Gases   at Dischar e of SJAE   (uCi/sec.)
Date         Xe-138         Kr-87           Kr-88         Kr-85m       Xe-135      Xe-133 9-02-80      1. 33E+03      4. 43E+02       2. 87E+02     1. 47E+02     1.21E+03     3.10E+03 Off-gas flow rate   13 scfm 0   >&#xc3;t 9-23-80       4.72K+04       1.76E+04       8.87E+03     6.44E+03     2.62E+04     1.45E+04 Off-gas flow rate   50 scfm 3265   11Wt Unit 2 Reactor Water Iodines     uCi/sec.)
Date         I-131         I-132             I-133           I-134        I-135 9-04-80      3.36E+00       1.74E+01         6.40E+00       2.25E+01     1.04E+01 9-22-80      (Unit Outage)
Fission Gases   at Dischar e of SJAE   uCi/sec.)
Date         Xe-138         Kr-87           Kr-88        Kr-85m        Xe-135      Xe-133 9-02-80      9.52E+03       1.42E+03       8.16E+02     6.06E+02     2.08E+03     6.97E+02 Off-gas flow rate 120 scfm 2985 Mit 9-23-80       (Unit Outage)
Off-gas flow rate   0 scfm 0 M<t
 
107 Fuel Claddin   Inte rit   parameters (Continued)
September   1980 Unit 3 Reactor Water Iodines (uCi/sec.)
Date         I-131          I-132          I-133        I-134      I-135 9-04-80       3.28E+01       2. 26E+02       5.49E+01     1.79E+02   9.23E+01 9-22-80      6.67E+00       l. 22E+01      7.04E+00      2.94E+Ol    9.64E+00 Fission Gases  at Dischar  e of SJAE (uCi/sec.)
Date         Xe-138         Kr-87         Kr-88       Kr-85m     Xe-135     Xe-133 9-02-80       3.27E+03       3.29E+02     1.62E+02   <4.86E+00. 4.62E+02   3.03E+02 Off-gas flow rate 42 scfm 2497     HWt 9-23-80       5.48E+03       6.83E+02     3.48E+02     2.09E+02   8.04E+02   2.24E+02 Off-gas flow rate   80 scfm 3018 MWt
 
j w r
                                                                                                              . 1980          Year THROUGHPUTS (1)
WASTE TREATMENT SYSTEM VOLUME (2)                 September         Month FLOOR TO CANAL FLOOR
: 9. 47E+04           DRAIN                           FLOOR                       DRAIN           1.40E+04                   2.53E+04 d                                                                 'RPLE                            gpd                   gpdd COLLECTOR                          DRAIN FILTER                        TANK
[ 2. 84E+06      ]
TANK
[ 4.19E+05         ]     [ 7.58E+05      ]
3 756
[ 2. 84E+06   ]
LAUNDRY DRAIN 7~27 E+0
[2. 18E+05
                                                                                                                                          ~pd
[   0 TANK                      ]
[  2. 42E+06     ]
EVAPORATOR 0'pd 0       gpf DISTILLATE
'2 . 00E+06                                                                                  TANK 4,03E+03 gpd              [0          ]
[ 1.21K+05 ]
WASTE                                                               WASTE                                            CONDENSATE WASTE                WASTE                               ~2.14K+05 pd     2.10E+05 gpd COLLECTOR                                                            SAMPLE                                            STORAGE TANK                  FILTER          DEMINERALIZE                TANK                                                TANK (4)                                              [6.42E+06   ] [ 6.30K+06 ]
308                130    ft
[6. 42E+06    ]     (9-17-80) gpd        evetage gallons pet day (1))Represents 30 days Values accurate to two (2) signifjcant figures                    [        ]      total gallons 240 Ft3 of powdered resins 516 Ft of mixed resin/filter media 3
116 Ft of powdered resins 192 'Ft of mixed resin/filter media (p )                                    3
 
'P 109 WATER TREADKNT CHEMICAL USE Browns Ferr   Nuclear Plant Month                 Year September             198,0 CHEMICALS REQUIRED               DESCRIPTION                     AMOUNT Grade, concentration %,   Pounds, Gallons, Cuft,         etc.
Anh drous   etc.
This Month/Year     To Date BOILER WATER MAKEUP TREATifENT Aluminum Sulfate                                           2700  lbs      8700  lbs Anthracite (filter media)
Coagulant aid, Polyelectrolyte (Wisprofloc 20)
Sodium hydroxide                                             11. 9 tons       65.8 tons Sulfuric acid, demineralizer                                  8.2 tons         65.9 tons Coagulant  liquid polymer (Magnifloc 575-C)                                  1000 lbs BOILER WATER SECONDARY TREATMENT Ammonium hydroxide                                             1  gal          13  gal Hydrazine, hydrate                                             1  gal          12  gal Powdex, PAO (Wet)                                       20,790 lbs      111,870 lbs Powdex, PCH (Wet)                                       51,650 lbs      272,650 lbs Resins, bead type (stator cooling)                             19 Cu  Ft        28 CU  Ft Celite, Supergel HSC                                       1,200 lbs        19,900 lbs Epicor PD-1 anion (Dry)                                     192 Cu    Ft    4,056 Cu Ft Epicor PD-3 cation (Dry)                                     216 CU    Ft    5,496 Cu Ft Epicor AC-31 Mixed Bed (Gravex Mixed Bed)                 196 Cu   Ft   2,112 Cu Ft Epifloc-Waste  Filter Graver Ecocote-condensate                                                    1,044  Cu  Ft Graver Ecodex-Fuel Pool  &
Waste  Filter                                            1,088  Cu Ft   3,788  Cu  Ft MISCELLANEOUS WATER TREATMENT (Includes sample and bearing cooling water systems, ash pond treatment, and other water systems, i.e., radwaste systems and fuel pool cleanup systems at nuclear plants requiring treatment.)
Sodium Nitrite (RBCCW and and Off Gas chiller)                                                          450  lbs SEWAGE TREATMENT Sodium Hypochlorite                                          620  gal      1,575 gal Soda Ash                                                                    5,500 lbs
 
0 cI 0                                0 4J Total  Pla>>nt Training            Summary
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/r lee}}
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Revision as of 01:32, 22 October 2019

Second Monthly Operating Rept for Sept 1980
ML18025B137
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 10/10/1980
From:
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML18025B135 List:
References
NUDOCS 8010160511
Download: ML18025B137 (123)


Text

TENNESSEE VALLEY AUTHORITY BROGANS FERRY NUCLEAR PLANT MONTHLY OPERATING REPORT BROWNS FERRY NUCLEAR PLANT SEPTEMBER 1980 Submitted By:

Plant Manager

-">>o;6 o5//

TABLE OF CONTENTS PART I Operations Summary Plant Operations Fuel Performance .

Refueling Information. 10 Equipment Performance. 12 Change in Procedures 16 Change in Facility Design. 16 Surveillance Testing 17 Containment Leak Rate Tests. 18 Changes, Tests, and Experiments Requiring Authorization from the NRC Pursuant to 10 CFR 50 59 ~ (a) ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ o 18 Changes in Plant Operating Organization. 18 Reports to NRC . 19 Changes, Tests, and Experiments Not Requiring Authorization from the NRC Pursuant to 10 CFR 50.59 (a) 20 Primary Coolant Chemistry.

Source Tests 0 ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 22 Environmental Technical Specification Requirements 23 Calculation of Usage Factor. 23 PART II Important Events. 24 Vis i'to 1 s ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~

Safety and First Aid. 27

TABLE OF CONTENTS (Continued)

PART II (Continued)

Accidental'

~ ~ ~ ~ o ~ ~ ~ 27 Plant Personnel Listing. 28 Personnel Changes Annual 31 Personnel Changes Hourly . 37 Significant Operational Events 40 Plant Instruction Revisions. 45 Reportable Occurrences 46 Primary Coolant Chemistry. 49 Average Daily Gross Capacity Factor. 51 Accumulated Average Daily Gross Factor . 52 Radwaste Monthly Average Discharge Rate/Total Activity Discharged. 57 Building and Stack Monthly Release Rates 58 Specification Comparison Building 'echnical and Stack Release Rates 59 Reactor Power Percent. 60 Nuclear Plant Operating Statistics 63 Unit Outage and Availability 64 Outage Summary . 67 Electrical Maintenance Summary 68 Electrical Maintenance Summary Charts CSSC Equipment. 70 Non-CSSC Equipment. 73 Mechanical Maintenance Summary 76

I TABLE OF CONTENTS (Continued)

PART II (Continued)

Mechanical Maintenance Summary Charts CSSC Equipment 77 Non-CSSC Equipment 80 Instrument Maintenance Summary. 82 CSSC Equipment 87 Radioactive Liquid Effluents. 88 Airborne Releases Solid Radioactive Waste 96 Effluent and Waste Disposal Monthly Report. 100 Resin Usage . 101 Powdered Resins  % Total Usage . ~ ~ 102 BFNP Filter Demineralizer Performance 103 Fuel Cladding Integrity Parameters. 106 Waste Treatment System Volume Throughputs 108 Water Treatment Chemical Use. 109 Total Plant Training Summary. 110

PART I 0 erations Summar September 1980 Unft 1 Unit 1 was critical for 703.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, produced 699,320 MWH (gross) with 3.07 percent station use, resulting'n a average hourly gross load of 1,003,012 Kw during the month. The average net heat rate for the month was 10,950 BTU/KWH. There are 192 full power days estimated remaining until the end of cycle 3 fuel. With a capacity factor of 85 percent the target EOC exposure would be reached on May 10, 1981. This includes 0 days of coastdown. The capacity factor for the month was 88.4 percent.

There were two scrams on the unit during the month. On September 1, the reactor scrammed when water from the offgas cooler dripped onto the stator cooling cabinet causing a short in a pressure relay tripping the turbine. The reactor scrammed on September 24, when a short circuit occurred in the sudden pressure trip caosing the 500 KV circuit breakers to open which caus'ed a general load reject.

There were seven power reductions during the month. On September 3, power was reduced because of maintenance to the "C" string high pressure heaters. Power was reduced on September 7, 20, and 27, for turbine control valve tests and Sl's.

On September 16, power was reduced when "A" recirculating water pump was taken out-of-service to place the unit on cooling towers. Power was reduced on September 19, when the "B" reactor feedwater pump was taken out-of-service for maintenance for excessive vibration. On September 29, power was reduced for condensate de-mineralizer backwash and precoat due to problems on three of the condensate demineralizers.

0 erations Summar (Continued)

September 1980 Evaluation of Unit 1 cycle performance shows that the unit operated 10,620 BTU/KWH gross heat rate which is 0.88 percent higher than expected.

Unit 2 Unit 2 was critical 118.78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br />, produced 113,120 NWH (gross) with 4.69 percent station use, resulting in an average hourly gross load of 952,349 kW during the month. The average net heat rate for the month was 10,850 BTU/KWH.

The EOC 3 refueling outage for Unit 2 began on September 5, 1980. The capacity factor for the month was 14.3 percent.

There was one scram on the unit during the month. On September 5, the reactor was manually scrammed in preparation for the beginning of the EOC-3 re-fueling outage.

There was one power reduction during the month. From September 1, to

'I September 5, power was reduced due to end of cycle coastdown to the EOC-3 refueling outage that began on September 5.

Evaluation of the Unit 2 cycle performance shows that the unit operated 10,350 BTU/KWH gross heat rate which is 2.72 percent lower than expected.

Unit 3 Unit 3 was critical for 654.2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />, produced 625,700 MK (gross) with 2.98 percent station use, resulting in an average hourly gross load of 956,245 kW during the month. The average net heat rate for the month was 10,820 BTU/KWH. There are 31 full power days estimated until the end of

.cycle 3 fuel. With a capacity factor of 85 percent the target EOC exposure would be reached on October 31, 1980. This includes 26 days of coastdown.

The capacity factor for the month was 79.1 percent.

0 erations Summar (Continued)

September 1980 There were two scrams on the unit during the month. On September 12, the reactor was manually scrammed to begin a short maintenance outage on the "B" inboard main steam isolation valve. The reactor scrammed on September 20, when a 480 V shutdown board failed to transfer from alternate to normal feed pro-ducing a loss of RPS MG set and the isolation of a SJAE which caused a main condenser low vacuum.

There were seven power reductions during the month. On September 1, power was reduced when "A" recirculation pump tripped. Power was reduced on September 7 and 27, for turbine control valve tests and SI's. From September 7 to September 12, power was reduced when the closure time was found to be too fast on MSIV 1-26 and the valve was closed until a short maintenance outage on September 12. Power was reduced on September 23, for a control rod pattern adjustment. On September 24, power was reduced due to loss of the computer while performing preconditioning to full power.

Evaluation of the Unit 3 cycle performance shows that the unit operated at 10,550 BTU/KMH gross heat rate which is 1.42 percent lower than expected.

0 erations Summar (Continued)

September 1980 Reliabilit and Availabilit The accumulated average daily gross (AADG) capacity factors, based upon midnight IÃH meter readings, for each unit is tabulated below for each month during the last calendar year. The second column compares this year' performance with last year.

Unit No. 1 Unit No. 2 Unit No. 3 1979 1980 1979 1980 1979 1980 Jan *17.4

  • 7.6 94.8 86.4 90.8 37.4 (28)

Feb 50.7

  • 3.8 94.0 62.5 93.3 67.4 (29) 59.2 2.9 91.5 65.9 93 ' 77.8 (22)

Apr 67. 0 18. 1 *90.4 69.4 93.6 83.1 72.5 31.1 *72.3 72.9 90.5 84.1 June 75.7 38.9 72.4 73.1 85.0 84.2'uly 78.0 44.9 75.2 73.3 85.0 7.94 Aug 79.9, 51.0 77.7 75.0 *81.8 81.4 Sept 79.1 55.2 79.0 *68.2 *72.7. 81.1 (25)

Oct 80. 0 80.6 * *65. 5 Nc (39)

Nov 79.6 81.5 *59 '

Dec(') 80.1 79.5 *58.7

  • Refuel Outage (Days of Month)

(1) Yearly Average Unit 1 can achieve an AADG capacity factor of about 62.7% for CY '80 if it averages 85% CF (presently averaging 77.8%) for the remainder of the year, considering unit operating time (i.e.: not in refuel). Similarly, Units 2 and 3 can reach about 64.8% and 73.0% AADG capacity factors, re-spectively. Presently these units are averaging 75.0% and 81.1%, respectively.

0 erations Summer (Continued)

September 1980 Reliabilit and Availabilit (Continued)

The largest capacity factor loss (12%) this month was on Unit 3 due to an inoperable HSIV (1-26 "B" inboard valve). This valve was closed and limited to 75% power for about 5.8 days.

The next largest CF loss (Unit 1 ~ 4.9%, Unit 3 = 2.9%) involves automatic scrams caused by equipment malfunctions. A significant controllable CF loss involved control rod pattern limitations on unit 1 and 3 at 0.8% and 1.7% re-spectively. These losses result from postponing rod pattern adjustment until weekends when more favorable system load requirements exist.

l, RELIABILITY AND AVAILABILITY(CONTINUED)

CAPACITY FACTOR LOSSES September 1980 Unit 1 Unit 2 Unit 80.1% 88.4 79.5% 14.3 58.7% 79.1 Losses were caused by:

l. Refueling 5.5 9.5 83. 6 29.3
2. P CION 2.8 1.9 2.5 1.8 2.1
3. End of cycle coastdown 1.4 0.2 2-. 1
4. Feed piping failure 1.4
5. Startup testing 0.9 0.5 1.0
6. Administrative limitations 0.8
7. Steam tunnel temperature switches 0.7
8. Reactor feed pump maintenance 0.6 ;0.6 0.6 1.3
9. High condenser backpressure 0.6 1.8 0.1 0.3 0.2
10. Thermal limits 0.5 I
11. Recirculation pump motor bearing problems 0.5 I 3.9
12. Automatic scram 0.5 >4.9 .0.6 0.8. 2.9
13. Drywell air leakage 0.4
14. Reduced thermal limits 0.4
15. Turbine vibration and balancing 0.3
16. Heater problems 0.3 0.2
17. Hoisture separator high level 0.3
18. Recirculation pump starting problems 0.3 0.2
19. Feedwater control problems 0.2 0.8 0.1
20. EHC and turbine valve problems 2.2 0.2
21. THI related modifications 1.5
22. Recirculation system vibration evaluation 0.6
23. Hain steam valve maintenance 0.'3 12;0
24. Recirculation H-G set brush changes 0.3
25. Rod sequence exchange 0.6 0.2 0.2
26. TIP system 0.2 0' 0.2
27. CMf system hydrogen sensor failure 0.5
28. Offgas system malfunction 0.3
29. Power cable replacement 0.3
30. Testable check valve maintenance 0.2
31. Load following demonstration test
32. Demineralizer problems 0.2
33. Low pressure air line break 0.1

RELIABILITY AND AVAILABILITY(CONTINUED)

CAPACITY FACTOR LOSSES September 1980 Unit 1 Unit 2 Unit 3 80.1% 88.4 79.5% 14.3 58.7% 79.1 Losses were caused by:

34. Rod pattern, full core flow 0.8 1.7
35. Surveillance instruction 0.1 0.1
36. Recirculation pump trip 0.4
37. Feedwater system leak 0.9
38. Control rod adjustment 0.2

0 erations Summar (Continued)

September 1980 Common The radwaste system performed as designed. Approximately 7.58E+05 gallons of waste liquid were discharged containing approximately 1.36E+00 curies of activities. Floor drain system through-put increased this month primarily because of decontamination activities associated with the unit two refueling outage.

Radwaste shipments to Barnwell, S. C. were interrupted for approximately 8 days due to a delay in the receipt of the required state shipping permit.

There were 14 shipments for an approximate total volume of 5,600 cubic feet.

There were 399 (55 gallon) drums of radwaste generated during the month at an average rate of 13.3 drums per day. There were 33 boxes of trash and irradiated components generated during the month at an average rate of 1.1 boxes per day.

0 erations Summar (Continued)

September 1980 Fuel Performance Unit 1 The reactor was operated at a nominal maximum thermal power level of 99.2% of rated. Typical thermal limits for this condition include CMFLPD, 0.973; MAPRAT, 0.945 and CMFCP, 0.885. The reactor operated in control rod sequence "A" 12 days, and in sequence "B" the remainder of the month.

Fuel preconditioning at the rate of 0.11 kw/ft/hr was conducted for approximately 1.4 days in sequence "A", and 3.1 days in sequence "B".

Unit 2 The reactor was operated at a nominal maximum thermal power level of 90% of rated. Typical thermal limits for this condition included CMFLPD, 0.731; HAPRAT, 0.730; CMFCP, 0.810. The reactor operated in control rod sequence "B" for the entire month.

Fuel preconditioning at the rate of 0.11 kw/ft/hr was conducted for approximately 0 days in sequence "B".

Unit 3 The reactor was operated at a nominal maximum thermal power level of 99.2% of rated. Typical thermal limits for this condition CttFPLD, 0.850:

MAPRAT, 0.827; and CMFCP, 0.965. The reactor operated in control rod sequence "A" for 14 days, and in sequence "B" the remainder of the month.

Fuel preconditioning at the rate of 0.11 Kw/ft/hr was conducted for 1.5 days in sequence "A", and 3.5 days in sequence "B".

10 Operations Summary (Continued)

September 1980 Refuelin Information Unit 1 Unit 1 'is scheduled for its fourth refueling beginning on or about April 15, 1981, with a scheduled restart date of July 25, 1981. This re-fueling will involve loading additional 8 x 8 R (retrofit) fuel assemblies into the core, the final fix on, the sparger modification, power supply on LPCI modification, and torus modifications if all approvals are received.

There are 764 fuel assemblies in the reactor vessel. The spent fuel storage pool presently contains 550 spent 7 x 7 fuel assemblies, five 8 x 8 fuel assemblies, and one 8 x 8 R fuel assembly. Because of modification work to increase spent fuel pool capacity to 3471 assemblies, present capacity is limited to 1152 assemblies.

Unit 2 Unit 2 is presently in its EOC 3 refueling outage. Unit 2 is scheduled for its fourth refueling beginning on or about March 1, 1982, with a scheduled restart date of June 14, 1982. This refueling outage will involve completing relief valve modifications, torus modifications if all approvals are received, "A" low pressure turbine 'inspection, and loading additional 8 x 8 R fuel assemblies into the core.

There are 764 fuel assemblies in the reactor vessel. At the end of the there were 132 discharged cycle 1 fuel assemblies, H+'onth, 156 discharged cycle 2 fuel assemblies, and 352 discharged cycle 3 fuel assemblies in the spent storage pool. The present storage capacity of the spent fuel pool is 820 assemblies. With present capacity, the 1979 refueling was the last

Operations Summary (Continued)

September 1980 Refuelin Information Unit 2 (Continued) refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.

However, new high density storage racks are being installed during the third refueling of Unit 2.

Unit 3 Unit 3 is scheduled for its third refueling beginning on or about November 2, 1980, with a scheduled restart date of December 11, 1980. This EOC-3 refueling, involves loading additional 8 x 8 R (retrofit) assemblies into the core, and power supply on LPCI modification.

There are 764 fuel assemblies presently in the reactor vessel. There are 144 discharged cycle 2 fuel assemblies, 208 discharged cycle 1 fuel assemblies, and 164 new P 8 x 8 R assemblies in the spent fuel storage pool. The present storage capacity of the spent fuel pool is 1528 assemblies. With present capacity, the 1980 refueling would be the last refueling that could be discharged to the spent fuel pool without exceeding that capacity and maintaining full core discharge capability in the pool.

12 0 erations Summar (Continued)

September 1980 E ui ment Performance On September 16, at approximately 1730 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.58265e-4 months <br />, localized flooding was ex-perienced in the yard in front of the radwaste and the unit 1 and 2 diesel building. The flooding began during an attempt to place Unit 1 on cooling towers. Gate lA1 was closed and the resulting back pressure forced open a cover-plate sealing the top of the CCW conduit. Opening gate 1Al halted the flow of water into the yard area. The cover-plate on the Unit 1 conduit has been securely refastened.

While performing leak checks on 2D RHR heat exchanger, it was discovered that a check valve in the raw service water charging connection to RHR service water was stuck open. This allowed a leak test on 2D RHR heat exchanger to be interpreted as positive indication of leakage because it placed 2D RHR heat ex-changer (RHR side) in communication with RHRSW through 2B RHR heat exchanger which was known to be leaking. The check valve was repaired and a satisfactory leak check of 2D RHR heat exchanger was performed.

Unit 1 Reactor Building Equipment Drain Sump Heat Exchanger was determined to be providing inadequate cooling for the contents of the Reactor Building Equip-ment Drain Sump. This was indicated by steam rising through the sump pump support plate. Investigation thus far points to inadequate cooling water flow from RBCCW to the sump heat exchanger. This investigation continues.

13 0 erations Summar (Continued)

September 1980 E ui ment Performance (Continued)

High vibration on 1B Reactor Feedwater Pump was noted during routine weekly vibration checks this month. Increased surveillance revealed a high axial vibration level initially. This then shifted to high horizontal vib-ration at a frequency two times the pump run speed. As this is indicative of misalignment and the vibration levels continued to become more severe, the pump was removed from service and the coupling disassembled. It was found that all of the oil had been thrown out of the coupling. The oil was replaced and the pump returned to service without further problems.

Prior to the beginning of Unit 2 refueling outage, performance checks on both spent fuel storage pool cooling pumps for Unit 2 determined both pumps to be performing at less than 85% of their design capacities. Both pumps were rebuilt and subsequently performed at greater than design criteria.

High differential pressures were experienced on 2B reactor water clean-up filter demineralizer. Investigation revealed that a failure of the stainless steel filter elements allowed precoat material to accumulate on the resin trap.

The problem was corrected by replacement of the filter elements and associated resin trap.

Resin traps on reactor water clean-up demineralizers 1A and 1B were removed I

and examined to determine the cause of high differential pressure. An accumulation of rust was found on the traps. The source of the rust is still under investigation.

There was no indication of problems with filter element integrity. New resin traps were installed and the demineralizers were successfully returned to service.

14 0 eration Summar (Continued)

September 1980 E ui ment Performance (Continued)

Problems were experienced with the condensate demineralizers on Unit 1.

Failure of the filter element on vessels J and E allowed resin to accumulate on the downstream resin traps. High differential pressure across the resin traps forced replacement of the traps along with the failed filter elements.

The reason for unusually short service runs on vessel 1D was investigated. The vessel's filter elements were found to be severely fouled with iron oxide. It is believed the fouling resulted from improper precoating techniques which failed to protect the element with an over-lay of resin. The fouled elements were re-placed and the vessel was satisfactorily returned to service. Precoating records are being reviewed to determine if additional corrective action is warranted.

A visual inspection was made of the Unit 2 CCW tunnel on September 17, 1980. Algae growth covering approximately 10% of the wall surface (bottom and sides) of the tunnel was noted. The floor of the tunnel was covered with silt and mud that ranged from 1/2 inch to 2 inches in thickness. At the intake butterfly valves, there was approximately 1.5 ft3 of clams accumulated in the discharge from CCH pump B. At the inlet to the water boxes, there was approximately 0.5 ft3 of clams scattered around the tunnel floor.

TIP problems on Unit 3 affected the ability to establish full power rod patterns throughout the month of August. Problems with two of the five TIP machines resulted in fewer TIP sets being run than otherwise would have been run.

Detector "A" was replaced on September 22, 1980, and a PORC approved PMR was completed to eliminate problems with "D" machine. At the end of the month, all five TIP machines were operational.

0 erations Summar (Continued)

September 1980 E ui ment Performance (Continued)

The plant purchased a helium leak detection instrument to check the integrity of the main condensers. The instrument was not fully operational in time to check the Unit 2 condensers at the start of the refueling outage.

A leak check on the Unit 2 condenser is planned prior to the end of the outage when condenser vacuum is re-established.

18 0 erations Summar (Continued)

September 1980 Containment Leak Rate Tests

'rimary containment penetration leak rate tests were performed during the month. The results are within technical specification limits and are listed in the following table.

Leaka e (scfm T e Test Unit 1 Unit 2 Unit 3 Type A (integrated containment) No Test Incomplete No Test Type B (Drywell/torus hatches) No Test 0.0011 Personnel Air Lock (X2) 0.2119 Equipment hatches Electrical Penetration (X107B) 0.0173 Type C (Isolation valves) No Test 0.3236 No Test Totals 0.0 0.3420 0.2119 Chan es Test and E. eriments Re uirin Authorization From the NRC Pursuant to 10 CFR 50.59 a)

There was one revision to the Unit 3 Technical Specification comprised of pages ix through xxxi EPL 1 through 22, 156, 157, 170 and 171. Inoperable time was changed from 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to 10 days on standby coolant supply capability.

Chan e in Plant Or anization There was one change to the plant staff for those positions designated as key supervisory personnel positions in the Technical Specifications.

A Plant Shift Engineer, M-4, was selected as Plant Assistant Operations Supervisor, M-4.

19 0 erations Summar (Continued)

September 1980 Re orts to NRC There were 23 reportable occurrences, a revision to one of these, and 2 cancelled reportable occurrences were reported to the NRC during the month.

20 0 erations Summar (Continued)

September 1980 Chan es Tests and Ex eriments Not Re uirin Authorization from the NRC Pursuant to 10 CFR 50.95 (a S ecial Test 186 "Scram Discharge Volume (SDV) Drain Valve Closure Pressure on Loss of Control Air Unit 2" This test was performed to determine the control air pressure at which the SDV drain valves would drift shut on a loss of control air. It was originated to aid in the evaluation of the potential for flooding the SDV as a result of a decrease in control air pressure.

STEAR 80-20 "I and C Bus A and B Load Current Determination" Test involved measuring current to various branch circuits feeding from I and C bus A and B. Data was submitted to EN DES to be used in their eval-uation of the voltage reliability analysis performed for these buses. This was in response to NRC inquiries.

Plant modifications will be submitted in the annual report.

21 0 erations Summar (Continued)

September 1980 Primar Coolant Chemistr Unit 1 The conductivity of the reactor coolant exceeded technical specification and fuel warranty limits for a total of 30.1 hours1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> during the month. A rup-tured tube in Cl waterbox and transients associated with Scrams 135 and 136 were responsible for the conductivity increases. Chloride concentrations and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month. This calendar year the technical specifications and fuel warranty limits has been exceeded for 140.9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br />.

Unit 2 The" conductivity of the reactor coolant remained within technical speci-fication,and fuel warranty limits for the month. Chloride concentration and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month. This calendar year technical specification and fuel warranty conductivity limit has been exceeded for 71.3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />.

Unit 3 The conductivity of the reactor coolant remained within fuel warranty limits during the month. The conductivity of the reactor coolant remained within technical specifications of 2.0 pmhos during the month. Chloride concentration and pH of the reactor coolant remained within technical specification and fuel warranty limits during the month. This calendar

22 0 erations Summar (Continued)

September 1980 Primar Coolant Chemistr year the fuel warranty conductivity limit has been exceeded for 27.55 hours6.365741e-4 days <br />0.0153 hours <br />9.093915e-5 weeks <br />2.09275e-5 months <br />, and technical specification limit has been exceeded for a total of 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />.

Source Test None

23 0 erations Summar (Continued)

September 1980 Environmental Technical S ecification Re uirement

-

The raw water chlorination system was not operated during the month of September.

Reservoir water temperatures exceeded technical specification limits on two different days during the month of September. On September 28th and 29th the temperature rise was 5.1'. The average intake water temp-erature for the month was 83.6'., The largest water temperature rise was 5.1', with an average downstream water temperature of 85.3'.

Approximately 700,000 gallons of water was released from the unlined pond to the Tennessee River. The pH of the release was maintained within technical specification limits of 6.0 to 9.0.

Calculation of Usa e 'Factor The cumulative usage factors for the reactor vessel are as follows:

Location Usa e Factor Unit 1 Unit 2 Unit 3 Shell at water line 0.00487 0.00369 0.00314 Feedwater nozzle 0.23254 0.11570 0.15822'.12899 Closure studs 0.19566 0.09194

24 0 erations Summar (Continued)

September 1980 Im ortant Events September The Plant Manager and the Plant Operations Supervisor attended a briefing on Division Plan to Compensate Nuclear Power Employees and an Operator Staffing Presentation in Chattanooga.

The Plant Manager attended the Bi-Weekly Plant Manager Meeting in Chattanooga.

879 A Plant Outage Civil Engineer and a Plant Outage Electrical Engineer attended a meeting in Knoxville, on the Post-Accident Sampling Facility.

15-19 The Plant Chemical Unit Supervisor taught a chemistry and radio-chemistry course at the Power Operation Training Center for the STA's.

15-30 Two Plant Chemical Engineers attended an engineering training course at the Power Operation Training Center in Chattanooga.

The Plant Manager attended a meeting in Chattanooga on recommendations from Management Training Committee for M position profile plan.

The Plant Acting Compliance Supervisor attended a meeting in Chattanooga on IE Bulletin 79-01B.

19 The Plant Systems, Analyst attended a meeting in Huntsville, AL.,

with Chattanooga Central Office personnel and PIC Systems, Inc.,

to review the design of the PRIME/GE 4020 link.

A meeting was held at the plant between EN DES Knoxville, personnel, and the Plant Instrument Maintenance personnel to discuss power sources for the Feedwater Control System.

The Plant Outage Director attended a meeting in Chattanooga on Instrumentation Sensing Lines.

20 The Plant Acting Compliance Supervisor attended the NRC Region II, meeting in Atlanta on NUREG-0660 clarifications/TMI Action Plans.

22 The Plant Manager and representatives from the plant Co-op group attended a "kick-off" for combined 'Federal Campaign at the Marshall Space Flight Center in Huntsville, AL.

25 0 erations Summar (Continued)

September 1980 Im ortant Events September 22-25 The Plant Mechanical Results Unit Supervisor, the Plant Equipment Diagnostics Engineering Associate, and a Plant Mechanical Engineer attended a Vibration Training Class in Chattanooga.

23-24 The Plant Manager attended a Nuclear power Quality Meeting in Chattanooga.

24 The Plant Outage Director attended a Division Meeting in Chattanooga.

25 The Plant Manager and representatives from the Plant Co-op group attended the- United May "Kick-off" dinner in Huntsville, AL.

30 The Plant Quality Assurance Supervisor attended a QA Supervisor Meeting at the Power Operation Training Center.

The Plant Manager, the Plant Electrical Maintenance Supervisor, a Plant Shift Engineer, and two Plant Outage Electrical Engineers attended a meeting in Knoxville on Browns Ferry Nuclear Plant Under-voltage Modifications.

The Plant Outage Refuel Floor Coordinator attended a meeting in Chattanooga on Multi-Stud Tensioners.

Visitors September Mr. Dale Nix, Plant Engineering Staff; Mr. Frank Kelly, Reactor Engineering Staff; and Mr. C. D. Evans, EN DES Knoxville, met with the Plant Chemical Supervisor concerning PASF and revised design criteria.

Mr. Tom Hall, London Nuclear Services, was onsite to meet with the Plant Assistant Outage Director and the Plant Outage Drywell Coor-dinator, concerning chemical decontamination of CRD scram headers.

Mr. Barry Smith, General Electric Customer Service Plant and AMPS, met with various plant section supervisors.

Representatives from the Hewlett-Packard Corporation met with the Plant Chemical Supervisor to demonstrate the HP 9845 for PASF.

0 erations Summar (Continued)

September 1980 Visitors September Ms. Marilyn Taylor, Director of Personnel, was on site to meet with employees regarding various employee concerns. Her visit was a result fo Chairman Freeman's visit in July when questions regarding personnel were addressed to him. Job surveys were performed at nuclear plant positions by members of Ms. Taylor's staff and representatives of the Division of Nuclear Power personnel office. The results of these surveys will be compared to job surveys to be performed at a fossil plant.

4-5 Messrs. Ralph Thompson, Charlie Howell, and Frank Garrett, Chattanooga Industrial Safety and Fire Protection Engineering Staff was onsite to conduct an air flow test Unit 1 Reactor Building.

8-11 Office of Power Quality Assurance auditors were onsite to audit special processes and maintenance activities.

10-12 General Electric representatives were onsite to meet with the Plant Manager concerning HPCI and RCIC performance.

A 5-man team from Occupational Health and Safety was onsite to audit the outage operation.

12 Mr. Ron Westbrook, IS and FPE Supervisor, CHattanooga, was onsite for a Safety Inspection Audit Exit Meeting.

15 Two NRC licensing personnel were onsite to administer reactor operator and senior reactor operator licensing examinations to 10 Browns Ferry operators.

15-18 Three representatives from PLC (Professional Loss Control, Inc.)

were onsite to perform an audit of the fire protection system as required by technical specifications.

16 An NRC inspector was onsite to audit the inservice program.

22-25 Representatives from the Division of Occupational Health and Safety conducted a safety audit of outage work.

23 Mr. Marvin Lane, Executive Vice Pr'esident of Graver Water Company, met with the Plant Results Section Supervisor and others on the problems of contaminated powdered resins.

23-26 Office of Power Quality Assurance auditors were onsite to perform an audit of document control and technical specifications.

27 0 erations Summar (Continued)

September 1980 Safet and First Aid The regular weekly safety meetings of salary policy and trades and labor groups were held this month.

Accidents There were 2 loss-of-time accidents during the month of September.

28 NUCLEAR PLANT PERSONNEL Browns Ferry Nuclear PLANT End of End of Previous Present TITLE Month Changes Month Power Plant Superintendent~ M-8 Assistant Power Plant Superintendent M 6 Records Officer SA-2 eosIMst Mechanical En ineer SD-3 S ecification En ineer SD-3 En ineerin Aide SE-2 Safety Engineer SO 3 ngzneer ng i e Sa ety SE-Su ervisor, Mana ement Services Section M-5 Su ervisor Administrative Services hbck Unit H-4

~fctttsttgtttofstetocMZ Su ervisor Document Control Unit H-

~otaotctNsttgLeffttttxtnTgtrimst7BItsd Su ervisor Plt Services Unit H Secretar SB.4

>tlaarttISmNcgtgtPtorILM- Editor SA-2 Clerk Typist SB 3 15 Clerk-Typist SB 2 zfftetsofrftsfcs88.8 Clerk SB-2 Payroll Clerk SB 5 Pa roll Clerle%8Q<

Payroll ClerleSBR SB-3 File Clerk SB.3 Supervisor Services H-4 Su ervisor Qualit Assurance Stalf M 5 Qualit Assurance En ineer SO 4 Quality Assurance Engineer SO-3 Quality Assurance Engineer SO 2 Engineering Aide (Quality Assurance) SE 5 En ineerin Aide (Quality Assurance) SE.4 n ineerin Aide ualit Assurance) SE-3 lerk, SB-3 ail Clerk SB-2 Power Plant Results Supervisor M.5 Assistant Power Plant Results Supervisor M4 ower Plt Maintenance Supvr (Inst) H-5 Instrument Engineer SO 4 IfecuttttgtfrBI@tttmtcs88 Personnel Clerk SB-4 otttramstBBM S stems Anal st, SD-3 enior Instrument Mechanic Instructor Irgtmtdge8agtsrtttt~".ItttL(saacsflsft Programming Technician SE-4 Engineering Aide SE 3 Senior Instrument Mechanic Foreman 15 16 Senior Instrument Mechanic 44 43 Instrument Mechanic Instrument Mechanic Ap rentice- '4th Pd. 22 27 Instrument I'ftechanic Apprentice- 3rd Pd. 10 ctsrssrotttuntnhtacttmt(enectprzmfeme Pthc Nord Processor SB-4 sst. Power Plt. Maintenance Supervisor (Inst) M-4 Reactor En ineer SO 4 5U@tnBmjNI@SttgO7B Clerk SB-4 Engineering Aide (Nuclear) ZSA SE-5 TAMNQNSBrp;IftmttSGAz Supervisor, Mechanical Unit M-4 Mechanical En ineer SO 3 Engineerin Aide(Statistician)BRA SE-5 ttgfotroc'otg7rtfsfm(lamISr18ntaias)ISED Data Entry Clerk SB-2 Engineering Aide (Test Bt Studies) SE.3 TVA 7037 (PP-10.77) sheer 1 M mn,r September >>80

29 NUCLEAR PLANT PERSONNEL Browns Ferr Nuclear PLA14T End of Eno of Previous PfeSenl T IT t.s Month Chonoes Montn Mechanical En ineerin Associate SE 6 En ineerin Aide (Mechanical) SE 4 En ineerir. Aide (Mechanical) SE-3 En ineerin Aide (Instrument) SE.

En ineerin Coo Student (N) SE.3 Enoineerin 'Coo Student OQXZSZ (M) SE-3 Supervisor Chemical Unit if-4 Chemical En ineer SO 4 Chemical En ineer SO 3 Chemical Enoineerin Associate SE 6 Radiochelnical Laboratory Analyst SE 5 Radiochemical Laboratory Analyst SE 4 Chemical Laborator~ Anal st SE 3 Engineering Coop Student (C) SRR SE-4 En ineerinn Coo Student (C) SE.2 +1 -1 Radiochemical Laborato Anal st Tr SE-3 Su ervisor Reactor Unit M-4 Power Plant Operations Supervisor M 5 Assistant Power Plant Operations Supervisor M.4 Clerk SB 3 Shift Engineer M-4 16 15 Assistant Shift Engineer M-3 Assistant Shift Engineer-SR L 15 15 Unit Operator Unit Operator-RL 20 Assistant Unit Operator Student Generating Plant Operator- th Pd.

tu ent eneratxng ant perator r Clerk SB-2 Supervisor Janitorial Services i'-3 Janitor SF 3 Janitor SF 2 +17 -4 17 Janitor SF.l 55 +27 -20 62 Power Plant Maintenance Su ervisor E M-5 Power Plant Maintenance Supervisor M 5 Assistant Power Plant Klaintenance Supervisor (E) M 4 Assistant Power Plant Maintenance Supervisor (M) M 4 General Electrical Foreman M-4 Electrical Engineer SO 4 Electrical En. ineer SO 3 General Mechanical Foreman M-4 Mechanical Engineer SO.4 Mechanicaf En ineer SO 3

&rJcttacthsgtt(:cttxftfzstutstnt)Ms'echanical Engineer SD-2 En ineerin Aide (41echanical) SE 3 Engineering Coop Student (M) SE.

Xmxnnmsmmm~unx!&SR En ineerin Aide Electrical SE-Electrician Foreman 10 10 Electrician 46 + . -2 Electrician Apprentice- Pd.

Electrician Apprentice- 1st Pd. B 10 Electrician Apprentice- 1st Pd. A TVA 7OS7 (PP tO 77) Sheet 2 September,(0

30 I'JUCLEAR PLANT PERSONNEL PLANT end or End or Previous Present TITLE Month ChangeS Month Machinist Foreman Machinist Machinist Welder Machinist A orentice- 4th Pd Machinist Apprentice- 3rd Pd.

Machinist Apprentice- 2nd Pd.

Hachinist A I7rentice 1st Pd. B Hachinist A rentice 1st Pd. A Boilermaker Foreman Boilermaker Boilermaker Welder Boilermaker Apprentice- Pd.

Boilermaker Apprentice- Pd.

Sheetmetal Worker A rentice 1st Pd. A Steamfitter Foreman Steamfitter 24 Steamfitter Welder Steamfitter Ap rentice- 5th Pd Steamfitter'Apprentice- 1st Pd. A 12 12 General Labor Foreman H-3 Car enter Foreman Asbestos Worker Foreman ainter Apprent3.ce st P . A Structural Ironworker Sheetmetal Worker Foreman Sheetmetal Worker Asbestos Worker Car enter Painter Foreman Painter Heavy Equipment Operator-Power Labor Foreman Nuclear Plant Laborer 23 23 Truck Oriver I Sign Painter Total Annual Salary Policy 233 +67 -33 267 Total ATL Operations 112 + 7 -13 106 Total ATL Maintenance Total Plant 660 +91 -60 691 Hourly-List Titles Car enter 23 Car enter 1 Construction Laborer 71 Hortar Hixer 1 63 +12 Boilermaker (10) Hach Wldr (1) Steamfitter 15 20 26 Hach 28 Bricklaver 1 Painter 13 Asbestos Worker 2 Crane 0 erator 2 Sheetmetal Worker 3 Truck Driver I 2 Total Hourly 152 TVA 7037 (PP.10.77) Sheet 3 Month or

L 0

31 Se tember 1980 Personnel Chan es Annual Name Title Effective Date Betty J. Grimes Janitor F01 09 02 80 Billy J. Allen Janitor F01 09 03 80 Kenneth E. Howard Janitor F01 09 03 80 Richard L. Ingram Janitor FOl 09 03 80 William C. Jones, Jr. Janitor FOl 09 03 80 Arthur L. Littleton Janitor FOl 09 03 80 Jose I. Lozano Janitor F01 09 03 80 Michael E. Maples Janitor F01 09 03 80 Margaret L. Reach Janitor FOl 09 03 80 Larry D. Smith Janitor F01 09 03 80 Jack W. Vinson Janitor F01 09 03 80 Barbara L. Weigart Janitor F01 09 03 80 Randall L. Keeton Janitor FOl 09 04 80 Dennis M. Castell Janitor F01 09 05 80 Wayne E. Guthrie Janitor F01 09 05 80 M. Neil Haraway Janitor F01 09 05 80 Kenneth D. Sylvester Janitor FOl 09 05 80 Gary R. Cobb Janitor F01 09 08 80

32 Se tember 1980 Personnel Chan es Annual Name Title Effective Date Russell B. Huffman Janitor F01 09 08 80 Willie M. Jenkins Janitor F01 09 08 80 Robert L..Rice Janitor F01 09 08 80 Nicholas L. Austin Janitor F01 09 09 80 Thomas I. Vines Janitor FOl 09 09 80 Robert C. Murphy Janitor F01 09 10 80 Charles Crawley Janitor F01 09 11 80 James R. Hine Janitor FOl 09 15 80 Harlon L. Ramsey Janitor F01 09 17 80 B. Reclassifications Effective Name Former Title New Title Date Rickey E. Holtzclaw SGPO 4th Pd Asst Unit Op 07 23 79 James C. Hall SGPO 4t}1 Pd Asst Unit Op 10 01 79 Danny L. Tuggle Inst Mech AP3 Inst Mech AP4 06 23 80 Wendell K. Holt Elect APlA Elect AP1B 07 21 80 Kenneth W. Brown Elect APlA Elect AP1B 08 04 80 Timothy D. Lane Inst Mech AP3 Inst Mech AP4 08 04 80 Linda G. Murphy Elect APlA Elect AP1B 08 04 80

33 Se tember 1980 Personnel Chan es Annual B. Reclassifications (Continued)

Effective Name Former Title New Title Date Elizabeth L. White Elect AP1A Elect AP1B 08 11 80 Kenneth E. Davis Elect AP1A Elect AP1B 08 18 80 Tony D. Hill Elect AP1A Elect APlB 08 18 80 Patricia F. Roland Inst Mech AP3 Inst Mech AP4 08 18 80 Lona C. Belue Clerk B03 Word Processor B04 08 24 80 Roger D. Shireman Radiochem Lab Radiochem Lab 08 24 80 Anal E04 Anal E05 James A. Green Asst Shft Engr M03 Sup, Janitorial 08 31 80 Servs M03 Robert E. Stone, Jr. Inst Mech AP3 Inst Mech AP4 09 01 80 James S. Watson Elect (H) Elect 09 01 80 Thomas M. Thompson Elect (H) Elect 09 03 80 Lardell Goodloe, Elect (H) Elect 09 04 80 Dan C. Barger Janitor FOl Janitor F02 09 07 80 Martha C. Barnett Janitor F01 Janitor F02 09 07 80 Nellarene P. Cobb Janitor F01 Janitor F02 09 07 80 Larry W. Cole Janitor F01 Janitor F02 09 07 80 Leonard A. Cole Janitor FOl Janitor F02 09 07 80 Michael W. Davis Clerk B02 Clerk B03 09 07 80 Helen J. Franklin Janitor F01 Janitor F02 09 07 80 William C. Freeman Janitor F01 Janitor F02 09 07 80

34 Se tember 1980 Personnel Chan es Annual B. Reclassifications (Continued)

Effective Name Former Title New Title Date James O. George Janitor F01 Janitor F02 09 07 80 Bobby F. Grizzard Janitor F02 Janitor F03 09 07 80 David S. Haney Janitor F01 Janitor F02 09 07 80 Robert L. Ingram Janitor F02 Janitor F03 09 07 80 Martin Johnson Janitor F01 Janitor F02 09 07 80 John W. Maynor, Jr. Janitor F01 Janitor F02 09 07 80 Morris W. Morell Janitor F01 Janitor F02 09 07 80 William L. Sandy Janitor F01 Janitor F02 09 07 80 Burl D. Stark Janitor F02 Janitor F03 09 07 80 E. Jane Wilkerson Janitor FOl Janitor F02 09 07 80 Thomas L. Williamson Janitor FOl Janitor F02 09 07 80 Robert E. Woods Janitor FOl Janitor F02 09 07 80 Garfield J. Taylor, Jr. Sr Inst Mech Sr Inst Mech Fmn 09 08 80 Inez H. Bedingfield Janitor F01 Janitor F02 09 21 80 Austin L.,Burnette Shft Engr H04 Asst Pr Plt Op 09 21 80 Sup M04 David T. Davis Inst Mech AP3 Inst Mech AP4 09 21 80 Herbert L. Johnson Qual Assurance Engr D02 Qual Assurance 09 21 80 Engr D03 Donell King Janitor F01 Janitor F02 09 21 80 Richard W. Shultz Inst Mech AP3 Inst Mech AP4 09 21 80 Ardie R. Champion Unit Op RL Asst Shft Engr M03 09 29 80 James C. Coz Unit Op RL Asst Shft Engr M03 09 29 80 .

Willard B. Dawes, Jr. Asst Unit Op Unit Op 09 29 80

35 Se tember 1980 Personnel Chan es Annual B. Reclassifications (Continued)

Effective Name Former Title New Title Date Johnny E. Duke Asst Unit Op Unit Op 09 29 80 Russell R. Eades Asst Unit Op Unit Op 09 29 80 Charles B. Fisher Asst Unit Op Unit Op 09 29 80 Steve R. Gray Asst Unit Op Unit Op 09 29 80 Charles G. McClain Unit Op RL Asst Shft Engr M03 09 29 80 Marvin L. Meek Unit Op RL Asst Shft Engr H03 09 29 80 Michael V. Hiller Unit Op RL Asst Shft Engr M03 09 29 80 C. Transfers Out Former New Place Effective Name Title Title TQ Date Jeannette Y. Johnson Clk B02 Clk B02 OCH&S 09 07 80 James L. Turner Radiochem Lab Chemist-D01 Trng Ctr 09 21 80 Anal E04 D. Transfers In Former New Place Effective Name Title Title From Date George N. Veal Shmtl Qcr Shmtl Wkr W Creek 08 25 80 David E. Newton Elect Elect Service 09 02 80 Shops Michael N. Brown Radchm Lab Ana Radchm Lab Ana Trng Ctr 09 21 80 Tr E03 Tr E03 James tJ. Burton III Chem Engr D02 Chem 'Engr D03 Ctl & Test 09 21 80 B. Joan Chandler Clk B02 Data Engry Op P&Svs 09 21 80 B02

36 Se tember 1980 Personnel Chan es Annual D. Transfers In (Continued)

Former New Place Effective Name Title Title From Date Edward J. Frederick Radchm Lab Ana Radchm Lab Ana Trng Ctr 09 21 80 Tr E03 Tr E03 Aaron J. Goode Radchm Lab Ana Radchm Lab Ana Trng Ctr 09 21 80 Tr E03 Tr E03 Albert M. Reynolds Radchm Lab Ana Radchm Lab Ana Trng Ctr 09 21 80 Tr E03 Tr E03 E. Return From LWOP Name Title Effective Date Brian E. Williams Engg Coop Student E03 (M) 09 02 80 William B. Pendergrass Engg Coop Student E02 (C) 09 08 80 Theresa M. Pickney Engg Coop Student E04 (C) 09 08 80 F. Placed On LWOP Name Title Effective Date David A. Robeson Engg Coop Student E02 (C) 09 08 80 G. Terminations Name Title Effective Date Fred Fraser Janitor F02 09 02 80 Betty J. Grimes Janitor F01 09 09 80 Harlon L. Ramsey Janitor F01 09 10 80 Randall C. Arnold Elect 09 15 80 John D. Quigley Elect 09 15 80 Joe E. Rice Unit Op RL 09 19 80

37 Se tember 1980 Personnel Chan es Houri Name Title Effective Date J. R. Daniel Mach 09 02 80 Robert W. Daniels Mach 09 02 80 Jimmy D. Dean Mach 09 02 80 Jimmy W. Embry Stftr 09 02 80 Billy J. Emmons Stftr 09 02 80 William E. Griggs Mach 09 02 80 Harry F. Hacker Mach 09 02 80 Bennie D. Stults Mach 09 02 80 Thomas M. Thompson Elect 09 02 80 Harold F. Wilson Stftr 09 02 80 Willie T. Eggleston Stftr 09 03 80 Jack D. Gaston Stftr 09 03 80 Lardell Goodloe Elect 09 03 80 Charles W. Warhurst Mach 09 03 80 Bill C. Thornton Stftr 09 04 80 Edwin R. Warren Mach 09 04 80 Morris G. Brown Cons Lbr 09 05 80 Earnest E. Cosby Cons Lbr 09 05 80 William H. Draper Cons Lbr 09 05 80 James P. Fields Cons Lbr 09 05 80 Leon Pope Cons Lbr 09 05 80

38 Se tember 1980 Personnel Chan es Houri e

Name Title Effective Date Thomas F. Schemeltz Cons Lbr 09 05 80 James J. Smothermon Cons Lbr 09 05 80 Loyd C. Canon Cons Lbr 09 08 80 James J. Cashion Cons Lbr 09 08 80 Jimmie 0. Garrett Cons Lbr 09 08 80 A. D. Jackson Cons Lbr 09 09 80 Kenneth R. Smith Mach 09 15 80 Esadore Meeks Cr Op 09 17 80 Albert S. Smith Mortar Mixer 09 30 80 B. Reclassifications Former New Name Title Title Effective Date James S. Watson Elect Elect (A) 09 01 80 Thomas M. Thompson Elect Elect (A) 09 03 80 Lardell Goodloe Elect Elect (A) 09 04 80 C. Transfers Out None D. Transfers En None

16 0 erations Summar (Continued)

September 1980 Chan e in Procedure There were 54 revisions to plant instructions during the month. 47 instructions were changed primarily for corrections. The remaining 7 revisions related to the safe operation of the plant.

Chan e in Facilit Desi n All changes in facility design will be included in the unit outage summary report.

0 erations Summar (Continued)

September 1980 Surveillance Testin Unit 1 A total of 478 surveillance tests were completed on Unit 1 per 151 different test instructions.

Unit 2 A total of 205 surveillance tests were completed on Unit 2 per 95 different test instructions.

Unit 3 A total of 328 surveillance tests were completed on Unit 3 per 115 different test instructions.

39 Se tember 1980 Personnel Chan es Houri E. Terminations Name Title Effective Date Leslie L. Abernathy Cons Lbr 07 15 80 Gary D. Nichols Hach 08 27 80 Charlie E. Keener Cons Lbr 09 04 80 Lloyd W. Guthrie Carpenter 09 16 80 Johnny Norton Mortar Mixer 09 22 80 Harty F. Hacker Hach 09 29 80

40 Si nificant 0 erational Events Unit 1 Date Time Event 9/01/80 0001 Reactor thermal power. at >99%, steady state control rod sequence "A".

1341 Reactor Scram No. 135 from >99% on turbine stop valves closure, due to water causing a short in pressure relay 62-C1, which caused relay KT 303 to trip turbine.

1736 Commenced rod withdrawal.

2025 Reactor Critical No. 156.

2230 Rolled T/G.

2343 Synchronized generator, commenced power ascension.

9/02/80 1500 Commenced PCIOHR from 82% thermal power.

9/03/80 0040 Reactor thermal power at 95%, holding due to "C" string high pressure heaters isolation due to relief valve flange leak.

1939 "C" string high pressure heaters maintenance completed and heaters placed in service.

2030 Resumed PICOHR from 95% thermal power.

9/05/80 1500 Reactor thermal power at 99%, maximum flow.

9/07/80 0015 Reduced thermal power from 99% to 85% for turbine C. V.

tests and SI's.

0230 Turbine C. V. tests and SI's completed, commenced power ascension.

0705 Commenced PCIOHR from 95% thermal power.

0905 Reactor thermal power at >99%, steady state.

9/10/80 1500 Reactor thermal power at >99%, steady state.

9/12/80 2100 Reduced thermal power from >99% to 50% for control rod sequence exchange from "A" to "B".

9/13/80 0205 Control rod sequence exchange from "A" to "B" completed, commenced power ascension.

2130 Commenced PCIOHR from 82% thermal power.

9/14/80 2300 Reactor thermal power was >99%, steady state.

9/16/80 "1843 Reduced thermal power from >99% to 90% for removal of "A" circulating water pump to allow stop log lA1 to be lifted.

1905 "A" circulating water pump placed in service, (mode to cooling towers would not operate due to stuck gate),

commenced power ascension.

2030 Commenced PCIOHR from 95% thermal power.

2300 Reactor thermal power at >99%, steady state.

41 Si nificant 0 erational Events Unit 1 Date Tillle Event 9/19/80 2230 Reduced thermal power from >99% to 77% for removal of "B" reactor feedwater pump for maintenance (excessive vibration).

9/20/80 0216 Reduced thermal power from 77% to 70% for turbine C. V. tests and SI's.

0315 Turbine C. V. tests and SI's completed, commenced power ascension.

1220 Reduced thermal power from 77% to 50% due to loss of unit preferred power, when shutdown board power supply was trans-ferred.

1225 Commenced power ascension.

2030 Commenced PCIOIR from 80% thermal power.

9/21/80 1550 Reactor thermal power at >99%, steady'state.

9/24/80 2222 Reactor Scram No. 136 (1) from >99% thermal power on load re-ject trip from negative ground on main transformer sudden pressure relay circuit.

9/25/80 0530 Commenced rod withdrawal.

0820 Reactor Critical No. 157, sequence "B".

1038 Rolled T/G.

1107 Synchronized generator, commenced power ascension.

2110 Commenced PCIOIK from 67% thermal power.

9/27/80 0015 Reduced thermal power from 99% to 85% for turbine C. V.

tests and SI's.

0125 Turbine C. V. tests and SI's completed, commenced PCIOMR.

1500 Reactor thermal power at >99%, steady state.

9/28/80 1500 Reactor thermal power at >99%, steady state.

9/29/80 0115 Reduced thermal power from >99% to 85% for backwash and precoat condensate demineralizers.

9/30/80 2400 Reactor thermal power at 85%, holding for condensate de-mineralizer problems.

42 Si nificant 0 erational Events Unit 2 Date Time Event 9/01/80 0001 Reactor thermal power at 92%, EOC-3 coastdown control rod sequence "B" .

1500 Reactor thermal power at 90%, EOC-3 coastdown.

9/04/80 1500 Reactor thermal power at 89%, EOC-3 coastdown.

9/05/80 2130 Commenced reducing thermal power from 89% for refuel shut-down (EOC-3).

2247 Reactor Scram No. 109 (manual) from 35% thermal power to accommodate refueling outage.

9/12/80 1320 Received permission for fuel movement operation, holding due to communication porblems.

1650 Communications restored, commenced fuel movement operation to accommodate LPRM maintenance.

9/19/80 1000 Commenced core fuel shuffle operations.

9/30/80 2400 Refueling operation in progress.

43 Si nificant 0 erational Events Unit 3 Date Time Event 9/01/80 0001 Reactor thermal power at >99%, steady state control rod sequence "A".

1455 Reduced thermal power from >99% to 63% due to "A" recir-culation pump trip from a spurious trip.

1522 Reduced thermal power from 63% to 54% due to "A" recircu-lation pump being out-of-service.

2055 "A" recirculation pump maintenance completed and pump placed in service, commenced power ascension.

2200 Commenced PCIOMR from 75% thermal power.

9/03/80 1500 Reactor thermal power at >99%, steady state.

9/07/80 0230 Reduced thermal power from 99% to 75% for turbine C. V.

tests and SI's.

0330 Reduced thermal power from 75% to 67% due to MSIV-1-26 closing too fast (~1.3 seconds).

0430 Turbine C. V. tests and SI's completed, holding at 67%

due to MSIV 1-26 being left in closed position, awaiting maintenance.

1500 Increased reactor thermal power from 67% to 75%, holding due to closure of MSIV 1-26.

9/10/80 1500 Reactor thermal power at 75%, holding due to MSIV 1-26 being closed.

9/12/80 2245 Commenced reducing thermal power from 75% for shutdown for MSIV 1-26 mainte~y~ce.

2355 Reactor Scram No. 88 (manual) from 35% thermal power to accommodate maintenance to MSIV 1-26.

9/14/80 0525 Maintenance to MSIV 1-26 completed, commenced rod with-drawal.

1009 Reactor Critical No. 98.

1706 Reactor was made subcritical due to a feedwater valve (3-219A) leak.

2233 Repairs to feedwater valve 3-219A completed, commenced rod withdrawal.

2243 Reactor Critical No. 99.

9/15/80 0155 Rolled T/G.

0233 Synchronized generator, commenced power ascension.

1600 Commenced PCIOMR from 76% thermal power.

44 Si nificant 0 erational Events Unit 3 Date Time Event 9/16/80 2330 Reactor thermal power at 92%, maximum flow, awaiting rod,pattern adjustment load drop.

9/17/80 2300 Reactor thermal power at 91%, maximum flow, awaiting rod pattern adjustment load drop, 9/18/80 0700 Reactor thermal power at 90%, maximum flow.

9/20/80 1358 Reactor Scram No. 89 (1) from 90% thermal power, on loss of preferred power when "A" 480 volt shutdown board failed to transfer back to normal causing loss of "A" RPS MG set.

2230 Commenced rod withdrawal.

9/21/80 0104 Reactor Critical No. 100.

0440 Rolled T/G.

0500 Synchronized generator, commenced power ascension.

1500 Commenced PCIOMR from 67% thermal power.

9/22/80 2240 Reactor thermal power at 90%, maximum flow.

9/23/80 2145 Reduced thermal power from 90% to 75% for control rod pattern adjustment.

2255 Control rod pattern adjustment'ompleted, commenced power ascension.

2300 Commenced PCIOMR from 82% thermal power.

9/24/80 0725 Reactor thermal power at 93%, holding due to computer malfunction.

2130 Computer back in service, resumed PCIOMR from 93%

thermal power.

9/25/80 0200 Reactor thermal power at 99%, maximum flow.

1500 Reactor thermal power at 98%, maximum flow.

9/27/80 0130 Reduced thermal power from 98% to 80% for turbine C. V.

Tests and SI's.

0217 Turbine C.V. tests and SI's completed, commenced power ascension.

0300 Commenced PCIOMR from 90% thermal power.

1200 Reactor thermal power at >99%, steady state.

9/30/80 2400 Reactor thermal power at >99%, steady state.

(1) Equipment Malfunction

45 Plant Instruction Revisions September 1980 Cate or Instruction Reason for Re uest Change in EHI-46 To include heat tapes at Facility Freeze Protection Program cooling tower.

Design SI 4.2.A.6 Junction boxes have been Primary Containment and added for test purposes.

Reactor Building Isolation Instrumentation Low Pressure Main Steam Line SIHI-3 Density compensation removed System Instrument Maintenance per ECN P-0130, DCR 1533, Index 3- Instruction Reactor workplan 9870 for Unit 2 only.

Feedwater System SIMI-46 Pressure compensation removed System Instrument Maintenance per ECN P-0129, DCR 1532, Index 46 Instruction Feedwater workplan 9838 for Unit 2 only.

Control System Change EMI-44 To implement DPH N 80 Ml, which Required to Reactor Protection System requires an inspection of the Improve the Scram Solenoid Relays movable contacts for a possible Safety of binding problem.

Operation EMI-80 Recurrence control for LER Maintenance of Inboard and Outboard Drywell Leak Detection Isolation Valves 50-259/8040.'TI-23A When controlling in "A" water Refueling Test Instruction level sensor element in case 23A, Feedwater System of 250 VDC normal supply failure.

46 Re ortable Occurrences Occurrence BFRO Date Descri tion Unit 1 50-259/8060 8/14/80 While performing SI 4.2.B-60, thermostat TS-64-73 for "B" core spray pump area cooler fan was found set above the technical specification limit.

50-259/8061 8/14/80 While performing SI 4.2.B-57, a thermal overload on the breaker for 1A RHR area cooler fan was found tripped.

50-259/8063 8/20/80 While performing SI 4.8.B.4.2, CAM 1-RM-90-251 for the turbine building vent was removed from service for a period exceeding one hour.

50-259/8064 8/20/80 While performing SI 4.8.B.4.2, CAM 1-RM-90-249 for the turbine building roof vents was removed from service for a period exceeding one hour.

50-259/8065 8/28/80 Wind direction at elevation 887 M.S.I.

failed. The LCO to restore the inoperable channel to operating status within 7 days was exceeded.

50-259/8066 9/02/80 Operations personnel observed an annunciation on the torus hydrogen containment atmospheric monitoring.

50-'259/8068 9/01/80 Inspection of the fire protection system by a qualified fire consultant was not per-formed within the 3 year interval as required by Technical Specification 3.11.E.2.

50-259/8069 9/02/80 While performing SI 4.2.A-17, channel B of "refueling zone isolation static pressure permissive and static pressure logic systems units 1, 2, and 3" modulating damper 0-PDC 64-8 failed to close.

50-259/8070 9/19/80 During a review of Unit 1 core verification video tape bundle TY 582 at core location 11-06 was found to be 90'ut of proper orientation.

47 Re ortable Occurrences Occurrence BFRO Date Descri tion Unit 2 50-260/8033 8/15/80 During routine test TI-36A an indicated leak was found on RHR heat exchanger 2B.

50-260/8034 8/15/80 During a routine test TI-36A RHR heat exchanger 2C was found leaking.

50-260/8035 8/30/80 Test personnel detected an increase in pressure on the shell side of RHR heat exchanger 2D while performing TI-36A, RHR heat exchanger leak test.

50-260/8036 8/29/80 During normal operation while performing SI 4.7.H, the H H-76-39 hydrogen monitor for the drywell would not calibrate.

50-260/8037 9/14/80 Fuel assemblies TZ 758 in core location 15-26 and TX 399 in core location 29-28 were found to be rotated 90'rom their correct orientation.

50-260/8038 9/11/80 With the unit in cold shutdown during a scheduled refueling outage, HPCI check valve 2-73-609 failed the local leak rate test.

Unit 3 50-296/8031 8/09/80 During the performance of 1'RI 303 it was found that the EECW flow was below the minimum allowed flow on 3B RHR pump seal heat"exchanger.

50-296/8032 8/25/80 While performing RCIC steam line space high temperature SI 4.2.B-32, lead wires were accidently pulled out of the RCIC speed feedback magnetic pickup connector.

50-296/8033 8/15/80 During routine test TI-36A, a leak on RHR heat exchanger 2B was indicated.

50-296/8034 '/29/80 While investigating overload setting for RHR area cooler fans, the overload for 3A RHR pump area cooler fan was found to be set too high.

When the overload was adjusted to the proper setting, the overload relay failed causing the fan to trip.

50-296/8035 9/Ol/80 . The "A" reactor recirculation pump tripped.

The 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO for one pump operation was initiated I,'Technical Specification 3.6.F.1).

48 Re ortable Occurrences Occurrence BFRO Date Descri tion Unit 3 50-296/8036 9/04/80 While running SI 4.9.A.l.a after SEMI-18 had been performed, it was found that diesel generator 3A would not trip to idle speed from a loaded condition.

50-296/8037 9/09/80 During normal operation, while performing SI 4.7.H, H2M-76-39 would not calibrate.

50-296/8038 9/07/80 While running SI 4.7.D.l.b.2 with unit at 99%

steady state power, main steam isolation valve FCV 3-1-26 closed too fast.

Primar Coolant Chemistr September 1980 Parameter Unit 1 Unit 2 Unit 3

1. Gross Radioactivit
a. Crud on 0.45 millipore filter (uCi/ml)

High 3.98E-03 8. 68E-03 5.32E-03 Low 5.00E-04 3.60E-05 4.64E-04 Average 1.22E-03 1.47E-03 1.12E-03

b. Filtrate (uCi/ml)

High 4.01E-01 1.56E-01 2.36E-01 Low 1.13E-01 1.60E-03 6.47E-02 Average 1.79E-Ol 3.29E-02 1.26E-01

2. Sus ended Solids Stained 0.45 milli ore filter ( b High 25 10 Low <10 <10 <10 Average <10 <25 <10
3. Gross Tritium (uCi/ml)

High 1.44E-03 1.17E-03 2.18E-03 Low 1.14E-03 9.88E-04 1.53E-03 Average 1.27E-03 1.04E-03 1.81E-03

4. Iodine-131

~(uC i/ml High 1.02E-03 1.92E-03 7.64E-03 Low 1.89E-04 3.43E-05 2.07E-05 Average 6.88E-04 5.01E-04 1.75E-03 (1) Unit down

50 Primar Coolant Chemistr (Continued)

September 1980 Parameter (Continued) Unit 1 Unit 2 Unit 3

5. Ratio of Todine-131 to iodine-133 High 4.33E-01 1.72E+02 1.32E+01 Low 1.02E-01 3. 45E-01 3.33E-01 Average 2.13E-01 4.93E+Ol 2.64E+00
6. Chloride (ppb)

Limit 100 High <50 <50 Low <50 <50 <50 Average <50 <50 <50 Limit 5.6 or 8.6 High 6.7 6.7 7.0 Low 6.0 5.7 5.8 Average 6.4 6.3 6.2

8. Conductivit (umho/cm 8 25' C.)

eratin Limit 1.0 umho/cm 8 25'.)

Shutdown Limit 10.0 umho/cm 8 25'C.

High 2 8(1) 2 4(l) 2 4(l)

Low .36 .38 .15 Average .72 .81 .53 (1) Unit down

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. V. Jg o ed. i.n ce- - amm =T'ld RR eac OV Scr PN -~tO,88. (ma ua7 ue1 pr. GO I dit on 1ng+ US .J.O axi lunl -l'l- eac or s44p m-. =l2 ont ol- r.od pa tel nL omp lte 5.-0 --S rvi I 2 3 4 5 6 7 8 9 10 11 - 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 28 29 30 31 MONTH OF~Sptkmmer 10 80 ' 63 TVA 7382'PP.l 1 78) NUCLEAR PLANT OPERATING STATISTICS Browns Ferr Nuclear plant Period I lours Month Sen tember 19 80 Item No. Unit No. Average Hourly Gross Load, kW Maximum Hour Net Generation, MWh 3 Core Thermal Energy Gen., GWD(t) 90.660 14.3365 80.1247 Gross Electrical Gen., MIVh 699 320 113 120 625 700 1 438 4 Station Use. MWh 21 477 302 18 Net Electrical Gen., MWh 677 843 107 818 607 023 1 2 4 7 Station Use. Percent 3.07 4.69 2. 8 8 Accum. Core Exposure MWD/Ton 12 610 16 028 1 27 42 9 CTEG This Month, 10 6TU 7,425,276 1 170 328 6 570 852 15 166 456 10 Hours Reactor Was Critical 703.30 118.78 669.05 14 1.13 Unit Use, Hours.Min. 697:13 118:47 654:20 1 470:2 12 Capacit Factor. Percent 88.4 14.3 79.1 60". 6 13 Turbine Avail. Factor, Percent 99. 5 19. 0 100 72. 8 Generator Avail. Factor. Percent 100 19.0 100 Turbocen. Avail. Factor. Percent 99.5 19.0 100 16 Reactor Avail. Factor, Percent 100 16. 5 100 72. 2 17 Unit Avail. F ctor, Percent 98.5 16.5 4.0 18 Turbine Startups 0 19 Peactor Cold Startups 0 0 0 20 21 Gross Heat Rate, Btu/kWh 10,620 10 350 10 500 10 550 22 Net Heat Rate, Btu/kWh 10,950 10,850 10 820 10 890 Cl lJ 23 24 25 26 Throttle Pressure, psig 950 913 38 27 Throttle Temperature, F 539 534 28 Exhaust Pressure, InH Abs. 3.12 3.33 29 Intake Water Temp., F 82.9 87.0 83.8 30 31 32 33 Reactor Feedwater, M Ib/hr 12.4 11.8 11.7 12e 34 Makeup, Percent 36 37 Full Pr. Days to End of Cycle (E) (3) 192 31 38 Oil Fired for Generation, Gallons 2 39 Oil Heatin Value. Btu/Gal. 137 60 40 Diesel Generation, MWh 29.4 Max. Hour I'let Gen. Max. Day Net Gen. Load MWh Time Date MWh Date Factor, % 43 2,972 0600 9-5-80 72, 284 9-4-80 65. 1 Pemarks 1 ~ Informa tion unavailable.

2. Unit 2 refuel outage (EOC-3) began at 2247 hours0.026 days <br />0.624 hours <br />0.00372 weeks <br />8.549835e-4 months <br /> on 9-5-80.

Based on 5% capacity tactor. D t 5 bmitted Date Revised Plant Superintendent TVA 4'C Irn-3 1st UNIT OUTAGE AND AVAILABILITY Brouns Parr Nuclear Plant l licensed Aeactor Power 3293 MIVRh) Unit No. 1152 MW(e) MonthiYear Septcnber 1980 Generator Rata)g Design Gross Electrical Rating 1098 4 MW Period Hours Vail METHOD OF UN I T CORRECTIVE ACTION T)dne Vn)l Available Time NOt Ava))able SHUTTING STATUS Time T)me OUTAGE CAUSE TAKEN TO PAEVENT Vn) I O)dt In DOsvN DURING REPETITION Total Nol V)ed Tw bine Reactor REACTOR OUTAGE sids radn )S)S rdbn ~lr) s Mn Nds M)n H)$ Mdn I srs Min lbs M)n I id) Mdn ~58 06 07 ~0) 55 03 r 55 13 41 23 43 Turbine trl due to sto Scrub liat Standby 24 00 5 IO 12 13 15 18 P.t S~ "4 22 22 00 24 100 22 t22 0~138 22l 22 ~l,d

  • d Scran Oot Standby

~tt on natn transforner sudden 25 J 8~0 L22 )3 ~01 37 05 130 07 ~r) ~41 ressure rota 27 29 30 gC 0 31 1 'tat 1~08 57 )79 13 11 44 03 I 55 11 03 >C OC t, UNIT OUTAGE ANO AVAILABILITY Nuclear Plant Licensed Reactor Power 3293 MW(lh) Urut No Generator Rating~252 MW(e) Month/Year Se cenbee 1980 Design Gross Oectricat Rating~~84 Mw Period Hours 720 Vnil METIIOO OF UNIT CORALCTIVE AC1ION time Vml Avaelbre Time eeet AVasrabre Time Time SIIUTTING STATUS TAI<EN 10 PREVENT OUTAGE CAUSE 1 nrar ~ Cen. llOl Vied Tw bine Aeactor Vml Ovt In DOWN DURING ACPLT ITION nay I lis 4'I n I lis l.bn lbs rvbn ~lus. Msn lbl Mm ~S4S ItlIn l 4S Msn lb s Min llis Mm REACTOR OUTAGE I 24 I 00 24 00 2 ~24 00 ~24 00 22 I 47 22 lC7 06 54 06 i 54 0LLL3 24 '00 &1~ 24L 00 24 00 24 00 I 12 13 15 22 I I I I 25 2Ci I I 27 29 drs ~24 L" Intel 118 47 18 47 582 I 54 82 54 ~ 'is i Licensed Rcatlnr Power 3293 Gcncialnr Rating 1152 Design Gioss Electrical Rating I.IW(c) hIW(th) 1090 ~ 4 MSV U is N .~ UNIT OUTAGE ANO AVAILABILITY Srovns Petr Nuclear Plant hlonih/Year Period Hours Se 720 tenbec 19SO Vnsl Tinsc Unit AvaiNbte Time Not Available METHOD OF UNIT CORRECTIVE ACTION Time Time SHUT TING STATUS TAKEN TO PREVENT OUTAGE CAUSE Toter Gcn, Nol Vscii Tsss bine Reactor Vnil Ovl In DOWN DURING REPETITION trst Mn t ris c.lsn Cist htsn ~trit lain leS Min ~its r Min ~His Mso lrsr htin tlii Min REACTOR OUTAGE 24 i00 24 00 c c sJ IO II 24 IOO 24 ~00 12 00 l05 ~23 55 Maintenance to MSIY 1-26 and Manual llot Stan b 13 c 24 00 feedvater valve 3-219A I ~4 13~08 l5 2it I00 21.IQL 02 33 )fi l7 18 lg +4 I 0 0 jk I 0 08 I32 13 5S lass of nAn RPS MG Sct Stean Ilot Standb ?I ?7 2'K I28 24 1'9i 00 ~05 00 00 05 00 ~7 I ?l c ?6 27 29 t c 30 2~4 24 00 I 3l I Trit.tt 676 31 654 20 22 11 43 9 67 OUTAGE

SUMMARY

September 1980 The unit two reactor shutdown sequence was conducted in an orderly process on September 5, 1980, for refueling activities and routine maintenance to plant equipment. The refuel activities involve disassembly of Unit 2 reactor for refueling operation with reactor startup scheduled for October 26, 1980.

The routine maintenance involves inspection and repairs to major components and safety systems within the plant. The initial containment entry was conducted at 1:05 P.H. on September 6, 1980.

The planned duration for the Unit 2 cylce 3 refuel outage is 49 days. The pre-planned schedule shows that turbine inspection and maintenance work sequence as the critical work path, a fix'st at Browns Ferry Nuclear Plant. In order to prevent the outage duration from exceeding the 49 day schedule, non-curcial modifications are being minimized, however, major modifications intended to meet safety requirements are being performed.

68 ELECTRICAL MAINTENANCE

SUMMARY

September 1980 Unit 1 There were no major maintenance on CSSC or non-CSSC equipment during the month. Unit 1 tripped when a ground in the wiring to the sudden

~

pressure relay caused a transformer trip. The ground was cleared and the unit returned to service. A summary of non-CSSC and CSSC maintenance activities is given in the following electrical maintenance summary.

Unit 2 Major activities include major maintenance inspections to PCB's 5244 and 5248, inspection of 2A 500 kV transfoxmer, and inspection and repair of leaks on 2B and 2C main transformers. At the close of the month, work is 90% complete on PCB 5248 and 25% complete on PCB 5244. The inspection of 2A main transformer is complete and final testing in progress. Work continues on 2B main transformer. The 2B condenser circulating water pump motor failed on September 2. After testing, the motor was sent to the service shop for repairs. The motor is due back in early October.

Routine refueling outage activities are in progress. A summary of other non-CSSC and CSSC maintenance activities are given in the following elec-trical maintenance summary.

Unit 3 A scram occurred on Unit 3 when returning 480 volt shutdown board 3A to service following changing the tap setting on transformer TS3A. The tap setting was also changed on transformer TS3B and TS3E. There was no

69 ELECTRICAL MAINTENANCE

SUMMARY

(Continued)

September 1980 Unit 3 (Continued) major maintenance on CSSC and non-CSSC equipment. A summary of other non-CSSC and CSSC maintenance act'ivities is given in the following elec-trical maintenance summary.

Common NONE

DROWNS PEit1;YiilUCLHtll PLAIT UHIT 1 ELECTRICAL HAINTENANCE SRBfhRY 1'or the Honth of E ect on Sa c Action Taken 0,". te System Component Nature of Operation of Cause of Results of To Preclude Haintenance The Reactor Halfunction Halfunction Recurrence 9/2/8 Neutron RBH Bypass RBH Bypass NONE RBH Switch Bad Switch would not go Replaced RBH switch.

Honitor in Switch Switch on in bypass Checked switch for panel 9-5 proper operation.

needs repair- Switch functioned ing okay. TR8 179518 9/23/80 RNR ECV-74-71 RHR valve Unit in limiting Hotor burned up Valve inoperable. Performed EHI 71.

1.-74-71 won' condition for Replaced old motor.

run operation Performed EHI 18.

(TS.3.5.8.7) Valve now functioning properly. TR8 165755 LER No. BPRO 50-259/

8072 o

URU!'UR "URRT UUCUElS PXRUT UUXT 2 IQ,XNTENANCE SUtkfARY For the Honth of September ]9 80 E ectonSae Action Taken Nature of Operation of Cause of Results of To Preclude D.". te System Component ftmc tion Recurrence Haintenance The Reactor Halfunction ~Rfal 2B i 9/21/80 RBCCH RBCCH Pump 2B RBCCH pump NONE tutor failed. Loss of 2B RBCCH Hotor repaired motor trips pump motor. shop, then at'ervice out. Sparks returned to service.

reported com- TlU/ 178647, 160689 ing from the motor.

9/22/80 RHR FCV-74-24 Valve will NONE Hire loose in alve would not cycle Tightened loose wire not cycle . motor starter> on overload assembly overload assembly in motor starter.

Valve operated okay. TRt 1'78632

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URONNS PERRY NUCLEAR PLRNT UNIT ELECTRICAL MAINTENANCE

SUMMARY

NON-CSSC E UIPMENT Pot tbe Noetb oP SePtelnber IP SO Nature of Cause of Malfunction or onent Maintenance Maintenance Action Corrective Action DaLe System Com 9/13@0 RWCU 2A RMCU 2A RWCU demin. F Step switch not working Adjusted step switch. Checked demin. valve will not properly. okay. TR8 169260 open during precoat step.

9/17/80 Reactor water 2B reactor 2B RMCU pump Motor bad. Replaced with rebuilt motor.

cleanup. water clean- 'motor locked up Checked okay, Tlg 180452 up.pump motor 9/19/80 Main steam FCV-1-59 Valve will not Motor burned up and Replaced motor an'd torque switch.

operate. torque switch bad. Performed EMI 18. Checked okay,

-

TR8 160644 9/21/80 FCV-69-8 RMCU demin, bypass Broken limit switches in Replaced broken limit switches.

valve will only, valve FCV-2-69-8. Performed EMI 16 and 18. Checked open and close. okay. T1UI 169299

UROIINS PERRY NUCLEAR PLAN'1'NLT NON-CSSC E UZPlmNT ELK'CTRXCAL ifAXHTENANCH SUiQlARY pot tha Hooth of RapteaIbet 19 80 Nature of Cause of Halfunction or l)a te System Com onent Haintenance Haintenance hction Corrective Action 1

9/25/80 RWCU 3A RMCU 3A RMCU demin. Switch .contacts dirty. - "

Inspeated switches and cleaned demin. stepping switch contacts. Checked okay. Tip stepping needs to be 179.318 switch cleaned and checked.

76 MECHANICAL MAINTENANCE SALARY September 1980 Unit 1 On September 19, 1980, the 1B RFP was experiencing high vibration problems. The RFP coupling was inspected and was found to be low in lub-ricant. The RFP coupling was disassembled, cleaned, and filled with new lubricant. This corrected the vibration problem. The mechanical controls on all RFP turbines were inspected for proper lubrication and cleanliness.

Unit 2 Twenty-three of the CRD scram pilot solonoid valves were rebuilt during the month. A number of valves throughout the turbine and reactor building were worked on for packing leaks, broken diaphragms and o-rings.

Some of the small hand control valves were replaced due to steam cuts around bonnet gasket surfaces. The 2A RCW booster pump discharge check valve was replaced because the old discharge check valve was stuck in the open position and beyond repair. The 2B reactor water cleanup demineralizer resin trap was replaced on 'September 6, 1980. 2A RCW pump isolation valves were dis-assemble, cleaned and reassembled. The RCIC turbine and pump were inspected during the last week of September and all outage work was completed September 30, 1980. The Unit 2 HPCI work is behind schedule due to delayed shipment of the new pedestal. The disassembly work has begun on the removal of the temporarily repaired pedestal performed earlier this year due to water hammer damage. The RHR and recirculation system valves graffoil packing was adjusted during the month.

77 MECHANICAL MAINTENANCE

SUMMARY

(Continued)

September 1980 Unit'3 Unit 3 ran essentially all month with only minor repair work with the exception of repair work to 3B MSIV. The MSIV had closed too fast during a routine surveillance instruction test. The unit was removed from service September 13, 1980, for inspection and repair to the MSIV.

The valve operator was found to be approximately three quarts low of oil.

Oil was added to the operator and the valve functioned properly. No sign of oil was evident on the floor or around the valve at the initial inspection.

3B CRD filter required replacing on September 25, 1980. The Unit 3 RCIC had to have three quarts of oil added on 'September 8, 1980. The outboard packing on 3A fuel pool cooling pump required tightening on September 22, 1980.

Common Scheduled maintenance of all service air compressors were performed September 24, 1980. No significant problems were found. The raw cooling water. lines to the CRD pump bearing were cleaned during the first part of the month. The 1B RHRSW pump vibration reading was above the acceptable limits on September 25, 1980, and the pump was pulled and disassembled during 'the last few days in September.

2

'I CSSC E UXP:kk;I!T IKCIU.NXCAL HAXNTENAN"F. SUIQ4<RY EFFECT ON SEVE ACZXON TAI'EN DATE SYSTP~I CC~!PONENT NATUIIK OP OE'EBATXO:I OF CAUSE OP RESULTS OF '19 PRECLUDE E'i1.ViTENAi ICE TIIE -RI~CTOR I!.'iLPUNCTXON I'ALFUNCTXON RECURRENCF.

9/22/80 RCTC Turbine exhaus Ruptured none old disk Ruptured disk Replaced disk with rupture disk disk ruptured new one TR 103732

3 CSSC EOUXPH 2!T HECHAKXCAL KXINTENANCE SUGARY EFFECT ON SAFE ACTION TAl:i;N BATE SYSTBf CGiaiPONEN T iB.'L'URE OF OPERATXO:i'F CAUSE OF RESULTS OF '10 PRECLUDE KXXNTENANCE 1dE REACTOR Y~LFUNCTION NALFUNCTXGN RECURRENCE 9/17/80 Fuel pool 3A FPC pump Outboard pack- None Packing leak Packing leak coolin Adjusted packing in TR 178817

1 I.'02-CSSC~EUIPl KHT lKCHANICAI, MLU"HA11CE SLMQRY For the ltoeth of September tp 80 Nature of Cause of 14alfu>>ction or Date S stem Com nnent ?faintenance llaintenance Action Corrective Action 9/12/80 Radwaste FSV-77-19 Bad solenoid valve Bad solenoid valve Replaced solenoid valve TR 182079 9/19/80 Reacotr Feed- 1B RFP High vibration Lube oil dried out in Cleaned coupling and put new oil um cou lin TR 103114

t0:4-CSSC~F. UIPl KHT >?EC?>AHICgZ. HAP?T"HAHCE SEQfAPY For the ?fonth of September 19 80 Nature of Cause of Malfunction or Date S stem Com onent  ? fai.n tenance llaintenance Action Corrective Action S

9/80 RCW 2A RCM pump Isolation valve Isolation valve out of Removed, cleaned, and a'djusted, and isolation 2-24-516 A,B,&C adjustment reinstalled valves ,2-24-520 A,B,&C TR 119083, 119085, 119086 would not close

.9/28/80 Hain Steam PCV 1-167 Valve binding Valve binding Cleaned, lubricated, and adjusted valve TR 166667 9/24/80 Heater drains LCV-6-73A Bad o-rings and Bad o-rings and diaphragm Replaced o-rings, diaphragm.

and vents diaphragm Adjusted packing and lubricated ste TR 166658 9/25/80 Heater drains LCV-6-73B Bad o-rings and Bad o-rings and diaphragm Replaced o-rings, diaphragm.

and vents diaphragm Adjusted packing and lubricated sten TR 166659 9/25/80 Heater drains LCV-6-62A Bad o-rings and Bad o-rings and diaphragm Replaced o-rings, diaphragm.

and vents diaphragm Adjusted packing and lubricated ste TR 166661 9/25/80 Heater drains LCV-6-62B Bad o-rings and Bad o-rings and diaphragm Replaced o-rings, diaphragm.

and vents diaphragm Adjusted packing and lubricated stem TR 166662 9/10/80 Feedwater HCV-3-211A Bad seat in valve Bad seal in valve Replaced valve TR 180437 9/9/80 Heater drains HCV-6-418A Bad seat in valve Valve seat worn Replaced valve and vents TR 180438

82 INSTRUMENT MAINTENANCE SALARY September 1980 Unit 1 There were no major instrument maintenance or modification activities on Unit 1 this month.

Unit 2 Extensive time and effort has been expended this month on refueling outage related routine calibration, maintenance and modification activities. Major areas include:

Installed the Hays-Republic oxygen and hydrogen analyzer system, including writing of new surveillance instructions, maintenance procedures, and initial calibrations.

Implemented DCR 1937 by work plan 6617. This modification replaces six mercoid pressure switches in the condensate system.

Implemented DCR 1892 by work plant 9818. This modification prevents feed-water control loops from reading downscale upon meter failure.

Replaced twelve LPRM detector assemblies due to end of life criteria. An additional LPRM assembly had to be replaced due to being irreparably damaged during preliminary LPRM activities. All thirteen assemblies are of the GE NA-200 breeder types.

Representatives from the General Electric Company in conjunction with Instrument Maintenance personnel conducted extensive testing on the EHC system to resolve the tubing vibration and servo valvea'ilure problems. Realignment and modifications include: increase the dampening on the fluid pressure sensors, changed the valve movement operating point to the second slope of the Diode Function Generator and attached the sensing line to the wall at four foot intervals.

83 INSTRIRKNT MAINTENANCE

SUMMARY

(Continued)

September 1980 Unit 3 N

There were no major instrumentation maintenance or modification activities on Unit 3 this month.

Common DCR's were initiated this month concerning the following modifications:

-1. Replacement of FE-66-111 in the off-gas system, due to the flow element not being reliable and spare parts not available.

2. Enclose and air condition the off-gas hydrogen analyzer area. This modification will imporve the environment of the electronics and therefore improve the reliability of the system.
3. Incorporate additional HPCI and RCIC testing parameters'into the Real-time evaluation, monitoring and analysis system.
4. Replacement of the freestanding E-Field mounted on the face of pilars at the intake pumping station with a microwave transmitter and receiver system.
5. Extending the E-Field in sectors 4 and 5 along the wingwalls of the intake to the waterline.
6. Installation of additional standby batteries in the PERIM-ALERT and Wells Fargo system to sustain operation for at least 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following a power failure. This modification is due to NRC specification WA-00450B.

INSTR12KNT MAINTENANCE SUKfARY (Continued)

September 1980 Com uter S stem System availability for the units 1 and 2, and unit 3 process computer was 98.47% and 99.86% respectively. Downtime was due to analog scanner problems which was resolved by replacing 25 leaking diodes.

System availability for the PRIME computer was 100% with only routine mainte-nance being performed.

System availabiltiy for the RRRMS PDP 1134 computer was 99.93%. Downtime was due to high temperature in the computer room (1/2 hour).

The Instrument Maintenance section in conjunction with the Controls & Test Section has installed two NOVA 1200 computers in the secondary alarm station to monitor the RUSCO MAC S40. This system will allow report generating and up-to-

'

date cross reference of all coded data form the cardkey system.

Securit S stems RUSCO Card Access S stem On September 2, we experienced another system malfunction due to power transfer. As of this date, we still have not received the recommendations from Chattanooga or Knoxville for an uninterruptable power supply to help stabilize our power source.

CCTV Browns Ferry now has 18 CCTV cameras in operation. These cameras and associated monitors are requiring daily maintenance for adjustment and re-location for security and fuel pool activities.

Intrusion Detection Hells Far o Performed routine maintenance and repair on MP2 modules, AS24 boards, and Cu-3 boards. Failure rates on these components are much higher than expected.

85 INSTRUMENT MAINTENANCE St&MARY The following instrument Maintenance Summary tabulates man-hours expended on instrument maintenance, calibration, loop checks, and work plans for various plant systems.

Unit Total Svs tern 3 M-H Main Steam 30

2. Condensa te Ho 0 39 515 74 62
3. Reactor Feedwater
5. Extraction Steam
6. Heater Drain and Vent 40 320
12. Auziliarv Boiler
18. Fuel Oil
23. RHR Service Water 51 51
24. Raw Coolin Water
25. Raw Service Water
26. High-Pressure Fire Protection
27. Condenser Circulatin Water 36
28. Water Treatment
31. Air Condition Coolin and Heatin 10 10
32. Control Air 21
33. Service Air
34. Vacuum Primin
35. Generator H dro en Coolin
37. Gland Seal Water
39. COo
40. Station Draina e
43. Sam lin and Water Oualitv 45 45 94
44. Buildin Heatin
46. Feedwater Control
47. Turbo enerator Control 21 181 207
53. Demineralizer Backwash Air
56. Temo rature Monitorin 102 71 173
58. Biothermal Research 10 10
63. Standbv Li uid Control Prima ~ Con tainmen t 51 55 28 134
65. Standbv Gas Treatm nt 66 Off-Gas 157 237 468

'7.

Eeer enc E nionen~ttoolin !Pater 12 12 32

68. Reactor Water Recirculation 304 28 340
69. Reactor Water Cleanup 35 147 187
70. Reactor Buildin Closed Coolin Hater 49 55
71. Reactor Core Isolation Coolin
73. Hi~h-Pressure Coolin In ection 43 72 10 125
74. Residual Heat Removal 34
75. Core Sorav Isolation Coolin 32 32

86 INSTRUMENT MAINTENANCE S'CHARY (Continued)

Unit Total S stem M-H

76. Containment Inertin
77. Radvaste 1 0
78. Fuel Pool Coolin and Demineralizin
80. Prima Containment Coolin
82. Standb Diesel Generator
84. Containment Air Dilution
85. Control Rod Drive H draulic
90. Radiation Monitorin 308 550 228 1086
92. Neutron Monitorin Travelin In-Core Probe TIP 26 24 50
96. Recirculation Floe Control
99. Reactor Protection RPIS 330 335 EHC 245 259 SI 743 1075 781 2599 IMI 129 151 504 427 1211 Comouter 4020 313 313 Prime RRK 1S Pere herials 321 321 Card Ke 203 203 intrusion Detection 304 304 Closed Circuit T.V. 256 256 Portal Monitors 49 49 98 Standards 16 319 319 654 Coolin Towers 331 331 General Instrument Pork 443 179 139 761 Instrument Repair 32 32 Recorder Maintenance 223 223 General Employee Trainin 65 177 61 307 ADDrentice Trainin 262 308 204 774 H P. Trainin 12 8 39 B'.JR Instrumentation) Trainin "C" Zone Dressout 100 211 127 438 Radiochem 1ab 260 260 520 H P Lab 255 255 TR's Received/Completed 45 45 96 86 33 27 125 111 299/269 Dual Rate Foremen 62 20 93 Outa e Sup ort 25 Hand and Foot Monitors 47 47 X Rav 17 17 I.D. Camera 42 Overtime Seismic Monitors'2 292 239 30 5003 441 5975 30

BROWS l FERkY'UCLEAR PLANT UNIT 1,2,3 INSTRUI'IENT MAINTENANCE SUI MARY I

CSSC E UIPlfENT FOR THE HONTII OF September 19 80 NATURE EFFECT ON SAFE CAUSE ACTION TAKEN DATE SYSTEH COMPONENT OF OPERATION OF OF RESULTS OF TO PRECLUDE MAINTENANCE THE REACTOR MALFUNCTION MALFUNCTION RECURRENCE Unit 1 9-2 Containment H 2

A-76-37 Replace None Faulty Heter Alarm would not None Inerting reset P rimary PDT-64-138 Calibrate None Zero 'Shif t Did Not Indicate None Containment with Redundant 9-24 Reactor TI-70-56 Replace None Broken Indicator Did Not Indicate None Building Closed Cool-ing Hater Unit 2 9-23 lligh Press- PS-26-78J Calibrate None Instrument Drift Setpoint Incorrect None ure Fire Protection Unie 3 9-25 Emergency FI-67-9A Calibrate None Zero Shif t Indicated Low Flow None Equipment -12A Cooling Mater RllR Service PT-23-11 Calibrate None Zero Shift Indicated Low Pressur None Hater FH-23-42 Calibrate None Zero Shift Indicated Low Flow None FH-23-48 Calibrate None Zero Shift Indicated Low Flow None

88 Radioactive Li uid Effluents September 1980

1. Gross Radioactivit Units a) Total Release (1) Curies 1.36E+00 b) Average Diluted Concentration Released uCi/ml 3.16E-08 c) Maximum Concentration Released uCi/ml 1.91E-07 d) Percent of Applicable Limit (20 Ci/quarter) 6.80E+00
2. Tritium a) Total Release Curies 1. 93E+00 b) Average Diluted Concentration Released uCi/ml 4.49E-08 c) Percent of Applicable Limit (3E-03 uCi/ml) 1.50E-03
3. Dissolved Noble Gases (2) a) Total Release Curies <3.07E-02 b) Average uCi/ml <7.12E-10 c) Percent of Applicable Limit (6E-06 uCi/ml) <1.19E-02
4. Gross Al ha Radioactivit a) Total Release Curies 3.96E-05 b) Average Diluted Concentration Released uCi/ml 9.19E-13
5. Volume of Li uid Waste to Dischar e Canal Liters 2.87E+06
6. Volume of Dilution Water Liters 4.33E+10
7. Isoto es Released Ci Ba/La-140 <5.15E-04 Co-58 <1.85E-03 (1) Based on pre-release analyses which are not decay corrected (2) includes Xe-133, Xe-135, and others (3) Released on basis of MPC

89 Radioactive Li uid Effluents (Continued)

September 1980 Isoto es Released (Continued) Units Co-60 <1.31E-02 Cr-51 <1.56E-02 Cs-134 <2.64E-02 Cs-137 <3,20E-02 Fe-59 <8.01E-04 I-131 <6.94E-03 Mn-54 <2.58E-03 Mo-Tc-99m <8.39E-04 Na-24 2.71E-02 Nb-95 <1.17E-03 Sr-89 2.98E-03 Sr-90 4.07E-04 Zn-65 <1.51E-02 Zr-95 <1.25E-03 Others F-18 7.94E-04 Cs-136 <9.02E-04 Cu-64 <9.62E-03 I-133 <2.04E-03

90 Radioactive Liquid Effluents (Continued)

September 1980 Others (Continued) Uni ts Ci Mn-56 <1.47E-04 Sb-122 <3.53E-03 Sb-124 <7.03E-04 Xe-133 <1.51E-02 Xe-135 <1.17E-02 I-135 <6.82E-03 Br-82 <1.07E-03 As-76 <3.78E-03 Ag-110m <2.02E-03 Sb-125 <7.39E-04 As-74 <7.39E-04 NOTE: Symbol < indicates sums of nuclide activity influenced by values representing threshold limit of analytical sensitivity. Thus, re-ported values are conservatively higher than actual release.

91 Airborne Releases (1)

September 1980 Summation of All Releases Unit This Month A. Fission and Activation Gases

1. Total Release Ci <1.43E+04
2. Average release rate for period uCi/sec. <4.73E+03
3. Percent of Technical Specification limit 9.46E+00 B. Iodines
1. Total Iodine-131 Ci 7.50E-03
2. Average release rate for period uCi/sec. 2.48E-03
3. Percent of Technical Specification limit 6.21E-01 C. Par ticulates
1. Particulates with half-lives 8 days <3.29E-03
2. Average release rate for period uCi/sec. <1.09E-03
3. Percent of Technical Specification limit 2.7E-01
4. Gross Alpha radioactivity Ci <1.43E-09 D. Tritium
1. Total release Ci 7. 07E+00
2. Average release rate for period uCi/sec. 2.34E+00
3. Percent of Technical Specification limit 1.87E+00
4. Ground Level Release Ci 6.74E+00
5. Elevated Release 3.31E-01 (1) Reporting period 35 days

92 Airborne Releases (Continued)

September 1980 Elevated Releases A. Fission Gases Unit This Ifonth

1. Krypton-85 Ci 7.73E+00
2. Krypton-85m 2.05E+03
3. Krypton-87 <8.19E+02
4. Krypton-88 Ci <3.18E+03
5. Xenon-133 6.28E+03
6. Xenon-135 <1.88E+02
7. Xenon-135m Ci <8.17E+01
8. Xenon-138 Ci <4.60E+02 Others (specify)
9. Argon-41 Ci <3.13E001 Unidentified Ci NA Total for Period Ci <1. 31E+04 B. Iodines
l. Iodine-131 Ci 5.18E-03
2. Iodine-133 <4.45E-03
3. Iodine-135 <3.99E-03 Total for Period <1.36E-02

93 Airborne Releases (Continued)

September 1980 Elevated Releases C. Particulates Unit This Month

l. Strontium-89 Ci 4.61E-06
2. Strontium-90 3.82E-07
3. Cesium-134 <1.03E-05
4. Cesium-137 Ci <1.01E-05
5. Barium-140 <6.55E-05
6. Zirconium-95 Ci <2.19E-05
7. Niobium-95 <9.79E-06
8. Cobalt-58 Ci <1.02E-05
9. Ifanganese-54 <8.85E-06
10. Zinc-65 Ci 3.78E-05
11. Tron-59 <2.25E-05
12. Cobalt-60 1.73E-05 Other (speci fy)

N/A

13. Lanthanum-140 <6.70E-05 Total for Period Ci <2.86E-04 D. Tritium Ci 3.31E-01

94 Airborne Releases (Continued)

September 1980 Ground Level Releases A. Fission Gases Unit This Month

1. Krypton-85 <3.69E-03
2. Krypton-85m <2.78E+01
3. Krypton-87 Ci <6.80E+Ol
4. Krypton-88 <9.11E+01
5. Xenon-133 <1.22E+02
6. Xenon-135 <1.85E+02
7. Xenon-135m <1.86E+02
8. Xenon-138 Ci <4.89E+02 Others (specify)
9. Argon-41 <4.14E+01 Unidentified Total for Period <1.21E+03 B. Iodines
l. Iodine-131 Ci 2.32E-03
2. Iodine-133 <1.79E-03
3. Iodine-135 Ci <9.94E-03 Total for Period <1.41E-02

95 Airborne Releases (Continued)

September 1980 Ground Level Releases C. Particulates Unit This Month

1. Strontium-89 Ci 1.93E-06
2. S trontium-90 1.79E-06
3. Cesium-134 <1.35E-04
4. Cesium-137 Ci 1.30E-04
5. Barium-140 Ci <4.87E-04
6. Zirconium-95 <2.69E-04
7. Niobium-95 <1.21E-04
8. Cobalt-58 <1.18E-04
9. Manganese-54 <1.20E-04
10. Zinc-65 <4.98E-04
11. Iron-59 2.88E-04
12. Cobalt-60 4.32E-04 Others (specify)

N/A

13. Lanthanum-140 Ci <3.94E-04 Total for Period <3.00E-03 D. Tritium 6.74E+00

96 Solid Radioactive Waste (1)

September 1980 Low Level Shi, ments Approximate Volume of Sludge Shipped 42.1 Cu. M. (1486 Cu. Ft.)

Total Curies Shipped 195.2 Principal isotopes MAP, MCP (Dewatered Resins)

Dis osal Facilit 9/08/80 Barnwell, SC 9/10/80 Barnwell, SC 9/12/80 Barnwell, SC 9/16/80 Barnwell, SC 9/18/80 Barnwell, SC 9/21/80 Barnwell, SC 9/23/80 Barnwell, SC 9/30/80 Barnwell, SC Hi h Level Shi ments Approximate Volume of Sludge Shipped 17.7 Cu. M. (624 Cu. Ft.)

Total Curies Shipped 282.6 Principal isotopes MAP, MCP (Dewatered Resins)

Dis osal Facilit 9/09/80 Barnwell, SC 9/15/80 Barnwell, SC 9/19/80 Barnwell, SC 9/24/80 Barnwell, SC Footnotes on next page.

97 Solid Radioactive Waste (Continued)

September 1980 Slud e Inventor Condensate and Waste Phase Separator Sludge on Hand 34.0 CU. M. (1199 CU. Ft.)

Cleanup Phase Separator Sludge on Hand 5.7 Cu. M. ( 200 Cu. Ft.)

Drummed Shi ments (2)

Total Number of Drums 233 Total Curies Shipped 18. 2 Principal Isotopes CR5 1 ~ CS 1 37 ~ ZN65 j C060 ~ MN54 ~ SR90 Date Shi ed Dis osal Facilit 9/17/80 Barnwell, SC 9/19/80 Barnwell, SC

98 Solid Radioactive Waste (Continued)

September 1980 Boxed Shi ments (2)

Total Number of Boxes 22 Total Curies Shipped 0.1 Principal Isotopes CR51,CS137,ZN65,C060,i$ 54,SR90 Dis osal Facilit 9/11/80 Barnwell, SC 9/17/80 Barnwell, SC (1) All shipments by Sole-use truck.

(2) Combination box/drum shipments on these dates.

99 Solid Radioactive Waste (Continued)

September 1980

~scmaac Shipped to Stored Allotted Barnwell Onsite ~sac e Drums 1747.5 ft 1650 ft 6149.5 ft Boxes 2292 ft 3100 ft Resin 2110 6149.5 ft 4750 ft 6149.5 ft

100 Effluent and Waste Dis osal Monthl Re ort September 1980 Su lemental Information

1. Batch Releases Li uid Units a) Number of batch release Each 32 b) Total time period for batch releases Minutes 10883 c) Maximum time period for a batch release Minutes 783 d) Average time period for batch release Minutes 340.1 e) Minimum time period for a batch release Minutes 180
2. Batch Releases Gaseous None
3. Abnormal Releases Liquid None
4. Abnormal Releases Gaseous None

101 Resin Usage for September 1980 Resin Cu. Ft.

Powdered Volume Bead Resins Radwaste Floor Drain Filter 516.0 516.0 Waste Demineralizer 130.0 Waste Filter 192.0 192.0 Fuel Pool Demineralizers (1) 16.0 16.0 Reactor Water Cleanu Unit 1 120.0 120.0 Unit 2 56.0 56.0 Unit 3 12.0 12.0 Condensate Demineralizers U it 1 827.0 827. 0 Unit 2 198.0 198.0 Uni 376.0 376.0 Totals 2313.0 130.0 2313.0 (1) Total Resin Volume includes 16.0 cu. ft. of Overlay Haterial.

(2) Total Resin Volume includes 63.0 cu. ft. of Overlay Haterial.

(3) Total Resin Volume includes 20.0 cu. ft. of Overlay Haterial.

(4) Total Resin Volume includes 17.0 cu. ft. of Overlay Haterial.

102-Powdered Resins  % Total Usa e September 1980 Radwaste Usa e Total Floor Drain Filter 516.0 / 2313.0 22.3 Waste Filter 192.0 / 2313.0 8.3 Reactor Water Cleanu Unit 1 120.0 / 2313.0 5.2 Unit 2 56.0 / 2313.0 2.4 Unit 3 12.0 / 2313.0 0.5 Condensate Demineralizers U it 1 827.0 / 2313.0 35.8 U.it 2 198.0 / 2313.0 8.6 (4)

"'.it 3 376.0 / 2313.0 16.3 Fuel Pool Demineralizers (1)

ALL UNITS 16.0 / 2313.0 0.7 (1) Total Resin Volume includes 16.0 cu. ft. of Overlay Material.

(2) Total Resin Volume includes 63.0 cu.-. ft. of Overlay Material.

(3) Total Resin Volume includes 20.0 cu. ft. of Overlay Material.

(4) Total Resin Volume includes 17.0 cu. ft. of Overlay Material.

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106 Fuel Claddin Inte rit Parameters September 1980 Unit 1 Reactor Water Iodines (uCi/sec.)

Date I-131 I-132 I-133 I-134 I-135 9-04-80 2. 97E+00 1. 68E+01 6.86E+00 3.71E+Ol 1.24E+01 9-22-80 l. 92E+01 3. 15E+02 1.08E+02 3.77E+02 1.82E+02 Fission Gases at Dischar e of SJAE (uCi/sec.)

Date Xe-138 Kr-87 Kr-88 Kr-85m Xe-135 Xe-133 9-02-80 1. 33E+03 4. 43E+02 2. 87E+02 1. 47E+02 1.21E+03 3.10E+03 Off-gas flow rate 13 scfm 0 >Ãt 9-23-80 4.72K+04 1.76E+04 8.87E+03 6.44E+03 2.62E+04 1.45E+04 Off-gas flow rate 50 scfm 3265 11Wt Unit 2 Reactor Water Iodines uCi/sec.)

Date I-131 I-132 I-133 I-134 I-135 9-04-80 3.36E+00 1.74E+01 6.40E+00 2.25E+01 1.04E+01 9-22-80 (Unit Outage)

Fission Gases at Dischar e of SJAE uCi/sec.)

Date Xe-138 Kr-87 Kr-88 Kr-85m Xe-135 Xe-133 9-02-80 9.52E+03 1.42E+03 8.16E+02 6.06E+02 2.08E+03 6.97E+02 Off-gas flow rate 120 scfm 2985 Mit 9-23-80 (Unit Outage)

Off-gas flow rate 0 scfm 0 M<t

107 Fuel Claddin Inte rit parameters (Continued)

September 1980 Unit 3 Reactor Water Iodines (uCi/sec.)

Date I-131 I-132 I-133 I-134 I-135 9-04-80 3.28E+01 2. 26E+02 5.49E+01 1.79E+02 9.23E+01 9-22-80 6.67E+00 l. 22E+01 7.04E+00 2.94E+Ol 9.64E+00 Fission Gases at Dischar e of SJAE (uCi/sec.)

Date Xe-138 Kr-87 Kr-88 Kr-85m Xe-135 Xe-133 9-02-80 3.27E+03 3.29E+02 1.62E+02 <4.86E+00. 4.62E+02 3.03E+02 Off-gas flow rate 42 scfm 2497 HWt 9-23-80 5.48E+03 6.83E+02 3.48E+02 2.09E+02 8.04E+02 2.24E+02 Off-gas flow rate 80 scfm 3018 MWt

j w r

. 1980 Year THROUGHPUTS (1)

WASTE TREATMENT SYSTEM VOLUME (2) September Month FLOOR TO CANAL FLOOR

9. 47E+04 DRAIN FLOOR DRAIN 1.40E+04 2.53E+04 d 'RPLE gpd gpdd COLLECTOR DRAIN FILTER TANK

[ 2. 84E+06 ]

TANK

[ 4.19E+05 ] [ 7.58E+05 ]

3 756

[ 2. 84E+06 ]

LAUNDRY DRAIN 7~27 E+0

[2. 18E+05

~pd

[ 0 TANK ]

[ 2. 42E+06 ]

EVAPORATOR 0'pd 0 gpf DISTILLATE

'2 . 00E+06 TANK 4,03E+03 gpd [0 ]

[ 1.21K+05 ]

WASTE WASTE CONDENSATE WASTE WASTE ~2.14K+05 pd 2.10E+05 gpd COLLECTOR SAMPLE STORAGE TANK FILTER DEMINERALIZE TANK TANK (4) [6.42E+06 ] [ 6.30K+06 ]

308 130 ft

[6. 42E+06 ] (9-17-80) gpd evetage gallons pet day (1))Represents 30 days Values accurate to two (2) signifjcant figures [ ] total gallons 240 Ft3 of powdered resins 516 Ft of mixed resin/filter media 3

116 Ft of powdered resins 192 'Ft of mixed resin/filter media (p ) 3

'P 109 WATER TREADKNT CHEMICAL USE Browns Ferr Nuclear Plant Month Year September 198,0 CHEMICALS REQUIRED DESCRIPTION AMOUNT Grade, concentration  %, Pounds, Gallons, Cuft, etc.

Anh drous etc.

This Month/Year To Date BOILER WATER MAKEUP TREATifENT Aluminum Sulfate 2700 lbs 8700 lbs Anthracite (filter media)

Coagulant aid, Polyelectrolyte (Wisprofloc 20)

Sodium hydroxide 11. 9 tons 65.8 tons Sulfuric acid, demineralizer 8.2 tons 65.9 tons Coagulant liquid polymer (Magnifloc 575-C) 1000 lbs BOILER WATER SECONDARY TREATMENT Ammonium hydroxide 1 gal 13 gal Hydrazine, hydrate 1 gal 12 gal Powdex, PAO (Wet) 20,790 lbs 111,870 lbs Powdex, PCH (Wet) 51,650 lbs 272,650 lbs Resins, bead type (stator cooling) 19 Cu Ft 28 CU Ft Celite, Supergel HSC 1,200 lbs 19,900 lbs Epicor PD-1 anion (Dry) 192 Cu Ft 4,056 Cu Ft Epicor PD-3 cation (Dry) 216 CU Ft 5,496 Cu Ft Epicor AC-31 Mixed Bed (Gravex Mixed Bed) 196 Cu Ft 2,112 Cu Ft Epifloc-Waste Filter Graver Ecocote-condensate 1,044 Cu Ft Graver Ecodex-Fuel Pool &

Waste Filter 1,088 Cu Ft 3,788 Cu Ft MISCELLANEOUS WATER TREATMENT (Includes sample and bearing cooling water systems, ash pond treatment, and other water systems, i.e., radwaste systems and fuel pool cleanup systems at nuclear plants requiring treatment.)

Sodium Nitrite (RBCCW and and Off Gas chiller) 450 lbs SEWAGE TREATMENT Sodium Hypochlorite 620 gal 1,575 gal Soda Ash 5,500 lbs

0 cI 0 0 4J Total Pla>>nt Training Summary

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(>>(>

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